ML17347A692

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Monthly Operating Repts for Feb 1988
ML17347A692
Person / Time
Site: Saint Lucie, Turkey Point, 05000000
Issue date: 02/29/1988
From: Grant N
FLORIDA POWER & LIGHT CO.
To:
Shared Package
ML17347A693 List:
References
NUDOCS 8803210463
Download: ML17347A692 (32)


Text

.~EE DAILY UNIT PURER LEVEL

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DOCKET NO. 50-250 UNIT Turke Point Uni t 3 DATE March 15, 1988 CONPLETED BY N.M. Grant TELEPHONE 305 694-4432 N)NTH Februar , 1988 DAY AVERA6E DAILY POMER LEVEL (N Qe-Net) 2/ 1/88 -5 2/ 2/88 -5 2/ 3/88 -5 2/ 4/88 -5 2/ 5/88 -7 2/ 6/88 -10 2/ 7/88 -11 2/ 8/88'/

-15 9/88 -15 2/10/88 -16 2/11/88 -17 2/12/88 -17 2/13/88 -17 2/14/88 "19 2/15/88 -19 2/16/88 -19 2/17/88 2/18/88 -19 2/19/88 -19 2/20/88 -19'28 2/21/88 2/22/88 188 2/23/88 462 2/24/88 671 2/25/88 680 2/26/88 689 2/27/88 694 2/28/88 688 2/29/88 686 8803210463 05000250 880229'PDR ADOCK R DCD

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QF'Ef" ATXNG DATA REF'ORT DOCKET NO 50 250 DATE 3/14/88 COMPLETED BY Ni H, GRANT TELEF'HONE 305/694/4432 QPFRATING STATUS

1. UNTT NAME: TURKEY POINT UNIT 3
2. RFF'ORTING PERIOD: FEBRUARY 1988
3. LICENSED THERMAL F'OWER (MWT): 2200 4 NAMEF'l ATE RATING (GROSS MWE)

'66 760

'o o

5. DESIGN ELECTRICAL RATING (NET MHE): 693 6 MAXIMUM DEF'ENDABLE CAF'AC1TY (GROSS'HE): 699
7. MAXIMUM DEPENDABLE CAF'ACITY (NET MWE)
8. IF CHANGES OCCUR XN CAF'ACITY RATINGS (1TEMS NUMBER 3 THROUGH 7)

SINCE LAST REPORT'~ GIVE REASONS i 9, POWER LEVEL TO WHICH RESTRICTED~ IF ANY (NET MHE) lei REASONS FOR RESTRICTIONS> IF ANY:

MONTHLY -YTD- CUMULATiVE ii. l-lOURS IN, REF'ORT PERIOD'Z, NUMBER OF HOURS REACTOR WAS CRXTICAL 696, 210i5 anne 5iii9 133569+6 38487o6

13. REACTOR RESERVE SHUTDOWN HOURS OoO OiO 844.4 14 o l-lOURS GENERATOR ON-LINE 189i4 469oi 87304.2
15. UNIT RESERVE SHUTDOWN HOURS 0 0 121i8 lb. GROSS THERMAL ENERGY GENERATED (MHH> 370671 389041 180693304 17+ GROSS ELECTRICAL ENERGY GENERATED (MHH) 120325 280685 57878686

'l'S. NET ELECTRICAL ENERGY GENERATED (MWH) 106581 254512 54733293 UNIT SERVICE FACTOR 27 ' 32o6 65i4 20+ UNIT AVAILABILITYFACTOR 27'+ 2 32i6 65i5

21. CAF'ACITY FACTOR (USING MDC NET> 23+0 '26)5 62+9 ZZ+ CAPACITY FACTOR (USING DER NET) 22'o 1 25o5 59ii
23. UNIT FORCED OUTAGE RATE 72o8 67o4 11i2
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS 25 o IF SHUT DOWN AT END'F REPORT PERIOD ~ ESTIMATED DATE OF STARTUP o

0 0 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

Turkey Point Unit 83 DATE Harch 15, 1988 REPORT MONTH February 1988 COMPLETED By

~5. 2 Method of Shutting Ucensee Cause & Corrective Down Event System Component Action to No. Date Type'uration (Hours) Reason~ Reactor Report ¹ Code~ Codes Prevent Recurrence 02 880113 F 506. 5 RB CRDRVE Unit 83 remained shutdown to repair the "C" reactor coolant pump seal, a leaking uAu residual heat removal pump seal 5 a failed gate filter module card on the battery chargers, to perform maintenance on the source range detectors, and .

to perform several other minor repairs and adjustments. Following completion of these items the unit was returned to power operation, holds were experienced at 305 power for secondary chemistry and again at 50$

power to make control rod position indication adjustments.

F Forced Reason Method Exhibit G-!nstructhns S Scheduled A - Equipment Ftulure (Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram Entry Scheets Ucensee C - Refueling 3 - Automatic Scram Event Report(LER) Rle, D - Regulatory Restriction 4 - Continued (NUREG4161)

E - Operator Training & Ucense Examination 5 - Load Reduction F - Administrative 9 - Other (Explain)

G - Operational Error (Explain) Exhibit 1-Same Source H - Other (Explain)

0 aUMMARY OF OPERATING EXPER CE DOCKET,'NO.

50-250'urkey UNIT Point Uni;t ¹3 DATE ttarch 15, 1988 COMPLETED BY N. W. Grant TELEPHONE (305)694-4432 REPORT MONTH February, 1988 See the '"Unit Shutdowns and Power Reductions" report.

II 4l AVERAGE DAILY UNIT PURER LEVEL DOCKET NO. 50-251, UNIT Turke Point Uni't 4 DATE March 15, 1988 CONPLETED BY N.M. Grant TELEPHONE MONTH February, 1988 DAY.',AVERAGE DAILY POMER LEVEL

'N We-Net) 2/ 1/88 657 2/ 2/88 697 2/ 3/88 696 2/ 4/88 693, 2/ 5/88 683 2/ 6/88 676 2/ 7'/88 503 2/ 8/88 -16 2/

2/10/88 9/88 -ii

-8 2/ii/88 -7 2/12/88 2/13/88 -1 2/14/88 2 2/15/88 -2 2/16/88 <<7 2/17/88'/18/88

-1'2,

-12 2/19/88

-12 2/28/88 -12 13 2/21/88'/22/88.

-16 2/23/88 -15 2/24/88 12 2/25/88 168 2/26/88 618 2/27/88 705 2/28/88 705 2/29/88 704

Ot OPERATING DATA REF'QRT DOCKET NO 50 251 DATE 3/14/88 CQMPLErED BY N.: W. GRANT TFLEF'HONE 305/694/4432 OPERATING STATUS

i. UNIT NAME: TURKEY POINT UNIT 2>>, REPORTING PERIOD>> FEBRUARY 1988 3>> LICENSED THERMAL,F'ONER <MAT): 2200 NAMEPLATE RATING (GROSS MME): 760
5. DESIGN El ECTRICAL RATING (NET MME)>> 693 6 ~ MAXIMUM DEPENDABL'E CAF'ACITY ( GROSS MME)>>'99
7. MAXIMUM DEPENDABLE CAF'ACITY (NET MME): . 666
8. IF CHANGES OCCUR XH CAF'ACITY RATINGS (1TEMS NUMBER 3 THROUGH 7)

SINCE LAST REF'QRT r GIVE REASONS>>

9. POWER LEVEL TO WHICH RESTRICTED~ IF ANY (NET MME)
10. REASONS FOR RESTRICTIONS v IF ANY>>

MONTHLY -YTD- CUMULATIVE 11 ~ HOURS XN REF'ORT F'ERIQD 696 1440 127301>>0 NUMBER OF HOURS REACTOR HAS CR1TICAL

2.

,292>>3 1036>>3 86222.8

13. REACTOR RESERVE SHUTDOMN HOURS 0>>0 0>>0 166>>6 HOURS GENERATOR OH-LINE 282>>5 1026>>5 83232.6 15>> UNXT RESERVE SHUTDOWN. HOURS 9 0 32>>1 16>> 'GROSS THERMAL ENERGY GENERATED (MHH) 575809 2208360 175663983 17>> GROSS ELECTRICAL ENERGY GENERATED < MHH) 189335 730175 56029939 18>> NET ELECTR1CAL FNERGY GENERATED (MMH) 175903 692539 53011321 19>> UNXT SERVICE FACTOR 40>>6 71>>3 65>>4
20. 'NXT AVAILABILITYFACTOR 40>>6 71>>3 65>>4 21>> CAF'ACXTY FACTOR (USING MDC NET) 37>>9 72.2 63>>9'0>>

22, CAF'ACITY FACTOR <USING DER NET) 36>>5 69>>4 1 23>> UNXT FORCED OUTAGE RATE 59>>3 28>>7 li>>1 24>> SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS 25>> ZF SHUT DOWN AT EHD OF REPORT PERIOD r ESTIMATED DATE OF STARTUP ~

Cl 4l Page 1 of 2 50-251 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

UNiT NAMF Turkey Point Uni t iI 4 March 15, 1988 COMPLETED BY N. W. Grant February, 1988 TELEPHONE ( 305) 694- 4432 Method of Shutting Ucensee Cause 8 Corrective Down Event System Component Acthnto Date Ttrpe'uration (Hours) Reason2 Reactor Report¹ Codei Codes Prevent Recurrence 0.0 HA XXXXXX Unit iII4 reduced power to adjust 01 880201 the turbine Governor impeller oil adjustable orifice due to a turbine governor impeller oil pressure problem. The reactor was then returned to power operatiorf; 880205 0.0 HA XXXXXX The Unit again reduced power for 02 adjustments to the turbine governor impeller oil adjustable orifice, due to a turbine governor impeller oil pressure problem. The reactor was then returned to power.

412. A 251-88-003 EC BATTRY A reactor shutdown was performed 03 880207 3 due to the loss of the 4A and 4S battery chargers caused by the failure of the gate filter module card. While the unit was down work was also performed on the B RCP notor and the CRDM cables.

4 F Forced Reason Method Exhibit G- Instructions S Scheduled A - Equipment Failure (Exphln) 1 - Manual for Preparation of Data 8 - Maintenance or Test 2 - Manual Scram Entry Scheets Ucensee C - Refuelng 3 - Automatic Scram Event Report(LER) Re D - Reguhtory Restrkthn 4 - Continued (NUBEG-D161)

E - Operator Training 8 Ucense Examination 5 - Load Reduction F - Admlnhtratlve 9 - Other (Exphin)

G - Operathnal Error (Exphln) Exhibit 1-Same Source H - Other (Exphln)

4l Page 2 of 2 50- 251 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

Turkey Point Unit i%4 DATE March 15, 1988 COMPLETED BY N. W. Grant February, 1988 TELEPHONE ~305) 694-4432 Method of Shutting Ucensee Reporting Cause & Corrective Duration Down Event System Component Action to No. Date Type (Hours) Reason~ Reactor Code i Codes Prevent Recurrence 04 880224 F 0.0 HA TURB IN A power reduction was initiated to allow for performance of the turbine overspeed test. Following completion of this test the unit was returned to power operation at which time a hold was experienced 't 30'5 power due to secondary side chemistry.

F Forced Reason Method Exhibit G-Instructions S Scheduled A - Equipment Failure(Exphln) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram Entry Scheets Licensee C - Refueling 3 - Automatic Scram Event Report(LER) File D - Reguhtory Restriction 4 - Continued (NUREG4161)

E - Operator Training & License Examination 5 - Load Reduction F - Administrative 9 - Other(Exphin)

G - Operational Error (Explain) Exhibit1-Same Source H - Other (Explain)

MMARYOF OPERATING EXPERI CE DOCKET NO. 50-251',

UNIT Turkey, Point Un~t 84

-DATE March 15, 1988 COMPLETED:BY 'N. W. Grant TELEPHONE (305) 694-4432 REPORT MONTH February, 1988 See the "Unit Shutdowns and Power Reductions." report.

0 4>>

.'AA6E OAILY UNIT PURER LEVEL

~

DOCKET NO. 50-335 UNIT St. Luci DATE March 15, 1988 CONPLETED BY N.lf. Grant TELEPHONE February, 1988 DAY AVERAGE DAILY PINER LEVEL (N Qe-'Net) 2/ 1/88., 864

.2/ 2/88 S62 2'/ 3/88 860 2/ 4/88 S60 2/ 5'/88 859 2/ 6/88 864 2/ 7/88 867'69 2/ 8/88 2/ 9/88 847 2/10/88 85669 2/11/88 2/12/88 'S69 2/13/88 S7,1 2/14/88 869'69 2/15/88 2/16/88 867 2/1'7/88 866 2/18/88 865 2/19/88 862.

2/20/88 S63, 2/21/88 S62 2/22/88 864

.2/23/88 863 2/24/88 861

.2/25/88 863 2/26/88 866 2/27/88 867 2/28/88'/29/88

'868 865

41 OF'ERATXHG DATA REF'ORT DOCI(ET HO bO 33&

DATE 3/14/88 COMPLETED BY N<<'o GRANT TELEF'HONE 305/694/4432 OPERATING STATUS

1. UNIT NAME: ST. LUCXE UNIT 2 ~ REF'ORT1HG PERIOD: FEBRUARY 1988
3. LICENSED THERMAL POWFR (MWT): 2700' 6

AMEF'LATE RATING ( GROSS MWE DESIGN ELECTRICAL RATING (NET MWE);

MAXIMUM DEF'ENDABLE CAF'ACXTY ( GROSS'WE)

7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): .

8+ IF CHANGES OCCUR XN CAF'ACITY RATINGS

):

'72 (ITEMS 850 830 839 NUMBER 3 THROUGH 7)

SXHCE LAST REPORTS GIVE REASONS'OWER LEVEL TO WHICH RESTRICTED ~ XF ANY (NET MWE)

10. REASONS FOR RESTRICTIONS'F AHY:

MONTHLY - YTD- CUMULATIVE

11. HOURS IN REF'ORT PERIOD t 696 1440 98112iO
12. NUMBER OF HOURS REACTOR WAS CRITICAL 696i0 144eiO 72984o4 13m REACTOR RESERVE SHUTDOWN HOURS OiO OiO 205o3 14+ HOURS GENERATOR'N-LINE 696+0 1440oO 72409o9
15. UNIT RESERVE SHUTDOWN HOURS 0 0 39+3 ihi GROSS THERMAL ENERGY GENERATED (MWH) 1877156 63271'8 3884263 185231933 60832585
17. GROSS ELECTRICAL ENERGY GENERATED <MWH) 1309600 18+ NET ELECTRICAL ENERGY GENERATED (MWH) 601389 1244268 57445427 19, UNIT SERVICE FACTOR lee,+ e 10eoO 73+8 20 i UHIT AVAILABXLITYFACTOR 100+0 100iO 73o8
21. CAPACITY FACTOR (USXNG MDC NET) 103'o 0 103iO 73+2 22, CAPACITY FACTOR (USXNG DER NET) 104+1 104+1 71.8 23 o UNIT FORCED OUTAGE RATE 0 0 3o9 24, SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS 25 i IF SHUT DOWN AT END OF REPORT PERIOD v ESTIMATED DATE OF STARTUP i

!I .II UNlT SHUTDOWNS AND POWER REDUCTlONS DOCKET NO.

UNIT NAME t. Lucie Uni t ¹1 rs DATE Ha rch 15, 1988 COMPLETED BY REPORT MONTH TELEPHONE ~305'94-443~

Method of Shutting Ucensee Cause & Corrective Duration Down Event System Component Actionto Date Type (Hours) Reason2 Reactor Report¹ Code4 odes Prevent Recurrence signifi-Unit dl had no shutdowns cant power reductions.

or

~

3 4 F Forced Reason Method Exhibit G-instructions S Scheduled A - EquipmentFailure(Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram Entry Scheets Ucensee C - Refueling 3 - Automatic Scram Event Report(LER) File D - Regulatory Restriction 4 - Continued (NUREG4161)

E - Operator Training 8 Ucense Examination 5 - Load Reduction F - Administrative 9 - Other(Explain)

G - OperationaIError (Explain) Exhibit1-Same Source H - Other(Explain)

Og 1sgl

~ ~

MMARY'OF OPERATING EXPER CE DOCKET NO. 50-335 UNIT St. Lucie Unit ¹I

,DATE triarch 15, 1988 COMPLETED BY N. W. Grant TELEPHONE (305) 694-4432 REPORT. MONTH'ebruary, 1988 Unit ¹1 operated at essentially full power. and had no "Unit shut-downs or significant power, reductions."

In accordance with requirements of Technical Specifications 6.9. 1.6, there were no challenges to PORV or safety valves during the report month.

ORA66 'DAILV URIT PINER. LEVEL ~

DOCKET NO. 50-389 NIT St Lucie Unit 2 DATE March 15, 1988 CONPLETED SY, N.M.

TELEPNNE 305 694-4432 February, 1988 OAY AVERA6E DAILY POMKR LEVEL (N Qe-Net) 2/ 1/88 865 2/ 2/88 864 2/ 3/88 864 2/ 4/88 863 2/ 5/88 863 2/ 6/88 863 2/'/88 867 2/ 8/88 S66 2/ 9/88 868 2/10/88 868 2/11/88 '868 2/12/88 868 2/13/88'/14'/88 870 869 2/15/88 869 2/16/88'/17/88 867

'867 2/18/88 866 2/19/88 865 2/28/88 865 2/21/88 864 2/22/88 '843'41 2/23/88 2/24/88 864 2/25/88. 865 2/26/88 867 2/27/88 868 2/28/88 868 2/29/88 '868

OF'ER*TING DATA REF'ORT DOCKET NO 50 38'9 DATE 3/14/88 COMPLETED BY Ni W+ GRANT TELEF'HONE 305/694/4432 OPERATING STATUS

}. + UNTT NAME t ST+ LUCZE UNIT 2 REF'ORTING PERIOD: FEBRUARY 1988

3. LICENSED THERHAL POWER (HWT): 2700 6,

7.

8, NAMEF'LATE RATING (GROSS MWE) o DESIGN ELECTRICAL RATING (NET MWE) +

MAXIMUM DEF'ENDABLE CAPACITY (GROSS HWE):

HAXIHUM DEPENDABLE CAPACITY (NET HWE) '39 850 830 882

'o IF CHANGES OCCUR IN CAF'ACITY RATINGS (ITEMS NUMBER 3 THROUGH 7)

SINCE LAST REPORT ~ GIVE REASONS'OWER LEVEL TO WHICH RESTRICTED IF ANY (NET HWE) 10, REASONS FOR RESTRICTIONS IF ANY:

MONTHLY - YTD- CUMULATIVE 11, HOURS IN REF'ORT PERIOD: 696 1440 40009.0 12 o NUMBER OF HOURS REACTOR WAS CRITICAL 696i8 1448iO 34198+0

13. REACTOR RESERVE SHUTDOWN HOURS 8+0 8iO OiO 14 o HOURS GENERATOR ON-LINE 696i8 1440+8 33477.6 15 o UNIT RESERVE SHUTDOWN HOURS 8 0 0 16+ GROSS THERMAL ENERGY GENERATED (MWH) 1876508 3881805 86878445
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 633310 1309540 28998200
18. NET ELECTRICAL ENERGY GENERATED (MWH) 601719 1244179 27411967
19. UNIT SERVICE FACTOR 180+8 180i8 83o7 "8, UNIT AVAILABILITYFACTOR. 108i8 108i0 83o7

'

CAF'ACITY FACTOR (USING MDC 183' 103i8 84o2 C*F'ACITY FACTOR (USING DER NET)

NET)'2.

104i2 184+1 83' 23m UNIT FORCED OUTAGE RATE 0 0 8 24> SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS o 25, IF SHUT DOWN. AT END OF REF'ORT PERIOD~ ESTIMATED DATE OF STARTUP:

41 II UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

UNIT NAME St Lucie Unit ¹g DATE March 15, 1988 COMPLETED BY N. W. Grant REPORT MONTH Februar 1988 TEI EPHONF (305 694-4432 Method of Shutting Ucensee Cause & Corrective Down Event System Component Action to No. Date Type'uration (Hours) Reason~ Reactor Report¹ Code4 Codes Prevent Recurrence Unit ¹2 had no shutdowns or signifi-cant power reductions.

F Forced Reason Method Exhibit G-Instructions S Scheduled A - Equipment Failure(Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram Entry Scheets Licensee C - Refueling 3 - Automatic Scram Event Report(LER) Fde, D - Reguhtory Restriction 4 - Continued (NUREG4161)

E - Operator Training & LIcense Examination 5 - Load Reduction F - Administrative 9 - Other(Explain)

G - Operational Error (Explain) Exhibit1-Same Source H - Other (Explain)

4>

f

WMMARYOF OPERATING EXPER CE DOCKET 'NO. 50-389.

UNIT St Lucie Unit ¹2 DATE March 15 . 1988 COMPLETED" BY N. W. Grant TELEPHONE 305 694-4432 REPORT MONTH'ebruary, 1988 Unit ¹2 operated at essentially. full power and had no "Unit shut-downs or significant power reductions."

In accordance with requirements of Technical Specifications 6.9. 1..6, there were no challenges to PORV or safety valves during the report, month.

II ~ .