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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
0 CATEGORY e REGULATORY XNPORMATXON DZSTR1BUTZON SYSTEM (RIDS)
ACCESSION NBR:9905280059 DOC.DATE: 99/05/21 NOTARIZED- NO DOCKET FACZL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH.NAME ~ AUTHOR AFFILIATION ST MARTIN,J.T. Rochester Gas Ec Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECZP.NAME RECZPXENT AFFILXATXON VISSZNG, G. S.
SUBJECT:
LER 99-006-00:on 990421,start of turbine-driven auxiliary feedwater pump was noted. Caused by'MOV being left in open position. Closed manual isolation valve to secure steam to pump. With 990521 ltr.
DISTRIBUTION CODE: ZE22T COPIES RECEIVED:LTR 1 ENCL I SIZE: E TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72) . 05000244 0
RECIPIENT COPIES RECIPIENT COPIES ZD CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL LPD1-1 PD, 1 1 'ZSSZNG,G. 1 1 INTERNAL: AEOD/SPD/RRAB 1 1 PILE CENTER+0 1 1 NRR/DZPM/XOLB 1 1 R'/DZPM/IOME 1 1 NRR/DRIP/REXB 1 1 NRR/DSSA/SPLB 1 1 RES/DET/EZB 1 1 RGN1 PILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LMITCO MARSHALL 1 1 .D NOAC POORE,W. 1 1 NOAC QUEENER, DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 N
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE HASTE. TO HAVE YOUR NAME OR ORGA'NIZATION OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU REMOVED FROM DISTRI BUTION LISTS OR YOUR ORGANIZATION, CONTACT THE DOCUMENTT CONTROL DESK (DCD) ON EXTENSION 415-2083 CON FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 16 ENCL 16
4ND ROCIIESTER GAS AND ELECTRIC CORPORATION ~ 89 EASTAVENLIE, ROCHESTER, N. Y Iddd9 LI00I AREA CODE7ld Sdd-2r 00 ROBERT C. MECREDY V<e President t4vcteor Ooerotions May 21, 1999 U.S. Nuclear Regulatory Commission Document Control Desk Attn: Guy S. Vissing Project Directorate I-1 Washington, D.C. 20555
Subject:
LER 1999-006, Valve in Unexpected Position Results in Start of Turbine-Driven Auxiliary Feedwater Pump R.E. Ginna Nuclear Power Plant Docket No. 50-244
Dear Mr. Vissing:
The attached Licensee Event Report LER 1999-006 is submitted in accordance with 10 CFR 50,73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "Any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS) ".
Very truly yours, a..d obert C. Mecre xc: Mr. Guy S. Vissing (Mail Stop SC2)
Project Directorate I-1 Division of Reactor Projects -
Office of Nuclear Reactor Regulation I/II U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Regional Administrator, Region I U. S. Nuclear Regulatory Commission 898 475 Allendale Road King of Prussia, PA 19406 U.S. NRC Ginna Senior Resident Inspector 9'tt05280059 990521 PDR ADGCK 05000244 S PDR
C NRC ORM 366 U.S. NUCLEAR REGULATORY COMMISSION IB 1BBB)
ECLAT'aukefI r ra"9ke~AW'p~A'L'PJNP coBection request: 50 hrs. Reported lessons learned 'nformation are inceporated into the licensing process and fed back to LICENSEE EVENT REPORT (LER) hdusay. Forward comments regarding burden estimate to the Records Management Branch (T4 F33), U.S, Nudear Regulatory Cornmisskxt, Wash!ngton, DC 205550001, and to (See reverse for required number of the Pa pervrork ReducBon Pro)oct {31504104), 05ce of digits/characters for each block) Management and Budget, Washington, DC 20503. If an ktformaUon coBecUon does not display a currently val OMB control number. the NRC may not conduct or sponsor, and a FACILITY NAME I1l DOCKET NUMBER lzl PAGE I3I R. E. Ginna Nuclear Power Plant 05000244 1 OF 6 TITLE te)
Valve in Unexpected Position Results in Start of Turbine-Driven Auxiliary Feedwater Pump EVENT DATE (5) LER NUMBER {6) REPORT DATE {7) OTHER FACILITIES INVOLVED {8)
FACIUTY NAME OOCKETNVMBER SLOUTNTIAL RENSION MONTH OAY YEAR MONTH OAY YEAR NUMBER NUMBER 05000 04 21 1999 1999 - 006 - 00 05 21 1999 FACIUTY NAME DOCKET NVMBER 05000 OPERATING THIS REPORT IS SUBMITTED PU RSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)
MODE {9) 20.2201 (b) 20.2203(a) (2) (v) 50.73(a) (2) (i) (6) 60.73(a)(2) (viii)
POWER 20.2203(9) (1) 20.2203(a)(3)(I) 50.73(a)(2)(ii) 50.73(a)(2)(x)
LEVEL (10) 002 20.2203(a) {2)(i) 20.2203{a)(3)(ii) 50.73(a) 12)(iii) 73.71 20.2203(a)(2) (ii) 20.2203{a) (4) X 50.73(a)(2)(iv) OTHER
- 20. 2203(a) (2) (iii) 50.36(c) (1) 50.73(a)(2)(v) Specify in Abstract below 20.2203{a) {2)(iv) 50.36(c)(2) 50.73(a)(2) {vii) or In NRC Form 366A LICENSEE CONTACT FOR THIS LER (12)
NAME TELEpHoNE NvMBER orroarde Area code)
John T. St. Martin - Technical Assistant (716) 771-3641 REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER 'fo EPIX CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX SUPPLEMENTAL REPORT EXPECTED (l4] EXPECTEO MONTH OAY YES NO SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). X OATE {f5}
ABSTRACT {Limitto 1400 spaces, i.e., approximately 15 single*spaced typewritten lines) (16)
On April 21, 1999, at approximately 1947 EDST, the plant was in Mode 2 at approximately 2% reactor power with the reactor coolant system being maintained at a temperature of 549 degrees F and a pressurizer pressure of 2235 PSIG.
Testing of a motor-operated valve which isolates steam to the turbine-driven auxiliary feedwater pump was being completed, and the valve was,left in the open position.
The manual isolation valve was then opened, admitting steam to the turbine-driven auxiliary feedwater pump. This started the turbine-driven auxiliary feedwater pump.
Immediate action was to isolate auxiliary feedwater flow from the turbine-driven auxiliary feedwater pump and close the manual isolation valve to secure steam to the pump.
The underlying cause of this event was the motor-operated valve was left in the open position following diagnostic testing. This event occurred at a time when the valve would normally have been expected to be closed.
Corrective action to prevent recurrence is outlined in Section V.B.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (8 1998)
L(CENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET (2) LER NUMBER (6) PAGE (3)
WA 8(BIIBI)gt IIEYISIOII IIUMBN IIBMBBI R.E. Ginna Nuclear Power Plant 05000244 .-
1999 006 00 2 OF 6 TEXT llfmore spaceis required, use edditionel copies of NRC Form 366AI (17)
PRE-EVENT PLANT CONDITIONS II On April 21, 1999, at approximately 1947 EDST, the plant was in Mode 2, holding at approximately 2%
reactor power preparing for startup from the 1999 refueling outage. The reactor coolant system (RCS) was being maintained at a temperature of approximately 549 degrees F and a pressurizer (PRZR) pressure of .
approximately 2235 PSIG. The steam generator (SG) atmospheric relief valves (ARVs) were being operated to maintain constant RCS temperature. When the ARVs operate, significant steam flow noise is present in the area around the ARVs.
Testing of motor-operated valve (MOV) 3505A (MOV steam admission valve to the turbine-driven auxiliary feedwater (TDAFW) pump from the "A" SG) was being completed per Maintenance Procedure M-64.1.2 (MOVATS Testing of Motor-Operated Valves) and Test Procedure PT-50.7 (Differential Pressure Testing of TDAFW Pump Steam Supply Valves MOV-3504A and/or MOV-3505A). Procedure M-64.1.2 is a generic procedure, which allows for the installation and removal of test equipment, and the acquisition and analysis of test data. M-64.1.2 is performed by a team from the Reliability Test group, composed of a team leader and an electrician. Procedure PT-50.7 is a test procedure to obtain specific differential pressure test data of the listed MOVs, and is performed by Performance Monitoring and Reliability Test personnel in conjunction with Control Room operators. MOV-3505A is in the vicinity of the ARVs. Performance Monitoring personnel had completed procedure PT-50.7 and had verified that MOV-3505A was in the closed position, as specified in PT-50.7.
II. 'ESCRIPTION OF EVENT:
A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
o April 21, 1999, 1947 EDST: Event date and time.
o April 21, 1999, 1947 EDST: Discovery date and time.
o April 21, 1999, 1948 EDST: TDAFW pump is secured.
EVENT:
.Prior to the start of M-64.1.2, during a discussion in the Control Room, it had been determined that confirmation stroking of MOV-3505A, required by a step in M-64.1.2, would be deferred and documented as complete when a similar step is performed in 'periodic test procedure PT-16Q-T, "Auxiliary Feedwater Turbine Pump - Quarterly" Personnel from the Reliability Test group,
~
Performance Monitoring, and Control Room operators were involved in this discussion.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (B.I998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET (2) LER NUMBER (6) PAGE (3) 8EOUEKEIA( BEMBIOK KUMBN KUMBN R.E. Ginna Nuclear Power Plant O5OOO244 -
1999 006 00 3 OF 6 TEXT ilfmore spaceis required, use edditionel copies of NRC Form 366AI (17)
Reliability Test personnel submitted an isolated work area request (" hold" request) to hold closed V-3505 (the manual isolation valve to MOV-3505A) during MOYATS testing. MOY diagnostic tests were then performed per procedure M-64.1.2 on MOV-3505A. As required, the DC power was removed from MOV-3505A during these tests. Removal of DC power removes position indication for MOY-3605A on the Main Control Board (MCB). MOY-3505A was stroked several times while performing the MOV diagnostic testing, and was left in the open position by Reliability Test personnel, as permitted by M-64.1.2. When the testing portion of M-64.1.2 was completed, the Reliability Test personnel began to remove the MOV diagnostic test equipment in preparation for restoring MOV-3505A to service.
During this restoration process, the Reliability Test personnel informed the Control Room operators to begin restoring MOV-3505A to service. Communications between Reliability Test personnel and Control Room operators did not adequately include a discussion of the current valve position for MOV-3505A, nor that DC power was still in the process of being restored for the MOV. Since DC power had not been restored for MOV-3505A, there were no MCB annunciator alarms or other MCB indications to alert the Control Room operators that MOV-3605A was open.
After requesting release of the "hold" from the Reliability Test team leader, the Control Room operators proceeded to remove the holds associated with MOV-3505A and to realign valves. A Control Room operator directed an Auxiliary Operator (AO) to open V-3505,'the manual isolation valve for MOV-3605A. The AO started to open this valve, which is in the vicinity of the ARVs. As this valve was being opened, steam was beginning to be supplied to the TDAFW pump, and the pump started. This steam flow would otherwise have been a direct indication of the improper condition, but due to the significant noise in the area, the AO did not detect steam flow as he opened V-3605. There were no alarm indications available in the Control Room to alert the Control Room operators to the start of the TDAFW pump.
The AFW System systems engineer was in the vicinity of the TDAFW pump during these activities (which is on next floor directly below the ARVs, MOV-3505A, and V-3606) anticipating performance of procedure PT-16Q-T, which would stroke MOY-3605A and operate the TDAFW pump. He observed the TDAFW pump starting and notified the Control Room of this condition.
Around the same time, the Reliability Test electrician contacted the Control Room operators by telephone, requesting that DC power be restored to MOV-3505A. This action would auto-close MOV-3605A, which was believed (by the Control Room operators) to have already been done prior to the release of the hold for V-3606. The Control Room operators, having been notified by the AFW systems engineer, observed feedwater flow from the TDAFW pump on the MCB, and then realized there had been an unexpected start of the TDAFW. The Control Room operators promptly secured feedwater flow from the TDAFW pump by manually closing air-operated discharge flow control valves at the Main Control Board. The Control Room operator then notified the AO to locally re-close V-3605 to secure steam to the TDAFW pump.
A review of data indicated that during the time the TDAFW pump was operating, there was a slight cooldown of the RCS of approximately two (2) degrees F and a TDAFW pump run of about one (1) minute.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (B.IBBB)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME l1) DOCKET I2) LER NUMBER l6) PAGE l3)
SB)UBITIAL REVISION IIUMBFR IIUMBBI R.E. Ginna Nuclear Power Plant 05000244 1999 - - 00 006 4 OF 6 TEXT /If more space is required, use addi Iional copies of NRC Form 366A/ l17)
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None E. METHOD OF DISCOVERY:
This event was identified by the AFW systems engineer, who observed the TDAFW pump starting and notified the Control Room of this condition.
F. OPERATOR ACTION:
After confirming the start of the TDAFW pump, the Control Room operators promptly secured feedwater flow from the TDAFW pump and directed the AO to secure steam to the TDAFW pump.
The Control Room operators subsequently notified higher supervision and notified the NRC per 10CFR50.72 (b} (2} (ii}, non-emergency four hour notification, at approximately 2230 EDST on April 21, 1999.
G. SAFETY SYSTEM RESPONSES:
None III. CAUSE OF EVENT A. IMMEDIATECAUSE:
The immediate cause of the start of the TDAFW pump was opening V-3505 with MOV-3505A in an unexpected position (open}.
- 8. INTERMEDIATE CAUSE:
The intermediate cause for MOV-3505A being in an unexpected position was the deferral of steps in M-64.1.2 requiring confirmation stroking and not verifying the position of MOV-3505A prior to removing the hold tag for V-3505.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6 IBBB)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITV NAME (1) DOCKET (2) LER NUMSER (6) PAGE (3)
S(BII(tnIAL II(VISIBM It(1MB@ ttIIMBER R.E. Ginna Nuclear Power Plant 05000244 tees - ooe - oo 5 OF 6 TEXT llfmore space is required, use additional copies of NRC Form 366AJ (17)
C. ROOT CAUSE:
The underlying cause for MOV-3505A being in an unexpected position was less than adequate guidance in procedure M-64.1.2 to ensure the proper sequence of completion activities. Steps were allowed to be deferred, which no longer assured that restoration of DC power, confirmation stroking, and final valve position are completed prior to removal of the hold on the isolated work area.
These errors were cognitive errors. Performance Monitoring personnel left MOV-3605A closed at the completion of PT-50.7, but the subsequent re-positioning of MOV-3505A by Reliability Test personnel per M-64.1.2 was not a'dequately communicated to the other groups. Control Room operators removed the hold on V-3505, but the Reliability Test team leader and Control Room operators made a cognitive error in assuming that MOV-3605A was closed at this time. These errors were associated with activities that were covered by approved procedures. However, there was not sufficient detail included within these procedures with respect to requirements for valve, cycling. Significant steam flow noise in the area of the ARVs where the AO opened the manual isolation valve contributed to the error, in that the AO could not detect steam flow to the TDAFW pump as he opened this valve. Personnel involved in this event included licensed operators, a non-licensed operator, and other licensee personnel from the Performance Monitoring and Reliability Test groups ~
IV. ANALYSIS OF EVENT:
This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv),
which requires a report of, "Any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)". The start of an AFW pump is an actuation of an ESF.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to the unexpected start of the TDAFW pump because:
The start of the TDAFW pump occurred with acceptable levels in both SGs.
The additional feedwater flow from the TDAFW pump was promptly secured and V-3606 was closed to secure steam to the TDAFW pump to minimize the cooldown of the reactor coolant system (RCS).
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION IBIBBB)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 11) DOCKET 12) LER NUMBER IB) PAGE {3)
SEBVENIML RDBBIBN NUMBER NUMBER R.E. Ginna Nuclear Power Plant 05000244 1999 QQ6 QQ 6 OF 6 TEXT llfmore space is required, use additional copies ol iVRC Form 366Al I17) o The limiting case for this event is a sudden increase in feedwater flow at hot zero power. The case analyzed in the Ginna Station Updated Final Safety Analysis Report (UFSAR), Section 15.1.2 involves a step increase in feedwater flow to both steam generators to 110% of the nominal full power flow rate initiated at hot zero power with the reactor control in manual rod control. The plant condition at the time of this event was Mode 2. The specific criterion used to evaluate a feedwater malfunction event initiated at hot zero power is that the maximum reactivity insertion rate that results from the cooldown should be less than the reactivity insertion rate that has been analyzed in the rod withdrawal from a subcritical condition analysis. This event resulted in a cooldown of approximately 2 degrees F, which resulted in a negligible reactivity change.
Based on the above, it can be concluded that the public's health and safety was assured at all times.
V. CORRECTIVE ACTION:
A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
Feedwater flow from the TDAFW pump was secured and steam to the TOAFW pump was secured to minimize the cooldown of the RCS.
ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
MOV diagnostic testing procedures, including M-64.1.2, will be revised to identify a final required valve position following diagnostic testing.
The lessons learned from this event will be incorporated into the planning and coordination of MOV. diagnostic testing.
VI. ADDITIONALINFORMATION:
A. FAILED COMPONENTS:
None B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause could be identified. However, LERs96-004, 96-008, and 96-010 and 96-011 are similar events (start of an auxiliary feedwater pump) with different root causes.
C. SPECIAL COMMENTS:
None