ML19317H071

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RO 50-313/77-11:on 770331,4.71 Ci Pu-Be Source Used by Plant Personnel Found Not Tested for Leakage within Six Months. Caused by Personnel Error.Importance of Conducting Test on Schedule re-emphazed.Source Tested & Found Acceptable
ML19317H071
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 04/29/1977
From: Mardis D
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML19317H067 List:
References
NUDOCS 8004110843
Download: ML19317H071 (4)


Text

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89 80 I sc.utoutz. I FACUTv METHC0 OF STATUS 4 POWER OTHER STATUS CISCOVERY DISCOVERY DESCRipTON 1

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lo le lo l I ww I-7 89 11 12 0 80 0FFSITE CONSEQUENCES DE I %K l 7 89 80 LOSS OR DAMAGE TO FAC:tlTY TYPE DESCR@ TON 1 lij l e I.

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1. Reportable Occurrence Report No.

50-313/77-11

2. Report Date: April 29, 1977 3. Occurrence Date: March 31,1977 4 Facility: Arkansas Nuclear One-Unit 1 Russellville, Arkansas 72801

__ _5. _ Identification of Occurrence: - -

The occurrence is the failure to perfom a surveillance test at the required frequency.

6. Conditions Prior to Occurrence:

Steady-State Power Reactor Power 0 MWth Hot Standby Net Output 0 MWe Cold Shutdown Percent of Full Power 0  %

Refueling Shutdown Load Changes During Routine Power Operation j Routine Startup Operat2cn Routine- Shutdown Operation Other (specify) X Starting Plant Heatup Following Refueling

._. 7. Description of Occurrence: -

At approximately 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> on March 31, 1977, it was discovered that the 4.71 C1 Pu-Be Source had not been leak tested in the last 6 months in accordance with Technical Specification 4.14 prior to use by ISC l personnel during the period 3/12/77 to 3/15/77. The sealed source leak test was due to be perfomed on 12/26/76 the the +2S% allowance would have expired on approximately 2/4/77. -

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%) Reportable Occurrence Report No. S0-313/77-11

8. Designation of Apparent Cause of Occurrence:

Design Procedure Manufacture Unusual Service Condition Including Environmental -

~~

Installation /

Construction Component Failure (See Failure Data)

Operator Other (specify) X Administrative Control

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9. Analysis of Occurrence:

Since the source was leak tested satisfactorily and there was no removable surface contamination found, no hazard to the health and  ;

safety of the public existed.  ;

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Reportable Occurrence Report No.

10. Corrective Action:

Tlw source was leak tested on March 31, 1977 and the importance of

-- comp.?eting source leak testing on schedule has been reemphasi:ed to plant personnel. The Pu-Be source is being tagged to show last

-- leak. check date and date due. - -- -

l l

11. Failure Data:

There has been no other occurrence reported due to the failure of the Health Physics Group to perfo m surveillance tests at the required frequency.

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