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 Issue dateTitleTopic
ML20052E5363 May 1982RO 82-013/01T-0:on 820503,battery 2D12 Had Cell W/Voltage Less than Tech Spec requirements.Out-of-spec Readings Recorded 820501-03 & No Immediate Corrective Action Applied. Cause Not Stated
ML20050E2715 April 1982Ro:On 820402,two HPI Nozzles on Facility RCS Found to Require Corrective Action.Defects Will Be Corrected Before Returning to Power Operation
ML20041B01329 January 1982RO 82-001/01T-0:on 820107,six RCS Resistance Temp Detectors Did Not Meet Tech Spec Time Constant.Caused by Inadequate Coupling Between Detectors & Thermal Wall Due to Dried Out Couplant Compound.Couplant Replaced
ML20040B6157 January 1982RO 82-001/01T-0:on 820107,determination Made That Six RCS Resistance Temp Detectors Did Not Meet Required Response Time.Shutdown Initiated
ML20039B4949 December 1981RO SO-313/81-014 Re GE Model 12CFD12B1A Relays Used on Emergency Diesel Generators for Monitoring Proper Voltage to Current Phase Angle.Potential Problems Exist If Mechanical Agitation Precedes Circuit Energization
ML20003A95519 January 1981RO 50-313/81-01:on 810117,discussion W/Manufacturer Revealed Reactor Bldg Cooling Unit Piping Nozzles Should Not Be Considered Rigid Anchors as IE Bulletin 79-14 Analysis Indicated.Addl Piping Supports to Be Installed
ML19353A18622 December 1980RO 80-91:on 801220,channel Checks on Refueling Water Tank Level Indication Revealed That Channels A,C & D Indicated 100% & Channel B 82%.Caused by Frozen Refueling Water Tank Level Transmitters
ML19338F0644 September 1980RO 80-072:on 800903,review of 800820 Containment Coolant Surveillance Test Revealed Inadequate Svc Water Flows Through Containment Cooling Unit Coolers.Caused by Severe Plugging of Svc Water Flow Instrument Sensing Lines
ML19344E0191 August 1980RO 50-313/80-28:on 800731,access Plug Removal in Unit 1 Subjected Structure to Penetration of Wind Generated Missiles.Personnel Access Doors in Units 1 & 2 Do Not Appear to Be Missile Proof Barriers.Remedial Action Under Review
ML19330A54026 June 1980ROs 50-313/80-22 & 50-368/80-042:on 800624,events Occurred on 500 Kv Power Lines Which Resulted in Loss of All 500 Kv Power Lines & Reactor Trips of Both Units.Cause Not Stated. Both Units Stable.Followup Rept Will Be Transmitted
ML19318A6344 June 1980RO 50-368/80-037:on 800603,safety Injection Tank Boron Concentrations Reported Out of Tech Spec Condition. Possibly Caused by Boron Stratification.Boron Concentration Adjusted & Cause Being Investigated
ML19323B0037 April 1980RO I-80-01:800407,reactor Tripped.Caused by Loss of All Offsite Power.Natural Circulation Established.Bus A1 Put on Startup Transformer 2.Bus B2 Was Tied to B1.B3 Which Was Tied to B4.Diesel Generators Secured
ML19309F12919 March 1980RO 50-368/80-016:on 800318,after Reviewing C-E Ltr Re Discrepancy in Shutdown Margin for Boron Dilution in Mode 5 Util Notified NRC by Telcon.Tech Spec Change Request Will Be Submitted to Ensure Greater than 2% Shutdown MarginShutdown Margin
ML19309F09417 March 1980RO 50-313/80-007:on 800315,B&W Notified Util Decay Heat Pumps Contain Mating Wear Rings of Unequal Hardness Value. Mating Wear Rings Could Gall & Lock Up.B&W Recommends Replacement.Decay Heat Pumps Are Functioning Normally
ML19247B43225 July 1979RO 50-368/79-34 Has Been Voided
ML19248C58727 June 1979LER 79-N/A/99X-0 on 790522:during Routine Maint Investigation,Cable Leads at Location C-46,1-8-5,termination 2 & 6 Found to Be Lifted,But Not Tagged.Cause Unknown.Leads Reconnected
ML19242B43222 May 1979Special Rept 79-N/A/99X-0 on 790522:during Routine Insp, Cable Leads Were Found Lifted But Not Tagged.Lifted Leads Prevented Automatic Opening of Emergency Feedwater Valves. Cause Unknown.Leads Reconnected
ML19276F15616 March 1979Non-Routine Rept 50-313/79-01:on 790216,max Differential Temp Across Condenser Exceeded Tech Specs Limit.Caused by Excessive Fish Impingement on Water Intake Screen.Isolation Valves Being Cycled to Wash Off Debris
ML19309D9955 May 1978RO 50-313/78-12:on 780424,Group 7 Control Rods Dropped Into Core Due to Gate Drive Circuit Failure.Caused by Component Failure.Group 6 Inserted to Obtain Required overlap.780425 Telecopy Encl
ML19309D99625 April 1978RO 50-313/78-12:on 780424,Group 7 Control Rods Dropped Into Core Due to Gate Drive Circuit Failure.Cause Unknown.Group 6 Inserted to Obtain Required Overlap.Gate Will Be Repaired or Replaced
ML19326B51217 April 1978Nonroutine Radilogical Environ Rept 50-313/78-02:on 780403, I-131 Activity Levels for Milk Samples Were Higher than Normal & Above Tech Spec Limits.Caused by Chinese Nuclear Weapon Test of 780304.No Action Required by Util
ML19326B41614 April 1978RO 50-313/78-09:on 780413,B&W Informed Util That Analysis Results for 0.04 Ft Squared RCS Pump Discharge Break Unacceptable.Correction Action Will Be Proposed by 780417 & Operation Will Continue
ML19309D9201 November 1977Nonroutine Radiological Environ Rept 50-313/77-02:during Month of Oct 1977,milk & Vegetation Samples Produced Extrapolated Annual Dose Rates Greater than Tech Spec Design Limit.Caused by Fallout from Chinese 770917 Test
ML19309D9031 November 1977RO 50-313/77-20:on 771023,diesel Generator 1 Failed to Start During Monthly Test.Caused by Starter Failure Due to Time Delay Relay Setpoint Drift & Diode Shorting Out.Diode Replaced & Jumpered.Relay Setpoint Reset
ML19320A41714 October 1977Nonroutine Radiological Environ Rept 50-313/77-01:on 771005 & 06,I-131 Activity Levels in Milk Samples Exceeded Tech Spec Limit.Caused by Radioactive Fallout from Chinese Nuclear Weapon Test.No Corrective Action Required
ML19309D85722 September 1977RO 50-313/77-17:on 770824,small Leak Discovered in Casing Drain Line of E Primary Makeup Pump B.Cause Unknown.Leaking Drain Line Removed & New One Installed
ML19319E48320 September 1977RO 50-313/77-19:on 770906,during Review of Emergency Ventilation Sys for North & South Electrical Equipment Rooms, & North & South Battery & Charger Rooms,No Qualified or Emergency Sys Found to Exist.Caused by Design Error
ML19309D8458 September 1977RO 50-313/77-18:on 770826,surveillance Test Revealed That Hydrogen Purge Sys Failed to Indicate Proper Flow Rate. Caused by Water in Filters Due to Incorrect Sequence of Valve Operation During Placement.Filters Replaced
ML19319E5186 September 1977RO 50-313/77-19A:on 770920,heating,ventilation & Air Conditioning Equipment Found Insufficient for Cooling Sys in Electrical Equipment,Battery & Charger Rooms.Caused by Inadequate Design.Emergency Cooling Sys UsedSafe Shutdown
ML19309D88625 August 1977RO 50-313/77-15:on 770726,surveillance Test Revealed Three Penetrations W/High Leakage Rate.Caused by Foreign Matter in Isolation Valves.Repairs to Isolation Valves Reduced Leakage
ML19309D88025 August 1977RO 50-313/77-16:on 770805,monthly Surveillance Test on Diesel Generator Not Performed at Specified Time.Caused by Personnel Error.Importance of Performing Test on Timely Basis re-emphasized
ML19309D8948 July 1977RO 50-313/77-14:on 770612,penetration Room Ventilation Sys Circuit Breakers 52-6313 & 52-6314 Tripped.Caused by Thermal Overload Settings for Circuit Breakers Set to Low.Circuit Breaker Setting Reset to Higher Value
ML19319E5741 July 1977RO 50-313/77-13:on 770602,reactor Bldg Cooling Fan VSFM-1A Found Inoperable.Caused by Motor Failure Due to Insufficient Lubrication of Motor Bearings.Vendor Will Repair Motor. Bearings Will Be Lubricated on Frequent Schedule
ML19319E5833 June 1977RO 50-313/77-12:on 770505,leak Discovered at pipe-to-pipe Weld in High Discharge Piping to Spent Fuel Pool.Cause Unknown.Leak Isolated from Sys.Repairs to Be Made as Soon as Possible
ML19317H06829 April 1977RO 50-313/77-10:on 770331,leak Rate Test Improperly Performed on Reactor Bldg Escape Hatch.Caused by Personnel Error Failing to Check Cavity Between Hatch Doors.Hatch Retested & Found Acceptable
ML19317H07129 April 1977RO 50-313/77-11:on 770331,4.71 Ci Pu-Be Source Used by Plant Personnel Found Not Tested for Leakage within Six Months. Caused by Personnel Error.Importance of Conducting Test on Schedule re-emphazed.Source Tested & Found Acceptable
ML19326C0329 April 1977RO 50-313/76-1A:on 760105,required Overlap Between Operating Control Rod Groups Lost.Caused by Component Failure. Redundant Relay Addition in Circuitry Will Require Simultaneous Failure to Cause Ratchet Trip
ML19320A1508 April 1977RO 50-313/77-5A:on 770128,pinhole Leak Observed on pipe-to- Flange Weld Between Valve & Seal During Routine Investigation.Cause Unknown.Defective Weld Repaired During Refueling Outage
ML19326C0208 April 1977RO 50-313/76-03:on 760325,reactor Surveillance Specimen Holder Tube Failed.Caused by Missing Spring Cartridge & Push Rod & Journal Bearing.Reactor Will Be Defueled,Internals Removed,Loose Parts Retrieved & Mods & Insp Initiated
ML19319E5618 April 1977RO 50-313/77-09:on 770310,penetration Room Ventilation Sys Valve CV-2123 Found Inoperable During Engineered Safeguard Actuation Sys Integrated Test.Caused by Inadequate Breaker Overload Heaters.Heaters Replaced W/Higher Amperage Rating
ML19319E57018 March 1977RO 50-313/77-08:on 770218,reactor Bldg Chilled Water Inlet Isolation Valve CV-6202 Failed to Remain Closed During Local Leak Rate Testing of Penetration 51.Caused by Foreign Matl in Solenoid Valve.Valve Replaced
ML19319E58514 March 1977RO 50-313/77-06:on 770219,surveillance Test Indicated Two HPI Flow Transmitters on Loop a Failed & Two Flow Transmitters on Loop B Out of Tolerance.Caused by Bellows Fatigue & Overpressurization.Bellows Replaced
ML19319E57610 March 1977RO 50-313/77-07:on 770224,two Fuel Pins Damaged While Loading New Fuel Assembly Into Core Position 1-2.Caused by Slight Warping of Fuel Assemblies.Assembly Removed.Awaiting New Assembly.Fuel Loading ContinuedFuel cladding
ML19320A1557 March 1977RO 50-313/77-5:on 770128,at Hot Shutdown Conditions During Routine walk-through Investigation,Pinhole Leak Discovered on Upstream pipe-to-valve Weld of Valve RBW-77B.Cause Unknown.Repair of Weld Scheduled for Refueling Outage
ML19319E56015 February 1977RO 50-313/77-04:on 770124,control Room Emergency Ventilation Unit 2VSF-9 Taken Out of Svc to Be Replaced W/Larger Capacity Unit.Caused by Need to Upgrade Sys.Larger Unit Installed
ML19319E56615 February 1977RO 50-313/77-03:on 770122,steam Driven Emergency Feedwater Pump P-7A Bearings Began to Smoke Following Surveillance Test & Pump Shutdown.Caused by Component Failure.Bearings Replaced
ML19326B4657 February 1977RO 50-313/77-02:on 770120,leak Discovered on Reducer Weld Located in Spent Fuel Demineralizer Resin Transfer Line. Cause Not Determined.Section of Line & Reducer Cut & Replaced.Similar Cracks Reported in ROs 76-28 & 76-34
ML19319E5542 February 1977RO 50-313/77-01:on 770110,four Frozen Sensing Lines & Actuated Pressure Switch PS2668B in Red Channel Discovered When Slbic Alarm Sounded in Control Room.Caused by Subfreezing Temps.Slbic Removed from Svc While Lines Thawed
ML19319E54130 December 1976RO 50-313/76-34:on 761201,valve SF-10 in Spent Fuel Cooling Sys Leaked.Caused by Crack in Heat Affected Zone of Valve SF-11.Valve SF-11 Will Be Replaced
ML19319E42210 December 1976RO 50-313/76-33:on 761122,fire Sys Deluge Trip Rendered Diesel Generator 1 Inoperable.Caused by Leak Off of Sealing Pressure to Deluge Valve.Engine & Exciter Control Cabinets Dried & Deluge Valve to Be Shut to Ensure Sealing Pressure