ML17264A755
| ML17264A755 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 11/30/1996 |
| From: | Walden J, Widay J ROCHESTER GAS & ELECTRIC CORP. |
| To: | Vissing G NRC (Affiliation Not Assigned), NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9612180076 | |
| Download: ML17264A755 (7) | |
Text
CATEGORY 1 REGULAT ci INFORMATION DISTRIBUTION STEM (RIDS)
ACGESNION NBR:9612180076 DOC.DATE: 96/ll/30 NOTARIZED: NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester AUTH.NAME AUTHOR AFFILIATION WALDEN,W.
Rochester Gas a Electric Corp.
WIDAYtJ.A Rochester Gas a Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION DOCKET G
05000244 VISSINGiG.S.
SUBJECT:
Monthly operating rept for Nov 1996 for Ginna Station.
W/96121'1 ltr.
DISTRIBUTION CODE:
IE24D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: Monthly Operating Report (per Tech Specs)
NOTESLicense Exp date in accordance with 10CFR2,2.109(9/19/72).
05000244 8
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~ 'IIII"'~Z iuZZZ ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER, N.K 14649-0001 TKLEPHONf AREA coDc 7I4 546-2700 December 11, 1996 US Nuclear Regulatory Commission Document Control Desk Attn:
Guy S. Vissing Project Directorate I-1 Washington, DC 20555
Subject:
Monthly Report for November, 1996 Operating Status Information R.E.
Ginna Nuclear Power Plant Docket No. 50-244
Dear Mr. Vissing:
Pursuant to Ginna Improved Technical Specifications Section 5.6.4, attached is the monthly operating status report for Ginna Station for the month of November, 1996.
Very truly yours, seph A. Wid Plant Manager xc:
U.S. Nuclear Regulatory Commission Mr. Guy S. Vissing (Mail Stop 14C7)
Project Directorate I-1 Washington, D.C.
20555 U. S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 U.l'S".
NRC Ginna Senior Resident Inspector Attachments
'P6i2i80076 96i i30 PDR ADOCK 05000244 R
I 7
OPERATING DATAREPORT COMPLETED BY:
TELEPHO 50-244 De mber 11 1996 John V. Walden (716) 771-3588
- 1. Unit Name:
R.E. GINNANUCLEAR POWER PLANT Notes:
- 2. Reporting Period:
November 1996 3,
Licensed Thermal Power (MWI):
1520 4.
Nameplate Rating (Gross MWe):
517 5.
Design Electric Rating (Net MWe):
470 6.
Maximum Dependable Capacity (Gross MWe):
490 7.
Maximum Dependable Capacity (Net MWe):
470 8.
IfChanges Occur in Capacity Rating (Items Number 3 Through 7) Since Last Report, Give Reason:
9.
Power Level to Which Restricted, IfAny (Net MWe:
- 10. Reason For Restrictions, IfAn:
This Month Yr.-to.Date Cumulative**
- 11. Hours in Reported Period
- 12. Number of hours Reactor Was Critical
- 13. Reactor Reserve Shutdown Hours
- 14. Hours Generator On-line
- 15. Unit Reserve Shutdown Hours
- 16. Gross Thermal Energy Generated (MWH)
- 17. Gross Electrical Energy Generated (MWH)
- 18. Net Electrical Energy Generated (MWH)
- 19. Unit Service Factor (%)
- 20. Unit AvailabilityFactor (%)
- 21. Unit Capacity Factor (using MDC Net) (%)
- 22. Unit Capacity Factor (using DER Net) (%)
- 23. Unit Forced Outage Rate (%)
720.0 444.7 0.0 437.3 0.0 648596.0 221450.0 210915.6 60.7 60.7 62.3 62.3 39.3 8040.0 5503.2 0.0 5433.8 0.0 7883691.0 2661410.0 2529839.8 67.6 67.6 66.9 66.9 14.5 236808.0 189170.3 1687.6 186182.5 8.5
'64746999.0 87723910.0 83277651.8 78.6 78.6 75.9 75.9 5.8
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date and Duration of Each):
- 25. I(Shutdown At End of Report Period, Estimate Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forcast Achieved INITIALCRIT(CALITY INITIALELECTRICITY COMMERCIALOPERATION
'UMULATIVETOTALCOMMENCINGJANUARY 1, 1975 "CUMULATIVETOTALCOMMENCING NOVEMBER8, 1969
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO:, 50-244 UNIT: R.E.
Ginna Nuclear Power Plant DATE:
December 11 1996 COMPLETED BY:
TELEPHONE:
John Walden 6
771-3588 MONTH November 1996 DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 17.
494 2.
18.
494 3.
19.
495 20.
495 21.
496 6.
22.
496 7.
23.
496 24.
495 9.
-10 25.
495 10.
-10 26.
495
-10 27.
495 12.
13 28.
495 13.
353 29.
495 14
~
495 30.
496 15.
16.
494 494 31.
INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in reporting month.
Compute to the nearest whole megawatt.
UNIT SHUTDOWN AND POWER REDUCTIONS REPORT hlONTH DOCKET NO.
tJNI1 NAMI R E CilNNA NUCLEAR POWER PLANT DA1 E 9.6
(;OhIP LI:.1'I'.D I3Y ohn Walden 1996 1 I:LI:P)ION
( 716) 771-3588 Ho.
Date
.o e
o
~
o o X O~
CV c0Ill OO CL cn o-0 ocu ohio tt.'l' 0
CI Ltcensee Event Report tI Ew 0
0 0
I/l C0 lA 0C Q
o O
Cause 5 Correchve Action to Prevent Recurrence lf)/24 /tl6 F
470.9 Iridication of a main trans-former hot spot caused a forced shutdown.
Replacement of main transformer with spare is complete.
F: Forced S:
Scheduled Reason:
A-Equipmcnt Failure (Explain)
B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training 8c License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain) hlethod:
I-hlanual 2-Manual Scram.
3-Automatic Scram.
4-Other (Explain)
Fxhibit G - Instructions for Preparation of Data Entry Sheets for Liccnscc Event Rcport (LER) File (NURF(-
OI 61)
Exhibit I - Same Source
NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE DOCKET NO: 50-244 UNIT: R.E.
Ginna Nuclear Power Plant DATE:
December 11 1996 COMPLETED BY:
TELEPHONE:
John Walden 716 771-3588 MONTH November 1996 Replacement of the main transformer was completed.
The unit was placed on line on November 12, 1996.
Full power was reached on November 13, 1996.
The unit remained at full power for the remainder of the month.