ML19242B432
| ML19242B432 | |
| Person / Time | |
|---|---|
| Site: | Arkansas Nuclear |
| Issue date: | 05/22/1979 |
| From: | Shively C ARKANSAS POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML19242B424 | List: |
| References | |
| NUDOCS 7908080511 | |
| Download: ML19242B432 (1) | |
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U. $_ NUCLE AR RE GUL ATORY COMMisstON hRC F ORM 366 (7 77l LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCK-l l l l \\ ]
(PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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EVENT D ATE 74 ib HEPOM T D ATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h
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Lpurinc a routine maintenance investigation, cable leads at location i
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- o l a i I C-46. 1-8-5 termination 2 6 6 were found to be lifted, I
Ibut were not tarred in accordance with procedure 1005.04, I
o 1" Control 6 Use of Bypass 6 Jumpers". The lifted leads prevents the i
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l automatic opening cf ICS control Emergency Feedwater valves cv-2670 j
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o > 16 cv-2620: however, thev were operable by manual control. There have I
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i been no similar occurrences.
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C AUSE DESCR.PTION AND CORREC rive ACTIONS h IThe valves were actuated automatically last on 12/31/78. A search o
t i li j iof maintenance documentation failed to reveal when or why the i
ii12i 11eads were lifted, but it is postulated that they were lifted i
lduring the present refueling outage. The leads were reconnected 3
land the valves proven operable.
ISC and electrical personnel to review oc.currencc i
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