ML20199H154

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Insp Repts 50-348/97-11 & 50-364/97-11 on 970907-1018. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering
ML20199H154
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 11/17/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20199H100 List:
References
50-348-97-11, 50-364-97-11, NUDOCS 9711260033
Download: ML20199H154 (43)


See also: IR 05000348/1997011

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U.S. NUCLEAR REGULATORY COMMISSION (NRC)

REGION 11

Docket Nos: 50-348 and 50-364

License Nos: NPF-2 and NPF-8

Report No- 50 348/97-11 and 50 364/97-11

License'. Southern Nuclear Operating Company. Inc.

Facility: Farley Nuclear Plant (FNP). Units 1 and 2

Location: 7388 North State Highway 95

s Columbia. AL 36319

Dates: September 7 through October 18, 1997

Inspectors: T. Ross. Senior Resident inspector (SRI)

J. Bartley. Resident inspector (RI)

R. Caldwell. R1

J. Canady - Itl from Hatch Nuclear Plant

(Sections M8.1 and M8.2)

N. Merriweather. Region 11 Reactor Inspector

(Sections E8.4 - E8.25)

J. Zimmerman. NRR (Section E1.2)

Approved by: P. Skinner. Chief. Reactor Projects Branch 2

Division of Reactor Projects

9711260033

PDR

971117

0 ADOCK 05000348

PDR

Enclosure 2

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EXECUTIVE SUMMARY s

Farley Nuclear Pcwer Flant. Units 1 and 2

NRC Inspection Report 50 348/97 11, 50-364/97-1)

This integrated ' inspection included aspects of licensee operations,

engineering, maintenance. and plant support. The report covers a 6 week

period of onsite resident inspector and region based specialist inspections.

Doerations

e Operator attentiveness to main control board (MCB) annunciator alarms

and response to changing plant conditions were prompt. Management's

persistent efforts to reduce the number of MCB deficiencies and achieve

" blackboard ~ were evident. Operating crews demonstrated a high level of

awareness of plant conditions and ongoing activities (Section 01.1).

c, Control Room professionalism, operator demeanor. teomwork. and

conduct of business in the main control room were appropriate and

effective. Shift supervisor (SS) command and control functions

and operations management oversight were evident (Section 01.1).

e Overall material conditions of Unit 1 and 2 structures, systems and

components (SSCs) were good. Almost all plant areas were clear of trash 0

and debris. Areas inside Unit 2 containment were in satisfactory

condition (Section 02.1).

  • Safety system walkdowns and tours verified that accessible portions of

selected systems were adequately maintained and operational

(Sections 02.1 and 02.2).

e Operations had become complacent in its implementation of the Night

Orders Book (NOB). It was evident that some SSs were not always

reviewing the NOB in a timely manner (Section 03.1).

e Operations management implemented immediate and effective compensatory .

measures for Unit 1 by establishing more restrictive administrative

controls over primary coolant specific activity to address increased

projected end-of cycle (E0C) steam generator (SG) conditional tube

leakage (Section 04.1).

Maintenance

e Maintenance and surveillance testing activities were generally conducted

in a thorough and competent manner by qualified individuals in

accordance with plant procedures and work instructions (Section M1.1).

e Maintenance and sup) ort activities associated with the replacement of

PT456. Pressurizer >ressure Channel 2, were generally well-controlled,

and performed by competent and experienced personnel. A technical issue

concerning the adequacy of response time testing and the capability of

Foxboro transmitters to respond to high ramp rates was identified

(Section M1.2).

Enclosure 2

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e While the calibration and RTT associated with the realccement of PT456

were being )erformed. the OC supecvisor recognized tlat the transmitter

was not EQ 3ased on the purchase order number. (Section M1.2)

e Design change for R11/12 Containment Air Particulate and Gas Radiation

Monitors war properly implemented and exhibited good craftsmanship

(bection M1.3).

  • Corrective actions were aroperly identified and satisfactorily

implemented for several _icensee Event Reports, and NRC violations and

open items (Section M8.1 through M8.7).

Emineerinq

e Engineering test procedure for fully withdrawing Unit 2 control rods to

a new position was well written and controlled. The evolution was

conducted in a smooth and deliberate manner (Section El.1),

o The NRC staff found Southern Nuclear Operating Company's (SNC's)

" Generic Letter 95-05 Safety Assessment" in response to Generic Letter 95-05 requirements to be adequate. Compensatory actions were

appropriate, and reporting requirements were adequately addressed

(Section E1.2).

o Overall. licensee response to identified service water pipe corroded

conditions was prompt and effective (Section E1.3).

e Resolution of Updated Final Safety Analysis Report (UFSAR) discrepancy

  1. 089 were not thorough. Calculations supporting the design of the a'.c

start system were non-conservative and were not validated against

existing air start test data. (Section E8.1).

  • A violation was identifieJ for not performing reverse flow testing of

the turbine driven auxiliary feedwater (TDAFW) discharge check valve

V003 or V0020. F. and H to verify that the disk travels to the ser. on

cessation or reversal of flow (Section E8.6).

  • A violation was identified for failure to recognize a TS change was

required for the safety evaluations performed for changes to the

Auxiliary Building Battery Service Test Procedure FNP-1(2)-STP.905.1 and

UFSAR Section 8.3.2 associated with PCN B-92-0-8099 to include the

results of Calculation 07597-E144 addressing design basis requirements

for battery duty cycle, load profile and voltage requirements (Section

E8.22),

o A violation was identified for failure to have a test program and

procedures for service testing of the TDAFW Class 1E battery to ensure

that the battery would meet the required battery duty cycle (Section

E8.8).

e A violation was identified for inapprc~iate acceptance criteria in the

surveillance procedure for verifying t.e forward flow of check valve

VO(n and for failure to follow drawings and instructions in the

Enclosure 2

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installation of the Unit 2 TDAFW battery structural / electrical component

installations (Section E8.7 and E8.9).

e A violation was identified because desigr control measures did not

ensure that calculations were verified and controlled adequately

(Section E8.16 and E8.25).

  • A violation was identified for failure to correct a aeficiency

identified during the 1990 Safety System Self-Assessment (SSSA) of the

Component Cooiing Water (CCW) system involving differences between

Piping and Instrumentation Drawings (P&lDs) and procedures in

identifying caps on vent and drain lines (Section E8.20).

Plant Suonort

e On occasion, operators demonstrated poor work practices in applying

protective actions to prevent the inadvertent spread of contamination

during partial entries into contaminated areas. (Section R1.1).

e Overall cleanliness and housekeeping of radiologically controlled areas

(RCA) of the auxiliary building was good. Ongoing decontamination

efforts by the Health Physics (HP) department to reduce contaminated

surface areas were aggressive and continue to be successful (Section

R2.1).

e HP actions to address long-term storage of spent resins were prompt and

thorough (R8.1).

e An announced drill of the licensee's emergency plan was considered to be

reasonably challenging. Response facilities were manned and fully

03erational in a timely manner. Emergency response personnel properly

claracterized evolving events and made accurate and timely emergency

classifications and notifications (Section Pl.1).

e Security personnel activities observed during the inspection period were

performed well. Site security systems remained functionally adequate to

ensure physical protection of the plant (Section Sl.1).

  • A violation was identified for failure to adequately control and mark

the Safeguard Information (SGI) maintained in the at-the-controls area

of the Main Control Room (Section $3.1).

Enclosure 2

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Report Details

Sunmary of Plant Status

Unit 1 operated continuously at 100% power for the entire inspection period.

Unit 2 operated continuously at 100% power for the entire inspection period.

On October 16. the unit reached 300 days of continuous operation at power.

I. Operations

01 Conduct of Operations

01.1 Routine Observations of Control Room Doerations

a. Insoection Scoce (Insnection Procedure (IP) 71707)

Inspectors conducted frequent inspections of ongoing plant operations in

the Main Control Room (MCR) to verify proper staffing, operator

attentiveness, adherence to approved operating procedures,

communications, and command and control of operator activities.

Inspectors reviewed operator logs and Technical S)ecification (TS)

Limiting Conditions of Operation (LCO) tracking sleets, walked down the

Main Control Boards (MCBs), and interviewed members of the operating

shift crews to verify operational safety and compliance with the TSs.

The inspectors frequently attended morning plant status meetings and

shift turnover meetings to maintain awareness of overall facility

operations, maintenance activities, and recent incidents. Morning

reports and Occurrence Reports (ors) were reviewed on a routine basis to

assure that the licensee properly reported and resolved potential

operational safety concerns.

b. Observations and Findinas

Overall control and awareness of plant conditions during the inspection

Seriod remained a strength, inspectors observed that the Unit 1 MCB.

Jnit 1 Balance of Plant (BOP), and the Emergency Power Board (EPB)

annunciator alarm aanels were frequently " blackboard." However, the

Unit 2 MCBs and B03 panels continued to have a few persistent

annunciators for known equipment problems. Management efforts to

maintain MCB deficiencies at very low levels and blackboard conditions

continued. The combined MCB deficiencies on Units 1 and 2 dropped to

ten, the lowest level for several months. Only two of the MCB

deficiencies were on Unit 1. The majority of the deficiencies involved

non safety-related instrumentation or equipment, and none resulted in a

TS LCO. Tagging and work control activities were conducted outside the

at-the controls (ATC) area of the MCR. Access to the ATC area was

controlled to limit unnecessary activities.

0)erator attentiveness to MCB annunciator alarms and response to

clanging plant conditions remained effective. Interviews with members

of the operating crew verified that they were consistently aware of

plant conditions and ongoing activities. There were no challenging

incidents or transients necessitating operator response during the

report period. Steady-state operations of both units were

Enclosure 2

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well-controlled and continued without any significant events. Operator

logs were of sufficient detail and scope. Shift staffing was verified

to be in compliance with procedural and TS requirements. Pre-shift

briefings of the operating crews by the shift supervisors (SS) were

generally concise and provided operators with shift direction and

priorities. Shift turnovers were accomplished in an orderly manner,

following a board walkdown by the off-going and on-coming operators and

SSs.

c. Conclusions

Control Room professionalism remained good. Operating crew

demeanor, team work, and conduct of business were effective. Unit

SS command and control, and operations management oversight were

evident.

0)erator attentiveness to MCB annunciator alarms and response to

clanging plant conditions were prompt. Management's persistent efforts

to reduce the number of MCB deficiencies were evident. The operating

crew consistently demonstrated a high level of awareness of existing

plant conditions and ongoing plant activities.

02 Operational Status of Facilities and Equipment

02.1 General Tours of Soecific Safety-Related Areas (IP 71707)

(:eneral tours of safety-related areas were performed by the inspectors

tcroughout both units to examine the physical condition of plant

equipment and structures, and to verify that safety systems were

properly aligned. These general walkdowns included the accessible

portions of safety-related structures, systems. and components (SSC).

Overall material conditions of Unit 1 and 2 SSCs were good. Almost all

)lant areas were clear of trash and debris. Some minor equipment and

lousekeeping problems identified by the inspectors during their routine

tours were reported to the responsible SS and/or maintenance department .

for resolution. None of the problems constituted an immediate safety or

compliance issue. However, some of the more significant findings

identified by the inspectors during routine plant tours did require

prompt response by the licensee, as follows:

1) The inspectors toured the Service Water Intake Structure (SWIS)

with the Team Leader (TL) responsible for the painters. The

inspectors pointed out the examples of the poor painting

preparation referenced in Inspection Report (IR) 50-348,

364/97-10. The TL concurred with the inspectors assessment. The

licensee's staff is evaluating methods to remove the old paint and

corrosion products from these areas for proper preservation and

painting. During the tour. inspectors also identified significant

external corrosion (i.e. , rust) on the 42-inch diameter Service

Water System (SWS) discharge piping where it penetrated the north

wall of the SWIS. The piping was subsequently examined by

Engineering Support (ES) personnel (see report section El.3 for

details), and properly cleaned and painted.

Enclosure 2

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2) On September 19. during a routine tour of the Emergency Diesel -

Generators-(EDGs), the inspectors identified that the locking tabs

for the IB EDG fuel rack jam nuts for cylinders 1,2.3.4,5.7.

8, 9 and.10 were not engaged. The inspectors verified that the

lock tabs were engaged on the 1-2A and 28 EDGs. The inspectors

immediately informed an SS. Occurrence Report (OR) 1-97-356 was

generated to document the issue. The licensee promptly evaluated

.the deficiency, checked the jam nuts to ensure'that they were not

--loose, and engaged the locking tabs. The licensee concluded that

-EDG operability was not impacted due to finding the jam nuts tight

prior to engaging the locking tabs.

3). During a routine tour on September 12. the inspectors identified

that an amphenol connection on the Unit 2 radiation monitor R29E

was disconnected. This lead provided power to the check source

mechanism for iodine detector Channels 3 and 4. The inspector

identified this to the SS and the lead was subsequently

reinstalled. The inspector reviewed Updated Final Safety Analysis

Report (UFSAR) Section 11.4, " Process and Effluent Radiological

Monitoring Systems " and found that paragraph 11.4.4.3 stated that

these radiation monitors would be source checked on a monthly or

quarterly basis. Although all of the TS recuired radiation

monitors were being regubrly source checkec , neither the

inspectors nor the licer >e could identify any procedures

requiring a monthly or quarterly source check of R-29A/B. This

UFSAR discrepancy was not previously identified by the licensee's

UFSAR reverification program. By the end of the report period,

the licensee was still investigating the need to conduct regular

source checks.

4) Although within TS required limits for level, the inspectors

questioned whether the 1A Accumulator water level was decreasing

at a faster rate than the other accumulators. Operations

personnel-performed a level trend analysis and were unable to

account for approximately 30 to 40 gallons of accumulator water.

At the next opportunity,

investigate a possible slow leak. Operations planned a containment entry to

5) Although previously identified as a deficient condition, the

inspectors found that leakage from the 1C. Component Cooling Water

(CCW) pump casing vent had increased significantly from its

original 1 drop per minute (dam) to 4-5 dpm. This increased

leakage resulted in considera)1y more uncontrolled wetting of the

pump skid surfaces with toxic, potentially contaminated chromated

water, After notifying the SS the inspectors observed that a

catch device was promptly installed.

While at power, a limited tour of the Unit 2 containment was conducted

on October 3,1997, in conjunction with a job to replace one of the

pressurizer pressure transmitters. The containment areas toured were in

satisfactory condition.

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02.2 Biweekly Insoections of Safety Systems (IP 71707)

Inspectors verified the operability of the following selected safety

systems and/or equipment:

e Unit 2 High Head Safety injection (HHSI) System. A and B Train

e Unit 1 and 2 Residual Heat Removal (RHR) System. A and B Train

Accessible portions of the systems listed above were verified to be

properly aligned. The inspectors also observed them to be adecuately

maintained and in good operating condition. The inspectors dic not

identify any issues that adversely affected system operability. Minor

deficiencies noted were discussed with the appropriate SS. The

licensee's work to reduce the amount of potentially contaminated areas

has significantly improved radiological conditions in the Unit 1 A and B

Train RHR Pump Rooms. The majority of each room has been reclaimed

which allowed routine touring without donning protective clothing.

Decontaminatica efforts on the Unit 2 RHR pump rooms were in-progress.

These decontamination efforts were considered a proactive and positive

i ddiologiCal practice.

02.3 Verification of Safety Taaaina

a. Insoection Stone (IP 71707)

The inspectors verified that selected tagouts were implemented in

accordance with procedural requirements. The inspectors reviewed and

walked down selected devices tagged by the following tag orders (TOs):

e TO# 97-2283 Unit 1 Radiation Monitors Rll and R12

  • TO# 97-2387-1 1B Emergency Air Compressor

b. Observations and Findinas

The inspectors verified that devices identified on the tag orders were

properly tagged. The device identifications were correct, tags were

conspicuously placed on the devices and the tags did not obscure control

room panel indications. The administrative aspects of filling out the

tagging order forms were complete and correct. The tags placed were

adequate for personnel safety and equipment protection.

c. Conclusion

The inspector; concluded that the reviewed safety tagging activities

were correct and met the procedural requirements.

02.4 TS LCO Trackina (IP 40500 and IP 717071

The inspectors routinely reviewed the TS LC0 tracking sheets filled out

by the shift foremen. All reviewed tracking sheets for Units 1 and 2

were consistent with plant conditions and TS requirements.

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103: Operations Procedures'and Documentation- ,

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03l1 Nicht Orders (IP 71707)

' Administrative procedure FNP-0-AP-16. Conduct of'0peration 1 0perations-

Group;: Revision 27. Section 6.2, establishes general requirements for

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the Night Orders-Book (NOB) maintained in the ATC area of the MCR.  :

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Occasionallyr0perations_ management issued night orders for-the SSs to-

read and implement as appropriate. Resident inspectors routinely review J

the NOB for new entries. In the past. inspectors observed that the SSs-

were:very conscientious about initialing new night orders, acknowledging

that they had read and understood the entry. However, the inspectors -

frecently observed that- most of the SSs were no longer initialing new .

entries in the NOB. Although AP-16 did not require initialing of night

orders, this has been considered a good practice in the past.

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Furthermore, based on inspector interviews with SSs during the week of

-September 15. it became evident that some SSs were not always reviewing

the NOB in a timely manner (even when a specific entry'that expressly

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requested that it be-reviewed prior to going on-shift). The inspectors

discussed the use and purpose of the NOB with Operations management to

better understand its role and management expectations. After these

discussions..the N0B was reorganized to improve its useability and SSs

were coached-regarding its purpose.

04 Operator Knowledge and Performance

[ 04.1 Administrative Limit For Primary Coolant Activity-(IP 71707)

On September 11. Southern Nuclear Operating Company (SNC) held a

L conference call with the NRC to discuss its latest results regarding

end-of-cycle (E0C) steam generator (SG) conditional tube leakage and

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burst calculations using data from the last Unit I refueling outage

(UlRF14). During this call SNC concluded that it was required by

Generic Letter (GL) 95-05. " Voltage-Based Re) air Criteria for

Westinghouse Steam Generator Tubes Affected )y Outside Diameter Stress

Corrosion _ Cracking." Section 6. to notify the NRC that the EOC accident -

leakage exceeded the site-allowable leakage limit for Unit 1. By letter

. dated September 12. SNC submitted its GL 95-05 safety assessment and

-compensatory measures (see report paragraph E1.2 below).

. Also during the conference call. SNC committed to implement immediate

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compensatory measures for _ Unit 1 by establishing more restrictive

administrative controls over primary coolant specific activity. These

administrative controls would limit the specific activity of primary-

! coolant to.0.15-microcurie per gram dose equivalent I.-131 (DEI) for

steady-state conditions and to 9 microcurie 3er gram DEI for transient

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conditions. The new limits are one-half of t1e limits specified by

^TS 3.4~.9. Specific Activity. On the following day, the inspectors

verified' that the NOB contained an entry regarding the new

administrative . limit for' primary coolant specific activity, The

inspectors also interviewed the Unit 1 day-shift SS- regarding his

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-knowledge of--the new DEI-limits. The inspectors also verified that all *

oncoming Unit 1 and 2 licensed operator crews were-subsequently briefed

on the new administrative limits prior to assuming on-shift duties.-

SNC's. commitment:to implement the more restrictive administrative limits

did not apply to Unit-2 until November 1.1997.

By letter dated September 17. SNC-submitted a license amendment for

UnitsEl and 2 to revise TS-3.4.9 to make it consistent with the more

restrictive' administrative limits for primary coolant specific activity.

II. Maintenance-

M1 Conduct of Maintenance

'M1.1- General Comments

x a. -Insoection Scone (IP 61726 and IP 62707)

Inspectors observed and reviewed portions of various licensee corrective

and preventive maintenance activities, and witnessed routine

surveillance testing to determine-conformance with plant procedures,

work instructions, industry codes and standards. TSs. and regulatory-

requirements. The inspectors observed all or portions of the following

maintenance and surveillance activities, as identified by their

-associated work order (W0), work authorization (WA), or surveillance

test procedure (STP):

e FNP-2-STP-80.1 2B EDG Operability Test. Revision 24

e FNP-1-SOP-7.0A

- Residual Heat Removal System

o FNP-1-SOP-7.0 Residual Heat Removal System

.e W0#S00079791 Perform DCP S96-2-9060 on U2 R11/12

e FNP-1-STP-201.18 Reactor Coolant System TE-412A-and TE-4120 Loop

Calibration and Functional Test. Revision 39

e FNP-2-STP-256.4 Pressurizer Pressure Sensor. Response Time Test.

Revision 5

e W0#M97006793 1B Emergency Air Compressor

e W0#00487300

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Calibrate Train B Differential Pressure

Transmitter per FNP-1-IMP-218.2. Control Room

Differential Pressure PDT-2768B. Revision 8

e FNP-1-STP-226.1 BIG Sequencer Operability Test Revision 6

e WA# WOO 482489- -1B Auxiliary Build _ing Battery-Equalization per

FNP-1-EMP-1341.08. Revision 3

e FNP-1-STP-11.2 1B RHR-Pump Quarterly Inservice Test. Revision

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e WA#W00483S49~ Preventative maintenance task on 2A Boric Acid

Tank temperature indication and alarm

b. Observations. Findinos and Conclusions

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.All observed maintenance work and surveillance testing was-performed in

accordance with work instructions procedures, and applicable clearance

controls. In general, safety-related maintenance and surveillance

1 testing evolutions were well-planned and execut: d. Responsible

l, personnel demonstrated familiarity.with administrative;and radiological

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controls. Surveillance tests of safety-related equipment were.

consistently performed in a deliberate step-by-step manner by personnel

in close communication with the Main Control Room (MCR). Overall,

operators, technicians, and craftsman were observed to be knowledgeable,

experienced, and well trained for the tasks performed.

M1.2 Reolacement of Unit 2 Pressurizer Pressure Transmitter

a. Insoection Scone (IP 62707 and IP 61726)

The inspectors observed maintenance and surveillance activities

associated with the replacement of 02B31PT456. Pressurizer Pressure

Channel 2. Specific activities included observation of time response

testing and calibration of the new transmitter, observation of various

pre-job briefings, reviews of completed test and calibration data

sheets, and an-at-power containment entry to observe installation of the

new transmitter. The inspectors reviewed FNP-2-STP-256.4. " Pressurizer

Pressure Sensor Response Time Test." Revision 5. FNP-0-IMP-430.16.

" Environmentally Qualified Instrument Replacement Procedure."

Revision 11'. FNP-2-STP-201.5. " Pressurizer Pressure PT-456." Rev. 22.-

Updated Final Safety Analysis Report (UFSAR) Section 15.4. " Condition IV

- Limiting Faults." UFSAR Section 7.2. " Reactor Trip System."

Westinghouse WCAP-13632. " Elimination of Pressure Sensor Response Time

Testing Requirements." Rev. 2. Electric Power Research Institute (EPRI)

' Report NP-7243. " Investigation of Response Time Testing Requirements."

and TS 3.3.1 requirements for reactor trip system instrumentation.

b. Observations and Findinas

On September 17.1997. PT456 drifted up approximately 10 pounds per

square inch gauge (psig) over an 8-hour period. On Seatember 23. PT456

failed a channel check and was declared inoperable. T1e licensee

initiated an LC0 and placed Channel II in trip within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, per

TS 3.3.1. Action 7. Occurrence Report (OR) 2-97-361 was generated to

document the failure.

Work order #97006926 was issued for re)lacement of PT456. On

September 24. the inspector observed t1e calibration and response time

testing (RTT) of the replacement Barton Model 763 pressure transmitter.

The calibration was performed in accordance with plant procedures with

no discrepancies.

While the calibration and RTT were being performed. the licensee

discovered that the replacement transmitter was not environmentally

- qualified (E0) even though it had been issued as E0. This was

identified by Quality Control (OC) personnel while answering questions

Josed by maintenance concerning E0 splices for the transmitter pigtails.

Juring the discussions, the QC supervisor recognized that the

transmitter was not E0 based on the purchase order number. Maintenance

was immediately notified that the transmitter was not E0 and to suspend

work. The licensee generated OR 2-97-369 to document the deficiency.

The licensee did not have any more Barton Model 763 transmitters in

stock but was able to locate several at another plant and arranged to

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have two transmitters shipped. However, on October 2. due to'

-complications with documentation and span differences, the licensee

decided to install a Foxboro transmitter (Model NEll) the same.as

installed on Unit-1.

The Foxboro transmitter was-installed under Design Change Package (DCP)

S-97-2 9276. The physical changeout of the original Barton transmitter

only required changing the mounting bracket and rerouting the sensing

line. The inspectors reviewed the DCP and determined that it adequately

addressed the mechanical aspects of the modification. Westinghouse

Electric Corporation provided SNC an evaluation comparing the Foxboro

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and Barton transmitters which concluded that'the performance of the two

transmitters was the same with respect to the uncertainty calculations.

However, the DCP and associated technical evaluation worksheet, did not

address possible response ramp rate differences between the Foxboro and

Barton transmitters.

The inspectors observed the calibration and RTT of the Foxboro  ;

transmitter. The calibration was completed again with no discrepancies.

The transmitter response time was determined to be within the specified

limit of 0.23 seconds.

Technicians identified a problem while installing the transmitter on the

manufacturer-provided seismic mounting plate. The 3/8-inch Grade 5

bolts supplied with the mounting plate were too long. Therefore, the

maintenance staff shortened and rethreaded the bolts. When the

technicians attempted to torque one of the bolts, the threads stripped.

The licensee initiated OR 2-97-378 to document the event. The licensee

determined that the bolt failed due to poor workmanshi) when rethreading

the bolt. The licensee replaced the provided Grade 5 Solts with-

Grade B7 bolts. The inspectors concluded that this was adequate.

An inspector accompanied licensee personnel during the at-power entry

into Unit 2 Containment on October 3.1997, to observe installation of

the Foxboro transmitter. Inspectors attended the pre-job briefing and

ALARA briefings for Radiation Work Permit (RWP) 2-97-2490. The

briefings were comprehensive and com The containment entry was

conducted in a professional manner. plete.team demonstrated

The entry

teamwork and ex)editiously completed the assigned tasks. in tight

l quarters and a lostile environment. However, one problem arose due to

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not energizing electrical outlets in the work area prior to the entry.

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-The local portable air samples were unable to be collected. This pre-

planning issue was discussed with the on-shift SS.

The ins)ectors subsecuently reviewed the Foxboro and Barton RTT data.

! UFSAR Clapter 15. anc background documentation. The inspectors

l identified an issue affecting the adequacy of the test procedure to

accurately measure the sensor response time. Accurately measuring

sensor response time is required to ensure that the total Reactor Trip

System (RTS) response time is less than the 2 seconds assumed in the

accident analysis. The RTS response time was defined in the background

documentation and licensee submittal as "...the time interval from when

the monitored parameter exceeds its trip setpoint at the channel sensor

Luntil loss of stationary gripper coil voltage."

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Enclosure 2

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The TS currently requires periodic time response testing of the RTS from

the output of the transmitters to the loss of stationary gripper coils.

The response time portion for the sensor is measured prior to installing

a new transmitter or after significant repairs to a transmitter. The

current limit-of 0.23 seconds for the transmitter was based on the

slowest response' time of a pressure transmitter determined through a

historical record search of FNP-transmitter respoilse times.

While reviewing the response time traces. the inspectors noted that

while the reference pressure transmitter was responding to the set ramp

rate of approximately 540 sig/sec, the Foxboro was only capable of--

responding at approximate 1 300 psig/sec. This difference in response

rate could be significant ecause the RTT procedure specified measuring

the response time for only a 40 psig 3ressure drop whereas the actual

pressure dro) during an accident is a)out 400 psig from normal operating

pressure (NO3) to the low pressure trip setpoint. If the transmitter

was able to respond at the tested ramp rate the test could adequately

measure the sensor response time. However, due to the transmitter's

slower response rate and the small 40 psig pressure drop. current RTT

does not accurately or conservatively measure sensor response time for

high ramp rates.

The inspectors also reviewed the ex)ected Reactor Coolant System (RCS)

pressure ramp rate for large break oss of Coolant Accidents (LOCAs) as

identified in Section 15.4 of the UFSAR. Figures 15.4-3A through -3E

indicated that core pressure dro)s to 1600 asig in less than 0.5

seconds. This ramp rate was muc1 greater tlan even the tested 540

psig/second. The inspectors determined that, based on an actual

response rate of 300 psig/second the Foxboro transmitter could have a

real response time of approximately 1 second for the expected transient.

This is greater than the 0.23 seconds accounted for in the licensee *s

reactor. protection system (RPS) response time equations.

This issue was discussed in detail with licensee management on

October 8. On October 10. the licensee 3rovided the inspectors with the

test data Jackages for the most recent R)S and engineering safety

features (ESF) response time testing. The test data showed that, even

if I second was added to account for the slow response time of the

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Foxboro transmitter, the RPS'and ESF time response would be within the

required limits. Also, the licensee identified that the accident

analysis for large break LOCAs did not depend on the control rod

insertion to shutdown the reactor. The accident analysis determined

that the reactor would be shutdown due to voiding and loss of moderator.

and would remain shutdown due to the injection of borated water from the

Refueling Water Storage Tank-(RWST) and cold leg accumulators. The

accident analysis information along with the current test data

alleviated the immediate safety significance of this issue.

Enclosure 2

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c. Conclusions

Maintenance and support activities associated with the replacement of

PT456 were generally well-controlled, and performed by competent and

experienced personnel. However, a non-E0 instrt. ment was inappropriately

issued for an E0 application and a re-threaded bolt failed due to poor

workmanship. Also, a technical issue concerning RTT and the capability

of Foxboro pressure transmitters to respond to high ramp rates was

identified. Due to the generic 1mplications of this issue, further

review will be cordacted by the NRC. This is identified as IFI 50-

364/97-11 01: RPS Response Time Testing.

M1.3 DCP S96-2-9060. Unit 2 R11/12 Containment Air Particulate and Gas

Radiation Moaitors (IP 62707 and P 37551)

The DCP was perfermed under WO S00079791 The purpose of the DCP was to

eliminate paper drive problems due to high flow rate through the paper

drive unit. The DCP accomplished this by bypassing approximately 40% of

the flow around the paper drive unit. The inspector reviewed the design

calculations (SJ-95-1024-001. Rev 0) and verified that Rll still met the

designed sensitivity with +.he reduced sample flow. The installation was

performed in accordante with the DCP. Craftsmanship was good. The

inspector verified that no new elbows of sharp bends were created which

could affect the sample flow.

H8 Miscellaneous Maintenance Issues (IP 92700 and IP 92902)

M8.1 (Closed) Licensee Event Reoort (LER) 50-364/97-03: Failure To Perform

Diesel Generator Surveillance Recuiremants Due To Procedural Inadecuacy

The licensee determined that the required 18-month surveillance of

TS 4.8.1.1.2.c.8 had not been performed on Unit 2 for EDG 1-2A. This

issue was discussed in Section M1.8 of IR 50 ^ 7. 364/97-05 and was

cited as an example of violation 50-348. 364 - 15-03.

The ins)ectors reviewed the Shared (Unit 1 and 2) Surveillance Schedule.

This scledule had a note for EDG 1-2A that instructed the Operations

group to ensure that the surveillance recu rements of procedure

FNP-0-STP-80.8. " Diesel Generator 1-2A 1000KW Load Rejection Test."

Rev. 10. were accomplished for each Unit.

. The inspectors were informed during discussions with licensee personnel

that procedure FNP-0-STP-80.8 was to be replaced with surveillance test

procedures FNP-1-STP-80.17 and FNP-2-STP-80.17. These procedures are

currently in draft and will enhance the licensee's corrective actions by

implementing unit-specific procedures for the 1-2A shared EDG.

Similarly, procedure FNP-0-STP-80.9 for the IC EDG was to be replaced

.with procedures FNP-1-STP-80.18 and FNP-2-STP-80-18.

Based upon the inspectors' review of documentation and the licensee's

'ctions this LER is closed.

Enclosure 2

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M8.2 (Closed) LER 50-348/97-05: Failure To Perform Nuclear Instrumentation

Surveillance Reauirements Prior To Mode 2 And 3 Entry

.-The licensee discovered that the reactor trip instrumentation

surveillance requirements of TS Table 4.3-1 were not met during a unit

shutdown on March 15, 1997. This issue was discussed in Section M1.8 of

IR 50 348, 364/97-05 and was an example of violation 50-348,

364/97-05 03.

The inspectors-reviewed the new maintenance surveillance test procedures

(Revision 0) for performing the nuclear instrumentation system (NIS)

source range channel level trip calibration and functional test. The

procedures are performed quarterly and ensure that the surveillance

requirement is met for functional testing while in mode 1. The

procedures are for source range channels N31 and N32 for both units.

The inspectors reviewed the licensee's Commitment Action Tracking

Licensing Information Processing System (CATLIPS). This system tracked

the licensee's corrective actions. Commitment #10172 of CATLIPS

documents the commitment to change the UFSAR to allow performing NIS

power range (PR) neutron flux low setpoint bistable calibration in

mode 1 to ensure that TS 4.3.1.1 surveillance requirements are met for

unit shutdowns.

The inspectors also reviewed the lessons learned training advisory

notice associated with the issues discussed in LER 50-348/97-05.

Based upon the inspectors * review of documentation and the licensee's

actions, this LER is closed.

M8.3 (Closed) Violation (VIO) 50-348. 364/97-05-03: Failure To Follow

Multiole TS Surveillance Reagjrements

The inspectors reviewed licensee corrective actions. Initial actions to

alleviate the adverse conditions satisfactorily addressed the immediate

issues. l.icensee Event Report 50-348/97-05. Failure To Perform Nuclear

Instrumentation Surveillance Requirements Prior To Mode 2 And 3 Entry.

documented the failtre to perform the quarterly functional tests and

shiftly channel checks for the NIS source range.(SR) and the NIS PR

channels low flux trip for mode 2. This LER was discussed and closed in

section M8.2 of this report. Licensee Event Report 50-364/97-03.

Failure to Perform Diesel Generator Surveillance Requirements Due to

Procedural Inadequacy, documented the missed surveillance associated

with not. conducting the 1-2A DG Load Rejection test for each individual

unit prior to taking surveillance credit. This LER was discussed and

closed in section M8.1 of this report. Selected u) dated Unit Operating

Procedures (UOPs) were reviewed and determined to lave been

appropriately revised. Additionally, the Shared (Unit 1 and 2)

Surveillance Schedule was reviewed and appropriate changes verified.

The inspector verified that training was provided to appropriate

personnel, concerning Code of Federal Regulations (CFR) 10 CFR 50.59

screening. Based on the licensee *s actions. this VIO is closed.

Enclosure 2

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M8.4 (Closed) liI 50-348. 364/96-09-04: CCW HX Ecoxy Coatino'and Broken Tubes

This item was opened to follow the performance of the epoxy coating

process used on the Component Cooling Water (CCW) heat exchangers (HXs)

and the-adequacy of the licensee's Nonconformance Disposition Reports

(NDR) in that the missing tube fragments would not impact the

operability of the CCW system.

The inspectors reviewed the' licensee's areventive maintenance (PM) tasks

for the CCW HXs and verified that a tas( was added to specifically

inspect the epoxy coating at 18-month intervals. The licensee inspected-

all three Unit 1 CCW HXs and one Unit 2 CCW HX after approximately three

to four months of onservice time. Some minor deficiencies were

identified and they were repaired prior to returning the HX to service.

The inspectors examined two of the HXs when they were opened for the

licensee's inspection. The coatings were intact with no signs of

separation from the base metal or erosion of material.

To assess the adequacy of the licensee's NDRs. the inspectors reviewed-

LERs written from January 1. 1997 to September 15. 1997. for instances

of foreign material probler's in the CCW system. The inspectors also

reviewed the documentation of licensee inspections of the CCW HXs and

interviewed the licensee personnel who conducted the inspections. No

issues involving foreign materials, i.e. tube fragments, were

identifled during the period reviewed. No further degradation of the

tubes, tube failures and fragmentation, were identified by the

licensee's subsequent inspections.

The inspectors concluded that the licensee's efforts to reduce erosion

of the CCW HXs tube sheets through epoxy coating were effective and the

coating was holding up well. The licensee's NDRs were accurate and

thorough as demonstrated by no instances of tube fragments impacting the

performance of the CCW system. The efforts to capture the broken and

severed tubes and establish " fences" to prevent tube fragment migration

were successful. Based on the inspectors review, this IFI is closed.

M8.5 (Closed) Inspector Followun item (IFI) 50-348. 364/96-13-03: Foreion

Material From Seal Injection System To Reactor Coolant Pumo (RCP) Seals

During the past Unit 2 refueling outage (U2RF11), very small pieces of

debris from the seal water injection filter 0-rings were discovered in

W e downstream seal water supply check valves. The inspectors reviewed

completed OR 2-96-325 and interviewed responsible personnel and

management. As part of their corrective actions, licensee maintenance

personnel inspected both seal injection filters, verified that existing

0-rings were in place, and lubricated the 0-rings per the vendor manual.

All three seal injection lines were subsequently flushed, with no

additional debris identified. Maintenance procedure FNP-0-MP-2.8.

' Replacement of Seal Injection Filters. Rev. O was written to ensure

proper installation of seal water injection filters, including 0-ring

Enclosure 2

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lubrication.- A 10 CFR E0.59 safety evaluation was also documented

regarding the potential introduction of foreign 0-ring material into the

reactor-coolant pump seals. This evaluation concluded that, due to the ,

size and constituency of the debris along with the torturous path of the-

RCP seal package, the likelihood of seal failure was minimal. This IFl

is closed.

M8.6 (Closed) LER 50-364/96-03: Steam Generator Tube Dearadation and Tube

Status

This LER was provided to satisfy TS 4.4.6.5.c which requires that steam

generator (SG) tube inspection results which fall into Category C-3

shall be considered a reportable event and reported ]ursuant to 10 CFR

50.73 prior to resumption of plant operation. The LER also served to

satisfy TS 4.4.6.5.a which requires that following each In-Service

Ins)ection (ISI) of SG tubes, the number of tubes plugged or repaired in

eac1 SG'shall be reported to the Commission within fif teen days of the

completion of the inspection, plugging, or repair effort. This LER is

closed.

M8.7 (Closed) VIO 50-348. 364/97-130 01014: Failure To Prescribe Document.ed

. nstructions For Procedures to Imolement Penetration Room Filtration

(PRF) Testina and Goeration

The inspectors reviewed the licensee's Commitment Action Tracking

Licensing Information Processing System (CATLIPS). Reply to the Notice

of Violation dated May 28, 1997. and procedures associated with the

applicable corrective actions. Twenty procedures were reviewed and

determined to have been appropriately revised in accordance with the

corrective action plan. Based on this review of the corrective actions

this VIO is closed.

III. Enaineerina

El Conduct of Engineering

E1.1. Unit 2 Rod Control Cluster Assemblies (RCCA) Full Withdrawn Rod Position

C!!Mlgt

a. Review Scone (IP 37551)

On September 19. a resident inspector observed Operations. Instrument

and Controls (I&C), and Engineering Support (ES) personnel im)lement

FNP-2-ETP-3607. RCCA Fully Withdrawn Repositioning At Power. Revision 0,

to fully withdraw the Unit 2 RCCAs from 225 steps to 226 steps,

b. Observations and Findinos

This infrequently performed evolution was briefed in accordance with

FNP-0-AP-92. Infrequently Performed Tests Or Evolutions. Revision 3. by

the Unit 1 Operations Superintendent. The procedure was well written

-and controlled by the ES test director. Operations personnel

implemented the procedure in a deliberate step-by-step manner under the

direct supervision of the ES test director and oversight of the

Enclosure 2

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0perations-Su)erintendent. The~ evolution went smoothly except that

annunciator F 5. COMP ALARM / ROD SE0/DEV. came into alerm and would not- ')

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clearo 1This condition was investigated and later explained to thel

inspector as an expected phenomenum when considering the pre existing }

- digital. rod position' indication--(DRPI) Data A Channel failure.of rod

-J09.

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c. Conclusions

The evolution was properly controlled and the reason for the annunicator ,

alarm was-adequately understood.

El.2E Generic i ztter (GL) 95-05 Reoortability and Safety Assessment

i

a. Review Scoce (IP 37551)

By-letter dated September 12.'1997. SNC addressed the reportability and

safety assessment requirements of GL-95-05. Section 6. The Materials

-and Chemical Engineering Branch of the Office of Nuclear Reactor- '

Regulation (NRR) reviewed SNC's letter using the criteria of GL 95-05.

Section 6. Specifically, the NRC staff reviewed SNC's safety

assessment compensatory measures, and reportability determination

(e.g. 10 CFR 50.72 or 50.73). .

b; Observations and Findinas

Voltage-based Steam Generator (SG) tube repair criteria was im)lemented

at Units 1 and 2. in accordance with GL 95-05. SNC evaluated tie affect

that recent SG tube leak and burst test results have on the End-of-cycle

.(EOC) conditional leakage and probability of burst calculations and

concluded that inclusion of the latest leak and burst test results

L caused Units 1 and 2 to reach the NRC staff notification limits of GL 95-05.

h ' GL 95-05 Section 6. Reporting Requirements, requires NRC staff

notification under certain conditions. One condition that requires NRC

staff notification occurs when a licensee determines that the E0C

accident' leakage will exceed the site-allowable leakage limit: another

occurs when a licensee determines the E0C conditional burst probability

exceeds 1 x 10. SNC calculated a limiting probability of burst-~to be

1.4 x 10' , which is below the NRC staff notification level. However,

when SNC incorporated the leak and burst test results from the recent

L -Unit 1 and 2. tube )ulls into the correlations used'as part of the GL 95-

-05 leakage and pro) ability of burst calculations, the projected E0C

. leakage from Unit 1 increased from 15.7 gpm to 20.4 gpm. This increase

i placed Unit -1 in-thelosition of having exceeded the =allcwable leakage-

'

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limit"of:13.7 gpm. . T1e revised E0C burst-probability was calculated to

be 1.2=x:10. -SNC also notified the staff that, with the most recent

! tube pull results-in the leakage and burst correlations the Unit 2 -

leakage was projected.to exceed the allowable leakage limit on November  ;

l: 6L 1997 : The probability of bg'rst value remained under the NRC

notification limit- at 3.2 x 10 .

Enclosure 2  :

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On September 12. 1997, SNC provided the NRC staff a " Generic letter

95-05 Safety Assessment" for Unit 1 in accordance with the requirements

of GL 95-05 Section 6. It was also part of a September 17. 1997.

license amendment request for Units 1 and-2; The license amendment -

involved the reduction in the specific activity limits of dose

equivalent l* (DEI) steady sta;e and transient values from 0.3

microcurie / gram to 0.15 microcurie / gram, and 18 micro curies / gram to 9

-micro curies / gram, respectively. The DEI level reductions effectively

increase the maximum allowable accident leakage limit associated with

voltage based repair criteria from 13.7 gpm to 23.8 gpm (room

temperature conditions).

The staff reviewed the licensee's assessment against the criteria in

Section 6 of GL 95-05. Specifically. the review included SNC's

assessment of the safety significance, com)ensatory measures taken, and

actions with respect to reportability of t1e event.

SNC's assessment cf the safety significance of the increased EOC -

accident leakage was based on the actual plant steady state value of DEI

(less than 0.01 microcurie / gram). Using actual plant conditions, SNC

concluded that the radiological ex)osure from SG tube leakage in the

event of a main steam line break (iSLB) would not have exceeded the

licensing basis. However, the licensee failed to explicitly address the

radiological consequences of a MSLB assessed in two ways: (1) assuming

a preexist;ng iodine spike and (2) assuming an accioent-initiated iodine

spike. Since the licensee implicitly addressed both cases when the

licensee changed its administrative limits for both steady state and

transient values of DEI, the staff concurred with SNC's safety

assessment with respect.to leakage. Regarding the increased burst

probability. SNC citeg' operator action and engineering judgement to

conclude the 1.2 x 10 burst probobility was not safety-significant.

The staff concurred with SNC's conclusion.

SNC evaluated the reportability of the revised leakage and burst

probability numbers and determined the reportability of the issue was

covered by the requirements of Gl. 95-05 and no other reportability

requirements (e.g. , 50.72 or 50.73) ap)1ied. The staff reviewed the

reporting requirements and concluded tlat SNC has complied with the

requirements of Technical Specification 3.4.6 by having followed the

applicable reporting requirements outlined in Section 6 of GL 95-05.

4

c. Conchsiqos

The NRC staff'found SNC's " Generic Letter 95-05 Safety Assessment" in

res)onse to.the GL 95-05 requirements to be adequate. With respect to

leacage, the actual plant conditions combined with the administrative

limits established by SNC appear to ensure E0C accident leakage will not

result in radiological exposures exceeding regulatory limits. With

respect to conditional burst probability. the staff concludes the small

-increase is not safety-significant, The licensee's compensatory actions

were appropriate, and the reporting requirements appear to have been

adequately addressed.

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Enclosure 2

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E1.3 FWS Discharoe Pine Corrcsion (IP 37551)

In response to inspector concerns regarding excessive SWS pipe corrosion

(see report section 02.1), the licensee initiated W0s #S97006667 and

  1. S97006668 to clean the Unit 1 and 2 SWS pipe and conduct nondestructive

examinations. Under the cognizance of ES engineers, plant personnel

performed ultrasonic testing (UT) of the affected SWS piping. The UT

results. including pit depth measurements, were then transmitted to

corporate engineering. Southern Company Services (SCS), for review as a

Request for Engineering Assistance (REA) 97-1557. In particular. SCS

was requested to calculate the minimum acceptable wall thickness.

Inspectors observed evidence of the SWS pipe cleaning. UT. and

subsequent priming of the external piping surface. An inspector also

reviewed the UT data recorded in the W0s, and reviewed the SCS reply to

REA 97-1557. The average UT )ipe wall thickness readings were ty)ically

0.51 inches, with a wall thic(ness of as low as 0.390 inches in tie

corroded areas. As noted in the original piping specification, this

piping was purchased for a minimum thickness of 0.428 inches. The

licensee concluded that the dee)est pit was approximately 0.125 inches

deep. Subsequent calculations )y SCS concluded the minimum allowed wall

thickness was 0.229 inches. Consequently, the existing SWS pipe

condition was acceptable. Overall, licensee response to the identified

SWS pipe corroded conditions was prompt and effective.

E8 Hiscellaneous Engineering 1ssues (92903)

E8.1 (Onen) IFI 50-348. 364/97-10-02: UFSAR Reverification Corrective Actions

a. Inspection Scoce

The inspectors selected 18 of the 868 UFSAR discrepancies for followup.

During this report period item #089 concerning the capacity of the EDG

air start systems was reviewed. An inspector reviewed the documented

response to the discrepancy. licensee calculations. UFSAR Sections 8.3

(Onsite Power Systems) and 9.5.6 (Diesel Generator Starting System). NRC

Standard Review Plan (SRP) 9.5.6. Rev. 1. and pre-startup EDG test data.

The review of the calculations was limited to the air starting

requirements for the Colt-Pielstic PC2 EDGs.

b. Observations and Findinas

The concern as stated in the UFSAR Verification database was: "The

statement that the accumulators have the capacity for five air starts

should be investigated to its origin in order to establish if it is a

design requirement which has been satisfied or if it is a one-time or

periodic testing requirement."

The licensee's closecut response to the questien was that this was a

design requirement and that based on calculations "no explicit testing

of this requirement and revision to the UFSAR" was necessary. The

inspector requested copies of the design calculations SM-90-1779-001.

" Diesel Generator - Air Start System." Rev.1. and SM-90-1779-02. " Air

Start System leakage Rate." Rev. 1. for review. These calculations were

performed in 1992 and 1993.

Enclosure 2

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The inspector reviewed the above calculations. including the licensee

assumptions. The. inspector also performed inde)endent calculations

_using the licensee's assumptions and formulas. )ut with the actual

pressure drop' observed by the inspector during routine EDG surveillance.

starts, to validate the licensee's-methodology. The inspector also-

compared the licensee's results to original CDG startup test data. The

' inspector determined the licensee's calculational methodology was non-

conservative. The licensee had failed to compare their methodology

against data from original EDG startup tests, specifically performed to

validate the design cf the air start system receiver capacity, nor did

the licensee's calculations reflect actual EDG surveillance data. The

inspector concluded that the licensee's response to the UFSAR

discrepancy lacked thoroughness in that the licensee's review failed to

recognize the existence of actual startup test data or use pressure ,

drops observed during routine surveillance testing.

The inspector also concluded that the startup test data demonstrated

that the EDGs were capable of five sequential starts from one receiver

without recharge. In response to the inspector's comments. the licensee

revised their resolution of item #089 to document existence of the

startup tests.

l While researching the above issues the inspectors identified another

!

UFSAR discrepancy. UFSAR section 8.3.1.1.7.2. Response to Design Basis

Events, states that the maximum required loads will not exceed the

continuous rating of any of the four design. basis diesel generators.

This statement was not accurate in that current design basis load for

the 1C EDG exceeds the continuous rating but is less than the 2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />

rating. The inspectors have reviewed the loading of the 1C EDG

previously and determined that exceeding the continuous rating was

acceptable because the licensee's TS surveillance tests the 1C EDG to

the 2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> rating. This UFSAR discrepancy was identified to the

licensee for correction.

c, Conclusions ,

i

The licensee resolution of UFSAR discrepancy #089 was not thorough or

complete. Calculations supporting the design of the air start system

l- were non-conservative and were not validated against existing test data.

L However, the inspector verified that startup test data demonstrated the

l

air start system was adequately sized. i

l

This IFI remains open pending additional review of the UFSAR ,

- reverification corrective actions. i

! E8.2 FClosed) IFI S0-348.'364/96-13-07: Certain Hiah Enerav Line Break (HELB) l

solation Sensors Not Described In UFSAR l

l- This-NRC identified UFSAR discrepancy was originally entered into  !

i CATLIPS for tracking as commitment #10253. However. as part of the

L u) coming conversion to the Improved Standard TS (ISTS). TS 3.3.3.7 for

i "ligh Energy Line Break Isolation Sensors" is to be removed and

l relocated to the UFSAR. Consequently, the licensee has closed CATLIPS

Enclosure 2

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commitment #10253 and opened item #506 in the ISTS conversion action

item database to track this UFSAR discrepancy. An inspector reviewed

item #506 of thc-ISTS conversion database. Since this item will be

-include'J in the ISTS revf ew, this IFI is considered closed.

E8.3 LClased) VIO 50-364/96-155-01014: Ste m. Genera, tor Tube Flaws With F*

Distance

"

Closeout M this V10 was previously documented in Section M8.1 of NRC

IR 50-348. 364/96-09.

E8.4 (Closed) Unreso'ved item 50-348(364)l37-201-01: Unorotected CST

Connections

On October 21, 1994. during the safety system self-assessment (SSSA) of

the auxiliary feedwoter (AFW) system, the licensee discovered that a

. number of piping and transmitter tubing connections to the Unit 1 and

Unit 2 Condensate Storage Tanks were not provided with missile

protection as described in the UFSAR. Section 9.2.6.6 of the UFSAR

stated that the lower 12 feet of the CST was designed to withstand any

rupture caused by missiles. To resolve this issue, the licensee issued

Incident Report 1-94-299. Licensee Event Report (LER) 94-005-00, and an

UFSAR change and associated 10 CFR 50.59 Safety Evaluation. The

inspectors noted that the licensee's LER (94-005-00) and the subject

Safety Evaluation had been reviewed previously by NRC as documented by

NRC Reports 95 20 and 96-07. respectively.

The licensee's corrective action involved issuing a change to the UFSAR

to reflect the as-built configuration of the CST piping without the

tornado missile arotection. The 10 CFR 50.59 Safety Evaluation of the

proposed UFSAR c1ange was completed on November 17. 1994. The 10 CFR

50.59 Safety Evaluation included a question (question number 6) asking.

"May the proposed activity create the possibility of a malfunction of

equipment important to safety of a different type than any previously

evaluated in the UFSAR?" The licensee answered this question "No."

However, the inspectors noted that as a result of this condition. a

tornado missile could damage some CST connections, thereby resulting in

a loss of inventory from the safety-related tank and affecting the

operability of the entire AFW system.

A 3robablistic risk analysis was pre)ared and documented in Calculation

REES-F-94-014 which indicated that t1e impact frequency with which a

tornado missile could strike exposed CST piping was on the order of

1.0 x 108 per year. The safety evaluation for the UFSAR change

compared the calculated impact frequency with which a tornado missile

could strike exposed CST piping (approximately 1.0 x 10~8 per year) to

the probability of occurrence ~of a design basis external event

-(approximately 1 x 10 per year) and concluded that this postulated

tornado event was-not required to be analyzed as an " accident" in the

UFSAR. The UFSAR was subsequently revised to include the PRA results

and to delete the requirement for missile protection of the subject CST

con 9ections-. However, the inspectors concluded that the comparison was

not an appropriate justification to determine that an unreviewed safety

Enclosure 2

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question-(US0) did not exist when the as-built )lant-configuration did

not conform to the configuration-described in t1e UFSAR.

In a letter to NRC dated July 11. 1997. the licensee committed to

provide missile protection for the subject connections by March 15,

1998 The insSector found that the licensee had developed and issued

DesihnChange)ackages(DCPs) 97-1-9172 and 97-2-9173 to add tornado

missile protective structures to CST connections in the lower 12' of

the tank The CST connections identified in the DCP to be tornado

missile protected were tank drain, vacuum degasifier tank connection,

and level transmitters with associated electrical conduit.

10 CFR 50.59 allows licensees to make changes to the facility as

described in the safety analysis report, without prior Commission

approval unless the proposed change, involves a change in the

technical specifications or an unreviewed safety question. The NRC has

reviewed the circumstances related to this issue and determined that a

USQ did exist; however, as described in the cover letter to this

report, the NRC is exercising enforcement discretion to not cite the

violation in accordance with Section VII.B.6 of the Enforcement Policy.

This unresolved item is closed.

E8.5 fClosed) URI 348.364/97-201-02: Tornado Protection of CST Level

. nstrumentation

UFSAR Sections 3.2.1.5 and 9.2.6.1 and Table 3.2-1 state that the AFW

system instrument and control (l&C) system equi 3 ment and CST equipment

were classified as Category I., respectively. U:SAR Section 3.5.4

states that Category I equipment and piping outside containment are

either housed in Category I structures or buried underground. However,

durir.g the walkdown of the Unit 1 CST. the inspectors observed that the

safety-related CST level transmitters and enclosures, as well as the

associated cables and conduits.'were outside, and routed above ground

around the tank perimeter without missile protection.

In a letter to NRC dated July 11, 1997, the licensee committed to

provide missile protection for the CST level transmitters and

associated conduits by March 15, 1998. As stated earlier, the licensee

had isseed'0 cps 97-1-9172 and 97-2-9173 to install missile protection

at both the Unit 1 and Unit 2 CSTs. The inspector verified that these

instruments were included in the scope of the DCPs.

This unresolved item is dis p itioned with URI 97-201-01, as described

in E8.4 and is now closed.

E8.6 -(Closed) URI 50-348.254/97 201-03: AFW Check Valve Reverse Flow Testina

The ins)ectors identified that TDAFW pump discharge check valves V003

or-V002L F and H wers nct included in the IST program for a reverse

flow valve closure test es required by the ASME Code. The licensee

agreed that either check valve V003 or check valves V0020. F and H were

required to close in order to perform the required safety function.

The licensee issued OR 1-97-048 on March 3. 1997, to assure that

required corrective actions were implemented in a timely manner. The

Enclosure 2

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licensee revised the Unit l' and -2.IST Plans. FNP-1-M 46 and FNP-2-M-071-

to require reverse flow testing of TDAFW check. valves V002D -F and.He .

every refueling outage. The.IST Program was also revised to identify

Lthat these valves have a safety function in the open and closed

position.

1

Surveillance Test Procedure FNP-1-STP-22:29. " Turbine Driven Auxiliary

- Feedwater Check Valve Reverse Flow Closure Operability Test." Revision 7

-

,

10; dated April 18, 1997, was issued to implement reverse flow testing - ,

on the subject valves for Unit 1. The 3rocedure was implemented on-

Unit 1 and satisfactorily completed on iay 21, 1997.  ;

In a letter to'NRC dated July 11. 1997, the licensee indicated that all- .

corrective actions had been completed including issuance of procedures .

1

-to perform the required testing. This response was in error in that: ~

-the Unit-2 procedure was not issued until September 12, 1997. The

inspector found that the scheduled date of completion-for-issuance of

-the Unit 2 Surveillance Procedure was in accordance with the corrective-

- action described in Occurrence Report 1-97-048 and the Open Commitment-

Tracking Report dated September 15. 1997. In accordance with these

documents, the Unit 2 Surveillance Test-Procedure FNP-2-STP-22.29 was

L scheduled to be issued and comaleted satisfactorily prior to Unit 2

Startup from refueling outage RF12 which is scheduled for Spring 1998.

. The licensee informed the inspector'of this discrepancy and-indicated  :

'

that a revised submittal would be provided if necessary to clarify the

procedure' status. The inspector concluded that based on review of the

Occurrence Report and the Commitment Tracking database that the

,

'

corrective actions were being properly tracked and completed and no .

additional response on this item would be required. *

The ins)ector concluded that the failure to reverse flow test either

TDAFW cleck valve V003 or check valves V0020. F and H as required by

the ASME Code was a violation of TS Section 4.0.5 which requires

inservice testing of ASME Code classes 1. 2 and 3 pumps and valves in

o -accordance with Section XI of the ASME Boiler and Pressure Vessel Code .

-

and applicable Addenda. This is identified as Violation 50-348.364/97-

11-02. Failure to Perform Adequate IST of TDAFW Check Valves on-

Cessation or Reversal of Flow.

The unresolved item is closed. .

- E8 J (Ciosed) URI 348.364/97-201-04
AFW Check Valve Forward Flow Testina

'

The inspectors reviewed Surveillance Test Procedure FNP-1-STP-22.13.

'

<

" Turbine Driven Auxiliary Feedwater Pump Check Valves Flow

Verification." Revision .14. dated May 7.1996. The insoectors noted

~

that because' of the testing lineup with the minimum recirculation flow

path open the-flow through TDAFW check valve V003 would be on the order

'

of 530 gpm when the pump was operated at.625 gpm. The; team concluded

'

that the acceptance criteria of' 625-gpm in Section 2.2 of FNP-1(2)-STP- -

22.13 was not consistent with the actual-test flow. The licensee

Lagreed with the finding and issued Temporary Change Notice (TCN) .14A

_

and 12A to, revise procedures FNP-1(2)-STP-22.13.'

'

Enclosure 2

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The licensee's correspondence dated July 11, 1997. stated that

procederes have been revised to reflect current acceptance criteria and-

a review of Other orocedures was in progress. The ins)ector reviewed

Surveillance Test 3rocedures FNP-1(2)-STP-22.13 dated rebruary 28.

1997. and verified that they had been properly revised to reflect the

correct acceptance criteria for. full flow testing of check valves

01N23V003 and 02N23V003. The acceptance criteria for total flow i

-through the valve was changed to 450 gpm and the flow was being

measured down stream of the minimum recirculation flow path at flow

indicator FI-3229.

"

The failure to have adequate acceptance criteria in the surveillance

test procedure for verifying the forward flow for check valve V003 was

a-violation of 10 CFR 50 Appendix B. Criterion V. T;.ls is identified

as Violation 50-348.364/97-11-03. TDAFW Battery Installation and Check

Valve Test Deficiencies.

Based on the above the unresolved item is closed.

E8.8 (Closed) URI 50-348.364/97-201-05: TDAFW Pumo Battery Testina

The inspectors questioned the lack of service testing for the TDAFW UPS

Batteries to demonstrate the ability of the tattery to meet the design

duty cycle specified in the battery Design Basis Calculation 07597-E-

106. The inspectors did not have any immediate safety concern, since

the licensee's maintenance and testing provided reasonable assurance

that the battery could support the assigned load. The inspector

followed up on this item and concluded based on the review that a

failure to have a test program and procedures for service testing of

the TDAFW Class lE battery to ensure that the battery would meet the

required duty cycle was a violation of 10 CFR 50 Appendix B. Criterion

XI and TS Sectirn 6.8.1.a. This is identified as Violation 50-

348.364/97-11-04 Failure to Implement a Test Program for Service

Testing of the TDAFW Battery.

The licensee committed to aerform battery service testing during

refueling outage RF14 for Jnit 1 and RF12 for Unit 2 and to establish a

task to perform a service test every 18 months thereafter. The

architect engineer provided the licensee a draft procedure and safety

evaluation in Letter No. FP 97-0179 dated April 4. 1997. The Procedure

FNP-1-EMP-1352.04. " Turbine Driven Auxiliary Feedwater (TDAFW) UPS

-Battery Service Test." Revision 0 was issued on April 22, 1997. The

procedure was satisfactorily completed on Unit 1 on April 23. 1997.

The inspector reviewed the test results and the procedure and found

both to be acceptable. The battery test was a combined test to.

demonstrate that the as-found battery capacity was adequate to supply

calculated design basis accident load requirements for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and

station blackout load requirements for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The load profile

consisted of 70 amperes for the first minute followed by 53 am)eres for

the following.239 minutes. The acceptance criteria was that t1e

- battery terminal voltage remained greater than 42.6 volts dc after

being subjected to the service discharge test profile above.

This unresolved item is closed.

Enclosure 2

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E8.9 (Closed) URI 50-348.364/97-201-06: TDAFW Battery Installation

The inspectors reviewed the Unit 2 TDAFW battery installation and found

that various structural and electrical components were not installed in

accordance with the manufacturer's drawings and instructions. The

inspectors identified 6 specific deficiencies and 5 of those

deficiencies involved discrepancies between the battery installation

cod druings or procedures. The following deficiencies were noted:

e Five polystyrene s)acers were installed between the battery cell

and t1e end rail w1ere none were required.

  • Structural steel bracing in the rear of the rack did not agree

with the drawing.

  • Bolts were missing from the upper- and lower-tier tie rod

brackets.

e Silicon bronze bolting hardware was utilized at the cable

terminations in lieu of stainless steel hardware.

e The intercell battery connections were torqued to 75 in-lbs

instead of the required 125 in-lbs specified in the battery

manufacturer's instruction manual.

e The battery rack steel rails and tie rods exhibited corrosion.

The inspectors' review of these issues concluded that the failure to

install the Unit 2 TDAFW battery and rack in accordance with drawings.

procedures or instructions was a violation of 10 CFR 50 Appendix B.

Criterion V. This is identified as an example of Violation 50-

348.364/97-11-03. TDAFW Battery Installation and Check Valve Test

Deficiercies.

In licensee correspondence dated July 11. 1997, the licensee indicated

that the battery rack would be rebuilt per approved drawings and the

work would be completed by June 15, 1998.

The licensee issued REA 97-1408 to reconcile the differences between

the battery rack design and the installed configuration; and REA 97-

1444 to revise TDAFW battery maintenance procedures and appropriate

documentation to clarify acceptable fastener material. T1e licensee

received a response to REA 97-1408 in a letter dated July 31. 1997, and

indicated that the rack support frames had been installed 29 inches

apart instead of 25 inches apart as required by the drawings. The

recommended corrective action was to disassemble the rack and relocate

one of the sup) ort frames to within 25 inches of the other in

accordance wit 1 the design drawing. The response also included a

proposed work sequence to disassemble and reassemble the battery rack.

The licensee received a response to REA 97-1444 in Letter No. FP 97-

0396 dated July 31. 1997. Attached to this letter was a draft ABN

which provided information reflecting the acceptability of silicon

bronze or stainless steel fastener material for use on the Units 1 and

2 TDAFW UPS battery intercell and field cable connections.

Enclosure 2

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The licensee found that the maintenance procedures (for individual cell

replacement as well as periodic cleaning and inspection) specified

torque values that were less than recommended by the venuor. The

licensee evaluated this issue and determined that the torque values did

not affect the battery's safety function based on frequent periodic

battery maintenance and information received from the vendor that

indicated that acceptable connection resistance readings were

obtainable over a wide range of torque values. The licensee indicated

a review of torque values for all safety-related batteries was in

progress and the procedures would be revised appropriately. The

licensee indicated the specific TDAFW battery procedures would be

revised by June 15. 1998.

The licensee issued Deficiency Report #537766 to cleanup the battery

rack corrosion and install missing hardware. Tnis work was completed

on February 12, 1997.

The unresolved item is closed.

E8.10 (Closed) IFI 50-348/97-201-07: CST Level Alarm

The inspectors reviewed Calculation SM-87-4380-001, Revision 0 and

identified the following two concerns:

e The drift error for the sensor was not addressed in the

calculation.

e The total instrument tolerance calculated did not include the

deadband of 1% of span. (The inspectors found that it was not

clear from the design guidance document as to the circumstances

when to use deadband in uncertainty calculations.)

The inspector found that Calculation SM-87-1-4380-001 had been

superseded by Calculation SJ-97-1407-001 and Calculation SM-97-1407-

002. Calculation SM-97-1407-002. Condensate Storage Tank Low-Low Level

Alarm Setpoint Revision O. dated August 18. 1997, determined the

lowest allowable low-low level alarm setpoint on the Unit 1 and 2 CSTs.

The lowest allowable low-low level alarm setpoint was determined to be

1.456 feet from the bottom of the tank. However, to ensure adequate

margin, the licensee administratively set the low level alarm setpoint

at 5 feet - 3 inches or 63 inches. The administrative setpoint of 63

inches was used as an input into Calculation SJ-97-1407-001.

Calculation to Establish the Total Loop Uncertainty for Loops L-515 and

L-516. Revision 0. dated August 19, 1997. This calculation determined

the total loop tolerance for L-515 and L-516 and applied the loop

tolerance to the designated setpoint and process limit to verify that

all inaccuracies and allowances made would not ca$ e the alarm

initiation to fall outside safe process limits. The impector reviewed

Jortions of these calculations and verifled that sensor and rack drift

' lad been adequately addressed.

In regard to the issue on deadband, the licensee had revised the

Project Desk Instruction (PDI) 005.16. Process Instrumentation and

Control Setpoints, dated August 26, 1997, to clarify when the deadband

Enclosure 2

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component should be used in establishing 6cceptable setpoint tolerances

in uncertainty calculations. The inspector found the revision to PDI

005.16 clarifying when deadband should be considered to be acceptable.

This item is closed.

E8.11 (Ocen) URI 50-348.364/97-201-08: Tornado Protection of TDAFW Pumo Vent

Slak

.

The inspectors observed that the safety-related TDAFW pump vent stack

was installed on the roof of the Auxiliary Building and was not

protected from tornado generated missiles. UFSAR Section 3.5.4 states

that Category I equipment and piping outside containment are either

housed in Category I structures or buried underground. UFSAR Sections

6.5.1. 3.2.1.3. 3.2.1.5 and Table 3.2-1 state that AFW system equipment

and piping are Category 1. The ins)ectors noted that the requirements

of Criterion 111 and V of Appendix 3 to 10 CFR Part 50 were not met

because the installed condition of the TDAFW aump vent stack did not

conform to FNP design and licensing basis. T11s issue will remain open

pending additional NRC review.

E8.12 (00en) URI 50-348.364/97-201-09: Tornado Missi' Spectra

The inspectors observed that the safety-related emergency diesel

generators and the station blackout diesel generator exhaust silencers

for both units were installed on the roof of the diesel generator

building. The eaiament was judged to be protected ;M ust horizontal

generated missiles ay the b.ilding walls. However, a concern Nas

identified that the equipment was susceptible to vertical missiles and

other non-horizontal missiles. The licensee took the position that the

design basis for FNP was for horizontal missiles only. The issue was

left as an unresolved item pending further review by NRC to determine

if the tornado missile protection in the FNP design and lict ' sing bases

included missile spectra other than horizontal missiles. In a letter

to NRC dated May 28, 1997 the licensee provided additional information

to support its position on vertical missiles. This information was

being reviewed oy NRR and the' review is scheduled to be completed by

November 1997. This item will remain open pending completion of this

review.

E8.13 (Closed) IFl 50-348/97-201-10: CST Level Transmitter Freeze Protection

The inspectors identified three potential deficiencies with the

installation of the CST level transmitter 01P11LT516 and associated

freeze protection. In response to these concerns, the licensee issued

Work Orcors (WO) # 97001089. 97002478. and 97003706 to have maintenance

inspect and evaluate the adequacy of the heat tracing and islation

for level instruments 01P11LT515 and LTS16 and repair as required. All

work orders were completed on May 21, 1997. The inspector reviewed the

work history records to d-termine if the work was performed

satisfactorily and addressed the concerns. Based on this review, this

item is closed.

E8.14 (Closed) URI 50-348.364/97-201-11: AFW UFSAR Discreoancies 3

1

Enclosure 2

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The inspectors identified the following discrepancies between the

UFSAR as-built plant and design:

1. UFSAR Section 6.5.2.2.4 stated. "All valves in the AFW flow path

from the condensate storage tank to the steam generators were

normally open, with the exception of the fail open AFW flow-

control valves." This statement implied the AFW flow control

valves were not normally open. In accordance with the plant's ,

c)erating procedures, these valves were normally maintained in

t1e open position. The inspectors considered the UFSAR statement

was not correct.

2. UFSAR Section 3K.4.1.2.7, item F states the lowest safety-

related equipment in the main steam room is the atmospheric

relief valves at eltvation 133 ft. 3 inches. During the design

inspection aviit in February - March 1997, a walkdown identified

that the lowest safety-related components in the main steam valve

room were the Motor Driven A'ixiliary Feedwater (MDAFW) and

Turbine Driven Auxiliary Feedwater (TDAFW) discharge valves (HV-

3227A. B. C: HV-3228A B. C). The lowest solenoid valve was

located at elevation 131' - 0". Because thesc valves were

hated at a lower elevation than the atmospneric relief valves,

as stated in the above UFSAR statement, a concern existed

regarding the validity of the statement in the UFSAR that the

plant personnel would have approximately 4 additional hours to

isolate the turbine driven pump discharge through the feedwater

line break before water levels in the main steam room could

potentially ap3 roach the bottom of a safety-related component.

In addition, t1e inspectors observed that the limit switches

associated with the main steam isolation valves (MSIVs) were

located less than 1 foot above the floor, which was also below

the analyzed flood level.

3. DCP S-96-1-9008-0-001 replaced two - 3 amp fuses on the output of

TDAFW pump UPS rectified output with 5 amp fuses. However. UFSAR

section 8.3.3.2.C on page 8.3-41 still had references to 3 amp

fuses.

In response to items 1 and 2. the licensee issueri ABN 97-0-1074 to

revise the UFSAR. Design Calculation BM-97-1074-001. " Basis for time

in UFSAR Section 3K.4.1.2.7. Item F " was developed to support ABN 97-

0-1074 and document the design basis for the UFSAR statement regarding

time available to isolate the TDAFW pump flow through a feedwater line

break in the main steam valve room. The calculation results indicated

that the plant personnel would have approximately 3.18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> instead of

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> to isolate the turbine driven Jump discharge from the feedwater

line break before the water level in t1e main steam room reaches the

bottom of the safety related solenoid located at elevation 131'

UFSAR Section 6.5.2.2.4 was being revised to identify that the normal

position of the auxiliary feedwater control valves was open except

during auxilt ry feedwater system testing. In addition. -Section

6.5.2.3.3 wds being revised to reflect the normal position of the AFW

Enclosure 2

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flow control valves and their operation on an automatic pump start

signal.

The inspector found that the issue on fuse sizing had been previously

addressed by the licensee in ABN 93-0-0224. Revision 2. which was

issued in letter No. FP 95-0511 from Southern Company Services to

Southern Nuclear dated August 31, 1993. This ABN (93-0-0224) included

a revision to UFSAR Section 8.3.3.2.C to delete the fuse rating from

the UFSAR on the basis that fuse design was controlled by the fuse

manuals (Documents A 181987 and A-201987) and therefore, fuse rating

details need not be documented in the UFSAR. Attached to the ABN was a

50.59 Safety Evaluation, and UFSAR markups. The ins)ector reviewed the

UFSAR markup of the aroposed change and found it to 3e acceptable. The

ABN was approved by 31 ant Operations Review Committee (PORC) on

February 8. 1996. Based on these actions, item 3 is being

dispositioned in accordance with Enforcement Guidance Memorandum (EGM)

96 005 with no further action.

The inspector concluded that deficiencies 1 and 2 were examples of a

violation of 10 CFR 50.71(e). In accordance with the Enforcement

Policy, the failure to update the UFSAR normally would be categorized

as a Severity Level IV violation. However, at discussed in the cover

letter of this inspection report. enforcement discretion is being

exercised in accordance with Section Vll.B.3 of the Enforcement Policy.

The unresolved item is closed.

E8.15 (Ocen) URI 50-348.364/97-201-12: Stress Analysis Temoerature

This issue was identified to review the 'icensee's root cause

evaluation and corrective actions for the design deficiency documented

in Deficiency Notice (DN)97-001 involving incorrect dimensions and an

incorrect temperature utilized in the Com3onent Cooling Water (CCW)

piping stress calculations. The subject )N was generated to document

the as-found condition and initiate the corrective action process. The

DN stated that a Root Cause Evaluation Team (RCET) made up of SCS, SNC.

and BPC representation would be established to determine the root

cause: perform a review; and provide corrective action recommendations.

The .aspector found that this root cause evaluation was still in

progress. However, the corrective action to revise the Unit 1 and 2

CCW stress calculations had been completed. The licensee had issued

REA 97-1415 to revise the Unit 1 and 2 CCW Stress Calculations. A list

of the ind;vidual calculations as well as the criteria used to

determine if a calculation required revision were documented in DN 97-

001. Table A of DN 97-001 listed the CCW stress calculations for Units

1 and 2. The DN indicated in the notes whether a Change Notice had

been issued against a calculation or if the calculation was required to

be revised, Licensee letter No. FP 97-0394 dated July 31, 1997 which

was a final response from the design for REA 97-1415. inoicated that 30

CCW Stress calculations required revision as a result of this

deficiency. However, it indicated that additional calculations were

revised as part of the snubber reduction program for a total of 35

calculations that were revised.

Enclosure 2

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lhis item will remain open pending review of the results of the

licensee's root cause evaluation and proposed corrective actions.

E8.16 (Closed) URI 50-148.364/97 11 13: MOV Desinn Basis Differential

Pressure

The inspectors identified that the design basis differeritial pressures

identified in MOV Design Basis Document. U418109. Revision A for CCW

system containment isolation valves MOV 3046. 3052 and 3182 were non-

conservative as the effect of post-LOCA containment pressure was not

considered. These valves were located in the piping at penetration

numbers 42 and 14. which were the CCW supply to the RCPs and the CCW

return from the RCP oil coolers. UFSAR Table 6.2-31 identified these

penetrations as Type 11. UFSAR Section 6.2.4.1 defined Type 11

penetrations as serving those lines that connect directly to the

containment atmosphere. Therefore, the design basis differential

pressure for the containment isolation valves should have considered

the maximum post LOCA containment pressure that could exist when tlia

valves operate. The inspector concluded that the licensee's failure to

check and verify the adequacy of the design was a violation of 10 CFR

50 Appendix B Criterion 111. This is identified as an example of

Violation 50-348.364/97-11-05. Design Control Measures Did Not Ensure

that Calculations Were Verified and Controlled Ad?quately.

ABN 97-0-1098 was issued by the licensee on September 9. 1997, to

revise Units 1 and 2 MOV Design Basis Drawings. U418109 (Sheets 768.

78B. and 918) and U418110 (Sheets 618, 63B. and 76B). to incorporate

the new closing differential pressure values for the subject MOVs. The

ABN and associated 50.59 Safety Evaluation was reviewed and found to be

acceptable. The new c ksing differential pressure value for MOVs 3046

and 3182 was F psid and 52 psid for MOV 3052.

The unresolved item is closed.

E8.17 (Closed) IFl 50-3dL264/97-Il-J4. CCW Pomo Testina

Bechtel Calculation (41.4; BM-95-0776-001 "CCW System Evaluation Using

Degraded CCW Pump Curve." Revision 0 was performed under REA 95-0776.

This calculation documented the acceptability of the CCW system

performance with the pumas degraded approxiniately 10% from the vendor

test curves and stated tlat this degraded pump curve will be used for

comparina test data to verify the performance capability of the CCW

pumps. !he inspectors noted that the Inservice testing of the CCW

pumps was performed in accordance with procedure FNP-2-STP-23.1. "2A

Component Cooling Water Pump Quarterly inservice Test." Revision 14.

and similar )rocedures existad for the other two pumps. The inspectors

also noted tlat the CCW Functional System Description (FSD) and

procedure had not been revised to incor] orate the results of the above

calculation. An IFl was identified to review the revised IST procedure

and associated safety evaluation.

97-0-1080. Revision 0 and associated 10

Theinsb.ectorfoundthatABN

CFR 50. 9 Safety Evaluation )rovided for revising the UFSAR. CCW FSD.

SWS FSD, RHR FSD and CCW P&l)s to allow CCW pump opec 3tica with the

Enclosure 2

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minimum flow line isolated. This ABN revised affected documentation

based on using minimum analyzed CCW pump )erformance data for various

normal and accident configurations with tle minimum flow line open and

for operating the CCW pumps with the minimum flow line isolated. The

inspector reviewed the Component Cooling Water Functional System

Description. (A 181000). Revision 8 and observed that Revision 0 of ABN

97 0-1080 was incorporated into the FSD on July 8. 1997. The inspector

reviewed the lv CFR 50.59 Safety Evaluation for ABN 97-0-1080. Revision

1 and no unreviewed safety question was identified. This item is

closed.

E8.18 (Closed) URI 50-348.364/97 201-15: Post Modification Testina

This issue involved Design Change Package (DCP) 96 0-9012 2-006.

" Process Coating for CCW Heat Exchangers." which provided direction for

mndification of the CCW heat exchangers y application of an epoxy

coating (Plastocor) to the tubesheets, channel head, channel cover.

channel head shell relief line, approximately 12 inches into the

service water inlet and outlet lines, and 12 inches of the inlet end of

the tubes. The DCP, along with REA 96-1211. also provided direction

for plugging and stabilizing tubes. Procedure FNP 0-ETP-4418. "CCW

Heat Exchanger Epoxy Coating Application." Revision 1. implemented the

epoxy coating and Work Orders 96001476. 96001477, and 9600'.178 '

installed the stabilizing rods in the tubes. The inspectors noted that

neither the procedure used to apply the epoxy coating nor DCP 96-0-

9012-2-006 recuired post modification testing to ensure design flow

capability hac been maintained. The inspector concluded that the

concern that a flow test was required was based on engineering

,)udgement. The inspector could not identify any specific regulatory

requirements that would require flow testing. Therefore. this issue is

closed.

In a letter to NRC dated July 11. 1997. the licensee indicated that '

appropriate procedures would be revised by August 15. 1997, to

delineate post-mod testing requirements for maintenance replacement

design changes. The ins)ector reviewed Plant Modifications Procedure

FNP-0 PMP-100. " Design C'1ange Engineering Evaluation Preparation."

Revision 16 and noted that. It had been revised to delineate

requirements for post-modification testing for Maintenance Replacement

DCPs.

Enclosure 2

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E8.19 (Onen) IFl 50 348.364/97-201-16: Calculation Discrenancies

lhe inspectors identified several discrepancies in Calculation SC-96-

1211002. "CCW Heat Exchanger Maintenance Repairs * Revision 1. This

calculation documented the seismic and mechanical acceptability of the

modification. The deficiencies were noted in Sections 2.1. 2.3. 2.4.

and 2.5 of the calculation. The licensee issued REA 97 1407 to revise

the calculation. This item was identified to review the revised

calculation. The inspector followed up on this item and found that the

calculation had not been revised. However, in a letter to NRC dated

Juiv 11. 1997. the licensee committed to have the calculation revised

bytctober 15. 1997. This item will remain open pending issuance and

revi?w of the revised calculation.

E8.20.(L)osed)URI 50-348.364/97-201-17: Drawinn and Procedure Discrenanedgg

Procedures FNP-2 SOP 23.0A. " Component Cooling Water System." Revision

5: FNP-2-50P 2.lA. "themical and Volume Control System." Revision 8:

and FNP 2 SOP-1.lA. " Reactor Coolant System." Revision 6 were

checklists for the normal positions of valves and circuit breakers.

The inspectors identified numerous differences between the P&lDs for

the system (D-205002 Sheet 1. Revision 21: Sheet 2. Revision 10: and

Sheet 3. Revision 2) and procedures FNP-2-50P-23.0A and FNP-2-SOP 2.lA

concerning the existence of caps on vent and drain lines The

inspectors noted that item 5 of safety system self assessment (SSSA)

observation CCW-CM 01 was related to this item but was apparently not

corrected by the licensee. The SSSA observation was issued on April

19. 1990. The inspectors reviewed this issue and concluded that the

failure by the licensee to take corrective action for an identified

deficiency was a violation of 10 CFR 50 Appendix B. Criterion XVI.

This is identified as Violation 50 348.364/97-11-06. Failure to Take

Corrective Action for Difference Between CCW System Piping and

Instrument Drawings and System Operating Procedures.

Based on this action the unresolved item is closed.

E8.21 1 Closed) URI 50-348.364/97-201-18: CCW UFSAR Discrenancies

The inspectors identified the following discrepancies in the UFSAR:

1. Table 9.4-6A listed the room temperature for the Component

Cooling Pump Room at the beginning of the post-accident period as

119 degrees F whereas Table 3.11-1 indicated a design

temperature of 104 degrees F for the same room.

2. There are four relief valves (02P17V153. V154. V155. V158) on CCW

pipingbetweentheinboardandoutboardcontainmentisolation

vaives. These relief valves represent a release path to the

environment. However, these relief valves were not listed in

UFSAR Table 6.2-39 as containment isolation valves.

3. Table 9.3-1 did not ;nclude valve HV 2229, which was also a

safety-related, air-operated valve that received a safety

injection actuation signal (SlAS).

Enclosure 2

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. . _ _ _ _ _ -____ _ _ _ -

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4. Several differences existed between UFSAR Tables 9.2-6 and 9.2-7 <

and Tables T-1 through T 5 in the CCW FSD. for example. UFSAR

Table 9.2 6 listed the charging pump lube oil cooler fle as 20  ;

gpm and FSD Table T 2 lists this flow as 30 gpm.  ;

,

With the exception of item 1 above, the other deficiencies are

considered violations of 10 CFR 50.71(e) for failure to ensure that the

latest develo)ed material was included in the UFSAR. However. as .

discussed in E8.14 enforcement discretion is being exercised regarding i

these violations. In regard to item 1. the ins

item and concluded that no deficiency existed. pector reviewed this

This unresolved item is closed.

'

E8.22 (Closed) URI 50 348.364/97-201-19: TS Chance for Auxiliary Buildina

li10Cf1

Unit 1 and 2 Technical Specifications Section 4.8.2.3.2.c.5 for

Auxiliary Building battery service test specified a minimum cell

voltage requirement of 1.75 volts dc. Surveillance Procedures FNP-1-

STP-905.1 and FNP-2 STP 905.1. which perform the required service test

on the batteries s)ecified a minimum acceptable voltage at the end of ,

the service test w11ch was higher than that specified in the TS. The  ;

inspectors noted that the 10 CFR 50.59 Safety Evaluations performed for

PCN B-92 0-8099 and the changes to FNP-1(2)-STP 905.1 stated that TS

were not affected. However, these changes required battery terminal

voltages higher than those specified in 1S. ,

10 CFR 50.36(c)(3). Technical Specification. Surveillance Requirements,

states that surveillance requirements are related to test to assure

that the necessary quality of systems and components are maintained and

that the limiting conditions for operation will be met. The failure by

the licensee to identify a required TS change and to submit the

application for license amendment is identified as Violation 50-

348.364/97-11-07. Failure to Change TS for Auxiliary Building Battery.

In a letter to NRC dated July 11, 1997, the licensee committed to

submit a revised TS by December 31, 1997.

Based on this action the unresolved item is closed.

E8.23 (Closed) URI 50-348.364/97-201-20: Fire Barrier Penetration Seal

Documentation

The inspectors noted that silicone foam fire penetration seal 45-121-26

contained copper tubing, This configuration deviated from the tested

u configuration, and an engineering evaluation of the acceptability of

-the deviation had not been documented in accordance with UFSAR Section

98.2.2.5.3. Inspection Report 97-12 identified other concerns with the

as built configurations of silicone foam fire barrier penetration- l

seals. An inspector followup item was identified to review the

L licensee's evaluations of deviations from tested fire barrier

configurations. This issue is added as another example to be reviewed

as part of IFl 50 348.364/97-12 01. Review of Engineering Evaluations

-

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Enclosure 2

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to Establish the Fire Rating or Fire Resistant Capabilities of Fire  :

Rated Silicone foam Penetration Seals. Therefore, the unresolved item

is closed, t

E8.24 (Closed) URI 50 348.364/97 201-21: Electrical UFSAR Discrenancies ,

The inspectors identified the following discrepancies in the UFSAR: ,

1. UFSAR Section 8.3.1.1.3.A.2 stated that the unit auxiliary

transformer "B" megavolt ampere (MVA) rating at 65 degrees C was -.

47.99 instead of 46.7 as shown on drawing D 202706 t

2. Section 8.3.1.1.98 referred to Section 8.3.1.1.3 for interrupting

capacities for distribution panels. However, Section 8.3.1.1.3

did not include interrupting capacity data for distribution i

panels. >

3. Section 8.3.1.2 stated there were 21 600 V/208-V motor control

centers, however, the actual number of motor control centers

identified in the UFSAR totaled 19.

In regard to items 1 and 2 above. the inspector concluded that these

were additional violations of 10 CFR 50.71(e). However, as discussed

in E8.14. enforcement discretion is being exercised regarding these

violations. The inspector noted that item 3 had previously been

identified by the licensee's UFSAR Verification Program as item #070M.

A 50.59 safety evaluation. FVP-025 (B19500 Section 8), had been

prepared to revise the UFSAR. Included as part of the UFSAR change was

a markup of the UFSAR deleting the refersice to the quantity of load

centers. . The inspector reviewed the Safety Evaluation and UFSAR Markup

and found them to be acceptable, The inspector considered the

licensee's corrective action for item 3 to be adequate.

The unresolved item is closed.

E8.25 (Closed) URI 50-348.364/97-201-22: Control of Calculations

The inspectors identified that in several cases calculations that had

previously been superseded were not identified as such on the

calculation index: design basis calculations were not appropriately

revised to show the existing design condition; and affected

calculations were not-revised when new calculations were performed.

The inspector followed up on this issue and concluded that the

licensee's design control measures diri not ensure that calculations

were verified and controlled adequately. The failure to ensure

.

'

adequate design controls for calculations is identified as an example

l of violation 50-348,364/97-11-05. Design Control Measures Did Not

Ensure that Calculations Were Verified and Controlled Adequately.

Based on the above, the unresolved item is closed,

- Enclosure 2

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IV. Plant Supg r,t

R1 Radiological Protection and Chemistry Controls (IP 71750)

RI.1 Partial Entries into Contaminated Areas

An inspector observed a number of partial entries into contaminated

areas, in general, maintenance personnel were more conscientious than

operators in applying protective actions to prevent the inadvertent

spread of contamination during partial entt.es. The inspector observed

some examples of poor operator )ractices during partial entries. These

observations were discussed wit 1 Operations management.

R2 Status of Radiological Protection and Chemistry Controls Facilities and

Equipment (IP 71750)

R2.1 Radiolooically Controlled Area. Units 1 and 2

During tours of the radiologically controlled areas (RCA) of the

auxiliary building for Units 1. inspectors observed that overall

cleanliness and housekee)ing was good. Ongoing decontamination efforts

by the Health Physics (H3) department to reduce contaminated surface

areas continue to be successful. Floor spaces in the RHR pump rooms,

dnd Certain spent fuel o001 (SFP) cooling pump skids, have been

decontaminated due to HPs aggressive efforts. In concert with

decontamination efforts. HP has also redesigned catch devices to

minimize contamination and still control minor leaks.

R8 Miscellaneous RP&C (IP 92904)

R8.1 (Closed) IFl 50-348. 364/97-10-03: Review Licensee Evaluation for

Extended Onsite Storace of Contaminated Wet Resin

The licensee performed inspections of all the Sure)aks on September 9

and 19, 1997. The inspector observed the pre-job 3rief and portions of

the licensee's inspections of the Surepaks and steel liners containing

the contaminated wet resin. The inspections were thorough and

concentrated on the outer surface of the liners which were raised by a

crane for the inspection. The surface of the liners were acceptable

with only minor surface corrosion visible. The licensee also obtained

water samples of the water in the liner and the standing water in the

bottom of the Surepak for 3H analysis. This analysis indicated that

the water was of neutral pi and was not accelerating the minor-

corrosion observed. The licensee performed followup inspections on

October 16 and determined that the resins were not generating any

measurable quantities of gaseous products. The inspector reviewed the

licensee's )rocedure and schedule for periodically inspecting the

Surepak. T1e inspection data sheet required an inspection on a

quarterly basis. The licensee considers that these inspections will be

adequate to identify liner degradation before it becomes a problem.

This item is closed based on the licensee's actions.

Enclosure 2

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P1 Conduct of EP Activities (IP 71750)

>

Pl.1 Emernency Plan Drill

On September 10. 1997. resident inspectors and the NRR project manager

participated in an announced drill of the licensee's emergency plan.

As drill players. the inspecto-s considered the drill scenario

reasonably challenging. The Technical Support Center (TSC). Operations

Support Center (OSC) and Emergency Operations facility (EOF) were all

manned and fully operational in a timely manner. Durin9 the drill,

emergency respcnse personnel properly characterized evolving events and

made accurate and timely emergency classifications and notifications.

S1 Conduct of Security and Safeguards Activities (71750)

51.1 Routine Observations qi Plant Security Measures

During routine inspection activities inspectors verified that portions

of site security program plans were being properly implemented. This

was generally evidenced by: proper display of picture badges by plant

personnel: appropriate key carding of vital area doors: adequate

stationing / tours in the protected area by security personnel: proper

searching of packages / personnel at the primary access point and service

water intake structure: and adequate condition of security systems.

Security personnel activities observed during the inspection period

were performed acceptably. Site security systems remained functionally

adequate to ensure physical protection of the plant.

S3 Security and Safeguards Procedures and Documentation (IP 71750)

S3.1 Safenuards Material in The MCR Not Positively Controlled

On September 17. 1997, a resident inspector reviewed the following

safeguards documents located in the Unit 1 Shift Supervisor's (SSs)

l desk drawer in the at-the-controls (ATC) area of the Main Control Room

(MCR): a) Security Plan. Revision 32: b) Contingency Plan. Revision 7:

c) Contingency implementing Procedures, and d) Security Procedures.

the inspector verifjed that all these safeguards plans and procedures

were of the latest revision. However, the inspector identified the

following problems:

a) The folders containing the Contingency implementing Procedures

and Security Procedures were not marked as Safeguards Information

(SGI):

b) Access to the Unit 1 SS's desk was not positively controlled by a

lock nor constantly attended by the SS: and.

c) Although the MCR is an access-controlled vital area, access to

the MCR is not limited solely to those personnel authorized to

review SGl. Personnel not authorized to review SGI were

regularly granted access to the MCR. including the ATC area.

Enclosure 2

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The inspectors met with the Deputy Security Chief, and then with an

Operations Superintendent, to express concern that SGI located in the

MCR was not properly controlled to prevent access by unauthorized

personnel. All SGI was promptly removed from the MCR. placed in the

Central Alarm Station (CAS) which was required to be continually

staffed b security personnel, and properly marked as SGl. Inspectors

verified he licensee's corrective actions.

FNP 0-AP-72. Protection of Safeguards Information. Revision 9. Step

6.2.1. states "SGI is required to be under the control of an authorized

individual while in use to prevent unauthorized disclosure to persons

without a need to know. The requirement for control of SGI is met if

the matter is attended by an authorized individual even though the

information is not constantly being used." SGI in the MCR was not

being attended by an authorized individual during those aeriods every

day when the Unit 1 SS leaves his desk, and especially w1en both SSs

leave the ATC area. Step 9.1 of AP-72 also requires each document that

contains SGI to be positively marked in a precise manner, that was not

apparent on the SGI maintained in the MCR.

The provisions of AP-72 were consistent with the requirements of 10 CFR

73.21(d) for storing SGI in a locked security storage container

whenever left unattended; and, 10 CFR 73.21(e) for marking SGI in a

conspicuous manner as " Safeguards Information." Failure to adequately

control and mark the SGI maintained in the ATC of the MCR constituted a

violation of NRC regulations and licensee procedures as identified as

VIO 50-348, 364/97-11-8. Unattended And Unmarked SGI left in the MCR.

However. licensee corrective actions have been prompt and effective to

ensure SGI was controlled and marked pursuant to regulatory

requirements.

F8 Hiscellaneous Fire Protection Issues (IP 92904)

F8.1 (Closed) IFl 50 348. 364/96 006 07- Fire Main Failures

This item was opened pending metallurgical analysis of the failed

piping and implementation of longterm corrective actions. Southern

Company Services provided the results of the metallurgical analysis and

recommendations for action via letter dated December 5. 1996. The

inspectors previously reviewed this issue. but were unable to close the

item because the recommended corrective actions had not been

implemented.

The licensee implemented the recommended corrective action on September

1. 1997. Licensee staff identified all outside fire protection piping -

and inspected it to verify the integrity of the insulation and flashing

and that no water had penetrated and soaked the insulation, No

discrepancies were identified. The licensee also implemented an

eighteen month preventive maintenance task to perform this inspection.

The inspector verified the new PM task was entered into the information

management system.

The inspectors concluded that the corrective actions were thorough.

Based on the licensee's corrective action this IFl is closed.

Enclosure 2

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_ _ _ _ _ ___ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ ____ _ _ _ _ _ _ _ _ - - - - - _ _______-__

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V. Manaaement Meetinas and Other Areas

X1 Review of Updated Final Safety Analysis Report Commitments

A recent discovery of a licensee o>erating its facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspect ?ns

discussed in this re) ort, the inspectors reviewed the applicable

portions of the UrSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures and/or parameters, except for:

1) EDGs running in excess of their continuous rating (see Section

E8.1); and.

2) R-29 not being routinely source checked (see Section 02.1).

X2 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management on October 21, 1997, af ter the end of the inspection period.

The licensee acknowledged the findings presented. The inspectors asked

the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was

identi fied.

PARTIAL LIST OF PERSONS CONTACTED

Licensee

A. Harris. SNC Corporate Engineering Manager *

M. Aj1 uni, SNC Corporate Licensing Manager *

R. Badham. Safety Audit and Engineering Review (SAER) Supervisor

R. Coleman. Maintenance Manager

C. Collins. Operations Superintendent - Administration

S. Fulmer. Technical Manager

D. Gambrell. Design Team Leader. Southern Company Services (SCS)*

D. Grissette. Operations Manager

P. Harlos. Plant Health Physicist

R. Hill General Manager

C. Hillman. Security Chief

R. Johnson. Operations Superintendent - Support

D. Jones. Configuration Management Manager

H. Mahan SNC Corporate Senior Engineer *

R. Martin Maintenance Team Leader

l D. McKinney. Engineering and Licensing Manager *

M. Mitchell. Health Physics Superintendent

R. Monk. Engineering Support Supervisor

D. Morey Vice President - Farley Nuclear Project *

l C, Nesbitt, Assistant General Manager. Plant Support

l R. Ponder. SNC Corporate Senior Engineer *

Enclosure 2

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0. Shelton. SCS Engineering Manager *

M. Stinson Assistant General Manager. Operations

G. Wilson SCS Senior Engineer *

MG

J. Zimmerman. NRR Project Manager

  • Supported NRC ins)ection at SNC Corporate offices and attended pre-exit

interview on Septem>er 19. 1997.

INSPECTION PROCEDURES (IP) USED

IP 37551-. Onsite Engineering

IP 40500. Effectiveness of Licensee Controls in Identifying. Resolving, and

Preventing Problems

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 92700: Onsite followup of LERs

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

IP 92904: Followup - Plant Support

ITEMS OPENED. CLOSED, AND DISCUSSED

Op311cd

lyng _ Item Number S.t31us Description and Reference

IFl 50-348. 364/97-11-01 Open RPS Response Time Testing (Section

M1.2).

VIO 50-348, 364/97-11-02 Open Failure to Perform Adequate IST of

TDFW Check Valves on Cessation or

Reversal of Flow (Section E8.6).

VIO 50-348, 364/97 11-03 Open TDAFW Battery Installation and

Check Valve Test Deficiencies

(Sections E8.7 and E8.9).

VIO- 503348. 364/97-11-04 Open r ailure to Implement a Test Program

for Service Testing of the TDAFW

Battery (Section E8.8).

V10 50 348, 364/97-11-05 Open Design Control Measures did not

ensure that calculations were

verified and controlled (Sections

E8.16 and E8.25).

Enclosure 2

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VIO 50 348, 364/97-11-06 Open inadequate Corrective Action To

Resolve Differences Between CCW

System P&lDs And Operating

Procedures (Section E8.20).

VIO 50 346, 364/97-11 07 Open Auxiliary Building Battery

Surveillance Test Criteria

inconsistent With TS (Section

E8.22).

VIO 50 348, 364/97-11-08 Open Unattended And Unmarked SGI left in

the MCR (Section S3.1).

G101Cd

lyne Item Number Status Descriotion and Reference

IFI 50 348. 364/97-10 03 Closed Review Licensee Evaluation for

Extended Onsite Storage of

Contaminated Wet Resin (Section

R8.1).

VIO 50-348. 364/97-11-11 Closed Unattended And Unmarked SGI Left in

The MCR (Section 51.1).

LER 50 364/97-03 Closed Failure To Perform Diesel Generator

Surveillance Requirements Due To

Procedural Inadequacy (Section

M8.1).

LER 50-348/97-05 Closed Failure To Perform Nuclear

Instrumentation Surveillance

Requirements Prior To Mode 2 And 3

Entry (Section M8.2).

VIO 50-348, 364/97-05-03 Closed Failure To follow Multiple TS

Surveillance Requirements (Section

M8.3).

IFl 50 348, 364/96-09-04 Closed CCW HX Epoxy Coating and Broken

Tubes (Section M8.4).

IFl 50 348, 364/96 06-07 Closed Fire Main Failures (Section F8.!'.

IFl 50 348, 364/96-13-03 Closed Foreign Material From Seal

Injection System To RCP Seals

(Section M8.5).

IFI 50-348. 364/96 13-07 Closed Certain HELB Isolation Sensors Not

Described In UFSAR (Section E8.2).

LER 50-364/96-03 Closed Steam Generator Tube Degradation

and Tube Status (M8.6).

Enclosure 2

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VIO 50-364/96-155 01014 Closed Steam Generator Tube Flaws With F*

Distance (Section E8.3).

VIO 50-348/97-130-01014 Closed failure To Prescribe Documented

50-364/97-130 01014 Instructions For Procedures To

implement PRF Testing and Operation

(Section M8.7).

URI 50-348. 364/97-201-01 Closed Unprotected CST Connections

(Section E8.4).

t

URI 50 348, 364/97-201 02 Closed Tornado Protection of CST Level

Instrumentation (Section E8.5).

URI 50-348. 364/97 201-03 Closed AFW Check Valve Reverse Flow

Testing (Section E8.6).

URI 50 348. 364/97-201-04 Closed AFW Check Valve Forward Flow

Testing (Section E8.7).

URI 50-348. 364/97-201-05 Closed TDAFW Battery Testing (Section

E8.8).

URI 50-348, 364/97-201-06 Closed TDAFW Battery Installation (Section

E8.9).

IFl 50-348/97-201-07 Closed CST Level Alarm (Section E8.10).

IFl 50-348/97-201-10 Closed CST Level Transmitter Freeze

Protection (Section E8.13).

URI 50 348. 364/97-201-11 Closed AFW UFSAR Discrepancies (Section

E8.14).

URI 50-348. 364/97-201-13 Closed MOV Design Basis Differential

Pressure (Section E8.16).

Ifl 50-348. 364/97-201-14 Closed CCW Pump Testing (Section E8.17).

URI 50 348, 364/97-201-15 Closed Post Modification Testing (Section

E8.18).

URI 50-348. 364/97-201-l'/ Closed Drawing and Procedure Discrepancies

(Section E8.20).

URI 50-348, 364/97 201-18 Closed CCW UFSAR Discrepancies (Section

E8.21).

URI 50-348, 364/97-201-19 Closed TS Change for Auxiliary Building

Battery (Section E8.22).

URI 50-348, 364/97-201-20 Closed Fire Barrier Penetration Seal

Documentation (Section E8.23).

Enclosure 2

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URI 50-348, 364/97-201-21 Closed Electrical UFSAR Discrepancies

(Section E8.24).

URI 50-348, 364/97-201-22 Closed Control of Calculations (Section

E8.25).

Discussed

Iygg Item Number Status Eescriotion and Reference

IFI 50 348. 364/97-10 02 Open UFSAR Reverification Corrective

Actions (Section E8.1).

URI 50-348. 364/97-201-08 Open

'

Tornado Protection of TDAFW Pump

Vent Stack (Section E8.11).

URI 50 348, 364/97-201-09 Open Tornado Missile Spectra (Section

E8.12).

URI 50 348. 364/97-201-12 Open Stress Analysis Temperature

(Section E8.15).

IFI 50 348. 364/97-201-16 Open Calculation Discrepancies (Section

E8.19).

Enclosure 2