LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl |
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Public Service Company *f OcDondo 16805 Road 19 1/2, Platteville, Colorado 80651-9298 i
February 3, 1983 Fort St. Vrain Unit No. 1 m '~7 0 f r (c'[i
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FEB ~ 71983 g Mr. John T. Collins, Regional Administrator bL Region IV
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d Nuclear Regulatory Commission 1
611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76011
Reference:
Facility Operating 3.icense No. DPR-34 Docket No. 50-267
Dear Mr. Collins:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/83-003, Final, submitted per the requirements of Technical Specification AC 7.5.2(b)2.
- Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/83-003.
V trul yours,
/
Don Warembourg Manager, Nuclear Production i
DW/cis Enclosure cc:
Director, MIPC k@
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8302150001 830203 DR ADOCK 05000
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REPORTABLE OCCURRENG DISTRIBUTION Number of Copies De p a rtmen t o f Ene rgy - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 1 (P I4tter)
San Frmeisco operations Office Atta California Patent Group 1333 Broadway Oakland, California 94612 De p a r t me n t o f En e r gy - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 1 (P IAtter)
Mr. Glen A. Newby, Chief HTR Branch Division of Nuclear Power Development Mail Station B-107 Washin gton, D.C.
20545 De p a r t men t o f En e r gy - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 1 (P 14tter)
Attn: Project Manager P. O. Box 81608 San Diego, California 92138
!!r. John T. Collins, Regional Administrator ------------------
1 (Original of P I4tter)
Region IV Nuclear Regulatory Conumission 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76011 M r. Ge o rge Kuzmy cz - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 1 (P Intter)
Nuclear Regulatory Commission 7920 Norfolk Avenue Bethesda, Maryland 20034 Di re c t o r - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P Intter)
Office of Management Information and Program Control Nuclear Regulatory Commission Washington, D.C.
20555 i
INFO Records Center 1 (P Letter)
Suite 1500 1100 circle 75 Parkway Atlanta, G4 30339 Mr. Richard Phelps, ' FSV, CA, Site Rep resentative - - - - - - - - - - - - - - - - 1 (P Letter)
General Atomic Conq)any 16864 Weld County Road 191/2 Platteville, Colorado 80651 1 (P 14tter)
NRC Resident Site Inspector l
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1 i
O REPORT DATE:
February 3, 1983 REPORTABLE OCCURRENCE 83-003 ISSUE O OCCURRENCE DATE:
January 5, 1983 Page 1 of 5 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298 REPORT NO. 50-267/83-003/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
During the period January 5, 1983, through January 18, 1983, the reactor plant was operated in a degraded mode of LCO 4.2.10 on 14 separate occasions.
These events are reportable per Fort St. Vrain Technical Specification AC 7.5.2(b)2.
EVENT
DESCRIPTION
At approximately 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> on January 5, 1983, the concentration of total primary coolant oxidants (sum of water, carbon monoxide, and carbon dioxide) exceeded 10 parts per million (ppm) by volume. This impurity concentration increase occurred during a rise in power following a normal startup with the average core outlet temperature greater than 1200 degrees fahrenheit.
The concentration of total primary coolant oxidants returned to less than the 10 ppm limit of LCO 4.2.10 on January 7,1983, at 0345 hours0.00399 days <br />0.0958 hours <br />5.704365e-4 weeks <br />1.312725e-4 months <br /> as a result of primary coolant cleanup through the helium purification system, but continued to fluctuate about 10 ppm until 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> on January 18, 1983.
A total of 14 events occurred in which the 10 ppm limit was exceeded.
l Each event is described in Table 1 and illustrated in Figure 1.
l
CAUSE
DESCRIPTION:
The reactor plant had been maintained in either a low power or shutdown condition for several months. During this period, several maintenance activities took place, including the isolation of a steam generator tube leak (Reportable Occurrence 82-049). As a result of this tube leak, feedwater entered the reactor vessel and became entrained in the primary coolant.
[
j Following the steam generator tube maintenance, the primary coolant I
purification system was utilized to remove sufficient moisture to l
allow plant startup. However, due to the hygroscopic properties of the reactor core graphite and absorption in the vessel liner insulation, some of the moisture was retained.
REPORTABLE OCCURRENCE 83-003 ISSUE O Page 2 of 5 As the core temperature was increased, the retained moisture was released from the reactor vessel internal components and chemically reacted with the core graphite.
This process caused the total oxidant concentration to fluctuate about 10 ppm until all moisture had been removed.
CORRECTIVE ACTION:
In all 14 events, the total oxidant concentration was reduced below the LCO 4.2.10 limit by utilization of the helium purification system.
No further corrective actions are anticipated or required.
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REPORTABLE OCCURRENCE 83-003 ISSUE O Page 3 of 5 TABLE 1 Maximum Start End PPM Event No.
Date/ Time Date/ Time Attained 1
830105/0030 830107/0345 51.0 2
830107/0415 830108/0050 14.2 3
830108/0230 830108/1500 15.4 4
830108/1700 830108/2245 12.6 5
830109/0130 830109/0400 11.8 l
6 830109/0400 830109/1100 12.2 7
830109/1530 830109/1715 11.2 8
830109/1900 830109/2315 11.6 9
830110/0100 830111/1200 15.3 10 830111/1200 830112/0800 14.4 11 830112/0800 830112/1430 10.5 12 830112/1930 830113/0330 10.4 13 830114/2330 830115/0030 10.5 14 830118/0700 830118/0900 13.2 l
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REPORTABLE OCCURRENCE 83-003 ISSUE O Page 4 of 5
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REPORTABLE OCCURRENCE 83-003 ISSUE O Page 5 of 5 Prepared By:
Auw k. b who Owen J. CLayton O
Senior Technical Services Technician Reviewed By:
/b Charles Full'er Technical Services neering Supervisor r
Reviewed By:
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Station Man'll f' Edwin D. Hi ager Approved By:
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Don Warembourg
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Manager, Nuclear Pfoduction
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| 05000267/LER-1983-001-01, /01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs | /01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs | | | 05000267/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-002-03, /03L-0:on 830104,seven Unsampled Releases Made from Reactor Bldg Sump on 821221 & 22.Caused by Personnel Error.Daily Sample Taking Resumed on 821223.Responsible Personnel Retrained | /03L-0:on 830104,seven Unsampled Releases Made from Reactor Bldg Sump on 821221 & 22.Caused by Personnel Error.Daily Sample Taking Resumed on 821223.Responsible Personnel Retrained | | | 05000267/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-003-03, /03L-0:on 14 Separate Occasions,Total Primary Coolant Oxidants Exceeded Acceptable Limits.Oxidant Offgassing Caused by Increasing Temps During Normal Reactor Startup & Rise to Power.Oxidant Concentration Reduced | /03L-0:on 14 Separate Occasions,Total Primary Coolant Oxidants Exceeded Acceptable Limits.Oxidant Offgassing Caused by Increasing Temps During Normal Reactor Startup & Rise to Power.Oxidant Concentration Reduced | | | 05000267/LER-1983-004, Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-004-03, /03L-0:on 830203-04,five Class I Snubbers Found Inoperable.Caused by Leaking Seals & O-rings or Broken Oil Reservoir.Snubbers Rebuilt & Tested or Replaced W/Tested Qualified Spares & Reinstalled | /03L-0:on 830203-04,five Class I Snubbers Found Inoperable.Caused by Leaking Seals & O-rings or Broken Oil Reservoir.Snubbers Rebuilt & Tested or Replaced W/Tested Qualified Spares & Reinstalled | | | 05000267/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-005-03, /03L-0:on 830207,reactor Dewpoint Exceeded Limits. Caused by Buffer Helium Sys Upset Due to 830128 Trip. Dewpoint Reduced W/Helium Purification Sys | /03L-0:on 830207,reactor Dewpoint Exceeded Limits. Caused by Buffer Helium Sys Upset Due to 830128 Trip. Dewpoint Reduced W/Helium Purification Sys | | | 05000267/LER-1983-006-03, /03L-0:on 830215,loop 2 Pcrv Cooling Water Temp Exceeded 120 F.Caused by Blown Instrument Bus 2 Power Inverter Fuse.Instrument Bus re-energized & Power Inverter Repaired | /03L-0:on 830215,loop 2 Pcrv Cooling Water Temp Exceeded 120 F.Caused by Blown Instrument Bus 2 Power Inverter Fuse.Instrument Bus re-energized & Power Inverter Repaired | | | 05000267/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-007-03, /03L-0:on 830215,instrument Power Invertor 1B Failed.Caused by Blown 150 Amp Fuse.Reactor Manually Scrammed,Instrument Bus 2 re-energized & Fuse Replaced | /03L-0:on 830215,instrument Power Invertor 1B Failed.Caused by Blown 150 Amp Fuse.Reactor Manually Scrammed,Instrument Bus 2 re-energized & Fuse Replaced | | | 05000267/LER-1983-007, Forwards RO 83-007 & LER 83-007/03L-0 | Forwards RO 83-007 & LER 83-007/03L-0 | | | 05000267/LER-1983-008, Forwards LERs 80-047/03X-1,83-038/03L-0 & Corrected LER 83-008/03X-2 | Forwards LERs 80-047/03X-1,83-038/03L-0 & Corrected LER 83-008/03X-2 | | | 05000267/LER-1983-008-03, During Valve Maint W/Secondary Covers & Missile Shields Removed,Pcrv Helium Pressure Exceeded Tech Spec Limits.Caused by Operator Error. Operator Reminded to Comply W/Tech Specs | During Valve Maint W/Secondary Covers & Missile Shields Removed,Pcrv Helium Pressure Exceeded Tech Spec Limits.Caused by Operator Error. Operator Reminded to Comply W/Tech Specs | | | 05000267/LER-1983-009-01, /01T-0:on 830223,four Masonry Walls Found to Have Inadequate Structural Strength to Withstand Design Criteria Load Combination.Caused by Lack of Dur-O-Wall.Mod Reinforcing Walls W/Steel Bar Straps Completed | /01T-0:on 830223,four Masonry Walls Found to Have Inadequate Structural Strength to Withstand Design Criteria Load Combination.Caused by Lack of Dur-O-Wall.Mod Reinforcing Walls W/Steel Bar Straps Completed | | | 05000267/LER-1983-009, Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-010-03, /03L-0:on 830302,during Release of Radioactive Liquid Effluent from Reactor Bldg Sump,Overflow from Liquid Waste Sump Drained Into Reactor Bldg Sump.Caused by Personnel Error.Release Terminated | /03L-0:on 830302,during Release of Radioactive Liquid Effluent from Reactor Bldg Sump,Overflow from Liquid Waste Sump Drained Into Reactor Bldg Sump.Caused by Personnel Error.Release Terminated | | | 05000267/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-012, Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-012-03, /03L-0:on 830308-15,reactor Dewpoint Exceeded Limits Three Times.Caused by Plant Upsets Resulting in Increased Moisture Levels & Subsequent Vaporization Exceeding Helium Purification Sys Removal Rate | /03L-0:on 830308-15,reactor Dewpoint Exceeded Limits Three Times.Caused by Plant Upsets Resulting in Increased Moisture Levels & Subsequent Vaporization Exceeding Helium Purification Sys Removal Rate | | | 05000267/LER-1983-014-03, /03L-0:on 830309,emergency Set 1B Emergency Diesel 1D Tripped Due to Dc Electrical Sys Intermittent Ground. Caused by Loose Conduit Termination Lock Nut.Nut Tightened & Secured | /03L-0:on 830309,emergency Set 1B Emergency Diesel 1D Tripped Due to Dc Electrical Sys Intermittent Ground. Caused by Loose Conduit Termination Lock Nut.Nut Tightened & Secured | | | 05000267/LER-1983-014, Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-015-03, /03L-0:on 830311,emergency Feedwater Supply to Loop 1 Helium Circulator Pelton Wheel Drives Isolated.Caused by Excessive Wear Requiring Maint.Pipe Section Replaced & Flanges Installed | /03L-0:on 830311,emergency Feedwater Supply to Loop 1 Helium Circulator Pelton Wheel Drives Isolated.Caused by Excessive Wear Requiring Maint.Pipe Section Replaced & Flanges Installed | | | 05000267/LER-1983-016, Forwards LER 83-016/03L-0.Detailed Event Analysis Encl | Forwards LER 83-016/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-016-03, /03L-0:on 830331,two Class 1 Hydraulic Shock Suppressors Found Inoperable.Caused by Fully Extended Snubbers,Due to Thermal Pipe Movement.One Snubber Adjusted & Other Replaced | /03L-0:on 830331,two Class 1 Hydraulic Shock Suppressors Found Inoperable.Caused by Fully Extended Snubbers,Due to Thermal Pipe Movement.One Snubber Adjusted & Other Replaced | | | 05000267/LER-1983-017-01, /01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced | /01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced | | | 05000267/LER-1983-018-03, /03L-0:on 830517,w/reactor Shutdown,All Outside Power Lost Due to High Winds & Snow.Emergency Diesel Generator Load Shedding & Sequencing Relays Failed to Operate.Caused by Coil Failures.Relays Tested | /03L-0:on 830517,w/reactor Shutdown,All Outside Power Lost Due to High Winds & Snow.Emergency Diesel Generator Load Shedding & Sequencing Relays Failed to Operate.Caused by Coil Failures.Relays Tested | | | 05000267/LER-1983-019-01, /01T-0:on 830606,discovered That Reactor Operated Between 5% Power & Shutdown W/O Operable Analytical Moisture Monitors on 830603.Caused by Accidental Isolation of Sample Paths to Monitors | /01T-0:on 830606,discovered That Reactor Operated Between 5% Power & Shutdown W/O Operable Analytical Moisture Monitors on 830603.Caused by Accidental Isolation of Sample Paths to Monitors | | | 05000267/LER-1983-020-03, /03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal Wear | /03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal Wear | | | 05000267/LER-1983-022-03, W/Reactor Operating at Approx 13% Power,One Class I Hydraulic Shock Suppressor Found Inoperable.Faulty Rod Seal Allowed Gradual Loss of Operating Fluid from Reservoir.Snubber Replaced | W/Reactor Operating at Approx 13% Power,One Class I Hydraulic Shock Suppressor Found Inoperable.Faulty Rod Seal Allowed Gradual Loss of Operating Fluid from Reservoir.Snubber Replaced | | | 05000267/LER-1983-023-03, /03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve Calibr | /03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve Calibr | | | 05000267/LER-1983-024-03, /03L-0:on 830706,level in Liquid Storage Tank T-2501 Decreased Below Tech Spec Limit.Caused by Personnel Error.Personnel Counseled on Tech Spec Requirements | /03L-0:on 830706,level in Liquid Storage Tank T-2501 Decreased Below Tech Spec Limit.Caused by Personnel Error.Personnel Counseled on Tech Spec Requirements | | | 05000267/LER-1983-025-03, /03L-0:on 830721-0806,reactor Operated in Degraded Modes of Limiting Condition for Operation 4.2.10.Caused by 830317 High Moisture Scram.Reactor Power Restricted While Helium Purification Sys Removed Impurities | /03L-0:on 830721-0806,reactor Operated in Degraded Modes of Limiting Condition for Operation 4.2.10.Caused by 830317 High Moisture Scram.Reactor Power Restricted While Helium Purification Sys Removed Impurities | | | 05000267/LER-1983-026-03, /03L-0:on 830722 & 23,reactor Bldg Sump Pump Proportional Sampler Discovered Inoperable.Caused by Personnel Error.New Sampler Not Functionally Tested Prior to Returning Sys to Svc.Procedures Will Be Revised | /03L-0:on 830722 & 23,reactor Bldg Sump Pump Proportional Sampler Discovered Inoperable.Caused by Personnel Error.New Sampler Not Functionally Tested Prior to Returning Sys to Svc.Procedures Will Be Revised | | | 05000267/LER-1983-029-03, /03L-0:on 830730,level in Liquid Nitrogen Storage Tank Dipped Below 650 Gallons.Caused by Load of Liquid Nitrogen Not Dispatched from Supplier.Shipment Received on 830730 | /03L-0:on 830730,level in Liquid Nitrogen Storage Tank Dipped Below 650 Gallons.Caused by Load of Liquid Nitrogen Not Dispatched from Supplier.Shipment Received on 830730 | | | 05000267/LER-1983-031-03, /03L-0:on 830818,one Hydraulic Snubber Found Inoperable.Caused by Leaking Reservoir Fittings Allowing Loss of Oil.Snubber Replaced W/Rebuilt Snubber | /03L-0:on 830818,one Hydraulic Snubber Found Inoperable.Caused by Leaking Reservoir Fittings Allowing Loss of Oil.Snubber Replaced W/Rebuilt Snubber | | | 05000267/LER-1983-032-03, /03L-0:on 830819,motor Driven Boiler Feed Pump Removed from Svc to Repair Leaking Water Valve.Caused by Normal Wear.Valve,Pipe & Flange Assembly Prefabricated & Installed | /03L-0:on 830819,motor Driven Boiler Feed Pump Removed from Svc to Repair Leaking Water Valve.Caused by Normal Wear.Valve,Pipe & Flange Assembly Prefabricated & Installed | | | 05000267/LER-1983-033-03, /03L-0:on 830827,gas Waste Vacuum Tank Rupture Disc Found Ruptured.Date of Rupture Undeterminable.Cause Not Stated.Disc Disassembled,Replaced & Returned to Svc | /03L-0:on 830827,gas Waste Vacuum Tank Rupture Disc Found Ruptured.Date of Rupture Undeterminable.Cause Not Stated.Disc Disassembled,Replaced & Returned to Svc | | | 05000267/LER-1983-034-03, /03L-0:on 830921,problems Experienced W/Diesel Generator Set 1A During Weekly Surveillance Test.Caused by Diesel Engine 1A Overheating Due to Failure of Cooling Water Temp Control Valve to Open.Generator Shut Down | /03L-0:on 830921,problems Experienced W/Diesel Generator Set 1A During Weekly Surveillance Test.Caused by Diesel Engine 1A Overheating Due to Failure of Cooling Water Temp Control Valve to Open.Generator Shut Down | | | 05000267/LER-1983-035-03, /03L-0:on 830922,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Isolated to Allow Repair of Leaking Relief Valve & Calibr of Two Associated Pressure Control Valves.Valve Repaired | /03L-0:on 830922,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Isolated to Allow Repair of Leaking Relief Valve & Calibr of Two Associated Pressure Control Valves.Valve Repaired | | | 05000267/LER-1983-036-03, /03L-0:on 830928,emergency Feedwater Supply Header to Loop I Helium Circulator Water Turbine Drives Isolated Twice to Perform Maint on Two Leaking Header Safety Valves & One Pressure Control Valve.Valves Repaired | /03L-0:on 830928,emergency Feedwater Supply Header to Loop I Helium Circulator Water Turbine Drives Isolated Twice to Perform Maint on Two Leaking Header Safety Valves & One Pressure Control Valve.Valves Repaired | | | 05000267/LER-1983-037-03, /03L-0:on 830928,one Bearing Water Makeup Pump Taken Out of Svc While Reactor at 65% Power.Caused by Leaking Mechanical Seal Due to Normal Operation & Wear.Seal Replaced.Pump Returned to Svc | /03L-0:on 830928,one Bearing Water Makeup Pump Taken Out of Svc While Reactor at 65% Power.Caused by Leaking Mechanical Seal Due to Normal Operation & Wear.Seal Replaced.Pump Returned to Svc | | | 05000267/LER-1983-038-03, /03L-0:on 830927,during Scheduled Surveillance Testing on Circulator 1C Circuitry,A Logic CT-2A2 Module Found Inoperable.Caused by Loose Connection in Logic Module. Module Replaced | /03L-0:on 830927,during Scheduled Surveillance Testing on Circulator 1C Circuitry,A Logic CT-2A2 Module Found Inoperable.Caused by Loose Connection in Logic Module. Module Replaced | | | 05000267/LER-1983-039-03, /03L-0:on 830929,w/reactor Operating at 65% Power, Problems Experienced W/Diesel Generator 1B Set During Performance of Weekly Surveillance Test.Caused by Failed Engine Trip Circuit Due to heat-brittlement of Insulation | /03L-0:on 830929,w/reactor Operating at 65% Power, Problems Experienced W/Diesel Generator 1B Set During Performance of Weekly Surveillance Test.Caused by Failed Engine Trip Circuit Due to heat-brittlement of Insulation | | | 05000267/LER-1983-040-03, /03L-0:on 830928,while Operating at 65% Power,One of Three Loop II Plant Protective Sys Dewpoint Moisture Monitors Discovered Inoperable Due to Overheating of Mirror. Caused by Slight Pressure Decrease in Monitor | /03L-0:on 830928,while Operating at 65% Power,One of Three Loop II Plant Protective Sys Dewpoint Moisture Monitors Discovered Inoperable Due to Overheating of Mirror. Caused by Slight Pressure Decrease in Monitor | | | 05000267/LER-1983-041-03, /03L-0:on 831005,emergency Diesel Engine 1D of Emergency Generator Set 1B Taken Out of Svc to Repair Air Leak in Filter.Caused by Blown Out Petcock Drain in Filter.Polycarbonate Bowl Replaced & Tested | /03L-0:on 831005,emergency Diesel Engine 1D of Emergency Generator Set 1B Taken Out of Svc to Repair Air Leak in Filter.Caused by Blown Out Petcock Drain in Filter.Polycarbonate Bowl Replaced & Tested | | | 05000267/LER-1983-042-03, /03L-0:on 831006,boiler Feedpump 1A Removed from Svc to Resolve Speed Oscillation Problems While Boiler Feed Pump 1C Out of Svc for Repairs.Caused by Loose/Worn Governor Linkage.Linkage Remachined & Fitted W/New Bushings | /03L-0:on 831006,boiler Feedpump 1A Removed from Svc to Resolve Speed Oscillation Problems While Boiler Feed Pump 1C Out of Svc for Repairs.Caused by Loose/Worn Governor Linkage.Linkage Remachined & Fitted W/New Bushings | | | 05000267/LER-1983-043-01, /01T-0:on 831011,during Spec LCO 4.1.9 Review, Assumptions Supporting Analysis Discovered Nonconservative, Obviating Basis for Spec.Interim Conservative Guidelines Followed Until Analysis Completed | /01T-0:on 831011,during Spec LCO 4.1.9 Review, Assumptions Supporting Analysis Discovered Nonconservative, Obviating Basis for Spec.Interim Conservative Guidelines Followed Until Analysis Completed | |
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