ML20247H555
ML20247H555 | |
Person / Time | |
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Site: | Rancho Seco |
Issue date: | 07/21/1989 |
From: | Martin J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
To: | Keuter D SACRAMENTO MUNICIPAL UTILITY DISTRICT |
References | |
NUDOCS 8907310063 | |
Download: ML20247H555 (3) | |
See also: IR 05000312/1988039
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....+g WALNUT CREEK, CALIFORNIA M8065308 JUL 211989 Docket No. 50-312 Rancho Seco Nuclear Generatir.g Station Sacramento Municipal Utility District 14440 Twin Cities Road . Herald, California 95630-9799 Attention: Mr. D. R. Keuter i Assistant General Manager Nuclear Plant Manager Gent'.emen: This refers to the NRC's Systematic Assessment of Licensee Performance (SALP) Board Report dated March 28, 1989 for your Rancho Seco Nuclear Generating . Station and to the written comments provided in your May 11, 1989 letter in response to the SALP Board's report. We have reviewed your May 11, 1989 response and have concluded that your response was appropriate. Based on discussions held between our respective staffs, and in the absence of verbal identification of discrepancies within the report or written comments from you which require resolution, we have concluded that no changes to.the March 28, 1989 SALP Board Report are deemed , necessary. Related NRC conclusions are presented in Appendix I to this l letter. 1 In accordance with 10 CFR 2.790(a), a copy of this letter and the enclosures will be placed in the NRC Public Document Room. Should you have any questions concerning this letter or Appendix I hereto, or the SALP Board's report, we will be pleased to discuss them with you. Since ely, & hfM J. 3. Martin j Regienal Administrator j i Enclosures- l 1. Appendix I, NRC Conclusions l 2. SALP Meeting Report No. 50-312/88-39 1 3. Licensee response to SALP Report, dated May 11, 1989 j ! CC. 1 Steve L. Crunk, Manager, Nuclear Licensing State of Californic i \ \ ) ) 8907310063 890721 # {DR ADOCK 05000312 PDC j .
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2 T * g3 gg . l' -2- i bec w/ enclosures: Docket File Resident Inspector " i Project Inspector. 'G. Cook B. Faulkenberry J. Martin : R. Nease, NRR l T. Murley, NRR NRC Commissioners bec w/o enclosures: M. Smith J. Zo111 coffer REGION V 3 gfg SRichards/jg RZimmerman JBMartin RScay/89 7 /M/89 1/ g9 / 7 7 /20/89 JEST COPY , REG)EST COPY ] REQUEST - Y ] REQUEST COPY ; ES / NO YFJ/ /: N0 3YES / NO ] YES / NO v w/ - %DTOPDR ' YES) / NO , _ _ _ _ _ _ _ _ - . _ . _ _ _ _ _ ______.__.m_.__________ ___ _ _ _ _ _ _ _ _ _ _ _ _
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, 4 . . APPENDIX I NRC CONCLUSIONS i A. Conments Received From Licensee Sacramento Municipal Utility District's (SMUD) May 11, 1989 response to the Rancho Seco SALP Report presented no objections to the specific content of the report. Because there were no objections, no changes . were made to the SALP Report. l i . SMUD did provide c.larifying comments regarding situations described in , the SALP Report. These clarifications were noted, and will be considered in future inspections. ! ' .B; NRC Conclusions Regarding Acceptability of Licensee's Planned , Corrective Actions q
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' We concluded that your proposed actions to address areas needing ,l , improvement were responsive. We will review your progress..asc.part.of -{ our future inspection program, as appropriate. 1 C. : Regional Administrator's Conclusions Based on Consideration of , 3 Licensee's Response ' I have concluded that the overall ratings in the affected areas have not. . changed. _ ___-
. - _ . - _ - . _ _ _ - - - - _ _ - _ 1 w - ' , e ' UNITED STATES " .,[ g. NUCLEAR REGULATORY COMMISSION * ~L : j- REGION V % g 1450 MARIA LANE, SulTE 210 % WALNUT CREEK, CALIFORMA 94596 4 . . . . + ,d , MAR 2 81989 ' Docket No. 50-312 Rancho Seco Nuclear Generating Station - Sacramento Municipal Utility District '14440 Twin Cities Road Herald, California 95638-9799 Attention: Mr. Joseph F. Firlit -- Chief Executive Officer, Nuclear Gentlemen: SUBJECT: SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE The NRC Systematic Assessment of Licensee Performance (SALP) Board has completed its periodic evaluation of the perfomance of Rancho Seco Nuclear Generating Station _during the period July 1, 1986 through December 31, 1988. The perfomance of Rancho Seco was evaluated in the functional areas of. plant operations, radiological controls, maintenance / surveillance, emergency- preparedness,. security, engineering / technical support, anc safety assessment / quality verification. In addition, the performance of Rancho Seco was also evaluated in a special functional area, startup testing. The extensive startup testing performed necessitated evaluation of this additional functional area. The crite.rfa used in conducting this assessment and the SALP Board's evaluation of your performance in these functional areas are contained in the enclosed SALP report. , Arrangements for a meeting to discuss the results of the SALP Board's assessment will be made with your staff in the near future. i As I discussed with you during our meeting at Rancho Seco on March 2, 1989, SMUD's performance, on balance, since restart in March 1988 has been good and ! somewhat better than the average of other plants in the Region. The events of ; - December 12, 1988 and January 31, 1989 have been recent exceptions to an otherwise strong record of careful operation and testing since restart. Your response to both of those events, however, indicates that SMUD has improved substantially over the last four years. Overall, the SALP Board found your performance to be acceptable and directed toward of strength. safe facility operation. Your startup testing was perceived as an area In addition, improved performance was noted in all areas. Specific strengths were noted in the generally professional and knowledgeable l conduct of operations by control room operators, the engineering support for the accomplishment of complex plant modifications, and the improved
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involvement of the quality department in plant activities. '~ {}'l'j'} )) ( ) ,. ?y * ___-___-:_-__------_---- - - - - - - -
_ _ _ - _ -- __ -__- _ * . ' . , .- . s . -2- However, several concerns were identified by the NRC during this assessment period which warrant your attention. Concerns comon to several functional areas were the need for management to encourage greater use of your nonconforming condition reporting system for identifying and correcting discrepancies, and the need for management attention in assuring timely completion of identified corrective actions including commitments to the NRC. . A specific weakness in the area of plant operat, ions was the need for improved ; communication and decision making among mid and upper level plant management. In the area of radiological controls, continued improvement is needed with respect to liquid effluent management. A management sumary of this assessment is provided in Section II of the enclosed report. Perceived strengths and weaknesses and Board recommendations are discussed in Section IV, Performance Analysis. You are requested to provide to this office, within 30 days after our management meeting, a written response to this report. This response should describe actions which you have taken or plan to take to provide improved performance. Actions described in previous correspondence may be included by reference if appropriate. Your response may also include comments on, or amplification of, the SALP report as appropriate. In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2, Title 10, Code of Federal Regulations, a copy of this letter, the ene.losed SALP report, and your response will be placed in the NRC's Public Document Room. The NRC's Office for Analysis and Evaluation of Opertional Data performed an assessment of licensee event reports submitted for Rancho Seco. This assessment was provided as an input to the SALP process; a copy is therefore provided as Attachment I to the enclosed report. The response requested by this letter is not subject to the clearance procedures of the Office of Management and Budget as required by the Paperwork Reduction Act of 1980, PL 96-511. Should you have any questions concerning the SALP report, we will be pleased tc discuss them with you. [ Si erely, ,, 1 Regional Administrator Enclosure: SALP Report No. 50-312/88-39 Attachment 1 Enclosed in SALP Report
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SALP BOARD REPORT
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U. S. NUCLEAR REGULATORY COMMISSION REGION V SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE 50-312/88-39 : SACRAMENTO MUNICIPAL UTILITIES DISTRICT RANCHO SECO NUCLEAR GENERATING STATION JULY 1, 1986 THROUGH DECEMBER 31, 1988 . M p .5# W* ' I)(? ! \ ; . I . . . _ _ _ _ _______________j
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A. Licensee Activities 1
l B.. Direct Inspection and Review Activities 2 L [' II. Summary of Results 2 l
A. Effectiveness of Licensee Manag*? cat 2 - B. Results of Board Assessment 3 C. Changes in SALP Ratings 4 III. Criteria 4 IV. Performance Analysis 5 A. - Plant Operations 5 B. Radiological Controls 9 C. Maintenance / Surveillance 13 D. Emergency Preparedness 15 E. Security 16 F.- Engineering / Technical Support 19 G. Safety Assessment / Quality Verification 21 H. 'Startup Testing 24 V. Supporting Data and Summaries 25 A. Enforcement Activity 25 B. Confirmation of Action Letters 26 C. .AEOD Events Analysis 26 D. Detailed Description of Licensee Activities 26 TABLES Table 1 - Inspection Activities and Enforcement Summary 29 Table 2 - Enforcement Items 30 Table 3 - Synopsis of Licensee Event Reports 34 Attachment 1 - AEOD Review of Licensee Event Reports 35 - 1
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- - _ _ - _ - _ . .. ; M - s . . . . 4 1. INTRODUCTION, The Systematic Assessment of Licensee Performar.ce (SALP) is an NRC staff integrated effort to collect.available observations and data on a periodic basis and evaluate licensee's performance based on this information. The program is supplemental to normal regulatory processes used to ensure compliance with NRC rules and regulations. It is intended to be sufficiently diagnostic to provide a rational basis for allocating NRC resources and to provide meaningful feedback to the licensee's management regarding the NRC's assessment of their facility's performance in each functional area. An NRC SALP Board, composed of the members listed below, met in the Region V office on February 2, 1989, to review observations and data on > the licensee's performance in accordance with NRC Manual Chapter 0516, " Systematic Assessment of Licensee Performance," dated June 6, 1988. The Board's findings and recommendations were forwarded to the NRC Regional Administrator for approval and issuance. This report is the NRC's assessment of the licensee's safety performance j at Rancho Seco for the period July 1, 1986 through December 31, 1988. l l The SALP Board for Rancho Seco was composed of: I **A. E. Chaffee, Acting Director, Division of Reactor Safety and Projects, Region ~V (Board Chairman) **G. W. Knighton, Director,' Project Directorate V, NRR **G. P. Yuhas, Chief, Emergency Preparedness and Radiological Protection j Branch *H. S. North, Acting Chief Facilities Radiological Protection Section *M. D. Schuster, Chief, Safeguards Section *R. Fish, Chief Emergency Preparedness Section **L. F. Miller Jr., Chief, Reactor Projects Section II **R. P. Zimmerman, Reactor Projects Branch **G. Kalman, NRR Project Manager **T. D'Angelo, Senior Resident Inspector **W. P. Ang, Proj ect Inspector *K. Pendergast Emergency Preparedness Analyst *D. Schaefer, Safeguards Inspector *R. Pate, Chief, Nuclear Materials Safety and Safeguards Branch *6 Denotes voting member in all functional creas. A. Licensee Activities Rancho Seco was in an extended shutdown outage from the start of the evaluation period until March 30, 1988. After being. granted Commission approval, a gradual approach to full power commenced with plant startup on March 30, 1988 until the end of the evaluation period. The gradual approach to full power included a rigorous power acension test program. In general, Rancho Seco operated satisfactorily from March 30, 1988 through December 31, 1988. A detailed discussion of the significant occurrences during the period is provided in Section V.D of this report.
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i , B. Direct Inspection and Review Activities Approximately 15,427 on-site inspection hours were spent in performing a total of 100 inspections by resident, region-based, headquarters, and contract personnel. Inspection activity in each functional area is summarized in Table 1. The unusually large number of inspection hours was a result of the extended SALP interval and a large inspection program prior to restart on March 30, 1988. II. SUMMARY OF RESULTS A. Effectiveness of Licensee Management The licensee's management organization stabilized somewhat in mid- 1987 with the appointment of a Chief Executive Officer (CEO), Nuclear on May 4,1987, and the formation of a new organizational structure. Subsequent to restart, on June 16, 1988, a new CEO, Nuclear was appointed, and the organization's subordinate managers have changed assignments, in some cases, as well. During this SALP period SMUD senior management initiated several major programs for improvement of Rancho Seco performance. These included: * An Action Plan for Performance Improvement * A Systems Review and Test Program * An Engineering Action Plan * A Procurement Action Plan * Installation and Testing of a Safety Grade Emergency Feedwater Initiation and '?nntrol System * Installation end Testing of Two Additional Emergency Diesel Generators The improvements undertaken by management are reflected in the improved SALP ratings. However, numerous tasks remain to be completed by the current management to improve plant reliability. Included in these are commitments to the NRC such as the establishment of design basis documents, and an effective engineering oversight. The need for i>acreased involvement by the current senior plant management in important plant evolutions was evidenced by the December 12, 1988 feedwater transient. This senior management involvement should be in sufficient detail to assure greater caution and a more thorough understanding of plant activities. Management attention needs to be focused on assuring plant standards for performance established by the startup and test program for testing are not relaxed as was evident by the auxiliary feedwater overpressure event which occurred after the SALP period. B. Results of Board Assessment The SALP period was unusually long (July 1986 to December 1988) and covered a period of plant operations that was characterized by _ _ _ _ _ _ - _ - _ - - - _ _ - _ - _ _ - _ _ - _ _ - - _ _ _ _ - _ _ - _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ __ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ - _ _ _ -
_ _ _ _ _ _ _ , . . .. ' L . 3 .* . ; ' . several changes in plant management end organization and by diverse plant evolutions associated with SMUD attempts to upgrade Rancho Seco following an NRC imposed plant shutdown on December 26, 1985. The plant restarted in March 1988 and commenced a power ascension program which was completed in December 1988. This SALP focused on post-restart operations and on the current management and staff. Discussions of pre-restart evolutions and performances are included when these events appeared relevent to the evaluation of currently existing plant conditions and personnel. Overall, the SALP Board found the performance of NRC licensed activities by the licensee to be acceptable and directed toward safe operation of Rancho Seco. The SALP Board has made specific recommendations in most functional areas for licensee management consideration. The results of the Board's assessment of the licensce's performance in each functional area, including the previous assessments, are as follows: Rating Rating Last This Functional Area * Perioi Period Trend ** A. Plant Operations 3 2 B. Radiological Controls 3 2 C. Maintenance / Surveillance 3/2 2 D. Emergency Preparedness 3 2 Improving E. Security 3 2 F. Engineering / Technical Support 2 2 G. Safety Assessment / Quality 3 2 H. Startup Testing Not Rated 1 * Maintenance and Surveillance were separate functional areas during the last SALP period. Safety Assessment / Quality Verification is a new functional area this period. It is similar to, but more comprehensive than, the Quality Programs and Adminiscretive Controls Affecting Safety functional area which it replaced. Other functional areas rated separately during the last SALP period, such as Fire Protection and ; Training, were evaluated as appropriate within the scope of the functional areas listed above. ** The trend indicates the SALP Board's appraisal of the licensee's direction of performance in a functional area near the close of the assessment period such that continuation of this trend may result in a change in performance level. Determination of the performance trend is made selectively and is reserved for those instances when it is necessary to focus NRC and licensee attention on an area with a declining performance trend, or to acknowledge an improving trend in licensee performance. It is not necessarily a comparison of performance during the current period with that in the previous period. l i
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' ' ,..- - 4 . C. Changes in SALP Ratings Performance during this SALP period has inproved from that of the previous SALP period. These improvements occurred because major changes were made to equipment, personnel, and programs during-the extended shutdown. Satisfactory accomplishment of these changes was indicated by the Nuclear Regulatory Commission's approval of plant , ' s restart on March 22, 1988. The Plant Operations, Radiological
l Controls, Maintenance, Emergency Preparedness, Security, and Safety
Assessment and Quality Verification areas improved from Category 3 . to Category 2 ratings. III. CRITERIA Licensee performance is assessed in selected functional areas, depending on whether:the facility is in a construction or operational phase. l Functional areas normally represent areas significant to nuclear safety and.the environment. In this evaluation, a special area of Startup Testing was added due to the large amount of testing which was conducted by the licensee prior.to restart in March, 1988. ! The following evaluation criteria were used, as applicable, to assess each functional area: 1. Assurance of quality, including management involvement and control. 2. Approach to resolution of technical issues from a safety standpoint. 3. Responsiveness to NRC initiatives. 4. Enforcement history. 5. Operational events (including response to, analysis of, reporting of, and corrective actions for events). 6. Staffing (including management). 7. Effectiveness of tha training and qualification program. However, the NRC is not limited to these criteria and others may have been used where appropriate. On the basis of the NRC assessment, each functional area evaluated was rated according to three performance categories. The definitions of thece performance categories are as follows: .. Category 1: Licensee management attention and involvement are readily evident and place emphasis on superior performance of nuclear safety or safeguards activities, with the resulting performance substantially exceeding regulatory requirements. Licensee resources are ample and effectively used so that a high level of plant and personnel performance is being achieved. Reduced NRC attention may be appropriate.
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' . Category 2: Licensee management attention to and involvement in the performance of nuclear safety or safeguards activities are good. The licensee has attained a level of performance above that needed to meet regulatory requirements. Licensee resources are adequate and reasonably allocated so that good plant and personnel performance is being achieved. NRC attention may;be maintained at normal levels. ' Category 3: Licensee management attention to and involvement in the performance of nuclear safety or safeguards activities are not sufficient. The licensee's performance does not significantly exceed that needed to meet minimal regulatory requirements. Licensee resources appear to be strained or not effectively used. NRC attention should be increased above normal levels. IV. PERFORMANCE ANALYSIS The following is the Board's assessment of the licensee's performance in j each of the functional areas, plus the Board's conclusions for each area and its recommendations with respect to licensee actions and management emphasis. A. Plant Operations 1. Analysis During the SALP period, approximately 4029 hours of direct inspection effort were applied in the Plant Operations area. Plant Operations has improved significantly during this SALP period. The mo2t important accomplishments were th improved professionalism of operators, and the reduction or operator errors during intricate plant manipulations. Other strengths were observed such as improved equipment control procedures and significant upgrading of procedures. However, improved communication among managers at different levels in the organization appeared warranted. ' Prior to plant restart in early 1988, the licensee began a performance improvement program designed to enhance the quality ' of future plant operations. The program included: (a) Plant Emergency Operating Procedures were completely rewritten in accordance with the latest Babcock and Wilcox and NRC guidance. (b) The Safety Parameter Display System (SPDS) was added to j enable plant operators to quickly assess critical plant j parameters. The system provided Rancho Seco operators ! with a useful, user friendly display and helped them to I respond correctly to transients. l 1 (c) The Technical Specifications (TS) were upgraded in format, I Limiting Conditions for Operation (LCO) were added, and previously included LCO's were modified to clarify the Rancho Seco TS. _ _ _ _--_--_-__-__- _ _ _ _ _ - _ _ _
. . - _ _ _ _ _ . <. ' .. 6 , . (d) The licensee requested that Rancho Seco be a lead plant in adopting the " Improved B&W TS" which are currently being finalized by Babcock and Wilcox and the NRC. The resident inspectors observed licensee operation daily, including random backshift observations. Operations staffing was observed to be correct, and operations personnel were consistently observed to be knowledgeable and attentive to plant conditionc. Control room demeanor was always observed to be professional. One negative observation was that during the event on December 12, 1988, decision making on the appropriate actions to be taken was made by operations management without the involvement of senior plant management for review. Senior plant management subsequently recognized this weakness in communications and decision making and established an action plan to improve in this area. Management presence within the plant has steadily increased following the implementation of the licensee's management monitoring program. Frequent tours of the power block by all levels of plant management were observed by the resident inspectors. A weakness existed in the oversight role which plant management performed in its control of the specific plant departments. An example was identified which concerned the progress on near term commitments made to the NRC prior to plant restart in early 1988. The commitments which were made involved improvements to the plant which had been identified by the licensee's programs established as a result of the December 26, 1985 event. The inspectors noted that plant management was not knowledgeable of the status of some of the significant commitments which had been made to improve engineering and procurement, in particular. The licensee responded to the issue in a timely fashion with goals established for the facility to complete previously identified items.
l l The licensee's approach to the resolution of operational safety l
issues was generally sound. Conservatism was routinely exhibited by the control room staff when the potential for
I safety significant failures existed. During the startup l
program, detailed tests such as the Loss of Offsite Power Test,
l Emergency Feedwater Initiation and Control System Test and the
Steam Generator Secondary Pressure Test were properly conducted and performed. These tests reed significantly abnormal valve lineups of both the electrical and mechanical plant systems. The December 12, 1988 reactor trip was an exception to this overall trend. In that event, the licensee kept the reactor operating despite a double failure in the controls for the steam supply to the main feedwater pump. Also, the AFW overpressure event demonstrated weakness in the conduct of post maintenance testing. I
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i t Throughout this extended SALP period, the licensee's responsiveness to NRC initiatives has been rapid and thorough, particularly prior to the March 30, 1988 restart of Rancho Seco. This was evidenced by the implementation of several major programs resulting from NRC observations or inquiries. These included: * An Action Plan for Performance Improvement * A Systems Review and Test Program * An Engineering Action Plan * A Procurement Action Plan * Installation and Testing of a Safety Grade Emergency H Feedwater Initiation and Control System * Insta11acion and Testing of Two Additional Emergency
f Diesel Generators (EDG)
Three Severity Level IV violations were issued during the assessment period involving the failure to provide reports required by 10 CFR 50.73. Licensee management satisfactorily resolved the deficiencies through clarification of their procedure for controlling notifications to the NRC. A total of 36 LER's were submitted in this functional area. Most of the LER's were attributable to personnel error. Nine of these dealt with fire protection discrepancies that predominately involved missed fire watches. During these periods extensive modifications and testing were in process with the plant in off normal configurations. The remaining LER's appear to be attributable to weah procedures and isolated events. Those LERs received additional management attention to ensure improved performance and procedures. The licensee developed an Operations Department Action Plan in December 1987 which resulted in improved performance and few LERs since have related to personnel error or procedural deficiencies. In the early phases of the test program, a number of operational errors were committed during testing which ultimately lead to suspension of testing during the Loss of Offsite Power tests. In response to the difficulties . experienced at the time, the Operations Department Action Plan mentioned above was developed. Operator performance since that time improved considerably with no significant operator errors being detected. The licensee conducted an extended power ascension program which included significant Integrated Control System (ICS) tuning and two preplanned reactor trips. During this phase, the control room operators were also challenged by two unplanned reactor trips, one which led to the reactor coolant system being on natural circulation. During these events, performance by the control room personnel was sound and timely in response to the unexpected plant transients which had occurred. In addition, the ICS and main feedwater system caused several plant transients which were correctly addressed __- _ _ - _ .
,--------_ __ - - . . . . 1 .. , ' 8 , ~ . . - . by the plant operators who prevented a reactor trip by quickly ' identifying the condition and correcting the cause for the abnormal condition. The licensed operator training program was effective during the SALP period. This was evidenced by a high pass rate of 90 percent (9 passes of 10 candidates) on annual requalification examinations and a 100 percent pass rate (17 out of 17) on the 1987 and the 1988 replacement examinations. The licensee has started construction of an Engineering and Training a11 ding 'during this SALP period with completion (ready for training) scheduled for the Summer 1990. Arrival and startup of the site specific simulator is scheduled for mid-1990. The licensee's operations staff has remained stable throughout this SALP period. All licensed operator positions are filled and only one vacancy occurred in the last year. During this SALP period, the licensee's overall fire protection program improved. Some deficiencies in fire barriers, fire alarm systems, fire suppression systems, fire brigade training and the performance of fire pumps continued; however, both a plan and resources for correction of these deficiencies were established by the liccuaee. Routine and corrective maintenance activities appeared to be responsive to the need for safe and reliable performance of fire protection systems. Conclusion Performance Assessment - Category 2 Board Recommendations The Board recommends that the licensee continue to emphasize improving communication and decisionmaking among mid and upper level plant managers. Action should also be taken to enhance specific plant knowledge among the plant management staff to improve assessment and recognition of unusual or abnormal plant conditions. B. Radiological Controls 1. Analysis A total of thirteen routine and four special inspections were conducted by the regional staff during this assessment period in the areas of organization and management, occupational radiation safety, radiological effluent control _and monitoring, radioactive vaste management, transportation of radioactive materials, training and qualifications, and confirmatory measurements. In addition, the resident inspectors provided continuing observations in this area. i For the last assessment period, the licensee was assigned a ! Category 3 rating. The board had recommended that the licensee f
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' 9 7. 3 ' t implement the reorganization of the Chemistry, Radiation Protection and the Technical Support group in a timely fashion, and fill the vacant Chemistry Superintendent's position as quickly as possible; improve.the NRC commitment tracking system; amend the Technical Specifications to improve the Radioactive Environmental Monitoring Program to assure compliance with 10 CFR Part 50, Appendix I; complete the installation and testing of the Post Accident Sampling System (PASS). There has been significant improvement in management support in the. radiological controls area. During the beginning of this assessment period, management was slow in providing the needed support. However, changes in upper management during the last two years have resulted in increased support and improved performance. Specific examples include: implementation of an effective NRC commitment tracking system; demonstration of an operable PASS prior to reactor restart (March 1988); revision of the Technical Specifications and Off-Site Dose Calculations Manual to improve the Radiological Effluent and Environmental Monitoring programs, and assure compliance with 10 CFR 50, Appendix I. The QA organization has been effective in providing independent critical review, particularly, in the area of the radioactive effluent control and monitoring program. Surveillance conducced by the Corporate Health Physics and Chemistry Services group have been effective in identifying deficiencies _in the radiation protection and effluents pro. grams. A monthly management observation program was instituted which resulted in increased involvement of site management in plant activities. Weekly supervisory plant walkdowns have been effective in identifying and correcting deficiencies and improvement in housekeeping practices. A continuing concern involved the frequent changes in management personnel, organization, and assignment of responsibility for implementation of the radioactive effluent programs. During the latter part of 1987, the responsibility -! for offsite dose calculations was transferred from the Radiation Protection Depertment to the Environmental Monitoring l 6 Emergency Preparedness (EM&EP) Department, with liqufd and gaseous effluent sampling being performed by Radiation Protection, and sample counting by Chemistry. On July 15, i ' 1988, responsibility for implementing the effluents program was transferred to Chemistry. By February 1, 1989, Chemistry will have responsibility for effluent sampling. The instability i resulting from continuing changes in responsibility for management of the effluent programs has inhibited the establishment of a program with well-developed procedures and i experienced personnel. Due to these changes, the licensee has not always been timely in responding to and taking corrective action for deficiencies identified through internal assessments. During the last month of this essessment period, the Chemistry group appeared to be aggressively working to develop an effective program.
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. e * 10 + . . On February 4,1988, the licensee experienced an event that resulted in a worker receiving a calculated dose to a small area of skin of whole body in excess of the quarterly limit from a " Hot Particle." Review of this event indicated a lack of management oversight with respect to communications, training and implementation of the procedures to control hot particles. Shortly after the incident, management recognized the seriousness of the problem and took prompt and extensive corrective actions to prevent recurrence. The licensee accelerated implementation of their hot particle program and completed training of all onsite workers on the hazards and controls related to hot particles by April, 1988. The licensee resolved most technical issues with appropriate conservatism, technical competence, and supporting documentation. This was notably demonstrated in the licensee's response and corrective actions to the February 4, 1988 hot particle incident. With respect to the effluents program, in implementing their new Radiological Effluent Technical Specifications (RETS), the licensee identified counting times required to meet new lower limit of detection (LLD) requirements for radioactive liquid pre-batch releases and l composite samples that were unattainable for certain gamma emitting isotopes. The long counting times (about 8 hours) resulted in difficulties in making releases in a timely fashion. It appeared that the licensee had failed to properly evaluate their capabilities for meeting the LLD values prior to submission of the request for license amendment. After a more thorough review of this matter, the licensee submitted a prcposed license amendment changing the LLD for specific radionuclides, without affecting the bases of the LLD values, thereby reducing the counting times. The licensee's responsiveness towards resolving the operational aspects of the liquid effluent issue has not been fully satisfactory. While many plans have been presented, NRC inspection findings, licensee audits and operational events continue to reveal the need for additional management attention. Changes which would allow operation within the envelope of expected events without exceeding 10 CFR 50 Appendix I values should be completed. During this assessment period, the licensee has been generally responsive to NRC initiatives and concerns. This included implementation of the SALp Board's recommendations from the previous assessment, management's continued support of the radiation protection program and improvements in facilities and management of the dry radioactive waste program. Housekeeping has been effective in minimizing contaminated areas. A number of long outstanding items have been addressed. One Severity Level III, nine Severity Level IV, and six Severity Level V violations were issued during this assessment period. The Severity Level III violation involved (1) an
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* , .. 11 . , occupational dose to a small area of the skin of the whole body [ of a worker that exceeded the regulatory limit, . (2) the failure to notify an in.fividual in writing of his exposure, (3)la ' failure to properly instruct workers in precautions and procedures for minimizing exposures when working in a " Hot Particle Zone", and (4) the failure of certain individuals to adhere to procedures for control of personnel exposure. An enforcement conference was held to discuss the apparent violations and the licensee's corrective actions to prevent recurrence. . Based on the licensee's prompt and extensive corrective actions to prevent recurrence, a Notice Of Violation was issued without a civil penalty. The other violations identified during this long assessment period as indicated in Table 2, appeared to be isolated occurrences that did not indicate a programmatic breakdown in the management of the radiological controls program. In addition, prompt and I effective corrective actions were taken to prevent recurrence. ! A total of 22 LERs were submitted in this functional area. Most of the LERs were attributable to personnel error. One of 1 ! the LERs was related to the Severity Level III violation and the others appeared to be isolated events. It appears that additional management attention is needed to reduce the number ; ' of personnel errors. During the early part of this assessment period, several~ weaknesses were identified in the ALARA program. The , weaknesses were attributable to a lack of QA involvement, j training for engineers and foremen, and poor planning. Management's support for the ALARA program, resulted in the implementation of an effective training program for supervisors, engineering, and the design review staffs. The work planning procedures were revised to include ALARA planning in the initial phases of processing work requests. A new ALARA Policy was issued and ALARA procedures were revised to strengthen the program. For 1986, the licensee expended about 505 person-rem with a goal of 165 person-rem. In 1987, the ' goal vac set at 350 person-rem with 299 person-rem expended. For 1988, the licensee's initial goal of 250 person-rem was adjusted to 95 person-rem with about 79 person-rem expended as of November 30, 1988. The long shutdown time and consequent lower source term was a major contributor to the exposure ; ' reduction. There has been significant instability in organization and : staffing during this assessment period. During most of the t assessment period, the Radiation Protection Manager's (RPM) position was filled on a temporary basis by several 1 individuals. The Chemistry Superintendent's position was ; staffed with contract employees and experienced a high rate of i turnover. The EM&EP group also experienced several management and organizational changes. The changes in responsibility for management of the effluent programs has been a major contributor to these changes. During the last six months, the I ___________
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Radiation Protection group appears to have stabilized with key
!
positions staffed with permanent employees that included . additions to the technical staff. In July, 1988, the RPM's position was filled with a permanent employee, and as of October 1988, the EM&EP Manager's position was staffed on a permanent basis. - The Chemistry group continues to be staffed by contract employees in key supervisory and technical positions. The EM&EP Department also has a high number of contract employees filling positions. The licensee has made significant improvements in the training program. During the last year, the licensee has received full accreditation of their training programs from the Institute of Nuclear Power Operations. A new upgraded General Employee Training Program will be initiated in January, 1989. The licensee's training and qualification program also included contract employees. During this assessment period, there were several events where deficiencies in training were identified as causitive factors. The licensee took prompt action to correct the deficiencies to prevent recurrence. The licensee has established a satisfactory program for performing radiochemical measurements. Laboratory quality control and quality assurance activities were substantially improved during this period due to improvements in procedures. Inter-laboratory comparisons of radiochemical measurements were also improved, as the licensee began participating in a new contract laboratory intercomparison program. Onsite intercomparisons with NRC measurements were successful. 2. Conclusion Performance Assessment - Category 2 3. Board Recommendations . l i The licensee needs to continue their efforts in the staffing of Chemistry and EM&EP with permanent employees, in the identification and correction of deficiencies in the radioactive effluent programs, and in the control of liquid waste. C. Maintenance / Surveillance l 1. Analysis During the SALP period, approximately 2096 hours.of direct inspection effort were applied in the area of Plant Maintenance and Surveillance. Strengths were observed in the work request system with the installation of an automated computer based generation, tracking and retrieval system for work request documents. Preventive maintenance procedures were completely revised during this SALP period and included monitoring and ] trending of machine vibration, thermography, oil analyses and _ _ _ _ _ -
_ - - _ . _ _ _ _ _ . - k., , . A t . 13 .. . , mean failure times. A continuing weakness during the SALP period involved the failure to idetaify and document material deficiencies when discovered during' repair or rework of plant - equipment. For example, repeated trips of the feedwater heater drain pump were not aggressively investigated. The licensee programs to ensure follow-up and trending of failed surveillance, clearance of equipment, performance of required maintenance and curveillances.'and quality control of safety related materials were found to be adequate in this
., period. A strength was noted in the generation and revision of I maintenance procedures for specific plant equipment. Such
procedures had included extensive use of graphics with enlarged views of equipment showing internals. Some weakness was demonstrated in the control of post maintenance testing during the overpressurization of the AFW system after the SALP period ended. Staffing of maintenance and surveillance organizations was considered adequete. The licensee had some difficulty in maintaining secoadary diusolved oxygen levels within procedural requirements late in this asseesment period. On one occasion, feedwater oxygen concentration limits were exceeded with the consent of management. However, the need to exceed the procedural requirement was not recognized as a deficiency to be evaluated
L by the licensee's deficiency reporting system.
Licensee manaFement was actively involved in the scheduling and j coordination c; :aintenance and surveillance activities. The licensee was considered to be responsive in addressing NRC concerns. Maintaining and utilizing current day industry standards for preventive and predictive maintenance activities appeared to be a goal of the Maintenance Department management. Action was also taken to reduce work request backlogs, to i control and reduce valve packing leaks, and to successfully !
conduct a secondary side hydrostatic test of the Main Steam system following the large number of significant modification made to that system. The principal maintenance weaknees observed during this SALP period was insufficient identification and focumentatiou of deficiencies observed during the conduct of planned work activitios or plant evolutions. For example, as discussed above, difficulty in maintaining secondary side chemistry was not documented as required. Another example was the licensee's failure to recognize that improperly sized packing had been used for the repacking of the auxiliary feedwater pumo during a repair effort. Subsequent failure of the pump seal was encountered during a start of the pump due to this error. As noted above, after the SALP period, the overpressurization of AFW indicated post maintenance testing as another area of ! significant concern. l
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- - . . - . - 4 e ; p., 14 An industry accredited training program for maintenance and surveillance personnel was developed and initiated. However, s , the training of these personnel was deficient on at least one occasion late in the period in that maintenance personnel and supervisors did not reject kinked hydraulic hoses that they were aware of on a feedwater valve controller. ; Ten Severity Lev 21 IV and two Severity Level V violations, and one deviation wsre issued during the SALP period. The majority of the enforcement action was related to a failure to follow procedures or to have an adequate procedure for the work activity in process. While neue of the violations was individually indicative of a programmatic breakdown, taken collectively it appears that additional management attention is needed.to reduce the number of maintenance personnel errors. During the SALP period, 20 LER's were issued.in the area of maintenance and surveillance. Of these 20 LER's, six involved personnel error, 4 involved installation error, nine involved defective procedures and one involved a component failure. The LER's adequately described the major aspects of the events and the corrective actions taken or planned to prevent recurrence. Extensive maintenance program development (which included procedure revisions) appeared to have resolved the conditions which were reported. Conclusion PerformanceIAssessa--? - Category 2 Board Recommendations Plant management should focus special attention on identification and documentation of discrepant material conditions and improvement in post maintenance testing. Licensee management should continue to emphasize the development of work procedures for specific plant equipment, and to improve personnel performance and procedure adherence. including the chemistry area. D. Emergency Preparedness 1. Analysis The area of emergency preparedness (EP) was the subject of 12 inspections, including the observation of three (3) exercises, during this SALP period. These inspections represented approximately 590 hours of direct inspection effort. The resident inspectors assisted the regional inspectors in accomplishing the inspections. The previous SALP assessment concluded that the performance in the area of EP was a Category 3. Recommendations to improve management support and oversite in numerous areas of the EP program uere made to Flant Management by the previous SALP report.
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._ _ _ _ _ 4 . * 15 ,. , There has been a significant improvement in the management support of the emergency preparedness program during the SALP period. At the beginning of the period management support was poor, reflective of the SALP 3 rating. The changes in upper management during the last two years have brought increased support for emergency preparedness to the extent that presently it is considered a strength, particularly with respect to devoting resources necessary to insure an adequate capability is maintained. Considerab]c contractor support was obtained to l provide adequate support for the changes needed to be made in emergency preparedness. The required changes included a major rewrite of the Emergency Plan and implementing procedures and significant improvements in the records system and emergency preparedness training program. l Technical issues associated with dose nssessment and meteorology have been addressed during this SALP period. Needed improvements in the area of meteorology were identifded and are being implem nted. In the interim, the licensee has made adjustments to the dose assessment program to better address the uncertainties in the meteorological drta. The licensee has displayed an increasing responsiveness to NRC initiatives. The changes to the Emergency Plan and implementing procedures that were made support this finding. In addition, the responses to the violations identified during i the SALP period have been more complete during the latter part j of the period. Three minor violations of NRC requirements were identified during the course of the assessment period. Two of the violations appeared to result from a failure by middle management (EP management at the time) to asstre identified ] deficiencies were corrected in a timely and thorough manner. There was considerable variation in the licensee's emergency preparedness staffing during the SALP period. At the beginning of the period the supervision and staffin5 was weak. Shortly thereafter, supervision was strengthened in an effort to correct the many problems that existed. In addition, a uumber of contractor personnel were hired to provide adequate staffing to accomplish the numerous tasks to be performed. During the last half of the SALP period anoervision of emergency preparedness was in a state of fjux due to several persons filling the supervisor'c position. At the present time the staffing appears to have stabilized with the hiring of a new employee to the position of Manager, Environmental Monitoring and Emergency Preparedness. Also, permanent emergency preparedness positions have been established to elirinate most of the need for contractor support. ! At the beginning of the SALP period the emergency preparedness j training program was considered to be a significant weakness. I During the last two years the licensee has expended
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, considerable effort to improve this training program. The program is now well defined and lesson plans have been prepared. The exercise results have demonstrated the licensee's ability "s respond to emergencies and identified areas for improvements. 2. Performance Rating Category 2, improving trend. 3. Board Recommendations Continued management oversite to incure emergency preparedness continues to improve and that identified problems are corrected in a thorough and timely manner. E. Security 1. Analysis During this SALP assessment period, Region V couducted seven physical security inspections at Rancho Seco. Approximately 460 hours of direct inspection effort were expended by regional inspectors. In addition, the resident inspectors provided continuing observations in this trea. There were no material control and accounting inspections conducted during this j- assessment period. I ~ Thz previous SALP report recommended that licensee management expand their support to the overall security program. Since the initial operation of Rancho Seco, the Security Department , reported directly to Corporate Security, loccted approximately ) 35 miles from the site. In January 1988, the site Security l Department severed their direct tie with Ca porate Security, and commenced reporting directly to plant management. Thls change, together with a major reorganization of the security organization has improved the efficiency of the Security Department by realigning key security positions and responsibilities. The reorganization of the Security Department has also improved the licensee's ability to implement remedial measures to correct deficiencies identitied in the course of both internal and NRC security inspections. On March 7, 1986, approximately four months prior to this SALP period, the licensee published a Security Performance Improvement Plan (SPIP) for security operations at Rancho Seco. This SPIP identified 79 separate actions the licensee intended to complete in order to upgrade their security program to resolve earlier NRC concerns. Additionally, in response to the 'eptet'ser 1987 NRC Regulatory Effectiveness Review (RER) report, the licensea identified 19 additional actions. The majority of these actions have been completed, and have provided the licensee with an increased capability to defend against the design basis threat.
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, _ _ _ _ _ _ _ - - - . - - > .. 4 . ' . . 17 The previous SALP report also identified problems with security force training. During this assessment period, as a result of the Security Departments' reorganization, the Training Section assigned a permanent supervisor, increased their training staff, and acquired larger training support facilities. Increased management emphasis resulted in development of a Special Weapons and Tactics (SWAT) security response force, and upgraded annual refresher training. The previous SALP report also encouraged licensee management to increase the frequency of compliance monitoring of the security , program. As a result of their SPIp, and the reorganization of their Security Department, the full-time security auditor (assigned to Corporate Security) coordinates his compliance review with the licensee's Quality Assurance Department. Security management has continued to demonstrate a coordinated effort with oth6r plant staff in prevenving safety / security problems at Rancho Seco. Currently, a new site radio communication system is being installed which will increase the overall communication ability of the Operations and Security Departments. The licensee anticipates initial operation of this new radio system by January, 1969. During the assessment period, thirteen information notices related to security were issued. The licensee's actions, as reviewed to date, were found to be appropriate. The enforcement history for the period of Ju..y 1, 1986 through ' December 31, 1988 includes five Severity Level IV violations for the licensee's failure to: provide adequate illumination of an area inside the protected area; provide two physical barriers for the protection of vital equipment; provide proper storage protection for safeguards information; deny site access to unauthorized personnel; and, test access alarms for certain vital area portals. Additionally, the enforcement history included one deviation for the licensee's failure to adequately revalidate security badges every 31 days. During this SALP period, Rancho Seco reported 51 safeguards events. Three of these events occurred after the October 1987 change in the reporting requirements of 10 CFR 73.71(c), and thus were reported in the Licensee Event Report (LER) format. These events related to: repositioning plant toggle switches (21); unauthorized (mistaken) entry into plant vital areas (14); loss of security computers (4); bomb threats and threatening telephone calls (4); unlocked vital ~ area portals
! (2); inadequate compensatory measures (1); degraded vital a rea j barrier (1); drugs found inside protected area (1); cutting of J equipment wires (1); unescorted visitor inside protected area
(1); and security-related document found on site (1). The majority (94%) of these events occurred during the first half of the SALP assessment period.
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.. + . , 18 . .- In response to the August 1986, NRC policy statement on Fitness for Duty of nuclear power plant personnel, licensee management continues to support their established Fitness for Duty Program. This program, applicable to all licensee and contract personnel, consists primarily of: Pre-Employment Drug Screening; Medical Clarification Examinations; Routine Testing After Employment; For-Cause Drug Testing; and an Employee Assistant Program. The medical clarification examination is administered on a random basis, and consists of a short physical examination designed to determine the presence'of drugs and alcohol in the employee's system, plus a medical / psychological evaluation. Licensee employees who work on or operate vital equipment, and contract employees granted access to site vital areas, qualify for this examination. If, in the judgement of the examining practitioner, the employee is considered to have indications of drug or alcohol use, the employee is required to submit to a drug and alcohol urine scieen. The routine testing after employment, is required when a physical examination is mandated by a regulatory agency. . Additionally, the licensee's Program includes the random unannounced use of drug detection dogs inside the' protected area. 2.- Conclusion Performance Assessment - Category 2. 3. Board Recommendation Licensee management is encouraged to continue their support to the overall security program, and to finalize ongoing improvements identified in the Security Performance Improvement Plan, and the responses to the RER report. F. Engineering / Technical Support I- Analysis puring the SALP period, approximately 1902 hours of direct ins 9cetion effort were applied to the Engineering / Technical Support area. In addition to continuing coverage by the resident inspectors, a NRC Augmented System Review and Test Program (ASRTP) team inspection was performed along with enhanced observation by senior regional staff. The major weakness in this area involved the discovery of significant inadequacies in the control of design and engineering work, largely resulting from a poorly defined plant design basis and insufficient attention to plant design details. In contrast, a l strength observed during the latter part of the SALP period involved the self-critical attitude demonstrated by senior SMUD management in acknowledging the need for imprev,'d performance in this area, including engineering reorganization. >
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The initial findings of the NRC ASTRP inspection identified several weaknesses in engineering involvement in the resolution of problems identified by the licensee's systems review and test program. The team also identified several deficiencies with some engineering analyses for ongoing system modifications. SMUD management subsequently developed and implemented an innovative Engineering Action Plan (EAP) to restore confidence in the Rancho Seco engineering design and design process. The EAP included organizational, administrative, and cultural changes to provide a better definition of responsibility and authority for engineering activities. SMUD also contracted with an independent group of technical consultants to perform an expanded ASTRP (EASTRP) inspection similar.to the NRC inspection on the remainder of the systems not previously inspected by the NRC. A revision to the EAP provided further technical aspects of the plan. This included: * Upgrading the engineering design change process to improve the control and quality of future work. * Review of calculations for technical accuracy and completeness. * Review of technical work performed during the outage to assure design adequacy. * Reestablishment of the plant system design bases. The EASTRP was performed and the EAP initiated prior to restart. An evaluation of EASTRP by the NRC ASTRP inspection team concluded that the EASTRP inspection process provided adequate confidence that any significant problems with the design of Rancho Seco were being identified before restart. The NRC ASTRP team also assessed the EAP and concluded that the EAP appeared to improve the quality of calculations and analyses performed. to support system design. Although many aspects of the EAP were cotpleted prior to plant restart, many other portions of the EAP remain to be completed. The second revision of the EAP, dated September 16, 1988, was issued to identify items completed and the long range items still to be finished. One of the more significant aspects of the EAP that remains to be corrpleted is the establishrnent of system design basis documents. The licensee has a;ireed to complete the initial portion (14 systems) of this very extensive program by~ the end of the next refueling outage. Plant restart was contingent on several major system additions and modifications. Engineering performance to support these projects was excellent. Operational scfety was enhanced significantly by the addition of the Emergency Feedwater Initiation and Control (EFIC) system and the Safety Parameter
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---- - _ - ' . i * 20 + . . . Display System (SPDS). Hardware reliability and hu. nan ! engineering features associated with these, relatively complex, j systems are indicative of SMUD's capacity for engineering 1 excellence. J The addition of two diesel generators and modifications to the ) emergency electrical distribution system are additional j examples of excellent engineering capability and performance. Diesel angine vibrations and cable routing discrepancies, tasked the engineering organizations ability to respond to unexpected problems. In both instances, these complex issues were resolved in a thorough and professional manner. Three enforcement items were identified in this functional area. Specifically, one Severity Level IV violation was identified for failure to establish written procedures for radiographic inspections of decay heat removal pump drain lines; one Severity Level V violation was identified for an inadequate drawing - four different welds had two redundant weld number identifiers; and a deviation was identified for the use of silicone sealants in the essential HVAC system. During this SALP period 11 LERS were attributed to this functional area. All of the LERs resulted from technical discrepancies such as the lack of channel isolation devices for two channels of the Reactor Protection System power summing amplifier. The extendad' outage during this SALP period required increased technical manpower to support the varied codifications that were initiated and completed. Licensee technical staff was heavily supplemented by contract personnel to support the workload. The supplemental contractor work force was reduced following completion of the modifications and upon plant restart. Despite the heavy workload, no significant discrepancies were attributed to the adequacy of technical staffing. Similarly, effectiveness of training and
,
qualifications of the technical staff appeared to be sufficient
I for the technical tasks that were being performed. l The licensee has been very responsive to NRC initiatives and
has taken extensive corrective action to improve the quality of engineering's activities. For example a new design control process utilizing a design change package (DCP) approach was i
j established. Although the licensee's corrective actions
appeared to be extensive and complete, no new engineering products were available for audit to determine the effectiveness of the licensee's revised design control process. A number of significant weaknesses were identified by both the NRC and licensee in past procurement practices utilized by the licensee in the purchase of safety-related parts. Of specific concern to the NRC was the practices used to upgrade commerical
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grade parts for use in safety-related systems. The practices utilized in procurement before July, 1987 were not adequate. The licensee revised their procurement program to incorporate improved practices to prevent use of substandard parts in safety related systems. After the SALP period, the ovarpressurization of the AFW system event revealed two weaknesses in this area as related to this event: weak engineering oversight of maintenance activities and continued weakness in procurement. Conclusion Performance assessment - Category 2 Board Recommendation Management attention is needed to maintain a permanent, stable site engineering staff. Engineering efforts to complete the design basis records project should continue, and a review of the effectiveness of the current design change process should be conducted once a representative sample is c7ailable. Management attention is needed to enhance engineering oversight of maintenance activities in light of the AFW overpressure event. G. Safety Assessment / Quality Verification 1. Analysis During the SALP period, approximately 5739 hours of direct inspection effort were applied in the area of safety assessment / quality verification. Significant strengths noted during the SALP period included the implementation of a root cause analysis process and an aggressive approach by management to involve outside organizations, mainly INPO, in reviewing problem areas and providing recommended corrective action. However, several significant weaknesses were also noted in this functional area. These included the need for more aggressive use of the licensee's nonconforming condition reports (termed potential deviations from quality (FDQs) by SMUD), and a lack of progress in the completion of several post-restart commitments such as the creation of design bases. Over the lengthy evaluation period, many technical submittals were reviewed by the staff. These included technical specification change requests, NUREG-0737 itemst exemption and relief requests, responses to generic letters, licensee activities related to resolution of safety issues, and responses to other regulatory initiatives. The plant was shut down for a significant portion of the evaluation period because of major problems at the plant that required full technical resolution prior to restart. Several of these issues involved a substantial interface with the NRC technical staff. Issues
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- included addition of two emergency diesel generators, envf.ronmental qualification, fire protection, upgrades to emergency feedwater and instrument air systems, addition of hydrogen recombiners, establishment of a minimum meteorological monitoring program, system review and test program, reactor trip system reliability modification, and others. Licensee submittals were generally found to be adequate and responsive to the subject matter. Contractor assistance and licensee management oversight of the. contractors appeared to be edequate as reflected by the submittals. A conservative approach to fire protection issues has been evident. However, two supplemental changes were submitted up to a year after the original amendment submittal. This was indicative of a lack of attention to detail. Specifically, all _ parts of the technical specifications that needed to be changed were not considered. These changes resulted from oversights that failed to incorporate original plant areas in tables and j charts. This oversight appeared to be inconsistent with other submittals and was ccasidered to be an isolated case. Inspection activities during the SALP period resulted in the identification of twelve enforcement items. Specific enforcement topics included two Severity Level IV violations for inadequate closure of nonconforming condition reports; three Severity Level IV violations for inadequate control of safety related material in the warehouse; one Severity Level IV violation for not performing a 10 CFR'50.59 evaluation for gagging two decay heat removal (DHR) system relief valves; one Severity Level.IV violation for failure to perform cable routing inspections; one Severity Level IV violation for performance of liquid penetrant inspections of the spent fuel pool liner plate without appropriate acceptance criteria; one Severity Level IV violation for numerous housekeeping violations; and one Severity Level V violation for failing to retain radiographic records of degraded DER lines. The two violations identified for failing to write nonconforming condition reports were indicative of a persistant hesitancy on the part of licensee personnel to report nonconformances properly. A preference to use work requests for identifying and correcting nonconforming conditions was noted on several occasions. This demonstrated the need for greater management emphasis to ensure nonconformances are properly identified. _ No LERs were specifically attributed to this area. However, weaknesses in the licensee's safety assessment and quality verification performance contributed to numerous LERs such as the cable routing problems, the AFW pump packing material discrepancy, and non-inclusion of containment isolation valves in the local leak rate test program. J _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -
, _ _ - - _ _ . * 23 . . * . . On several occasions during this SALP period, the licensee demonstrated a v1111ngness to review its own programs to identify weaknesses. These reviews included EASTRP, INPO readiness for operation evaluation, Babcock and Wilcox transient assessment team evaluation, and independent assessments of the QA program. These reviews demonstrated increased willingness by the licensee to be self-critical and to learn from the expertise of outside organizations. The licensee's quality verification program has shown improvement in various areas such as increased on-the-job QC inspection of maintenance and modifications, performance of QA surveillance and the implementation of a new nonconforming condition reporting program. In March, aaae and August of 1988, an enhanced operational NRC inspection taam evaluated performance of operating crews and supporting otAanizations during the plant's power ascension from the extended shutdown period. The team observed that the Plant Review Committee (PRC) did not include department level managers. This weakness has since been corrected by inclusion of several department managers on the PRC. During an extendea inspection of the Augmented System Review and Test Program (ASRTP) between December 1986 and February 1987, it appeared that QA and the Management Safety Review Committee (MSRC) did not actively review closeout of audit findings. Additionally QA audit and surveillance programs were not providing plant management with adequate feedback of safety activities. Subsequent inspections by the inspection team confirmed that these problems had been corrected. Staffing, training, and qualifications of the licensee's Nuclear Quality Department and Licensing Department appeared to be adequate during the SALP period. Toward the end of the SALP period, Region V inspections observed that the licensee was not completing post-restart commitments as scheduled. Management meetings between the licensee and NRC Region V, on November 14, 1988, and December 12, 1988, were held to review SKUD's commitments for work to be accomplished post restart, including the various aspects of the EAP that remain to be completed. During the meetings, the licensee agreed that numerous near and long term items still remained to be completed, but reaffirmed its original commitment to promptly resolve the near term items. 2. Conclusion ~ Performance Assessment - Category 2 3. Board Recommendations The licensee should ensure the full use of the established system to identify and resolve nonconformances. The licensee
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_ __ _ _ _ _ . . * , 24 I , _ , is encouraged to complete action on the near term commitments as previously agreed upon. I H. Startup Testing l Analysis l During the SALP period, significant inspection of startup testing ] was performed. Strengths were observed in the integrated system ' functional testing approach and in the development of a system status report which documented known past problems with specific 1 plant systems. A significant strength observed was an initiative by ) the licensee to develop and implement an inspection technique which was patterned after the NRC's Augmented System Review and Test j Program (ASRTP) inspections that identified plant system performance ) or documentation problems. A weakness identified during the early ) portion of the SALP period r,'ss the initial planning and completeness l of the test program. The hTC inspected licensee startup testing activities during hot functional testing and power ascension, with particular attention to the adequacy of special test procedures and clearance boundaries, where used. Evaluations were made of the adequacy and depth of the testing to determine whether the specific system under test was performing according to the design bases of that system. A specific strength was noted in the licensee's responsiveness to NRC identified problems in the Auxiliary Feedwater system and the onsite electrical distribution system during the ASRTP inspection. Lfcensee management actively participated in the generation of the test program purpose and scope. An extensive program was undertaken to identify and document known past problems with the thirty-three selected systems which were determined by the licensee to be important to safety. This high integrity system was used as an input source to the test program development. Specific system functions and test requirements were soundly and thoroughly documented within a system status report (SSR) document. Technical and management reviews were conducted by the Plant Review Committee and were effective in identifying potentini underlying test problems. 10 CFR 50.59 reviews were conducted prior to the conduct of each test with edequate documentation of the test's technical rationale. The program was .onducted slowly, methodically, with high mansgement attention to ensuring preparation for each testing evolution. A weakness was observed in the identification and documentation of conditione which were potentially detrimental to quality. Spet.f fically, during a portion of the loss ot offsite power testing,
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a deficiency was identified with an emergency diesel generator. The deficiency was not reported on the licensee's nonconformance reporting system. Significant management attention was subsequently devoted to the identified problem with both the specific hardware __ _
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' , .. ., ' 25 i deficiency being resolved and the programmatic problem being resolved. No enforcement action was issued during the SALP period in this functional area. Two LER's were submitted documenting e start of the emergency diesel generator (emergency safety features - equipment start) and a reactor trip following a preplanned turbine generator trip. The licensee's corrective action for these LERs was appropriate. j During the period of significant testing, staffing was adequate and commensurate with testing in process. Expertise ef the testing staff was adequate for both the management of the program and conduct of testing. Conclusion Performance Assessment - Category 1 Board Recommendations The licensee's effort in this functional c.taa has been completed except for some minor testing at the 100% power plateau. Lessons learned from this program should be evaluated for application to routine post maintenance testing in light of the auxiliary feedwater overpressurization event. V. SUPPORTING DATA AND SUMMARIES A. Enforcement Activity Three resident inspectors were assigned to Rancho Seco during the SALP assessment period. 100 inspections were conducted during this lengthy SALP period that encompassed the extended shutdown of Rancho Seco. Significant team inspections included: * Two NRC headquarters Augmented Systems Review and Test Program Inspection Teams during 1986 and 1987 * NRC headquarters Operational Readiness Inspection Team in 1988 * NRC headquarters Procurement Inspection Team in 1988 * Regional Enhanced Operational Inspection Team in 1988 A total of 15,427 hours of direct inspection were performed during this SALP period. A summary of inspection activities- is provided in Table 1 along with a summary of enforcement items from these inspections. A description of the enforcement items is provided in Table 2. B. Confirmatory Action Letters ; _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _
. _ _ _ - -_ _ _ _ _ _ _ _ _ , ' . . * . . 26 One Confirmatory Action Letter (CAL) was issued during this assessment period. The letter confirmed licensee corrective action activities for the December 12, 1988 main feedwater pump trip event. Shortly after the appraisal period ended, a CAL was also issued concerning the licensee's planned actions following the January 31, 1989 auxiliary feedwater system overpressurization event. C. AE00 Events Analysis The Office for Analysis and Evaluation of Operational Data (AE0D) reviewed the licensee's events at Rancho Seco and prepared a report which is included as Attachment 1. AEOD reviewed the LERs and significant operating events for quality of reporting and effectiveness of identified corrective actions. D. Detailed Description of Licensee Activities * Before the December 26, 1985 transient, a number of criteria (performance level monitoring, plant performance statistics, and systematic assessments of licensee performance had indicated that Rancho Seco was below the industry norm for similar plants. This, plus a 1984 evaluation by a consultant, moved the licensee's Board of Directors to take action to improve the performance level at Rancho Seco. Before these actions were implemented, a number of undesirable operating experiences, culminating in the event of December 26th, further demonstrated the need for performance improvement. On the basis of the review of the December 26th event by the NRC and the utility, the licensee developed the " Rancho Seco Action Plan for Performance Improvement." The initial portions of that plan were implemented as the Plant Performance and Management Improvement Program (PPMIP). The PPMIP was designed to systematically evaluate the plant, its systems and their operation, and the management programs and organization necessary to support the safe and reliable operation of Rancho Seco. The specific goals of the PP&MIP were to: (1) reduce the number of reactor trips, (2) reduce challenges to safety systems, (3) ensure that the plant remains within allowed ranges of reactor coolant system pressures and temperatures immediately following a reactor trip, (4) ensure compliance with license requirements, (5) minimize the need for operator actions outside the control room, and (6) improve the reliability and availability of the plant. On the basis of anticipated benefits from the PP&MIP, the licensee established near-term performance goals for returning Rancho Seco to power operations. Those goals included plant availability exceeding 60%, a forced outage rate of less than 10%, and fewer than three reactor trips per year. l l During the extended shutdown period, the licensee developed a j system review and test program (SRTP) the objective of which - was to demonstrate, before plant restart, that systems ! i
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_ _ _ _ _ _ _ - _ - - _ - _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - - _ _ 9. , * * 27 4 . . important to safety were capable of performing their required function. The SRTP was performed by the licensee to provide a comprehensive review and functional demonstration of 33 selected systems thac were important to safe plant operation.. The licensee's SRTP identified the functional decription for the 33 systems, design changes or modifications required for the systems, testing necessary to demonstrate functions important to safe plant operations, and final acceptance of the systems. * On November 21, 1986, while attempting to fill, vent and pressurize the primary system, approximately 11 of 35 pressurizer heater bundles were damaged when the heaters were energized without sufficient water covering them. Operators disregarded correct pressurizer level indications due to incorrect status information for properly functioning level channels. The operators relied on the remaining level channel, which had a drained reference leg caused by loosely controlled troubleshooting of the level channels (operators being unaware of that condition). * On March 15', 1988 and on March 21, 1988, while the plant was in hot standby, letdown system relief valves PSV-22031 (March 15, 1988) and PSV-22024 (March 22, 1988) lifted and resulted in a discharge of water from the letdown system to the Reactor Building sump. The cause of both events was a steam / water transient involving isolation of letdown system piping and heat exchangers, flashing of water to steam in the low pressure area, and rapid expansion of the steam. * On August 6, 1988, as part of a planned Emergency Feedwater Initiation and Control System (EFIC) test, the reactor was manually tripped from 80 percent power and EFIC was manually initiated. Both auxiliary feedwater (AW) pumps started as designed. Approximately one hour siter both A W pumps started, smoke was observed in the vicinity of the outboard packing ! gland of AW pump P318. P318 was immediately secured and the EFIC test was completed using the other AW pump, P319. Subsequent licensee investigation determined that an identical AW pump packing overheating event had previously occurred on July 7, 1988. The event was attributed to the installation of incorrectly sized vendor supplied packing. * On December 12, 1988, while conducting a plant startup, with the reactor at 12 percent power, and one of two Main Feedwater ( W) pumps inoperable, feedwater flow to the Once Theough Steam
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Generators (OTSG) was reduced significantly by fluctuations of the steam pressure to the operating W pump n.rbine. The reduced W flow resulted in low OTSG 1evels reaching the EFIC system actuation setpoint and initiation of EFIC. Proper OTSG 1evels were reestablished by EFIC. The operators subsequently manually tripped the reactor with the belief that main feedwater was no longer available. The initial response of the plant to the reactor trip was normal. However, the licensee
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_ - _ _ - _ _ _ - - - _ _ _ - _ _ - _ _ _ _ _ _ . _ _ - _ - _ _ _ . :..***- ..... * ~28 J. * ; O 1 . soon became concerned that the reactor coolant system was j cooling down more than expected, due to continued steaming from the."B" OTSG, and, by procedure isolated AFW flow to the "B" OTSG. This resulted in emptying the 'B' OTSG for'approximately . 15 minutes. The licensee located an unexpected' steam demand- from the-auxiliary steam supply to the fourth point FW heater, isolated the auxiliary steam to the fourth point FW heater, and refilled the "B" OTSG. Subsequent licensee analysis attributed- the initiation of the event to operator actions while manually controlling two different. auxiliary steam pressure reducing stations for the steam. supply to the low pressure FW pump turbines. * On January 31, 1989, after the SALP period..while testing a newly installed governor for the. dual-driven auxiliary , feedwater pump, the steam turbine for the pump oversped. The i auxiliary feedwater system pressure was estimated to have . reached approximately 3800 psig for about three minutes. The system design pressure is 1325 psig. The NRC and licensee investigation of this event revealed weaknesses in post maintenance testing, communications, maintenance program, use of generic information, and procurement. ;
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. . ' . * . . TABLE 1 INSPECTION ACTIVITIES AND ENFORCEMENT SUMMARY (07/01/86 - 11/30/88) RANCHO SECO Inspections Conducted Enforcement Items Functional Inspection * Percent Severity Level ** Area *** Hours of Effort I II III IV V D A. Plant Operations 4029 26.1 - - - 3 - - B. Radiological 664 4.3 - - 1 9 6 - Controls C. Maintenance / 2096 13.6 - - - 10 2 1 Surveillance D. Emergency Prep. 590 3.8 - - - 3 - - E. Security 407 2.7 - - - 5 - 1 F. Engineering / 1902 12.3 - - - 1 1 1 Technical Support G. Safety Assessment / 5739 37.2 - - - 12 2 - Quality Verif. _ _ _ _ _ _ Totals 15427 100.0 1 43 11 3 * Allocations of inspection hours to each functional area are approximations based upon NRC form 766 data. ** Severity levels are in accordance with NRC Enforcement Policy (10 CFR Part 2, Appendix C). *** Inspections hours for the special functional area of startup testing were not distinguished in the NRC Form 766 data. Those hours were included in the other functional areas and predominantly were included in the hours for plant operations. .. l _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _
_ _ _ _ _ _ ' . ' . .- . Table 2 Rancho Seco Enforcement Items Report Severity Functional Number Subject Level Area 86.27 FAILURE TO REPORT TS TABLE 3.16-1 4 B RADIOACTIVE GASEOUS EFFLUENT VIOLATION. 86.27 FAILURE TO POST AND CONTROL HI RAD AREA - B 4 B OTSG IDWER CHANNEL HEAD. 86.30 FAILURE TO ESTABLISH WRITTEN PROCEDURES FOR 4 F RADIOGRAPHIC INSPECTIONS. ! 86.30 FAILURE TO RETAIN RADIOGRAPHIC RECORDS OF 5 G : DEGRADED DHR DRAIN LINES. i 86.35 INADEQUATE ILLUMINATION INSIDE PROTECTED 4 E AREA. 86.37 PROCEDURES NOT PROVIDED FOR TESTING AND 4 B CALIBRATING RAD MONITORS R15701 AND 15702. 86.37 CLEARLY VISIBLE LABELS FOR LICENSED 5 B MATERIAL NOT PROVIDED IAW 10CFR2 0. 2 03 (F) (2 ) '.' 86.38 PROCEDURE FOR FUNCTIONAL TESTING OF 4 C SNUBBERS DID NOT PROVIDE APPROPRIATE , ACCEPTANCE CRITERIA FOR LOCH-UP VELOCITY - ; VELOCITY NOT CORRECTED FOR TEMPERATURE AS RECOIDIENDED BY THE VENDOR. 87.01 FAILURE TO SPECIFY CONTENT OF EMERGENCY 4 D PROCEDURES. ! 87.01 NO PROCEDURE FOR CRIMPING TOOL CALIBRATION 4 C l AND CONTROL. 87.01 CR/TSC HVAC HI AIR FLOW RA'E T DURING 4 C 12-26-85 EVENT. 87.02 UNUSUAL EVENT NOT DECLARED FOR SECURITY 4 D ALER1' AND ESCALATED SECURITY MEASURES. 87.03 INADEQUATE DRAWING - REDUNDANT WELD 5 F IDENTIFICATION NUMBERS ON SAME DRAWING FOR I DIFFERENT WELDS.
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- - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . a; i , * * ; 87.05 FAILURE TO PERFORM TS REQUIRED SR-89 AND 90 4 B ANALYSIS. 87.05 INADEQUATE YELLOW SHIPPING LABELS FOR 4 B RADIOACTIVE MATERIAL SHIPMENT. 87.06 STORAGE OF EXPIRED' SHELF LIFE ITEMS NOT 4 G CONTROLLED. 87.06 FAILURE TO NOTIFY NRC OF ACTUATION OF 4 A EMERGENCY DIESEL GENERATOR (EDG).-FAILURE TO REPORT CR/TSC HVAC MALFUNCTION. ' 87.06"NO PROCEDURE FOR GREEN TAGGING PARTS IN 4 G WAREHOUSE. 87.06 ABNORMAL TAG NOT WRITTEN FOR TEMPORARY 4 C MODIFICATION ON "A" TRAIN NUCLEAR SERVICE RAW WATER SYSTEM. 87.06 VOIDING OF NCR WITHOUT DETERMINING CAUSE OF 4 G EMERGENCY DIESEL GENERATOR NONCONFORMING CONDITION. 87.06 NCR NOT WRITTEN FOR NON-ISOIABLE PIPE 4 G LEAKAGE. 87.06 FAILURE TO PROVIDE 10 CFR 50.73 REPORT FOR 4 A MISCELLANEOUS CONDITIONS. 87.07 FAILURE TO PROVIDE TWO PHYSICAL BARRIERS 4 E FOR PROTECTION OF VITAL EQUIPMENT. ' 87.07 FAILURE TO PROVIDE PROPER STORAGE 4 E PROTECTION FOR SAFEGUARDS INFORMATION. ' 87.11 SURVEILLANCE PROCEDURES NOT REVISED TO D C REQUIRE DOCUMENTATION OF CALIBRATION DATA IAW COMMITMENT ON PREVIOUS VIOLATION RESPONSE. 87.13 CLEANLINESS PROCEDURE NOT FOLLOWED FOR A 5 C CIASS 1 WORK REQUEST. 87.13 LIQUID PENETRANT INSPECTION OF SPENT FUEL 4 G POOL LINER NOT CONTROLLED BY PROCEDURE WITH APPROPRIATE ACCEPTANCE CRITERIA, 87.13 REPLACEMENT FILTER FOR CBAST ISSUED AND 5 C
'- INSTALLED WITHOUT SMUD ACCEPT TAG. ..
87.14 FAILURE TO WRITE NCR FOR BROKEN REACTOR 5 G COOIANT PUMP CAPSCREW. l l : 1 I < - _ _ _ _ _ - _ - _ _ - - - _ - _ _ _ _ _ _ - - _ _ - _ .
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* . , ' . 4 * , 87.14 FAILURE TO COMPLY WITH COMMITTED CODES AND D F STANDARDS, USE OF SILICONE SEALANTS IN ESSENTIAL HVAC. 87.16 STROKE TIME NOT MEASURED FOR TESTING OF 4 C TV-1,2,3,4. SIM-19,20,21,22 NOT FULL STROKE TESTED EVERY COLD SHUTDOWN. 87.19 LICENSEE FAILED TO CORRECT DEFICIENCIES 4 D IDENTIFIED DURING 1986 HEALTH PHYSICS / MEDICAL DRILL. 87.20 HEAT TREATING OF VALVE YOKE WITHOUT 4 C PROCEDURE. 87.20 FAILURE TO PROVIDE REQUIRED CABLE BEND 4 C RADIUS AND CABLE TRAY EDGE BUMPERS. 87.21 FAILURE TO PERFORM CABLE ROUTING 4 G INSPECTIONS DURING 1983-1985 TIME FRAME. 87.22 MISCELLANEOUS VIOLATIONS OF AIARA PROGRAM. 5 B 87.26 RADIOACTIVE MATERIAL INSIDE RV HEAD STAND 4 B NOT SURVEYED. 87.26 DAILY SOURCE CHECKS NOT PERFORMED WHEN 4 B R15020 WAS OPERABLE, RHUT CONTAINED KNOWN ACTIVITY AND RELEASES MADE VIA THIS PATHWAY, 87.26 RADIOACTIVE MATERIAL INSIDE RV HEAD STAND 4 B NOT POSTED AS HIGH RAD AREA. 87.37 FAILURE TO FOLLOW MAINTENANCE WORK REQUEST 4 C INSTRUCTIONS. 87.37 FAILURE TO WRITE AN NCR FOR CR/TSC 4 G REFRIGERATION UNIT NONCONFORMING CONDITION OF AS BUILT WIRING. 87.44 NCR CLOSURE BY QE PRIOR TO COMPLETION OF 4 G
l WORK. CORRECTIVE ACTION INCORPORATED INTO I
ECN WITHOUT PRIOR CLOSURE OF ECN. 88.04 FAILURE TO REVALIDATE SECURITY BADGES EVERY D E 31 DAYS. 88.04 FAILURE TO DENY SITE ACCESS TO UNAUTHORIZED 4 E SITE PERSONNEL. - 88.06 EXPIRED SHELF LIFE ITEMS IN STOCK. REPEAT 4 G VIOLATION. _ _ - _ _ _ _ - _ - _ . - _ _ _ - - _ _ _ _ _ _
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" '. * 88.12 CR/TSC HVAC ACTUATION NOT REPORTED WITHIN 4 A
i FOUR HRS.
88.13 LICENSEE DID NOT MAINTAIN ON FILE RECORDS 5 B
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FOR RADIOACTIVE MATERIAL SHIPMENT.
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88.13 LICENSEE DID NOT OBTAIN WRITTEN 5 B CERTIFICATION FOR EMERGENCY SHIPMENT OF
i RADIOACTIVE MATERIAL.
88.17 FAILURE TO SUBMIT REQUIRED ANNUAL EXPOSURE 5 B REPORT. 88.20 FAILURE TO POST, MONITOR, CONTROL HOT 3 B PARTICLE ZONE. 88.23 TEMPORARY MODIFICATION FOR AFW PUMP P318 4 C OUTBOARD SEAL WAS NOT CONTROLLED AND ! DOCUMENTED IAW PROCEDURE. 88.24 INDIVIDUAL DID NOT WEAR TLD IAW RWP. 4 B 88.25 TWO PORTABLE DOSE RATE METERS EXCEEDED 5 B CALIBRATION FREQUENCY. 80.29 ALARMS FOR CERTAIN VITAL AREA DOORS NOT 4 E TES':lED. 88.31 Calibration interval for EFIC pressure 4 C transmitters changed without proper approvals required by procedure. 88.32 DHR RELIEF VALVES GAGGED WITHOUT ADEQUATE 4 G 10 CFR 50.59 REVIEW. 88.33 NUMEROUS HOUSEKEEPING VIOLATIONS - 4 G UNSECURED LEAD SHIELDING, UNSECURED ROLLER CARTS, LADDER TIED TO SAFETY RELATED CONDUIT. 88.33 PDQ FOR FEEDWATER OXYGEN CONCENTRATION NOT 4 G DELIVERED TO OPERATIONS TECHNICAL ADVISOR WITHIN 4 HOURS AS REQUIRED BY PROCEDURE. ..
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__ _ - _ _ _ _ _ - _ _ _ . . .. * , s * . . .. TABLE 3 S F PSIS OF RANCHO SECO LICENSEE EVENT REPORTS (LERs) SALY Cause Code * Functional Area A B C D E X Totals A. Plant Operations 11 8 3 3 10 1 36 B. Radiological 11 4 - 4 1 2 22 Controis C. Maintenance / 6 4 - 9 1 - 20 Surveillance D. Emergency Prep. - - - - - - - E. Security 2 - 1 - - - 3 F. Engineering / Technical Support 5 4 - 2 - - 11 G. Safety Assessment / - Quality Verification - - - - - - l Totals 35 20 4 18 12 3 92 The above data are based upon LERs 86-11 through 88-19. * Cause Code A - Personnel Error B - Design, Manufacturing or Installation Error C - External Cause D - Defective Procedures E - Component Failure X - Other
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_ ' . * .. . Attachment 1 AEOD Input to SAlp Review for Rancho Seco LER Review During the assessment period, 84 Licensee Event Reports (LERs) were submitted to the NRC. These reports, reviewed by AEOD, consisted of LERs 86-14 through 88-16. Significant Events Utilizing AEOD's screening process, the following 18 LERs were categorized as safety significant: i 86-14 Decay heat removal (DUR) system train B rendered inoperable due to a leaking weld on the pump casing drain line, while the train A emergency diesel generator was out-of-service. 86-16 Loss of DHR capability for a period of 13 minutes during cold shutdown as result of inadvertent closure of the DHR system suction drop 11ne isolation valve. Electrical arcing from I6C technician troubleshooting activities caused the valve closure. 86-25 Spent fuel pool liner leakage while containing 316 spent fuel assemblies. Contaminated water seeped through the concrete walls of the fuel storage building to an uncontrolled storm drain. About 275 gallons were released offsite, creating an estimated whole body dose of 0.14 mrem. 87-02 Fire protec'cion deficiency involving potential loss of alternate shutdown capability. A control room fire could cause an electrical short in the protective circuitry of a diesel generator's output breaker, causing the breaker to trip. A loss of offsite power is assumed to occur at the same f.ime as the control room fire. 87-06 Problems with safety related motor-operated valves identifed in response to IE Bulletin No. 85-03, problems included over thrust conditions, incorrect brate voltage ratings, undersized power cables, lack of stem nut staking, valve internals damage, unqualified operator grease, and incorrect pickup / dropout voltages. 87-08 Inadequate automatic sequencing of the high pressure injection pumps onto the emergency diesel generator bus, due to the pump lube oil l pressure bypass circuits defeating a three second time delay. 87-10 Fire protection inadequacy whereby the reactor coola t system high point vent valves were susceptible to opening from electrical shorts. 87-11 Safety related snubbers failed functional testing after temperature considerations were factored into lock-up velocity and bleed rated acceptance criteria,
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s - . ., * . . 4 87-15 Fire protection carbon dioxide deluge system left deactivated without appropriate compensatory measures. 87-23 Inadequate electrical isolation on the reactor protection system total nuclear power channels. Channel isolation devices required by IEEE-279 and General Design Criterion 20 were not provided. ! 87-29 Inadequate surveillance testing of unsupervised control room fire alarm annunication circuits. Required monthly testing was not performed since 1976.
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87-34 High pressure injection (HP1) pump mini-flow recirculation lines ! vere not seismically supported since original plant construction due to improper classification. Failure of the lines coincident with a LOCA would render HPI capability indeterminate. 87-36 Blockage of bearing cooling water system piping to both reactor , building spray pumps due to fouling. ) 874-41 Non-seismic level switches installed on nuclear service water pumps, which could prevent the pumps from starting on a safety features actuation signal (SFAS). 87-42 Failure of electrical connectors due to residual coating from cleaning solutions. Systems affected included the reactor protection system, integrated control system, SEAS, and non-nuclear i instrumentation. 87-44 Loss of nuclear services electric building essential heating. ventilation and air conditioning system, due to inadequately designed isolation dampers between Seismic I and Seismic II ducts. 1 88-02 10 CFR 21 report regarding a manufacturing defect in undervoltage devices, causing improper operation of the control rod drive trip . breakers. j l 88-11 Auxiliary feedwater pump inoperability due to incorrectly sized d vendor supplied packing in packing gland. Other Events ) AEOD's review also identified the following events, while not necessarily being individually categorized as safety significant, collectively represent adverse trends in plant performance worthy of additional plant management attention. Inadequate fire protection compensatory measures: -- l LER 86-18 Disabled smoke detectors in the reactor building with- out compensatory measures (fire watch) due to licensed operator error. LER 86+31 Hourly instead of continuous fire watch in 480 volt switchgear room due to licensed operator error.
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LER 86-32 Missed fire watch in the east nuclear services battery room due to nonlicensed personnel error. Additionally, LER 86-18 regarding missed compensatory measures, was not referenced in this LER. LER 87-01 Hourly rather than continuous fire watches on 1/17 and 1/27/87, due to licensed operator error. No reference to LER 86-18 included. LER 87-03 Continuous fire watches not posted on 12/27/86, 12/29/86, 12/30/86, 1/2/87, 1/3/87, 1/5/87, and 1/20/87. LER 87-04 Abandoned continuous fire watch post in nuclear services electrical building (NSEB) due to nonlicensed personnel error. No reference to the above 1987 similar LERs was provided. LER 87-15 Carbon dioxide fire protection systems were deactivated without establishing fire watches on 17 occasions in 1/87 and 2/87 due to nonlicensed personnel error. LER 87-19 Continuous fire watch posting not performed in the NS'EB due to licensed operator error. LER 87-33 11 missed hourly fire watches in 77 inspection zones due to administrative problems. Previous LERs on this subject.not referen:cd except for 87-04. LER 87-35 Continuous fire watch ar fire alarm panel abandoned due to nonlicensed operator error. LER 88-09 Missed hourly fire watches on NSEB fire barrier penetrations on 7/21/87 and 7/25/87 due to licensed operator error. LER 88-10 Missed fire watches on 7/14, 7/19, 7/25, 7/27, 7/28, and 8/10/88 due to nonlicensed personnel error. Effluent monitoring deficiencies: LER 86-19 Missed auxiliary building noble gas grab sample due to nonlicensed personnel error. LER 86-22 Missed continuous sampling of the auxiliary building gas due to procedural inadequacies. LER 86~27 Lost data from reactor building duct particulate air sample filter due to nonlicensed personnel error. LER 86-29 Sample valves open on auxiliary building stack exhaust sample line, rendering previous samples inaccurate.
--- ._ '~ .. * . , * . . , LER 86-33 Failure of a continuous noble gas monitor on the reactor building exhaust duct on two occasions, due to loss of electrical Tower when non-safety related loads were applied to a safety related power supply. LER 87-40 Required surveillance (daily source check) not performed from 8/84 to 8/87 on regenerant hold-up tank discharge monitor during periods of known tank activity due to procedural error.. LER 87-43 Unmonitored releases from the auxiliary building during effluent monitor and ventilation system testing due to nonlicensed personnel error. ; LER 87-47 Missed continuous sampling of reactor butiding purge effluent on two occasions due to licensed operator error. LER 88-01 Reactor building effluent particulate filter lest j prior to gross alpha activity analysis due to unknown 3 Causes. ! Causes l Root causes associated with the 84 LERs, categorized on a yearly basis, were: 1986 1987 1988 TOTAL Licensed operator errors 3 7 3 13 , ' Other personnel errors 5 10 3 18 Maintenance errors 0 4 0 4 i Design / installation / fabrication 6 13 2 21 Administrative control problems 5 12 2 19 Random equipment failures 1 1 2 4 Licensee Unidentified 0 1 4 5 Of the 19 administrative control problems identified, 14 were associated with inadequate procedures, and 3 were related to programmatic deficiencies.
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The licensee did not identify root causeo on five LERs. Additionally, the
l supplemental report specified in LER 88-06 (event date 4/14/88) has not yet
been received. LER Quality LER quality has improved since the end of 1986, when the ctility adopted a new
f '
LER format. LERs submitted adequately described the major aspects of each event, including identifying component or system failures that-contributed to the event. The reports were well written, easy to understand, and typically complete except for those with unidentified root causes. Corrective actions
f taken or planned to prevent recurrence were generally specified. However, in
writing the LER text, the use of the word " operator" should be clarified to indicate nonlicensed or Ideensed operator, as requird by 10 CFR 50.73(b)(2)(ii) (J)(2)(iv).
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- - - - _ _ - _ _ - - _ _ _ ' '. . , .. ., . ' . , - a- . , Preliminary Notifications AEOD's review of preliminary notifications issued by Region V concluded that no additional LERs were required of the licensee. l l . **
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, .. - . ' . , i- SMUD ._ SACRAMENTO * ilNICIPAL UTILITY DISTRICT D 6201 S Street, P.o Box 15830, Sacramento CA 958524830.(916)452 3211 AN ELECTRIC SYSTEM SERVING THE h(EART,OF CAllFORNIA CEO 89-236 NAY 11 1989 U. S. Nuclear Regulatory Commission Attn: -J. B. Martin, Regional Administrator Region V .1450 Maria Lane, Suite 210 Halnut Creek, CA 94S96 . ~ Docket No. 50-312 Rancho Seco Nuclear Generating Station License No. DPR-54 SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP) REPORT RESPONSE Dear Mr. Martin: The District has thoroughly reviewed the Commission's SALP Report evaluating Rancho Seco's performance during the period July 1, 1986 through December 31, 1 1988. Overall, the District considers the SALP Board's assessment to be fair, accurate, and technically correct. He appreciate the SALP B3ard's insight in identifying areas for further improvement and recommending appropriate actions. The attached response provides the actions taken or planned to continue improved performance. The District is committed to continuing the established safety culture at Rancho Seco. The success of this effort by the Rancho Seco team is evidenced . by the performance improvement trend recognized by the SALP Board. Our goal is to reach the upper performance quartile for U.S. nuclear plants by 1993. Continued constructive interaction with the Commission will assist us in meeting this goal. Members of your staff with questions requiring additional information or : clarification may contact Mr. Steve Crunk at (209) 333-2935, extension 4913. Sincerely, seph F. Firlit Chief Executive Officer Nuclear ,, f geg_j el e c_t , # ~~ e .: s'r # Attachment O.[F cc w/atch: A. D'Angelo. NRC, Rancho Seco Document Control Desk, Washington DC .m ' _ _ _ __
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{ @ f : * * . - ,, . . . . _l. RANCHO SECO RESPONSE TO 1989 SALP REPORT -
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l The Board recommends that the licensee continue to emphasize improving communication and decisionmaking among mid and upper level plant managers. Action should also be taken to enhance specific plant knowledge among the plant management staff'to improve assessment and recognition of unusual or abnormal plant conditions. j Assessment The District concurs with the analysis and recommendations. Significant improvement in plant operations was noted in the areas of communication / j decisionmaking and plant-specific knowledge among plant management staff. The District will continue its actions to assure improvement, emphasizing communication and decisionmaking (as highlighted by our response to the i December 12 event), commitment tracking, and plant-specific knowledge level of plant management staff. Accomolishmenti Following the December 12, 1988 event, a Management Systems Action Plan was developed to improve leadership, decisionmaking and communications, with emphasis on middle and upper management. The plan was developed based on several independent reviews of the area of concern. Significant accomplishments include: * A formal, senior management monthly review is conducted cr. key performance indicators. Degrading trends are identified and corrective actions are established. * Assistant positions have been established and filled for the CEO, Nuclear, AGM, Nuclear Plant Manager, and AGM, Nuclear Technical Services. This allows senior management more time for communicating with staff and being involved in plant operational decisionmaking. * The CEO, Nuclear has met with shift operating crews. * Management involvement has been increased in the review / approval process for significant evolutions by changing the focus of the Daily Plant Status Meeting attended by senior and middle management. Additionally, the AGM, Nuclear Plant Manager has reviewed the Lessons Learned regarding communication and decisionmaking with Operations management. Operations has lowered the threshold for informing senior management of off-normal conditions. * A training program for decisionmaking has been developed and training classes are beiag scheduled. _1 1 - - _ _ _ _ - - _ _ _ _ - - - _ _ - _ - - - - _ _ _ _ _ _ - - _ _ - _ _
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*> . A. Plant Operations '(Continued) Accomplishments (Continued). To enhance the plant-specific knowledge of plant management' staff, the District implemented an SRO-level training program for managers and staff in July 1988. The first class' completed the six month long, full-time, classroom phase in February 1989; the simulator phase is scheduled for August 1989. Participants included the Assistant Plant Manager, the Plant Per Manager,theMeterialsManager,andtheSupervisorofQualityEng$rmance ineering. Commitment tracking improvements are continuing. An integrated tracking list is produced weekly and a weekly status is provided to senior management. The CEO, Nuclear has issued a directive holding management accountable for meeting- commitments. As a result, the number of overdue commitments has been reduced significantly. ' A Plant Status Control Action Plan and schedule is being implemented, integrating Limiting Conditions for Operation tracking, turnover logs, routine logs, and panel walkdowns. The plan also includes features to minimize errors in status tracking. Plans for Further_ Improvement Plant operations will continue to improve as the Management Systems Action Plan, Plant Status Control Action Plan, Post-Maintenance Testing Action Plan, and management SRO-level training programs are continued. Additiona?ly, the new assistant positions discussed previously are providing senior management opportunity to become more involved in operational decisionmaking and assuring proper communication between middle and upper management. . i i ! -2- _ _ _ _ _ _ _ _ _ - - - _ _ _ _
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. - * f, B. Radiological Controls SALP_EQArd Recommendations _ The licensee needs to continue their efforts in the staffing of Chemistry and
l EM&EP with permanent employees, in the identification and correction of i
deficiencies in the radioactive effluent programs, and in the control of
I liquid waste.
Assessment -
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The District concurs with the performance assessment on radiological controls. Significant improvement continues in correcting organizational weaknesses and the radioactive effluent program. The District's continued actions are highlighted by the recent hiring of a Chemistry Department Manager and filling three Superintendent positions, ' previously staffed with contractors, with qualified permanent SMUD personnel. In addition, numerous effluent modifications were completed that will mitigate the consequences of an uncontrolled spill, decrease the volume of wastewater, and reduce the amount of radioactivity released. Accomplishments Chemistry has developed procedures, instituted programs and hired capable personnel to manage and implement the radioactive effluent program. In addition, a Radiological Effluent Information Management System (REIMS) is being implemented which automatically composes results and discharge permits, generates Semiannual Reports / Effluent Reports, and stores source term and dose information. Some of the majc,r restart enhancements were: e construction of a new makeup demineralized sump, e construction of the C Regenerant Hold-Up Tank (PHUT) for segregation of non-radioactive wastewater; e addition of a demineralized skid to provide effluent processing at the RHUTs, and * installation of an effluent strainer. The Projects Department is coordinating tasks which: * lessen the risk of unplanned offsite releases. * reduce both the volume of wastewater and the activity in wastewater, and * provide wastewater management under Steam Generator Tube Rupture (SGTR) conditions. i To lessen the risk of unplanned site releases, a splash guard was built around the RHUT demineralized. Additionally, the Retention Basins now have a berm surrounding them to reduce the migration of dirt. The moisture separator reheater and turbine deck drains can be rerouted to a controlled sump. Some of the near term tasks include installing an RHUT liner telltale drain and a radwaste solidification structure. -3-
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.', : - ... .. B. ' Radiological Controls (Continued) Accomplishments (Continued) 'To reduce the volume of wastewater, many sample flows, discharges and seal- . ' leakoffs are being routed to the condenser. To reduce the activity of wastewater, filters and a demineralized have been added to the polisher sluice water discharge. Near term tasks include rerouting the auxiliary feedwater (AFH) mini-flow and test lines.to the condensate storage tank. To provide wastewater management under SGTR conditions, a "MO-FLOH" demineralized is on site. This demineralized can process 600 gpm whereas the current demineralized'can process 100 gpm. A Hastewater Treatment Facility will be a long term solution for water management under SGTR conditions. Plans for Further Improvement Technical Specification Amendments and procedure changes needed to resolve longstanding problems regarding analysis sensitivity will soon be in place (LLD values). During the next several months, many of the tasks in progress should be complete. The two long term tasks, the Tank Farm uporade and the Hastewater Treatment Facility, are projected for completion by 1991. . 'E O
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' . l * . ..' . C. Maintenance / Surveillance SALP Board Recommendations Plant management should focus special attention on identification and documentation of discrepant material conditions and improvement in post maintenar.ce testing. Licensee management should continue to emphasize the development of work procedures for specific plant equipment, and to improve personnel performance and proctJure adherence, including the che stry area. Assessment A review of the analysis and recommendations reveals strengths in the Preventive Maintenance Program enhancements, Maintenance Procedures for specific plant equipment, quality control of safety related materials, responsiveness to NRC concerns, and actions to reduce Work Request backlogs. Specific weaknesses include the failure to identify and document material deficiencies, failure to appropriately control Post-Maintenance Testing, one instance of inadequate training of personnel to industry standards, and failure to follow procedures or to have an adequate procedure for the work activity in process. Maintenance Management acknowledges these as valid observations and will continue the Maintenance Improvement Program with special emphasis on the areas identified. Accomolishmenti The District addressed the NRC's concerns about documentation of discrepant material conditions and personnel performance by implementing meetings with all levels of plant personnel. These " Cascade Meetings" are part of the mana;ement communications program designed to reinforce management's policies of quality performance, pride of workmanship, verbatum procedure compliance, and root cause evaluation of failures. Meetings have been conducted at all levels of the organization including follow-up meetings to assure the flow of information has permeated each level of plant personnel. Maintenance Verification Testing requirements are specified on Hork Requests and guidance for those requirements are delineated in the Maintenance Administrative Manual. A Hanagement Event Review Board has been convened including the AGMs, Nanagers, and the CEO, as appropriate, to investigate instances of noncompliance to plant standards of professionalism and assure root causes are thoroughly identified and addressed. Responsibility for preparation and upgrades of Maintenance Procedures has been transferred to the Maintenance Engineering organization to ensure technical adequacy of those procedures issued for use. -5- _ - _ _ _ _ _
. _ _ _ _ - _ _ _ ^: ,. " . L . . ,: . .-- C. Maintenance / Surveillance (Continued) Accomplishments (Continued) The District improved post-maintenance testing by revising Maintenance Administrative Procedure MAP-0006, "Hork Request Planning." The procedure now requires all Work Requests to address Maintenance Verification Testing requirements and provides guidance for establishing those requirements. System Engineers are required to review post-maintenance testing rior to release _of the work package. Plans for Further Improvement The Maintenance Engineering organization is being re-structured to provide a staff of qualified Maintenance Engineers with plant-specific experience at Rancho Seco. The District is emphasizing the development of work procedures by transferring the responsibility for maintenance procedure preparation to the Maintenance organization. A program is in place to write new procedures and upgrade existing procedures prior to field use. This will help assure the technical adequacy of the procedures issued to the field. The Maintenance Improvement Program provides for up to one week of training of all maintenance' craftsmen each five to six week period. ! ,
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'The management involvement meetings will continue to be conducted on a routine basis to reiterate management's policies of profe.<!!cnalism and excellence. The Preventative Maintenance (PM) Group has been chartered to reduce the PM Hork Request backlog and has been provided with Planning personnel dedicated to that purpose. Outage support staffing will be provided to assure readiness of the PM Progrtm to support Cycle 8 refueling outage. -6- - _ _ - _ - .
' * , , N. D. Emergency Preparedness SALP Board Recommendations Contitried management oversite to insure emergency preparedness continues to improve and-that identified problems are corrected in a thorough and timely manner. Accomplishments J During the past six months, the District has filled the open Emergency Preparedness-(EP) positions to approved levels. Dependency on contractor support has been substantially reduced. The increased stability of the EP staff has resulted in improved relations and cooperation with the Rancho Seco Planning Team, including state and county agencies. Since 1986, the EP Section has completely reevaluated and rewritten the Emergency Plan and Implementing Procedures. The Emergency Response Facilities have been upgraded in response to audits and drill comments over the past three years. In recent drills, the number of facilities-related comments has decreased and most of the ccmments concern minor, easily repaired problems. The inventory of emergency equipment has been incorporated into procedures and the frequency of inspections has been increased. The EP Section has completed three successful Annual Exercises since the initiation of the restart effort. The last two exercises were completed without any significant findings. Each year the Section has increased the amount of realism in the scenarios to enhance the drills. EP has implemented a multi-discipline Scenario Review Group that is responsible for approval of all major drills and also assists in the development of technical data. The EP Section now maintains a full-time Emergency Preparedness Planner working in public education in addition to assistance provided by the District's Public Affairs Department.- The addition of this position has enabled the District to expand its public education efforts beyond the 10-mile Emergency Planning Zone. Plans for Further Improvement During 1989, the Department will begin developing an Emergency Preparedness Program Maintenance Manual. This document will provide a guideline for j performing all routine tasks in Emergency Procedures. The Drills and Exercises Coordinator is directing the development of standards for scenario development, which includes specific software applications for data preparation hnd style sheets for date presentation. Also, the Drills and Exercise Group is developing a scenario library to reduce time and cost for scenario development.
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*. , , ; ,. . . > ; ~; , .- . - .. .. D. Emergency Preparedness (Continued) ; I' Plans for Further Improvement (Continued) Emergency Preparedness is evaluating methods to expedite emergency callouts.
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The District is investigating an emergency callout system that utilizes both ! an autodialer and pagers. { The District will begin revising, as necessary, Emergency Preparaginess training modules in 1989 to include better graphics and student Mndouts. The District is evaluating Emergency Response Facilities for possible modifications. A list of proposed modifications has been prepared and is being evaluated and ranked by priority. The Emergency Response Organization is being reviewed for consolidation of functions and reassignment of personnel to more appropriate posittbns. I ) 1 i i i 1 l l l -8-
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_ - _ _ _ - - - . __. -_ _ __ . .. f 1 . ; '. L . , *i, ,_ . * E. Security SALP Board Recommendations ' Licensee management is encouraged. to continue their support to the overall security- program, and to finalize ongoing improvements identified in the Security Performance Improvement Plan, and the responses to the RER report. - Assessment Management support for the program is present, as evidenced in the ' Accomplishments' section. Nevertheless, there are security projects, notably
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the upgrading of site lighting and the completion of the Tank Farm fence
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modifications, which require continuing management support. Accomplishments The District has completed 75 of 79 NRC-recommended improvements. Of the 19 Regulatory Effectiveness Review (RER) commitments, only 4 remain. The District completed Armed Response Force selection and training and improved the weapons mix. i The District installed a Badge Detector. (The badge removal problem has been reduced by 75%.) Improved microwave detection along the entire perimeter was installed. Vital area barriers.throughout the plant have been strengthened. -The District installed a new radio system which is presently operational. Workplace Improvement Network committees have been established and are working well. The District established a compliance auditing program and initiated a QA interface under the auspices of the AGM, Nuclear Quality & Industrial Safety. ' The District selected a new Nuclear Security contractor. Significant improvements in contractor' performance are expected. The Security Training Department and its training programs were upgraded. The upgrades include supervisory training, lesson plans, and trainer certification. Plans for Further Improvement The District has planned and budgeted for site lighting upgrades in 1989 and 1990. An evaluation of vital area penetrations is being conducted and repairs effected. The Tank Farm fence and alarm system upgrade are to be completed by the end of 1989. An evaluation of systems and equipment essential to safe plant shutdown is j currently being performed to determine the adequacy of physical security protection. The District continues to improve its security officer training. A new Security System Upgrade Plan has been prepared by Projects Management, , i incorporating the remaining items from RER and NRC and any new items requiring management attention. ) 9_
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________ * .. . , .- - l i , 4 ,~ 1 F. Engineering / Technical Support SALP BoardJecommendations l Management attention.is needed to maintain a permanent, stable site engineering staff. Engineering efforts to complete the design basis records project'should continue, and a review of the effectiveness of the current design change process should be conducted once a representative sample is available. Management attention is needed to enhance engineeringsoversight of , maintenance activities in light of the Auxiliary Feedwater (AFH) overpressure j event. Assessment The District concurs with the NRC's recommendations. eccomolishmenti A permanent, SMUD Nuclear Engineering Manager was appointed in January. , Additionally,' each discipline engineering Manager and Supervisor is now a l i permanent District employee. Goals for both the retention and hiring of permanent District employees have been established as have goals for the j systematic reduction of contractor dependence. The District's commitment to the timely and satisfactory resolution of Configuration Management / Control issues remains unchanged as defined in the l Engineering Action Plan. Design bases reconstitution and completion of the j System Design Basis documents (SDBDs) remain on schedule. Fourteen SDBDs will - be issued on or before the end of Cycle 8 refueling outage. { Revision 3 to Rancho Seco Administrative Procedure RSAP-0303, ?lant Modifications," was issued as a result of a comprehensive review of the effectiveness of the design change process. The most significant changes in Revision 3 involve the general streamlining of the process and the inclusion of " parts equivalency evaluations" within the scope of the RSAP. These changes were precipitated by lessons learned from the AFH overpressurization event. Similarly, as a result of lessons learned from the AFH event, Plant ' Performance engineers are now required to participate in post-maintenance testing activities. Plans for Further Improvement Aggressive hiring policies will :.ontinue to oe implemented and turnover rates trended. The overall employment picture should imptove in June. The District will continue to adhere to the scope and schedules f(r configuration items defined in the Engineering Action Plan. Additionally, i close monitoring of the design change process will continue with emphasis placed on the trending of related Field Problem Rept,rts (FPRs) and Potential Deviations from Quality (PDQs).
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. .. . ' - F. Engineering / Technical Support. (Continued) Plans for further Improvement (Continued) Further improvement and strengthening of the Engineering / Maintenance interface is expected by the recent establishment of the on-shift support office and i participation.in turreover meetings. Both Keciear Engineerir.g and Plant ! . Performance personnel tre represented at and participate in these activities, providing input and feedback relative to design, operation, and Maintenance provides a " Maintenance Shift Supervisor" forshift thesupport onjpst issues. office. I ' i i - 11 - - - - _ _
_ _ _ _ _ _ _ _ _ _ , 1 , , .. 1 ,, f , ..., . , . .- . G. Safety Assessment / Quality Verification SALP Board Recommendations The licensee should ensure the full use of the established system to identify and resolve nonconformances. The licensee is encouraged to complete action on the near term commitments as previously agreed upon. Assessment 4 .e Rancho Seco management is keenly aware of the issue of ensuring nonconforming conditions are promptly and accurately reported via the PDQ program. The intent is for all nonconforming conditions to Le reported to plant management for prompt resolution. The fundamental problem is differentiating between a nonconforming condition and a condition which may be corrected by a Work RequGst. The District agrees with the SALP finding of a persistent hesitancy to report nonconforming conditions properly. However, the PDQ pror.ess is designed to allow an individual to initiate one document to identify any problem, hardware or nonhardware. The condition noted in the SALP finding is believed to have improved during the latter part of the reporting period after the March 1988 implementation of the PDQ program. In the past six months significant improvements have been made in tracking and resolution of commitments. An attempt is being made to consolidate the existing tracking systems. An integrated commitment tracking list has been provided daily to all managers. Each week a status report on commitments has been provided to senior management. The CEO, Nuclear has issued a directive stating that commitments are to be completed by the due dates and holding ma.N ement accountable to see that commitments are met. Meetings have been held to implement the commitment closure philosophy. As a result of these actions the number of overdue commitments has been reduced significantly and an overall improving trend can be raported. Accomplishments I The implementation of the PDQ program was for the purpose of encouraging the identification of nonconforming conditions. This was accomplished by allowing personnel to initiate just one document whether the problem was hardware or nonhardware. The District later modified the PDQ process to allow personnel to initiate a PDQ on a problem regardless of QA classification.
i This information was given in formal training to site supervisory and
management personnel during October and November 1988. In particular, specific PDQ training has been provided to Maintenance personnel to ensure they understand the importance of properly identifying nonconforming
i conditions. During the period of September - December 1988, ?44 site
personnel received PDQ-specific training. The importance of and the proper process for documenting deficiencies is also being emphasized in General Employee Training sessions. Additionally, Hork Requests are being reviewed to see if PDQs should be initiated. - 12 - - - _ _ - _ - - - _ _ . - _ - _ _
_. _ _ _ _ . _ _ _ _ _ _ _ _ * 't <- ;. . o . * :y , :. ' G. Safety Assessment / Quality Verification (Continued) Accomplishments' (Continued) To further encourage the use of PDQs to report nonconforming conditions, the . PDQ procedure was split.into two procedures, one covering only.the initiation phase of PD0s. This allows personnel to review the procedure and become familiar with PDQ initiation separate from the PDQ processing details. The AGM, Nuclear Quality and Industrial Safety reinforced the importa,1ce of documenting nonconforming conditions in discussions with plant milagement. P1ans'for Further Improvement Rancho Seco will continue PDQ-specific training for non-supervisory personnel. Plant Management will continue to emphasize to plant personnel the. importance of properly identifying nonconforming conditions. Quality Assuranc6 will continuously monitor the program and refine the process as necessary. :
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' .. , H. Startup Testing SAi.P Board Recommendations The licensee's effort in this functional area has been completed except for some minor testing at the 100% power plateau. Lessons learned from this program should be evaluated for application to routine post maintenance testing in light of the auxiliary feedwater overpressurization event. Accomolishmenti J ' The group responsible for the System Review and Test Program (SRTP) which did the startup testing at Rancho Seco transitioned into the Plant Performance Department in late spring of 1988. The personnel core of the SRTP group became the new System Engineers (SEs) of the Department, in order to maintain continuity of the experience gained during the Restart program. Likewise, the success of the testing program which included the ccmponent, functional, and integrated testing of all modified equipment continues by the proceduralization of the entire Special Test Procedure (STP) process. Current procedures control test director qualifications, the procedure format, the review cycles, and the emphasis of Operations personnel involvement. The minor testing that is continuing after the plant reached the maximum power level is receiving a similar amount of review as those tests during the Restart effort. The minor testing includes ICS data gathering for tuning and . high power performance confirmation. ! The District rcvised procedure MAP-0006, "Hork Recuest Planning" to incorporate many of the Lessons Learned from the System Review and Test l Program. To ensure that the Lessons Learned are not limited to o' iy STPs, the SEs have been included in the development of Post-Maintenance Testing (PMT) and Post-Maintenance Verification (PMV). Thus, any maintenance and post- m;intenance testing, including that work considered routine, is reviewed by the SE and may not proceed throagh work planning without his authorization. Additionally, SEs have the responsibility of Dedicated Outage Coordinators (DOCS) who control the scope of system work during the Quarterly System Scheduled outages (OSSs). The return to service of the system and each of the components is also under the guidance of the SE. i ! < - 14 - - _ _ _ _ _
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