IR 05000382/2007007

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IR 05000382-07-007, on April 9 Through May 31, 2007, Waterford Unit 3 - NRC Component Design Bases Inspection Report
ML071940133
Person / Time
Site: Waterford Entergy icon.png
Issue date: 07/13/2007
From: Clark J
NRC/RGN-IV/DRP/RPB-E
To: Walsh K
Entergy Operations
References
IR-07-007
Download: ML071940133 (36)


Text

uly 13, 2007

SUBJECT:

WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC COMPONENT DESIGN BASES INSPECTION REPORT 05000382/2007007

Dear Mr. Walsh:

On May 31, 2007, the US Nuclear Regulatory Commission (NRC) completed a component design bases inspection at your Waterford Steam Electric Station. The enclosed report documents our inspection findings. The preliminary findings were discussed on May 10, 2007, with Mr. J. Laque and other members of your staff. After additional in-office inspection, a final telephonic exit meeting was conducted on May 31, 2006, with you and other members of the your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The team reviewed selected procedures and records, observed activities, and interviewed cognizant plant personnel.

This report documents five findings of very low safety significance (Green). Four of these findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they were entered into your corrective action program, the NRC is treating these violations as noncited violations (NCVs), consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any of the NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Waterford Steam Electric Station, Unit 3, facility.

Entergy Operations, Inc. -2-In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosures, and your response, if any, will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA John Hanna for/

Jeff A. Clark, P. E.

Chief, Project Branch E Division of Reactor Projects Docket: 50-382 License: NPF-38

Enclosure:

NRC Inspection Report 050000382/2007007 w/Attachment: Supplemental Information

REGION IV==

Docket: 50-382 License: NPF-38 Report Nos.: 05000382/2007007 Licensee: Entergy Operations, Inc.

Facility: Waterford Steam Electric Station, Unit 3 Location: Hwy. 18 Killona, Louisiana Dates: April 9 through May 31, 2007 Team Leader: G. Larkin, Senior Resident, Waterford Steam Electric Station, Unit 3 Assist. Team J. Nadel, Reactor Inspector, Engineering Branch 1 Leader:

Inspectors: G. Replogle, Senior Project Engineer, Projects Branch E S. Garchow, Operations Examiner, Operations Branch R. Azua, Reactor Inspector, Engineering Branch 1 Accompanying H. Anderson, Mechanical Engineer, Beckman and Associates Personnel: S. Kobylarz, Electrical Engineer, Beckman and Associates Others: M. Runyan, Senior Reactor Analyst Approved By: J. Clark, PE, Chief Project Branch E-1- Enclosure

SUMMARY OF FINDINGS

IR05000382/2007007; April 16 through May 31, 2007; Waterford Steam Electric Station, Unit 3:

baseline inspection, NRC Inspection Procedure 71111.21, Component Design Basis Inspection.

The report covers an announced inspection by a team of four regional inspectors, two contractors and one senior resident inspector. Five findings were identified. All of the findings were of very low safety significance. The final significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

NRC-Identified Findings

Cornerstone: Mitigating Systems

Green.

The team identified a noncited violation of 10 CFR 50.65(a)(2) for the failure to adequately demonstrate the performance or condition of the dry cooling tower motor-driven sump pumps. Specifically, the licensee failed to periodically verify that the pump flow rates were consistent with their design basis requirements and pump performance problems were likely to go unnoticed. Therefore, the licensee had no technical justification for continued Maintenance Rule (a)(2) status.

The finding was greater than minor because it could be a more significant safety concern if left uncorrected. In addition, the finding was similar to non-minor finding Example 7.b in NRC Inspection Manual Chapter 0612 Appendix E, Examples of Minor Issues, in that there were performance concerns associated with the dry cooling tower sump pumps. Using the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheet, the finding was determined to be a qualification deficiency confirmed not to result in loss of operability per Part 9900, Technical Guidance,

Operability Determination Process for Operability and Functional Assessment (Section 1R21.b.1).

Green.

The team identified a finding for the failure to properly implement the site foreign material exclusion procedure for the dry cooling tower sumps. Specifically, the procedure required the establishment of a foreign material exclusion area if foreign materials could adversely impact equipment function. The area surrounding the dry cooling tower sumps met this criteria but the licensee failed to establish a foreign material exclusion area to protect the sump pump system from damage. The sump pumps had previously suffered damage due to foreign material intrusion.

The finding was more than minor because it affected the mitigating systems cornerstone objective (external factors attribute) to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the finding was determined to be a qualification deficiency confirmed not to result in loss of operability per Part 9900, Technical Guidance, Operability Determination Process for Operability and Functional Assessment. The finding had a crosscutting aspect in the area of human performance (work practices component) in that the licensee failed to effectively communicate expectations regarding procedure adherence and personnel failed to follow the site procedure (H.4(b)). The finding was indicative of current plant performance because the open sump and the foreign material vulnerability were known to plant personnel on an ongoing basis (Section 1R21.b.2).

Green.

The team identified a noncited violation of Technical Specification 6.8.1.a,

Procedures, for inadequate procedural guidance for operators to respond to a postulated loss of offsite power event coincident with a design basis rain event. The design basis calculation specified that, during certain rain precipitation events, operators must transfer the pump power to a safety related power source within 30 minutes of a loss of offsite power to protect safety related motor control centers from flooding. The motor control centers are needed to ensure ultimate heat sink operability. Due to the sequencing of steps in the procedure, operators took approximately 50 minutes to transfer essential power to the pumps. In addition, if offsite power was restored before safety related power was provided to the pumps, there was no instruction to restore the normal power supply (which would have tripped).

This finding was more than minor because it affected the mitigating systems cornerstone objective (external factors component) to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. In addition, the finding was similar to non-minor finding Example 3.k in NRC Inspection Manual Chapter 0612 Appendix E, Examples of Minor Issues, in that there was reasonable doubt of the operability of the system under certain heavy rain conditions. Using the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheet, the team determined that a Phase 2 significance determination was required because the finding potentially represented a loss of system safety function. The team performed a Phase 2 significance determination and found the finding was potentially greater than Green in significance. A Region IV senior reactor analyst performed a Phase 3 significance determination and found the issue was of very low safety significance (Section 1R21.b.3).

Green.

The Team identified a noncited violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, for the failure to ensure that the 125 Vdc safety-related batteries would remain operable if all the intercell and terminal connections were at the resistance value of 150 micro-ohms as allowed by Technical Specification Surveillance Requirement 4.8.2.1.b.2 and 4.8.2.1.c.3.

The finding was greater than minor because it affected the mitigating systems cornerstone objective (design control attribute) to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheet, the finding was determined to be a design deficiency confirmed not to result in loss of operability per Part 9900, Technical Guidance, Operability Determination Process for Operability and Functional Assessment, (Section 1R21.b.4).

Green.

The team identified a noncited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Actions, for the failure to promptly correct a condition adverse to quality (dirt and debris in the dry cooling tower heat exchanger fins). The condition adversely impacted the heat exchangers heat removal rates. The dry cooling towers had very little design margin under some scenarios. In addition, the licensee failed to respond to trend data that showed degraded heat exchanger performance, had no basis for the specified 5 year cleaning interval specified in their heat exchanger program, and hadnt actually cleaned the towers for approximately 11 years.

This finding was more than minor because it was similar to non-minor Example 3.k in NRC Inspection Manual Chapter 0612 Appendix E, Examples of Minor Issues, in that there was a reasonable doubt of the operability of the dry cooling towers. Using Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the finding was determined to be of very low safety significance (Green) because the finding was a qualification deficiency confirmed not to result in loss of operability per Part 9900,

Technical Guidance, Operability Determination Process for Operability and Functional Assessment. The finding had a crosscutting aspect in the area of problem identification and resolution (corrective action program attribute) in that the issue was identified but corrective actions were not taken in a prompt manner (P.1(d)). The issue was indicative of current performance because the system engineer was aware of the degraded cooling tower condition for several years (Section 1R21.b.5).

Licensee-Identified Violations

.

None.

REPORT DETAILS

REACTOR SAFETY

Inspection of component design bases verifies the initial design and subsequent modifications and provides monitoring of the capability of the selected components and operator actions to perform their design bases functions. As plants age, their design bases may be difficult to determine and important design features may be altered or disabled during modifications. The plant risk assessment model assumes the capability of safety systems and components to perform their intended safety function successfully. This inspectable area verifies aspects of the Initiating Events, Mitigating Systems and Barrier Integrity cornerstones for which there are no indicators to measure performance.

1R21 Component Design Bases Inspection

The team selected risk-significant components and operator actions for review using information contained in the licensees probabilistic risk assessment. In general, this included components and operator actions that had a risk achievement worth factor greater than two or a Birnbaum value greater than 1E-6.

a. Inspection Scope

To verify that the selected components would function as required, the team reviewed design basis assumptions, calculations, and procedures. In some instances, the team performed calculations to independently verify the licensee's conclusions. The team also verified that the condition of the components was consistent with the design bases and that the tested capabilities met the required criteria. The team reviewed maintenance work records, corrective action documents, and industry operating experience records to verify that licensee personnel considered degraded conditions and their impact on the components. For the review of operator actions, the team observed operators during simulator a scenario, as well as during simulated actions in the plant.

The team performed a margin assessment and detailed review of the selected risk-significant components to verify that the design bases have been correctly implemented and maintained. This design margin assessment considered original design issues, margin reductions because of modifications, and margin reductions identified as a result of material condition issues. Equipment reliability issues were also considered in the selection of components for detailed review. These included items such as failed performance test results; significant corrective actions; repeated maintenance; 10 CFR 50.65(a)1 status; operable, but degraded, conditions; NRC resident inspector input of problem equipment; system health reports; industry operating experience; and licensee problem equipment lists. Consideration was also given to the uniqueness and complexity of the design, operating experience, and the available defense in-depth margins.

The inspection procedure requires a review of 15-20 risk-significant and low design margin components, 3 to 5 relatively high-risk operator actions, and 4 to 6 operating experience issues. The sample selection for this inspection was 20 components, 5 operator actions, and 5 operating experience items.

The components selected for review were:

  • 125 Vdc Battery Train A
  • High Pressure Safety Injection Pump Train A
  • Condensate Storage Pool
  • Train B Component Cooling Water Heat Exchanger
  • Reactor Water Storage Pool
  • Turbine Driven Emergency Feedwater Pump Steam Trip and Throttle Valves
  • Auxiliary Component Cooling Water Valve ACC-126B The selected operator actions were:
  • Align potable water to instrument air compressors.

The operating experience issues were:

b. Findings

.1 Failure to Meet Maintenance Rule Requirements for Dry Cooling Tower Sump Pumps

Introduction.

The team identified a Green noncited violation of 10 CFR 50.65(a)(2) for the failure to adequately demonstrate the performance or condition of the dry cooling tower motor-driven sump pumps. Specifically, the licensee failed to periodically verify that the pump flow rates were consistent with their design basis requirements and pump performance problems were likely to go unnoticed. Therefore, the licensee had no technical justification for continued Maintenance Rule (a)(2) status.

Description.

Section (a)(1) of the Maintenance Rule requires periodic monitoring of systems within the scope of the rule against licensee established goals in a manner sufficient to provide reasonable assurance that the equipment remains capable of fulfilling its intended functions. Section (a)(2) of the rule specifies that monitoring against goals is not required where it has been demonstrated that the performance of the equipment is being effectively controlled through maintenance. The licensee had placed the dry cooling tower sump pumps in (a)(2) status. Normally, when placing equipment in (a)(2) status, licensees will establish performance monitoring criteria to demonstrate continued effective maintenance and compliance with the Maintenance Rule.

The dry cooling tower sump pumps are critical to the continued operation of the Waterford-3 ultimate heat sink during heavy rain events. While not safety-related, the pumps are required to meet 10 CFR Part 50, Appendix A, General Design Criterion 2, Design Bases for Protection Against Natural Phenomena. If the motor-control centers flood, the fans to the ultimate heat sinks could fail.

The licensees ultimate heat sink included two redundant trains, each consisting of one dry and one wet cooling tower. The dry cooling tower area was open to the environment and extended below grade level. Each dry cooling tower basin had a sump with two non-safety motor-driven sump pumps and one portable diesel driven pump. During design basis rainfall events, if water collected in the dry cooling tower basin to a level of approximately 1.5 feet, the motor-driven sump pump motors would be submerged and could fail. The sump pumps protect the Train A and B safety related motor control centers, which were located near the bottom of the basins. The motor control centers provided safety related power to all the fans in both the dry and wet cooling towers. The design bases calculation MD(Q)-9-38 assumed the motor-driven pumps discharged water at 270 gallons per minute (gpm) and the diesel driven pump discharged at 300 gpm.

For the dry cooling tower sump pumps, the team reviewed the licensees Maintenance Rule performance criteria to verify compliance with the rule. The team identified several concerns, as follows:

1. The licensee had established inadequate performance criteria for monitoring

pump performance. The licensee had defined a Maintenance Rule Functional Failure as any failure which causes the flow rate from one dry cooling tower area (defined as one diesel pump and two motor-driven pumps) to be less than 325 gpm. The team identified that the minimum design basis flow rate was actually 570 gpm (300 gpm from the diesel-driven pump and 270 gpm from one motor-driven pump).

2. The licensee did not adequately monitor pump flows to verify that the

performance criteria were met. The licensees Maintenance Rule reliability criteria was:

The pumps experience no functional failures in 18 months and no repeat maintenance rule functional failures in 36 months.

To qualify as a functional failure, the licensee specified that two of the three pumps would have to fail at the same time. However, if the emergency diesel pump failed, the two motor driven pumps may not have sufficient flow to meet the 570 gpm design need. The licensee only monitored diesel driven pump flow every five years and performed no meaningful monitoring of the motor driven pumps. While the system engineer stated that he periodically checked pump flow rates after it rained (when a pump was operating) and that according to an informal calculation (not written down) the pump flow rate was about 270 gpm, the team identified the following problems with this method:

  • The uncertainty with the computer point timing method (that the engineer used) was +/- 59 seconds at the start and stop points. Since the engineer only monitored flow for one minute, the data was not meaningful.
  • In most cases, only one pump was operating at the time when the check was performed. The second pump would not start unless sump level reached a second higher setpoint.
  • The method, had it been adequate, did not demonstrate that both motor-driven pumps could pump 270 gpm when pumping at the same time.

The pumps discharged to a common header. If one pump can discharge at 270 gpm into the header, its a well known fact that two pumps pumping into the same discharge header pump discharge flows are reduced. The discharge head (back-pressure) increases with two pumps operating and reduces the discharge flow.

3. Foreign materials in the dry cooling tower sump could result in unidentified

degraded system performance. The licensees monitoring efforts were inadequate to consistently detect this condition. Foreign material lodged in the pumps and/or piping could partially block flow. During this NRC inspection, the team noted wood and insulation in the vicinity of the dry cooling tower sumps. In addition, the Train A dry cooling tower sump cover plate did not cover the entire sump, making it easy for the materials to accidently end up in the sump. The team also noted the following past foreign material related problems:

  • On August 28, 2005, during Katrina, the control room received dry cooling tower and fuel handling building high sump alarms. An operator reported that the dry cooling tower sump drains were clogged with debris.
  • In August 2000, a dry cooling tower sump pump seized and had to be completely replaced. The licensee determined that the pump failed due to foreign material in the pump strainer and pieces of cloth were found wrapped around the pumps impeller.

While catastrophic failures of one of the motor driven pumps might be identified through normal operation, the more likely scenarios involving partial flow blockage could easily go unnoticed.

Due to the lack of periodic flow test data, problems demonstrating pump performance from maintenance rule functional failure and reliability criteria, and historical problems with intrusion of foreign material into the dry cooling tower sumps, the team concluded that the licensees Maintenance Rule performance demonstration for these pumps was neither technically justifiable nor reasonable. Therefore, the licensee did not demonstrate acceptable performance in accordance with the Maintenance Rule Section (a)(2) and was required to place the pumps in (a)(1) status.

In response to the teams concerns, the licensee performed flow testing of the pumps and verified that the pumps could produce their design basis flow rates.

Analysis.

The failure to develop and implement technically justifiable performance criteria for the motor-driven sump pumps, for compliance with provisions of the Maintenance Rule, was a performance deficiency. The finding was greater than minor because it could be a more significant safety concern if left uncorrected. In addition, the finding was similar to non-minor finding Example 7.b in NRC Inspection Manual Chapter 0612 Appendix E, Examples of Minor Issues, in that there were performance concerns associated with the dry cooling tower sump pumps. Using the Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the finding was determined to be a qualification deficiency confirmed not to result in loss of operability per Part 9900, Technical Guidance, Operability Determination Process for Operability and Functional Assessment.

Enforcement.

10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, (a)(1) states Each holder of a license to operate a nuclear power plant... shall monitor the performance or condition of structures, systems, or components, against licensee established goals, in a manner sufficient to provide reasonable assurance that such structures, systems, and components... are capable of fulfilling their intended functions. The Maintenance Rule, (a)(2) states, Monitoring as specified in paragraph (a)(1) of this section is not required where it has been demonstrated that the performance or condition of a structure, system, or component is being effectively controlled through the performance of appropriate preventive maintenance, such that the structure, system, or component remains capable of performing its intended function. Contrary to the above, the licensee has failed to establish goals sufficient to provide reasonable assurance that the dry cooling tower sump pumps could perform their intended function and failed to demonstrate, through the performance of appropriate preventative maintenance, that the dry cooling tower sump pumps remained capable of performing their intended function. Because the violation is of very low safety significance and has been entered into the licensees corrective action program as Condition Report CR-WF3-2007-02004, this violation is being treated as a noncited violation (NCV), consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000382/2007007-01) Failure to Meet Maintenance Rule Requirements for Dry Cooling Tower Sump Pumps.

.2 Failure to Implement Foreign Material Exclusion Procedure for Dry Cooling Tower

Sumps

Introduction.

The team identified a Green finding for the failure to properly implement the site foreign material exclusion procedure for the dry cooling tower sumps.

Specifically, the procedure required the establishment of a foreign material exclusion area if foreign materials could adversely impact equipment function. The area surrounding the dry cooling tower sumps met this criteria but the licensee failed to establish a foreign material exclusion area to protect the sump pump system from damage. The sump pumps had previously suffered damage due to foreign material intrusion.

Description.

During a plant walkdown, the team noted foreign material near the opening to the Train A dry cooling tower sump, including wooden doorstop wedges, pieces of plastic and trash. As noted in Section 1R21.b.1 of this report, the sump pumps are critical to maintaining ultimate heat sink operability during heavy rain events.

Procedure EN-MA-118, Foreign Material Exclusion, Revision 2 states, in part:

This procedure applies to all Station activities having the potential to introduce foreign material into systems or components which could impact plant safety, power generation, or system reliability. The requirements of this procedure should be applied when maintenance, modifications, repairs, inspection, and operating activities are being conducted on open piping, vessels, tubing, instrumentation, mechanical, and electrical equipment.

The procedure required that a foreign material exclusion zone be established to prevent foreign materials from adversely impacting system reliability. It applied to safety and non-safety related systems.

Contrary to the above, the Train A dry cooling tower sump was open (lost lid) for over 7 years and the area was not controlled as a foreign material exclusion zone.

Consequently, on several occasions foreign materials entered the sump and adversely impacted sump pump performance. For example, in August 2000 foreign material became bound around one of the pump impellers, destroying the pump. It was noted that the pump suction side was full of debris (CR-WF3-2000-0879).

Analysis.

The failure to properly implement the site foreign material exclusion procedure was a performance deficiency. The finding was more than minor because it affected the mitigating systems cornerstone objective (external factors attribute) to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the finding was determined to be a qualification deficiency confirmed not to result in loss of operability per Part 9900, Technical Guidance, Operability Determination Process for Operability and Functional Assessment. The finding had a crosscutting aspect in the area of human performance (work practices component) in that the licensee failed to effectively communicate expectations regarding procedure adherence and personnel failed to follow the site procedure (H.4(b)). The finding was indicative of current plant performance because the open sump and the foreign material vulnerability were known to plant personnel on an ongoing basis.

Enforcement.

Since the finding involved non-safety related equipment, no violation of NRC requirements occurred. The licensee entered this finding into their corrective action program as Condition Report WF3-2007-01859 (FIN 05000382/2007007-02),

Failure to Implement Foreign Material Exclusion Procedure for Dry Cooling Tower Sumps.

.3 Inadequate Procedure for Restoring Power to Dry Cooling Tower Sump Pumps

Introduction.

The team identified a Green NCV of Technical Specification 6.8.1.a, Procedures, for inadequate procedural guidance for operators to respond to a postulated loss of offsite power event coincident with a design basis rain event. The design basis calculation specified that, during certain rain precipitation events, operators must transfer the pump power to a safety related power source within 30 minutes of a loss of offsite power to protect safety related motor control centers from flooding. The motor control centers are needed to ensure ultimate heat sink operability. Due to the sequencing of steps in the procedure, operators took approximately 50 minutes to transfer essential power to the pumps. In addition, if offsite power was restored before safety related power was provided to the pumps, there were no instructions to restore the normal power supply (which would have tripped).

Description:

The Train A and B ultimate heat sinks each consist of a dry cooling tower and a wet cooling tower. The cooling towers are located below grade, in the cooling tower basins. A safety related motor-control center (one for each set of cooling towers)is also located below grade, close to the bottom of the basins. Two motor-operated and one diesel driven non-safety related sump pumps are located in each cooling tower basin to, in part, protect the motor-control centers and the operability of the ultimate heat sinks.

During a loss of offsite power, coincident with a design basis rain event, Calculation MD(Q)-9-38, Capacity of Wet Cooling Tower Basins, Revision 4 assumed operators align safety grade power to the dry cooling tower sump pumps within 30 minutes of event initiation. Emergency Operating Procedure OP-902-004, Excess Steam Demand Recovery, Revision 10, was one of several emergency operating procedures that were used to direct the required 30 minute action. It stated, in part:

IF offsite power has been lost, AND can NOT be restored within 30 Minutes, THEN REFER TO Appendix 20, Energize DCT [dry cooling tower] Sump Pumps and energize at least one DCT sump pump in each sump.

In addition to the above, Waterford 3 made a commitment (W3P82-0652) to the NRC as part of the licensing basis that the emergency operating procedures would include provisions for switching the dry cooling tower sump pump power supplies to the emergency bus within 30 minutes of a loss of off-site power.

During a steam generator tube rupture exercise in the simulator (that included a loss of offsite power) followed by an in-plant observation, the team observed that the crew took approximately 50 minutes to complete the required step. The team evaluated the impact of the additional actions associated with responding to a steam generator tube rupture, as these would not normally be performed for a loss of offsite power with design basis rain. However, the additional steps did not make a meaningful difference in the timing. Under optimistic conditions, the team estimated that a best-case time would be 37 minutes. The significant contributor to the delay was the steps late placement within the implementing procedure. The team noted that, once ordered, operators could perform the step in 12 minutes.

The team considered whether operators might recognize the importance of the step and perform it earlier than the procedure would dictate. The licensees process allowed this step to be performed out of sequence. The team reviewed training materials and noted that the action was discussed but was not one of the learning objectives. Further, the team interviewed licensed operators and found that operators, in general, were not familiar with the requirement, or the basis for the requirement. Accordingly, the team determined that the operators were not likely to recognize the importance of performing the step earlier, out of sequence. They were more likely to perform this step in the specified order.

A second, related, concern involved a scenario where offsite power was initially lost but was recovered shortly thereafter. In this case, the feeder breaker to the sump pumps would automatically trip off when offsite power was lost. When offsite power was restored, the pumps would not have power and there was no procedural step that required that power be provided to the pumps within 30 minutes. The previously noted procedure step would only be completed if operators believed that offsite power would be lost for more than 30 minutes.

In response to the teams concerns, the licensee provided prompt training to all operating crews regarding the importance of ensuring that the pumps are powered within 30 minutes in response to any loss of offsite power, regardless of duration, and to perform the necessary steps out of sequence, if necessary. In addition, the licensee initiated action to make appropriate procedure changes.

Analysis.

The failure to provide adequate emergency operating procedures was a performance deficiency. This finding was more than minor because it affected the mitigating systems cornerstone objective (external factors component) to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. In addition, the finding was similar to non-minor finding Example 3.k in NRC Inspection Manual Chapter 0612 Appendix E, Examples of Minor Issues, in that there was reasonable doubt of the operability of the system under certain heavy rain conditions. Using the Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the team determined that a Phase 2 Significance Determination Process, was required because the finding potentially represented a loss of system safety function. The team performed a Phase 2 Significance Determination Process, and found the finding was potentially greater than Green in significance. A Region IV senior reactor analyst performed a Phase 3 Significance Determination Process, and found the issue was of very low safety significance (Green). The primary assumptions included:

  • The frequency for the design basis rainfall rate was 1.9E-7/yr.
  • The time to restore power following a loss of offsite power event is conservatively assumed as one hour.
  • The diesel powered sump pump would be started at 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> into the event.
  • Offsite power is lost at the beginning of the precipitation event.
  • The delay of 30 minutes in restoring power would add approximately 0.1 feet to the maximum depth in the basin.
Enforcement:

Technical Specification 6.8.1.a, Procedures, requires, in part, that written procedures be established, implemented, and maintained for the activities specified in Regulatory Guide 1.33, Revision 2, Appendix A. Item 6© of Appendix A required procedures for combating emergencies and significant events, including the loss of electrical power. The noted emergency operating procedure directed operator

actions for combating a loss of offsite power, including the restoration of electrical power to the dry cooling tower sump pumps within 30 minutes. Contrary to the above, the procedure was inadequate, in that the procedure steps were sequenced in a manner that made it highly unlikely that operators would provide alternate power to the dry cooling tower sump pumps within the 30 minute requirement. In addition, if off-site power was restored before the power transfer occurred, the procedure contained no step to ensure that the normal power (which tripped off) was restored. Because the violation is of very low safety significance and has been entered into the licensees corrective action program as Waterford Condition Report CR-WF3-2007-01679, this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000382/2007007-03), Inadequate Procedure for Restoring Power to Dry Cooling Tower Sump Pumps.

.4 Inadequate Acceptance Criteria for Battery Cell-to-Cell and Terminal Connection

Resistance Value

Introduction.

The Team identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to ensure that the 125 Vdc safety-related batteries would remain operable if all the intercell and terminal connections were at the resistance value of 150 micro-ohms as allowed by Technical Specification Surveillance Requirement 4.8.2.1.b.2 and 4.8.2.1.c.3.

Description.

The team questioned the basis for the acceptance criteria of less than 150 micro-ohms for cell-to-cell and terminal connections that were found in the Station Battery Bank and Charger Quarterly and 18-month maintenance Surveillance Procedures ME-003-210, Station Battery Bank and Charger (Quarterly), Revision 10, and ME-003-220, Station Battery Bank and Charger (18 Month), Revision 15, respectively, and that were used to satisfy Technical Specification Surveillance Requirements 4.8.2.1.b.2 and 4.8.2.1.c.3. The licensees engineers could not provide a documented technical basis for the 150 micro-ohm resistance acceptance criteria. The licensee initiated condition report CR-WF3-2007-01490 to address this concern. A previous NRC Design Inspection team also questioned the basis for the 150 micro-ohm criterion in a report on July 27, 1998, and the licensee had initiated condition report CR-WF3-1998-0758 to address the affect of inter-cell resistance on equipment voltage.

The apparent cause analysis performed under CR-WF3-1998-0758 considered the 150 micro-ohm basis for the cell-to-cell connection resistance to be unrealistic.

Further, the licensee determined that the battery would not remain operable with all of the intercell resistances at the allowed design limit. The team noted that this condition was inconsistent with 10 CFR 50.36, which contains requirements for technical specifications. The CFR specifies that the limits are the lowest functional capability or performance levels of equipment required for safe operation of the facility. Nonetheless, the 150 micro-ohm resistance value was neither validated nor changed. The team found that the 150 micro-ohms criterion is over 16 times the average installed resistance for terminal connections at Waterford 3 (when new), and on average approximately 5 times greater than the installed inter-cell connection resistance, based on more recent surveillance data for Battery A.

To ensure battery operability, the licensee administratively controlled the total station battery inter-cell and terminal connection resistance when performing the 18-month surveillance procedure ME-003-220. The surveillance procedure required an engineering evaluation if a connection measurement was found to be greater than 20 percent over an installed resistance value. The team considered this approach reasonable for the 18 month surveillance.

In contrast to the 18 month surveillance, the quarterly surveillance procedure contained no additional administrative controls. The team found that the 150 micro-ohms acceptance criteria for the subject terminal connections could allow for inter-cell and terminal resistance conditions that could exceed the calculated available margin.

Calculation EC-E98-001, Calculation of Maximum Allowable Battery Inter-Cell Connection Resistance, Revision 0, determined that the Train A battery had 829 micro-ohms of margin available. Just 6 cells, of the 60 cell battery, at the allowed 150 micro-ohm limit could exceed the available margin. The surveillance permitted all the battery cells intercell resistances to be up to the 150 micro-ohm limit.

Analysis.

The failure to adequately verify or check a design value in accordance with NRC design control requirements was a performance deficiency. The finding was greater than minor because it affected the mitigating systems cornerstone objective (design control attribute) to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the finding was determined to be a design deficiency confirmed not to result in loss of operability per Part 9900, Technical Guidance, Operability Determination Process for Operability and Functional Assessment.

Enforcement.

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program.

Contrary to the above, the licensee failed to properly check the adequacy of the 125 Vdc battery design, in that the 150 micro-ohm acceptance criteria used in surveillance procedures was not adequate to ensure battery operability. Because this finding is of very low safety significance and has been entered into the licensees corrective action program as CR-WF3-2007-01490 and CR-WF3-2007-01722, this violation is being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy (NCV 05000382/2007007-04), Inadequate Acceptance Criteria for Battery Cell-to-Cell and Terminal Connection Resistance Value.

.5 Failure to Take Prompt Corrective Measures to Address Degraded Dry Cooling Towers

Introduction.

The team identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Actions, for the failure to promptly correct a condition adverse to quality (dirt and debris in the dry cooling tower heat exchanger fins). The condition adversely impacted the heat exchangers heat removal rates. The dry cooling towers had very little design margin under some scenarios. In addition, the licensee failed to

respond to trend data that showed degraded heat exchanger performance, had no basis for the specified 5 year cleaning interval specified in their heat exchanger program, and hadnt actually cleaned the towers for approximately 11 years.

Description.

During a plant walkdown on April 17, 2007, the team noted debris between the dry cooling tower fins. The dry cooling tower heat exchangers are water to air heat exchangers. Each train has 15 large electric fans that force cooling air across the heat exchanger fins. There is a small gap between each of the fins, where air must be able to pass to ensure proper heat exchanger performance. The gaps were clogged in several areas of the heat exchangers. The licensee had determined that, when new, the dry cooling tower heat exchangers had only about 3 percent margin for the post-tornado response and about 15 percent margin for the large break loss of coolant accident response.

The team noted that industry guidance documents clearly cautioned against dirt and debris between heat exchanger fins. For example, Electric Power Research Institutes Alternative to Thermal Performance Testing and/or Tube-Side Inspections of Air-to-Water Heat Exchangers, specified, in part, that the licensee should demonstrate by inspection that the air-side flow paths are unobstructed. The document further explained that one must be able to provide assurance that the air-side finned surface is not blocked by foreign material such as lint and that the entire surface area of the heat exchanger is available to transfer heat. The team noted that the licensee appeared to be actively using this document but had failed to follow this important guidance.

Performance Trending: The team identified that the licensee had not taken any action in response to adverse performance trend data and was not meeting a Final Safety Analysis Report commitment for performance monitoring. The team asked the licensee for trend or performance information for the heat exchangers. The licensee provided a trend of fan motor-power (this was the only trending the licensee was performing). The theory suggested that, as flow through the heat exchanger is impeded, the fans would use less power (they drive less air). The team noted that fan power usage had decreased over time. For example, in 1999, over three years after the last cleaning (and the first data point) the average fan motor power usage for Train A was 42.6 horse power. By 2001, the average fan power usage was only 39 horse power (only two data points were taken). For Train B, the available data was more limited with respect to the time between data gatherings. In 2000, the average fan power usage was 38 horse power and one year later it was still 38 horse power. Since the Trains A and B heat exchangers were identical, and motor power usage for clean heat exchangers should be the same, it appeared that Train B was degraded as well. Engineers stated that they were taking the data but werent using the information. This was inconsistent the Final Safety Analysis Report. Section 3.1.4.2 states, in part:

Normally, both dry towers are continuously operated. Therefore, the structural and leaktight integrity of the components and the operability of their active components are demonstrated in this way. Data is taken periodically during normal plant operation to confirm heat transfer characteristics.

Contrary to the above, the licensee had taken dry cooling tower data but failed to evaluate the data and confirm the heat transfer characteristics.

Prior Opportunities: The team also identified that the licensee had previously noted dirt and debris in the heat exchanger fins (a condition adverse to quality) but had failed to promptly correct the condition. For example, Work Request 00004284, dated June 17, 2003, stated, in part:

The finned tubes [dry cooling Tower A] have a buildup of dust and debris and need to be cleaned at the next opportunity.

Dry cooling Tower B finned tubes have a buildup of dust and debris and need to be cleaned at the next opportunity.

Contrary to the instructions of the work request, the dry cooling towers had not been cleaned, almost 4 years later. The team considered the failure to promptly correct the condition adverse to quality a violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Actions.

Cleaning Interval: The team identified that the licensee had no basis for the 5 year cleaning interval specified in their heat exchanger monitoring program and the licensee had not actually cleaned the heat exchangers for about 11 years. Cooling Tower A exterior was last cleaned in April 1996, while cooling Tower B was cleaned in May 1996.

The licensee had included the dry cooling towers in their program for monitoring and cleaning heat exchangers in accordance with Generic Letter 89-13, Service Water System Problems Affecting Safety-Related Equipment.Section III.B of the generic letter recommends: 1) periodic thermal performance testing of heat exchangers; or 2)trend test results for both the air and water flow rates in the heat exchangers and perform visual inspections of both the air and water sides. The nominal recommended test/inspection interval was 18 months but licensees could extend the interval based on sound technical justification.

The team asked the licensee for the inspection interval justification. The justification only considered the condition of the water side of the heat exchanger and made no reference to the buildup of dirt and debris on the air side. Further, the licensee failed to perform meaningful trending of the air flow rates and did not act on results from the visual inspections. The team considered the licensees justification for the 5 year inspection and cleaning interval for the air-side inadequate.

Licensee Response: In response to the teams concerns, the licensee performed thermography of the heat exchanger surfaces and determined that the data was inconsistent with clean heat exchangers. The licensee took actions to promptly clean the heat exchangers within the next few months. This was reasonable because the heat

exchangers are extremely large and cleaning must be performed by a qualified contractor. In addition, the cleaning would be completed before the hottest summer months.

The licensee performed an operability evaluation and determined that the heat exchangers were degraded but capable of performing their safety functions. While there was little design margin, the licensee was able to take advantage of margin elsewhere in the plant. For example, the wet cooling towers (which are also part of the ultimate heat sink) had more design margin. In addition, the licensee had not experienced the worst case design basis outside temperature and humidity conditions in the past year.

Analysis.

The failure to promptly correct a condition adverse to quality (degraded dry cooling tower heat exchangers) was a performance deficiency. This finding was more than minor because it was similar to non-minor Example 3.k in NRC Inspection Manual Chapter 0612 Appendix E, Examples of Minor Issues, in that there was a reasonable doubt of the operability of the dry cooling towers. Using Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the finding was determined to be of very low safety significance (Green) because the finding was a qualification deficiency confirmed not to result in loss of operability per Part 9900, Technical Guidance, Operability Determination Process for Operability and Functional Assessment. The finding had a crosscutting aspect in the area of problem identification and resolution (corrective action program attribute) in that the issue was identified but corrective actions were not taken in a prompt manner (P.1(d)). The issue was indicative of current performance because the system engineer was aware of the degraded cooling tower condition for several years.

Enforcement.

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Actions, states, in part, Measures shall be established to assure that conditions adverse to quality, such as... deficiencies and nonconformances are promptly identified and corrected. On June 17, 2003, the licensee identified a deficiency, in that the dry cooling towers were degraded because they had dirt and debris on the heat transfer surfaces. This was a condition adverse to quality. Contrary to the above, the licensee failed to take prompt corrective measures to address the condition adverse to quality. Because the violation is of very low safety significance and has been entered into the licensees corrective action program as Condition Report CR-WF3-2007-01433, this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000382/2007007-05), Failure to Take Prompt Corrective Measures to Address Degraded Dry Cooling Towers.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

The team reviewed Waterford 3 condition reports associated with the selected components, operator actions and operating experience notifications. In addition, this report contains the following issue that has problem identification cross-cutting aspects.

Section 1R21.b.5 documents an issue where the licensee failed to take prompt corrective measures to address dirt and debris in the dry cooling towers.

4OA6 Meetings, Including Exit

On May 10, 2007, the team leader presented the preliminary inspection results to Mr. J. Loque, Acting General Manager for Plant Operation, and other members of the licensees staff. On May 31, 2007, the Component Design Bases Inspection Team Leader conducted a telephonic final exit meeting with Mr. K. Walsh, Vice President and other members of the licensee's staff. The licensee acknowledged the findings during each meeting. While some proprietary information was reviewed during this inspection, no proprietary information was included in this report.

ATTACHMENTS:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

K. Walsh, Vice President, Operations
H. Brodt, Engineer, Probabilistic Safety Assessment
K. Cook, Director, Nuclear Safety Assurance
R. Dodds, General Manager, Plant Operations (Acting)
C. Fugate, Manager, Operations (Acting)
J. Holman, Manager, Safety and Engineering Analysis
J. Meibaum, Electrical Maintenance Supervisor
M. Mills, Training Manager
R. Murillo, Manager, Licensing
R. Putnam, Manager, Programs and Components
J. Rachal, Design Engineering Supervisor
R. Stewart, Component Engineering Supervisor

NRC Personnel

D. Overland, Senior Resident Inspector (Acting)

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000382/2007007-01 NCV Failure to Meet Maintenance Rule Requirements for Dry Cooling Tower Sump Pumps
05000382/2007007-02 FIN Failure to Implement Foreign Material Exclusion Procedure for Dry Cooling Tower Sumps
05000382/2007007-03 NCV Inadequate Procedure for Restoring Power to Dry Cooling Tower Sump Pumps
05000382/2007007-04 NCV Inadequate Acceptance Criteria for Battery Cell-to-Cell and Terminal Connection Resistance Value
05000382/2007007-05 NCV Failure to Take Prompt Corrective Measures to Address Degraded Dry Cooling Towers Attachment

LIST OF DOCUMENTS REVIEWED