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The inspectors performed a system walkdown on service water and/or closed cooling water systems to determine whether the licen see's assessment on structural integrity was adequate. In addition, the inspectors reviewed available licensee's testing and inspections results, licensee's disposition of any active thru wall pipe leaks, and the history of thru wall pipe leakage to identify any adverse trends since the last NRC inspection. For closed cooling water systems, the inspectors reviewed operating logs or interviewed operators or system engineer, to identify adverse make-up trends that could be indicative of excessive leakage out of the closed system. For buried or inaccessible piping, the inspectors reviewed the licensee's pipe testing, inspection, or monitoring program to determine whether structural integrity was ensured and that any leakage or degradation was appropriately identified and dispositioned by the licensee.
The inspectors performed a system walkdown on service water and/or closed cooling water systems to determine whether the licen see's assessment on structural integrity was adequate. In addition, the inspectors reviewed available licensee's testing and inspections results, licensee's disposition of any active thru wall pipe leaks, and the history of thru wall pipe leakage to identify any adverse trends since the last NRC inspection. For closed cooling water systems, the inspectors reviewed operating logs or interviewed operators or system engineer, to identify adverse make-up trends that could be indicative of excessive leakage out of the closed system. For buried or inaccessible piping, the inspectors reviewed the licensee's pipe testing, inspection, or monitoring program to determine whether structural integrity was ensured and that any leakage or degradation was appropriately identified and dispositioned by the licensee.


The inspector performed a system walkdown of the service water intake structure to determine whether the licensee's assessment on structural integrity and component functionality was adequate and that the licensee ensured proper functioning of traveling screens and strainers, and structural integrity of component mounts. In addition, the inspectors determined whether service water pump bay silt accumulation was monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments were functional and routinely monitored. The inspectors also determined whether the licensee's ability to ensure functionality during adverse weather conditions was adequate. In addition, the inspectors reviewed condition reports related to the heat exchangers/coolers and heat sink performance issues to determine whether the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. Documents reviewed are listed in the Attachment. These inspection activities constituted four heat sink inspection samples as defined in IP
The inspector performed a system walkdown of the service water intake structure to determine whether the licensee's assessment on structural integrity and component functionality was adequate and that the licensee ensured proper functioning of traveling screens and strainers, and structural integrity of component mounts. In addition, the inspectors determined whether service water pump bay silt accumulation was monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments were functional and routinely monitored. The inspectors also determined whether the licensee's ability to ensure functionality during adverse weather conditions was adequate. In addition, the inspectors reviewed condition reports related to the heat exchangers/coolers and heat sink performance issues to determine whether the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. Documents reviewed are listed in the Attachment. These inspection activities constituted four heat sink inspection samples as defined in IP 71111.07-05.
 
==71111.07 - 05.==


====b. Findings====
====b. Findings====

Revision as of 18:28, 12 October 2018

IR 05000395-13-005 & 05000395-13-502; 10/01/2013 - 12/31/2013: Virgil C. Summer Nuclear Station, Unit 1; Other Activities
ML14041A474
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 02/10/2014
From: King M F
NRC/RGN-II/DRP/RPB5
To: Gatlin T D
South Carolina Electric & Gas Co
References
IR-13-005, IR-13-502
Download: ML14041A474 (30)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 February 10, 2014

Mr. Thomas Vice President - Nuclear Operations South Carolina Electric & Gas Company Virgil C. Summer Nuclear Station P.O. Box 88 Jenkinsville, SC 29065

SUBJECT: VIRGIL C. SUMMER NUCLEAR STATION, UNIT 1 - NRC INTEGRATED INSPECTION REPORT 05000395/2013005 and 05000395/2013502

Dear Mr. Gatlin:

On December 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Virgil C. Summer Nuclear Station, Unit 1. On February 5, 2014, the NRC inspectors discussed the results of this inspection with you and members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

NRC inspectors documented in this report one NRC-identified finding of very low safety significance (Green) and which involved violations of NRC requirements. The NRC is treating the violation as a non-cited violation (NCV)

consistent with Section 2.3.2.a of the NRC Enforcement Policy. If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-

0001; and the NRC Resident Inspector at the Virgil C. Summer Nuclear Station, Unit 1.

Additionally, if you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the Virgil C. Summer Nuclear Station, Unit 1. As a result of the Safety Culture Common Language Initiative, the terminology and coding of cross-cutting aspects were revised beginning in calendar year (CY) 2014. New cross-cutting aspects identified in CY 2014 will be coded under the latest revision to IMC 0310. Cross-cutting aspects identified in the last six months of 2013 using the previous terminology will be converted to the latest revision in accordance with the cross-reference in IMC 0310. The revised cross-

cutting aspects will be evaluated for cross-cutting themes and potential substantive cross-

cutting issues in accordance with IMC 0305 starting with the CY 2014 mid-cycle assessment review.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's Agencywide Document Access and managem ent System (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ Michael King, Chief Reactor Projects Branch 5

Division of Reactor Projects Docket No.: 50-395 License No.: NPF-12

Enclosure:

NRC Integrated Inspection Report 05000395/2013005

w/Attachment:

Supplemental Information

cc Distribution via ListServ

_________________________ SUNSI REVIEW COMPLETE FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRP RII:DRS RII:DRP RII:DRP RII:DRP SIGNATURE Via email Via email Via email Via email SON /RA/ BDB /RA/ NAME JReece ECoffman DBacon RWilliams SNinh JParent BBishop DATE 02/03/2014 01/31/2014 01/23/2014 01/27/2014 01/28/2014 01/27/2014 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRP SIGNATURE MFK /RA/ NAME MKing DATE 02/10/2014 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO Letter to Thomas from Michael King dated February 10, 2014

SUBJECT: VIRGIL C. SUMMER NUCLEAR STATION, UNIT 1 - NRC INTEGRATED INSPECTION REPORT 05000395/2013005

Distribution

C. Evans, RII L. Douglas, RII OE Mail RIDSNRRDIRS

PUBLIC RidsNrrPMSummer Resource

Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION II

Docket No. 50-395

License No. NPF-12

Report No. 05000395/2013005 and 05000395/2013502

Licensee: South Carolina Electric & Gas (SCE&G) Company

Facility: Virgil C. Summer Nuclear Station, Unit 1

Location: P.O. Box 88 Jenkinsville, SC 29065

Dates: October 1, 2013, through December 31, 2013

Inspectors: J. Reece, Senior Resident Inspector E. Coffman, Resident Inspector R. Williams, Senior Reactor Inspector (Section 1R07) D. Bacon, Senior Operations Engineer (Section 1R11.3)

J. Laughlin, Emergency Preparedness Inspector (Section 1EP4)

Approved by: Michael King, Chief Reactor Projects Branch 5 Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000395/2013005; 10/01/2013 - 12/31/2013: Virgil C. Summer Nuclear Station, Unit 1;

Other Activities

The report covered a three month period of inspection by resident inspectors and three health physicists from the region. One NRC-identified finding was identified and determined to be a Green, non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspects were determined using IMC 0310,

"Components Within the Cross Cutting Areas." Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process" Revision 4, dated December 2006.

Cornerstone: Barrier Integrity

  • Green: An NRC-identified Green non-cited violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings,"was identified for the licensee's failure to prescribe an adequate procedure for control of temporary containment penetration devices. The violation is in the licensee's corrective action program as condition report 13-00739.

The inspectors determined that the failure to have an adequate procedure for control of temporary containment penetration devices was a performance deficiency (PD). The PD is more than minor and therefore a finding because it impacted the barrier integrity cornerstone objective to provide reasonable assurance that physical design barriers such as the containment, protect the public from radionuclide releases caused by accidents or events and the attribute of procedure quality because the affected procedure allowed the use of silicone foam in configurations which did not provide adequate pressure retention capabilities. The inspectors evaluated the finding in accordance with NRC Inspection Manual Chapter 0609, "Significant Determination Process," attachment 4, appendix G, and appendix H and determined that an analysis was required by a senior reactor analyst. A regional SRA performed an SDP assessment of this finding. The licensee containment penetration testing and results were reviewed as well as the licensee's risk evaluation. The conclusion was that the finding represented a condition B finding which would only impact large early release fraction (LERF) and not core damage frequency. The test results showed that the finding would not meet the leakage criteria necessary for the finding to be >GREEN per NRC IMC 0609 Appendix H. The conditions necessary to achieve the leakage criteria were determined to be <1E-7 for LERF which represented a GREEN finding of very low safety significance. There are no cross-cutting aspects because the finding was not representative of current licensee performance. (Section 4OA5.2)

REPORT DETAILS

Summary of Plant Status

The unit began the inspection period at full Rated Thermal Power (RTP) and operated at or near

full RTP for the remainder of the quarter.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness

1R01 Adverse Weather Protection

Seasonal Weather Susceptibilities

a. Inspection Scope

The inspectors performed one seasonal extreme weather inspection for readiness of cold weather for two risk significant components. The inspectors verified the licensee had implemented applicable sections of operations administrative procedure (OAP)-109.1, Revision (Rev.) 3F, "Guidelines for Severe Weather." The inspectors reviewed preparations for extreme cold weather and walked down the refueling water storage tank (RWST) and associated outside emergency core cooling system (ECCS) piping and walked down the sodium hydroxide (NaOH) tank and associated outside piping to assess whether the equipment was adequately protected from cold weather and would function as expected during an accident event. Also, the inspectors reviewed the licensee's corrective action program (CAP) database to verify that freeze protection problems were being identified at the appropriate level, entered into the CAP, and appropriately resolved.

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial System Walkdowns

a. Inspection Scope

The inspectors conducted three partial equipment alignment walkdowns which are listed below, to evaluate the operability of selected redundant trains or backup systems with the other train or system inoperable or out of service (OOS). Correct alignment and operating conditions were determined from the applicable portions of drawings, system operating procedures (SOP), and technical specifications (TS). The inspections included review of outstanding maintenance work orders (WO) and related condition reports (CR) to verify that the licensee had properly identified and resolved equipment alignment problems that could lead to the initiation of an event or impact mitigating system availability. Documents reviewed are listed in the Attachment.

  • Partial walkdown of 'B' motor driven emergency feedwater (MDEFW) and turbine driven emergency feedwater (TDEFW) components during planned maintenance on 'A' MDEFW pump
  • Partial walkdown of 'A' and 'B' MDEFW components during planned maintenance on the TDEFW pump

b. Findings

No findings were identified.

1R05 Fire Protection

Quarterly Fire Protection Walkdowns

a. Inspection Scope

The inspectors reviewed recent CRs, WOs, and impairments associated with the fire protection system. The inspectors reviewed surveillance activities to determine whether they supported the operability and availability of the fire protection system. The inspectors assessed the material condition of the active and passive fire protection systems and features, and observed the control of transient combustibles and ignition sources. Documents reviewed are listed in the attachment. The inspectors conducted routine inspections of the following five areas (respective fire zones also noted):

  • Charging pump rooms (fire zones AB-1.5, 1.6 and 1.7)
  • Control room (fire zones CB-17.1)
  • Control building 412' and 425' elevations (fire zones CB-1.1, 1.2, CB-2, and CB-5)
  • HVAC chilled water pump rooms 'A' and 'B' (fire zones IB-7.2, IB-9, and IB-23.1)
  • Intermediate building 412' elevation (fire zones IB-1, IB-2, IB-3, IB-4, IB-5 and IB-27)

b. Findings

No findings were identified.

1R06 Flood Protection Measures

Internal Flooding

a. Inspection Scope

The inspectors reviewed and walked down the control building CB-436 feet, 448 feet and 463 feet elevations regarding internal flood protection features and equipment to determine consistency with design requirements, final safety analysis report (FSAR), and flood analysis documents. Risk significant structures, systems, and components (SSCs) in these areas included the nuclear steam support system (NSSS) relays, NSSS process cabinets, solide state protection system (SSPS) cabinets, and the main control board. The inspectors reviewed the licensee's CAP database to verify that internal flood protection problems were being identified at the appropriate level, entered into the CAP, and appropriately resolved. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

Triennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors reviewed operability determinations, completed surveillances, vendor manual information, associated calculations, performance test results, and cooler inspection results associated with the service water (SW) pump 'A' motor cooler, the reactor building cooling unit (RBCU) 'A' and the charging/safety injection (SI) pump oil cooler. These heat exchangers/coolers were chosen based on their risk significance in the licensee's probabilistic safety analysis, their important safety-related mitigating system support functions and their relatively low margin.

For the SW pump 'A' motor cooler and the RBCU 'A', the inspectors determined whether testing, inspection, maintenance, and monitoring of biotic fouling and macrofouling programs were adequate to ensure proper heat transfer. This was accomplished by determining whether the test method used was consistent with accepted industry practices, or equivalent, the test conditions were consistent with the selected methodology, the test acceptance criteria were consistent with the design basis values, and reviewing results of heat exchanger performance testing. The inspectors also determined whether the test results appropriately considered differences between testing conditions and design conditions, the frequency of testing based on trending of test results was sufficient to detect degradation prior to loss of heat removal capabilities below design basis values, and test results considered test instrument inaccuracies and differences.

In addition, the inspectors determined whether the condition and operation of the SW pump 'A' motor cooler and the RBCU 'A' heat exchangers were consistent with design assumptions in heat transfer calculations, and as described in the final safety analysis report. This included determining whether the number of plugged tubes was within pre-established limits based on capacity and heat transfer assumptions. The inspectors determined whether the licensee evaluated the potential for water hammer and established adequate controls and operational limits to prevent heat exchanger degradation due to excessive flow induced vibration during operation. In addition, eddy current test reports and visual inspection records were reviewed to determine the structural integrity of the heat exchanger.

For the charging/SI pump oil cooler, the inspectors determined whether the condition and operation of the heat exchanger were consistent with design assumptions in heat transfer calculations, and as described in the final safety analysis report. This included

determining whether the number of plugged t ubes was within pre-established limits based on capacity and heat transfer assumptions. The inspectors determined whether the licensee evaluated the potential for water hammer and established adequate controls and operational limits to prevent heat exchanger degradation due to excessive flow induced vibration during operation. In addition, eddy current test reports and visual inspection records were reviewed to determine the structural integrity of the heat exchanger. The inspectors determined whether the licensee's chemical treatment programs for corrosion control were consistent with industry norms and implemented accordingly.

The inspectors determined whether the performance of ultimate heat sinks (UHS), and their subcomponents such as piping, intake screens, pumps, valves, etc., was appropriately evaluated by tests or other equivalent methods, to ensure availability and accessibility to the in-plant cooling water systems. The inspectors determined whether the licensee's inspection of the UHS was thorough and of sufficient depth to identify degradation of the shoreline protection or loss of structural integrity. This included determination whether vegetation present along the slopes was trimmed, maintained, and was not adversely impacted the embankment. In addition, the inspectors determined whether the licensee ensured sufficient reservoir capacity by trending and removing debris, or sediment buildup, in the UHS. The inspectors reviewed the licensee's performance testing of service water system and UHS results. This included a review of the licensee's performance test results for key components and service water flow balance test results. In addition, the inspectors compared the flow balance results to system configuration and flow assumptions during design basis accident conditions. The inspectors also determined whether the licensee ensured adequate isolation during design basis events, consistency between testing methodologies and design basis leakage rate assumptions, and proper performance of risk significant non-safety related functions.

The inspectors performed a system walkdown on service water and/or closed cooling water systems to determine whether the licen see's assessment on structural integrity was adequate. In addition, the inspectors reviewed available licensee's testing and inspections results, licensee's disposition of any active thru wall pipe leaks, and the history of thru wall pipe leakage to identify any adverse trends since the last NRC inspection. For closed cooling water systems, the inspectors reviewed operating logs or interviewed operators or system engineer, to identify adverse make-up trends that could be indicative of excessive leakage out of the closed system. For buried or inaccessible piping, the inspectors reviewed the licensee's pipe testing, inspection, or monitoring program to determine whether structural integrity was ensured and that any leakage or degradation was appropriately identified and dispositioned by the licensee.

The inspector performed a system walkdown of the service water intake structure to determine whether the licensee's assessment on structural integrity and component functionality was adequate and that the licensee ensured proper functioning of traveling screens and strainers, and structural integrity of component mounts. In addition, the inspectors determined whether service water pump bay silt accumulation was monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments were functional and routinely monitored. The inspectors also determined whether the licensee's ability to ensure functionality during adverse weather conditions was adequate. In addition, the inspectors reviewed condition reports related to the heat exchangers/coolers and heat sink performance issues to determine whether the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. Documents reviewed are listed in the Attachment. These inspection activities constituted four heat sink inspection samples as defined in IP 71111.07-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Resident Quarterly Review of Operator Requalification

a. Inspection Scope

The inspectors observed an operator requalification exam validation occurring on December 2, 2013. The inspectors observed crew performance in terms of communications; ability to prioritize failures in order to take timely and proper actions; prioritizing, interpreting, and verifying alarms; correct use and implementation of procedures, including the alarm response procedures; timely control board operation and manipulation, including high-risk operator actions; and oversight and direction provided by the shift supervisor, including the ability to identify and implement appropriate TS actions and when required, emergency action levels as the Site Emergency Director. The inspectors reviewed the licensee's critique comments to verify that performance deficiencies were captured for appropriate corrective action.

b. Findings

No findings were identified.

.2 Resident Quarterly Observation of Control Room Operations

a. Inspection Scope

During the inspection period, the inspectors conducted observations of licensed reactor operator activities to ensure consistency with licensee procedures and regulatory requirements. For the two listed activities, the inspectors observed the following elements of operator performance: 1) operator compliance and use of plant procedures including technical specifications; 2) control board component manipulations; 3) use and interpretation of plant instrumentation and alarms; 4) documentation of activities; 5) management and supervision of activities; and 6) control room communications.

  • Observation of 'B' train solid state protection system (SSPS) surveillance test and respective pre-job brief; reactor coolant system (RCS) dilutions
  • Observation of alternate seal injection (ASI) performance testing

b. Findings

No findings were identified.

.3 Annual Review of Licensee Requalification Examination Results

a. Inspection Scope

On August 15, 2013, the licensee completed the comprehensive biennial requalification written examinations and the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of

Federal Regulations 55.59(a)(2), "Requalification requirements," of the NRC's "Operators' Licenses." The inspectors per formed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, "Licensed Operator Requalification Program and Licensed Operator Performance." The results were compared to the thresholds established in Section 3.02, "Requalification Examination Results," of IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors evaluated two equipment issues described in the CRs listed below to verify the licensee's effectiveness with the corresponding preventive or corrective maintenance associated with structure, system, and components (SSCs). The inspectors reviewed Maintenance Rule (MR) implementation to verify that component and equipment failures were identified, entered, and scoped within the MR program.

Selected SSCs were reviewed to verify proper categorization and classification in accordance with 10 CFR 50.65. The inspectors examined the licensee's 10 CFR 50.65(a)(1) corrective action plans to determine if the licensee was identifying issues related to the MR at an appropriate threshold and that corrective actions were established and effective. The inspectors' review also evaluated if maintenance preventable functional failures or other MR findings existed that the licensee had not identified. The inspectors reviewed the licensee's controlling procedures consisting of engineering services procedure (ES)-514, Rev. 6, "Maintenance Rule Program Implementation," and station administrative procedure (SAP)-0157, Rev. 1, "Maintenance Rule Program," to verify consistency with the MR program requirements.

  • CR-12-01982 and CR-12-05975, steam generator (SG) power operated relief valves (PORVs) in (a)(1) for exceeding reliability criteria
  • CR-13-00054 and CR-13-01781, maintenance preventable functional failure of instrument air compressor to pressurizer PORV's exceeds reliability performance criteria and results in (a)(1) status

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessment and Emergent Work Control

a. Inspection Scope

The inspectors performed risk assessments, as appropriate, for the four selected work activities listed below: 1) the effectiveness of the risk assessments performed before maintenance activities were conducted; 2) the management of risk; 3) that, upon identification of an unforeseen situation, necessary steps were taken to plan and control the resulting emergent work activities; and, 4) that emergent work problems were adequately identified and resolved. The inspectors evaluated the licensee's work prioritization and risk characterization to determine, as appropriate, whether necessary steps were properly planned, controlled, and executed for the planned and emergent

work activities.

  • Work Week 46, yellow risk condition for Parr 115kV line out of service, 'A' and 'B' emergency alternating current (AC) buses tied to a common source
  • Work Week 48, yellow risk condition due to TDEFW planned maintenance
  • Work Week 51, yellow risk condition due to ASI being out of service
  • Work Week 51, yellow risk condition for scheduled maintenance on 'A' SW pump and associated components

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed five operability evaluations listed below, affecting risk significant mitigating systems to assess, as appropriate: 1) the technical adequacy of the evaluations; 2) whether operability was properly justified and the subject component or system remained available, such that no unrecognized increase in risk occurred; 3) whether other existing degraded conditions were considered; 4) that the licensee considered other degraded conditions and their impact on compensatory measures for the condition being evaluated; and, 5) the impact on TS limiting conditions for operations and the risk significance in accordance with the significance determination process. The inspectors also verified that the operability evaluations were performed in accordance with SAP-209, Rev. 1, "Operability Determination Process," and SAP-999, Rev. 11, "Corrective Action Program."

  • CR-12-02152, NRC identified PVC based material melted on stainless steel RHR valves and piping, Rev. 1
  • CR-13-01027, NRC identified a seimic issue with the 'B' safety-related incoming 7.2 kV breaker cubicle door being open
  • CR-13-01755, 'B' train wide range reactor vessel level indication has signs of signal degradation
  • CR-13-03468, 'B' component cooling water (CCW) heat exchanger performance degraded

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed one temporary modification and completed review of two permanent plant modifications or engineeri ng change requests (ECR) as noted below to evaluate the change for adverse effects on system availability, reliability, and functional capability. Documents reviewed included engineering calculations, WOs, site drawings, applicable sections of the FSAR, supporting 10 CFR 50.59 evaluations, TS, and design basis information. The inspectors evaluated the change documents and associated 10 CFR 50.59 reviews against the system design basis documentation and FSAR to verify that the changes did not adversely affect the safety function of safety systems. The inspectors also reviewed any related CRs to confirm that problems were identified at an appropriate threshold, were entered into the CAP, and appropriate corrective actions had been initiated. Other documents reviewed are listed in the attachment.

  • WO1300346, Main control room 3-phase display of transformer, XTF31, high side currents for open phase event detection
  • ECR-50780, ASI system installation
  • ECR-50825, Burial of the Parr 115kV Line Segment

b. Findings

Introduction:

An unresolved item (URI) regarding ECR-50780 was identified by the inspectors for a performance deficiency associated with inadequate post modification testing for the ASI system.

Description:

During the Fall, 2012 refueling outage, the licensee completed ECR-50780 and placed the ASI system in service to provide a backup for reactor coolant pump (RCP) seal injection in the event of a station blackout (SBO) or other events resulting in low normal RCP seal injection flow. The inspectors noted during their review that the ASI system has a mission time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> with no operator action required and consists of a positive displacement pump powered by a dedicated diesel generator, valves,piping, flow transmitters, and other components. The inspectors noted that the RWST provides the suction source, and the discharge of the ASI system ties in to the chemical volume control system (CVCS) upstream of the normal seal water injection filters (SWIFs) of which there are two in parallel, one normally in service and manual operator action required to realign on high differential pressure. The inspectors also noted that the filters used for normal operation are sized at

.1 micron.

The inspectors review of post modification testing identified that the potential clogging of the SWIFs was not considered as an impact on the mission time. The licensee initiated CR-13-000642 for an evaluation and initiated a Special Order for heightened awareness of a SWIF differential pressure annunciator occurring during those events resulting in actuation of the ASI system.

The inspectors also reviewed technical work record (TWR) 14809 dated December 10, 1997, which allowed the use of

.1 micron filters via the licensee's equal to - better than

process (ETBT) #157A and respective 50.59 screening. The inspectors determined that the impact of filter clogging during a design basis accident was not considered. The licensee initiated CR-13-01853, to evaluate this problem. Pending completion of evaluations in determining related PDs and their characterization, this issue is identified as URI 05000395/2013005-01, Seal Water Injection Filter Impact on Alternate Seal Injection System and Design Basis Accidents.

1R19 Post Maintenance Testing

a. Inspection Scope

For the four maintenance activities listed below, the inspectors reviewed the associated post-maintenance testing (PMT) procedures and either witnessed the testing and/or reviewed test records to assess whether: 1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel; 2) testing was adequate for the maintenance performed; 3) test acceptance criteria were clear and adequately demonstrated operational readiness consistent with design and licensing basis documents; 4) test instrumentation had current calibrations, range, and accuracy consistent with the application; 5) tests were performed as written with applicable prerequisites satisfied; 6) jumpers installed or leads lifted were properly controlled; 7) test equipment was removed following testing; and, 8) equipment was returned to the status required to perform its safety function. The inspectors verified that these activities were performed in accordance with general test procedure (GTP)-214, "Post Maintenance Testing Guideline," Rev. 5, Change B.

  • WO 1306266-001, remove and replace 'C' SW pump motor bearing cooling spool pieces
  • WO 1313581-001, adjust seal for the inboard bearing on the 'A' CCW pump and verify no external leakage
  • WO 1313389-001, retest of 'A' accumulator test line isolation valve following striker and regulator work

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed and/or reviewed four surveillance test procedures (STPs) listed below to verify that TS or risk significant surveillance requirements were followed and that test acceptance criteria were properly specified to ensure that the equipment could perform its intended safety function. The inspectors verified that proper test conditions were established as specified in the procedures, that no equipment preconditioning activities occurred, and that acceptance criteria were met.

In-Service Tests

  • STP- 205.004, "RHR Pump and Valve Operability Test," Rev. 7A
  • STP- 205.003, "Charging/Safety Injection Pump and Valve Test," Rev. 7, for 'C' SI pump and associated valves Reactor Coolant System
  • STP-345.074, "Solid State Protection System Actuation Logic and Master Relay Test, Train B," Rev. 13A

b. Findings

No findings were identified.

Cornerstone:

Emergency Preparedness 1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The NSIR headquarters staff performed an in-office review of the latest revisions of various Emergency Plan Implementing Pr ocedures (EPIPs) and the Emergency Plan located under ADAMS accession numbers ML13010A516, ML12307A085, ML13207A411, and ML13259A278, as listed in the Attachment.

The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, these revisions are subject to future inspection. Documents reviewed are listed in the Attachment. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

a. Inspection Scope

On November 20, 2013, the inspectors reviewed and observed the performance of an emergency preparedness training drill that involved a hostile attack on the station. The inspectors assessed the emergency procedure usage, emergency plan classifications, notifications, and protective action recommendation development. The inspectors evaluated the adequacy of the licensee's conduct of the drill and critique performance.

The inspectors verified that the drill critique identified drill performance weaknesses and entered these items into the licensee's CAP. Additional information is also documented in NRC Inspection Report 05000395/2013503.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Mitigating Systems Cornerstone

a. Inspection Scope

The inspectors verified the accuracy of the licensee's PI submittals listed below for the period July 2012 through June 2013. The inspectors used the performance indicator definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Rev. 7, "Regulatory Assessment Performance Indicator Guideline," and licensee procedure SAP-1360, Rev. 1, "NRC and INPO/WANO Performance Indicators," to check the reporting of each data element. The inspectors sampled licensee event reports (LERs),

operator logs, plant status reports, CRs, and performance indicator data sheets to verify that the licensee had properly reported the PI data. Also, the inspectors discussed the PI data with the licensee personnel associated with the performance indicator data collection and evaluation.

  • Mitigating System Performance Index (MSPI) - Heat Removal System
  • MSPI - Cooling Water Systems
  • Safety System Functional Failures

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As required by IP 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished by either attending daily screening meetings that briefly discussed major CRs, or accessing the licensee's computerized corrective action database and reviewing each CR that was initiated.

b. Findings

No findings were identified.

.2 Semi-Annual Review to Identify Trends

a. Inspection Scope

The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The review was focused on repetitive equipment issues, but also considered trends in human performance errors, the results of daily inspector corrective action item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The review was expanded to include the past two years.

Documents reviewed included licensee monthly and quarterly corrective action trend reports, engineering system health reports, maintenance rule documents, department self-assessment activities, and quality assurance audit reports.

b. Findings

In general, the licensee has identified trends and has addressed the trends within their CAP. However, inspectors noted that continued problems have existed with a replacement safety-related chiller on the 'A' train installed in August, 2011. Engineering change request (modification) ECR-50585 was originally initiated to replace both the 'A' and 'B' train chillers and the 'C' chiller capable for alignment to either train. The modification was performed for 'A' train, but delayed, for the other two chillers.

Specifically from August 5, 2011, through November, 2013, the inspectors identified the following CRs involving 'A' chiller trips or failure to start:

  • CR-11-04585, Low refrigerant suction pressure trip
  • CR-12-02364, Chiller trip on circuit 1 high discharge pressure
  • CR-12-05003, Chiller trip on circuit 1 high discharge pressure
  • CR-12-05414, Chiller would not start during alternate AC testing
  • CR-13-00166, Chiller tripped on circuit 2 low oil level
  • CR-13-02694, Circuit 1 pump down cycle time limit exceeded results in trip
  • CR-13-03124, Trip due to circuit 2 low suction pressure
  • CR-13-03952, Trip due to circuit 2 low oil level The inspectors noted that the 'A' chiller has been on the licensee's top plant issues list multiple times as defined in station scheduling procedure, SSP-007, "T-Week Planning Process," Revision 6, and the subject of LER 05000395/2013-003-00, "Trip Setpoint Renders Chiller and Control Room Emergency Filtration Inoperable." The residents issued a previous Green, NCV 05000395/2012002-06, "Failure to Promptly Correct Conditions Adverse to Quality for Lightning Induced Trips of Safety-Related Chillers." And more recently, the above LER was closed to a Green, NCV 05000395/2013008-01, "Failure to Design the Safety-related Chiller Modification to Appropriate Quality Standards," in a recent NRC triennial modification inspection documented in report 05000395/2013008. The inspectors noted the 'A' chiller remains inoperable due to the problem leading to the subject LER and has remained as such pending completion of licensee corrective actions. The inspectors continue to follow the licensee's actions to return this component to an operable status.

.3 Annual Sample Review of CR-13-02250

a. Inspection Scope

The inspectors reviewed CR-13-02250, NRC identified a nonconforming condition involving submerged cables in pull box, PB-SG-01, dated May 23, 2013, in detail to evaluate the effectiveness of the licensee's corrective actions for important safety issues. The inspectors assessed whether the issue was properly identified, documented accurately and completely, properly classified and prioritized, adequately considered extent of condition, generic implications, common cause, and previous occurrences, adequately identified root causes/apparent causes, and identified appropriate and timely corrective actions. Also, the inspectors verified the issues were processed in accordance with procedure, SAP-999, "Corrective Action Program," Rev. 11.

b. Findings

No findings were identified. The inspectors reviewed condition reports as far back as CR-01-00888, dated 2001, which found 8.5" of water in PB-SG-01 and noted that the low voltage instrument cables in the pull box have had a history of being periodically submerged. For each condition report, the inspectors noted the licensee would manually pump the water out of the pull box, but the licensee did not promptly identify and correct the source of the water leak. The inspectors reviewed recent CAP documents and identified the following:

  • CR-12-01923 - 2.75 inches of water was found in PB-SG-01
  • CR-12-03537 - 2 inches of water was found in PB-SG-01
  • CR-12-05355 - 2 inches of water was found in PB-SG-01
  • CR-13-02004 - NRC identified no CR was initiated as required by the inspection procedure when

.5 inches of water was found in PB-SG-01

The inspectors determined that the affected cables were not qualified for submergence and that two of the nineteen cables are safety-related. The inspectors also determined that the two safety-related cables are post accident monitoring (PAM) system instrumentation cables for emergency feedwater (EFW) wide-range flow to the 'B' and 'C' steam generators. The inspectors noted that CR-13-02250 states in part: "failure of the electric cable would result in unreliable wide range flow indication for EFW system supply to "B" or "C" steam generator, and might potentially result in automatic isolation of the associated flow control valve on indicated high flow."

The inspectors reviewed SAP-999 and conclud ed that cable submergence is a non-conforming condition as well as a condition adverse to quality. The licensee initiated CR-13-02250 to evaluate and concluded that the two safety-related cables are operable, but degraded or non-conforming. The licensee has written WO 1310529 to perform cable testing during the next refueling outage.

The inspectors noted that 10 CFR Part 50, Appendix B, Criterion XVI states in part that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. The inspectors concluded that the licensee's failure to identify and correct the source of the water impacting the safety-related cables was contrary to the Criterion XVI requirement and therefore a performance deficiency (PD). However, the inspectors also determined that the PD was of minor significance because the cables remained functional based on visual inspection showing no indication of degradation, and the cable's instrumentation signals showing no sign of noise.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.

b. Findings

No findings were identified.

.2 (Closed) URI 05000395/2012005-05, Adequacy of Temporary Containment Penetration Design for Shutdown Operations

a. Inspection Scope

The inspectors opened the above URI in NRC integrated inspection report 05000395/2012005 to allow further review of the identified issue of concern to determine any related performance deficiencies and if the significance was more than minor. The inspectors have completed their review of the aforementioned URI which is hereby closed as discussed below.

b. Findings

Introduction:

An NRC-identified Green non-cited violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," was identified for the licensee's failure to prescribe an adequate procedure for control of temporary containment penetration devices. The violation is in the licensee's corrective action program as condition report 13-00739.

Description:

On October 18, 2012, during the first 8 days of the refueling outage the inspectors noted that the licensee was using Dow Corning 3-6548 silicone foam as a sealant for a temporary containment penetration fixture installed in penetration, XRP-602, allowing cable pass-through during the refueling outage to support various work activities within containment. The inspectors also identified that the licensee was taking credit for this penetration even though the foam had not cured for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> as required by the vendor's installation instructions. The inspectors reviewed licensee operations administrative procedure, OAP-108.4, "Oper ations Outage Control of Containment Penetrations," Revision 1, of which portions stated the following in part:

  • Step 4.1: Acceptable Alternate - An approved penetration closure device that may be used in place of installed containment integrity equipment in Modes 5 or 6. A temporary sealant such as silicone sealant would be acceptable for use in a spare penetration.
  • Step 4.2: Containment Closure - A containment condition in which all penetrations providing Direct Access from the containment atmosphere to the outside atmosphere are closed by at least one automatic isolation valve, blind flange, or manual valve.
  • Step 4.3: Containment Penetrations - Those structures which penetrate the Reactor Building containment for the purpose of allowing piping or tubing to pass through the containment wall while still providing a leak tight barrier.
  • Step 4.5: Direct Access - A pathway from the containment atmosphere to the outside atmosphere that presents no obstacle to air movement. Obstacles which prevent this movement may include water loop seals, temporary closure devices or system pressure as with the service air, breathing air, fire protection or other plant system. The inspectors had knowledge of previous problems involving the use of foam for pressure retention and questioned the licensee on the adequacy of their 'acceptable alternate' design. The licensee subsequently performed testing under CR-13-00739 and documented the results in engineering information request, EIR-81980A. Various prototypes were fabricated and testing done at various stages of foam cure times. The inspectors reviewed the results indicating that the foam started leaking with a pressure as low as 2 psig. However, the foam was generally not expelled from the test rig until an average of 5.5 to 8 psig based on multiple tests performed. The testing also showed that failure pressures generally increased as the cure time increased.

The inspectors were also aware of a unit uprate of 2775 MWth to 2900 MWth and reviewed the respective 50.59 evaluation performed for the respective modification, MRF-90102, and identified that the licensee had failed to account for the increased decay heat in a design calculation, DC00020-006, which determined the increase in

containment pressure following a loss of RHR. The licensee initiated CR-13-00490 for an evaluation which resulted in an action to revise the calculation. The inspectors noted that while this action has not yet been completed, the licensee performed an approximation for an evaluation to include with the test results documented in EIR-81980A. This resulted in the conclusion that utilizing one RBCU and one high head charging pump, containment pressure would increase to approximately 2.6 psig. The inspectors observed that this pressure would result in leakage through the foam seals, but not a complete ejection of the foam from the conduits.

The inspectors concluded that leakage past the foam seals did not meet the licensee's definition of an obstacle that would prevent air movement through a penetration; consequently, OAP-108.4 was inadequate because it allowed the use of silicone sealant.

The inspectors also concluded the licensee's failure to consider the unit uprate impact on core decay heat and resulting impact on containment pressure was of minor significance.

Analysis:

The inspectors determined that the failure to have an adequate procedure for control of temporary containment penetration devices in accordance with 10 CFR 50, Appendix B, Criterion V, was a performance deficiency (PD). The PD is more than minor and therefore a finding because it impacted the barrier integrity cornerstone objective to provide reasonable assurance that physical design barriers such as the containment, protect the public from radionuclide releases caused by accidents or events and the attribute of procedure quality because the affected procedure allowed the use of silicone foam in configurations which did not provide adequate pressure retention capabilities. The inspectors evaluated the finding in accordance with NRC Inspection Manual Chapter 0609, "Significant Determination Process," attachment 4, appendix G, and appendix H and determined that an analysis was required by a senior reactor analyst. A regional SRA performed an SDP assessment of this finding. The licensee containment penetration testing and results were reviewed as well as the licensee's risk evaluation. The conclusion was that the finding represented a condition B finding which would only impact large early release fraction (LERF) and not core damage frequency.

The test results showed that the finding would not meet the leakage criteria necessary for the finding to be >GREEN per NRC IMC 0609 Appendix H. The conditions necessary to achieve the leakage criteria were determined to be <1E-7 for LERF which represented a GREEN finding of very low safety significance. There are no cross-cutting aspects because the finding was not representative of current licensee performance.

Enforcement:

10 CFR 50, Appendix B, Criterion V requires, in part, that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances. Contrary to the above, on August 27, 2012, procedure OAP-108.4 did not adequately prescribe the requirements for a temporary containment closure device that resulted in the use of a sealing device which was demonstrated to leak at containment pressures expected following a loss of RHR. This violation is in the licensee's corrective action program as CR-13-00739, and is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy: NCV 05000395/2013005-02, Inadequate Procedure for Control of Containment Penetrations.

.3 (Closed) NRC Temporary Instruction 2515/190, "Inspection of Proposed Interim Actions Associated with Near-Term Task Force (NTTF) Recommendation 2.1 Flooding Hazard

Evaluations"

a. Inspection Scope

The Inspectors verified that the licensee's submitted interim actions, associated with the NTTF recommendation 2.1 for flooding hazard evaluations, will perform their intended function for flooding mitigation.

The inspectors conducted an independent verification to confirm the following:

  • The procedures or activities can be executed as specified/written, and within available time, if time-dependent.
  • Water levels and associated effects, and severe weather conditions would not impair support functions and would not impede performing necessary interim actions
  • Equipment availability or staffing issues would not prevent implementation of the interim actions.
  • Proposed interim actions do not result in adverse consequences.

Documents reviewed are listed in the Attachment.

b. Findings

The inspectors completed TI-190 but continue to evaluate flooding issues of concern which will be closed to URI 05000395/2013003-01, "Modification Leads to Auxiliary Building Flood Vulnerability," in a future report.

4OA6 Meetings, Including Exit

On February 5, 2014, the resident inspectors presented the integrated inspection report results to Mr. T. Gatlin and other members of the licensee staff. The licensee acknowledged the results of these inspections. The inspectors confirmed that inspection activities discussed in this report did not contain proprietary material.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Archie, Senior Vice President, Nuclear Operations
A. Barbee, Director, Nuclear Training
M. Browne, Manager, Quality Systems
M. Coleman, Manager, Health Physics and Safety Services
G. Douglass, Manager, Nuclear Protection Services
T. Gatlin, Vice President, Nuclear Operations
M. Harmon, Manager, Chemistry Services
R. Haselden, General Manager, Organizational / Development Effectiveness
R. Justice, Manager, Nuclear Operations
G. Lippard, General Manager, Nuclear Plant Operations
M. Mosley, Manager, Nuclear Training
D. Perez, Supervisor, Health Physics - Technical Support
S. Reese, Specialist, Nuclear Licensing
J. Rinehart, Supervisor, Health Physics - Field Operations
M. Roberts, Supervisor, Health Physics II, New Plant, Environmental, Rad Waste
D. Shue, Manager, Maintenance Services
W. Stuart, General Manager, Engineering Services
B. Thompson, Manager, Nuclear Licensing
J. Wasieczko, Manager, Organization Development and Performance
D. Weir, Manager, Plant Support Engineering
B. Wetmore, Design Engineering
R. Williamson, Manager, Emergency Planning
S. Zarandi, General Manager, Nuclear Support Services

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000395/2013005-02 NCV Inadequate Procedure for Control of Containment Penetrations (Section 4OA5.2)

Opened

05000395/2013005-01 URI Seal Water Injection Filter Impact on Alternate Seal Injection System and Design Basis Accidents (Section 1R18)

Attachment

Closed

05000395/FIN-2012005-05 URI Adequacy of Temporary Containment Penetration Design for Shutdown Operations (Section 4OA5.2)
TI 2515/190 TI Inspection of the Licensee's Proposed Intermin Actions as a Result of the Near-Term Task Force Recommendation 2.1 Flooding Reevaluation (Section 4OA5.3)

Discussed

05000395/2013003-01 URI Modification Leads to Auxiliary Building Flood Vulnerability (Section 4OA5.3)

LIST OF DOCUMENTS REVIEWED

Section 1R04: Equipment Alignment

Partial Walkdowns:
SOP-115, Residual Heat Removal, Rev. 21E
Drawing E-302-641, Residual Heat Removal, Rev. 20

Section 1R05: Fire Protection

Fire Protection Plan FPP00003,
CB 400&412 Elevation, dated 7/24/02
Fire Protection Plan FPP00004,
CB 425 Elevation, dated 2/17/04 Fire Protection Plan FPP00006,
CB 463 Elevation, dated 10/15/01

Section 1R06: Flood Protection Measures

Design Calculation
DC 03390-002, Evaluation for Control Building Pipe Rupture/Flooding
Effects, Rev. 0A

Section 1R07: Heat Sink Performance

Procedures

CP-400, Administrative Guidelines Procedure for the Oil Lab, Rev. 21
ES-505, Service Water System Corrosion Monitoring and Control Program, Rev. 2
ES-560.211, Service Water System Heat Exchanger Performance, Rev. 11
QSP-516, Ultrasonic Thickness Determination, Rev. 8
STP-223.002A, Service Water Pump Test, Rev. 9

Calculations

DC05600-085, Review of Water Hammer Forces on SI, RHR, and SP Pump Discharge Piping Due to Gas Voids, Rev. 1
DC05600-086, Review of Water Hammer Forces on SI, RHR, and SP Pump Suction Piping Due

to Gas Voids, Rev. 1

Corrective Action Documents
CR-12-00844
CR-12-02011
CR-13-04098
Attachment

Other Documents

Annunciator Response Procedure
ARP-001-XCP-601, Rev. 5 Annunciator Response Procedure
ARP-001-XCP-602, Rev. 5
Annunciator Response Procedure
ARP-001-XCP-603, Rev. 5
Annunciator Response Procedure
ARP-001-XCP-604, Rev. 7
Annunciator Response Procedure
ARP-001-XCP-605, Rev. 6
Annunciator Response Procedure
ARP-001-XCP-614, Rev. 6
AOP-102.2, Abnormal Operating Procedure Loss of Charging, Rev. 0
AOP-117.1, Abnormal Operating Procedure Loss of Service Water, Rev. 3
AOP-118.1, Abnormal Operating Procedure Total Loss of Component Cooling Water, Rev. 2
Charging/SI Pump B Lube Oil Reservoir Sample Test Results: 11/20/2012, 02/18/2013,
05/08/2013 and 08/08/2013 Charging/SI Pump B Oil Cooler Outlet Temperature Data Trend: 08/01/2013 - 09/26/2013
CMP-300.003, Preparation of Components for Flow Accelerated Corrosion and Service Water System Monitoring, Rev. 9
Component Cooling Water Important to Maintenance Rule System Function Worksheet, 12/03/10
ICP-240.024, Charging/SI Pump B Oil Cooler Outlet Temperature Instrument Data Sheet,
03/07/85
PSEG-07, Trending, Rev. 4
PSEG-35, Heat Exchanger Inspection, Rev. 0
Service Water Pond Level Trend: 2010 - 2013
Virgil C. Summer Nuclear Station Updated Final Safety Analysis Report, Chapter 9

Section 1R15: Operability Evaluations

WO 1308170, 'B' RVLIS wide range 1322 channel is failing

Section 1R18: Plant Modifications

WO 1300346-09, Install temporary cable from
CB-448 (XPN7144 area) to
CB-463 (CR area) per attached troubleshooting plan.

Section 1EP4: Emergency Action Level and Emergency Plan Changes

Change Packages Radiation Emergency Plan, Revision 62 Evacuation Time Estimate Study Update
EPP-005, "Offsite Dose Calculation," Revision 20 Emergency Plan, Revision 63

Section 4OA5: Other Activities

TI 2515/190 Documents Reviewed
OAP-109.1, Guidelines For Severe Weather, Rev. 3F
CR-12-02916, Heavy rains results in water intrusion in buildings
CR-12-06169, Excessive water leakage via conduits into
AB 412 elevation
CR-13-02782, Water intrusion from heavy rains Enclosure
CR-13-02022, During ISFSI excavation a condition was created allowing water into AB via
EMH-8
CR-13-03087, Excessive water leakage via conduits into
AB 412 elevation
CR-13-03949, NRC concerns with post Fukushima flood inspection documentation
CR-13-04258, Water intrusion via conduits into
AB 412 elevation
CR-13-05384, Excessive water leakage via conduits into
AB 412 elevation
US Army Corps of Engineers, Sandbagging Techniques
TR02060-003, Response to NRC Request for Information Pursuant to 10
CRF 50.54(f) Regarding the Flooding Aspects of Recommendation 2.1 of the Near-Term Task Force Review of Insights From the Fukushima Accident, Flood Hazard Reevaluation Report for VCSNS, Rev 0

LIST OF ACRONYMS

AB Auxiliary Building
AAC Alternate
AC [[]]

AC Alternating Current

ADAMS Agency Document

Access and Management System

ALARA As Low As Reasonably Achievable
ASI Alternate Seal Injection
CAP Corrective Action Program
CAQ Condition Adverse to Quality
CB Control Building
CFR Code of Federal Regulations
CR Condition Report
CRB Control Room Pressure Boundaries
CVCS Chemical and Volume Control System
DAW Dry Active Waste
DPW Declared Pregnant Worker
ECCS Emergency Core Cooling System
ECR Engineering Change Request
ED Electronic Dosimeter
EDG Emergency Diesel Generator
EFW Emergency Feedwater
ES Engineering Services Procedure
ETBT Equal To/Better Than
FSAR Final Safety Analysis Report
GTP General Test Procedure
HP Health Physics
HPT Health Physics Technician
HRA High Radiation Area
IB Intermediate Building
IMC Inspection Manual Chapter
INPO Institute of Nuclear Power Operations
IP Inspection Procedure
IR Inspection Report
ISFSI Independent Spent Fuel Storage Installation kV Kilovolt
LER Licensee Event Report
LHRA Locked High Radiation Area
LOCA Loss of Coolant Accident
MDEFW Motor Driven Emergency Feedwater
MR Maintenance Rule
MSPI Mitigating System Performance Index
NCV Non-Cited Violation
NEI Nuclear Energy Institute
NPF Nuclear Power Facility
NPR Negative Pressure Respirator
NPU Negative Pressure Unit
NRC Nuclear Regulatory Commission

NSTS National Source Tracking System

Attachment

NVLAP National Voluntary Laboratory Accreditation Program
NUREG Nuclear Regulatory
OOS Out of Service
PARS Publicly Available Record
PD Performance Deficiency
PI Performance Indicator
PMT Post-Maintenance Testing Radwaste Radioactive Waste
RB Reactor Building
RBCU Reactor Building Cooling Unit
RCA Radiologically Controlled Area
RCS Reactor Coolant System
RCP Reactor Coolant Pump
REV. Revision
RHR Residual Heat Removal
RS Radiation Safety
RTP Rated Thermal Power
RWP Radiation Work Permit
RWST Refueling Water Storage Tank
SAP Station Administrative Procedure
SBO Station Blackout
SCBA Self-contained Breathing Apparatus
SCE&G South Carolina Electric and Gas
SDP Significance Determination Process
SFP Spent Fuel Pool
SI Safety Injection
SOP System Operating Procedure
SPB Steam Propagation Barriers
SRI Senior Resident Inspector
SSC System, Structures, and Components
SSP Station Scheduling Procedure
SSPS Solid State Protection System
STP Surveillance Test Procedure
SW Service Water
SWIF Seal Water Injection Filter
TDEFW Turbine Driven Emergency Feedwater
TEDE Total Effective Dose Equivalent
TLD Thermo Luminescent Dosimeter
TS Technical Specification
TWR Technical Work Record

TYRA Three-year Rolling Average

U1 Unit 1

URI Unresolved Item
VHRA Very High Radiation Area
WANO World Association of Nuclear Operators
WBC Whole-body Count WO Work Order