|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld ML20195G4591999-06-10010 June 1999 Forwards MORs for May 1999 & Revised Repts for Apr 1999 for LGS Units 1 & 2 ML20195H0531999-06-0909 June 1999 Forwards Revised Bases Pages B3/4 10-2 & B3/4 2-4 for LGS Units 1 & 2,in Order to Clarify That Requirements for Reactor Enclosure Secondary Containment Apply to Extended Area Encompassing Both Reactor Enclosure & Refueling Area ML20195E7701999-06-0707 June 1999 Provides Notification of Change to NPDES Permit PA0052221, for Bradshaw Reservoir Facility Which Supports Operation of Lgs,Units 1 & 2,per EPP Section 3.2 ML20195C7631999-06-0101 June 1999 Notifies NRC That PECO Energy Has Completed Installation of New Large Capacity,Passive Strainers on RHR & Core Spray Sys Pump Suction Lines at Lgs,Unit 2,in Response to Ieb 96-003 ML20195D5381999-05-26026 May 1999 Forwards 1998 Occupational Exposure Tabulation Rept for LGS Units 1 & 2. Encl Is Diskette & Instructions.Rept Is Being re-submitted to Reset 12 Month Time Period.Without Disk ML20195B2821999-05-24024 May 1999 Requests That NRC Distribution Lists for LGS Be Updated. Marked-up Distribution List Showing Changes Is Attached ML20196L2891999-05-20020 May 1999 Provides Status Update of Thermo-Lag 330-1 Fire Barrier Corrective Actions,Iaw Commitments Made in ML20195B2951999-05-20020 May 1999 Forwards Rev 0 to LGS Unit 2 Reload 5,Cycle 6 COLR, IAW TS Section 6.9.1.12.Values Listed Have Been Determined Using NRC-approved Methodology & Are Established Such That All Applicable Limits of Plants Safety Analysis Are Met 05000352/LER-1999-003, Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv1999-05-19019 May 1999 Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv 05000353/LER-1999-002, Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 9904191999-05-18018 May 1999 Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 990419 ML20206E2001999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept (Non- Radiological) for Limerick Generating Station,Units 1 & 2. Rept Submitted IAW Section 5.4.1 of App B of Fols,Epp (Non- Radiological) & Describes Implementation of EPP for 1998 ML20206D8801999-04-27027 April 1999 Forwards Rev 2 to LGS Unit 1 Reload 7,Cycle 8 COLR, IAW TS Section 6.9.1.12.COLR Provides cycle-specific Parameter Limits for Noted Info ML20206A5461999-04-21021 April 1999 Responds to Conference Call Between Util & NRC on 990420,re TS Change Request 98-07-2,revising TS Section 2.0 to Incorporate Revised MCPR Safety Limits.Attached Ltr Contains Info Requested ML20205T0441999-04-17017 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept 15, IAW TS Section 6.9.1.7.REMP for 1998,confirmed That LGS Environ Effects from Radioactive Release Were Well Below LGS TSs & Other Applicable Regulatory Limits ML20205Q7581999-04-15015 April 1999 Forwards Response to RAI Re ISI Program First & Second 10-Yr Interval Relief Requests.Revs to Identified by Vertical Bar in Right Margin 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059K3671990-09-14014 September 1990 Informs of Revised Commitments Re Crud Induced Localized Corrosion Related to Fuel Cladding Failures.Deep Bed Demineralizers Installation Activities Will Be Performed in Unit 1 Subsequent to Third Refueling Outage ML20065D4421990-09-14014 September 1990 Responds to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule. Proposed Schedules for Operator Licensing Exams, Requalification Exams & Generic Fundamental Exams Encl ML20064A5831990-09-0707 September 1990 Responds to Violations Noted in Insp Repts 50-352/90-17 & 50-353/90-16 Re Differential Pressure for Pumps.Corrective Actions:Licensee Will No Longer Use Expanded Ranges as Acceptance Criteria for Inservice Testing Program Tests ML20064A4821990-08-31031 August 1990 Forwards Rev 20 to Emergency Plan.Changes Necessitated by Annual Emergency Plan Update & Administrative in Nature ML20059E6071990-08-29029 August 1990 Forwards Semiannual Effluent Release Rept,Jan-June 1990 & Rev 8 to Odcm ML20059B0751990-08-24024 August 1990 Forwards Rev 0 to Updated FSAR for Limerick Generating Station,Units 1 & 2,Vols 1-19.W/one Oversize Encl. Proprietary Vol 7A (App 3B) Withheld (Ref 10CFR2.790) ML20064A6471990-08-24024 August 1990 Forwards Public Version of Revised Epips,Consisting of Rev 10 to EP-101,Rev 2 to EP-112,Rev 13 to EP-208,Rev 11 to EP-230 & Rev 22 to EP-291 ML20059E9861990-08-24024 August 1990 Provides Justification for Applicability of Reload Methodology Topical Repts to Facility & Requests NRC Approval for Application of Reload Analysis Methodologies ML20058N9591990-08-13013 August 1990 Forwards Revised Response to Violations Noted in Insp Repts 50-352/90-13 & 50-353/90-13.Corrective Actions:Ltr Issued to All Plant Personnel Providing Instructions on Proper Use & Handling of Controlled Documents in Controlled Locations ML20058N1771990-08-10010 August 1990 Responds to NRC Re Unresolved Items Noted in Insp Repts 50-352/90-80 & 50-353/90-80.Plant-specific Technical Guideline Has Been Revised to Ref Contingency Numbers Rather than Transient Response Implementation Plan Procedures ML20063P9461990-08-10010 August 1990 Provides Plans for Ultimate Disposition of Recirculation Inlet Nozzle to Safe End Weld Indication.Alternative Corrective Actions to Disposition Nozzle to Safe End Weld Indication Include Repair by Weld Overlay W/O Monitoring ML20058N1281990-08-0909 August 1990 Forwards Correction to Rev 10 to EPIP EP-234, Obtaining Containment Gas Samples from Containment Leak Detector During Emergencies ML20058N1991990-08-0909 August 1990 Advises of Change of Address for Correspondence Re Util Operations.All Incoming Correspondence Must Be Directed to One of Listed Addresses ML20058P1261990-08-0909 August 1990 Forwards Monthly Operating Repts for Jul 1990 for Limerick Units 1 & 2 & Rev 1 to June 1990 Rept ML20058M9951990-08-0808 August 1990 Responds to NRC Re Violations Noted in Insp Repts 50-352/90-15 & 50-353/90-14.Corrective Actions:Personnel Counseled on Importance of Procedure Compliance & Operations Manual Revised ML18095A3761990-07-26026 July 1990 Forwards Decommissioning Repts & Certification of Financial Assurance for Plants ML20055J0241990-07-26026 July 1990 Forwards Response to NRC Regulatory Effectiveness Review Rept for Plant.Response Withheld Per 10CFR73.21 ML20056A9731990-07-25025 July 1990 Forwards Facility Written Exam Comments for NRC Insp Repts 50-352/90-10 & 50-353/90-11.Written Exam for Reactor Operator & Senior Reactor Operator Considered Comprehensive & Thorough ML20055H8511990-07-24024 July 1990 Responds to NRC 900720 Request for Addl Info Re Util 900516 Request for Exemption from Full Participation During 1990 Onsite/Offsite Emergency Exercise.Nrc Region I & FEMA Support Feb 1991 Exercise,Per 900718 Telcon ML20055H8331990-07-20020 July 1990 Submits Change of Addresses for Correspondence Re Util Nuclear Operations ML20055H0231990-07-12012 July 1990 Forwards Public Version of Revised Epips,Including Rev 10 to EP-210,Rev 19 to EP-231 & Rev 13 to EP-237 ML20044A1041990-06-22022 June 1990 Forwards Application for Amends to Licenses NPF-39 & NPF-85, Consisting of Tech Spec Change Requests 90-03-0 & 90-04-0, Revising Surveillance Requirement 4.9.6.1 for Section 3.9.6 Refueling Platform Re Main Hoists/Auxiliary Hoists ML20043J0371990-06-20020 June 1990 Forwards Description,Scope,Objectives for Plant 1990 Annual Emergency Exercise Scheduled for 900920,per 890809 Ltr.Util Will Submit Revised Objectives for Exercise to Reflect Limited Participation,If Exemption Request Approved ML20043H6081990-06-19019 June 1990 Corrects 900427 Response to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing - 10CFR55 & Conforming Amends. ML20055C7621990-06-18018 June 1990 Informs NRC of Plans Re Licensing of Senior Reactor Operators (Sros) Limited to Fuel Handling at Plants.Util in Process of Implementing New Program for Establishment & Maint of Licensed SROs Limited to Fuel Handling at Plants ML20055C7471990-06-15015 June 1990 Requests That Listed Operator Licenses Be Discontinued ML20043G1331990-06-14014 June 1990 Responds to NRC 900614 Ltr Re Violations Noted in Insp Repts 50-352/90-13 & 50-353/90-12.Corrective Actions:Boxes of Completed Procedures Improperly Stored Shipped to Util Storage Vault by 900406 ML20043G9981990-06-12012 June 1990 Forwards, Core Operating Limits Rept for Unit 1 Reload 2, Cycle 3 & Core Operating Limits Rept for Unit 2,Cycle 1. Repts Submitted in Support of Tech Spec Change Request 89-13 Re Parameter Limits,Per Generic Ltr 88-16 ML20043G7311990-06-0808 June 1990 Provides Addl Response to Generic Ltr 88-01, NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping. Welds Examined During Last Refueling Outage Addressed ML20043G7501990-06-0808 June 1990 Requests Withdrawal of 900516 Tech Spec Change Request 90-11-1 Re Extension of Snubber Visual Insp Period.Change No Longer Needed Since Unit Shutdown on 900605 & Visual Insp of Three Affected Snubbers Performed on 900607 ML20043F8021990-06-0808 June 1990 Forwards Monthly Operating Repts for May 1990 for Limerick Units 1 & 2 & Revised Pages to Mar 1990 Rept for Unit 2 & Apr 1990 Rept for Units 1 & 2 ML20043D8101990-05-29029 May 1990 Forwards Application for Amends to Licenses NPF-39 & NPF-85, Consisting of Tech Specs Change Request 89-07 to Relocate Radiological Effluent Tech Specs to ODCM or Process Control Program,Per Generic Ltr 89-01 ML20043E6571990-05-25025 May 1990 Forwards Public Version of Rev 135 to Epips,Including Rev 11 to EP-202,Rev 14 to EP-282,Rev 12 to EP-284,Rev 8 to EP-312 & Rev 9 to EP-410.W/DH Grimsley 900607 Release Memo ML20055C5121990-05-18018 May 1990 Provides Info Inadvertently Omitted in Re Property Insurance Coverage for Plants.Limerick Generating Station Unit 2 Should Have Been Ref as Being Included Under Insurance Coverage ML20043A7881990-05-16016 May 1990 Requests Exemption from Requirement to Perform Biennial full-participation Onsite/Offsite Emergency Exercise for Plant During 1990 ML20055C4851990-05-15015 May 1990 Forwards Annual Financial Repts for 1989 for Philadelphia Electric Co,Pse&G,Atlantic Energy,Inc & Delmarva Power & Light Co ML20043B1501990-05-14014 May 1990 Forwards Public Version of Rev 134 to Epips,Consisting of Rev 10 to EP-230,Rev 4 to EP-255,Rev 1 to EP-302,Rev 7 to EP-304 & Rev 3 to EP-314.Release Memo Encl ML20043A2361990-05-14014 May 1990 Responds to NRC 900413 Ltr Re Violations Noted in Insp Repts 50-352/90-07 & 50-353/90-06.Corrective Actions:Sampling Review of Plant Baseline Data Will Be Performed to Ensure Product Code Number Correctness for Components ML20042F4481990-05-0101 May 1990 Advises That Plant Transient Response Implementing Plan Procedures & Related Ref Matls Provided to Dj Florek,Nrc Region I,On 900430.Documents Provided in Response to NRC 900327 Ltr Re Preparation for Planned NRC Insp of Procedure ML20042E8741990-04-27027 April 1990 Responds to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing. Certifies That Limerick Operator Requalification Training Program Renewed on 900125 & Peach Bottom Subj Program Renewed on 890622 ML20042E0881990-04-0909 April 1990 Forwards Addl Info Re 891011 Tech Spec Change Request 89-09 to Reduce Number of Suppression chamber-to-drywell Vacuum Breakers Required to Be Operable ML20042E0201990-04-0606 April 1990 Forwards Vols 1-3 to Preservice Insp Summary Rept, & Books 1-3 to Form NIS-2 for Preservice Insp Interval 1985-1990, Per 10CFR50.55a(g) & ASME Code Section Xi,Paragraph IWA-6230 ML20012E2151990-03-20020 March 1990 Responds to Generic Ltr 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants,' for Peach Bottom.Response for Limerick Generating Station Will Be Provided by 900504 ML20012C2931990-03-12012 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey, Per 900118 Request ML20012D9511990-03-0909 March 1990 Forwards Public Version of Revised Epips,Including Rev 10 to EP-203,Rev 12 to EP-317 & Rev 18 to EP-292.W/DH Grimsley 900322 Release Memo ML20012A3631990-03-0101 March 1990 Responds to NRC 900131 Ltr Re Violations Noted in Insp Rept 50-353/89-32 on 891211-15.Corrective Action:Util Will Document Both Receipt & Shipment of Fuel Loading Chambers on Next Semiannual Doe/Nrc Form 742 ML20012A1151990-02-28028 February 1990 Forwards Semiannual Effluent Release Rept 11,Jul Through Dec 1989 & Annual Tower 1 Joint Frequency Distributions of Wind Direction & Speed by Atmosphere Stability,Rept 5 for 1989. W/O Annual Tower 1 Rept ML20012A2621990-02-16016 February 1990 Forwards Public Version of Revs 124 & 125 to Epips, Consisting of Rev 9 to EP-201,Rev 20 to EP-291 & Rev 21 to EP-291 ML20006E7731990-02-16016 February 1990 Requests Discontinuation of Listed Operator Licenses ML20006E6511990-02-15015 February 1990 Discusses & Forwards Results of Field Verification Testing of Unit Spds,Per Licensee Commitment to Submit Rept within 30 Days After Unit SPDS Declared Operational.No Significant Problems Encountered W/Spds During Power Ascension Testing 1990-09-07
[Table view] |
Text
, .
~
i PHILADELPHIA ELECTRIC COMPANY ,
o LIMERICK GENER ATING STATION P. O. DOX A j SAN ATOG A. PENNSYLVANI A 1$464
{t t $) 3271200, EXT. 3000 GN AH AM M LEITCH -
m . ........,
u............m ....n.a Docket Nos. 50-352 50-353 License Nos. NPF-39 NPF-85 i U.S. Nuclear Regulatory Commission Attn Document Control Desk Washington. DC- 20555 t
SUBJECT:
Limerick Generating Station, Units 1 and 2 Response to NRC Unresolved Items Identified in Inspection Report Nos. 50-352/90-80 and 50-353/90-80 Dear Sirs
- Attached is Philadelph?a Electric Company's reply to a request for a written response to NRC Inspection Report Nos. 50-352/90-80 and 50-353/90-80 for Limerick Generating Station (LGS), Units 1 and 2.
NRC letter dated July 3, 1990, transmitted the Inspection Report which covered the~ Transient Response Implementation Plan (TRIP) procedures.
This letter requested that we respond to the unresolved items .
. identified in the inspection report within 30 days of receipt of the ,
report. We received the report at LGS on July 13, 1990. The Attachment to this letter provides our response to the unresolved items as well as the other concerns identified throughout the ,
aspection Report. Specifically, this response identifies the short term actions;which have been taken to resolve certain of the concerna '
described in the' Inspection Report. The long term actions to resolve the remaining concerns will be determined by Dacember 31, 1990, and
.provided in a supplement to this response by January 30, 1991.
If you have any questions or require additional information, please do not hesitate to contact us.
Very tyu'y ours,
/
/
DCS:cah Attachment '
cc: T. T. Martin, Administrator, Region I, USNRC l
T. v. Kenny, USNRC Senior Resident Inspector, LGS /
01 9008130276 900810 1 L, hDR ADOCK 05000352PDC I
\.
i
Attachm3nti
, .. Paga 1 of-10 Inspection Report 50-352, 353/90-80 Limerick Generating Station, Units 1 and 2 Response to NRC Unresolved Items Identified in '
Inspection Report Nos. 50-352/90-80 and 50-353/90-80 The cover letter that transmitted NRC Inspection Report Nos.-
50-352/90-80 and 50-353/90-80 requested that we provide our short and '
long term' actions relative to the unresolved items identified in the-Executive Summary. The two unresolved items are 352 and 353/90-80"01.
and'352 and 353/90-80-02.- Below is our response to each of these unresolved items. Additionally, we have provided our response to the other concerns identified throughout the report. Each item is addressed below in the order that they appeared in-the Details section of the report.
The Short Term actions (designated ST) make certain enhancements in the Plant Specific Technical Guideline (PSTG) and Transient Response i Implementation Plan ' RIP) procedures.
s The PSTGs and affected-TRIP procedures were all revised, reviewed by the Plant Operations Review
-Committee (PORC).and approved by the Operatio<o and Technical Staffs before July- 15, 1990.- Implementation and the necessary training of
-these changes is expected to be completed by September 15, 1990. Long:
Term items (designated LT) will be reviewed and appropriate actions planned by December 31,-'1990. The results of this review and the action plan will be submitted in a supplement to this response
. expected to be issued by January 30, 1991.
Independent Technical Adequacy Review of the TRIP Procedures, Unresolved Item 90-80-01, Section 4.0 l Item 1 The in3pection team identified that when transitioning to the contilgency portion of the PSTG, the PSTG refers to specific procedure numbe;s, such as the T-100 secies, rather than the individual PSTG contingencies.
Response
I The PSTG has been revised to reference contingency numbers rather than TRIP procedure numbers (ST).
Item'2 The inspectors identified a TRIP procedure deviation from the PSTG on entering T-100 (SCRAM procedure) instead of entry into the Reactor Pressure Vessel (RPV) Cor. trol procedure, T-101. Tais constitutes l' extra steps which may not be required and has the potential to cause l operator error.
L L
b l L
- 7. '
A'#
h Attcchmant H . Paga 2 of 10 Inspection Report 50-352, 353/90-80
Response
We will; evaluate whether the operator should enter T-101 (RPVLControl) [
instead of-T-100 (SCRAM precedure) when directed to SCRAM in a TRIP
~
procedure (LT).
1 Item 3 !
A deviation between the PSTC and the TRIP procedures was identified.
-The:PSTG direction given, when emergency RPV depressurization is j required, is to enter T-101 at Step RC-1 and execute it concurrently.
The TRIP procedures only direct entry into T-ll2, Emergency Blowdown.
' Procedure T-112 has direction to SCRAM the reactor if it has not already been SCRAMed, therefore, entry into T-101 is redundant. The inspect 3an team concludeo that since T-101 gives the operator guidance !
'to contcol level and power-that T-112 does not, T-101 should be i entered when emergency blowdown is required.
Response
This concl.usion will be reviewed and appropriate actions planned (LT).
Item 4 There were several examplee of incorrect information in the PSTG that- 1 Lreflect on system capability. . The PSTG refers to the steam condensing j mode of RHR, HPCI use for boron injection, LPCI loops C and D heat' ;
exchanger capability and RPV flooding sources, none of~which exist ~in !
the plant.
Response j The PSTG,has been revised to reference only Limerick Gene-". ting
-Station (LGS) systems and not generic systems'(ST). i Item 5 '
t
.There are several actions contained in the TRIP. procedures which are 1 not directed by the PSTGs. In T-101 (RPV control), when an'SRV is cycling,-adequate core cooling is not considered when establishing suppression pool cooling. T-112 contains direction to avald emergency depressurization of the reactor vessel below 100 psig unless motor driven pumps are available. Technical Specifications actions are included in the SP/T portion of T-102.
Response
We will evaluste whether to remove suppression pool ecoling operation from T-101 or specify to use an RHR pump which is not required for adequate core cooling (LT). T-ll2 has been revised to remove this direction (ST). We will evaluate whether these actions should be 1 removed from T-102 (LT).
F [
r ::
' Attcchm2nt .
Paga:3 of 10 Inspection Report 50-352, 353/90-80.
i 1
s ;_
Item 6 ,
A: number of. transition points'were found to be'in error in several TRIP procedures.
Response
All TRIP procedure ficwcharts have been reviewed and revised where necessary-to ensure the proper step numbers at the entry / exit arrows ,
~are correct providing proper transition directions (ST). ,
-Item 7 Terminology used in certain flowcharts is ambiguous. . These terms require concise definitions-that are-clearly understood by the operators.
Response ,
Administrative Procedure A-94, " Preparation of Transient Response Implementation Plan (TRIP) Procedures," has been revised ~to define terms such as " stabilize", " shutdown",.and " consider" (ST). We are evaluating if the TRIPS should give more' guidance on how the operator
- can determine if the reactor is " shutdown" (LT).
Item 8 N The RPV Control procedure, T-101, step RC/P-14, directed an operator to hold at~this step until " power is below 4%."' The PSTG~ requires that the operator determine if-the reactor is " shutdown" at'this '*
- point.
Response ,c 5
T-101 step RC/P-14 has been revised to verify the reactor is
" shutdown" rather than " power...below 4%" (ST).
' Item 9 l
The Primary Containment Control procedure,~T-102, steps SP/L-22 and SP/T-14, permit'depressurization only if boron injection is not required. The PSTG requires depressurization regardless of whether boron injection is' required. I Response i lq The wording "UNLESS BORON IS REQUIRED" has been removed from T-102 (ST).
l l
l 1
. , ;g
+ 4 y ;
?. Attachm3nt *
' --Pcga-4 of 10 Inspection Report 50-352,-353/90-80 "
Item:10
-The?PrimaryLContainment-Control procedure, T-102, step SP/L-8'has a' ;
note'whichl states that'at'17.8 feet suppression pool' level, the.
SPOTMOS temperature indication becomes invalid,- The noteLdoes not-
. direct the operator to use~an alternate indication, in this case [
- Residual' Heat Removal (RHR). pump suction' temperature indication with an'RHR~ pump in service.
J l Response Note #2 of-T-102 has in3n revised to add use of the RHR suction- 1 temperature' indicator-with:the RHR pump runningJ(ST).
-7 tem'll
'The Emergency Blowdown procedure, T-ll2, steps EB-1, EB-2 and EB-3, require the; operator to SCRAM the reactor and enter the~ SCRAM
-procedure,-T-100'. . This action is considered by the inspection team to v beia redundant step.since all T-112 entry conditions but one, T-102 DW/T, already; direct _thefreactor to be SCRAMed prior to~ entering T-
~
3 112.
o, a-Response j, We are evaluating placing the SCRAM direction in.T-102 DW/T and :
removing itifrom the T-112 procedure (LT). q i
Itemil2 T-ll2 step EB-19 directed securing HPCI on high. suppression pool 4'
. level.- This..is considered to'be redundant due to this guidance appearing in-T-102., gj
- Response Step EB-19 of'T-112 has been. deleted-(ST).
Item 13 The north:and south stack process radiation monitor HI-HI alarm i setpoints, used~as entry conditions.into the Radioactivity Release 1 Control. procedure, T-104, are conservative with respect to the BWR ,
Owners Group Emergency Proceduro Guideline (EOP) entry condition s requirement of " release rate above the offsite release race which requires an Alert." The T-104 entry conditions are satisfactory with ,
respect'to monitored releases, but do not directly address the t unmonitored release path scenario. }
, .' i i
{
I
b .
'1 '
C .
Attcchm3nt.
Pago 5 of:10 t *
-Inspection Report 50-352, 353/90-80 Response.
T-104 has been revised:to show an entry from EP-101 (ST). EP-101 has been revised-to.give direction to enter-T-104 on appropriate- !
radiological conditions (ST). The PSTG has been revised to J tincorporate the above-changes-(ST).
l
.; c ; Control Room and Plant _Walkdowns, Sections 5.0-and 10.0 i i
-Item 1 Based 1on walkdowns performed during the Emergency Operating Procedure (EOP) Inspection, the glare from the plexiglass covering the flowcharts in the Main Control Room (MCR) is excessive. The glare makes-it difficult to use the procedures.-
Response
i Actions are being planned to reduce the glare-on the plexig1c. (LT). j l
Item 2 1 1
Non-licensed operators (NLOs) occasionally had difficulty in locating infrequently operated. valves during the walkdown of the T-200 series procedures.
1
Response
1 The T-200 sviles procedures will be evaluated to determine why i operators are having difficulties in locating valves-and appropriate !
actions will-be taken to resolve this problem (LT). :
Simulator, Section 6.0
' Item 1 One of the comments noted during the plant walkdown was that the ,
. curves in the Safety Parameter Display System (SPDS) in the plant do ;
not agree with the curves in the TRIP procedures. The SPDS was not j used by operators in the simulator because it.is not yet functional in the simulator.
l
I -
Attachm2nt '
P ga 6 of.10-Inspection Report- 50-352,-353/90-80; r Response i
.. t The SPDS. curves are being revised to agree with those in the TRIP ;
procedures (LT).
Item 2 g The current 11ocation of the SPDS monitors is not conducive for use by the shift supervisor,while using the TRIP procedures. The SPDS *
. monitors are located on the shift supervisors. desk and the reactor.
opdtators' computer desk. .The TRIP procedures.are used by the shift supervisor _on.the back of the reactor operators.comouter desk. <
Neither monitor is visible to-the shift supervirs.
Response ,
~The need for relocating the SPDS terminals in tr.J MCR so & person using the TRIPS can read the terminals is being evaluated and >
appropriate' actions will be determined (LT). 3 Human Factors Review of the EOPs, Unresolved Item 90-80-02, Section 7.0 Item 1 Two principal human factors concerns about the TRIP flowcharts were identified size and complexity. .T-101-(RPV Control) and:T-102 (Primary. Containment Control) are inconvenient to use because of'their dimensions. The size of the flowcharts is related to the wording of .
the step instructions which are frequently long and complex.
Response
Actions .are being planned to reduce the si::e, words, and steps of flowcharts (LT). Additionally, specific human factors findings itemized in Attachment C will be addressed by an encompassing human' factors review'(LT).
Walkdown Comments, Attachment B E
Item 1 Many of the T-200 series procedures contain sets of steps which
' install jumpers or lift leads. However, the purpose for performing
! each-step is not always obvious.
1 l-
, 1 l
['
Attachmsnt
. Page 7 of 10 Inspection Report 50-352, 353/90-80 i n
Response _,
o -
A review will be performed to determine whether descriptive text'for o
each' major set of jumper / lifted lead steps should be added to the T-200 series procedures (LT).
L IEem 2 r Inspectors noted that some of the area maps an signs formerly located at the 'tcps of stairwells and entrances to areas have f al2 rn down, or are missing. .This makes it more difficult for operatore to locate infrequently operated components which are required to be operated in ,
the T-200 series procedures. i
Response
.A plan will~be developed to ensure all area maps in the Reactor Enclosure are-in place or to incorporate maps into appropriate TRIP procedures _(LT).
, Item 3 Step RC/P-8 of T-101~has the operator open the Main Steam Isolation Valves (MSIVs) to provide a heat sink, using procedure T-221-if necessary. LT-101 did not " Restore Instrument Air" after a.LOCA signal per procedure SE-10, nor.did T-221 restore instrument air to the i outboard MSIVs.- Without. instrument air, the outboard MSIVs.could not- i be opened. ,
Response
We added the proper steps to T-221_ prior to the inspection team t departing the site (ST). Additionally, we will review whether T-101 also requires a revision for this concern (LT).
Item 4 The T-102 related curves in the SPDS did not match the current revision of the BWR Owners Group EOPs. SPDS does caution the operators that the curves currently in SPDS are not valid'for use with
,the TRIP procedures. i
Response
Revision to the SPDS curves is ongoing and is expected to be completed by October 31, 1990.
1 l
l l
1 l
, i
- t a.-
- +-
Attachmsnt- {
Pcga 8 of 10 1 Inspection Report 50-352, 353/90-80
-ItemLS f a* '
Curve PC/P-3 (Primary. Containment Pressure Limit) of T-102 asks for 7: Drywell. Pressure on recorder PR57-*01 to calculate containment > level.
The recorder'is labeled 4"Pri Cont Atm" versus "Drywell' Pressure". '
(@ . -i Response 4 The: TRIP flowchart was corrected to agree with the recorder (ST).
Item 6 t 4
~
In step RF-19 of T-116, "RPV Plooding," the operator is directed to check for a 69 psid' pressure 1 difference between the reactor pressure
. vessel and the suppression pool. The RPV pressure instrument has 20- ,
psig scale increments.and the SP instrument has S psig scale 1"crements.. A 69 psid would be difficult to read.
' Response The 69 psid has been changed to 70 paid (ST). ;
.t Item 7 The borax and boric acid stored in the locker near the'SLC tank would 3 t
be of--little use for filling the CRD pump suction ' strainer body, as it s would need to be transported-down three floors and from the reactor- .
enclosute building to the-turbine building. The' locker contains'no- ;!
thermometer as specified~in the procedure. '
Response
c,
~'
A thermometer was added to the cabinet prior to the inspection team leaving'the site. The T-211 procedure, _"CRD System Boric Acid-Sodium. - ,.
Pentaborate Injection," has since been cancelled as recommended by the inspection team since this. procedure is not feasible to implement and
.more desirable methods are available (ST). [
p r , i 1
Item 8 The handswitch for SV-57-201 also controls SV-57-239, but is not labeled as - such on ttie control board. il
Response
l; A revieu of the Main Contfal Room panel labels will be conducted and L appropriate corrective actions planned (LT). ,
b lu o
l
i[
~.,$ , [ i' Attcchment Page 9'of 10-Inspection Report- 50-352,' 353/90-80 1- ,
i 1
Human' Factors Examplea, Attachment C Item 1' Administrative' Procedure A-94, " TRIP Writer's Guide," provides'no-guidance for the_ writing of logic statements.
Responne Guidance will be included in A-94 for writing logic statements (LT).
l Item 2
- A-94 does not define a very effective way of using color in the flowcharts.
f -,
Response
Guidance will be included in A-94 on effective use of color-in the flowcharts (LT). 1 1
Item-3 A-94tdoes not-fully state-the conventions.for presenting; referencing H
o: instructions (i.e.c instructions to execute.another procedure (
concurrently) 'and branching instructions (i.e., instructions to leave q
-the,present, procedure or branch and go_t'o-another procedure). In: the j flowcharts, references to T-200. procedures are put-inLcommand boxes. '
References to T-100: procedures are put in special symbols unless:the 0 reference is. conditional, in which case.it appears in the recheck step-
-command symboll These practices were found"to:be used consistently, .
but they are not mentioned in A-94. References.to'non-TRIP procedures
~
are not treeted-as consistently. Sometimes they are in;the command
- box and sometimes in the reference symbol. . Examples of this
- /
inconsistency are given in the findings related to the TRIP l
-procedures.
' Response.-
, Writer's guidance will be provided to ensure that consistency is :l maintained'(LT).
Item 4
'. A-94' specifies that_ flow lines are to be darker than the flowchart symbols. The difference in line intensity is substantial. The
_ guidance is inconsistent with the recommended practice (as indicated
'in NUREG/CR-5228). -
1 l
, 3-
' '); I 2 AttaN 'ont. )
t . Paga 10 10 i
. Inspection Report 50-352, 353/9m 30 1
Response
A-94 and the TRIP procedures will be reviewed with the current direction provided in NUREG/CR-5228 and'a resolution will be p ' determined for the difference identified-(LT). j L
Item 5-l
'A-94 does not provide guidance on the method of verification, i.e., it i does not say what will be done to verify a procedure or procedure revision. A-94 also.provides no guidance on how problems identified during thl's verification will be resolved.
Response
Additional guidance will be included in A-94 on methods of verification and validation (LT).
l Items 6 and 7 A-94 does not provide guidelines for determining when verification is ,
required >and when validation 11s required. These decisions are left to i the discretion'of the procedure writer who makes recommendations to the Plant Operations' Review Commit *;e (PORC). Additionally,-A-94 does notLmake'it completely clear that .erification and validation apply to ;
satellite procedures:(T-200 serit , as well as to the flowcharts. Of particular concern is the need to make sure that satellite procedures tare' walked down in sufficient detail to make sure that they are -
accurate, feasible, and appropriate for the. emergency. situation; that -
the'in plant components involved can be readily located; and that the tools, materials, and equipment needed to perform the tasks are available.
Response
- Actions will ba planned to ensure that all T-200 series and satellite procedures receive verification and validation (LT).
A root cause investigation of the noted EOP/ TRIP findings is not expected to yield significant or specific corrective actions for the
- process. Therefore, we do not plan to conduct such an investigation..
The. cover lettar that transmitted the inspection report also requested that we review these findings to determine if they affect the Peach Dottom Atomic Power Station (PBAPS) TRIP procedures. These items were discussed with Operations Support personnel at PBAPS and they agreed to perform the review. Additionally, these findings will be incorporated into the Nuclear Group Administrative Procedure which is being developed to provide a common procedure for the TRIP procedure development process ar.d writers guide for both LGS and PBAPS.