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* 1.
1.
                         .Non-Routina,'Non-Radiological Environmental Report No.              50-313/75-36'
                         .Non-Routina,'Non-Radiological Environmental Report No.              50-313/75-36' 2 .' ' Report-Date:          . June 24,'1975 3.1 Occurrence Date:      June 16, 1975
            * *
      .
2 .' ' Report-Date:          . June 24,'1975 3.1 Occurrence Date:      June 16, 1975
: 4.      Facility:
: 4.      Facility:
Arkansas Nuclear One-Unit 1
Arkansas Nuclear One-Unit 1
,
:-                                              Russellville, Arkansas S.
:-                                              Russellville, Arkansas S.
Identification' of Occurrence:
Identification' of Occurrence:
Ammonia plant      concentrations
Ammonia plant      concentrations
                               ~in excess                in condenser circulating water increased across the of ETS limits.
                               ~in excess                in condenser circulating water increased across the of ETS limits.
                          .
15.
15.
Conditions Prior to Occurrence:
Conditions Prior to Occurrence:
                            .
                       -Steady-State Power              X Reactor Power    .2465    MWth Hot Standby Net Output                ,MWe Cald Shutdown Percent of Full Power 96 g Refueling Shutdown Load Changes During' Routine Routine Startup                                    Power Operation Operation Routine Shutdown Operation Other (specify)
                       -Steady-State Power              X
_
Reactor Power    .2465    MWth Hot Standby Net Output                ,MWe Cald Shutdown Percent of Full Power 96 g Refueling Shutdown Load Changes During' Routine Routine Startup                                    Power Operation Operation Routine Shutdown Operation Other (specify)
    ,
: 7. Description of Occurrence:
: 7. Description of Occurrence:
Samples taken;from the discharge canal and at point 20 on June ,16
Samples taken;from the discharge canal and at point 20 on June ,16 1975, than ammonia concentration at pointETS                            20 limit by is0.'11    og/1. indic 0.05 mg/1.
                                                                                      .
1975, than ammonia concentration at pointETS                            20 limit by is0.'11    og/1. indic 0.05 mg/1.
                                                                                                                .
        .
         .)
         .)
                                      .
M e                                                                      v 8005020 3f                                                      j
M
                                                                !
e                                                                      v 8005020 3f                                                      j
                -                ,
                                        ,


                  ..
        ,
                                                                                          '
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I 7  ,
k
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                  ''
              . .            ,
            . ,
* s*'
* s*'
Non-Itoutine, Non-Itadiological Environmental Report No.      50-313/75-36 8.-  Designation of Apparent Cause of Occurrence:
Non-Itoutine, Non-Itadiological Environmental Report No.      50-313/75-36 8.-  Designation of Apparent Cause of Occurrence:
                                       ~ Design
                                       ~ Design Procedure Manufacture                          Unusual Service Condition Including Environmental Installation /
                                                              "
Procedure
                                                      '
Manufacture                          Unusual Service Condition Including Environmental Installation /
Construction                      Corponent Failure            __
Construction                      Corponent Failure            __
Operator Other (speciff)      X Neutralizing tank was draining to the discharge flume at time of sampling.
Operator Other (speciff)      X Neutralizing tank was draining to the discharge flume at time of sampling.
                                                                                                                       .c v
                                                                                                                       .c v
                                                          .
: 9. Analysis of Occurrence:
: 9. Analysis of Occurrence:
.,
The neutralizing tank, which contains water impurities remaining after regenerating condensate demineralizers an,d plant. makeup water dominera-
The neutralizing tank, which contains water impurities remaining after regenerating condensate demineralizers an,d plant. makeup water dominera-
                                         .lizers, was being drained into the discharge fiume when samples were
                                         .lizers, was being drained into the discharge fiume when samples were
     '-                                  taken. - No other liquid releases were in progress at time of sampling.
     '-                                  taken. - No other liquid releases were in progress at time of sampling.
            .
e 9
e 9
0 4
0 4
9 0
9 0
                              % >,
,.
my-
my-
          .
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                                                                                                                        -
_
                                                      ,                                .-
:.          ,          ~                                                                                  ,
:.          ,          ~                                                                                  ,
                   . ? ' , . ;, -
                   . ? ' , . ;, -
Line 102: Line 64:
                                                                   ~
                                                                   ~
Arkansas Department of Pollution Control and Ecology or the EPA.
Arkansas Department of Pollution Control and Ecology or the EPA.
                                                                                                *
                          .
                                                                                                                      .
                                                                    '              .
o
o
  '
                -
: 11.      Failure Data:
: 11.      Failure Data:
The circumstances of this report are similar to those50-313/75-25 reported in through Non-
The circumstances of this report are similar to those50-313/75-25 reported in through Non-Routine, Non-Radiological Environmental Reports No.
  ,
                      -
Routine, Non-Radiological Environmental Reports No.
50-313/75-35.
50-313/75-35.
. . .
s O
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                                                                                                                    .
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           .                      ).
           .                      ).
                                      ,
            .
      >
                                                                                  .
* o    ..
* o    ..
o      -                NRC DISTRIBUTION FOR PART 50 DOCKET MATERIAL
o      -                NRC DISTRIBUTION FOR PART 50 DOCKET MATERIAL
   ~
   ~
           .                                      (TEMPORARY FORM)
           .                                      (TEMPORARY FORM)
CONTROL NO:      6832 FILE:    Enviro FROM: Arkansas Power (4 Light CaOATE OF DOC                  DATE REC'D          LTR    TWX    RPT      OTHER Little Rock, Ark
CONTROL NO:      6832 FILE:    Enviro FROM: Arkansas Power (4 Light CaOATE OF DOC                  DATE REC'D          LTR    TWX    RPT      OTHER Little Rock, Ark Arch P. Pettit                  6-24-75          6-26-75            xxx TO:                                              ORIG        CC    OTHER          SENT NRC PDR          xv
* Arch P. Pettit                  6-24-75          6-26-75            xxx TO:                                              ORIG        CC    OTHER          SENT NRC PDR          xv
     !!r. B.C. Rusche                        1-signed                                  SENT LOCAL PDR ***
     !!r. B.C. Rusche                        1-signed                                  SENT LOCAL PDR ***
CLASS        UNCLASS      PROPINFO              INPUT      NO CYS REC'D            DOCVET NO:
CLASS        UNCLASS      PROPINFO              INPUT      NO CYS REC'D            DOCVET NO:

Latest revision as of 05:15, 1 February 2020

Nonroutine Nonradiological Environ Rept 50-313/75-36:on 750616,ammonia Concentrations in Condenser Circulating Water Increased Across Plant in Excess of ETS Limits.Caused by Neutralizing Tank Draining Into Discharge Flume
ML19320A381
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 06/24/1975
From:
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML19320A376 List:
References
50-313-75-36, NUDOCS 8005020397
Download: ML19320A381 (4)


Text

-- .

k I .

1.

.Non-Routina,'Non-Radiological Environmental Report No. 50-313/75-36' 2 .' ' Report-Date: . June 24,'1975 3.1 Occurrence Date: June 16, 1975

4. Facility:

Arkansas Nuclear One-Unit 1

- Russellville, Arkansas S.

Identification' of Occurrence:

Ammonia plant concentrations

~in excess in condenser circulating water increased across the of ETS limits.

15.

Conditions Prior to Occurrence:

-Steady-State Power X Reactor Power .2465 MWth Hot Standby Net Output ,MWe Cald Shutdown Percent of Full Power 96 g Refueling Shutdown Load Changes During' Routine Routine Startup Power Operation Operation Routine Shutdown Operation Other (specify)

7. Description of Occurrence:

Samples taken;from the discharge canal and at point 20 on June ,16 1975, than ammonia concentration at pointETS 20 limit by is0.'11 og/1. indic 0.05 mg/1.

.)

M e v 8005020 3f j

I 7 ,

k

  • s*'

Non-Itoutine, Non-Itadiological Environmental Report No. 50-313/75-36 8.- Designation of Apparent Cause of Occurrence:

~ Design Procedure Manufacture Unusual Service Condition Including Environmental Installation /

Construction Corponent Failure __

Operator Other (speciff) X Neutralizing tank was draining to the discharge flume at time of sampling.

.c v

9. Analysis of Occurrence:

The neutralizing tank, which contains water impurities remaining after regenerating condensate demineralizers an,d plant. makeup water dominera-

.lizers, was being drained into the discharge fiume when samples were

'- taken. - No other liquid releases were in progress at time of sampling.

e 9

0 4

9 0

my-

'k

. , ~ ,

. ? ' , . ;, -

,1 .

50-313/75-36

~

Non-Routine, Non-Radiological Environmental Report No.

10. Corrective Action _:

Ee are reviewing our ETS chemical limits with the Arkansas Departncnt of Pollution Control and Ecology. It has been determined that there is no basis for many of our ETS chemical discharge' limits and that our water

-sampling and testing program does not verify that we are meeting or are not meeting the conditions of our permits to discharge issued by the

~

Arkansas Department of Pollution Control and Ecology or the EPA.

o

11. Failure Data:

The circumstances of this report are similar to those50-313/75-25 reported in through Non-Routine, Non-Radiological Environmental Reports No.

50-313/75-35.

s O

s 9

i

}

. ).

  • o ..

o - NRC DISTRIBUTION FOR PART 50 DOCKET MATERIAL

~

. (TEMPORARY FORM)

CONTROL NO: 6832 FILE: Enviro FROM: Arkansas Power (4 Light CaOATE OF DOC DATE REC'D LTR TWX RPT OTHER Little Rock, Ark Arch P. Pettit 6-24-75 6-26-75 xxx TO: ORIG CC OTHER SENT NRC PDR xv

!!r. B.C. Rusche 1-signed SENT LOCAL PDR ***

CLASS UNCLASS PROPINFO INPUT NO CYS REC'D DOCVET NO:

xxxxxx 1 50-313 DESCRIPTION: ENCLOSURES:

Ltr notarized 6-24-75 ... trans the followint : Non-Routine Enviro Rpp #75-36 on 6-16-75 concerning Ammonia concentrations in condenser circulating water increased across the plant ACKNC,JLOSED in excess f ET S hmi t s . . . . . . .

Y' " "

IJ V h L .L 1 ,; g G PLANT NAME:

Arkansas #1 FOF> ACTION /lNFORMATION 6-26-75 JGB BUTLER (L) SCHWENCER (L)[ZIEMANN (L) REGAN (E)

W/ Copies W/ Copies W/[ Copies W/ Copies CLARK (L) STOLZ (L) DICKER (E) LE AR (L)

W/ Copies W/ Copies W/ Copies W/ Copies PARR (L) VASSALLO (L) KNIGHTON (E) sPIss W/ Copies W/ Copics J// Copies W/ Copies KNIEL (L) PURPLE (L) WOUNGBLOOD (E) LPH W/ Copics W/ Jopies Wf) Copies W/ Copies INTERNAL DISTRIBUTION hG FILC) TECH REVIEW JENTON llc ASST. A/T IND, pritw 6'U H SCliROEDER GRIMES R. DIGGS (L) BRAITMAN OGC, ROOM P.506A MACCARY GAMMILL H. GEARIN (L) SALTZMAN GOSSICK/ STAFF KNIGHT . KASTNER E. GOU LBOURNE (L) MELTZ CASE PAWLICKl A ALLARD P. KREUTZER (E)

GIAMBUSSO SHAO SPANG LER J. LEE (L) PLANS BOYD STELLO M. MAIGRET (L) MCDONALD MOORE (L) HOUSTON _ ENVI RO. S. REED (E) CHAPMAN DEYOUNG (L) NOVAK MULLER M. SERVICE (L) DUBE (Ltr)

SKOVHOLT (L) ROSS DICKER S. SHEPPARD (L) E. COUPE GOLLER (L) (Ltr) IPPOLITO KNIGHTON M. SLATER (E) PETERSON P. CO LLINS TEDESCO YOUNGBLOOD H. SMITH (L) HARTFIELD (2)

DENISE LONG AN S E ETS (L) KLECKER .

AEG OPR LAIN AS JECT LDR . WILLI AMS (L, EISENHUT flLE & REGION (2) BENAROYA g V WILSON (L) jWIGGINTON V MIPC JOLLMER ,

HAR LE IINGRAM (L) FQgg[(

40.J.t. e W f M. DUNCAN z>

W s

EXTERNAL DISTRIBUTION LOCAL PDR Russellville, Ark (Il TIC (ABERNATHY; J?M2)' 0) - NATIONAL LABS gSM 1 - PD R-SAN /LA/NY NSIC (BUCHANAN) 1 - W. PENNINGTON, Rm E-201 GT 1 - BROOKHAVEN NAT LAB

[1-ASLB 1 - CONSULTANTS 1 - G. ULRIKSON ORNL 1 - Newton Anderson NEWMARK/BLUME/AGBABIAN

- ACRS HOLDING /SENT