ML20247H555

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Advises That Util 890511 Response to SALP Meeting Rept 50-312/88-39 Appropriate & No Changes to 890328 SALP Board Rept Deemed Necessary
ML20247H555
Person / Time
Site: Rancho Seco
Issue date: 07/21/1989
From: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Keuter D
SACRAMENTO MUNICIPAL UTILITY DISTRICT
References
NUDOCS 8907310063
Download: ML20247H555 (3)


See also: IR 05000312/1988039

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                                        ....+g                                          WALNUT CREEK, CALIFORNIA M8065308
                                                                                                  JUL 211989
                                                Docket No. 50-312
                                               Rancho Seco Nuclear Generatir.g Station
                                                Sacramento Municipal Utility District
                                                14440 Twin Cities Road
                                       . Herald, California 95630-9799
                                              Attention: Mr. D. R. Keuter                                                                                                               i
                                                                   Assistant General Manager
                                                                   Nuclear Plant Manager
                                                Gent'.emen:
                                              This refers to the NRC's Systematic Assessment of Licensee Performance (SALP)
                                                Board Report dated March 28, 1989 for your Rancho Seco Nuclear Generating
                                          . Station and to the written comments provided in your May 11, 1989 letter in
                                                response to the SALP Board's report.
                                              We have reviewed your May 11, 1989 response and have concluded that your
                                                 response was appropriate. Based on discussions held between our respective
                                                staffs, and in the absence of verbal identification of discrepancies within
                                                the report or written comments from you which require resolution, we have
                                                concluded that no changes to.the March 28, 1989 SALP Board Report are deemed                                                            ,
                                                necessary. Related NRC conclusions are presented in Appendix I to this                                                                  l
                                                letter.
                                                                                                                                                                                        1
                                                 In accordance with 10 CFR 2.790(a), a copy of this letter and the enclosures
                                               will be placed in the NRC Public Document Room.
                                                Should you have any questions concerning this letter or Appendix I hereto, or
                                                  the SALP Board's report, we will be pleased to discuss them with you.
                                                                                                           Since ely,
                                                                                                            &      hfM
                                                                                                           J. 3. Martin                                                                 j
                                                                                                           Regienal Administrator                                                       j
                                                                                                                                                                                          i
                                                 Enclosures-                                                                                                                              l
                                                  1. Appendix I, NRC Conclusions                                                                                                          l
                                                 2. SALP Meeting Report No. 50-312/88-39                                                                                                1
                                                 3. Licensee response to SALP Report, dated May 11, 1989                                                                                 j
                                                                                                                                                                                          !
                                                 CC.                                                                                                                                      1
                                                 Steve L. Crunk, Manager, Nuclear Licensing
                                                  State of Californic
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                                                       8907310063 890721                                                                                      #
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       'G. Cook
        B. Faulkenberry
        J. Martin                                                                                                                                                                  :
        R. Nease, NRR                                                                                                                                                              l
        T. Murley, NRR
        NRC Commissioners
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        M. Smith
        J. Zo111 coffer
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                                                     APPENDIX I
                                                   NRC CONCLUSIONS
                                                                                                           i
                 A.    Conments Received From Licensee
                       Sacramento Municipal Utility District's (SMUD) May 11, 1989 response to
                       the Rancho Seco SALP Report presented no objections to the specific
                       content of the report. Because there were no objections, no changes                 .
                       were made to the SALP Report.                                                       l
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    .
                       SMUD did provide c.larifying comments regarding situations described in
      ,                the SALP Report. These clarifications were noted, and will be
                       considered in future inspections.                                                   !
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                .B;    NRC Conclusions Regarding Acceptability of Licensee's Planned
    ,
                       Corrective Actions                                                                 q
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                    ' We concluded that your proposed actions to address areas needing                   ,l
                    , improvement were responsive. We will review your progress..asc.part.of             -{
                       our future inspection program, as appropriate.                                      1
                 C.   : Regional Administrator's Conclusions Based on Consideration of
 ,      3
                       Licensee's Response
           '
                        I have concluded that the overall ratings in the affected areas have not.
                      . changed.
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                                    e                                         ' UNITED STATES
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               .,[                     g.               NUCLEAR REGULATORY COMMISSION
   *
                ~L                  :  j-                                          REGION V
                  %                   g                        1450 MARIA LANE, SulTE 210
                   %                                         WALNUT CREEK, CALIFORMA 94596
                       4 . . . . + ,d                     ,
                                                                                   MAR 2 81989
                        ' Docket No. 50-312
                          Rancho Seco Nuclear Generating Station                                       -
                          Sacramento Municipal Utility District
                         '14440 Twin Cities Road
                          Herald, California 95638-9799
                          Attention: Mr. Joseph F. Firlit                                                              --
                                            Chief Executive Officer, Nuclear
                          Gentlemen:
                          SUBJECT: SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
                          The NRC Systematic Assessment of Licensee Performance (SALP) Board has
                          completed its periodic evaluation of the perfomance of Rancho Seco Nuclear
                          Generating Station _during the period July 1, 1986 through December 31, 1988.
                          The perfomance of Rancho Seco was evaluated in the functional areas of. plant
                          operations, radiological controls, maintenance / surveillance, emergency-
                          preparedness,. security, engineering / technical support, anc safety
                          assessment / quality verification. In addition, the performance of Rancho Seco
                          was also evaluated in a special functional area, startup testing. The
                          extensive startup testing performed necessitated evaluation of this additional
                          functional area. The crite.rfa used in conducting this assessment and the SALP
                          Board's evaluation of your performance in these functional areas are contained
                          in the enclosed SALP report.                           ,
                          Arrangements for a meeting to discuss the results of the SALP Board's
                          assessment will be made with your staff in the near future.                                     i
                          As I discussed with you during our meeting at Rancho Seco on March 2, 1989,
                          SMUD's performance, on balance, since restart in March 1988 has been good and                   !
                          somewhat better than the average of other plants in the Region. The events of                   ;
           -              December 12, 1988 and January 31, 1989 have been recent exceptions to an
                          otherwise strong record of careful operation and testing since restart.
                          Your response to both of those events, however, indicates that SMUD has
                          improved substantially over the last four years.
                          Overall, the SALP Board found your performance to be acceptable and directed
                          toward
                          of strength.  safe facility operation. Your startup testing was perceived as an area
                                               In addition, improved performance was noted in all areas.
                          Specific strengths were noted in the generally professional and knowledgeable                   l
                          conduct of operations by control room operators, the engineering support for
                          the accomplishment of complex plant modifications, and the improved

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                          involvement of the quality department in plant activities.
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                                              However, several concerns were identified by the NRC during this assessment
                                              period which warrant your attention. Concerns comon to several functional
                                              areas were the need for management to encourage greater use of your
                                              nonconforming condition reporting system for identifying and correcting
                                              discrepancies, and the need for management attention in assuring timely
                                              completion of identified corrective actions including commitments to the NRC.   .
                                              A specific weakness in the area of plant operat, ions was the need for improved ;
                                              communication and decision making among mid and upper level plant management.
                                              In the area of radiological controls, continued improvement is needed with
                                              respect to liquid effluent management.
                                              A management sumary of this assessment is provided in Section II of the
                                              enclosed report. Perceived strengths and weaknesses and Board recommendations
                                              are discussed in Section IV, Performance Analysis.
                                              You are requested to provide to this office, within 30 days after our
                                              management meeting, a written response to this report. This response should
                                              describe actions which you have taken or plan to take to provide improved
                                              performance. Actions described in previous correspondence may be included by
                                              reference if appropriate. Your response may also include comments on, or
                                              amplification of, the SALP report as appropriate.
                                              In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2,
                                              Title 10, Code of Federal Regulations, a copy of this letter, the ene.losed
                                              SALP report, and your response will be placed in the NRC's Public Document
                                              Room.
                                              The NRC's Office for Analysis and Evaluation of Opertional Data performed an
                                              assessment of licensee event reports submitted for Rancho Seco. This
                                              assessment was provided as an input to the SALP process; a copy is therefore
                                              provided as Attachment I to the enclosed report.
                                              The response requested by this letter is not subject to the clearance
                                              procedures of the Office of Management and Budget as required by the Paperwork
                                              Reduction Act of 1980, PL 96-511.
                                              Should you have any questions concerning the SALP report, we will be pleased
                                              tc discuss them with you.
                                                                                           [  Si erely,       ,,
                                                                                                         1
                                                                                              Regional Administrator
                                              Enclosure:
                                              SALP Report No. 50-312/88-39
                                              Attachment 1 Enclosed in SALP Report

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                                 SALP BOARD REPORT

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                       U. S. NUCLEAR REGULATORY COMMISSION
                                         REGION V
                  SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
                                       50-312/88-39
                                                                                                                :
                     SACRAMENTO MUNICIPAL UTILITIES DISTRICT
                     RANCHO SECO NUCLEAR GENERATING STATION
                     JULY 1, 1986 THROUGH DECEMBER 31, 1988
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                                                                                            TABLE OF CONTEN1'S
                                                                                                                                                            P,ajte
                            1.           Introduction                                                                                                       1

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                                        A.                      Licensee Activities                                                                         1

l B.. Direct Inspection and Review Activities 2 L [' II. Summary of Results 2 l

                                        A.                      Effectiveness of Licensee Manag*? cat                                                       2
                                    - B.                        Results of Board Assessment                                                                 3
                                         C.                     Changes in SALP Ratings                                                                     4
                            III. Criteria                                                                                                                   4
                            IV.          Performance Analysis                                                                                               5
                                        A. -                    Plant Operations                                                                            5
                                         B.                     Radiological Controls                                                                       9
                                         C.                     Maintenance / Surveillance                                                                  13
                                        D.                      Emergency Preparedness                                                                      15
                                         E.                     Security                                                                                    16
                                         F.-                    Engineering / Technical Support                                                              19
                                         G.                     Safety Assessment / Quality Verification                                                    21
                                         H.                    'Startup Testing                                                                             24
                            V.            Supporting Data and Summaries                                                                                     25
                                        A.                      Enforcement Activity                                                                        25
                                         B.                     Confirmation of Action Letters                                                              26
                                         C.                    .AEOD Events Analysis                                                                        26
                                        D.                      Detailed Description of Licensee Activities                                                 26
                            TABLES
                            Table 1 - Inspection Activities and Enforcement Summary                                                                         29
                             Table 2 - Enforcement Items                                                                                                    30
                            Table 3 - Synopsis of Licensee Event Reports                                                                                    34
                            Attachment 1 - AEOD Review of Licensee Event Reports                                                                            35
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                         1.   INTRODUCTION,
                              The Systematic Assessment of Licensee Performar.ce (SALP) is an NRC staff
                              integrated effort to collect.available observations and data on a
                              periodic basis and evaluate licensee's performance based on this
                              information. The program is supplemental to normal regulatory processes
                              used to ensure compliance with NRC rules and regulations. It is intended
                              to be sufficiently diagnostic to provide a rational basis for allocating
                              NRC resources and to provide meaningful feedback to the licensee's
                              management regarding the NRC's assessment of their facility's performance
                              in each functional area.
                              An NRC SALP Board, composed of the members listed below, met in the
                              Region V office on February 2, 1989, to review observations and data on                                    >
                              the licensee's performance in accordance with NRC Manual Chapter 0516,
                              " Systematic Assessment of Licensee Performance," dated June 6, 1988. The
                              Board's findings and recommendations were forwarded to the NRC Regional
                              Administrator for approval and issuance.
                              This report is the NRC's assessment of the licensee's safety performance                                   j
                              at Rancho Seco for the period July 1, 1986 through December 31, 1988.                                      l
                                                                                                                                         l
                              The SALP Board for Rancho Seco was composed of:                                                            I
                            **A.             E. Chaffee, Acting Director, Division of Reactor Safety and Projects,
                                                                 Region ~V (Board Chairman)
                            **G. W. Knighton, Director,' Project Directorate V, NRR
                            **G. P. Yuhas, Chief, Emergency Preparedness and Radiological Protection                                     j
                                                                 Branch
                             *H. S. North, Acting Chief Facilities Radiological Protection Section
                             *M. D. Schuster, Chief, Safeguards Section
                             *R. Fish, Chief Emergency Preparedness Section
                            **L. F. Miller Jr., Chief, Reactor Projects Section II
                            **R. P. Zimmerman, Reactor Projects Branch
                            **G. Kalman, NRR Project Manager
                            **T.             D'Angelo, Senior Resident Inspector
                            **W. P. Ang, Proj ect Inspector
                             *K. Pendergast Emergency Preparedness Analyst
                             *D. Schaefer, Safeguards Inspector
                             *R. Pate, Chief, Nuclear Materials Safety and Safeguards Branch
                            *6 Denotes voting member in all functional creas.
                              A.                                  Licensee Activities
                                                                   Rancho Seco was in an extended shutdown outage from the start of the
                                                                   evaluation period until March 30, 1988. After being. granted
                                                                   Commission approval, a gradual approach to full power commenced with
                                                                   plant startup on March 30, 1988 until the end of the evaluation
                                                                   period. The gradual approach to full power included a rigorous
                                                                   power acension test program. In general, Rancho Seco operated
                                                                    satisfactorily from March 30, 1988 through December 31, 1988. A
                                                                    detailed discussion of the significant occurrences during the period
                                                                     is provided in Section V.D of this report.

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                                               B.                                                Direct Inspection and Review Activities
                                                                                                 Approximately 15,427 on-site inspection hours were spent in
                                                                                                 performing a total of 100 inspections by resident, region-based,
                                                                                                 headquarters, and contract personnel.                                                     Inspection activity in                                                       each
                                                                                                   functional area is summarized in Table 1.
                                                                                                 The unusually large number of inspection hours was a result of the
                                                                                                  extended SALP interval and a large inspection program prior to
                                                                                                  restart on March 30, 1988.
                           II.                 SUMMARY OF RESULTS
                                              A.                                                  Effectiveness of Licensee Management
                                                                                                  The licensee's management organization stabilized somewhat in mid-
                                                                                                   1987 with the appointment of a Chief Executive Officer (CEO),
                                                                                                  Nuclear on May 4,1987, and the formation of a new organizational
                                                                                                  structure. Subsequent to restart, on June 16, 1988, a new CEO,
                                                                                                  Nuclear was appointed, and the organization's subordinate managers
                                                                                                  have changed assignments, in some cases, as well.
                                                                                                 During this SALP period SMUD senior management initiated several
                                                                                                 major programs for improvement of Rancho Seco performance. These
                                                                                                   included:
                                                                                                   *
                                                                                                                                                     An Action Plan for Performance Improvement
                                                                                                   *
                                                                                                                                                     A Systems Review and Test Program
                                                                                                   *
                                                                                                                                                     An Engineering Action Plan
                                                                                                   *
                                                                                                                                                     A Procurement Action Plan
                                                                                                   *
                                                                                                                                                      Installation and Testing of a Safety Grade Emergency Feedwater
                                                                                                                                                      Initiation and '?nntrol System
                                                                                                    *
                                                                                                                                                       Installation end Testing of Two Additional Emergency Diesel
                                                                                                                                                     Generators
                                                                                                  The improvements undertaken by management are reflected in the
                                                                                                   improved SALP ratings. However, numerous tasks remain to be
                                                                                                   completed by the current management to improve plant reliability.
                                                                                                   Included in these are commitments to the NRC such as the
                                                                                                   establishment of design basis documents, and an effective
                                                                                                   engineering oversight. The need for i>acreased involvement by the
                                                                                                   current senior plant management in important plant evolutions was
                                                                                                   evidenced by the December 12, 1988 feedwater transient. This senior
                                                                                                  management involvement should be in sufficient detail to assure
                                                                                                   greater caution and a more thorough understanding of plant
                                                                                                   activities. Management attention needs to be focused on assuring
                                                                                                   plant standards for performance established by the startup and test
                                                                                                   program for testing are not relaxed as was evident by the auxiliary
                                                                                                   feedwater overpressure event which occurred after the SALP period.
                                                B.                                                 Results of Board Assessment
                                                                                                   The SALP period was unusually long (July 1986 to December 1988) and
                                                                                                    covered a period of plant operations that was characterized by
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                                               several changes in plant management end organization and by diverse
                                               plant evolutions associated with SMUD attempts to upgrade Rancho
                                               Seco following an NRC imposed plant shutdown on December 26, 1985.
                                               The plant restarted in March 1988 and commenced a power ascension
                                               program which was completed in December 1988. This SALP focused on
                                               post-restart operations and on the current management and staff.
                                               Discussions of pre-restart evolutions and performances are included
                                               when these events appeared relevent to the evaluation of currently
                                               existing plant conditions and personnel.
                                               Overall, the SALP Board found the performance of NRC licensed
                                               activities by the licensee to be acceptable and directed toward safe
                                               operation of Rancho Seco. The SALP Board has made specific
                                               recommendations in most functional areas for licensee management
                                               consideration. The results of the Board's assessment of the
                                               licensce's performance in each functional area, including the
                                               previous assessments, are as follows:
                                                                                     Rating    Rating
                                                                                     Last      This
                                                     Functional Area *               Perioi    Period    Trend **
                                               A.    Plant Operations                3         2
                                               B.    Radiological Controls           3         2
                                               C.    Maintenance / Surveillance      3/2       2
                                               D.    Emergency Preparedness          3         2         Improving
                                               E.    Security                        3         2
                                               F.    Engineering / Technical Support 2         2
                                               G.    Safety Assessment / Quality     3         2
                                               H.    Startup Testing                 Not Rated 1
                                               *     Maintenance and Surveillance were separate functional areas
                                                     during the last SALP period. Safety Assessment / Quality
                                                     Verification is a new functional area this period. It is
                                                     similar to, but more comprehensive than, the Quality Programs
                                                     and Adminiscretive Controls Affecting Safety functional area
                                                     which it replaced. Other functional areas rated separately
                                                     during the last SALP period, such as Fire Protection and                   ;
                                                     Training, were evaluated as appropriate within the scope of the
                                                     functional areas listed above.
                                               **    The trend indicates the SALP Board's appraisal of the
                                                     licensee's direction of performance in a functional area near
                                                     the close of the assessment period such that continuation of
                                                     this trend may result in a change in performance level.
                                                     Determination of the performance trend is made selectively and
                                                     is reserved for those instances when it is necessary to focus
                                                     NRC and licensee attention on an area with a declining
                                                     performance trend, or to acknowledge an improving trend in
                                                     licensee performance. It is not necessarily a comparison of
                                                     performance during the current period with that in the previous
                                                     period.
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                                 C.    Changes in SALP Ratings
                                       Performance during this SALP period has inproved from that of the
                                       previous SALP period. These improvements occurred because major
                                       changes were made to equipment, personnel, and programs during-the
                                       extended shutdown. Satisfactory accomplishment of these changes was
                                       indicated by the Nuclear Regulatory Commission's approval of plant   ,
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                                       restart on March 22, 1988. The Plant Operations, Radiological

l Controls, Maintenance, Emergency Preparedness, Security, and Safety

                                       Assessment and Quality Verification areas improved from Category 3
                                                                                                        .
                                       to Category 2 ratings.
                           III. CRITERIA
                                 Licensee performance is assessed in selected functional areas, depending
                                 on whether:the facility is in a construction or operational phase.         l
                                 Functional areas normally represent areas significant to nuclear safety
                                 and.the environment. In this evaluation, a special area of Startup
                                 Testing was added due to the large amount of testing which was conducted
                                 by the licensee prior.to restart in March, 1988.
                                                                                                            !
                                 The following evaluation criteria were used, as applicable, to assess
                                 each functional area:
                                 1.    Assurance of quality, including management involvement and control.
                                 2.    Approach to resolution of technical issues from a safety standpoint.
                                 3.    Responsiveness to NRC initiatives.
                                 4.    Enforcement history.
                                 5.    Operational events (including response to, analysis of, reporting
                                       of, and corrective actions for events).
                                 6.     Staffing (including management).
                                 7.     Effectiveness of tha training and qualification program.
                                 However, the NRC is not limited to these criteria and others may have
                                 been used where appropriate.
                                 On the basis of the NRC assessment, each functional area evaluated was
                                 rated according to three performance categories. The definitions of
                                  thece performance categories are as follows:
                                                                                            ..
                                  Category 1: Licensee management attention and involvement are readily
                                  evident and place emphasis on superior performance of nuclear safety or
                                  safeguards activities, with the resulting performance substantially
                                  exceeding regulatory requirements. Licensee resources are ample and
                                  effectively used so that a high level of plant and personnel performance
                                  is being achieved. Reduced NRC attention may be appropriate.
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                                                   Category 2: Licensee management attention to and involvement in the
                                                   performance of nuclear safety or safeguards activities are good. The
                                                   licensee has attained a level of performance above that needed to meet
                                                   regulatory requirements. Licensee resources are adequate and reasonably
                                                   allocated so that good plant and personnel performance is being achieved.
                                                   NRC attention may;be maintained at normal levels.
                                                  ' Category 3: Licensee management attention to and involvement in the
                                                   performance of nuclear safety or safeguards activities are not
                                                   sufficient. The licensee's performance does not significantly exceed
                                                   that needed to meet minimal regulatory requirements. Licensee resources
                                                   appear to be strained or not effectively used. NRC attention should be
                                                   increased above normal levels.
                                              IV.  PERFORMANCE ANALYSIS
                                                   The following is the Board's assessment of the licensee's performance in                             j
                                                   each of the functional areas, plus the Board's conclusions for each area
                                                   and its recommendations with respect to licensee actions and management
                                                   emphasis.
                                                   A.    Plant Operations
                                                         1.   Analysis
                                                              During the SALP period, approximately 4029 hours of direct
                                                               inspection effort were applied in the Plant Operations area.
                                                               Plant Operations has improved significantly during this SALP
                                                               period. The mo2t important accomplishments were th improved
                                                               professionalism of operators, and the reduction or operator
                                                               errors during intricate plant manipulations. Other strengths
                                                              were observed such as improved equipment control procedures and
                                                               significant upgrading of procedures. However, improved
                                                               communication among managers at different levels in the
                                                               organization appeared warranted.                                                         '
                                                               Prior to plant restart in early 1988, the licensee began a
                                                               performance improvement program designed to enhance the quality                          '
                                                               of future plant operations. The program included:
                                                               (a) Plant Emergency Operating Procedures were completely
                                                                     rewritten in accordance with the latest Babcock and Wilcox
                                                                     and NRC guidance.
                                                               (b) The Safety Parameter Display System (SPDS) was added to                              j
                                                                     enable plant operators to quickly assess critical plant                            j
                                                                     parameters. The system provided Rancho Seco operators                              !
                                                                     with a useful, user friendly display and helped them to                            I
                                                                     respond correctly to transients.                                                   l
                                                                                                                                                        1
                                                               (c) The Technical Specifications (TS) were upgraded in format,                           I
                                                                     Limiting Conditions for Operation (LCO) were added, and
                                                                     previously included LCO's were modified to clarify the
                                                                     Rancho Seco TS.
      _ _ _ _--_--_-__-__- _ _ _ _ _ - _ _ _
 .
     . - _ _ _ _ _
   .
              <.
                   '
      ..
                                                6
   ,        .
                     (d) The licensee requested that Rancho Seco be a lead plant in
                           adopting the " Improved B&W TS" which are currently being
                            finalized by Babcock and Wilcox and the NRC.
                     The resident inspectors observed licensee operation daily,
                     including random backshift observations. Operations staffing
                     was observed to be correct, and operations personnel were
                     consistently observed to be knowledgeable and attentive to
                     plant conditionc. Control room demeanor was always observed to
                     be professional.
                     One negative observation was that during the event on December
                     12, 1988, decision making on the appropriate actions to be
                     taken was made by operations management without the involvement
                     of senior plant management for review.     Senior plant management
                     subsequently recognized this weakness in communications and
                     decision making and established an action plan to improve in
                     this area.
                     Management presence within the plant has steadily increased
                     following the implementation of the licensee's management
                     monitoring program. Frequent tours of the power block by all
                     levels of plant management were observed by the resident
                     inspectors.
                     A weakness existed in the oversight role which plant management
                     performed in its control of the specific plant departments. An
                     example was identified which concerned the progress on near
                     term commitments made to the NRC prior to plant restart in
                     early 1988. The commitments which were made involved
                     improvements to the plant which had been identified by the
                     licensee's programs established as a result of the December 26,
                     1985 event. The inspectors noted that plant management was not
                     knowledgeable of the status of some of the significant
                     commitments which had been made to improve engineering and
                     procurement, in particular. The licensee responded to the
                     issue in a timely fashion with goals established for the
                     facility to complete previously identified items.

l l The licensee's approach to the resolution of operational safety l

                     issues was generally sound. Conservatism was routinely
                     exhibited by the control room staff when the potential for

I safety significant failures existed. During the startup l

                     program, detailed tests such as the Loss of Offsite Power Test,

l Emergency Feedwater Initiation and Control System Test and the

                     Steam Generator Secondary Pressure Test were properly conducted
                     and performed. These tests reed significantly abnormal valve
                     lineups of both the electrical and mechanical plant systems.
                     The December 12, 1988 reactor trip was an exception to this
                     overall trend. In that event, the licensee kept the reactor
                     operating despite a double failure in the controls for the
                      steam supply to the main feedwater pump. Also, the AFW
                     overpressure event demonstrated weakness in the conduct of post
                     maintenance testing.
                                                                                        I

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 ..
               "g ,
                 '
                              *

b .

           >
                                                           7
.- * .
                                                                                                  i
   t                            Throughout this extended SALP period, the licensee's
                                 responsiveness to NRC initiatives has been rapid and thorough,
                                particularly prior to the March 30, 1988 restart of Rancho
                                 Seco. This was evidenced by the implementation of several
                                major programs resulting from NRC observations or inquiries.
                                 These included:
                                 *
                                       An Action Plan for Performance Improvement
                                 *
                                       A Systems Review and Test Program
                                 *
                                       An Engineering Action Plan
                                 *
                                       A Procurement Action Plan
                                 *
                                       Installation and Testing of a Safety Grade Emergency      H
                                       Feedwater Initiation and Control System
                                 *
                                       Insta11acion and Testing of Two Additional Emergency

f Diesel Generators (EDG)

                                 Three Severity Level IV violations were issued during the
                                 assessment period involving the failure to provide reports
                                 required by 10 CFR 50.73. Licensee management satisfactorily
                                 resolved the deficiencies through clarification of their
                                 procedure for controlling notifications to the NRC.
                                 A total of 36 LER's were submitted in this functional area.
                                 Most of the LER's were attributable to personnel error. Nine
                                 of these dealt with fire protection discrepancies that
                                 predominately involved missed fire watches. During these
                                 periods extensive modifications and testing were in process
                                 with the plant in off normal configurations. The remaining
                                 LER's appear to be attributable to weah procedures and isolated
                                 events. Those LERs received additional management attention to
                                 ensure improved performance and procedures. The licensee
                                 developed an Operations Department Action Plan in December 1987
                                 which resulted in improved performance and few LERs since have
                                 related to personnel error or procedural deficiencies.
                                 In the early phases of the test program, a number of
                                 operational errors were committed during testing which
                                 ultimately lead to suspension of testing during the Loss of
                                 Offsite Power tests. In response to the difficulties
                                . experienced at the time, the Operations Department Action Plan
                                 mentioned above was developed. Operator performance since that
                                 time improved considerably with no significant operator errors
                                 being detected.
                                 The licensee conducted an extended power ascension program
                                 which included significant Integrated Control System (ICS)
                                  tuning and two preplanned reactor trips. During this phase,
                                  the control room operators were also challenged by two
                                 unplanned reactor trips, one which led to the reactor coolant
                                  system being on natural circulation. During these events,
                                 performance by the control room personnel was sound and timely
                                  in response to the unexpected plant transients which had
                                  occurred. In addition, the ICS and main feedwater system
                                  caused several plant transients which were correctly addressed
     __-            _ _ - _ .
          ,--------_ __ - - .                                                                                                   .
   . .                                                                                                                            1
                                ..
                                 ,
                                   '                                                     8
       , ~ .
     .
 -
                                     .
                                                              by the plant operators who prevented a reactor trip by quickly
   '
                                                              identifying the condition and correcting the cause for the
                                                              abnormal condition.
                                                              The licensed operator training program was effective during the
                                                              SALP period. This was evidenced by a high pass rate of 90
                                                              percent (9 passes of 10 candidates) on annual requalification
                                                              examinations and a 100 percent pass rate (17 out of 17) on the
                                                              1987 and the 1988 replacement examinations. The licensee has
                                                              started construction of an Engineering and Training a11 ding
                                                             'during this SALP period with completion (ready for training)
                                                              scheduled for the Summer 1990. Arrival and startup of the site
                                                              specific simulator is scheduled for mid-1990. The licensee's
                                                              operations staff has remained stable throughout this SALP
                                                              period. All licensed operator positions are filled and only
                                                              one vacancy occurred in the last year.
                                                              During this SALP period, the licensee's overall fire protection
                                                              program improved. Some deficiencies in fire barriers, fire
                                                              alarm systems, fire suppression systems, fire brigade training
                                                              and the performance of fire pumps continued; however, both a
                                                              plan and resources for correction of these deficiencies were
                                                              established by the liccuaee. Routine and corrective
                                                              maintenance activities appeared to be responsive to the need
                                                              for safe and reliable performance of fire protection systems.
                                                              Conclusion
                                                              Performance Assessment - Category 2
                                                              Board Recommendations
                                                              The Board recommends that the licensee continue to emphasize
                                                              improving communication and decisionmaking among mid and upper
                                                              level plant managers. Action should also be taken to enhance
                                                              specific plant knowledge among the plant management staff to
                                                              improve assessment and recognition of unusual or abnormal plant
                                                              conditions.
                                        B.               Radiological Controls
                                                         1.   Analysis
                                                              A total of thirteen routine and four special inspections were
                                                               conducted by the regional staff during this assessment period
                                                               in the areas of organization and management, occupational
                                                               radiation safety, radiological effluent control _and monitoring,
                                                               radioactive vaste management, transportation of radioactive
                                                               materials, training and qualifications, and confirmatory
                                                              measurements. In addition, the resident inspectors provided
                                                               continuing observations in this area.                               i
                                                               For the last assessment period, the licensee was assigned a         !
                                                               Category 3 rating. The board had recommended that the licensee      f

M - -__ --_--_- - - - -----__------.-sw -- -- - ._. -

                                                                                 - - _ _ _ - _ _ _ _ _ _ _ _ _
  . .,

li -

              '
                
                                             9
    7.      3
          '
  t
                   implement the reorganization of the Chemistry, Radiation
                   Protection and the Technical Support group in a timely fashion,
                   and fill the vacant Chemistry Superintendent's position as
                   quickly as possible; improve.the NRC commitment tracking
                   system; amend the Technical Specifications to improve the
                   Radioactive Environmental Monitoring Program to assure
                   compliance with 10 CFR Part 50, Appendix I; complete the
                   installation and testing of the Post Accident Sampling System
                   (PASS).
                   There has been significant improvement in management support in
                   the. radiological controls area. During the beginning of this
                   assessment period, management was slow in providing the needed
                   support. However, changes in upper management during the last
                   two years have resulted in increased support and improved
                   performance. Specific examples include: implementation of an
                   effective NRC commitment tracking system; demonstration of an
                   operable PASS prior to reactor restart (March 1988); revision
                   of the Technical Specifications and Off-Site Dose Calculations
                   Manual to improve the Radiological Effluent and Environmental
                   Monitoring programs, and assure compliance with 10 CFR 50,
                   Appendix I. The QA organization has been effective in
                   providing independent critical review, particularly, in the
                   area of the radioactive effluent control and monitoring
                   program.    Surveillance conducced by the Corporate Health
                   Physics and Chemistry Services group have been effective in
                   identifying deficiencies _in the radiation protection and
                   effluents pro. grams. A monthly management observation program
                   was instituted which resulted in increased involvement of site
                   management in plant activities. Weekly supervisory plant
                   walkdowns have been effective in identifying and correcting
                   deficiencies and improvement in housekeeping practices.
                   A continuing concern involved the frequent changes in
                   management personnel, organization, and assignment of
                   responsibility for implementation of the radioactive effluent
                   programs. During the latter part of 1987, the responsibility                                -!
                   for offsite dose calculations was transferred from the
                   Radiation Protection Depertment to the Environmental Monitoring                              l
                   6 Emergency Preparedness (EM&EP) Department, with liqufd and
                   gaseous effluent sampling being performed by Radiation
                   Protection, and sample counting by Chemistry. On July 15,                                    i
                                                                                                                '
                   1988, responsibility for implementing the effluents program was
                   transferred to Chemistry. By February 1, 1989, Chemistry will
                   have responsibility for effluent sampling. The instability                                   i
                   resulting from continuing changes in responsibility for
                   management of the effluent programs has inhibited the
                   establishment of a program with well-developed procedures and                                i
                   experienced personnel. Due to these changes, the licensee has
                   not always been timely in responding to and taking corrective
                   action for deficiencies identified through internal
                   assessments. During the last month of this essessment period,
                   the Chemistry group appeared to be aggressively working to
                   develop an effective program.

_ _ .

     .
           e
             *
                                         10
       + .
     .
               On February 4,1988, the licensee experienced an event that
               resulted in a worker receiving a calculated dose to a small
               area of skin of whole body in excess of the quarterly limit
               from a " Hot Particle." Review of this event indicated a lack
               of management oversight with respect to communications,
               training and implementation of the procedures to control hot
               particles. Shortly after the incident, management recognized
               the seriousness of the problem and took prompt and extensive
               corrective actions to prevent recurrence. The licensee
               accelerated implementation of their hot particle program and
               completed training of all onsite workers on the hazards and
               controls related to hot particles by April, 1988.
               The licensee resolved most technical issues with appropriate
               conservatism, technical competence, and supporting
               documentation. This was notably demonstrated in the licensee's
               response and corrective actions to the February 4, 1988 hot
               particle incident. With respect to the effluents program, in
               implementing their new Radiological Effluent Technical
               Specifications (RETS), the licensee identified counting times
               required to meet new lower limit of detection (LLD)
               requirements for radioactive liquid pre-batch releases and       l
               composite samples that were unattainable for certain gamma
               emitting isotopes. The long counting times (about 8 hours)
               resulted in difficulties in making releases in a timely
               fashion. It appeared that the licensee had failed to properly
               evaluate their capabilities for meeting the LLD values prior to
               submission of the request for license amendment. After a more
                thorough review of this matter, the licensee submitted a
               prcposed license amendment changing the LLD for specific
               radionuclides, without affecting the bases of the LLD values,
                thereby reducing the counting times.
                The licensee's responsiveness towards resolving the operational
                aspects of the liquid effluent issue has not been fully
                satisfactory. While many plans have been presented, NRC
                inspection findings, licensee audits and operational events
                continue to reveal the need for additional management
                attention. Changes which would allow operation within the
                envelope of expected events without exceeding 10 CFR 50
                Appendix I values should be completed.
                During this assessment period, the licensee has been generally
                responsive to NRC initiatives and concerns. This included
                implementation of the SALp Board's recommendations from the
                previous assessment, management's continued support of the
                radiation protection program and improvements in facilities and
                management of the dry radioactive waste program. Housekeeping
                has been effective in minimizing contaminated areas. A number
                of long outstanding items have been addressed.
                One Severity Level III, nine Severity Level IV, and six
                Severity Level V violations were issued during this assessment
                period. The Severity Level III violation involved (1) an
                            _ - - _ _ _ _ _ _   ._. _ - . .
          -
    ' il
                V

> .

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  ,        ..
                                                                                      11
        .     ,
                                                            occupational dose to a small area of the skin of the whole body
[                                                           of a worker that exceeded the regulatory limit, . (2) the failure
                                                            to notify an in.fividual in writing of his exposure, (3)la
'
                                                            failure to properly instruct workers in precautions and
                                                            procedures for minimizing exposures when working in a " Hot
                                                            Particle Zone", and (4) the failure of certain individuals to
                                                            adhere to procedures for control of personnel exposure. An
                                                            enforcement conference was held to discuss the apparent
                                                            violations and the licensee's corrective actions to prevent
                                                            recurrence. . Based on the licensee's prompt and extensive
                                                            corrective actions to prevent recurrence, a Notice Of Violation
                                                            was issued without a civil penalty. The other violations
                                                            identified during this long assessment period as indicated in
                                                            Table 2, appeared to be isolated occurrences that did not
                                                            indicate a programmatic breakdown in the management of the
                                                            radiological controls program. In addition, prompt and            I
                                                            effective corrective actions were taken to prevent recurrence.
                                                                                                                              !
                                                            A total of 22 LERs were submitted in this functional area.
                                                            Most of the LERs were attributable to personnel error. One of     1
                                                                                                                              !
                                                            the LERs was related to the Severity Level III violation and
                                                            the others appeared to be isolated events. It appears that
                                                            additional management attention is needed to reduce the number    ;
                                                                                                                              '
                                                            of personnel errors.
                                                            During the early part of this assessment period, several~
                                                            weaknesses were identified in the ALARA program. The              ,
                                                            weaknesses were attributable to a lack of QA involvement,         j
                                                            training for engineers and foremen, and poor planning.
                                                            Management's support for the ALARA program, resulted in the
                                                            implementation of an effective training program for
                                                            supervisors, engineering, and the design review staffs. The
                                                            work planning procedures were revised to include ALARA planning
                                                            in the initial phases of processing work requests. A new ALARA
                                                            Policy was issued and ALARA procedures were revised to
                                                            strengthen the program. For 1986, the licensee expended about
                                                            505 person-rem with a goal of 165 person-rem. In 1987, the        '
                                                             goal vac set at 350 person-rem with 299 person-rem expended.
                                                            For 1988, the licensee's initial goal of 250 person-rem was
                                                            adjusted to 95 person-rem with about 79 person-rem expended as
                                                             of November 30, 1988. The long shutdown time and consequent
                                                             lower source term was a major contributor to the exposure        ;
                                                                                                                              '
                                                             reduction.
                                                            There has been significant instability in organization and        :
                                                             staffing during this assessment period. During most of the       t
                                                             assessment period, the Radiation Protection Manager's (RPM)
                                                             position was filled on a temporary basis by several              1
                                                             individuals. The Chemistry Superintendent's position was         ;
                                                             staffed with contract employees and experienced a high rate of    i
                                                             turnover. The EM&EP group also experienced several management
                                                             and organizational changes. The changes in responsibility for
                                                             management of the effluent programs has been a major
                                                             contributor to these changes. During the last six months, the
                                                                                                                              I
                ___________
    _
                     _    - - _ _ _ _ _ _ _ _ _                 _ _ _ _

,

 ..
        .
                       *
                                                                               12

f;,* .

                                                     Radiation Protection group appears to have stabilized with key

!

                                                     positions staffed with permanent employees that included
                                                    . additions to the technical staff. In July, 1988, the RPM's
                                                     position was filled with a permanent employee, and as of
                                                     October 1988, the EM&EP Manager's position was staffed on a
                                                     permanent basis. - The Chemistry group continues to be staffed
                                                     by contract employees in key supervisory and technical
                                                     positions. The EM&EP Department also has a high number of
                                                     contract employees filling positions.
                                                     The licensee has made significant improvements in the training
                                                     program. During the last year, the licensee has received full
                                                      accreditation of their training programs from the Institute of
                                                     Nuclear Power Operations. A new upgraded General Employee
                                                     Training Program will be initiated in January, 1989. The
                                                      licensee's training and qualification program also included
                                                      contract employees. During this assessment period, there were
                                                      several events where deficiencies in training were identified
                                                      as causitive factors. The licensee took prompt action to
                                                      correct the deficiencies to prevent recurrence.
                                                      The licensee has established a satisfactory program for
                                                      performing radiochemical measurements. Laboratory quality
                                                      control and quality assurance activities were substantially
                                                      improved during this period due to improvements in procedures.
                                                      Inter-laboratory comparisons of radiochemical measurements were
                                                      also improved, as the licensee began participating in a new
                                                      contract laboratory intercomparison program. Onsite
                                                      intercomparisons with NRC measurements were successful.
                                                2.    Conclusion
                                                      Performance Assessment - Category 2
                                                3.    Board Recommendations                                             .
                                                                                                                       l
                                                                                                                       i
                                                      The licensee needs to continue their efforts in the staffing of
                                                       Chemistry and EM&EP with permanent employees, in the
                                                       identification and correction of deficiencies in the
                                                       radioactive effluent programs, and in the control of liquid
                                                      waste.
                         C.                     Maintenance / Surveillance                                              l
                                                1.     Analysis
                                                      During the SALP period, approximately 2096 hours.of direct
                                                       inspection effort were applied in the area of Plant Maintenance
                                                       and Surveillance. Strengths were observed in the work request
                                                       system with the installation of an automated computer based
                                                       generation, tracking and retrieval system for work request
                                                       documents. Preventive maintenance procedures were completely
                                                       revised during this SALP period and included monitoring and     ]
                                                       trending of machine vibration, thermography, oil analyses and
         _ _ _ _ _ -
                 _                                                     -      -   _ . _ _ _ _ _ . -
 k.,
  ,        .
 A         t .
                                             13
    ..   .
       ,
                   mean failure times. A continuing weakness during the SALP
                   period involved the failure to idetaify and document material
                   deficiencies when discovered during' repair or rework of plant                   -
                   equipment. For example, repeated trips of the feedwater heater
                   drain pump were not aggressively investigated.
                   The licensee programs to ensure follow-up and trending of
                   failed surveillance, clearance of equipment, performance of
                   required maintenance and curveillances.'and quality control of
                   safety related materials were found to be adequate in this

., period. A strength was noted in the generation and revision of I maintenance procedures for specific plant equipment. Such

                   procedures had included extensive use of graphics with enlarged
                   views of equipment showing internals. Some weakness was
                   demonstrated in the control of post maintenance testing during
                   the overpressurization of the AFW system after the SALP period
                   ended. Staffing of maintenance and surveillance organizations
                   was considered adequete.
                   The licensee had some difficulty in maintaining secoadary
                   diusolved oxygen levels within procedural requirements late in
                   this asseesment period. On one occasion, feedwater oxygen
                   concentration limits were exceeded with the consent of
                   management. However, the need to exceed the procedural
                   requirement was not recognized as a deficiency to be evaluated

L by the licensee's deficiency reporting system.

                   Licensee manaFement was actively involved in the scheduling and                  j
                   coordination c; :aintenance and surveillance activities. The
                   licensee was considered to be responsive in addressing NRC
                   concerns. Maintaining and utilizing current day industry
                    standards for preventive and predictive maintenance activities
                   appeared to be a goal of the Maintenance Department management.
                   Action was also taken to reduce work request backlogs, to                        i
                   control and reduce valve packing leaks, and to successfully                      !
                    conduct a secondary side hydrostatic test of the Main Steam
                    system following the large number of significant modification
                   made to that system.
                   The principal maintenance weaknees observed during this SALP
                    period was insufficient identification and focumentatiou of
                    deficiencies observed during the conduct of planned work
                    activitios or plant evolutions. For example, as discussed
                    above, difficulty in maintaining secondary side chemistry was
                    not documented as required. Another example was the licensee's
                    failure to recognize that improperly sized packing had been
                    used for the repacking of the auxiliary feedwater pumo during a
                    repair effort. Subsequent failure of the pump seal was
                    encountered during a start of the pump due to this error. As
                    noted above, after the SALP period, the overpressurization of
                    AFW indicated post maintenance testing as another area of                       !
                    significant concern.
                                                                                                    l

L_-___-__-_______

                               -      -    . . - .                -
         4
                                 e
                                   
;             p.,                                                               14
                                                       An industry accredited training program for maintenance and
                                                       surveillance personnel was developed and initiated. However,
     s              ,                                  the training of these personnel was deficient on at least one
                                                       occasion late in the period in that maintenance personnel and
                                                       supervisors did not reject kinked hydraulic hoses that they
                                                       were aware of on a feedwater valve controller.
                                                                                                                        ;
                                                       Ten Severity Lev 21 IV and two Severity Level V violations, and
                                                       one deviation wsre issued during the SALP period. The majority
                                                       of the enforcement action was related to a failure to follow
                                                       procedures or to have an adequate procedure for the work
                                                       activity in process. While neue of the violations was
                                                       individually indicative of a programmatic breakdown, taken
                                                       collectively it appears that additional management attention is
                                                       needed.to reduce the number of maintenance personnel errors.
                                                       During the SALP period, 20 LER's were issued.in the area of
                                                       maintenance and surveillance. Of these 20 LER's, six involved
                                                       personnel error, 4 involved installation error, nine involved
                                                       defective procedures and one involved a component failure. The
                                                       LER's adequately described the major aspects of the events and
                                                       the corrective actions taken or planned to prevent recurrence.
                                                       Extensive maintenance program development (which included
                                                       procedure revisions) appeared to have resolved the conditions
                                                       which were reported.
                                                       Conclusion
                                                       PerformanceIAssessa--? - Category 2
                                                       Board Recommendations
                                                       Plant management should focus special attention on
                                                        identification and documentation of discrepant material
                                                       conditions and improvement in post maintenance testing.
                                                       Licensee management should continue to emphasize the
                                                       development of work procedures for specific plant equipment,
                                                       and to improve personnel performance and procedure adherence.
                                                        including the chemistry area.
                                        D.         Emergency Preparedness
                                                   1.  Analysis
                                                       The area of emergency preparedness (EP) was the subject of 12
                                                        inspections, including the observation of three (3) exercises,
                                                        during this SALP period. These inspections represented
                                                        approximately 590 hours of direct inspection effort. The
                                                        resident inspectors assisted the regional inspectors in
                                                        accomplishing the inspections. The previous SALP assessment
                                                        concluded that the performance in the area of EP was a Category
                                                        3.  Recommendations to improve management support and oversite
                                                        in numerous areas of the EP program uere made to Flant
                                                        Management by the previous SALP report.

- - - _ _ _ - - _ _ - _ _ _ _ _

                                                                                         ._ _ _ _ _
         4
                .
                  *
                                                   15
        ,.    ,
                         There has been a significant improvement in the management
                         support of the emergency preparedness program during the SALP
                         period. At the beginning of the period management support was
                         poor, reflective of the SALP 3 rating. The changes in upper
                         management during the last two years have brought increased
                         support for emergency preparedness to the extent that presently
                         it is considered a strength, particularly with respect to
                         devoting resources necessary to insure an adequate capability
                         is maintained. Considerab]c contractor support was obtained to             l
                         provide adequate support for the changes needed to be made in
                         emergency preparedness. The required changes included a major
                         rewrite of the Emergency Plan and implementing procedures and
                         significant improvements in the records system and emergency
                         preparedness training program.
                                                                                                    l
                         Technical issues associated with dose nssessment and
                         meteorology have been addressed during this SALP period.
                         Needed improvements in the area of meteorology were identifded
                         and are being implem nted. In the interim, the licensee has
                         made adjustments to the dose assessment program to better
                         address the uncertainties in the meteorological drta.
                         The licensee has displayed an increasing responsiveness to NRC
                         initiatives. The changes to the Emergency Plan and
                         implementing procedures that were made support this finding.
                         In addition, the responses to the violations identified during             i
                         the SALP period have been more complete during the latter part             j
                         of the period.
                         Three minor violations of NRC requirements were identified
                         during the course of the assessment period. Two of the
                         violations appeared to result from a failure by middle
                         management (EP management at the time) to asstre identified                ]
                         deficiencies were corrected in a timely and thorough manner.
                         There was considerable variation in the licensee's emergency
                         preparedness staffing during the SALP period. At the beginning
                         of the period the supervision and staffin5 was weak. Shortly
                          thereafter, supervision was strengthened in an effort to
                          correct the many problems that existed. In addition, a uumber
                         of contractor personnel were hired to provide adequate staffing
                          to accomplish the numerous tasks to be performed. During the
                          last half of the SALP period anoervision of emergency
                          preparedness was in a state of fjux due to several persons
                          filling the supervisor'c position. At the present time the
                          staffing appears to have stabilized with the hiring of a new
                          employee to the position of Manager, Environmental Monitoring
                          and Emergency Preparedness. Also, permanent emergency
                          preparedness positions have been established to elirinate most
                          of the need for contractor support.
                                                                                                      !
                          At the beginning of the SALP period the emergency preparedness              j
                          training program was considered to be a significant weakness.               I
                          During the last two years the licensee has expended

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                                                                   _-_.     --     _ _ _ _
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                 .
                           .
                             *
                                                                 16
                     *

1 . .

                       ,
                                       considerable effort to improve this training program. The
                                       program is now well defined and lesson plans have been
                                       prepared. The exercise results have demonstrated the
                                       licensee's ability "s respond to emergencies and identified
                                       areas for improvements.
                                  2.   Performance Rating
                                       Category 2, improving trend.
                                  3.   Board Recommendations
                                       Continued management oversite to incure emergency preparedness
                                       continues to improve and that identified problems are corrected
                                       in a thorough and timely manner.
                               E. Security
                                  1.  Analysis
                                       During this SALP assessment period, Region V couducted seven
                                       physical security inspections at Rancho Seco. Approximately
                                       460 hours of direct inspection effort were expended by regional
                                       inspectors. In addition, the resident inspectors provided
                                       continuing observations in this trea. There were no material
                                       control and accounting inspections conducted during this                                                j-
                                       assessment period.                                                                                      I
                                                      ~
                                       Thz previous SALP report recommended that licensee management
                                       expand their support to the overall security program. Since
                                       the initial operation of Rancho Seco, the Security Department                                           ,
                                       reported directly to Corporate Security, loccted approximately                                          )
                                       35 miles from the site. In January 1988, the site Security                                               l
                                       Department severed their direct tie with Ca porate Security,
                                       and commenced reporting directly to plant management. Thls
                                       change, together with a major reorganization of the security
                                       organization has improved the efficiency of the Security
                                       Department by realigning key security positions and
                                       responsibilities. The reorganization of the Security
                                       Department has also improved the licensee's ability to
                                       implement remedial measures to correct deficiencies identitied
                                       in the course of both internal and NRC security inspections.
                                       On March 7, 1986, approximately four months prior to this SALP
                                       period, the licensee published a Security Performance
                                       Improvement Plan (SPIP) for security operations at Rancho Seco.
                                       This SPIP identified 79 separate actions the licensee intended
                                       to complete in order to upgrade their security program to
                                       resolve earlier NRC concerns. Additionally, in response to the
                                       'eptet'ser 1987 NRC Regulatory Effectiveness Review (RER)
                                        report, the licensea identified 19 additional actions. The
                                       majority of these actions have been completed, and have
                                       provided the licensee with an increased capability to defend
                                       against the design basis threat.

. - - _ _ _ - _ . _ _

, _ _ _ _ _ _ _ - - - . - -
                                                                                               >
   ..
                   4
                         .
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    .           .
                                                      17
                            The previous SALP report also identified problems with security
                            force training. During this assessment period, as a result of
                            the Security Departments' reorganization, the Training Section
                            assigned a permanent supervisor, increased their training
                            staff, and acquired larger training support facilities.
                            Increased management emphasis resulted in development of a
                            Special Weapons and Tactics (SWAT) security response force, and
                            upgraded annual refresher training.
                            The previous SALP report also encouraged licensee management to
                            increase the frequency of compliance monitoring of the security  ,
                            program. As a result of their SPIp, and the reorganization of
                            their Security Department, the full-time security auditor
                            (assigned to Corporate Security) coordinates his compliance
                            review with the licensee's Quality Assurance Department.
                            Security management has continued to demonstrate a coordinated
                            effort with oth6r plant staff in prevenving safety / security
                            problems at Rancho Seco. Currently, a new site radio
                            communication system is being installed which will increase the
                            overall communication ability of the Operations and Security
                            Departments. The licensee anticipates initial operation of
                            this new radio system by January, 1969.
                            During the assessment period, thirteen information notices
                            related to security were issued. The licensee's actions, as
                            reviewed to date, were found to be appropriate.
                            The enforcement history for the period of Ju..y 1, 1986 through
                                                                           '
                            December 31, 1988 includes five Severity Level IV violations
                            for the licensee's failure to: provide adequate illumination
                            of an area inside the protected area; provide two physical
                            barriers for the protection of vital equipment; provide proper
                            storage protection for safeguards information; deny site access
                            to unauthorized personnel; and, test access alarms for certain
                            vital area portals. Additionally, the enforcement history
                            included one deviation for the licensee's failure to adequately
                            revalidate security badges every 31 days.
                            During this SALP period, Rancho Seco reported 51 safeguards
                            events. Three of these events occurred after the October 1987
                            change in the reporting requirements of 10 CFR 73.71(c), and
                            thus were reported in the Licensee Event Report (LER) format.
                            These events related to: repositioning plant toggle switches
                             (21); unauthorized (mistaken) entry into plant vital areas
                             (14); loss of security computers (4); bomb threats and
                            threatening telephone calls (4); unlocked vital ~ area portals

! (2); inadequate compensatory measures (1); degraded vital a rea j barrier (1); drugs found inside protected area (1); cutting of J equipment wires (1); unescorted visitor inside protected area

                             (1); and security-related document found on site (1). The
                            majority (94%) of these events occurred during the first half
                            of the SALP assessment period.

I _ - -

        _ - _ _ _ _ _ - = _ _ _ _ _ _ _ _ _ _ _ .                                                                                         _             _       _             _ __            . _ _ . - _ _ _

L' #  ;

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      +
    .              ,                                                                                                                                 18
                                                                          .
 .-
                                                                                                                           In response to the August 1986, NRC policy statement on Fitness
                                                                                                                           for Duty of nuclear power plant personnel, licensee management
                                                                                                                           continues to support their established Fitness for Duty
                                                                                                                           Program. This program, applicable to all licensee and contract
                                                                                                                           personnel, consists primarily of: Pre-Employment Drug
                                                                                                                           Screening; Medical Clarification Examinations; Routine Testing
                                                                                                                           After Employment; For-Cause Drug Testing; and an Employee
                                                                                                                           Assistant Program. The medical clarification examination is
                                                                                                                           administered on a random basis, and consists of a short
                                                                                                                           physical examination designed to determine the presence'of
                                                                                                                           drugs and alcohol in the employee's system, plus a medical /
                                                                                                                           psychological evaluation. Licensee employees who work on or
                                                                                                                           operate vital equipment, and contract employees granted access
                                                                                                                           to site vital areas, qualify for this examination.         If, in the
                                                                                                                           judgement of the examining practitioner, the employee is
                                                                                                                           considered to have indications of drug or alcohol use, the
                                                                                                                           employee is required to submit to a drug and alcohol urine
                                                                                                                           scieen. The routine testing after employment, is required when
                                                                                                                           a physical examination is mandated by a regulatory agency.
                                                                                                                                                                                    .
                                                                                                                           Additionally, the licensee's Program includes the random
                                                                                                                           unannounced use of drug detection dogs inside the' protected
                                                                                                                           area.
                                                                                                                      2.-  Conclusion
                                                                                                                           Performance Assessment - Category 2.
                                                                                                                      3.   Board Recommendation
                                                                                                                           Licensee management is encouraged to continue their support to
                                                                                                                            the overall security program, and to finalize ongoing
                                                                                                                           improvements identified in the Security Performance Improvement
                                                                                                                           Plan, and the responses to the RER report.
                                                                                                     F.               Engineering / Technical Support
                                                                                                                       I-  Analysis
                                                                                                                            puring the SALP period, approximately 1902 hours of direct
                                                                                                                            ins 9cetion effort were applied to the Engineering / Technical
                                                                                                                            Support area. In addition to continuing coverage by the
                                                                                                                            resident inspectors, a NRC Augmented System Review and Test
                                                                                                                            Program (ASRTP) team inspection was performed along with
                                                                                                                            enhanced observation by senior regional staff. The major
                                                                                                                           weakness in this area involved the discovery of significant
                                                                                                                            inadequacies in the control of design and engineering work,
                                                                                                                            largely resulting from a poorly defined plant design basis and
                                                                                                                            insufficient attention to plant design details.        In contrast, a             l
                                                                                                                            strength observed during the latter part of the SALP period
                                                                                                                            involved the self-critical attitude demonstrated by senior SMUD
                                                                                                                           management in acknowledging the need for imprev,'d performance
                                                                                                                            in this area, including engineering reorganization.
                                                                                                                                                                                                              >

- _ - - - _ . - - - - - _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

                                          -_-__ - __ _.         _ - _ _ _            -_       _   _
                                                                                                      - - _ _ . -_-__              ___ _.
  ?       .
                                '                                                            19

j.... . ., 1; 1

                                                        The initial findings of the NRC ASTRP inspection identified
                                                         several weaknesses in engineering involvement in the resolution
                                                        of problems identified by the licensee's systems review and
                                                        test program. The team also identified several deficiencies
                                                        with some engineering analyses for ongoing system
                                                        modifications. SMUD management subsequently developed and
                                                         implemented an innovative Engineering Action Plan (EAP) to
                                                        restore confidence in the Rancho Seco engineering design and
                                                        design process. The EAP included organizational,
                                                        administrative, and cultural changes to provide a better
                                                        definition of responsibility and authority for engineering
                                                        activities.              SMUD also contracted with an independent group of
                                                        technical consultants to perform an expanded ASTRP (EASTRP)
                                                        inspection similar.to the NRC inspection on the remainder of
                                                        the systems not previously inspected by the NRC.
                                                        A revision to the EAP provided further technical aspects of the
                                                        plan.             This included:
                                                        *
                                                               Upgrading the engineering design change process to improve
                                                               the control and quality of future work.
                                                        *
                                                               Review of calculations for technical accuracy and
                                                               completeness.
                                                        *
                                                               Review of technical work performed during the outage to
                                                               assure design adequacy.
                                                        *
                                                               Reestablishment of the plant system design bases.
                                                        The EASTRP was performed and the EAP initiated prior to
                                                        restart.             An evaluation of EASTRP by the NRC ASTRP inspection
                                                        team concluded that the EASTRP inspection process provided
                                                        adequate confidence that any significant problems with the
                                                        design of Rancho Seco were being identified before restart.
                                                        The NRC ASTRP team also assessed the EAP and concluded that the
                                                        EAP appeared to improve the quality of calculations and analyses
                                                        performed. to support system design. Although many aspects of
                                                        the EAP were cotpleted prior to plant restart, many other
                                                        portions of the EAP remain to be completed. The second
                                                        revision of the EAP, dated September 16, 1988, was issued to
                                                        identify items completed and the long range items still to be
                                                        finished. One of the more significant aspects of the EAP that
                                                        remains to be corrpleted is the establishrnent of system design
                                                        basis documents.               The licensee has a;ireed to complete the
                                                        initial portion (14 systems) of this very extensive program by~
                                                        the end of the next refueling outage.
                                                        Plant restart was contingent on several major system additions
                                                        and modifications. Engineering performance to support these
                                                        projects was excellent. Operational scfety was enhanced
                                                        significantly by the addition of the Emergency Feedwater
                                                        Initiation and Control (EFIC) system and the Safety Parameter

- - _ _ _ - - _ - - - _ _ _ - -

 ----        - _                                                                               -
      '
                      .                                                                                                                                             i
                                                       *                                                                20
        +
      .       .
                                                                     .
                                                                                              Display System (SPDS).     Hardware reliability and hu. nan            !
                                                                                              engineering features associated with these, relatively complex,       j
                                                                                              systems are indicative of SMUD's capacity for engineering             1
                                                                                              excellence.                                                           J
                                                                                              The addition of two diesel generators and modifications to the        )
                                                                                              emergency electrical distribution system are additional               j
                                                                                              examples of excellent engineering capability and performance.
                                                                                              Diesel angine vibrations and cable routing discrepancies,
                                                                                              tasked the engineering organizations ability to respond to
                                                                                              unexpected problems. In both instances, these complex issues
                                                                                              were resolved in a thorough and professional manner.
                                                                                              Three enforcement items were identified in this functional
                                                                                              area. Specifically, one Severity Level IV violation was
                                                                                              identified for failure to establish written procedures for
                                                                                              radiographic inspections of decay heat removal pump drain
                                                                                              lines; one Severity Level V violation was identified for an
                                                                                              inadequate drawing - four different welds had two redundant
                                                                                              weld number identifiers; and a deviation was identified for the
                                                                                              use of silicone sealants in the essential HVAC system.
                                                                                              During this SALP period 11 LERS were attributed to this
                                                                                              functional area. All of the LERs resulted from technical
                                                                                              discrepancies such as the lack of channel isolation devices for
                                                                                              two channels of the Reactor Protection System power summing
                                                                                              amplifier.
                                                                                              The extendad' outage during this SALP period required increased
                                                                                              technical manpower to support the varied codifications that
                                                                                              were initiated and completed.     Licensee technical staff was
                                                                                              heavily supplemented by contract personnel to support the
                                                                                              workload. The supplemental contractor work force was reduced
                                                                                              following completion of the modifications and upon plant
                                                                                              restart.    Despite the heavy workload, no significant
                                                                                              discrepancies were attributed to the adequacy of technical
                                                                                              staffing.    Similarly, effectiveness of training and

,

                                                                                              qualifications of the technical staff appeared to be sufficient

I for the technical tasks that were being performed. l The licensee has been very responsive to NRC initiatives and

                                                                                              has taken extensive corrective action to improve the quality of
                                                                                              engineering's activities.     For example a new design control
                                                                                              process utilizing a design change package (DCP) approach was         i

j established. Although the licensee's corrective actions

                                                                                              appeared to be extensive and complete, no new engineering
                                                                                              products were available for audit to determine the
                                                                                              effectiveness of the licensee's revised design control process.
                                                                                              A number of significant weaknesses were identified by both the
                                                                                              NRC and licensee in past procurement practices utilized by the
                                                                                              licensee in the purchase of safety-related parts.        Of specific
                                                                                              concern to the NRC was the practices used to upgrade commerical

i i

          . _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _

r~ - ' l .

                     .
                       '
       ,.          ,
                                                          21

..

                                 grade parts for use in safety-related systems. The practices
                                 utilized in procurement before July, 1987 were not adequate.
                                 The licensee revised their procurement program to incorporate
                                 improved practices to prevent use of substandard parts in
                                 safety related systems.
                                 After the SALP period, the ovarpressurization of the AFW system
                                 event revealed two weaknesses in this area as related to this
                                 event: weak engineering oversight of maintenance activities
                                 and continued weakness in procurement.
                                 Conclusion
                                 Performance assessment - Category 2
                                 Board Recommendation
                                 Management attention is needed to maintain a permanent, stable
                                 site engineering staff. Engineering efforts to complete the
                                 design basis records project should continue, and a review of
                                 the effectiveness of the current design change process should
                                 be conducted once a representative sample is c7ailable.
                                 Management attention is needed to enhance engineering oversight
                                 of maintenance activities in light of the AFW overpressure
                                 event.
                         G. Safety Assessment / Quality Verification
                            1.   Analysis
                                 During the SALP period, approximately 5739 hours of direct
                                 inspection effort were applied in the area of safety
                                 assessment / quality verification. Significant strengths noted
                                 during the SALP period included the implementation of a root
                                 cause analysis process and an aggressive approach by management
                                 to involve outside organizations, mainly INPO, in reviewing
                                 problem areas and providing recommended corrective action.
                                 However, several significant weaknesses were also noted in this
                                 functional area. These included the need for more aggressive
                                 use of the licensee's nonconforming condition reports (termed
                                 potential deviations from quality (FDQs) by SMUD), and a lack
                                 of progress in the completion of several post-restart
                                 commitments such as the creation of design bases.
                                 Over the lengthy evaluation period, many technical submittals
                                 were reviewed by the staff. These included technical
                                 specification change requests, NUREG-0737 itemst exemption and
                                 relief requests, responses to generic letters, licensee
                                 activities related to resolution of safety issues, and
                                 responses to other regulatory initiatives. The plant was shut
                                 down for a significant portion of the evaluation period because
                                 of major problems at the plant that required full technical
                                 resolution prior to restart. Several of these issues involved
                                 a substantial interface with the NRC technical staff. Issues

_ _ _ _ _ - - _ _

                      _ _ - _ - - _ _ _ -
.
    . . .
                                          ..

L? . 22

  -
                                             included addition of two emergency diesel generators,
                                             envf.ronmental qualification, fire protection, upgrades to
                                             emergency feedwater and instrument air systems, addition of
                                             hydrogen recombiners, establishment of a minimum meteorological
                                             monitoring program, system review and test program, reactor
                                             trip system reliability modification, and others.
                                             Licensee submittals were generally found to be adequate and
                                             responsive to the subject matter. Contractor assistance and
                                             licensee management oversight of the. contractors appeared to be
                                             edequate as reflected by the submittals.
                                             A conservative approach to fire protection issues has been
                                             evident. However, two supplemental changes were submitted up
                                             to a year after the original amendment submittal. This was
                                              indicative of a lack of attention to detail. Specifically, all
                                             _ parts of the technical specifications that needed to be changed
                                             were not considered. These changes resulted from oversights
                                              that failed to incorporate original plant areas in tables and    j
                                              charts. This oversight appeared to be inconsistent with other
                                              submittals and was ccasidered to be an isolated case.
                                              Inspection activities during the SALP period resulted in the
                                              identification of twelve enforcement items. Specific
                                              enforcement topics included two Severity Level IV violations
                                              for inadequate closure of nonconforming condition reports;
                                              three Severity Level IV violations for inadequate control of
                                              safety related material in the warehouse; one Severity Level IV
                                             violation for not performing a 10 CFR'50.59 evaluation for
                                              gagging two decay heat removal (DHR) system relief valves; one
                                              Severity Level.IV violation for failure to perform cable
                                              routing inspections; one Severity Level IV violation for
                                              performance of liquid penetrant inspections of the spent fuel
                                              pool liner plate without appropriate acceptance criteria; one
                                              Severity Level IV violation for numerous housekeeping
                                             violations; and one Severity Level V violation for failing to
                                              retain radiographic records of degraded DER lines.
                                              The two violations identified for failing to write
                                              nonconforming condition reports were indicative of a persistant
                                              hesitancy on the part of licensee personnel to report
                                              nonconformances properly. A preference to use work requests
                                              for identifying and correcting nonconforming conditions was
                                              noted on several occasions. This demonstrated the need for
                                              greater management emphasis to ensure nonconformances are
                                              properly identified.
                                                                                                _
                                              No LERs were specifically attributed to this area. However,
                                              weaknesses in the licensee's safety assessment and quality
                                              verification performance contributed to numerous LERs such as
                                              the cable routing problems, the AFW pump packing material
                                              discrepancy, and non-inclusion of containment isolation valves
                                              in the local leak rate test program.
                                                                                                               J
     _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -
 ,     _ _ - - _ _
   .
              *
                                                                             23
              .    .
     *
   .        .
                                                    On several occasions during this SALP period, the licensee
                                                    demonstrated a v1111ngness to review its own programs to
                                                    identify weaknesses. These reviews included EASTRP, INPO
                                                    readiness for operation evaluation, Babcock and Wilcox
                                                    transient assessment team evaluation, and independent
                                                    assessments of the QA program. These reviews demonstrated
                                                    increased willingness by the licensee to be self-critical and
                                                    to learn from the expertise of outside organizations.
                                                    The licensee's quality verification program has shown
                                                    improvement in various areas such as increased on-the-job QC
                                                    inspection of maintenance and modifications, performance of QA
                                                    surveillance and the implementation of a new nonconforming
                                                    condition reporting program.
                                                    In March, aaae and August of 1988, an enhanced operational NRC
                                                    inspection taam evaluated performance of operating crews and
                                                    supporting otAanizations during the plant's power ascension
                                                    from the extended shutdown period. The team observed that the
                                                    Plant Review Committee (PRC) did not include department level
                                                    managers. This weakness has since been corrected by inclusion
                                                    of several department managers on the PRC. During an extendea
                                                    inspection of the Augmented System Review and Test Program
                                                    (ASRTP) between December 1986 and February 1987, it appeared
                                                    that QA and the Management Safety Review Committee (MSRC) did
                                                    not actively review closeout of audit findings. Additionally
                                                    QA audit and surveillance programs were not providing plant
                                                    management with adequate feedback of safety activities.
                                                    Subsequent inspections by the inspection team confirmed that
                                                    these problems had been corrected.
                                                    Staffing, training, and qualifications of the licensee's
                                                    Nuclear Quality Department and Licensing Department appeared to
                                                    be adequate during the SALP period.
                                                    Toward the end of the SALP period, Region V inspections
                                                    observed that the licensee was not completing post-restart
                                                    commitments as scheduled. Management meetings between the
                                                    licensee and NRC Region V, on November 14, 1988, and December
                                                    12, 1988, were held to review SKUD's commitments for work to be
                                                    accomplished post restart, including the various aspects of the
                                                    EAP that remain to be completed. During the meetings, the
                                                    licensee agreed that numerous near and long term items still
                                                    remained to be completed, but reaffirmed its original
                                                    commitment to promptly resolve the near term items.
                                                 2. Conclusion
                                                                                                      ~
                                                    Performance Assessment - Category 2
                                                 3. Board Recommendations
                                                    The licensee should ensure the full use of the established
                                                    system to identify and resolve nonconformances. The licensee

- _- - _ _ _ _ _ _ _ _ _ _ _ _ _

       _      __   _ _ _ _ .
                 .
                             *
    ,                                                           24                                        I
 , _ ,
                                        is encouraged to complete action on the near term commitments
                                        as previously agreed upon.
                                                                                                          I
                               H. Startup Testing                                                          l
                                  Analysis
                                                                                                          l
                                  During the SALP period, significant inspection of startup testing       ]
                                  was performed. Strengths were observed in the integrated system          '
                                  functional testing approach and in the development of a system
                                  status report which documented known past problems with specific        1
                                  plant systems. A significant strength observed was an initiative by     )
                                  the licensee to develop and implement an inspection technique which
                                  was patterned after the NRC's Augmented System Review and Test           j
                                  Program (ASRTP) inspections that identified plant system performance    )
                                  or documentation problems. A weakness identified during the early       )
                                  portion of the SALP period r,'ss the initial planning and completeness  l
                                  of the test program.
                                  The hTC inspected licensee startup testing activities during hot
                                  functional testing and power ascension, with particular attention to
                                  the adequacy of special test procedures and clearance boundaries,
                                  where used. Evaluations were made of the adequacy and depth of the
                                  testing to determine whether the specific system under test was
                                  performing according to the design bases of that system. A specific
                                  strength was noted in the licensee's responsiveness to NRC
                                  identified problems in the Auxiliary Feedwater system and the onsite
                                  electrical distribution system during the ASRTP inspection.
                                  Lfcensee management actively participated in the generation of the
                                  test program purpose and scope. An extensive program was undertaken
                                  to identify and document known past problems with the thirty-three
                                  selected systems which were determined by the licensee to be
                                  important to safety. This high integrity system was used as an
                                  input source to the test program development.
                                  Specific system functions and test requirements were soundly and
                                   thoroughly documented within a system status report (SSR) document.
                                  Technical and management reviews were conducted by the Plant Review
                                  Committee and were effective in identifying potentini underlying
                                   test problems.    10 CFR 50.59 reviews were conducted prior to the
                                   conduct of each test with edequate documentation of the test's
                                   technical rationale. The program was .onducted slowly,
                                  methodically, with high mansgement attention to ensuring preparation
                                   for each testing evolution.
                                   A weakness was observed in the identification and documentation of
                                   conditione which were potentially detrimental to quality.
                                   Spet.f fically, during a portion of the loss ot offsite power testing,

I

                                   a deficiency was identified with an emergency diesel generator. The
                                   deficiency was not reported on the licensee's nonconformance
                                   reporting system. Significant management attention was subsequently
                                   devoted to the identified problem with both the specific hardware
         __ _
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                                                                                                                                                           -      -       - _ _ _ _ _ _ _
    -

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                                                                                                                                   25
                                                                                                                                                                                           i
                                                                                                    deficiency being resolved and the programmatic problem being
                                                                                                    resolved.
                                                                                                    No enforcement action was issued during the SALP period in this
                                                                                                     functional area. Two LER's were submitted documenting e start of
                                                                                                     the emergency diesel generator (emergency safety features -
                                                                                                     equipment start) and a reactor trip following a preplanned turbine
                                                                                                     generator trip. The licensee's corrective action for these LERs was
                                                                                                    appropriate.                                                                          j
                                                                                                    During the period of significant testing, staffing was adequate and
                                                                                                     commensurate with testing in process. Expertise ef the testing
                                                                                                     staff was adequate for both the management of the program and
                                                                                                     conduct of testing.
                                                                                                    Conclusion
                                                                                                    Performance Assessment - Category 1
                                                                                                     Board Recommendations
                                                                                                    The licensee's effort in this functional c.taa has been completed
                                                                                                    except for some minor testing at the 100% power plateau. Lessons
                                                                                                     learned from this program should be evaluated for application to
                                                                                                    routine post maintenance testing in light of the auxiliary feedwater
                                                                                                     overpressurization event.
                                                       V.                                       SUPPORTING DATA AND SUMMARIES
                                                                                                A.   Enforcement Activity
                                                                                                     Three resident inspectors were assigned to Rancho Seco during the
                                                                                                     SALP assessment period. 100 inspections were conducted during this
                                                                                                     lengthy SALP period that encompassed the extended shutdown of Rancho
                                                                                                     Seco. Significant team inspections included:
                                                                                                     *
                                                                                                           Two NRC headquarters Augmented Systems Review and Test Program
                                                                                                           Inspection Teams during 1986 and 1987
                                                                                                     *
                                                                                                           NRC headquarters Operational Readiness Inspection Team in 1988
                                                                                                     *
                                                                                                           NRC headquarters Procurement Inspection Team in 1988
                                                                                                     *
                                                                                                           Regional Enhanced Operational Inspection Team in 1988
                                                                                                     A total of 15,427 hours of direct inspection were performed during
                                                                                                     this SALP period. A summary of inspection activities- is provided
                                                                                                     in Table 1 along with a summary of enforcement items from these
                                                                                                     inspections. A description of the enforcement items is provided in
                                                                                                     Table 2.
                                                                                                B.   Confirmatory Action Letters
                                                                                                                                                                                          ;
          _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _
                                                                                                         . _ _ _ - -_ _ _ _ _ _ _ _ _
,
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         .
                                   .
              *
         .                    .                                               26
                                             One Confirmatory Action Letter (CAL) was issued during this
                                             assessment period. The letter confirmed licensee corrective action
                                             activities for the December 12, 1988 main feedwater pump trip event.
                                             Shortly after the appraisal period ended, a CAL was also issued
                                             concerning the licensee's planned actions following the
                                             January 31, 1989 auxiliary feedwater system overpressurization
                                             event.
                                     C.      AE00 Events Analysis
                                             The Office for Analysis and Evaluation of Operational Data (AE0D)
                                             reviewed the licensee's events at Rancho Seco and prepared a report
                                             which is included as Attachment 1. AEOD reviewed the LERs and
                                             significant operating events for quality of reporting and
                                             effectiveness of identified corrective actions.
                                     D.      Detailed Description of Licensee Activities
                                             *
                                                   Before the December 26, 1985 transient, a number of criteria
                                                   (performance level monitoring, plant performance statistics,
                                                   and systematic assessments of licensee performance had
                                                   indicated that Rancho Seco was below the industry norm for
                                                   similar plants. This, plus a 1984 evaluation by a consultant,
                                                   moved the licensee's Board of Directors to take action to
                                                   improve the performance level at Rancho Seco. Before these
                                                   actions were implemented, a number of undesirable operating
                                                   experiences, culminating in the event of December 26th, further
                                                   demonstrated the need for performance improvement. On the
                                                   basis of the review of the December 26th event by the NRC and
                                                   the utility, the licensee developed the " Rancho Seco Action
                                                   Plan for Performance Improvement."
                                                   The initial portions of that plan were implemented as the Plant
                                                   Performance and Management Improvement Program (PPMIP).              The
                                                   PPMIP was designed to systematically evaluate the plant, its
                                                   systems and their operation, and the management programs and
                                                   organization necessary to support the safe and reliable
                                                   operation of Rancho Seco. The specific goals of the PP&MIP
                                                   were to:      (1) reduce the number of reactor trips, (2) reduce
                                                   challenges to safety systems, (3) ensure that the plant remains
                                                   within allowed ranges of reactor coolant system pressures and
                                                   temperatures immediately following a reactor trip, (4) ensure
                                                   compliance with license requirements, (5) minimize the need for
                                                   operator actions outside the control room, and (6) improve the
                                                   reliability and availability of the plant. On the basis of
                                                   anticipated benefits from the PP&MIP, the licensee established
                                                   near-term performance goals for returning Rancho Seco to power
                                                   operations. Those goals included plant availability exceeding
                                                   60%, a forced outage rate of less than 10%, and fewer than
                                                   three reactor trips per year.                                                        l
                                                                                                                                      l
                                                   During the extended shutdown period, the licensee developed a                      j
                                                   system review and test program (SRTP) the objective of which                       -
                                                   was to demonstrate, before plant restart, that systems
                                                                                                                                        !
                                                                                                                                        i

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ _

                                                     _ _ _ _ _ _ _ - _ - - _ - _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - - _ _
  9.    ,
            *
    *
                                                      27                                                             4
  .   .
                          important to safety were capable of performing their required
                          function. The SRTP was performed by the licensee to provide a
                          comprehensive review and functional demonstration of 33
                          selected systems thac were important to safe plant operation..
                          The licensee's SRTP identified the functional decription for
                          the 33 systems, design changes or modifications required for
                          the systems, testing necessary to demonstrate functions
                          important to safe plant operations, and final acceptance of the
                          systems.
                        *
                          On November 21, 1986, while attempting to fill, vent and
                          pressurize the primary system, approximately 11 of 35
                          pressurizer heater bundles were damaged when the heaters were
                          energized without sufficient water covering them. Operators
                          disregarded correct pressurizer level indications due to
                          incorrect status information for properly functioning level
                          channels. The operators relied on the remaining level channel,
                          which had a drained reference leg caused by loosely controlled
                          troubleshooting of the level channels (operators being unaware
                          of that condition).
                        *
                          On March 15', 1988 and on March 21, 1988, while the plant was in
                          hot standby, letdown system relief valves PSV-22031 (March 15,
                           1988) and PSV-22024 (March 22, 1988) lifted and resulted in a
                          discharge of water from the letdown system to the Reactor
                          Building sump. The cause of both events was a steam / water
                           transient involving isolation of letdown system piping and heat
                          exchangers, flashing of water to steam in the low pressure
                          area, and rapid expansion of the steam.
                        *
                          On August 6, 1988, as part of a planned Emergency Feedwater
                           Initiation and Control System (EFIC) test, the reactor was
                          manually tripped from 80 percent power and EFIC was manually
                           initiated. Both auxiliary feedwater (AW) pumps started as
                          designed. Approximately one hour siter both A W pumps started,
                           smoke was observed in the vicinity of the outboard packing                                !
                           gland of AW pump P318. P318 was immediately secured and the
                           EFIC test was completed using the other AW pump, P319.
                            Subsequent licensee investigation determined that an identical
                          AW pump packing overheating event had previously occurred on
                          July 7, 1988. The event was attributed to the installation of
                            incorrectly sized vendor supplied packing.
                        *
                           On December 12, 1988, while conducting a plant startup, with
                            the reactor at 12 percent power, and one of two Main Feedwater
                             ( W) pumps inoperable, feedwater flow to the Once Theough Steam

l_

                           Generators (OTSG) was reduced significantly by fluctuations of
                            the steam pressure to the operating W pump n.rbine. The
                            reduced W flow resulted in low OTSG 1evels reaching the EFIC
                            system actuation setpoint and initiation of EFIC. Proper OTSG
                             1evels were reestablished by EFIC. The operators subsequently
                           manually tripped the reactor with the belief that main
                             feedwater was no longer available. The initial response of the
                            plant to the reactor trip was normal. However, the licensee

- _ _ _ _ _ - _ - _ _ - _

           _ - _ _ - _ _ _ - - - _ _ _ - _ _ - _ _ _ _ _ _ . _ _ - _                                                       -     _ _ _ .
   :..***-
                                .....
                                                                     *
                                                                                                                                      ~28
  J. * ; O                                                1
                                                                                                                                                                         .
                                                                                                         soon became concerned that the reactor coolant system was       j
                                                                                                         cooling down more than expected, due to continued steaming from
                                                                                                         the."B" OTSG, and, by procedure isolated AFW flow to the "B"
                                                                                                         OTSG. This resulted in emptying the 'B' OTSG for'approximately
                                                                                                                              .
                                                                                                         15 minutes. The licensee located an unexpected' steam demand-
                                                                                                         from the-auxiliary steam supply to the fourth point FW heater,
                                                                                                         isolated the auxiliary steam to the fourth point FW heater, and
                                                                                                         refilled the "B" OTSG. Subsequent licensee analysis attributed-
                                                                                                         the initiation of the event to operator actions while manually
                                                                                                         controlling two different. auxiliary steam pressure reducing
                                                                                                         stations for the steam. supply to the low pressure FW pump
                                                                                                         turbines.
                                                                         *
                                                                                                         On January 31, 1989, after the SALP period..while testing a
                                                                                                         newly installed governor for the. dual-driven auxiliary            ,
                                                                                                         feedwater pump, the steam turbine for the pump oversped. The      i
                                                                                                         auxiliary feedwater system pressure was estimated to have
                                                                                                        . reached approximately 3800 psig for about three minutes. The
                                                                                                         system design pressure is 1325 psig. The NRC and licensee
                                                                                                         investigation of this event revealed weaknesses in post
                                                                                                         maintenance testing, communications, maintenance program, use
                                                                                                         of generic information, and procurement.
                                                                                                                                                                            ;

,. .

                                                                                                                                                                            J
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1 1 ..

                                             =___                      _   ____ -__ -_ - _______ _____-                                  .

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                                                                                                TABLE 1
                                                              INSPECTION ACTIVITIES AND ENFORCEMENT SUMMARY (07/01/86 - 11/30/88)
                                                                                             RANCHO SECO
                                                                                   Inspections Conducted    Enforcement Items
                                                      Functional                   Inspection *     Percent Severity Level **
                                                     Area ***                      Hours          of Effort I    II   III IV     V    D
                                                     A.      Plant Operations        4029            26.1   -     -    -
                                                                                                                              3    -    -
                                                      B.     Radiological            664             4.3    -     -
                                                                                                                        1     9    6    -
                                                             Controls
                                                       C.    Maintenance /           2096            13.6   -     -    -
                                                                                                                             10    2     1
                                                             Surveillance
                                                     D.      Emergency Prep.         590             3.8    -     -    -
                                                                                                                              3    -    -
                                                       E.    Security                407             2.7    -     -    -
                                                                                                                               5   -
                                                                                                                                         1
                                                       F.    Engineering /           1902           12.3    -     -    -
                                                                                                                               1    1    1
                                                             Technical Support
                                                       G.    Safety Assessment /     5739           37.2    -      -   -
                                                                                                                             12     2   -
                                                             Quality Verif.
                                                                                                            _     _    _      _    _    _
                                                                  Totals            15427           100.0               1    43  11      3
                                                       *     Allocations of inspection hours to each functional area are
                                                             approximations based upon NRC form 766 data.
                                                       **    Severity levels are in accordance with NRC Enforcement Policy (10 CFR
                                                             Part 2, Appendix C).
                                                       *** Inspections hours for the special functional area of startup testing were
                                                             not distinguished in the NRC Form 766 data. Those hours were included in
                                                             the other functional areas and predominantly were included in the hours
                                                             for plant operations.
                                                                                                                          ..
                                                                                                                                           l
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                                                                       Table 2
                                                                     Rancho Seco
                                                                  Enforcement Items
                             Report                                                 Severity Functional
                             Number                        Subject                   Level     Area
                               86.27 FAILURE TO REPORT TS TABLE 3.16-1                  4         B
                                      RADIOACTIVE GASEOUS EFFLUENT VIOLATION.
                               86.27 FAILURE TO POST AND CONTROL HI RAD AREA - B        4         B
                                      OTSG IDWER CHANNEL HEAD.
                              86.30 FAILURE TO ESTABLISH WRITTEN PROCEDURES FOR         4         F
                                      RADIOGRAPHIC INSPECTIONS.                                                    !
                               86.30 FAILURE TO RETAIN RADIOGRAPHIC RECORDS OF          5         G                :
                                      DEGRADED DHR DRAIN LINES.                                                    i
                              86.35 INADEQUATE ILLUMINATION INSIDE PROTECTED            4         E
                                      AREA.
                              86.37 PROCEDURES NOT PROVIDED FOR TESTING AND             4         B
                                      CALIBRATING RAD MONITORS R15701 AND 15702.
                              86.37 CLEARLY VISIBLE LABELS FOR LICENSED                 5         B
                                      MATERIAL NOT PROVIDED IAW
                                      10CFR2 0. 2 03 (F) (2 ) '.'
                              86.38 PROCEDURE FOR FUNCTIONAL TESTING OF                 4         C
                                      SNUBBERS DID NOT PROVIDE APPROPRIATE                                         ,
                                      ACCEPTANCE CRITERIA FOR LOCH-UP VELOCITY -                                   ;
                                      VELOCITY NOT CORRECTED FOR TEMPERATURE AS
                                      RECOIDIENDED BY THE VENDOR.
                              87.01 FAILURE TO SPECIFY CONTENT OF EMERGENCY             4         D
                                      PROCEDURES.
                                                                                                                     !
                              87.01 NO PROCEDURE FOR CRIMPING TOOL CALIBRATION          4         C                 l
                                      AND CONTROL.
                              87.01 CR/TSC HVAC HI AIR FLOW RA'E       T DURING         4         C
                                      12-26-85 EVENT.
                              87.02 UNUSUAL EVENT NOT DECLARED FOR SECURITY             4         D
                                      ALER1' AND ESCALATED SECURITY MEASURES.
                              87.03 INADEQUATE DRAWING - REDUNDANT WELD                 5         F
                                      IDENTIFICATION NUMBERS ON SAME DRAWING FOR                                     I
                                      DIFFERENT WELDS.

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                                                                                  - - _ _ _ _ _ _ _ _ _   _ _ _ _ _ _ _ _ _ _ _ _
  .
                         a;
                                                                                                        i
                                  ,
  *                 *
      ;                           87.05 FAILURE TO PERFORM TS REQUIRED SR-89 AND 90                                              4  B
                                          ANALYSIS.
                                  87.05 INADEQUATE YELLOW SHIPPING LABELS FOR                                                    4  B
                                          RADIOACTIVE MATERIAL SHIPMENT.
                                  87.06 STORAGE OF EXPIRED' SHELF LIFE ITEMS NOT                                                 4  G
                                          CONTROLLED.
                                  87.06 FAILURE TO NOTIFY NRC OF ACTUATION OF                                                    4  A
                                          EMERGENCY DIESEL GENERATOR (EDG).-FAILURE
                                          TO REPORT CR/TSC HVAC MALFUNCTION.
    '
                                  87.06"NO PROCEDURE FOR GREEN TAGGING PARTS IN                                                   4 G
                                          WAREHOUSE.
                                  87.06 ABNORMAL TAG NOT WRITTEN FOR TEMPORARY                                                    4 C
                                          MODIFICATION ON "A" TRAIN NUCLEAR SERVICE
                                          RAW WATER SYSTEM.
                                  87.06 VOIDING OF NCR WITHOUT DETERMINING CAUSE OF                                               4 G
                                          EMERGENCY DIESEL GENERATOR NONCONFORMING
                                          CONDITION.
                                  87.06 NCR NOT WRITTEN FOR NON-ISOIABLE PIPE                                                     4 G
                                          LEAKAGE.
                                  87.06 FAILURE TO PROVIDE 10 CFR 50.73 REPORT FOR                                                4 A
                                          MISCELLANEOUS CONDITIONS.
                                  87.07 FAILURE TO PROVIDE TWO PHYSICAL BARRIERS                                                  4 E
                                          FOR PROTECTION OF VITAL EQUIPMENT.                                                          '
                                  87.07 FAILURE TO PROVIDE PROPER STORAGE                                                         4 E
                                          PROTECTION FOR SAFEGUARDS INFORMATION.
                                ' 87.11 SURVEILLANCE PROCEDURES NOT REVISED TO                                                    D C
                                          REQUIRE DOCUMENTATION OF CALIBRATION DATA
                                          IAW COMMITMENT ON PREVIOUS VIOLATION
                                          RESPONSE.
                                  87.13 CLEANLINESS PROCEDURE NOT FOLLOWED FOR A                                                 5  C
                                          CIASS 1 WORK REQUEST.
                                  87.13 LIQUID PENETRANT INSPECTION OF SPENT FUEL                                                4  G
                                          POOL LINER NOT CONTROLLED BY PROCEDURE WITH
                                          APPROPRIATE ACCEPTANCE CRITERIA,
                                  87.13 REPLACEMENT FILTER FOR CBAST ISSUED AND                                                  5  C

'- INSTALLED WITHOUT SMUD ACCEPT TAG. ..

                                  87.14 FAILURE TO WRITE NCR FOR BROKEN REACTOR                                                  5  G
                                          COOIANT PUMP CAPSCREW.                                                                        l
                                                                                                                                      l
                                                                                                                                        :
                                                                                                                                        1
                                                                                                                                        I
                                                                                                                                        <
        - _ _ _ _ _ - _ - _ _ -                 - - _ - _ _ _ _ _ _ - - _ _ - _ .

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        4
                      *
            ,                    87.14 FAILURE TO COMPLY WITH COMMITTED CODES AND     D F
                                        STANDARDS, USE OF SILICONE SEALANTS IN
                                        ESSENTIAL HVAC.
                                 87.16 STROKE TIME NOT MEASURED FOR TESTING OF        4 C
                                        TV-1,2,3,4. SIM-19,20,21,22 NOT FULL STROKE
                                        TESTED EVERY COLD SHUTDOWN.
                                 87.19 LICENSEE FAILED TO CORRECT DEFICIENCIES        4 D
                                        IDENTIFIED DURING 1986 HEALTH
                                        PHYSICS / MEDICAL DRILL.
                                 87.20 HEAT TREATING OF VALVE YOKE WITHOUT            4 C
                                        PROCEDURE.
                                 87.20 FAILURE TO PROVIDE REQUIRED CABLE BEND         4 C
                                        RADIUS AND CABLE TRAY EDGE BUMPERS.
                                 87.21 FAILURE TO PERFORM CABLE ROUTING               4 G
                                        INSPECTIONS DURING 1983-1985 TIME FRAME.
                                 87.22 MISCELLANEOUS VIOLATIONS OF AIARA PROGRAM.     5 B
                                 87.26 RADIOACTIVE MATERIAL INSIDE RV HEAD STAND      4 B
                                        NOT SURVEYED.
                                 87.26 DAILY SOURCE CHECKS NOT PERFORMED WHEN         4 B
                                        R15020 WAS OPERABLE, RHUT CONTAINED KNOWN
                                        ACTIVITY AND RELEASES MADE VIA THIS
                                        PATHWAY,
                                 87.26 RADIOACTIVE MATERIAL INSIDE RV HEAD STAND      4 B
                                        NOT POSTED AS HIGH RAD AREA.
                                 87.37 FAILURE TO FOLLOW MAINTENANCE WORK REQUEST     4 C
                                        INSTRUCTIONS.
                                 87.37 FAILURE TO WRITE AN NCR FOR CR/TSC             4 G
                                        REFRIGERATION UNIT NONCONFORMING CONDITION
                                        OF AS BUILT WIRING.
                                 87.44 NCR CLOSURE BY QE PRIOR TO COMPLETION OF       4 G

l WORK. CORRECTIVE ACTION INCORPORATED INTO I

                                        ECN WITHOUT PRIOR CLOSURE OF ECN.
                                 88.04 FAILURE TO REVALIDATE SECURITY BADGES EVERY    D E
                                        31 DAYS.
                                 88.04 FAILURE TO DENY SITE ACCESS TO UNAUTHORIZED    4 E
                                        SITE PERSONNEL.                             -
                                 88.06 EXPIRED SHELF LIFE ITEMS IN STOCK. REPEAT      4 G
                                        VIOLATION.
               _ _ - _ _ _ _ -          _ -     _ . - _ _ _ - - _ _ _ _ _ _
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                                         '
                                                                                              -

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                                           88.12 CR/TSC HVAC ACTUATION NOT REPORTED WITHIN         4 A

i FOUR HRS.

                                           88.13 LICENSEE DID NOT MAINTAIN ON FILE RECORDS         5 B

l

                                                     FOR RADIOACTIVE MATERIAL SHIPMENT.

1

                                           88.13 LICENSEE DID NOT OBTAIN WRITTEN                   5 B
                                                     CERTIFICATION FOR EMERGENCY SHIPMENT OF

i RADIOACTIVE MATERIAL.

                                           88.17 FAILURE TO SUBMIT REQUIRED ANNUAL EXPOSURE        5 B
                                                     REPORT.
                                           88.20 FAILURE TO POST, MONITOR, CONTROL HOT             3 B
                                                     PARTICLE ZONE.
                                           88.23 TEMPORARY MODIFICATION FOR AFW PUMP P318          4 C
                                                     OUTBOARD SEAL WAS NOT CONTROLLED AND              !
                                                     DOCUMENTED IAW PROCEDURE.
                                           88.24 INDIVIDUAL DID NOT WEAR TLD IAW RWP.              4 B
                                           88.25 TWO PORTABLE DOSE RATE METERS EXCEEDED            5 B
                                                     CALIBRATION FREQUENCY.
                                           80.29 ALARMS FOR CERTAIN VITAL AREA DOORS NOT           4 E
                                                     TES':lED.
                                           88.31 Calibration interval for EFIC pressure            4 C
                                                     transmitters changed without proper
                                                     approvals required by procedure.
                                           88.32 DHR RELIEF VALVES GAGGED WITHOUT ADEQUATE         4 G
                                                     10 CFR 50.59 REVIEW.
                                           88.33 NUMEROUS HOUSEKEEPING VIOLATIONS -                4 G
                                                     UNSECURED LEAD SHIELDING, UNSECURED ROLLER
                                                     CARTS, LADDER TIED TO SAFETY RELATED
                                                     CONDUIT.
                                           88.33 PDQ FOR FEEDWATER OXYGEN CONCENTRATION NOT        4 G
                                                     DELIVERED TO OPERATIONS TECHNICAL ADVISOR
                                                     WITHIN 4 HOURS AS REQUIRED BY PROCEDURE.
                                                                                                ..

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                                                                                       TABLE 3
                                                              S F PSIS OF RANCHO SECO LICENSEE EVENT REPORTS (LERs)
                                                                                     SALY Cause Code *
                                                      Functional
                                                      Area                      A    B     C    D    E   X           Totals
                                                A.    Plant Operations         11    8     3    3   10   1            36
                                                 B.   Radiological             11    4     -    4    1   2            22
                                                      Controis
                                                 C.   Maintenance /             6    4     -
                                                                                                9    1   -            20
                                                      Surveillance
                                                 D.   Emergency Prep.           -    -     -    -    -   -             -
                                                 E.   Security                  2    -
                                                                                            1   -    -   -
                                                                                                                       3
                                                 F.   Engineering /
                                                      Technical Support         5    4     -
                                                                                                2    -   -
                                                                                                                      11
                                                 G.   Safety Assessment /
                                                                                                                       -
                                                      Quality Verification      -    -     -    -    -   -
                                                                                                                            l
                                                            Totals             35   20     4   18   12   3            92
                                                 The above data are based upon LERs 86-11 through 88-19.
                                                 * Cause Code
                                                 A - Personnel Error
                                                 B - Design, Manufacturing or Installation Error
                                                 C - External Cause
                                                 D - Defective Procedures
                                                 E - Component Failure
                                                 X - Other

l l

                                                                                                               . . .
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                                                     Attachment 1
                                       AEOD Input to SAlp Review for Rancho Seco
                 LER Review
                 During the assessment period, 84 Licensee Event Reports (LERs) were submitted
                 to the NRC. These reports, reviewed by AEOD, consisted of LERs 86-14 through
                 88-16.
                 Significant Events
                 Utilizing AEOD's screening process, the following 18 LERs were categorized as
                 safety significant:                                                               i
                 86-14      Decay heat removal (DUR) system train B rendered inoperable due to a
                             leaking weld on the pump casing drain line, while the train A
                            emergency diesel generator was out-of-service.
                 86-16      Loss of DHR capability for a period of 13 minutes during cold
                            shutdown as result of inadvertent closure of the DHR system suction
                            drop 11ne isolation valve. Electrical arcing from I6C technician
                            troubleshooting activities caused the valve closure.
                 86-25      Spent fuel pool liner leakage while containing 316 spent fuel
                            assemblies. Contaminated water seeped through the concrete walls of
                            the fuel storage building to an uncontrolled storm drain. About 275
                            gallons were released offsite, creating an estimated whole body
                            dose of 0.14 mrem.
                 87-02      Fire protec'cion deficiency involving potential loss of alternate
                             shutdown capability. A control room fire could cause an electrical
                            short in the protective circuitry of a diesel generator's output
                            breaker, causing the breaker to trip. A loss of offsite power is
                            assumed to occur at the same f.ime as the control room fire.
                 87-06      Problems with safety related motor-operated valves identifed in
                            response to IE Bulletin No. 85-03, problems included over thrust
                             conditions, incorrect brate voltage ratings, undersized power
                            cables, lack of stem nut staking, valve internals damage,
                            unqualified operator grease, and incorrect pickup / dropout voltages.
                 87-08      Inadequate automatic sequencing of the high pressure injection pumps
                             onto the emergency diesel generator bus, due to the pump lube oil    l
                            pressure bypass circuits defeating a three second time delay.
                 87-10       Fire protection inadequacy whereby the reactor coola t system high
                            point vent valves were susceptible to opening from electrical
                             shorts.
                 87-11       Safety related snubbers failed functional testing after temperature
                             considerations were factored into lock-up velocity and bleed rated
                             acceptance criteria,

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       4
                                             87-15          Fire protection carbon dioxide deluge system left deactivated
                                                            without appropriate compensatory measures.
                                             87-23          Inadequate electrical isolation on the reactor protection system
                                                            total nuclear power channels. Channel isolation devices required by
                                                            IEEE-279 and General Design Criterion 20 were not provided.
                                                                                                                                 !
                                              87-29         Inadequate surveillance testing of unsupervised control room fire
                                                            alarm annunication circuits. Required monthly testing was not
                                                            performed since 1976.

,  !

                                              87-34         High pressure injection (HP1) pump mini-flow recirculation lines     !
                                                            vere not seismically supported since original plant construction due
                                                            to improper classification. Failure of the lines coincident with a
                                                            LOCA would render HPI capability indeterminate.
                                              87-36         Blockage of bearing cooling water system piping to both reactor      ,
                                                            building spray pumps due to fouling.                                 )
                                              874-41        Non-seismic level switches installed on nuclear service water pumps,
                                                            which could prevent the pumps from starting on a safety features
                                                            actuation signal (SFAS).
                                              87-42         Failure of electrical connectors due to residual coating from
                                                            cleaning solutions. Systems affected included the reactor
                                                            protection system, integrated control system, SEAS, and non-nuclear
                                                                                                                                 i
                                                            instrumentation.
                                              87-44         Loss of nuclear services electric building essential heating.
                                                            ventilation and air conditioning system, due to inadequately
                                                            designed isolation dampers between Seismic I and Seismic II ducts.
                                                                                                                                  1
                                               88-02        10 CFR 21 report regarding a manufacturing defect in undervoltage
                                                            devices, causing improper operation of the control rod drive trip
                                                                      .
                                                            breakers.                                                             j
                                                                                                                                   l
                                               88-11        Auxiliary feedwater pump inoperability due to incorrectly sized       d
                                                            vendor supplied packing in packing gland.
                                              Other Events                                                                         )
                                              AEOD's review also identified the following events, while not necessarily
                                               being individually categorized as safety significant, collectively represent
                                               adverse trends in plant performance worthy of additional plant management
                                                attention.
                                                       Inadequate fire protection compensatory measures:           --              l
                                                           LER 86-18 Disabled smoke detectors in the reactor building with-
                                                                        out compensatory measures (fire watch) due to licensed
                                                                        operator error.
                                                           LER 86+31 Hourly instead of continuous fire watch in 480 volt
                                                                        switchgear room due to licensed operator error.

..

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                                                                                   _ _ _ _ _ _ _ _ _ _
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              LER 86-32 Missed fire watch in the east nuclear services battery
                         room due to nonlicensed personnel error. Additionally,
                         LER 86-18 regarding missed compensatory measures, was not
                         referenced in this LER.
              LER 87-01 Hourly rather than continuous fire watches on 1/17
                         and 1/27/87, due to licensed operator error. No reference
                         to LER 86-18 included.
              LER 87-03 Continuous fire watches not posted on 12/27/86,
                         12/29/86, 12/30/86, 1/2/87, 1/3/87, 1/5/87, and 1/20/87.
              LER 87-04 Abandoned continuous fire watch post in nuclear
                         services electrical building (NSEB) due to nonlicensed
                         personnel error. No reference to the above 1987 similar
                         LERs was provided.
              LER 87-15 Carbon dioxide fire protection systems were
                         deactivated without establishing fire watches on 17
                         occasions in 1/87 and 2/87 due to nonlicensed personnel
                         error.
              LER 87-19 Continuous fire watch posting not performed in the
                         NS'EB due to licensed operator error.
              LER 87-33 11 missed hourly fire watches in 77 inspection zones
                         due to administrative problems. Previous LERs on this
                         subject.not referen:cd except for 87-04.
              LER 87-35 Continuous fire watch ar fire alarm panel abandoned
                         due to nonlicensed operator error.
              LER 88-09 Missed hourly fire watches on NSEB fire barrier
                         penetrations on 7/21/87 and 7/25/87 due to licensed
                         operator error.
              LER 88-10 Missed fire watches on 7/14, 7/19, 7/25, 7/27, 7/28,
                         and 8/10/88 due to nonlicensed personnel error.
          Effluent monitoring deficiencies:
              LER 86-19 Missed auxiliary building noble gas grab sample due
                         to nonlicensed personnel error.
              LER 86-22 Missed continuous sampling of the auxiliary building
                         gas due to procedural inadequacies.
              LER 86~27 Lost data from reactor building duct particulate air
                          sample filter due to nonlicensed personnel error.
              LER 86-29 Sample valves open on auxiliary building stack
                          exhaust sample line, rendering previous samples
                          inaccurate.
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                                                               LER 86-33 Failure of a continuous noble gas monitor on the
                                                                            reactor building exhaust duct on two occasions, due to
                                                                            loss of electrical Tower when non-safety related loads
                                                                           were applied to a safety related power supply.
                                                               LER 87-40 Required surveillance (daily source check) not
                                                                            performed from 8/84 to 8/87 on regenerant hold-up tank
                                                                            discharge monitor during periods of known tank activity
                                                                            due to procedural error..
                                                                LER 87-43 Unmonitored releases from the auxiliary building
                                                                            during effluent monitor and ventilation system testing due
                                                                            to nonlicensed personnel error.
                                                                                                                                             ;
                                                                LER 87-47 Missed continuous sampling of reactor butiding purge
                                                                            effluent on two occasions due to licensed operator error.
                                                               LER 88-01 Reactor building effluent particulate filter lest                   j
                                                                            prior to gross alpha activity analysis due to unknown           3
                                                                            Causes.
                                                                                                                                             !
                                                     Causes
                                                                                                                                              l
                                                    Root causes associated with the 84 LERs, categorized on a yearly basis, were:
                                                                                             1986           1987            1988     TOTAL
                                                     Licensed operator errors                   3              7              3       13   ,
                                                                                                                                           '
                                                    Other personnel errors                      5            10               3       18
                                                    Maintenance errors                          0              4              0        4   i
                                                     Design / installation / fabrication        6            13               2       21
                                                    Administrative control problems             5            12               2       19
                                                     Random equipment failures                  1              1              2        4
                                                    Licensee Unidentified                       0              1              4        5
                                                     Of the 19 administrative control problems identified, 14 were associated with
                                                     inadequate procedures, and 3 were related to programmatic deficiencies.

,

                                                     The licensee did not identify root causeo on five LERs. Additionally, the

l supplemental report specified in LER 88-06 (event date 4/14/88) has not yet

                                                     been received.
                                                    LER Quality
                                                     LER quality has improved since the end of 1986, when the ctility adopted a new

f '

                                                     LER format. LERs submitted adequately described the major aspects of each
                                                     event, including identifying component or system failures that-contributed to
                                                      the event. The reports were well written, easy to understand, and typically
                                                     complete except for those with unidentified root causes. Corrective actions

f taken or planned to prevent recurrence were generally specified. However, in

                                                    writing the LER text, the use of the word " operator" should be clarified to
                                                      indicate nonlicensed or Ideensed operator, as requird by 10 CFR
                                                      50.73(b)(2)(ii) (J)(2)(iv).

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                                    Preliminary Notifications
                                    AEOD's review of preliminary notifications issued by Region V concluded that
                                    no additional LERs were required of the licensee.
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                     SMUD                                                                                         ._
                     SACRAMENTO * ilNICIPAL UTILITY DISTRICT D 6201 S Street, P.o Box 15830, Sacramento CA 958524830.(916)452 3211
                                                              AN ELECTRIC SYSTEM SERVING THE h(EART,OF CAllFORNIA
                      CEO 89-236
                     NAY 11 1989
                      U. S. Nuclear Regulatory Commission
                      Attn: -J. B. Martin, Regional Administrator
                      Region V
                     .1450 Maria Lane, Suite 210
                      Halnut Creek, CA 94S96
      .
                                                          ~
                      Docket No. 50-312
                      Rancho Seco Nuclear Generating Station
                      License No. DPR-54
                      SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP) REPORT RESPONSE
                      Dear Mr. Martin:
                      The District has thoroughly reviewed the Commission's SALP Report evaluating
                      Rancho Seco's performance during the period July 1, 1986 through December 31,                                            1
                      1988. Overall, the District considers the SALP Board's assessment to be fair,
                      accurate, and technically correct. He appreciate the SALP B3ard's insight in
                      identifying areas for further improvement and recommending appropriate
                      actions. The attached response provides the actions taken or planned to
                      continue improved performance.
                      The District is committed to continuing the established safety culture at
                      Rancho Seco.     The success of this effort by the Rancho Seco team is evidenced
                   .  by the performance improvement trend recognized by the SALP Board. Our goal
                      is to reach the upper performance quartile for U.S. nuclear plants by 1993.
                      Continued constructive interaction with the Commission will assist us in
                      meeting this goal.
                      Members of your staff with questions requiring additional information or
    :                 clarification may contact Mr. Steve Crunk at (209) 333-2935, extension 4913.
                      Sincerely,
                         seph F. Firlit
                      Chief Executive Officer
                      Nuclear                     ,,             f      geg_j
                                                     el e c_t
                                                                                                                                               ,
                                                 #            ~~
                                                                 e    .:  s'r
                                            #
                      Attachment                                                      O.[F
                      cc w/atch:    A. D'Angelo. NRC, Rancho Seco
                                    Document Control Desk, Washington DC                                                     .m
                                                                                                                                   '
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                              RANCHO SECO RESPONSE TO 1989 SALP REPORT
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                          A.           Plant Operations
                          SALPBbardRecommendations

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                                                                                                                                                              l
                          The Board recommends that the licensee continue to emphasize improving
                          communication and decisionmaking among mid and upper level plant managers.
                          Action should also be taken to enhance specific plant knowledge among the
                          plant management staff'to improve assessment and recognition of unusual or
                          abnormal plant conditions.                                                                                  j
                          Assessment
                          The District concurs with the analysis and recommendations. Significant
                           improvement in plant operations was noted in the areas of communication /                                                          j
                          decisionmaking and plant-specific knowledge among plant management staff.
                          The District will continue its actions to assure improvement, emphasizing
                           communication and decisionmaking (as highlighted by our response to the                                                            i
                          December 12 event), commitment tracking, and plant-specific knowledge level of
                          plant management staff.
                          Accomolishmenti
                           Following the December 12, 1988 event, a Management Systems Action Plan was
                           developed to improve leadership, decisionmaking and communications, with
                           emphasis on middle and upper management.
                          The plan was developed based on several independent reviews of the area of
                           concern. Significant accomplishments include:
                                           *           A formal, senior management monthly review is conducted cr. key
                                                       performance indicators. Degrading trends are identified and
                                                       corrective actions are established.
                                           *           Assistant positions have been established and filled for the CEO,
                                                       Nuclear, AGM, Nuclear Plant Manager, and AGM, Nuclear Technical
                                                       Services. This allows senior management more time for communicating
                                                       with staff and being involved in plant operational decisionmaking.
                                           *           The CEO, Nuclear has met with shift operating crews.
                                           *           Management involvement has been increased in the review / approval
                                                        process for significant evolutions by changing the focus of the Daily
                                                        Plant Status Meeting attended by senior and middle management.
                                                       Additionally, the AGM, Nuclear Plant Manager has reviewed the Lessons
                                                        Learned regarding communication and decisionmaking with Operations
                                                        management. Operations has lowered the threshold for informing
                                                        senior management of off-normal conditions.
                                           *           A training program for decisionmaking has been developed and training
                                                        classes are beiag scheduled.
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                                     A.      Plant Operations '(Continued)
                                      Accomplishments (Continued).
                                      To enhance the plant-specific knowledge of plant management' staff, the
                                      District implemented an SRO-level training program for managers and staff in
                                      July 1988. The first class' completed the six month long, full-time, classroom
                                      phase in February 1989; the simulator phase is scheduled for August 1989.
                                      Participants included the Assistant Plant Manager, the Plant Per
                                      Manager,theMeterialsManager,andtheSupervisorofQualityEng$rmance                        ineering.
                                      Commitment tracking improvements are continuing. An integrated tracking list
                                        is produced weekly and a weekly status is provided to senior management. The
                                      CEO, Nuclear has issued a directive holding management accountable for meeting-
                                       commitments. As a result, the number of overdue commitments has been reduced
                                       significantly.
                                                                                                                                       '
                                      A Plant Status Control Action Plan and schedule is being implemented,
                                       integrating Limiting Conditions for Operation tracking, turnover logs, routine
                                        logs, and panel walkdowns. The plan also includes features to minimize errors
                                        in status tracking.
                                       Plans for Further_ Improvement
                                        Plant operations will continue to improve as the Management Systems Action
                                        Plan, Plant Status Control Action Plan, Post-Maintenance Testing Action Plan,
                                        and management SRO-level training programs are continued. Additiona?ly, the
                                       new assistant positions discussed previously are providing senior management
                                       opportunity to become more involved in operational decisionmaking and assuring
                                        proper communication between middle and upper management.
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          B.   Radiological Controls
          SALP_EQArd Recommendations
            _
          The licensee needs to continue their efforts in the staffing of Chemistry and

l EM&EP with permanent employees, in the identification and correction of i

          deficiencies in the radioactive effluent programs, and in the control of

I liquid waste.

          Assessment                                                        -

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          The District concurs with the performance assessment on radiological
          controls. Significant improvement continues in correcting organizational
          weaknesses and the radioactive effluent program.
          The District's continued actions are highlighted by the recent hiring of a
          Chemistry Department Manager and filling three Superintendent positions,         '
          previously staffed with contractors, with qualified permanent SMUD personnel.
          In addition, numerous effluent modifications were completed that will mitigate
          the consequences of an uncontrolled spill, decrease the volume of wastewater,
          and reduce the amount of radioactivity released.
          Accomplishments
          Chemistry has developed procedures, instituted programs and hired capable
          personnel to manage and implement the radioactive effluent program. In
          addition, a Radiological Effluent Information Management System (REIMS) is
          being implemented which automatically composes results and discharge permits,
          generates Semiannual Reports / Effluent Reports, and stores source term and dose
          information.
          Some of the majc,r restart enhancements were:
                e   construction of a new makeup demineralized sump,
                e   construction of the C Regenerant Hold-Up Tank (PHUT) for segregation
                    of non-radioactive wastewater;
                e   addition of a demineralized skid to provide effluent processing at
                    the RHUTs, and
                *   installation of an effluent strainer.
          The Projects Department is coordinating tasks which:
                *   lessen the risk of unplanned offsite releases.
                *   reduce both the volume of wastewater and the activity in wastewater,
                    and
                *   provide wastewater management under Steam Generator Tube Rupture
                    (SGTR) conditions.
                                                                                           i
         To lessen the risk of unplanned site releases, a splash guard was built around
          the RHUT demineralized. Additionally, the Retention Basins now have a berm
          surrounding them to reduce the migration of dirt. The moisture separator
          reheater and turbine deck drains can be rerouted to a controlled sump. Some
         of the near term tasks include installing an RHUT liner telltale drain and a
          radwaste solidification structure.
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                          B. ' Radiological Controls (Continued)
                         Accomplishments (Continued)
                       'To reduce the volume of wastewater, many sample flows, discharges and seal-     .
                                                                                                        '
                          leakoffs are being routed to the condenser. To reduce the activity of
                         wastewater, filters and a demineralized have been added to the polisher sluice
                          water discharge. Near term tasks include rerouting the auxiliary feedwater
                          (AFH) mini-flow and test lines.to the condensate storage tank.
                         To provide wastewater management under SGTR conditions, a "MO-FLOH"
                          demineralized is on site. This demineralized can process 600 gpm whereas the
                          current demineralized'can process 100 gpm. A Hastewater Treatment Facility
                          will be a long term solution for water management under SGTR conditions.
                          Plans for Further Improvement
                          Technical Specification Amendments and procedure changes needed to resolve
                          longstanding problems regarding analysis sensitivity will soon be in place
                          (LLD values).
                          During the next several months, many of the tasks in progress should be
                          complete. The two long term tasks, the Tank Farm uporade and the Hastewater
                          Treatment Facility, are projected for completion by 1991.
                                                                .
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                                 C.    Maintenance / Surveillance
                                 SALP Board Recommendations
                                 Plant management should focus special attention on identification and
                                 documentation of discrepant material conditions and improvement in post
                                 maintenar.ce testing. Licensee management should continue to emphasize the
                                 development of work procedures for specific plant equipment, and to improve
                                 personnel performance and proctJure adherence, including the che stry area.
                                 Assessment
                                 A review of the analysis and recommendations reveals strengths in the
                                  Preventive Maintenance Program enhancements, Maintenance Procedures for
                                  specific plant equipment, quality control of safety related materials,
                                  responsiveness to NRC concerns, and actions to reduce Work Request backlogs.
                                  Specific weaknesses include the failure to identify and document material
                                  deficiencies, failure to appropriately control Post-Maintenance Testing, one
                                  instance of inadequate training of personnel to industry standards, and
                                  failure to follow procedures or to have an adequate procedure for the work
                                  activity in process.
                                  Maintenance Management acknowledges these as valid observations and will
                                  continue the Maintenance Improvement Program with special emphasis on the
                                  areas identified.
                                  Accomolishmenti
                                  The District addressed the NRC's concerns about documentation of discrepant
                                  material conditions and personnel performance by implementing meetings with
                                  all levels of plant personnel. These " Cascade Meetings" are part of the
                                  mana;ement communications program designed to reinforce management's policies
                                  of quality performance, pride of workmanship, verbatum procedure compliance,
                                  and root cause evaluation of failures. Meetings have been conducted at all
                                  levels of the organization including follow-up meetings to assure the flow of
                                  information has permeated each level of plant personnel.
                                  Maintenance Verification Testing requirements are specified on Hork Requests
                                  and guidance for those requirements are delineated in the Maintenance
                                  Administrative Manual.
                                  A Hanagement Event Review Board has been convened including the AGMs,
                                  Nanagers, and the CEO, as appropriate, to investigate instances of
                                  noncompliance to plant standards of professionalism and assure root causes are
                                  thoroughly identified and addressed.
                                  Responsibility for preparation and upgrades of Maintenance Procedures has been
                                  transferred to the Maintenance Engineering organization to ensure technical
                                  adequacy of those procedures issued for use.
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                           C.    Maintenance / Surveillance (Continued)
                           Accomplishments     (Continued)
                            The District improved post-maintenance testing by revising Maintenance
                            Administrative Procedure MAP-0006, "Hork Request Planning." The procedure now
                            requires all Work Requests to address Maintenance Verification Testing
                            requirements and provides guidance for establishing those requirements.
                            System Engineers are required to review post-maintenance testing rior to
                            release _of the work package.
                            Plans for Further Improvement
                            The Maintenance Engineering organization is being re-structured to provide a
                            staff of qualified Maintenance Engineers with plant-specific experience at
                            Rancho Seco. The District is emphasizing the development of work procedures
                            by transferring the responsibility for maintenance procedure preparation to
                            the Maintenance organization. A program is in place to write new procedures
                            and upgrade existing procedures prior to field use. This will help assure the
                            technical adequacy of the procedures issued to the field.
                            The Maintenance Improvement Program provides for up to one week of training of
                            all maintenance' craftsmen each five to six week period.                                      !
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                          'The management involvement meetings will continue to be conducted on a routine
                            basis to reiterate management's policies of profe.<!!cnalism and excellence.
                            The Preventative Maintenance (PM) Group has been chartered to reduce the PM
                            Hork Request backlog and has been provided with Planning personnel dedicated
                            to that purpose. Outage support staffing will be provided to assure readiness
                            of the PM Progrtm to support Cycle 8 refueling outage.
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                        D.      Emergency Preparedness
                        SALP Board Recommendations
                        Contitried management oversite to insure emergency preparedness continues to
                        improve and-that identified problems are corrected in a thorough and timely
                        manner.
                        Accomplishments
                                                                                          J
                        During the past six months, the District has filled the open Emergency
                        Preparedness-(EP) positions to approved levels. Dependency on contractor
                        support has been substantially reduced. The increased stability of the EP
                        staff has resulted in improved relations and cooperation with the Rancho Seco
                        Planning Team, including state and county agencies.
                        Since 1986, the EP Section has completely reevaluated and rewritten the
                        Emergency Plan and Implementing Procedures.
                        The Emergency Response Facilities have been upgraded in response to audits and
                        drill comments over the past three years.    In recent drills, the number of
                        facilities-related comments has decreased and most of the ccmments concern
                        minor, easily repaired problems. The inventory of emergency equipment has
                        been incorporated into procedures and the frequency of inspections has been
                        increased.
                        The EP Section has completed three successful Annual Exercises since the
                        initiation of the restart effort. The last two exercises were completed
                        without any significant findings. Each year the Section has increased the
                        amount of realism in the scenarios to enhance the drills. EP has implemented
                        a multi-discipline Scenario Review Group that is responsible for approval of
                        all major drills and also assists in the development of technical data.
                        The EP Section now maintains a full-time Emergency Preparedness Planner
                        working in public education in addition to assistance provided by the
                        District's Public Affairs Department.- The addition of this position has
                        enabled the District to expand its public education efforts beyond the 10-mile
                        Emergency Planning Zone.
                        Plans for Further Improvement
                        During 1989, the Department will begin developing an Emergency Preparedness
                        Program Maintenance Manual. This document will provide a guideline for         j
                        performing all routine tasks in Emergency Procedures.
                        The Drills and Exercises Coordinator is directing the development of standards
                         for scenario development, which includes specific software applications for
                        data preparation hnd style sheets for date presentation. Also, the Drills and
                         Exercise Group is developing a scenario library to reduce time and cost for
                         scenario development.

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                                                             D.       Emergency Preparedness (Continued)                                   ;
                                                                                                                                           I'
                                                              Plans for Further Improvement (Continued)
                                                              Emergency Preparedness is evaluating methods to expedite emergency callouts.

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                                                             The District is investigating an emergency callout system that utilizes both  !
                                                            an autodialer and pagers.                                                      {
                                                           The District will begin revising, as necessary, Emergency Preparaginess
                                                              training modules in 1989 to include better graphics and student Mndouts.
                                                             The District is evaluating Emergency Response Facilities for possible
                                                             modifications. A list of proposed modifications has been prepared and is
                                                              being evaluated and ranked by priority.
                                                             The Emergency Response Organization is being reviewed for consolidation of
                                                              functions and reassignment of personnel to more appropriate posittbns.
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                                    E.    Security
                                    SALP Board Recommendations
                                                                                                                      '
                                    Licensee management is encouraged. to continue their support to the overall
                                    security- program, and to finalize ongoing improvements identified in the
                                    Security Performance Improvement Plan, and the responses to the RER report.
     -
                                    Assessment
                                    Management support for the program is present, as evidenced in the
                                    ' Accomplishments' section. Nevertheless, there are security projects, notably

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                                    the upgrading of site lighting and the completion of the Tank Farm fence

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                                    modifications, which require continuing management support.
                                    Accomplishments
                                    The District has completed 75 of 79 NRC-recommended improvements. Of the 19
                                    Regulatory Effectiveness Review (RER) commitments, only 4 remain.
                                    The District completed Armed Response Force selection and training and
                                    improved the weapons mix.                                                         i
                                    The District installed a Badge Detector.      (The badge removal problem has been
                                    reduced by 75%.)
                                    Improved microwave detection along the entire perimeter was installed. Vital
                                    area barriers.throughout the plant have been strengthened.
                                   -The District installed a new radio system which is presently operational.
                                    Workplace Improvement Network committees have been established and are working
                                    well.
                                    The District established a compliance auditing program and initiated a QA
                                    interface under the auspices of the AGM, Nuclear Quality & Industrial Safety.     '
                                    The District selected a new Nuclear Security contractor. Significant
                                    improvements in contractor' performance are expected.
                                    The Security Training Department and its training programs were upgraded. The
                                    upgrades include supervisory training, lesson plans, and trainer certification.
                                    Plans for Further Improvement
                                    The District has planned and budgeted for site lighting upgrades in 1989 and
                                    1990. An evaluation of vital area penetrations is being conducted and repairs
                                    effected. The Tank Farm fence and alarm system upgrade are to be completed by
                                    the end of 1989.
                                    An evaluation of systems and equipment essential to safe plant shutdown is        j
                                    currently being performed to determine the adequacy of physical security
                                    protection. The District continues to improve its security officer training.
                                    A new Security System Upgrade Plan has been prepared by Projects Management,        ,
                                                                                                                        i
                                    incorporating the remaining items from RER and NRC and any new items requiring
                                    management attention.
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                     F.   Engineering / Technical Support
                     SALP BoardJecommendations                                                          l
                     Management attention.is needed to maintain a permanent, stable site
                     engineering staff. Engineering efforts to complete the design basis records
                     project'should continue, and a review of the effectiveness of the current
                     design change process should be conducted once a representative sample is
                     available. Management attention is needed to enhance engineeringsoversight of       ,
                     maintenance activities in light of the Auxiliary Feedwater (AFH) overpressure    j
                     event.
                     Assessment
                     The District concurs with the NRC's recommendations.
                     eccomolishmenti
                     A permanent, SMUD Nuclear Engineering Manager was appointed in January.            ,
                     Additionally,' each discipline engineering Manager and Supervisor is now a       l
                                                                                                       i
                     permanent District employee. Goals for both the retention and hiring of
                     permanent District employees have been established as have goals for the          j
                     systematic reduction of contractor dependence.
                     The District's commitment to the timely and satisfactory resolution of
                     Configuration Management / Control issues remains unchanged as defined in the    l
                     Engineering Action Plan. Design bases reconstitution and completion of the       j
                     System Design Basis documents (SDBDs) remain on schedule.    Fourteen SDBDs will -
                     be issued on or before the end of Cycle 8 refueling outage.                          {
                     Revision 3 to Rancho Seco Administrative Procedure RSAP-0303, ?lant
                     Modifications," was issued as a result of a comprehensive review of the
                     effectiveness of the design change process. The most significant changes in
                     Revision 3 involve the general streamlining of the process and the inclusion
                     of " parts equivalency evaluations" within the scope of the RSAP. These
                     changes were precipitated by lessons learned from the AFH overpressurization
                     event.
                     Similarly, as a result of lessons learned from the AFH event, Plant              '
                     Performance engineers are now required to participate in post-maintenance
                     testing activities.
                     Plans for Further Improvement
                     Aggressive hiring policies will :.ontinue to oe implemented and turnover rates
                     trended. The overall employment picture should imptove in June.
                     The District will continue to adhere to the scope and schedules f(r
                     configuration items defined in the Engineering Action Plan. Additionally,            i
                     close monitoring of the design change process will continue with emphasis
                     placed on the trending of related Field Problem Rept,rts (FPRs) and Potential
                     Deviations from Quality (PDQs).

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                                    F.    Engineering / Technical Support. (Continued)
                                    Plans for further Improvement (Continued)
                                    Further improvement and strengthening of the Engineering / Maintenance interface
                                    is expected by the recent establishment of the on-shift support office and             i
                                    participation.in turreover meetings. Both Keciear Engineerir.g and Plant               !
                                  . Performance personnel tre represented at and participate in these activities,
                                    providing input and feedback relative to design, operation, and
                                    Maintenance provides a " Maintenance Shift Supervisor" forshift    thesupport
                                                                                                            onjpst issues.
                                    office.
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                                                  G.   Safety Assessment / Quality Verification
                                                  SALP Board Recommendations
                                                  The licensee should ensure the full use of the established system to identify
                                                  and resolve nonconformances. The licensee is encouraged to complete action on
                                                  the near term commitments as previously agreed upon.
                                                  Assessment                                                          4
                                                                                                                     .e
                                                  Rancho Seco management is keenly aware of the issue of ensuring nonconforming
                                                  conditions are promptly and accurately reported via the PDQ program. The
                                                  intent is for all nonconforming conditions to Le reported to plant management
                                                  for prompt resolution. The fundamental problem is differentiating between a
                                                  nonconforming condition and a condition which may be corrected by a Work
                                                  RequGst.
                                                  The District agrees with the SALP finding of a persistent hesitancy to report
                                                  nonconforming conditions properly. However, the PDQ pror.ess is designed to
                                                  allow an individual to initiate one document to identify any problem, hardware
                                                  or nonhardware. The condition noted in the SALP finding is believed to have
                                                  improved during the latter part of the reporting period after the March 1988
                                                  implementation of the PDQ program.
                                                  In the past six months significant improvements have been made in tracking and
                                                  resolution of commitments. An attempt is being made to consolidate the
                                                  existing tracking systems. An integrated commitment tracking list has been
                                                  provided daily to all managers. Each week a status report on commitments has
                                                  been provided to senior management. The CEO, Nuclear has issued a directive
                                                  stating that commitments are to be completed by the due dates and holding
                                                  ma.N ement accountable to see that commitments are met. Meetings have been
                                                  held to implement the commitment closure philosophy. As a result of these
                                                  actions the number of overdue commitments has been reduced significantly and
                                                  an overall improving trend can be raported.
                                                  Accomplishments
                                                                                                                                 I
                                                  The implementation of the PDQ program was for the purpose of encouraging the
                                                  identification of nonconforming conditions. This was accomplished by allowing
                                                  personnel to initiate just one document whether the problem was hardware or
                                                  nonhardware. The District later modified the PDQ process to allow personnel
                                                  to initiate a PDQ on a problem regardless of QA classification.

i This information was given in formal training to site supervisory and

                                                  management personnel during October and November 1988.     In particular,
                                                  specific PDQ training has been provided to Maintenance personnel to ensure
                                                  they understand the importance of properly identifying nonconforming

i conditions. During the period of September - December 1988, ?44 site

                                                  personnel received PDQ-specific training. The importance of and the proper
                                                  process for documenting deficiencies is also being emphasized in General
                                                  Employee Training sessions. Additionally, Hork Requests are being reviewed to
                                                  see if PDQs should be initiated.
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                                      ' G.            Safety Assessment / Quality Verification (Continued)
                                            Accomplishments' (Continued)
                                            To further encourage the use of PDQs to report nonconforming conditions, the
                                       . PDQ procedure was split.into two procedures, one covering only.the initiation
                                             phase of PD0s.      This allows personnel to review the procedure and become
                                             familiar with PDQ initiation separate from the PDQ processing details. The
                                            AGM, Nuclear Quality and Industrial Safety reinforced the importa,1ce of
                                             documenting nonconforming conditions in discussions with plant milagement.
                                             P1ans'for Further Improvement
                                             Rancho Seco will continue PDQ-specific training for non-supervisory
                                             personnel. Plant Management will continue to emphasize to plant personnel the.
                                             importance of properly identifying nonconforming conditions. Quality
                                            Assuranc6 will continuously monitor the program and refine the process as
                                             necessary.
                                                                                                                            :

I

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                      H.  Startup Testing
                      SAi.P Board Recommendations
                      The licensee's effort in this functional area has been completed except for
                      some minor testing at the 100% power plateau. Lessons learned from this
                      program should be evaluated for application to routine post maintenance
                      testing in light of the auxiliary feedwater overpressurization event.
                      Accomolishmenti                                                   J                    '
                      The group responsible for the System Review and Test Program (SRTP) which did
                      the startup testing at Rancho Seco transitioned into the Plant Performance
                      Department in late spring of 1988. The personnel core of the SRTP group
                      became the new System Engineers (SEs) of the Department, in order to maintain
                      continuity of the experience gained during the Restart program. Likewise, the
                      success of the testing program which included the ccmponent, functional, and
                      integrated testing of all modified equipment continues by the
                      proceduralization of the entire Special Test Procedure (STP) process. Current
                      procedures control test director qualifications, the procedure format, the
                      review cycles, and the emphasis of Operations personnel involvement.
                      The minor testing that is continuing after the plant reached the maximum power
                      level is receiving a similar amount of review as those tests during the
                      Restart effort. The minor testing includes ICS data gathering for tuning and           .
                      high power performance confirmation.                                                   !
                      The District rcvised procedure MAP-0006, "Hork Recuest Planning" to
                      incorporate many of the Lessons Learned from the System Review and Test                l
                      Program. To ensure that the Lessons Learned are not limited to o' iy STPs, the
                      SEs have been included in the development of Post-Maintenance Testing (PMT)
                      and Post-Maintenance Verification (PMV). Thus, any maintenance and post-
                      m;intenance testing, including that work considered routine, is reviewed by
                      the SE and may not proceed throagh work planning without his authorization.
                      Additionally, SEs have the responsibility of Dedicated Outage Coordinators
                      (DOCS) who control the scope of system work during the Quarterly System
                      Scheduled outages (OSSs). The return to service of the system and each of the
                      components is also under the guidance of the SE.
                                                                                                              i
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