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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E9561999-05-28028 May 1999 Forwards Update to NRC AL 98-03,re Estimated Info for Licensing Activities Through Sept 30,2000 ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20207E7801999-05-21021 May 1999 Forwards Application for Amend to License NPF-3,allowing Use of Expanded Spent Fuel Storage Capacity.Proprietary & non- Proprietary Version of Rev 2 to HI-981933 Re Cask Pit Rack Installation Project,Encl.Proprietary Info Withheld ML20206N0231999-05-0606 May 1999 Forwards License Renewal Applications for Davis-Besse Nuclear Power Station,Unit 1 for ML Klein,Cn Steenbergen & CS Strumsky.Without Encls ML20206D2421999-04-28028 April 1999 Forwards Combined Annual Radiological Environ Operating Rept & Radiological Effluent Release Rept for 1998. Rev 11, Change 1 to ODCM & 1998 Radiological Environ Monitoring Program Sample Analysis Results Also Encl PY-CEI-NRR-2382, Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl1999-04-21021 April 1999 Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl ML20206B8831999-04-17017 April 1999 Forwards 1634 Repts Re Results of Monitoring Provided to Individuals at Davis-Besse Nuclear Power Station During 1998,per 10CFR20.2206.Without Repts ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl ML20205K3871999-04-0707 April 1999 Forwards Copy of Application of Ceic,Oec,Ppc & Teco to FERC, Proposing to Transfer Jurisdictional Transmission Facilities of Firstenergy Operating Companies to American Transmission Sys,Inc.With One Oversize Drawing ML20205J1171999-03-29029 March 1999 Forwards Rev 1 to BAW-2325, Response to RAI Re RPV Integrity, Per GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rev Includes Corrected Values in Calculations PY-CEI-NRR-2377, Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1)1999-03-29029 March 1999 Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1) ML20205F5961999-03-27027 March 1999 Forwards Comments on Preliminary Accident Sequence Percursor (ASP) Analysis of 980624 Operational Event at Dbnps,Unit 1, as Transmitted by NRC Ltr ML20205D4791999-03-26026 March 1999 Forwards Rept Submitting Results of SG Tube ISI Conducted in Apr 1998.Rept Includes Description of Number & Extent of Tubes Inspected,Location & Percent wall-thickness Penetration for Each Indication of Imperfection ML20205L2031999-03-26026 March 1999 Submits Correction to Dose History of Tj Chambers.Dose Records During 1980-1997 Were Incorrectly Recorded Using Wrong Social Security Number.Nrc Form 5 Not Encl ML20205C7371999-03-25025 March 1999 Certifies That Dbnps,Unit 1,plant-referenced Simulator Continues to Meet Requirements of 10CFR55.45(b) for Simulator Facility Consisting Solely of plant-referenced Simulator.Acceptance Test Program & Test Schedule,Encl ML20205E3551999-03-19019 March 1999 Requests That Proposed Changes to TS 6.8.4.d.2 & TS 6.8.4.d.7 Be Withdrawn from LAR Previously Submitted to NRC ML20204J6361999-03-17017 March 1999 Forwards Firstenergy Corp Annual Rept for 1998 & 1999 Internal Cash Flow Projection as Evidence of Util Guarantee of Retrospective Premiums Which May Be Served Against Facilities PY-CEI-NRR-2375, Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage1999-03-15015 March 1999 Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage ML20204E6821999-03-12012 March 1999 Requests That Listed Changes Be Made to NRC Document Svc List for Davis-Besse Nuclear Power Station,Unit 1 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20065D0491990-09-14014 September 1990 Forwards Operator & Senior Operator Licensing Exam Ref Matl for Exam Scheduled for Wk of 901112,per 900607 Request ML20065D4951990-09-14014 September 1990 Forwards Updated Exam Schedule for Facility,In Response to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule ML20059K4681990-09-14014 September 1990 Provides Supplemental Info Re Emergency Response Data Sys (Erds).Data Transmitted by Util ERDS Will Have Quality Tag of 4 & Point Identification for ERDS Renamed ML20059G2341990-09-10010 September 1990 Provides Response to Request for Addl Info Re Interpretation of Tech Spec 3/4.7.10, Fire Barriers. Interpretation Is Implemented & Unnecessary Compensatory Measures Removed.List of Fire Barriers Inspected on One Side Only Encl ML20059G4961990-09-0606 September 1990 Submits Voluntary Rept of Svc Water HX Testing During Sixth Refueling Outage.Expected Flow Rates Not Achieved.Periodic Tests Developed to Check Efficiency of Containment Air Coolers ML20064A6271990-09-0606 September 1990 Requests That Requirement Date for Installation & Testing of Alternate Ac Power Source & Compliance w/10CFR50.63 Be Deferred Until Completion of Eighth Refueling Outage ML20028G8611990-08-28028 August 1990 Forwards Davis Besse Nuclear Power Station Semiannual Rept: Effluent & Waste Disposal,Jan-June 1990. ML20059D4121990-08-28028 August 1990 Forwards Second 10-Yr Interval Pump & Valve Inservice Testing Program ML20059D5521990-08-24024 August 1990 Forwards Semiannual Fitness for Duty Rept for Jan-June 1990 ML20059B5291990-08-23023 August 1990 Forwards Updated Fracture Mechanics Analysis of Hpi/Makeup Nozzle,Per 900510 Meeting W/Nrc.Util Believes That Addl Analysis to Assess Structural Integrity of Nozzle Using More Conservative Fracture Model Supports Previous Analysis ML20058Q3911990-08-16016 August 1990 Requests NRC Concurrence on Encl Interpretation & Technical Justification of Tech Spec 3/4.7.10, Fire Barriers ML20058P7801990-08-10010 August 1990 Advises of Intentions to Revise Testing Requirements for Fire Protection Portable Detection Sys at Plant & Functional Testing of auto-dialer & Telephone Line Subsys from Daily to Weekly Testing ML20063P9981990-08-0909 August 1990 Submits Supplemental Response to Insp Rept 50-346/89-21. Util Rescinds Denial & Accepts Alleged Violation ML20056A5341990-08-0303 August 1990 Confirms Electronic Transfer of Payment of Invoice I0942 Covering Annual Fee for FY90,per 10CFR171 ML20058M7791990-08-0303 August 1990 Forwards Rev 10 to Industrial Security Plan & Rev 6 to Security Training & Qualification Plan.Revs Withheld ML20058L1821990-08-0101 August 1990 Forwards Davis-Besse Dcrdr Human Engineering Discrepancy Repts 1988 Summary Addendum 1,Vol 1, Per NRC Audit Team Request ML20056A8341990-07-23023 July 1990 Forwards Revised Monthly Operating Rept for June 1990 for Davis-Besse Nuclear Power Station Unit 1 ML20055H4601990-07-20020 July 1990 Discusses Resolution of Draft SER Open Item on Voluntary Loss of Offsite Power.Util Preparing License Amend Request Per Generic Ltrs 86-10 & 88-12 to Relocate Fire Protection Tech Specs & Update Fire Protection License Condition ML20055F9681990-07-17017 July 1990 Forwards Application for Amend to License NPF-3,adding Centerior Svc Company as Licensee in Facility Ol.Change Allows for Improved Mgt Oversight,Control & Uniformity of Nuclear Operations ML20055F8561990-07-17017 July 1990 Discusses Util Planned Activities Re Instrumented Insp Technique Testing Performed at Facility in View of to Hafa Intl.Relief Requests Being Prepared by Util for Sys on Conventional Hydrostatic Testing ML20044B3001990-07-12012 July 1990 Provides Written Confirmation of Util Electronic Transfer of Funds to NRC on 900711 in Payment of Invoice Number I1050 ML20044B1841990-07-10010 July 1990 Requests Approval of Temporary non-code Repair & Augmented Insp of Svc Water Piping,Per 900626 Telcon ML20055D9701990-06-29029 June 1990 Provides Written Confirmation of Util Electronic Transfer of Funds for Payment of Invoice 0111 Covering Insp Fees for 890326-0617 ML20043H5291990-06-14014 June 1990 Forwards Plans Re Reorganization & Combining of Engineering Assurance & Svc Program Sections ML20055C7521990-06-14014 June 1990 Responds to NRC Bulletin 89-002, Potential Stress Corrosion Cracking of Internal Preloaded Bolting in Swing Check Valves & Justification for Alternate Insp Schedule for One Valve. No Anchor Darling Swing Check Valves Installed at Plant ML20055F2261990-06-14014 June 1990 Forwards 1990 Evaluated Emergency Exercise Objectives for Exercise Scheduled for 900919 ML20043G5661990-06-14014 June 1990 Forwards Rev 9 to Industrial Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043G7811990-06-12012 June 1990 Forwards Info Re Implementation of NUREG-0737,Item II.F.2, Inadequate Core Cooling Instrumentation, Per NRC 900214 Safety Evaluation.Item II.B.1 Issue Re Reactor Vessel Head Vent Also Considered to Be Closed ML20043F6091990-06-11011 June 1990 Forwards Util Comments on NRC Insp Rept 50-346/90-12, Per 900601 Enforcement Conference Re Core Support Assembly Movement & Refueling Canal Draindown.Refueling Canal Draindown Procedure Provides Specific Draining Instructions ML20043E1301990-06-0101 June 1990 Withdraws 870831 & 890613 Applications to Amend License NPF-3.Changes Requested Addressed by Issuance of Amend 147 or Can Now Be Made as Change to Updated SAR Under 10CFR50.59 ML20043D5601990-05-31031 May 1990 Forwards Application for Amend to License NPF-3,revising Tech Spec 3/4.6.4.1, Combustible Gas Control - Hydrogen Analyzers. Request Consistent W/Nrc Guidance,Generic Ltr 83-37,dtd 831101,NUREG-0737 Tech Specs & Item II.F.1.6 ML20043D5691990-05-31031 May 1990 Forwards Application for Amend to License NPF-3,requesting Extension of Expiration Date of Section 2.H to Allow Plant Operation to Continue Approx 6 Yrs Beyond Current Expiration Date ML20043D1451990-05-31031 May 1990 Forwards Rev 11 to Updated SAR for Unit 1.Rev Updates Table 6.2-23 Re Containment Vessel Isolation Valve Arrangements ML20043D1621990-05-29029 May 1990 Documents Util Understanding of NRC Interpretation of Plant Tech Spec 3.7.9.1,Action b.2 Re Fire Suppression Water Sys, Per 891206 Telcon.Nrc Considered Electric Fire Pump Operable Provided Operator Stationed to Open Closed Discharge Valve ML20043C2331990-05-25025 May 1990 Forwards Summary of 900510 Meeting W/B&W & NRC in Rockville, MD Re Hpi/Makeup Nozzle & Thermal Sleeve Program.List of Attendees & Meeting Handout Encl ML20043B1701990-05-18018 May 1990 Forwards Revised Exemption Request from 10CFR50,Section III.G.2,App R for Fire Areas a & B,Adding Description of Specific Limited Combustibles That Exist Between Redundant Safe Shutdown Components in Fire Area a ML20043A5441990-05-16016 May 1990 Discusses Status of Safety & Performance Improvement Program Portion of B&W Owners Group EOP Review Project ML20043A2311990-05-11011 May 1990 Responds to Violation Noted in Insp Rept 50-346/90-08. Corrective Actions:Results of Analysis of Radiological Environ Samples & Radiation Measurements Included in 1989 Annual Radiological Environ Operating Rept ML20043A4901990-05-10010 May 1990 Forwards Summary of Differences Between Rev 5 to Compliance Assessment Rept & Rev 1 to Fire Area Optimization,Fire Hazards Safe Shutdown Evaluation, Vols 1-3.Rept Demonstrates Compliance W/Kaowool Wrap Removal ML20042F9801990-05-0404 May 1990 Provides Written Confirmation of Util Electronic Transfer of Payment of Invoice Number 10716 to Cover Third Quarterly Installment of Annual Fee for FY90 ML20042F5781990-05-0303 May 1990 Provides Status of Hpi/Makeup Nozzle & Thermal Sleeve Program.Nrc Approval Requested for Operation of Cycle 7 & Beyond Based on Program Results.Visual Insp of Thermal Sleeve Identified No Thermal Fatique Indications ML20042F0951990-04-30030 April 1990 Responds to Violations Noted in Insp Rept 50-346/90-02. Corrective Actions:Maint Technician Involved in Tagging Violation Counseled on Importance of Procedure Adherence W/ Regard to Personnel Safety ML20042F0841990-04-27027 April 1990 Responds to Violations Noted in Insp Rept 50-346/89-201 for Interfacing Sys LOCA Audit on 891030-1130.Corrective Actions:Plant Startup Procedure Will Be Revised Prior to Restart from Sixth Refueling Outage ML20042E7311990-04-27027 April 1990 Forwards Application for Amend to License NPF-3,deleting 800305 Order Requiring Implementation of Specific Training Requirements Which Have Since Been Superseded by INPO Accredited Training Program ML20042F1961990-04-27027 April 1990 Informs of Adoption of Reorganization Plan Re Plants on 900424.Reorganization Will Make No Changes in Technical or Financial Qualifications for Plants.Application for Amends to Licenses Adding Company as Licensee Will Be Submitted ML20043F7261990-04-20020 April 1990 Requests Exemption from 10CFR55.59(a)(2) to Permit one-time Extension of 6 Months for Reactor Operators & Senior Reactor Operators to Take NRC 1990 Requalification Exam. Operators Will Continue to Attend Training Courses ML20042E7091990-04-17017 April 1990 Forwards Annual Environ Operating Rept 1989 & Table 1 Providing Listing of Specific Requirements,Per Tech Spec 6.9.1.10 ML20012F5091990-04-0303 April 1990 Forwards Completed NRC Regulatory Impact Survey Questionnaire Sheets,Per Generic Ltr 90-01 ML20012F6001990-04-0202 April 1990 Submits Supplemental Response to Station Blackout Issues,Per NUMARC 900104 Request.Util Revises Schedule for Compliance W/Station Blackout Rule (10CFR50.63) to within 2 Yrs of SER Issuance Date ML20012E0181990-03-22022 March 1990 Forwards Application for Amend to License NPF-3,changing License Condition 2.C(4) Re Fire Protection Mods to Fire Extinguishers,Fire Doors,Fire Barriers,Fire Proofing,Fire Detection/Suppression & Emergency Lighting 1990-09-06
[Table view] |
Text
. G TOLEDO
% EDISON Docket No. 50-346 JOE VVILUAMs, JR.
sor va ww (419l 249-2300 License No. NPF-3 14'S1 48 5223 Serial No. 1-600 December 26, 1985 Mr. C. J. Paperiello, Director Division of Reactor Safety United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137
Dear Mr. Paperiello:
Toledo Edison acknowledges receipt of your November 22, 1985 letter (log No. 1-1280), Notice of Violation, and Inspection Report No. 50-346/85028 (DRS). Following an examination of the item of concern, Toledo Edison herein offers information regarding this item:
Violation: 10 CFR 50, Appendix B, Criterion V states, in part,
" Activities af fecting quality shall be prescribed by
'.ocumented instructions, procedures...of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures,..."
Contrary to the above, the licensee's procedures were inadequate for fabricating, installing, and inspecting the plant pressure retaining safety related flexible boot seals.
This is a Severity Level IV violation (Supplement I).
(50-346/85028-04)
Response: (1) Corrective action taken and results achieved.
An NRC concern was identified as a result of an investigation regarding the acceptance criteria for the overlap axial seam utilized in the fabrication and installation of BISCO flexible boots. Toledo Edison (TED) has contacted BISCO to provide the minimum al:.owable overlap axial seam required, and to provide dor.umentation which supports this criteria. BISCO has r512310206 851226 Provided this documentation and concludes that a EDR ADOCK 05000346 mit imum ove'. lap axial seam width of one inch is o PDR acceptabla regardless of pipe diameter. BISCO Test DEC 271985 THE TOLEDO EDISON COMPANY EDISON PLAZA 300 MADISON A'/ENUE TOLEDO, OHIO 43652
' 0 W/
J .. 7. w .
i Dockat No. 50-346
! ~ License No. NPF-3 4
Serial No. 1-600 l December 26, 1985 j Page 2 1
! Report 748-109 supports this conclusion and is avail-able for your review. This report, which was conduct-
! ed in part to determine the weakest pressure retaining section of the boot assembly, demonstrates that the I clamp assembly will fail before the one inch overlap axial seam will fail. In any event, both the axial seal and the clamp retained pressure greater than that required for its intended purpose. The test assembly was fabricated and installed using materials and procedures very similar to those utilized at Davis-Besse and provide TED with a high degree of confidence that l the one irch overlap axial seam criteria is acceptable.
In further discussions, BISCO noted that specifying two and three inch overlaps existed for ease of .
i j installation only. A one' inch overlap, as indicated in the previous discussions, is more than sufficient
! from a pressure retention perspective. However, with J larger diameter boot seals, it is difficult to work j with only a one inch overlap, and specifying two and
, three inch overlaps will help in preventing unneces-sary rework.
Based on the previous information, TED Engineering developed an Inspection Plan (IP-M-003) for Quality Control (QC) to establish the as-installed condition of the BISCO flexible boot overlap axial seams. For
- currently installed flexible boot seals, the governing acceptance criteria for the overlap axial seam will be that one inch is required as a minimum. The inspec-
! tion was completed on December 21, 1985. The results will be evaluated and all non-conforming conditions
! related to overlap axial seams will be corrected prior
- to February 21, 1986.
(2) Corrective action to be taken to avoid further violation. ,
On December 10, 1985 TED approved Procedure MP 1700.29.0, '
i Fabrication and Installation of Flexible Pressure and i j Fire Seals, for use at Davis-Besse. This procedure '
- identifies specific overlap axial seam requirements
, based upon the diameter of the pipe to be sealed.
- This procedure also requires documentation of cure times which will allow for appropriate QC review.
Procedure AD 1844.00.14, Maintenance, specifies that "All Nuclear Safety-Related,'ASME, ANSI B31.1, Fire 2
Protection System MWO's,. . .shall be routed. by MPG for i review by the QC Supervisor, Code Inspection Supervi-sor, or their designees to determine the inspection i
i i :
_ . . ___- _ . - . _ _ . - , . ~ . _ _ _ _ _ , . _ . . . _ _ , _ _ _ _ . _ _ _ , _ . _ _ . , _
Dsckst No. 50-346 License No. NPF-3 Serial No. 1-600 December 26, 1985 ,
Page 3 requirements." The QC/ Code reviewer will then enter any special instructions on the MWO which are required during the performance of the MWO. Instructions will typically inform maintenance when to contact the designated inspector for in process inspections or final inspection.
Procedure MP 1700.29 will be revised by January 24, 1986 to include QC hold witness points for the inspection of BISCO flexible boot seals during fabrication and installation.
(3) Date when full compliance will be achieved.
Full compliance will be achieved upon the completion of the current inspection and any flexible boot repairs necessary prior to February 21, 1986.
Very truly yours, Jn w 2 ).' ,3 v g JW:TJB:SGW:amb cc: DB-1 NRC Resident Inspector i
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1 g(M KC2 41985 i
l Jaeorgia Power Company
/ ATTN: Mr. R. J. Kelly Executive Vice President P. O. Box 4545 Atlanta, GA 30302 Gentlemen:
SUBJECT:
REPORT NOS. 50-424/85-53 AND 50-425/85-38 On November 18-22, 1985, NRC inspected activities authorized by NRC Construction Permit Nos. CPPR-108 and CPPR-109 for your Vogtle facility. At the conclusion of the inspection, the findings were discussed with those members of your staff identified in the enclosed inspection report.
Areas examined during the inspection are identified in the ' report. Within these areas, the inspection consisted of selective examinations of procedures and representative records, interviews with personnel, and observation of activities in progress.
Within the scope of the inspection, no violations or deviations were identified.
Should you have any questions concerning this letter, please contact us.
Sincerely,
// , d Virgil L. Brownlee, Chief Reactor Projects Branch 2 l Division of Reactor Projects
Enclosure:
l Inspection Report Nos. 50-424/85-53 l
and 50-425/85-28 l
l cc w/ encl:
I d . E. Conway, Senior Vice President Nuclear Power v6. O. Foster, Vice President and General Manager Vogtle Project 4.H. Gregory,III, General vd. Manager,VogtleNuclearConstruction Bockhold, Jr. , Vogtle d.PlantManager T. Gucwa, Chief Nuclear Engineer cc: (Continued See page 2)
", i Georgia Power Company 2 DEC2 41985 9e w/ encl: (Continued)
- Ruble A. Thomas, Vice President-Licensing Vogtle Project
/EdGroover, Quality f Assurance Site Manager WC. W. Hayes, QA Manager JJ. T. Beckham, Vice President
& General Manager - Operations JJ.A. Bailey,ProjectLicensing r
Manager WGeorge F. Trowbridge, Esq.
g Shaw, Pittman, Potts and Trowbridge 4 Bruce W. Churchill, Esq.
Shaw,-Pittman, Potts and Trowbridge 1 Ernest L. Blake, Jr. , Esq.
Shaw, Pittman, Potts and Trowbridge
,[ James E. Joiner, Troutman, Sanders, Lockerman and Ashmore lJamesG.Ledbetter, Commissioner Department of Human Resources
/CharlesH. Badger,Officeof Planning and Budget, Management t Review Division 40eppish Kirkland, III, Counsel Office of the Consumer's Utility Council JouglasC.Teper,GeorgiansAgainst D
Nuclear Energy
/ Laurie Fowler, Esq., Legal Environmental Assistance Foundation kimJohnson,ExecutiveDirector Campaign for a Prosperous Georgia IMortonB.Margulies,Esq., Chairman !
Administrative Judge, Atomic Safety i and Licensing Board Panel J Dr. Oscar H. Paris, Administrative Judge Atomic Safety and Licensing Board Panel JGustave A. Linenberger, Jr. , Administrative
.~ Judge, Atomic Safety and Licensing Board i Panel 4 Billie Pirner Garde, Citizens Clinic Director, Government Accountability Project bec w/ enc 1: (See page 3) l 'W B
Georgia Power Company 3 4
c w/ encl:
. Reis, ELD
. Sinkule, RII RC Resident Inspector Document Control Desk State of Georgia RII ; 7 RII
,g J arris:lb TConidn ARHerdt 12rg/85 12/ /85 12/J)/85
. _. _ _ - _ _ . _ _ _ . _ _ = _m . _____m. -_m , _ - ___
A Ric UNITED STATES
[ o NUCLEAR REGULATORY COMMISSION l [ n REGION 11 g j 101 MARIETTA STREET, N.W.
'
- I e ATLANTA, GEORGI A 30323
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! Report Nos.: 50-424/85-53 and 50-425/85-38
! Licensee: Georgia Power Company i P. O. Box 4545 i Atlanta, GA 30302 Docket Nos.: 50-424 and 50-425 License Nos.: CPPR-108 and CPPR-109 i
j Facility Name: Vogtle 1 and 2
. Inspection Conducted: November 18-22, 1985
) Inspector: k[ -
/2/.9 Y& T Date Signed i J. F. Harris Approved by Y / m c f?f1 W T. E. Conlon, Section Chief
/7 lM /L7.S" Date S'igned
'i Engineering Branch j Division of Reactor Safety
SUMMARY
j Scope: This routine, unannounced inspection entailed 37 inspector-hours on site j in the areas of structural concrete, post tensioning activities, and employee
- concerns in civil construction.
I
- Results: No violations or deviations were identified.
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REPORT DETAILS
- 1. Persons Contacted Licensee Employees
- R. E. Conway, Senior Vice President
- D. O. Foster, General Manager Vogtle Project
- M. H. Googe, Project Construction Manager
- E. D. Groover, QA Site Manager
- R. C. Harbin, Manager, Quality Control
- P. Ciccanes, Regulatory Compliance Specialist
- G. A. McCarley, Project Compliance Coordinator Other licensee employees contacted included construction craftsmen, engineers, and technicians.
NRC Resident Inspector
- 2. Exit Interview The inspection scope and findings were summarized on November 22, 1985, with those persons indicated in paragraph 1 above. The inspector described the areas inspected and discussed in detail the inspection findings. No dissenting comments were received from the licensee.
The licensee did not identify as proprietary any of the materials provided to or reviewed by the inspector during this inspection.
- 3. Licensee Action on Previous Enforcement Matters This subject was not addressed in the inspection.
- 4. Unresolved Items Unresolved items were not identified during the inspection.
- 5. Independent Inspection Effort Construction Progress The inspector conducted a general inspection of the soils and concrete testing laboratory, concrete structures, ongoing concrete curing operations and backfill operations to observe construction progress and construction activities.
2 Within the areas examined, no violations or deviations were identified.
- 6. Containment, Structural Concrete (47054) - Unit 2
't The inspector observed preparation for the final concrete placement of the Unit 2 containment dome. The placement was scheduled for hovember 22, 1985, but had to be rescheduled for November 26, 1985, due to a1 verse weather resultiag from Hurricane Kate. Acceptance criteria examined by the inspect.or appeared in the following documents:
Specification X2AP01, Placing, Finishing and Curing Concrete frocedure CD-T-02, Concrete Quality Control FSAR Sections 3, 12, and 17.
Observations showed that the area was being properly cleaned, that re-inforcing steel was properly installed, and that equipment was being in-stalled to allow proper placement of the concrete. Examination of the
, concrete testing laboratory and batch plant showed that the calibration of the batch plant and testing equipment were current and that they were in good working order. Discussions with QC inspectors and craft personw I concerning preparation for the dome placement indicated that they were aware
- of the specification and procedure requirements for the preparation and placement of the concrete pour for the dome.
Within the areas examined, no violations or deviations were identified.
- 7. Containment (Post-Tensioning) Observation of Work (47063) Unit 1 The inspector observed the stressing of horizontal tendon numbers 127, 129,
- and 139. Acceptance criteria examined by the inspector appear in the following documents
Specification X2AF04 - Rev. 3, Containment Post Tensioning System VSL Field Instruction Manual for Installation of Post-Tensioning 1 System, Rev. 10 Drawing PT-11.2-1, Horizontal Tendons, Unit 1 Drawing P1372.23, Horizontal Tendon Stressing Data Observations included checking calibration of the stressing rams, witnessing measurement of elongation of the tendon strands, seating measurements, lift off pressure, and cutting of wire strands following completion of stressing activities. Observations and review of stressing data showed that the stressing operations were being conducted in accordance with require-ments and that the operations were being monitored by quality control l
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3 inspectors. Discussions with craft and quality control personnel and responsible engineers indicated they understood the requirements for the stressing operations.
Within the areas examined, no violations or deviations were identified.
- 8. Containment (Post-Tensions) Review of Quality Records (47065) - Unit 1 The inspector examined quality records relating to post-tensioning activi-ties for horizontal tendons in the Unit 1 containment. Acceptance criteria examined by the inspector appear in the documents listed in paragraph 7.
Records examined were for horizontal tendon numbers 2, 3, 4, 9, 13, 14, 15, 19 and 20. Records examined included; tendon installation reports, quality control checklists, stressing reports, and tendon greasing reports.
Review of these records showed that the tendons were installed in accordance with specification requirements and that problems encountered during stressing operations were being identified and properly addressed.
Within the areas examined, no violations or deviations were identified.
- 9. Employee Concerns, Discussions, and Findings The fi lowing employee concerns were reviewed:
- a. Backfilling Against North Wall of Control Building (1) Concern The north wall of the control building (an exterior wall at level D) was backfilled before it cured. As a result, there was a lot of honeycombing on the wall.
(2) Discussion The inspector examined drawings of the control building, walked down the exterior and interior of the control building, discussed placement of concrete and backfill activities in the control building with quality control inspectors and engineers and examined records relating to backfill and concrete placement for the control building.
Review of drawings showed that the-exterior wall on the north side of the control building begins et level B at elevation 180 and not at the D level as stated in the concern. Discussions with QC inspectors and engineers and examination of records disclosed the backfill was placed against the north wall of the control building before the specified time. This was identified by a quality control inspector in Deviation Report CD-1762 dated February 17, 1982. This deviation report stated that backfill was placed
4 against the north wall of the control building to elevation 196 which was contrary to requirements that no backfill be placed above elevation 186 before placement of the level A concrete slob which ties into the north wall at elevation 200. This problem was submitted for engineering review and as a result the backfill was r :.7oved. Analysis by design engineers showed that no structural danage was done to the north control building wall. A walkdown of the control building by the inspector showed no evidence of any adverse cracking or structural damage.
Placement of the backfill against the wall would not cause honeycomb in the concrete because by the time the forms were removed, the concrete would have hardened to the point where the backfill could not have had any affect on the concrete surface.
Research of the literature and experience has shown that honeycomb is caused by inadequate vibration near the outer face of the walls where the reinforcing steel interferes with the flow of the plastic concrete.
(3) Findings Investigations showed that backfill was placed against the north wall of the control building before the specified time. This was identified and investigated by the licensee. The backfill was removed and the structure was evaluated to determine if the backfill had caused any structural damage. The analysis showed no structural damage due to the placement of the backfill. A walkdown of the structure by the inspector iisclosed no evidence of structural damage. Backfill against the walls would not cause honeycomb or defects in the concrete because the concrete would have been in a hardened state by the time the forms were removed.
No problems with the quality of the concrete were substantiated.
- b. Falsification of Soil Density Tests (1) Concern Soil dcnsity test results had been falsified. Proctor tests were run on the soil compaction which was done at the site. Proctor tests are tests to determine soil density and moisture and these test were done on the compacted soil for the power block.
Individuals involved in this matter manipulated the test results to indicate that they were acceptable. Results are too good to be true in that results are too perfect.
(2) Discussion The inspector examined Bechtel Specification X2AP01, " Earthwork and Related Site Activities", and Georgia Power Company procedure CD-T-01, " Earthwork Quality Control", and reviewed proctor and
l 5
field density test data on compaction of soil material in the power block from 1978 through 1980. The inspector also inter-viewed seven quality control inspectors that were involved in inspection of compaction of backfill in the power block.
Review of specification X2AP01 and procedure CD-T-01 showed that 4
the required field compaction of the backfill is specified in terms of percent of maximum dry density as determined from the laboratory modified proctor test (ASTM D-1557). In performance of the laboratory proctor test (ASTM D-1557), soil samples are compacted at varying moisture contents in a steel mold of known volume using a specified compacting effort. The purpose of the test is to determine the maximum soil density and the corre-sponding optimum moisture content at which this maximum density can be obtained. The test results are presented as a plot of the dry density versus moisture content. Connection of the plotted points results in a curve shaped line. A line to the curve peak from the vertical axis containing density values in pounds per i cubic foot represents the maximum dry density for that material and a vertical line from the peak of the curve to the horizontal
- axis containing water content values in percent of dry weight represents the optimum moisture content at which the maximum dry density is obtained. Specification X2AP01 requires that soil in the power block to be compacted to an average of 97 percent of the maximum dry density determined by the laboratory proctor test.
The specification also requires that the moisture content of the soil at the time of compaction be within minus three percent or plus two percent of the optimum moisture content determined by the laboratory proctor test.
Procedure CD-T-01 details the method for quality control testing
, of Category I backfill to assure the backfill is compacted to the density and moisture limits determined by the laboratory proctor test. The testing is performed by quality control (QC) soil inspectors using field density (sand cone) tests (ASTM D-1556).
The results of the field density tests and the soil samples collected in performance of the field density tests are sent to the soils laboratory by the QC field inspectors. In the soils lab, laboratory technicians test the soil samples and calculate the results of the field density tests. The field density test results are determined by comparing the density of the in-place soil (determined by sand cone method) with the laboratory proctor results and computing the percent compaction (field density divided by proctor density) of the in-place backfill material.
Review of the field density test data from 1978 through 1980 showed that, for the most part, the power block backfill was compacted to a density of 97 to 107 percent of the maximum density determined by the laboratory proctor. Some of the field density tests showed that backfill was compacted to 93 to 96 percent of the maximum proctor density. These low test results were identified and addressed by the licensee. Review of the data
..-_-y--. ,
6 indicated that the results were reasonable and normal for the compacted effort being used t) compact the backfill (compacted with a ten ton vibratory roller).
Interviews with the seven quality control inspectors disclosed no evidence of manipulation or falsification of soil test data. Two inspectors indicated that they heard one individual would some-times . aund a decimal up (e.g., 96.5 to 97.0) to make a test appear better, but that they had never witnessed or actually seen the individual do this. Review of test data by this inspector showed no evidence where decimals had been rounded up. All seven inspectors stated that they had no knowledge of any falsification of test data and indicated that they were satisfied with the quality of the compaction of the backfill.
In addition to the investigation of' compaction of soil material in the power block during this inspection to satisfy the stated concern, this NRC inspector and two other NRC inspectors from the Region II office have examined controls on backfill activities during routine inspections conducted from 1978 through 1985.
During these inspections, controlling specifications and proce-dures were reviewed, work activities were observed and records were examined to verify that backfill activities were being conducted in accordance with NRC requirements. During these visits, the inspectors also discussed quality control of backfill activities with civil quality control inspectors to verify that quality control inspectors understood the specification require-ments and that these requirements were being implemented. During these inspections, several minor violations regarding control of moisture content were identified. The licensee was responsive in addressing and correcting these items. During one of these inspections conducted on November 16-18, 1979, this NRC inspector was informed by the Georgia Power Company QA supervisor that a severe storm on November 2, 1979, had aggravated ongoing moisture problems and eroded part of the backfill. Because the applicant failed to report the deficient condition to the backfill as required by 10 CFR 50.55(e), a Notice of Violation was issued.
Subsequently a Confirmation of Action letter dated November 15, 1979, from NRC Region II to Georgia Power was issued in which it was understood that Georgia Power would not continue with backfill placement in or around the power block area or concrete placement on affected structures without concurrence of NRC. Meetings were held with the applicant at the site and at the Office of Nuclear Reactor Regulation (NRR) in Bethesda, Maryland regarding measures to be taken to correct the backfill. Corrective measures included testing to determine the extent of defective backfill, removal of defective backfill and foundation slabs, installation of drainage facilities and a dewatering system and application of gunite (sand cement mixture) on slopes to prevent additional erosion problems.
7 The NRC inspectors observed the corrective measures taken to correct the backfill and examined records documenting the corrective measures during several onsite inspections. Results of these inspections showed that the backfill was properly repaired and that measures were taken to prevent future erosion problems.
Reviews of backfill activities were also performed by Geotechnical Engineers from the NRC office of Nuclear Reactor Regulation (NRR).
These reviews resulted in some concerns being raised by an NRR Geotechnical Engineer regarding the density of the compacted backfill in the power block. To satisfy these concer s, samples representative of the Category I backfill were taken by the licensee and tested by both an independent testing laboratory and
, the licensee's testing laboratory. The sampling and testing of these samples were witnessed and reviewed by NRC inspectors.
Comparison of the test results from the two laboratories indicated that the methodology being used by the licensee to control the compaction of the backfill was reasonable and correct. In 4
addition to the laboratory tests, the licensee hired a drilling company to perform in-place standard penetration tests on the existing backfill to verify that the density of the backfill meets
, design requirements. These standard penetration tests were made by driving a two-foot eight-inch long cylindrical tube (called a sampling spoon) having a two-inch outside diameter and a one-and-three-eight inch inside diameter into the existing backfill. In this method, the sampling spoon, which is attached to drill rods, is driven into the soil by blows of a 140-pound hammer falling from a height of 30 inches and impacting on a driving collar attached to the drill rods. Each blow count is accomplished by raising the cylindrical shaped hammer, which has a center hole that allows it to be raised along the shaft attached to the drill collar, with a rope to a height of 30 inches and then allowing the hammer to free fall and strike the drive collar. After the sampling spoon has penetrated six inches into the soil, the penetration test is started and the number of blows required to produce the next one foot of penetration is recorded. Anything over 50 blows per foot is considered very dense. Review of the penetration data showed the following range of blow counts for the backfill: 0-10 feet, 32- 131 blows with a conservative average of 50 blows; 10 to 30 feet,62-200 blows with a conservative average of 100 blows; 30 to 80 feet, 100 to 200 blows with a conservative average value of 150 blows. Results of the confirmatory testing by the independent laboratory and the standard penetration tests
- indicated that the recorded density values accurately reflect the l in-place density and compaction of the backfill.
Review of NRC inspection reports also showed that a similar concern was identified in 1981. This concern indicated that results from backfill proctor analyses were altered to indicated that failing tests complied with specification requirements.- This
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1 concern was investigated by an NRC Region II inspector and an NRC investigator during the period of May 18 to August 7, 1981.
Results of this investigation, documented in NRC report number 50-424/81-09 and 50-425/81-09 dated October 22, 1981, indicated there was no evidence that test data was being e ttered to indicate failing tests meet requirements.
(3) Findings Review of records and discussions with civil quality control inspectors failed to show any evidence that backfill records were falsified. Additional independent confirmatory testing of the ba:kfill by independent organizations confirmed that the me".hodology being used and that the in-place density of the backfill met specification requirements. The concern was not substantiated.
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