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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217K9681999-10-19019 October 1999 Ack Receipt of Transmitting Rev 40 to Physical Security Plan for Washington Nuclear Plant 2.Based on Determination That Changes Do Not Decrease Effectiveness of Plan,No NRC Approval Required ML17284A8981999-10-14014 October 1999 Forwards Rev 0 to WNP-2 Cycle 15,COLR 99-15, IAW Requirements of TS 5.6.5 ML17284A9061999-09-24024 September 1999 Forwards Final Rept for 990812 out-of-sequence Drills for Energy Northwest Washington Nuclear Power Project 2 (Lab, Food Control Point & Milk Sampling).No Deficiences & No Areas Requiring C/A Identified in Three Drills ML17284A8881999-09-24024 September 1999 Informs NRC of Change in Schedule Pertaining to Final Implementation of Reactor Stability long-term Solution for WNP-2 ML17292B7591999-09-24024 September 1999 Forwards Rev 24 to WNP-2 Emergency Plan,Iaw 10CFR50.4(b), 50.54(q) & 10CFR50 App E.Detailed Synopsis of Changes,Encl ML17292B7581999-09-22022 September 1999 Forwards NRC Forms 396 & 398 for Nl Hancock,License SOP-50027-3,AR Herrington,License OP-50013-3,WH Sawyer, License SOP-50023-3 & Dl Strote,License SOP-50031-3,for Renewal of Licenses.Without NRC Forms 396 & 398 ML17284A8811999-09-0909 September 1999 Forwards Response to NRC 990623 RAI to Support Review of Pending Request for Amend to Reactor pressure-temp Limit Curve TS GO2-99-168, Forwards Rev 40 to Physical Security Plan.Rev Withheld,Per 10CFR2.790(a)(3)1999-09-0808 September 1999 Forwards Rev 40 to Physical Security Plan.Rev Withheld,Per 10CFR2.790(a)(3) ML17284A8711999-08-30030 August 1999 Informs Staff of Errors in world-wide-web Database Related to WNP-2 Reactor Vessel Structural integrity.Marked-up Pages Containing Errors or Omissions Will Be Forwarded by 991201 ML17284A8751999-08-30030 August 1999 Provides Correct Page from License NPF-21 Marked to Show Rev Addressed in 990729 Application for Amend,Which Included Page That Was Inadvertently Included as Attachment 4.Replace Attachment 4 with Attached Page & Disregard Attachment 5 ML17284A8721999-08-30030 August 1999 Forwards Proprietary Info to Support Review of Request for Amend to License NPF-21,re Min Critical Power Ratio Safety Limits Tss,As Requested During 990816 Conversation. Proprietary Encl Withheld ML17292B7531999-08-24024 August 1999 Requests That Eleven Individuals Listed Below Take BWR Generic Fundamentals Examination to Be Administered on 991006 ML17292B7511999-08-24024 August 1999 Forwards Fitness for Duty (FFD) Semiannual Performance Data Rept for Jan-June 1999,per 10CFR26.71(d) ML17284A8701999-08-19019 August 1999 Forwards NRC Form 396, Certification of Medical Exam by Facility Licensee & NRC Form 398, Personal Qualification Statement - Licensee, for Jd Prescott (License SOP-50262-1).Without Encls ML17292B7501999-08-19019 August 1999 Informs Staff That Licensee Has Completed Review of NRC SER for B&Wog Util Resolution Guidance Document Addressing ECCS Suction Strainer Blockage ML17284A8681999-08-12012 August 1999 Submits Two ISI Program Plan Relief Requests for NRC Review & Approval,Per 10CFR50.55a(a)(3)(i).Proposed Alternatives Provide Acceptable Level of Quality & Safety ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams ML17284A8541999-08-0202 August 1999 Forwards Proprietary Addl Info to Support Review of Pending Request for Amend to MCPR Safety Limit Ts.Info Consists of Proprietary Ltr from Abb Combustion Engineering,Inc.Encl Withheld ML17284A8531999-07-30030 July 1999 Forwards Estimate of Number of Licensing Action Requests Planned for Submittal in Future,As Requested in Administrative Ltr 99-02.Twenty-nine Submittals Scheduled for Fy 2000 & Four for Fy 2001 ML17284A8301999-07-22022 July 1999 Clarifies Change of Licensee Name from Wpps to Energy Northwest & Change of Facility Name from Wppss Nuclear Project Number 2 to WNP-2,as Requested in 990719 Telcon with Js Cushing of NRC.Marked-up OL Pages,Encl ML17292B7451999-07-20020 July 1999 Forwards Rev 23 to WNP-2 Emergency Plan,Iaw 10CFR50.4(b) & 50.54(q) & 10CFR50 App E.Rev 23 Provides Updated Description Re Establishment of Separate Emergency Operation Centers for Benton & Franklin Counties ML17292B7391999-07-16016 July 1999 Submits Withdrawal of Request for Amend to Secondary Containment & Standby Gas Treatment Sys Ts.Util Currently Plan to re-submit Amend Request in Entirety by 991112 ML17292B7381999-07-12012 July 1999 Forwards NRC Form 396 & NRC Form 398,for If Sumsion,License OP-50487 & Ga Westergard,License SOP-50415 for Renewal of Operator Licenses.Without Encls ML17292B7171999-07-0606 July 1999 Provides Notification of Early Completion on 990630 of Exception Noted in 990629 Ltr.Equipment within Scope of GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants, Evaluated & Y2K Ready ML17292B7181999-07-0202 July 1999 Responds to 990623 RAI to Support Review of Evaluation of Planar Indication Found on Weld Number 24RRC(2)A-1 During 1998 RO ML17292B7161999-06-30030 June 1999 Forwards Addl Info Requested in 990513 Ltr to Support Review of Pending Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves. ML17292B7131999-06-29029 June 1999 Forwards Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. ML17292B7091999-06-21021 June 1999 Forwards Proprietary Response to NRC 990603 RAI Re Licensee Request for Amend to MCPR Safety Limit Tss.Proprietary Info Withheld IAW Requirements of 10CFR2.790 ML17292B7041999-06-17017 June 1999 Forwards NRC Forms 396 & 398 for Three Individuals Listed Below for Renewal of Operator Licenses.Without Encls ML17292B7031999-06-10010 June 1999 Forwards Response to NRC 990511 RAI Re License Request for Amend to Secondary Containment & SGTS Tss.Results of Addl Benchmark of Gothic Computer Code Performed to Demonstrate Modeling Capability of Drawdown Response,Encl ML17292B6841999-06-0404 June 1999 Forwards Response to NRC 990326 RAI Re WNP-2 GL 96-05 Program for Periodic Verification of design-basis Capability of MOVs ML17292B6851999-06-0101 June 1999 Forwards 1999 Quality Audit of WNP-2 Emergency Preparedness Program, Per NUREG-0654,Section Ii,Criteria P.9.Seven Problem Evaluation Requests & Nine Recommendations for Improvement Were Issued as Result of Audit Activities ML17292B6831999-05-25025 May 1999 Informs That Request for NRC Approval of Changes to Emergency Plan Requesting Reduction in on-shift HP Staffing, Is Retracted.Util Will Resubmit Request with Required Addl Info at Later Date ML17292B6751999-05-25025 May 1999 Forwards Proprietary ABB-CE Ltr Re WNP-2 Cycle 15 SLMCPR & Core Reload Design Rept,Per Util Request for Amend Re MCPR Safety Limits.Proprietary Info Withheld,Per 10CFR2.790 ML20206U4501999-05-19019 May 1999 Ack Receipt of Which Transmitted Rev 39 to Physical Security Plan,Per 10CFR50.54(p).No NRC Approval Is Required,Since Changes Do Not Decrease Effectiveness of Security Plan ML17292B6661999-05-0707 May 1999 Requests Exemption to Requirement in 10CFR55.59(a)(2) Re Annual Operating Test requirements.One-time Exemption from Requirement to Period Not to Exceed 15-months from Last Date of Passing Operating Exam for Licensee at Facility ML17292B6531999-05-0303 May 1999 Forwards Response to NRC 990402 RAI Re Licensed Operator Positive Drug Test.Encl Withheld,Per 10CFR2.790 ML17292B6561999-04-29029 April 1999 Forwards Rev 0 to Calculation ME-02-98-04, Fracture Mechanics Evaluation of N1 Safe End & Calculation Mod Record CMR-98-0243, Fracture Mechanics Evaluation of N1A Nozzle Safe End, as Suppl Info to ISI Exam ML17292B6421999-04-19019 April 1999 Responds to NRC 990319 Ltr Re Violations Noted in Insp Rept 50-397/99-01.Corrective Actions:Provisions Are Presently in Place to Maintain Adequate Level of Security GO2-99-073, Forwards Rev 39 to WNP-2 Physical Security Plan,Per 10CFR50.54(p).Changes Do Not Decrease Effectiveness of Approved Plan.Encl Withheld IAW 10CFR73.21 & 10CFR2.7901999-04-19019 April 1999 Forwards Rev 39 to WNP-2 Physical Security Plan,Per 10CFR50.54(p).Changes Do Not Decrease Effectiveness of Approved Plan.Encl Withheld IAW 10CFR73.21 & 10CFR2.790 ML17292B6401999-04-13013 April 1999 Requests That WNP-2 Operator Requalification Program Be Granted one-time Extension Beyond Requirement in 10CFR55.59(a)(2) for Annual Operating Tests ML17292B6371999-04-12012 April 1999 Forwards Response to NRC 990211 RAI Re Util Request for Amend to Secondary Containment & SBGTS TS ML17292B6281999-04-0606 April 1999 Informs NRC That Insp Interval Ending Date for ISI Program Plan Has Been Extended by One Year to Dec 12,2005 Due to Changes in Plant Refueling Outage Schedule ML20196K6961999-03-30030 March 1999 Ack Receipt of ,Transmitting Rev 38 to Physical Security Plan for Plant.No NRC Approval Is Required,In Accordance with 10CFR50.54(p) GO2-99-060, Submits Rept of Status of WNP-2 Decommissioning Fund as of 981231,IAW 10CFR50.75(f)(1)1999-03-26026 March 1999 Submits Rept of Status of WNP-2 Decommissioning Fund as of 981231,IAW 10CFR50.75(f)(1) ML17292B6131999-03-24024 March 1999 Forwards Rev 0 to Calculation ME-02-98-04, Fracture Mechanics Evaluation of N1 Nozzle Safe End. Info Will Be Used to Assist NRC in Review of WNP-2 ISI Activities Associated with Evaluation of Planar Indication ML20204F0261999-03-19019 March 1999 Forwards Insp Rept 50-397/99-01 on 990201-04 & 0303-05.No Violations Noted.Areas of Physical Security Plan Effectively Implemented with Listed Exceptions ML17292B6001999-03-16016 March 1999 Responds to Weakness Noted in Insp Rept 50-397/98-24. Corrective Actions:Developed Document to Identify Areas Needing Improvement,Assigned Responsibility for Actions & Provided Milestones for Achievement ML17292B5941999-03-16016 March 1999 Forwards NRC Form 396, Certification of Medical Exam by Facility Licensee, & NRC Form 398, Personal Qualification Statement - Licensee, for MD Comstock,Mc Naulty & RR Nelson.Without Encls 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17284A8981999-10-14014 October 1999 Forwards Rev 0 to WNP-2 Cycle 15,COLR 99-15, IAW Requirements of TS 5.6.5 ML17284A9061999-09-24024 September 1999 Forwards Final Rept for 990812 out-of-sequence Drills for Energy Northwest Washington Nuclear Power Project 2 (Lab, Food Control Point & Milk Sampling).No Deficiences & No Areas Requiring C/A Identified in Three Drills ML17292B7591999-09-24024 September 1999 Forwards Rev 24 to WNP-2 Emergency Plan,Iaw 10CFR50.4(b), 50.54(q) & 10CFR50 App E.Detailed Synopsis of Changes,Encl ML17284A8881999-09-24024 September 1999 Informs NRC of Change in Schedule Pertaining to Final Implementation of Reactor Stability long-term Solution for WNP-2 ML17292B7581999-09-22022 September 1999 Forwards NRC Forms 396 & 398 for Nl Hancock,License SOP-50027-3,AR Herrington,License OP-50013-3,WH Sawyer, License SOP-50023-3 & Dl Strote,License SOP-50031-3,for Renewal of Licenses.Without NRC Forms 396 & 398 ML17284A8811999-09-0909 September 1999 Forwards Response to NRC 990623 RAI to Support Review of Pending Request for Amend to Reactor pressure-temp Limit Curve TS GO2-99-168, Forwards Rev 40 to Physical Security Plan.Rev Withheld,Per 10CFR2.790(a)(3)1999-09-0808 September 1999 Forwards Rev 40 to Physical Security Plan.Rev Withheld,Per 10CFR2.790(a)(3) ML17284A8751999-08-30030 August 1999 Provides Correct Page from License NPF-21 Marked to Show Rev Addressed in 990729 Application for Amend,Which Included Page That Was Inadvertently Included as Attachment 4.Replace Attachment 4 with Attached Page & Disregard Attachment 5 ML17284A8721999-08-30030 August 1999 Forwards Proprietary Info to Support Review of Request for Amend to License NPF-21,re Min Critical Power Ratio Safety Limits Tss,As Requested During 990816 Conversation. Proprietary Encl Withheld ML17284A8711999-08-30030 August 1999 Informs Staff of Errors in world-wide-web Database Related to WNP-2 Reactor Vessel Structural integrity.Marked-up Pages Containing Errors or Omissions Will Be Forwarded by 991201 ML17292B7531999-08-24024 August 1999 Requests That Eleven Individuals Listed Below Take BWR Generic Fundamentals Examination to Be Administered on 991006 ML17292B7511999-08-24024 August 1999 Forwards Fitness for Duty (FFD) Semiannual Performance Data Rept for Jan-June 1999,per 10CFR26.71(d) ML17284A8701999-08-19019 August 1999 Forwards NRC Form 396, Certification of Medical Exam by Facility Licensee & NRC Form 398, Personal Qualification Statement - Licensee, for Jd Prescott (License SOP-50262-1).Without Encls ML17292B7501999-08-19019 August 1999 Informs Staff That Licensee Has Completed Review of NRC SER for B&Wog Util Resolution Guidance Document Addressing ECCS Suction Strainer Blockage ML17284A8681999-08-12012 August 1999 Submits Two ISI Program Plan Relief Requests for NRC Review & Approval,Per 10CFR50.55a(a)(3)(i).Proposed Alternatives Provide Acceptable Level of Quality & Safety ML17284A8541999-08-0202 August 1999 Forwards Proprietary Addl Info to Support Review of Pending Request for Amend to MCPR Safety Limit Ts.Info Consists of Proprietary Ltr from Abb Combustion Engineering,Inc.Encl Withheld ML17284A8531999-07-30030 July 1999 Forwards Estimate of Number of Licensing Action Requests Planned for Submittal in Future,As Requested in Administrative Ltr 99-02.Twenty-nine Submittals Scheduled for Fy 2000 & Four for Fy 2001 ML17284A8301999-07-22022 July 1999 Clarifies Change of Licensee Name from Wpps to Energy Northwest & Change of Facility Name from Wppss Nuclear Project Number 2 to WNP-2,as Requested in 990719 Telcon with Js Cushing of NRC.Marked-up OL Pages,Encl ML17292B7451999-07-20020 July 1999 Forwards Rev 23 to WNP-2 Emergency Plan,Iaw 10CFR50.4(b) & 50.54(q) & 10CFR50 App E.Rev 23 Provides Updated Description Re Establishment of Separate Emergency Operation Centers for Benton & Franklin Counties ML17292B7391999-07-16016 July 1999 Submits Withdrawal of Request for Amend to Secondary Containment & Standby Gas Treatment Sys Ts.Util Currently Plan to re-submit Amend Request in Entirety by 991112 ML17292B7381999-07-12012 July 1999 Forwards NRC Form 396 & NRC Form 398,for If Sumsion,License OP-50487 & Ga Westergard,License SOP-50415 for Renewal of Operator Licenses.Without Encls ML17292B7171999-07-0606 July 1999 Provides Notification of Early Completion on 990630 of Exception Noted in 990629 Ltr.Equipment within Scope of GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants, Evaluated & Y2K Ready ML17292B7181999-07-0202 July 1999 Responds to 990623 RAI to Support Review of Evaluation of Planar Indication Found on Weld Number 24RRC(2)A-1 During 1998 RO ML17292B7161999-06-30030 June 1999 Forwards Addl Info Requested in 990513 Ltr to Support Review of Pending Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves. ML17292B7131999-06-29029 June 1999 Forwards Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. ML17292B7091999-06-21021 June 1999 Forwards Proprietary Response to NRC 990603 RAI Re Licensee Request for Amend to MCPR Safety Limit Tss.Proprietary Info Withheld IAW Requirements of 10CFR2.790 ML17292B7041999-06-17017 June 1999 Forwards NRC Forms 396 & 398 for Three Individuals Listed Below for Renewal of Operator Licenses.Without Encls ML17292B7031999-06-10010 June 1999 Forwards Response to NRC 990511 RAI Re License Request for Amend to Secondary Containment & SGTS Tss.Results of Addl Benchmark of Gothic Computer Code Performed to Demonstrate Modeling Capability of Drawdown Response,Encl ML17292B6841999-06-0404 June 1999 Forwards Response to NRC 990326 RAI Re WNP-2 GL 96-05 Program for Periodic Verification of design-basis Capability of MOVs ML17292B6851999-06-0101 June 1999 Forwards 1999 Quality Audit of WNP-2 Emergency Preparedness Program, Per NUREG-0654,Section Ii,Criteria P.9.Seven Problem Evaluation Requests & Nine Recommendations for Improvement Were Issued as Result of Audit Activities ML17292B6751999-05-25025 May 1999 Forwards Proprietary ABB-CE Ltr Re WNP-2 Cycle 15 SLMCPR & Core Reload Design Rept,Per Util Request for Amend Re MCPR Safety Limits.Proprietary Info Withheld,Per 10CFR2.790 ML17292B6831999-05-25025 May 1999 Informs That Request for NRC Approval of Changes to Emergency Plan Requesting Reduction in on-shift HP Staffing, Is Retracted.Util Will Resubmit Request with Required Addl Info at Later Date ML17292B6661999-05-0707 May 1999 Requests Exemption to Requirement in 10CFR55.59(a)(2) Re Annual Operating Test requirements.One-time Exemption from Requirement to Period Not to Exceed 15-months from Last Date of Passing Operating Exam for Licensee at Facility ML17292B6531999-05-0303 May 1999 Forwards Response to NRC 990402 RAI Re Licensed Operator Positive Drug Test.Encl Withheld,Per 10CFR2.790 ML17292B6561999-04-29029 April 1999 Forwards Rev 0 to Calculation ME-02-98-04, Fracture Mechanics Evaluation of N1 Safe End & Calculation Mod Record CMR-98-0243, Fracture Mechanics Evaluation of N1A Nozzle Safe End, as Suppl Info to ISI Exam ML17292B6421999-04-19019 April 1999 Responds to NRC 990319 Ltr Re Violations Noted in Insp Rept 50-397/99-01.Corrective Actions:Provisions Are Presently in Place to Maintain Adequate Level of Security GO2-99-073, Forwards Rev 39 to WNP-2 Physical Security Plan,Per 10CFR50.54(p).Changes Do Not Decrease Effectiveness of Approved Plan.Encl Withheld IAW 10CFR73.21 & 10CFR2.7901999-04-19019 April 1999 Forwards Rev 39 to WNP-2 Physical Security Plan,Per 10CFR50.54(p).Changes Do Not Decrease Effectiveness of Approved Plan.Encl Withheld IAW 10CFR73.21 & 10CFR2.790 ML17292B6401999-04-13013 April 1999 Requests That WNP-2 Operator Requalification Program Be Granted one-time Extension Beyond Requirement in 10CFR55.59(a)(2) for Annual Operating Tests ML17292B6371999-04-12012 April 1999 Forwards Response to NRC 990211 RAI Re Util Request for Amend to Secondary Containment & SBGTS TS ML17292B6281999-04-0606 April 1999 Informs NRC That Insp Interval Ending Date for ISI Program Plan Has Been Extended by One Year to Dec 12,2005 Due to Changes in Plant Refueling Outage Schedule GO2-99-060, Submits Rept of Status of WNP-2 Decommissioning Fund as of 981231,IAW 10CFR50.75(f)(1)1999-03-26026 March 1999 Submits Rept of Status of WNP-2 Decommissioning Fund as of 981231,IAW 10CFR50.75(f)(1) ML17292B6131999-03-24024 March 1999 Forwards Rev 0 to Calculation ME-02-98-04, Fracture Mechanics Evaluation of N1 Nozzle Safe End. Info Will Be Used to Assist NRC in Review of WNP-2 ISI Activities Associated with Evaluation of Planar Indication ML17292B5991999-03-16016 March 1999 Informs That Listed Property & Liability Insurance Coverage for WNP-2 Is in Force,In Compliance with Licensing Responsibilities Delineated in 10CFR50.54(w)(3) ML17292B5911999-03-16016 March 1999 Forwards 1998 Environ Operating Rept, Per Reporting Requirements of Section 5.4.1 of WNP-2 Epp.No Design or Operational Changes or Tests in 1998 Involved Unreviewed Environ Question ML17292B5941999-03-16016 March 1999 Forwards NRC Form 396, Certification of Medical Exam by Facility Licensee, & NRC Form 398, Personal Qualification Statement - Licensee, for MD Comstock,Mc Naulty & RR Nelson.Without Encls ML17292B6001999-03-16016 March 1999 Responds to Weakness Noted in Insp Rept 50-397/98-24. Corrective Actions:Developed Document to Identify Areas Needing Improvement,Assigned Responsibility for Actions & Provided Milestones for Achievement ML17292B5901999-03-11011 March 1999 Forwards Hard Copy of Addl Occupational Exposure Data Requested in GL 94-04,per 990303 e-mail.Original Electronic Version Was Corrupted ML17292B5681999-03-0101 March 1999 Forwards Radioactive Effluent Release Rept for 1998, IAW 10CFR50.36a(a)(2) & TS 5.6.3 & Complete Copy of WNP-2 ODCM Per TS 5.5.1 ML17292B5651999-02-22022 February 1999 Forwards Relief Request 2ISI-20,proposing Alternate Exam Expected to Reduce Dose Significantly & Still Provide Adequate Safety & Quality.Attached Relief Request Will Be Used to Support ALARA Dose Reduction Efforts During Maint ML17292B5581999-02-0404 February 1999 Requests Change to Co Which Modified WNP-2 OL to Reflect Schedule for Implementing Thermo-Lag 330-1 Fire Barrier C/As.Change Requested to Reflect That Final Implementation of C/As Will Be Completed During Fall 1999 Not Spring 1999 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML17286A2801990-08-27027 August 1990 Forwards fitness-for-duty Program Performance Data for 900103-0630,per 10CFR26.71(d) ML17286A2671990-08-23023 August 1990 Provides Info on Steps Taken to Minimize Potential Effects of NRC Maint Insp Interface Record, Form on Candor of Supply Sys Personnel When Talking W/Nrc Inspectors ML17286A2641990-08-20020 August 1990 Advises That Tech Spec Rev Re ATWS Recirculation Pump Trip Will Be Submitted by 900928,per Discussions W/ P Eng & H Lee ML17285B4341990-08-20020 August 1990 Withdraws 900302 Request for Amend to Tech Spec 3.8.1.1, AC Sources Reducing Excessive Testing of Diesel Generators. IR 05000397/19900141990-08-10010 August 1990 Provides Info Re Final Assessment of Causes & Corrective Actions Associated W/Recent 25 Kv iso-phase Bus Electrical Fault Incident,Per Request in Cover Ltr to Insp Rept 50-397/90-14.Plant Procedure 10.25.141 Will Be Revised ML17285B4171990-08-10010 August 1990 Provides Info Re Final Assessment of Causes & Corrective Actions Associated W/Recent 25 Kv iso-phase Bus Electrical Fault Incident,Per Request in Cover Ltr to Insp Rept 50-397/90-14.Plant Procedure 10.25.141 Will Be Revised ML17285B4041990-08-0202 August 1990 Submits Justification for Continued Operation W/Emergency Diesel Generator 2 Shorted Turns ML17285B3981990-07-30030 July 1990 Advises That Installation of Detector Check Valve in Fire Protection Underground Piping Sys Complete,Per 890911 Ltr. Sys Monitors for Underground Sys Leakage Over Entire Fire Protection Sys ML17285B3991990-07-27027 July 1990 Forwards Justification for Continued Operation Re Emergency Diesel Generator 2 Shorted Turns.Justification Concludes That Diesel Generator Capable of Supporting Present Operability Requirements of Tech Specs ML17285B3711990-07-12012 July 1990 Responds to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. Confirms That Items 1,2,3,4 & 5 of Requested Actions of Operating Reactors Completed ML17285B3761990-07-12012 July 1990 Discusses Potential for Surface Entry & Mining Near Plant Sites.Concludes That NRC Need Not Consider Issue as One Requiring Continued Monitoring ML17285B3781990-07-11011 July 1990 Requests Waiver of Compliance from Tech Spec 3.8.1.2 Re Ac Sources - Shutdown.Waiver Will Allow Performance of Rotor Pole Ac Voltage Drop Test to Provide Confirmation That for Extended Run Degradation Condition Will Not Occur ML17285B3841990-07-10010 July 1990 Forwards Util 1990 Emergency Exercise Scenario.W/O Encl ML17285B3661990-07-0505 July 1990 Advises of Listed Organizational & Personnel Changes, Effective 900707.J Burn Will Be New Director of Projects, C Powers Promoted to Director of Engineering & J Baker Promoted to Plant Manager ML17285B3641990-06-29029 June 1990 Advises That All Equipment Identified W/Atws Safety Function Acceptable from Environ Qualification Standpoint. ATWS Equipment Has Been Determined to Be Qualified to Normal Design Environ Conditions Followed by ATWS Accident Environ ML17285B3571990-06-28028 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. ML20055D2391990-06-28028 June 1990 Forwards Response to Re Violations Noted in Insp Rept 50-397/90-12.Response Withheld (Ref 10CFR73.21) ML17285B3501990-06-22022 June 1990 Advises That Mods to Recirculation Pump Trip Sys Implemented During 1990 Spring Refueling Outage.Remaining ATWS Items to Be Resolved as Listed ML17285B3511990-06-20020 June 1990 Forwards WPPSS-FTS-129, BWR Transient Analysis Model, for Review & Approval ML17285B3441990-06-20020 June 1990 Advises That Util Intends to Utilize R-value of 0.13% Delta K/K in Cycle 6 Implementing Procedures.Should R-value Change in Final Startup & Operations Rept,Changed Value Shall Be Used Instead ML17285B3451990-06-19019 June 1990 Forwards Rev 10 to EPIP 13.1.1, Classifying Emergency. Rev Includes New Format of Matrix Charts Intended to Improve Identification of Symptomatic & situation-based Emergency Conditions ML17285B3431990-06-18018 June 1990 Advises of Appointment of AL Oxsen to Position of Deputy Managing Director,Effective 900601 ML17285B3461990-06-15015 June 1990 Responds to NRC Evaluation Findings of Licensed Operator Requalification Program.Quality of Written Exam & Job Performance Measure Question Bank Testing Matls Will Be Improved to Meet Std Prior to Next Program Evaluation Cycle ML17285B3301990-06-12012 June 1990 Forwards Warrant for $50,000 in Response to Order Imposing Civil Monetary Penalty Dtd 900521 ML17285B3251990-06-0707 June 1990 Advises That Calculated Max Control Room Temp Re Station Blackout Will Be Provided by 900701 ML17285B2931990-05-29029 May 1990 Responds to NRC 900426 Ltr Re Violations Noted in Insp Rept 50-397/90-09.Validity of Violation Challenged.Opposes Issuance of Severity Level IV Violation Based on Listed Reasons ML17285B2861990-05-22022 May 1990 Advises That Submittal of Improved Tech Spec Scheduled for Mar 1991 & Implementation Tenatively Scheduled for Oct 1991 ML17285B2881990-05-11011 May 1990 Forwards Engineering Std EES-4,Rev 0, Setpoint Methodology, as Committed in Util 900329 Ltr.W/O Encl ML17285B2471990-05-0101 May 1990 Advises That No Changes to Tech Specs Required as Stated in 891130 Ltr in Response to Generic Ltr 89-21 Requesting Plant Status on Implementation of USI Re ATWS ML17285B2741990-04-26026 April 1990 Advises That Util Has No Comments on Licensed Operator Annual Requalification Exam During Wks of 900226 & 0305.All Comments Resolved When Exams Administered ML17285B2321990-04-25025 April 1990 Submits Revised Scheduled Completion Dates for Commitments Made in Response to Violations Noted in Insp Repts 50-397/89-06 & 50-397/89-17 ML17285B2121990-04-19019 April 1990 Responds to Fire Protection Issues Identified in 900201 Notice of Violation.Corrective Actions:Major Hardware Changes Implemented & Independent Consultant Will Be Employed to Review Fire Protection Program ML17285B2221990-04-16016 April 1990 Forwards Status Rept for Commitments Made in 891130 Ltr Re commercial-grade Dedication Process.Resolution of 10 Samples Identified by NRC & 50 Samples Identified by Cynga Completed ML17285B1881990-04-11011 April 1990 Responds to NRC 900312 Ltr Re Violations Noted in Insp Rept 50-397/90-01.Corrective Actions:Complete Job & Task Analysis Completed for Health Physics Technician Training Program & New Program Will Include Training on Fundamentals ML17285B1821990-04-0505 April 1990 Requests Exemption from Filing Requirements of 10CFR55.45(b)(2)(iii) & (IV) to Allow Delayed Submittal of NRC Form-474, Simulation Facility Certification & to Administer Simulation Test as Upgraded,Respectively ML17285B1741990-04-0505 April 1990 Advises That NRC Approved Use of Final Feedwater Temp Reduction in Amend 77 to License NPF-21 ML20012F6141990-04-0404 April 1990 Forwards Rev 17 to Physical Security Plan.Rev Withheld (Ref 10CFR73.21) ML17285B2041990-03-29029 March 1990 Requests Review of Encl Topical Rept WPPSS-FTS-127,Rev 0, Qualification of Core Physics Methods for BWR Design & Analysis. Upon Rept Approval,Tech Spec Changes (Per Generic Ltr 88-16) Scheduled for Jan 1992 ML17285B1421990-03-29029 March 1990 Forwards Revised Schedule for Plant Equipment Setpoint Methodology Program Plan.Methodology Revised to Incorporate Latest ISA Std Draft.Setpoint Program Design Team for FY90 Onsite,Trained & Began Work on 900312 ML17285B1381990-03-29029 March 1990 Forwards Concluding Rept of Results Requested by Generic Ltr 88-14, Instrument Air Supply Sys Problems Affecting Safety- Related Equipment. Air Quality Testing Performed to Date Reveals Steadily Improving Results ML17285B1131990-03-28028 March 1990 Advises of Release of Subchannel Thermal Hydraulic Computer Code & Requests Review of VIPRE-01 Mod-02 & Issuance of SER for PWR & BWR Applications.Bwr Qualification Analyses Completed & Rept on BWR Applications Encl ML17285B1331990-03-23023 March 1990 Responds to NRC 900221 Ltr Re Violations Noted in Insp Rept 50-397/89-40.Corrective Actions:Plant Procedure 10.25.63, Emergency Lighting Insp in Process of Being Expanded to Provide Instructions & Check Sheets to Ensure Uniform Insps ML17285B1311990-03-21021 March 1990 Forwards Proposed Bases Change Re 891129 Request for Amend to Tech Spec Table 4.3.6.1, Srm/Irm Detector Not-Full-In Functional Test. Bases Change Describes Special Circumstances Re Test Exception ML17285B1291990-03-19019 March 1990 Responds to Generic Ltr 89-19 Re Resolution of USI A-47 on Safety Implications of Control Sys in LWRs & Generic Ltr 89-21 Re Status of Implementation of Usis.Tech Specs Adequate to Verify Operability of Overfill Protection Sys ML17285B1171990-03-19019 March 1990 Suppls 900102 Response Re Implementation of fitness-for-duty Program at Facility.All Items Identified as Incomplete as of 900103 Completed at End of Jan 1990 ML17285B1121990-03-15015 March 1990 Provides Level of Property & Liability Insurance Coverage for Facility,Per 10CFR50.54(w)(2) Annual Requirement ML17285B0931990-03-0202 March 1990 Forwards Supplementary Info Re 900214 Application for Amend to License NPF-21,revising Tech Spec 3.3.7.5 to Address Failed Safety/Relief Valve Position Indicators ML17285B0741990-03-0202 March 1990 Responds to NRC 900201 Ltr Re Violations Noted in Insp Rept 50-397/89-30.Corrective Action:Plant Personnel Currently in Process of Making Improvements to Plant Operations Procedure Writers Guide ML17285B0861990-03-0101 March 1990 Forwards Compilation of Responses to Regulatory Impact Survey Questionnaire,Per Generic Ltr 90-01 ML17285B0581990-02-26026 February 1990 Forwards Washington Nuclear Plant-2 Semiannual Radioactive Effluent Release Rept,Jul-Dec 1989 & Amend 7 to Odcm. 1990-08-27
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Washington Public Power Supply System .
P.O. Box 968 3000 George Washington Way Richland, Washington 99352 (509)372-5000 Docket No. 50-397 September 19, 1983 G02-83-847 Mr. J. B. Martin Regional Administrator U. S. Nuclear Regulatory Commission Region V 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596
Subject:
NUCLEAR PROJECT NO. 2 tRC INSPECTION REPORT 83 NOTICE OF VIOLATION
Reference:
Letter D. M. Sternberg to C. S. Carlisle, dated August 30, 1983 Washington Public Power Supply System hereby replies to the Notices of Viola-tion designated "A" and "D" in Appendix A of the referenced letter.
Our replies, pursuant to the provisions of Section 2.201 of the NRC's " Rules of Practice" Part 2 Title 10 Code of Federal Regulations, consists of this letter and Attachments 1 and 2 which contain our responses to these Notices of Violation.
If you have any questions or desire further information, please contact Roger Johnson at (509) 377-2501, extension 2712.
- 901A Program Director, WNP-2 HAC/1kh cc: Mr. R. C. DeYoung, NRC I&E Mr. R. T. Dodds, NRC RV Mr. R. F. Heishman, NRC QASIP IE Mr. A. D. Toth, NRC Resident, WNP-2 ,
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8310120196 830928 PDR ADOCK 05000397 G PDR
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Attachment-1 WASHINGTON PUBLIC POWER SUPPLY SYSTEM ftJCLEAR PROICT NO. 2 000(ET NO. 50-397 LICENSE NO. CPPR-93 RESPONSE TO INSPECTION REPORT 83-38 NOTICE OF VIOLATION
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Statement of Violation
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'"As a result of the special inspection conducted by the E C Construction Ap-praisal Team on May 16-27 and June 6-22, 1983, and in accordance with the EC Enforcement Policy,10 CFR Part 2 Appendix C, the following violations were identified:
Criterion V of 10 CFR 50 Appendix B requires, in part, that " Activities affec-ting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished
-in accordance with these instructions, procedures or drawings. Instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance . criteria for determining that important activities have been sat-isfactorily accomplished."
The FSAR for the WNP-2 project, Section 17.1.1.5, accordingly describes that activities affecting quality are described in procedures, instructions, and drawings and that activities are conducted in accordance with these docu-
.ments. Procedures, instructions, and drawings include adequate quantitative and qualitative acceptance criteria to ascertain that the prescribed activi-ties have been satisfactorily accomplished.
- - A. The approved procedures and specifications for installation of weld-o-let fittings requires 100 percent reinforcament of attachment welds.
Contrary to Criterion V, 10 CFR 50, Appendix B, cited above, and the above requirement, weld-o-let fittings have been installed and accepted by quality control inspectors with less, that (sic) the 100 percent rein-
! forcement of the' attachment weld as observed at the time of the inspec-l tion on the four-inch weldolet installed at HPCS-630-ll.12/COND-356-9.12.
This is a Severity Level IV Violation, (Supplement II)."
Supply System Response An isometric drawing review was made of all weldolet type branch connec-
! tions (weldolets [B E], laterolets [B N], elbolets [B E], elbow pipets
[WFI], lateral pipets [WFI), pipets [WFI], bossets (WFI), sockolets [BN],
!. Page'l of 2
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. 3 and stainless products olet fittings) contained in contracts 215 and 220 work scope. Eight hundred twenty-three (823) olet type fittings were identifled. - This represents 100 percent' of the olet fittings. Eight fittings were not reinspected due to inaccessibillty by being either buried or under water. Of the 815.that were inspected, 714 were accept-able, being in strict conformance with the manufacturers' requirements.
One hundred one (101) olets inspected were not in strict conformance with the manufactur'ers requirements. Of the 101 nonconformances, 64 are of a
. minor nature (minor underweld/ concavity, minor contour anomaly,' minor lapping at weld edge, minor post weld surface preping/ grinding, missing fillet cap [WFI only), abrupt transition to run pipe) and are expected to be dispositioned as acceptable by the engineer. The remaining 37 contain underwelds greater than 1/8" or more serious contour anomalies. All 101 were identified on NCRs. The Architect Angineer (Burns and Roe) will evaluate each of the 101 on a case-by-case basis documenting the results in accordance with existing project procedures. . If the nonconformance meets all code requirements (NX-3000) for pressure and structural inte-grity for all modes of operation, the joints will be dispositioned as l
" acceptable as is". If not, the joint will be repaired.
No other contractors on the project used appreciable numbers of olets, with the exception of Contract 233.
Welding out of Weldolets installed under Contract 233, " Spray Pond Pip-ing", was reinspected by the Special PPIA Review Task Force. All weld-olets on six separate " tree risers" were inspected, three on each spray pond, which constitutes a 10 percent sample. All were found to be fully welded out, with no deficiencies encountered.
Corrective Action to Preclude Repetition This program covered 100 percent of the population. Inspectors have been retrained. - Deficiencies have been recorded 'as nonconformances and will be evaluated by the engineer and repaired if necessary.
Date of Full Compliance All nonconformances are scheduled to be dispositioned and required rework complete by November 1, 1983.
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Attachment 2 WASHINGTON PlBLIC POWER SUPPLY SYSTEM ;
MJCLEAR FROICT NO. 2 DOCKET NO. 50-397 '
, LICENSE NO. CPPR-93 RESPONSE TO INSPECTION REPORT 83-38 NOTICE OF VIOLATION Statement of Violation i "As a result of the special inspection conducted by the NRC Construction Ap-praisal Team on May 16-27 and June 6-22, 1983, and in accordance with the NRC Enforcement Policy,10 CFR Part 2 Appendix C, the following violations were Identified:
Criterion V of 10 CFR 50 Appendix B requires, in part, that " Activities affec-ting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures or drawings. Instructions,
, procedures, or drawings shall include appropriate quantitative or qualitative
' acceptance criteria for determining that important activities have been accomplished.
The FSAR for the WNP-2 project, Section 17.1.1.5, accordingly describes that activities affecting quality are described in procedures, instructions, and drawings and that activities are conducted in accordance with these docu-ments. Procedures, instructions, and drawings include adequate quantitative and qualitative acceptance criteria to ascertain that the prescribed activi-ties have been satisfactorily accomplished.
ED. . Contrary to Criterion V, 10 CFR 50, Appendix B, cited above, installed bolting materials for the following equipment and structures were not in accordance with the applicable design drawings and specifications when
-observed during the inspection.
- 1. - ASTM A-194 Grade 2H nuts were installed in lieu of Grade 7 on var-ious bolts, in the motor-pump couplings of pumps Rm-P2A, Rm-P2B, Rm -P2C, HPCS-P1 and LPCS-Pl.
- 2. One ASTM A-194 Grade 2 nut was installed in lieu of Grade 2H on pump
- SLC-Pl A.
- 3. Not all nuts were the required ASTM-A-194 Grade 2H in the relief valve SLC-RV-29B and pump RRC-P-1B penetration 41-e. The grade of these nuts was unknown.
This is a Severity Level IV Violation (Supplement II)."
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f a
Page 1 of 5
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Supply System Response The Supply System has reviewed bolting materials in various applications throughout the plant, since the CAT inspection, to determine compliance with design drawings and specifications. These sample inspections were established to obtain a representation of all major installers' installa-tions and were based on obtaining a 95 percent confidence level that less than 5 percent of the total fasteners were different than specification requirements using standard statistical methods. The 95 percent confi-dence level is. the same as that used by the NRC in Bulletin IE-79-02 Appendix A for evaluation of concrete expansion bolts, which is a similar situation as the fasteners reviewed here.
In total, the Supply System has reinspected over 6,000 individual fast-eners and has found that the number of material deviations are within the 95 percent confidence level. Following is a breakdown of these inspec-tions by bolting type:
Inspected Defects Pipe Flange Bolting 4238 139 Valve Bolting Pressure Boundary 1322 46 Non-Pressure Boundary 352 10 ECCS Pump Assembly Bolting 459 7 TOTALS 6371 202 Responding to the three items specifically mentioned, the following has been done:
- 1. All of the ECCS pump coupling bolts and nuts have been reinspected for proper material. While it is true that Grade 7 nuts were spec-ified for these pumps, the Grade 2H nuts installed are technically acceptable since the only difference is the minimum tempering temp-erature. Grade 7 nuts are tempered at 1100oF and Grade 2H nuts are tempered at 8500F. Since the pump coupling bolts operate at a rela-tively low temperature, this difference in nut grade does not affect the structural adequacy of the installation. Test and Startup re-moves, bags, and replaces the same bolting material, so it is pos-sible that the 2H nuts were supplied by the pump supplier, Ingersol Rand.
In addition to the ECCS Pumps, the following twelve additional pump groups are being inspected or reinspected for proper coupling bolt material.
Page 2 of 5
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- 1. RWCU-P-1A - Cleanup Circulating Pump RWCU-P-1B - Cleanup Circulating Pump
- 2. RCIC-P RCIC Pump
- 3. 'HPCS-P HPCS Water Leg Pump
- 4. CRD-P-1A - CRD Pump CRD-P-1B - CRD Pump
- 5. FPC-P-2A - Fuel Pool Holding Pump FPC-P-2B - Fuel Pool Holding Pump
- 6. TMU-P-1A - Cooling Tower Makeup Pumps TMU-P-1B - Cooling Tower Makeup Pumps TMU-P-lC - Cooling Tower Makeup Pumps
- 7. TSW-P-1A - Plant Service Water TSW-P-1B - Plant Service Water
- 8. FP-P-1 - Fire Pump FP-P-2A - Fire Pump FP-P-2B - Fire Pump FP-P-3 - Fire Pump FP-P-101 - Fire Protection Pump FP-P-102 - Fire Protection Pump FP-P-110 - Fire Protection Pump
- 9. CO @ -P-1A - Condensate Pump COND-P Condensate Pump CO 2 -P-lC - Condensate Pump
- 10. COND-P-2A - Condensate Booster Pump.
CO2-P-2B - Condensate Booster Pump COND-P-2C - Condensate Booster Pump
- 11. SW-P-1A - Standby Service Water Pump SW-P-1B - Standby Service Water Pump
- 12. CO2-P Reactor Building Condensate Supply Pump COND-P Radwaste Building Condensate Supply Pump CO2-P Condensate Filter /Demineralizer Backwash Pump To date, approximately 50 percent of these pumps have been reinspected with no identification of improper material.
- 2. Both of these items concern nuts of improper or unknown grade on flanged connections. The Supply System performed the following evaluation specifically for flange bolting.
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,.. o, PIPE FLANGE BOLTING Sample Evaluation MATERIAL I I I I I I I
.l l Sample Size l Material I Nuts I I l l l Studs l l Variations l Turned l Nuts l l
.l Installer I or Bolts.I Nuts l Studs l Nuts l Over l Unknown l I I I I I l Supplier l 32 l 64 1 0 1 7 l 4 1 3 l l l l l 1 I I I I I l C-233 l 120 l 120 1 0 1 0 1 0 1 0 l l I I I I I I I I I
-l C-220 1 32 1 56 1 0 1 0 l 1 1 0 l l l 1 1 I I I I I I I C-215 l 807 l 959 l 43 l 15 1 23 l 17 l l l 1 1 I I I I I I l C-250 l 419 l 592 1 10 l 56 l 16 1 31 l l l l l l 1 I I I I I Test & I I l l l l l l l Startup l 461 l 700 1 0 l 8 l 25 1 4 l l 1 I I l l l TOTALS 1,871 l 2,491 53 1 86 69 I 55 l l I I I I l TOTALS l 4,362 l 139 I ]?4 l l Of the total of 4,362 fasteners inspected,124 are nuts which would require removal to check for identification. Sixty nine of this 124 are clearly turned over so the identification marks were inaccess-ible. The other 55 nuts were inaccessible for identification for a variety or reasons such as paint, insulation, access, turned over, etc . To properly account for material variations that could exist in this 124, a percentage of exceptions was established using the total population of 4,362 reduced by the 124 giving 139 exceptions in a population of 4,238. This results in a possible 5 additional exceptions in the 124 nuts.
Therefore, in the total population of 4,362 fasteners a total of 144 exceptions could exist.
The allowable number of exceptions for a sample size of 4,362 is 194 to maintain a 95 percent confidence level that there are less than 5 percent material variations in the population not inspected.
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ihe sample shows that the material used in Quality Class I flange bolting is acceptable. Specific exceptions to specified materials identified in the inspection sample will be corrected by December 1, 1983.
A review of flange bolt loading was performed with Burns and Roe.
The actual flange bolt loading is generally much less than the al-1cwable bolt loading. These additional design margins are beyond the conservatism inherent in flange bolt loading design, providing addittonal assurance that a random nut or stud of a lesser tensile strength (A-307 versus A-193) is of no concern. Of the 53 stud material variations 43 were A-307 and 10 were unknown. Of the 86 nut variations 81 were A-307 and 5 had identification marks which could not be identified. However, the minimum material used is A-307, since this is the lowest grade commercially available for this type of fastener.
Corrective Action to Preclude Repetition The number of deficiencies found do not indicate a generic problem with fastener materials. The emphasis placed upon compliance with specifica-tion requirements or fastener installations by the thorough review con-ducted by the project, following the CAT audit, has sensitized organiza-tions participating in field work to the requirements of the specifica-tions, procedures, and responsibilities for compliance.
The Bechtel warehouse for fasteners, which is also used by the Supply System Test and Startup, was reinspected and material segregation pro-blems were corrected.
The overall WNP-2 fastener review / inspection program identified work on locking devicas and equipment mounting that was generically unacceptable and for which reinspection / rework is being implemented.
Date of Full Compliance Results of extensive sample inspections indicate that WNP-2 fastener mat-erials are in compliance with design drawings and specifications with a 95 percent confidence level that less than 5 percent defects exist.
Specific deficiencies identified in the sample inspections will be cor-rected prior to Decemtser 1,1983. Reinspection and rework implemented to correct the problems identified on locking devices and equipment mounting will likewise be completed prior to December 1, 1983.
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