LER-1983-012, Forwards LER 83-012/03L-0.Detailed Event Analysis Encl |
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public service company ce Odetrsde vn 16805 Road 19 1/2, Platteville, Colorado 80651-9298 April 7, 1983 Fort St. Vrain Unit No. 1 P-83138
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APR I i 1983 Mr. John T. Collins, Regional Administrator h:"
Region IV L-Nuclear Regulatory Commission 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76011
Reference:
Facility Operating License No. DPR-34 i
Docket No. 50-267
Dear Mr. Collins:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/83-012, Final, submitted per the requirements of Technical Specification AC 7.5.2(b)2.
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/83-012.
Very truly yours, Don Warembourg Manager, Nuclear Production DW/cis Enclosure cc:
Director, MIPC b
8304190349 830407 PDR ADDCK 0500026 S
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M REPORT DATE:
Aoril 7. 1983 REPORTABLE OCCURRENCE 83-012 ISSUE O CCCURRENCE DATE:
March 8, 1983 Page 1 of 4 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298 REPORT NO. 50-267/83-012/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
During the period March 8, 1983, through March 15, 1983, with the reactor operating and the average core outlet temperature between 725 and 1200 degrees fahrenheit, the reactor dewpoint exceeded the limits set forth by Figure 4.2.11-1 of LCO 4.2.11 on three separate occasions. Also during the sama period, with the average core outlet temperature greater than 1200 degrees fahrenheit, the total primary coolant oxidants exceeded limits set forth by LCO 4.2.10 on three separate occasions. All events constitute operation in a degraded mode of either LCO 4.2.11 or LCO 4.2.10 and are reportable per Fort St. Vrain Technical Specification AC 7.5.2(b)2.
EVENT
DESCRIPTION
Event #1 At 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on March 8, 1983, with the reactor operating at power and an average core outlet temperature near 970 degrees fahrenheit, the calculated reactor dewpoint entered the "non-acceptable" region of Figure 4.2.11-1 of LCO 4.2.11.
This condition existed until 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> on March 9, 1983, when the dewpoint returned to the
" limited acceptable" region.
The highest dewpoint reached was 51 degrees fahrenheit at an average core outlet temperature of 1030 degrees fahrenheit.
Event #2 At 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> on March 9, 1983, with the reactor operating at power and an average core outlet temperature near 1065 degrees fahrenheit, the calculated reactor dewpoint again entered the "non-acceptable" region of Figure 4.2.11-1 of LC0 4.2.11.
This condition existed until 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on March 10, 1983, when the dewpoint returned to the
" limited acceptable" region.
The highest dewpoint reached was 30 degree-fahrenheit at an average core outlet temperature of 1071 degrees fahrenheit.
s rep 0RTABLE OCCURRENCE 83-012 ISSUE O Page 2 of 4 Event #3 At 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> on March 11, 1983, with the reactor operating at power and the average core outlet temperature near 1004 degrees fahrenheit, the calculated reactor dewpoint again entered the "non-acceptable" region of Figure 4.2.11-1 of LCC 4.2.11.
This condition existed until 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> the same day when the dewpoint returned to the
" limited acceptable" region.
The highest dewpoint reached was 23 degrees fahrenheit at an average core outlet temperature of 1004 degrees fahrenheit.
Event #4 At 1115 hours0.0129 days <br />0.31 hours <br />0.00184 weeks <br />4.242575e-4 months <br /> on March 14, 1983, with the reacter operating at power, the average core outlet temperature increased beyond 1200 degrees fahrenheit with total primary coolant oxidants (sum of water, carbon monoxide, and carbon dioxide) above the 10 parts per million (ppm) limit of LCO 4.2.10.
This condition continued until 1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br /> the same day when the average core outlet temperature dropped below the 1200 degrees fahrenheit limit of LCO 4.2.10.
The highest oxidant concentration reached was 16.9 ppm.
Event #5 At 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br /> on March 14, 1983, with the reactor operating at power, the average core outlet temperature again increased beyond 1200 degrees fahrenheit with total primary coolant oxidants atave the 10 ppm limit of LC0 4.2.10.
This condition continued until 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br /> the same day when the average core outlet temoerature dropped below the 1200 degree fahrenheit limit of LCO 4.2.10.
The highest oxidant concentration reached was 13.2 ppm.
Event #6 At 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br /> on March 14, 1983, with the reactor operating at power, the average core outlet temperature again increased beyond 1200 degrees fahrenheit with total primary coolant oxidants above the 10 ppm limit of LCO 4.2.10.
At 1015 hours0.0117 days <br />0.282 hours <br />0.00168 weeks <br />3.862075e-4 months <br /> on March 15, 1983, total primary oxidants exceeded 100 ppm. This condition continued until 1945 hours0.0225 days <br />0.54 hours <br />0.00322 weeks <br />7.400725e-4 months <br /> on the same day when the average core outlet temperature dropped below the 1200 degree fahrenheit limit of LCO 4.2.10.
The highest oxidant concentration reached was 289.8 ppm.
CAUSE
DESCRIPTION
Moisture was introduced into the prestressed concrete reactor vessel as the result of a buffer helium system upset which occurred on February 15, 1983, following an electrical system upset.
When subsequent startup operations commenced and primary coolant temperatures increased, the vaporization rate of the water which was present in the reactor vessel increased to a point where moisture was
s REPORTABLE OCCURRENCE 83-012 ISSUE O Page 3 of 4 being entrained in the primary coolant fa:ter than the helium purification system could remove it.
CORRECTIVE ACTION:
In the first three events, the helium purification system was used to reduce the reactor dewpoint to within the " limited acceptable" region of Figure 4.2.11-1 of LCO 4.2.11 for the appropriate average core outlet temperature.
In the last three events, the average core outlet temperature was reduced below 1200 degrees fahrenheit, making LCO 4.2.10 no longer applicable.
No further corrective actions are anticipated or required.
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REPORTABLE OCCURRENCE 83-012 ISSUE O Page 4 of 4 G
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Prepared By:
ltize Owen J.(Clayton d Senior fedhnical 36rvices Technician b
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Reviewed By:
A x Frank"J/NovaBek Techni(al Services Engineering Supervisor Reviewed By:
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- - f L. M. McBride
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Station Manager l
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Approved By: b 2[d(N Oon Warembour( '
Manager, Nuclear Production l
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| 05000267/LER-1983-001-01, /01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs | /01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs | | | 05000267/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-002-03, /03L-0:on 830104,seven Unsampled Releases Made from Reactor Bldg Sump on 821221 & 22.Caused by Personnel Error.Daily Sample Taking Resumed on 821223.Responsible Personnel Retrained | /03L-0:on 830104,seven Unsampled Releases Made from Reactor Bldg Sump on 821221 & 22.Caused by Personnel Error.Daily Sample Taking Resumed on 821223.Responsible Personnel Retrained | | | 05000267/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-003-03, /03L-0:on 14 Separate Occasions,Total Primary Coolant Oxidants Exceeded Acceptable Limits.Oxidant Offgassing Caused by Increasing Temps During Normal Reactor Startup & Rise to Power.Oxidant Concentration Reduced | /03L-0:on 14 Separate Occasions,Total Primary Coolant Oxidants Exceeded Acceptable Limits.Oxidant Offgassing Caused by Increasing Temps During Normal Reactor Startup & Rise to Power.Oxidant Concentration Reduced | | | 05000267/LER-1983-004, Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | Forwards LER 83-004/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-004-03, /03L-0:on 830203-04,five Class I Snubbers Found Inoperable.Caused by Leaking Seals & O-rings or Broken Oil Reservoir.Snubbers Rebuilt & Tested or Replaced W/Tested Qualified Spares & Reinstalled | /03L-0:on 830203-04,five Class I Snubbers Found Inoperable.Caused by Leaking Seals & O-rings or Broken Oil Reservoir.Snubbers Rebuilt & Tested or Replaced W/Tested Qualified Spares & Reinstalled | | | 05000267/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-005-03, /03L-0:on 830207,reactor Dewpoint Exceeded Limits. Caused by Buffer Helium Sys Upset Due to 830128 Trip. Dewpoint Reduced W/Helium Purification Sys | /03L-0:on 830207,reactor Dewpoint Exceeded Limits. Caused by Buffer Helium Sys Upset Due to 830128 Trip. Dewpoint Reduced W/Helium Purification Sys | | | 05000267/LER-1983-006-03, /03L-0:on 830215,loop 2 Pcrv Cooling Water Temp Exceeded 120 F.Caused by Blown Instrument Bus 2 Power Inverter Fuse.Instrument Bus re-energized & Power Inverter Repaired | /03L-0:on 830215,loop 2 Pcrv Cooling Water Temp Exceeded 120 F.Caused by Blown Instrument Bus 2 Power Inverter Fuse.Instrument Bus re-energized & Power Inverter Repaired | | | 05000267/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-007-03, /03L-0:on 830215,instrument Power Invertor 1B Failed.Caused by Blown 150 Amp Fuse.Reactor Manually Scrammed,Instrument Bus 2 re-energized & Fuse Replaced | /03L-0:on 830215,instrument Power Invertor 1B Failed.Caused by Blown 150 Amp Fuse.Reactor Manually Scrammed,Instrument Bus 2 re-energized & Fuse Replaced | | | 05000267/LER-1983-007, Forwards RO 83-007 & LER 83-007/03L-0 | Forwards RO 83-007 & LER 83-007/03L-0 | | | 05000267/LER-1983-008, Forwards LERs 80-047/03X-1,83-038/03L-0 & Corrected LER 83-008/03X-2 | Forwards LERs 80-047/03X-1,83-038/03L-0 & Corrected LER 83-008/03X-2 | | | 05000267/LER-1983-008-03, During Valve Maint W/Secondary Covers & Missile Shields Removed,Pcrv Helium Pressure Exceeded Tech Spec Limits.Caused by Operator Error. Operator Reminded to Comply W/Tech Specs | During Valve Maint W/Secondary Covers & Missile Shields Removed,Pcrv Helium Pressure Exceeded Tech Spec Limits.Caused by Operator Error. Operator Reminded to Comply W/Tech Specs | | | 05000267/LER-1983-009-01, /01T-0:on 830223,four Masonry Walls Found to Have Inadequate Structural Strength to Withstand Design Criteria Load Combination.Caused by Lack of Dur-O-Wall.Mod Reinforcing Walls W/Steel Bar Straps Completed | /01T-0:on 830223,four Masonry Walls Found to Have Inadequate Structural Strength to Withstand Design Criteria Load Combination.Caused by Lack of Dur-O-Wall.Mod Reinforcing Walls W/Steel Bar Straps Completed | | | 05000267/LER-1983-009, Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-010-03, /03L-0:on 830302,during Release of Radioactive Liquid Effluent from Reactor Bldg Sump,Overflow from Liquid Waste Sump Drained Into Reactor Bldg Sump.Caused by Personnel Error.Release Terminated | /03L-0:on 830302,during Release of Radioactive Liquid Effluent from Reactor Bldg Sump,Overflow from Liquid Waste Sump Drained Into Reactor Bldg Sump.Caused by Personnel Error.Release Terminated | | | 05000267/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-012, Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-012-03, /03L-0:on 830308-15,reactor Dewpoint Exceeded Limits Three Times.Caused by Plant Upsets Resulting in Increased Moisture Levels & Subsequent Vaporization Exceeding Helium Purification Sys Removal Rate | /03L-0:on 830308-15,reactor Dewpoint Exceeded Limits Three Times.Caused by Plant Upsets Resulting in Increased Moisture Levels & Subsequent Vaporization Exceeding Helium Purification Sys Removal Rate | | | 05000267/LER-1983-014-03, /03L-0:on 830309,emergency Set 1B Emergency Diesel 1D Tripped Due to Dc Electrical Sys Intermittent Ground. Caused by Loose Conduit Termination Lock Nut.Nut Tightened & Secured | /03L-0:on 830309,emergency Set 1B Emergency Diesel 1D Tripped Due to Dc Electrical Sys Intermittent Ground. Caused by Loose Conduit Termination Lock Nut.Nut Tightened & Secured | | | 05000267/LER-1983-014, Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-015-03, /03L-0:on 830311,emergency Feedwater Supply to Loop 1 Helium Circulator Pelton Wheel Drives Isolated.Caused by Excessive Wear Requiring Maint.Pipe Section Replaced & Flanges Installed | /03L-0:on 830311,emergency Feedwater Supply to Loop 1 Helium Circulator Pelton Wheel Drives Isolated.Caused by Excessive Wear Requiring Maint.Pipe Section Replaced & Flanges Installed | | | 05000267/LER-1983-016, Forwards LER 83-016/03L-0.Detailed Event Analysis Encl | Forwards LER 83-016/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1983-016-03, /03L-0:on 830331,two Class 1 Hydraulic Shock Suppressors Found Inoperable.Caused by Fully Extended Snubbers,Due to Thermal Pipe Movement.One Snubber Adjusted & Other Replaced | /03L-0:on 830331,two Class 1 Hydraulic Shock Suppressors Found Inoperable.Caused by Fully Extended Snubbers,Due to Thermal Pipe Movement.One Snubber Adjusted & Other Replaced | | | 05000267/LER-1983-017-01, /01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced | /01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced | | | 05000267/LER-1983-018-03, /03L-0:on 830517,w/reactor Shutdown,All Outside Power Lost Due to High Winds & Snow.Emergency Diesel Generator Load Shedding & Sequencing Relays Failed to Operate.Caused by Coil Failures.Relays Tested | /03L-0:on 830517,w/reactor Shutdown,All Outside Power Lost Due to High Winds & Snow.Emergency Diesel Generator Load Shedding & Sequencing Relays Failed to Operate.Caused by Coil Failures.Relays Tested | | | 05000267/LER-1983-019-01, /01T-0:on 830606,discovered That Reactor Operated Between 5% Power & Shutdown W/O Operable Analytical Moisture Monitors on 830603.Caused by Accidental Isolation of Sample Paths to Monitors | /01T-0:on 830606,discovered That Reactor Operated Between 5% Power & Shutdown W/O Operable Analytical Moisture Monitors on 830603.Caused by Accidental Isolation of Sample Paths to Monitors | | | 05000267/LER-1983-020-03, /03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal Wear | /03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal Wear | | | 05000267/LER-1983-022-03, W/Reactor Operating at Approx 13% Power,One Class I Hydraulic Shock Suppressor Found Inoperable.Faulty Rod Seal Allowed Gradual Loss of Operating Fluid from Reservoir.Snubber Replaced | W/Reactor Operating at Approx 13% Power,One Class I Hydraulic Shock Suppressor Found Inoperable.Faulty Rod Seal Allowed Gradual Loss of Operating Fluid from Reservoir.Snubber Replaced | | | 05000267/LER-1983-023-03, /03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve Calibr | /03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve Calibr | | | 05000267/LER-1983-024-03, /03L-0:on 830706,level in Liquid Storage Tank T-2501 Decreased Below Tech Spec Limit.Caused by Personnel Error.Personnel Counseled on Tech Spec Requirements | /03L-0:on 830706,level in Liquid Storage Tank T-2501 Decreased Below Tech Spec Limit.Caused by Personnel Error.Personnel Counseled on Tech Spec Requirements | | | 05000267/LER-1983-025-03, /03L-0:on 830721-0806,reactor Operated in Degraded Modes of Limiting Condition for Operation 4.2.10.Caused by 830317 High Moisture Scram.Reactor Power Restricted While Helium Purification Sys Removed Impurities | /03L-0:on 830721-0806,reactor Operated in Degraded Modes of Limiting Condition for Operation 4.2.10.Caused by 830317 High Moisture Scram.Reactor Power Restricted While Helium Purification Sys Removed Impurities | | | 05000267/LER-1983-026-03, /03L-0:on 830722 & 23,reactor Bldg Sump Pump Proportional Sampler Discovered Inoperable.Caused by Personnel Error.New Sampler Not Functionally Tested Prior to Returning Sys to Svc.Procedures Will Be Revised | /03L-0:on 830722 & 23,reactor Bldg Sump Pump Proportional Sampler Discovered Inoperable.Caused by Personnel Error.New Sampler Not Functionally Tested Prior to Returning Sys to Svc.Procedures Will Be Revised | | | 05000267/LER-1983-029-03, /03L-0:on 830730,level in Liquid Nitrogen Storage Tank Dipped Below 650 Gallons.Caused by Load of Liquid Nitrogen Not Dispatched from Supplier.Shipment Received on 830730 | /03L-0:on 830730,level in Liquid Nitrogen Storage Tank Dipped Below 650 Gallons.Caused by Load of Liquid Nitrogen Not Dispatched from Supplier.Shipment Received on 830730 | | | 05000267/LER-1983-031-03, /03L-0:on 830818,one Hydraulic Snubber Found Inoperable.Caused by Leaking Reservoir Fittings Allowing Loss of Oil.Snubber Replaced W/Rebuilt Snubber | /03L-0:on 830818,one Hydraulic Snubber Found Inoperable.Caused by Leaking Reservoir Fittings Allowing Loss of Oil.Snubber Replaced W/Rebuilt Snubber | | | 05000267/LER-1983-032-03, /03L-0:on 830819,motor Driven Boiler Feed Pump Removed from Svc to Repair Leaking Water Valve.Caused by Normal Wear.Valve,Pipe & Flange Assembly Prefabricated & Installed | /03L-0:on 830819,motor Driven Boiler Feed Pump Removed from Svc to Repair Leaking Water Valve.Caused by Normal Wear.Valve,Pipe & Flange Assembly Prefabricated & Installed | | | 05000267/LER-1983-033-03, /03L-0:on 830827,gas Waste Vacuum Tank Rupture Disc Found Ruptured.Date of Rupture Undeterminable.Cause Not Stated.Disc Disassembled,Replaced & Returned to Svc | /03L-0:on 830827,gas Waste Vacuum Tank Rupture Disc Found Ruptured.Date of Rupture Undeterminable.Cause Not Stated.Disc Disassembled,Replaced & Returned to Svc | | | 05000267/LER-1983-034-03, /03L-0:on 830921,problems Experienced W/Diesel Generator Set 1A During Weekly Surveillance Test.Caused by Diesel Engine 1A Overheating Due to Failure of Cooling Water Temp Control Valve to Open.Generator Shut Down | /03L-0:on 830921,problems Experienced W/Diesel Generator Set 1A During Weekly Surveillance Test.Caused by Diesel Engine 1A Overheating Due to Failure of Cooling Water Temp Control Valve to Open.Generator Shut Down | | | 05000267/LER-1983-035-03, /03L-0:on 830922,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Isolated to Allow Repair of Leaking Relief Valve & Calibr of Two Associated Pressure Control Valves.Valve Repaired | /03L-0:on 830922,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Isolated to Allow Repair of Leaking Relief Valve & Calibr of Two Associated Pressure Control Valves.Valve Repaired | | | 05000267/LER-1983-036-03, /03L-0:on 830928,emergency Feedwater Supply Header to Loop I Helium Circulator Water Turbine Drives Isolated Twice to Perform Maint on Two Leaking Header Safety Valves & One Pressure Control Valve.Valves Repaired | /03L-0:on 830928,emergency Feedwater Supply Header to Loop I Helium Circulator Water Turbine Drives Isolated Twice to Perform Maint on Two Leaking Header Safety Valves & One Pressure Control Valve.Valves Repaired | | | 05000267/LER-1983-037-03, /03L-0:on 830928,one Bearing Water Makeup Pump Taken Out of Svc While Reactor at 65% Power.Caused by Leaking Mechanical Seal Due to Normal Operation & Wear.Seal Replaced.Pump Returned to Svc | /03L-0:on 830928,one Bearing Water Makeup Pump Taken Out of Svc While Reactor at 65% Power.Caused by Leaking Mechanical Seal Due to Normal Operation & Wear.Seal Replaced.Pump Returned to Svc | | | 05000267/LER-1983-038-03, /03L-0:on 830927,during Scheduled Surveillance Testing on Circulator 1C Circuitry,A Logic CT-2A2 Module Found Inoperable.Caused by Loose Connection in Logic Module. Module Replaced | /03L-0:on 830927,during Scheduled Surveillance Testing on Circulator 1C Circuitry,A Logic CT-2A2 Module Found Inoperable.Caused by Loose Connection in Logic Module. Module Replaced | | | 05000267/LER-1983-039-03, /03L-0:on 830929,w/reactor Operating at 65% Power, Problems Experienced W/Diesel Generator 1B Set During Performance of Weekly Surveillance Test.Caused by Failed Engine Trip Circuit Due to heat-brittlement of Insulation | /03L-0:on 830929,w/reactor Operating at 65% Power, Problems Experienced W/Diesel Generator 1B Set During Performance of Weekly Surveillance Test.Caused by Failed Engine Trip Circuit Due to heat-brittlement of Insulation | | | 05000267/LER-1983-040-03, /03L-0:on 830928,while Operating at 65% Power,One of Three Loop II Plant Protective Sys Dewpoint Moisture Monitors Discovered Inoperable Due to Overheating of Mirror. Caused by Slight Pressure Decrease in Monitor | /03L-0:on 830928,while Operating at 65% Power,One of Three Loop II Plant Protective Sys Dewpoint Moisture Monitors Discovered Inoperable Due to Overheating of Mirror. Caused by Slight Pressure Decrease in Monitor | | | 05000267/LER-1983-041-03, /03L-0:on 831005,emergency Diesel Engine 1D of Emergency Generator Set 1B Taken Out of Svc to Repair Air Leak in Filter.Caused by Blown Out Petcock Drain in Filter.Polycarbonate Bowl Replaced & Tested | /03L-0:on 831005,emergency Diesel Engine 1D of Emergency Generator Set 1B Taken Out of Svc to Repair Air Leak in Filter.Caused by Blown Out Petcock Drain in Filter.Polycarbonate Bowl Replaced & Tested | | | 05000267/LER-1983-042-03, /03L-0:on 831006,boiler Feedpump 1A Removed from Svc to Resolve Speed Oscillation Problems While Boiler Feed Pump 1C Out of Svc for Repairs.Caused by Loose/Worn Governor Linkage.Linkage Remachined & Fitted W/New Bushings | /03L-0:on 831006,boiler Feedpump 1A Removed from Svc to Resolve Speed Oscillation Problems While Boiler Feed Pump 1C Out of Svc for Repairs.Caused by Loose/Worn Governor Linkage.Linkage Remachined & Fitted W/New Bushings | | | 05000267/LER-1983-043-01, /01T-0:on 831011,during Spec LCO 4.1.9 Review, Assumptions Supporting Analysis Discovered Nonconservative, Obviating Basis for Spec.Interim Conservative Guidelines Followed Until Analysis Completed | /01T-0:on 831011,during Spec LCO 4.1.9 Review, Assumptions Supporting Analysis Discovered Nonconservative, Obviating Basis for Spec.Interim Conservative Guidelines Followed Until Analysis Completed | |
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