ML20137D506

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Forwards Insp Rept 50-289/85-25 Re 851022 Pipe Breaks & Releases Per 851022 Request.Accuracy of Wd Travers 850925 Memo to Ta Rehm Accurate.W/O Encl
ML20137D506
Person / Time
Site: Three Mile Island  Constellation icon.png
Issue date: 01/09/1986
From: Kane W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Jun Lee
AFFILIATION NOT ASSIGNED
Shared Package
ML20137D512 List:
References
NUDOCS 8601170015
Download: ML20137D506 (4)


See also: IR 05000289/1985025

Text

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UNITED STATES

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. 631 PARK AVENUE

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January 9,1986

Ms. Jane Lee

183 Valley Road

Etters, PA 17319

Dear Ms. Lee:

This is in response to your letter of October 22, 1985, to Commissioner

Asselstine in which you asked several questions related to Three Mile Island

Unit 1 (TMI-1) and made several comments related to TMI-2.

You requested a report on each of the pipe breaks and subsequent releases

reported by General Public Utilities (GPU) on October 22, 1985. Specifically,

you asked which pipes were broken, what was the condition of the steam tubes,

and exactly how much radiation was released.

The repairs to the leaks referred to in the GPU press release were associated

with lines external to the steam generators and were located inside the

reactor building. One of the leaks was located in a bolted flange connection

on an emergency spray ring header and the other was located in a valve body-

to-bonnet bolted connection on a steam generator level transmitter isolation

valve. Both of these leaks were temporarily repaired as discussed in NRC

Inspection Report 50-289/85-25, which was issued on November 29, 1985. A copy

of that report is enclosed. Small leaks of several drops per minute were

observed again at these same locations on January 2, 1985, and were again

temporarily repaired. Permanent repairs are scheduled during the required

steam generator inspection outage currently scheduled for March 1986. The

leaks were inside containment and there was no release to the environment.

William D. Travers, Director of the TMI-2 Cleanup Project Directorate, Office

of Nuclear Reactor Regulation, has reviewed your comments related to the refer-

enced memorandum from W. D. Travers to T. A. Rehm, dated September 25, 1985.

While acknowledging your continuing concern, the staff maintains the information

contained in the referenced memorandum, which responded to your September 24,

1985 request to Commissioner Asselstine, is accurate. In addition to reiterating

the concerns expressed in your September 24, 1985 letter, you noted that you

had made several attempts to obtain information on the disposal of charcoal

filters removed from TMI-2 in April 1979. We are unaware of any requests

directed to the NRC staff for such information. Dr. Travers has informed me

that he will obtain this information and send it directly to you.

Sincerely,

" f(v /

W liiam F./Kane, Director

TMI-1 Restart Staf f

Enclosure: As stated

9601170015 860109 ,

oR aooca 0500gg I[ , t

.

Ms. Jane Lee 2

Distribution:

A 001245

H. Denton, NRR

D. Eisenhut, NRR

T. Rehm, EDO

W. Travers, NRR

T. Murley, RI

R. Starostecki, RI

W. Kane, RI

R. Conte, RI

Pubile Docuinent Room (PDR)

Local Public Document Room (LPDR)

Region I Docket Room

l

.

S

I

January 9, 1986

Hs. Jane Lee

183 Valley Road

Etters, PA 17319

Dear Ms. Lee:

This is in response to your letter of October 22, 1985, to Commissioner

Asselstine in which you asked several questions related to Three Mile Island

Unit 1 (TMI-1) and made several comments related to TMI-2.

You requested a report on each of the pipe breaks and subsequent releases

reported by General Public Utilities (GPU) on October 22, 1985. Specifically,

you asked which pipes were broken, what was the condition of the steam tubes,

and exactly how much radiation was released.

The repairs to the leaks referred to in the GPU press release were associated

with lines external to the steam generators and were located inside the

reactor building. One of the leaks was located in a bolted flange connection

on an emergency spray ring header and the other was located in a valve body-

to-bonnet bolted connection on a steam generator level transmitter isolation

valve. Both of these leaks were temporarily repaired as discussed in NRC

Inspection Report 50-289/85-25, which was issued on November 29, 1985. A copy

of that report is enclosed. Small leaks of several drops per minute were

observed again at these same locations on January 2, 1985, and were again

temporarily repaired. Permanent repairs are scheduled during the required

steam generator inspection outage currently scheduled for March 1986. The

leaks were inside containment and there was no release to the environment.

William D. Travers, Director of the TMI-2 Cleanup Project Directorate, Office

of Nuclear Reactor Regulation, has reviewed your comments related to the refer-

enced memorandum from W. D. Travers to T. A. Rehm, dated September 25, 1985.

While acknowledging your continuing concern, the staff maintains the information

contained in the referenced memorandum, which responded to your September 24,

1985 request to Commissioner Asselstine, is accurate. In addition to reiterating

the concerns expressed in your September 24, 1985 letter, you noted that you

had made several attempts to obtain information on the disposal of charcoal

filters removed from TMI-2 in April 1979. We are unaware of any requests

directed to the NRC staff for such information. Dr. Travers has informed me

that he will obtain this information and send it directly to you.

Sincerely,

VY

William F. Kane, Director

THI-1 Restart Staff

Enclosure: As stated

1

o

Ms. Jane Lee 2

Distribution:

EDO 001245

H. Denton, NRR

D. Eisenhut, NRR

T. Rehm, EDO

W. Travers, NRR

T. Murley, RI

R. Starosteckt, RI

W. Kane, RI

R. Conte, RI

Pubite Document Room (PDR)

Local Public Document Room (LPDR)

Region I Docket Room

TMICPD RI:I

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agfb

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_ _ _ . _ _______

_ _ _ _

pe nsou UNITED ETATES

  • NUCLEAR REGULATORY COMMISSION

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Docket / License No. 50-289/DPR-50

GPU Nuclear Corporation

ATTN: Mr. H. D. Hukill

Director, TMI-1

P.O. Box 480

Middletown, Pennsylvania 17057

Gentlemen:

Subject: Inspection 50-289/85-25

During the period from October 18-25, 1985. members of the NRC TMI-1 Restart

Staff conducted routine and special safety inspections of operational activi-

ties at your facility. The results of these inspections are documented in the

enclosed inspection report. At the conclusion of the inspection Mr. R. Conte,

of my staff, summarized the inspection findings for you and other members of

your staff. On balance, the findings were favorable. Of particular note was

the continued high level of performance of the operations department in the

use of their skills to minimize challenges to safety systems. However, the

results in one area are of concern and warrant our continued examination; and,

in another area, there was an apparent violation of regulatory requirements.

Of particular concern to us during this period were the circumstances that

developed during and atter a routine surveillance test of the pressurizer

power operated relief valve (PORV) during the midshift on October 25, 1985.

The issues of concern include (1) a routine test that could not be completed

because a portion of the test was not conducted correctly, (2) the unnecessary

creation of both a deficiency sheet and an exception sheet as a result of that

test and, subsequently, throwing these sheets away and (3) the confusing

documentation used to substantiate the shift supervisor's determination of

operability of the PORV. As a result of our witnessing your retest, it was

clear to us within several hours that the PORV was in fact operable throughout

the period except, of course, while it was being tested. It is also clear to

us that there was prompt involvement by your senior management in the retest.

Our early involvement in this process, however, led to your discovery of the

exception and deficiency sheets that had been thrown away. We are aware that

  • 'r creantfa) information on these sheets aisc was available on other records

t..a j u r... :c a ... ..

Although we have no immediate safety concern at this point, we are concerned

with the actions that took place. Accordingly, we request that you provide us

with a report containing your analysis of this event. In particular, your

response should identify (1) any discrepancies in our understanding of th;

event as described in the inspection report, (2) the problems, their root

causes and lessons learned, and (3) corrective actions completed and/or

planned. This matter will remain unresolved pending our review of your

report.

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Also during the period, our inspectors identified one instance of your failing

to meet regulatory requirements as described in the enclosed Notice of

Violation (Appendix A). The apparent violation resulted from workers posting

uncontrolled circuit drawings and procedural notes on the inside of instrument

cabinets in the control room. In addition to following the instructions on

the attached Notice of Violation, please describe those measures in place or

planned to assure that similar problems do not exist in other instrument

cabinets outside the control room area.

Your cooperation with us in this matter is appreciated.

Sincerely,

dW lW

Willian I. Kane, Director

TMI-1 Restart Staff

Division of Reactor Projects

Enclosures:

1. Appendix A, Notice of Violation

2. NRC Region I Inspection Report Number 50-289/8.t-25

cc w/encls:

R. J. Toole, Operations and Maintenance Director, TM.-1

C. W. Smyth, TMI-1 Licensing Manager

R. J. McGoey, Manager, PWR Licensing

G. F. Trowbridge, Esquire

THI-1 Hearing Service List

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector (2 copies)

Commonwealth of Pennsylvania

-

GPU Nuclocr Ccrp::rction 3

'

.

bec w/encls:

.

'

Region I Docket Room (concurrence ccpy)

Management Assistant, RI (w/o encl)

H. Thompson, NRR

W. Travers, NRR

J. Taylor, IE

J. Partlow, IE

J. Thoma, PM, NRR

T. Murley, RI

J. Allan, RI

K. Abraham, RI

R. Starostocki, RI

T. Martin, RI

S. Ebneter, RI

H. Kister, RI

L. Bettenhausen, RI

N. Blumberg, RI

P. Wen, RI

R. Conte, RI

D. Haverkamp, RI

W. Baunack, RI

R. Urban, RI

F. Young, RI

R. Walker, RII

H. Dance, RII

D. Falconer, RII

E. Johnson, RIV

D. Hunnicutt, RIV

J. Cummins, RIV

.

.

'

, APPENDIX A

NOTICE OF VIOLATION

GPU Nuclear Corporation Docket No. 50-289

Three Mile Island Unit No. 1 License No. DPR-50

As a result of the inspection conducted on October 18 through 25, 1985, and in

accordance with the NRC Enforcement Policy (10 CFR 2. Appendix C), published

in the Federal Register on March 8, 1984 (49 FR 8583), the following violation

was identified:

Criterion VI of 10 CFR 50, Appendix B, requires in part that documents be

properly controlled to assure.that those located at work locations have

been reviewed for adequacy and properly approved. The GPU Nuclear

Operational Quality Assurance Plan, Revision 0, September 1, 1982,

Section 3.0, " Control of Documents and Records," requires, in part, that

measures be established to control issuance and distribution of

procedures and drawings and that drawings and procedures be reviewed for

adequacy and approved prior to release. Station administrative procedure

(AP) 1001H, Revision 1, dated March 9, 1983, " Drawing Utilization,"

paragraph 4.2.6 states, in part, "...The use of miscellaneous drawings,

sketches, or notes will not be authorized on any panels, walls,

equipment, etc...."

Contrary to the above, on October 25, 1985, miscellaneous circuit

drawings, sketches and notes were posted on the inside of all eight

radiation monitoring panel access doors, located on panel right front in

the control room, and on the inside of the access door to nuclear

instrument reactor protection system subassembly C, cabinet 1 door, also

located in the control room. These drawings and notes were not properly

reviewed for adequacy or approved prior to their release.

This is a Severity Level V violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, GPU Nuclear Corporation is hereby

required to submit to this office within 20 days of the date of the letter

transmitting this Notice, a written statement or explanation in reply, includ-

ing for each violation: (1) the corrective steps which have been taken and

the results achieved (2) the corrective steps which will be taken to avoid

,

further violations; and (3) the date when full compliance will be achieved.

!

Where good cause is shown, consideration will be given to extending the

response time.

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U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Report No. 50-289/85-25

Docket No. 50-289

License No. DPR-50 Priority -- Category C

Licensee: GPU Nuclear Corporation

Post Office Box 480

Middletown, Pennsylvania 17057

Facility At: Three Mile Island Nuclear Station, Unit 1

Inspection At: Middletown, Pennsylvania

Inspection Conducted: October 18-25, 1985

Inspectors: W. Baunack, Project Engineer, Region I

N. Blumberg, Lead Reactor Engineer, Region I

J. Cummins, Senior Resident Inspector (Wolf Creek),

Region IV

D. Falconer Jr., Lead Reactor Engineer, Region II

D. Haverkamp, Technical Assistant for TMI-1 Restart,

Region I

R. Urban, Reactor Engineer, Region I

P. Wen, Reactor Engineer, Region I

F. Young, Resident Inspector (TMI-1), Region I

Contractor Personnel: W. Apley, Associate Manager, Energy Systems,

Battelle Pacific Northwest Laboratories (PNL)

B. Gore, Senior Research Scientist, Battelle PNL

Approved By: * 6----f > H la's bf

en R. Conte, TMI-1 Restart M) nager Date

THI-1 Restart Staff

Division of Reactor Projects

Inspection Summary:

Routine and special (NRC shift coverage) safety inspection (352-hours) of

power operations focusing^*on operator and management performance; startup

- -

v! :P f- '._d c m - 1..c:.. is : re-f e t .d s * * .e r: . . f;: 'If *"

operations which included followup on rod exercise surveillance, calibration

indicators, repair of leaks in reactor building, drawing control, and storage

of combustible gases in safety-related areas; pressurizer power operated

relief valve surveillance Nuclear Safety and Compliance Committee staff

activities; and administrative controls implementation in the areas of removal

of equipment from service, instrument out of service control, caution tagging

and post reactor trip review.

'

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_ _ _ _ _ _ _ ._ _ _ __ -

10

,

. Inspection Results:

Operations department personnel continued to conduct activities in a pro-

fossional manner and to use their skills to minimize challenges to safety

related systems. Although some inexperience was apparent, non-licensed

personnel also conducted themselves in a professional manner and properly

implemented facility procedures in conjunction with licensed personnel. The

inspectors noted a trend in which there was an apparent lapse of attention to

detail in the documentation of certain events or abnormal conditions in

various control room operations logs. In those cases other records reflected

those observations for licensee corrective action which was completed or was

initiated.

The testing program, to date, was effective in uncovering facility problems

such as the unexpected interaction between the turbine bypass valves and the

steam generator safety valves. Licensee representatives properly implemented

the startup test procedures and they found that the data, with some

exceptions, conformed to the test acceptance criteria.

Although inspectors later found the pressurizer power operated relief valve

(PORV) had in fact been operable except during testing, the licensee's

instrument and control (I&C) department poorly handled both the test and the

retention of the test and deficiency documents for the PORV setpoint

surveillance. Operations and I&C personnel inexperienced in performing the

test contributed to the problem when shift personnel initially conducted the

surveillance during the midshift.

Nuclear Safety and Compliance Committee (NSCC) staff activities meet or exceed

regulatory requirements. However, NRC staff needs to complete its review of

the NSCC activities performed by the committee.

Licensee management continued their detailed attentiveness and involvement and

generally was responsive to NRC staff concerns. Management was particularly

responsive to the PORV surveillance exception and deficiency sheets being

thrown away and to inspector observations on personnel potentially violating a

contamination boundary.

Administrative control procedures were technically adequate and, in general,

were properly implemented. Also, the licensee needs to continue their

assessment and corrective action related to the use of calibration stickers.

The inspectors identified an apparent violation of drawing control regulatory

requirements for placards, sketches and drawings inside instrument cabinets in

the control room (paragraph 3.2.5). -

_-_ _ . _ _ _ _

- - . - . . _ - - - . - . _- .-. _ - _

'

DETAILS

1. Introduction and Overview

1.1 General

At the beginning of this inspection period on October 18, 1985, the

TMI-1 Restart Staff was providing around-the-clock coverage to

assess restart operating activities. At 6:00 p.m., on October 24,

1985, this inspection coverage was reduced to 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> a day

consistent with the reduced level of testing activity and

steady-state facility operation at the 48% power plateau. This

nearly continuous observation of plant activities was maintained by

inspectors from Regions II and IV and by reactor operator examiners

from Battelle Pacific Northwest Laboratories, an NRC contractor.

Also, Region I inspectors continued daily coverage of testing

activities. Additional Region I personnel were on site during

portions of the period to augment the resident inspection staff.

1.2 Facility Restart Operations

During the period of October 18-25, 1985, the significant TMI-1

restart operational milestones included: (1) completing main

turbine generator testing and electric power generation at the 40%

testing plateau, (2) completion of loss of main feedwater

reactor / turbine trip, and (3) initial main turbine generator

operation at the 48% plateau. The chronological summary of plant

operations during the period is presented below.

Date Time Operational Highlight or Milestone

10/18/85 7:00 a.m. Reactor at 7% of rated power pending

completion of turbine control valve

drain line repairs

9:05 a.m. Completed repairs to turbine control

valve drain line and placed turbine

generator on line

10/19/85 6:35 a.m. Increased power to 41%

10/21/85 6:04 p.m. Conducted loss of feedwater reactor

~

trip / turbine trip

..' ; . t. . C- --- ~ ~

.. . .

circulation

10/23/85 2:30 p.m. Region I Administrator authorized the

licensee to take the reactor critical

and proceed with the test program at

the 48% plateau

4:12 p.m. Commenced reactor startup

_ _ - _ . - _

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.

3

.

5:57 p.m. Reactor critical

8:26 p.m. Turbine generator on line

10/24/85 1:28 p.m. increased power to 48%

10/25/85 7:00 a.m. At the end of this inspection period

the reactor was at 48% of rated power,

reactor coolant average temperature was

578 degrees F arfd pressure was 2150

psig

1.3 Operational Events

As described in Inspection Report 50-289/85-24, recurring problems.

with weld failurar in two drain lines from the turbine control valve

headers had delayed the restart testing program for several days.

Repairs to tho frain lines were completed on October 18, 1985,

permitting continuation of the test program at the 40% power

plateau.

Two events occurred dut'ing this inspection period that were

considered either operationally significant or were matters of

special interest to the THI-1 Restart Staff. These events are

~ '

summarized below.

Date Operational Event

10/21/85 During post trip inspection.of t reactor

building, leaks were identified on an

emergency feedwater flange and on a steam

generator level instrument root valve (see

paragraphs 3.2.4 and,4.2.2.4)

10/22/85 Group 1 safety rods would not respond to

"in" command during pre-critical testing

The problem regarding movement of Group 1 safety rods was traced to

the inability to transfer the rods from the de hold bus to the

auxiliary power supply. The de hold bus does not provide motive

power for rod movement. The licensee suspected a malfunction with

transfer relays but the symptom was not repeated.

-

1.4 Summary

Inis inspection includeo continued progress of restart testing

activities up to the 48% power plateau. 'During this period there

was one interruption of the restart testing program while repairs

were made to two leaks identified during post-trip inspection of the

reactor building. The THI-1 Restart Staff remained sensitive to an

adverse impact on shift supervisor safety duties due to NRC shift

inspector questioning and discussions of matters of a progransnatic

nature. Accordingly, the shift inspectors referred only

implementation matters or status questions to the shift s.upervisor

i

. . - _ - - - - - - - . -. - _ - -

- 4

. and referred programmatic matters (event followup, design or

procedure adequacy problems) to resident and region-based NRC

personnel. Resident and region-based personnel interfaced with

licensee support groups in followup to shift inspector

referrals / concerns. The staff's observations and findings regarding

plant operation and testing and licensee response to operational

events is discussed in the report sections that follow.

2. Shift Inspection Activities

2.1 Scope of Reviaw and Observations

During the period of October 18-25, 1985, the TMI-1 Restart Staff

continued its augmented shift inspection coverage. The NRC shift

-

inspectors assessed the adequacy and effectiveness of operating

personnel performance based on the inspectors' observations of

4 operating and startup activities to determine that:

--

operators are attentive and responsive to plant parameters

and conditions

--

plant evolutions and testing are planned and properly

authorized;

--

procedures are used and followed as required by plant

policy;

--

equipment status changes are appropriately documented and

communicated to appropriate shift personnel;

--

the operating conditions of plant equipment are

effectively monitored and appropriate corrective action is

initiated when required;

--

backup instrumentation, measurements, and readings are

used as appropriate when normal instrumentation is found

to be defective or out of tolerance;

--

logkeeping is timely, accurate, and adequately reflects

plant activities and status;

.

--

operators follow good operating practices in conducting

plant operations; and '

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training.

The shift inspectors' observations included, but were not limited

to, those reactor plant operation and testing activities, periodic

surveillance activities, and preventive and corrective maintenance

activities listed below.

_ __ - _ _ _ _ , _ _ . _ . _ _ _ _ _ _ _ _ . . - . _ - _

- . ._

.

5 l

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Reactor Plant Operation and Testina Activities

s

-- routine control' room operations including annunciator

alarm response and control room logkeening

-- operating and emergency procedures discussions with shift

supervisors, shift foremen, control room operators and

shift technical advisors

--

periodic inspection observation tours of areas outside the

control room, including diesel generator rooms, emergency

feedwater rooms, control building, turbine building,

auxiliary building, intermediate building, electrical

switchgear rooms, and outside buildings and yard areas.

-- secondary plant auxiliary operator observation rounds and

discussion of water treat system instruments, controls and

5

interlocks

--

shift preparations and conduct of turbine startup

operations following drain line repairs

--

power level increase to 25% of rated power ,

--

power level increase to 40% of rated power 's

--

startup of B condensate booster pump

--

local startup of B heater drain pump

advance management planning for, reactor trip test

-

--

--

changeover from B to A heater drain pump

-- inspector operability verification of emergency diesel

generators systems valve and breaker positions

-- walkdown of secondary systems in company with an auxiliary

operator

-- instrument air compressor after cooler water trap blowdown'

-- shift turnover activities conducted by licensed operators ,

and operating crtw planning briefings conducted by shift

fere. ."

-- extensive operating crew and technical staff briefings in

preparation for reactor trip test

-- performance of loss of feedwater reactor / turbine trip at

40% of rated power

-- fire drill at the emergency safeguards motor control

center lA

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%

_ . - . _ . ___ _ _ . - - _ _ _

6

--

temporary change notice logbook, control room tagout and

control room operator checklist implementation

'

--

turbine shell/ chest heating activities prior to turbine

generator operation

--

special temporary procedures administrative controls

implementation

--

water addition to sodium hydroxide tank to increase tank

pressure

--

crew performance of long form pre-critical checklist per

procedure 1102-2

--

crew response to unexpected apparent reduction in shutdown

margin

--

estimated critical position calculations for criticality

--

operating crew performance during reactor startup

'

--

operator actions during startup in response to group IV

safety rods out interlock stopping group V control rod

withdrawal

--

operator actions during startup in response to

intermittent group I safety rods out interlock problem

--

turbine generator startup and load increase to 40% of

rated power

-- turbine load increase to 48% of rated power

--

operator actions in response to continuing main feedwater

systc= cscillations due to apparent centrcl proble= with

l

main feedwater valve FW-V-17A

! -- implementation of administrative controls for equipment

operation including caution tags, out-of-service stickers,

blue and red tags and switching logs

--

startup of B main feedwater pump -

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l cylinders found stored in close proximity to eacn other by

I backup instrument air compressor in intermediate building

-- shift foreman response to untethered pressurized hydrogen

l

bottle in Hayes gas analyzer room

!

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_ _ __ __, _ _ _ _ . _ _ _ -

7

Periodic Surveillance and Maintenance Testing

--

secondary service closed cooling water pump SC-P-1B

testing in response to request from maintenance

--

accelerometer vibration measurements of main steam drain

lines

--

local cycling of main feedwater regulating valves

FW-V-17A&B for post-maintenance testing of controllers and

valve position indication

--

portions of Surveillance Procedure 1303-7.2, " Source Range

Channel," regarding count rate amplifier calibration and

gain testing

--

procedure review of calibration tests for nuclear services

closed cooling water line break isolation channels A and B

--

condenser vacuum pump exhaust sampling and analysis

--

reactor building fire detector testing

--

power range nuclear instrument adjustments

--

reactor coolant system heat balance measurements

--

spent fuel cooling pump functional test

--

power imbalance detector correlation test

--

reactor coolant pump seal leakoff " bucket check"

--

reactor protection system monthly surveillance testing per

procedure 1303-4.1

--

high pressure injection and low pressure injection analog

channels monthly surveillance testing per procedure

1303-4.19

- --

radiation monitors system quarterly calibration testing

per procedure 1302-3.1

-

--

control rod movement tests per procedure 1303-3.1

--

pressure switch calibrations for emergency fesswater start

and reactor / turbine trip on loss of feedwater

--

emergency diesel generator monthly surveillance testing

per procedure 1107-3

--

emergency safeguards systems monthly surveillance testing

., - - ,- -

_

. 8

--

pressurizer power-oriented relief valve setpoint check

surveillance per procedure 1303-11.45

Preventive and Corrective Maintenance Activities

--

main steam drain line pipe threading in machine shop

--

packing leak adjustment to stop a leak in top of Amertap

tank TC-11A

--

collar welding on equalizing line around condensate

booster pump 1C suction valve CO-V-29C to stop a pinhole

leak

--

partial review of program for instituting and controlling

corrective maintenance activities

--

moisture separator drain tank sight glass level indication

verification

--

seal installation in C heater drain pump

--

reactor building fire detector maintenance

--

reactor building purge outlet valve preventive maintenance

(bushing inspection for wear and lubrication)

--

nuclear instrumentation channel 6 imbalance meter repairs

--

hydraulic oil addition to reactor coolant pumps

--

steam generator A emergency feedwater line flanged

connection leakage repairs

--

feedwater root valve FW-V-1093 leakage repairs

-- investigation of reported empty or low hydraulic fluid

reservoirs for snubbers in pressurizer safety valve relief

lines

--

alcohol cleaning of contacts in reactor protection system

cabinet 2 for nuclear instrumentation channel 4 log

amplifier and startup rate drawers -

.. ....s,. -.g. .e m. - 7 , - . (7,;... ,n. . 3 n g,. . ., :q ;

sporacle nig'n peaxing

--

repairs to inoperable controller for main feedwater pump B

recirculation valve FW-V-7B

.

't

_,

9

2.2 Assessments of Shift Inspectors

2.2.1 General

The shift inspectors assured that any potentially adverse

safety concern or regulatory finding was identified

promptly to both the licensee's shift supervisor and the

TMI-1 Restart Manager. Those items requiring additional

staff review or followup are described in paragraph 3 of

this report. Also, at the end of their assigned period of

shift inspection activities, the inspectors provided their

general assessment of facility operational readiness and

personnel performance. These general assessments

included, as applicable, each inspector's overall views

related to operating staff performance, fire protection,

maintenance, surveillance, radiological controls,

training, emergency planning, and physical security. The

inspectors' assessments are presented below.

2.2.2 Operating Staff Performance

Shift inspectors continued to provide many positive

comments on the knowledge level and overall quality of

'

performance of facility operating, maintenance and

technical staff personnel as described in detail in

previous inspection reports 50-289/85-22 and 50-289/85-24.

Those groups of individuals, that were closely monitored

in addition to control room operators and shift

supervisors were: shift technical advisers,

instrumentation and control (I&C) technicians, and

auxiliary operators.

The performance of certain individuals was noteworthy in

that it reflected a professional attitude. An I&C

technician took the initiative to clean the sediment out

of a moisture separator sight glass drain plug during his

troubleshooting efforts on a level control valve. A

training instructor took the initiative on a Saturday to

observe a heater drain pump seal installation. He

explained that he taught that mechanical maintenance

evolution and he wanted additional feedback on how to

improve the lesson plan. Also, as a side note, one shift

openly expressed disappointment that the post trip reactor

etartup was rescheduled for a different shift. Although

  • ? : r- c:1 :::1

. . .-

'

  • s
. *e : -' i

-% '

" - ' -

a relatively large organization, tne generai comments of

the shift inspectors reflect that there is a general sense

of dedication, motivation and caring displayed by the

majority of the personnel observed.

In general, procedures continued to be properly

implemented. Specific procedure implementation problems

were noted in paragraphs 3.2.3 and 3.2.5. Further, an

inspector observed an operator using a suberitical

. , , . _ - _ _ _ __ _ _.

_

_ , - - , .

__ _ _ _. _- __ _ _ _ . _ _ _ _

- 10

multiplication "l/M" plot that was not a replica (in

format) of the procedural required plot. This had no

adverse effect on the proper method of performing the 1/M

plot since the content of the form used was essentially

the same as prescribed by procedures. The inspector

brought this to the attention of licensee management and

stated that the proper form should be used. Licensee

management acknowledged the inspector's comments.

i

Overall, operators and technicians continued to perform in

a professional manner.

2.2.3 Training

i The reactor trip and subsequent startup during this period

provided operators with excellent opportunities to gain

operational experience, especially when the integrated

control system (ICS) needed to be operated in manual.

Shift supervisors and licensee management continued their

emphasis on every event being a learning experience.

.

The licensee also conducted a fire drill during this

period and it sufficiently demonstrated the fire fighting

preparedness of the fire brigade. Based on observations

of the shift fire drill and several on-shift training

briefs, the inspectors determined that training was being

conducted in a serious manner with appropriate

participation.

i Training appeared to provide plant personnel with

sufficient skills and knowledge necessary to perform

activities in a safe and proficient manner. Steady-state

operations, as well as transient evolutions, were

routinely utilized to provide an on-the-job training

medium to increase training intensity and to accelerate

shift operational experience. Observed on-the-job

training was effectively conducted with experienced

. supervisors not just monitoring crew performance, but

providing instruction before, during, and after

evolutions. There was considerable sharing of information

r between operators, with no indication that there was an

unwillingness on anyone's part to admit ignorance on a

-

particular issue.

- ..::.-

.

-.g , :r-<j._ ,.

+ue : n. : - . - - . .

.

were minimally adequate. Operators nad little time to

spend giving checkouts, and there seemed to be little

'

uniformity as to the level of detail that went into a

checkout. However, based on observations of personnel to

date, it appears that the overall training pipeline is

4

performance-oriented.

i

I

. _ _ _

~__ _ _ . _ _ _ , _ , ,_ .__ . _ _ _ _ , _ _ _ , _ _ _ . _ _ _ . _ _ _ _ . -

11

2.2.4 Fire Protection

Fire protection measures continued to be implemented

adequately, based on shift inspector visual inspection,

review of fire brigade assignments and training,

monitoring of system surveillances conducted during the

week, and fire extinguisher checks, none of which were

past their inspection due date. At the beginning of the

inspection period, the inspectors observed two instances

where fire doors were left open or ajar primarily because

of ventilation differential pressure imbalance and

indirectly because certain personnel were not attentive to

assure that the door was closed. The inspectors trended

this observation throughout the inspection period and

noted no additional instances of fire doors being left

open or ajar.

2.2.5 Maintenance

Corrective maintenance was aggressively pursued and

promptly effected. Maintenance personnel appeared to be

well qualified and trained. However, a lack of

experienced I&C supervision on the backshift became

apparent when inexperienced technicians had problems

calibrating the PORV reset setpoint during a backshift

surveillance (see paragraph 5).

"Furmanite" repairs to the emergency feedwater header and

to a valve inside the reactor building prior to restart

'

following a planned trip demonstrated the licensee's high

priority for maintaining the plant (see paragraph 3.2.4).

2.2.6 Surveillance

I

Surveillances required by the technical specifications

were conducted at the specified frequency without

exception. Technical specification required surveillances

were provided for and controlled by a strong

administrative program which ensured they were conducted

at the specified frequency.

The calibration frequency of some instruments which were

not related to technical specifications but provided

parameter status of systems important-to-safety were not

er r*-ir.te~tly maintP.ir.Oi 25 FV! 30*?Pd bV 'hO I' P0nthi

since the last calibration of the cecay heat closed

L

cooling surge tank level instruments. This frequency is

at the discretion of the licensee.

An isolated problem was identified in the surveillance

program concerning a technical specification required

demonstration of control rod operability prior to

criticality (see paragraph 3.2.2).

l

l

.. __ _ _ _ _ _ . . - _ _. _ _ _ __ - - _ _ . _ _ _ _ .

12

Operations supervision of surveillances was excellent,

both from the standpoint of knowing what was being done

and how it affected the plant. There were a number of

times when the assigned control room operator was

significantly pressed, and in each case he stopped

distracting evolutions to concentrate on monitoring

surveillances. An especially good job was done in

preplanning of plant conditions to allow for the effective

accomplishment of surveillances.

All surveillance procedures reviewed were adequate. One

potential problem concerned uncontrolled labelling and

schematic diagrams found in the back of the radiation

monitor panels. It was not determined if they were ever

used during surveillance testing (see paragraph 3.2.5).

2.2.7 Radiological Controls

Contaminated areas were posted and maps showing radiation

and contamination levels were present at entry pads.

Several components with potential leakage problems were

encased within transparent yellow plastic to contain

leakage. Tygon drain tubing crossing passage areas and

drain openings was taped in place. Cleanliness and

attention to minimize the spread of contamination were

apparent.

For radiation work permit (RWP) entries, radiological

control (radcon) technicians had considered ALARA

requirements. Low dose rates were expected in the regions

visited. Proper dosimetry including neutron monitoring

and/or continuous technician coverage were provided in

accordance with RWP requirements. Discussions with a

radcon foreman on the intent and interpretation of the

" continuous monitoring" requirements indicated a proper

concern and emphasis upon area surveys and job planning to

minimize personnel dose.

2.2.8 Physical Security

On one occasion the shift inspector discovered the

card-entry door to the control room complex ajar. A

security guard arrived within about two minutes to

investigate and secure the door. Based on routine

5, ,

. .e ;' : c..'*- .e: r c:- r :: A : !: -

r;;rd

performance no adverse conditions or problems were

identified in this area.

2.3 Conclusion

Personnel performed in a professional manner. There were procedure

implementation problems, but on a closer review it appeared they

were due to individual inexperience or lack of familiarization and

none adversely affected safe operation of the facility. Actual

. - - . - - - - _ _ . . . - - . . -

,

13

plant experience continued to be a valuable training vehicle to

support safe power operation. The operations department performed

well during major challenges to their skills, e.g. the 40% reactor

trip test and the subsequent natural circulation test during which

natural circulation was lost.

Overall, maintenance and surveillance activities were properly

,

conducted, although some examples of poor implementation practices

were noted. Area radiological contamination control continues to be

noteworthy. Radiological control procedures were properly

implemented with health physics personnel demonstrating a genuine

concern for worker radiation protection.

3. Plant Operations

3.1 Routine Review

The TMI-1 Restart Staff inspectors periodically inspected the

facility to determine the extent of the licensee's compliance with

general operating requirements of Section 6 of the Technical

Specifications (TS) in the areas listed below.

--

review of selected plant parameters for abnormal trends

--

plant status from a maintenance / modification viewpoint

including plant housekeeping and fire protection measures

--

control of ongoing and special evolutions, including

control room personnel awareness of these evolutions

. --

control of documents including log-keeping practices

--

implementation of radiological controls

'

--

implementation of the security plan including access

control, boundary integrity and badging practices

The inspectors focused their attention on the areas listed below.

--

control room operations during regular and backshift

hours, including frequent observation of activities in

'

progress and periodic reviews of selected sections of the

shift foreman's log and control room operator's log and

other control room daily logs

--

followup items identified by snift inspector activit:es

(paragraph 2)

--

areas outside the control room

--

selected licensee planning meetings

1

- _ . - - - . - . _ . ,,-, . , , . . . - . , . - - . - , . . - . , . , . . . - - _ . . . , - . , , - . , _ - _ - - - . . _ _ - - - - - _ _ ~ . . . , - . .. -

14

As a result of this review, the inspectors reviewed specific

concerns or events in more detail as described in the sections that

follow.

3.2 Findings

3.2.1 General

Licensee management continued their detailed involvement

in all phases of plant operation. The operations manager

directed major day-to-day plant activities while shift

supervisors were held responsible for accomplishment of

directives. Major plant evolutions were directly

supervised by senior plant management with additional

licensed personnel present to monitor plant parameters.

After achieving the 48% power plateau, shift supervisors

were allowed to fully direct routine shift activities and,

thereby, demonstrate their management capabilities.

'

Licensed shift supervision maintained a high level of

responsiveness to the concerns identified by the

inspectors. These concerns included snubber fluid levels,

water in the instrument air aftercooler water trap and

leakage of a condensate tank recirculation line valve.

The licensee's efforts in resolving and providing

corrective actions concerning the PORV documentation and

operability problems (see paragraph 5) further exemplified

their regulatory responsiveness. As an additional

example, licensee management was responsive to NRC

concerns on how major test briefings were conducted. They

conducted the briefing for the 40% trip test in the south

auditorium which was more environmentally suitable. The

briefing also included a discussion of response actions

for operational problems that might be encountered.

The high motivation of licensee management apparently has

filtered down to certain employees as described in

paragraph 2.2.2 on the motivation of personnel observed

performing work activities.

The radiological controls department was responsive in

resolving an inspector's observation of an apparent

violation of a contamination control barrier-(NRC

Inspection Report 50-289/85-24). Radeon department

-. --

:n . :r- - :b v:e re-er. et in : 1.~> ca ru~

12censee representativos cetermined tnat tne worters were

moving paint into the contaminated area. The inspector

had no further comments on this matter.

In general, administrative procedures were properly

implemented as described in paragraph 7. However, with

respect to log keeping, details of certain events were not

provided in the control room operator's log or shift

i

  • -----*----y--e--- - + - - - - - - - - -r w

_ - , - , _ _ . - - , .-y --

-r - - * - - % , .o,y9,---

-

9

, . . - . . -- -- -- -

15

,

foreman's log. The leaks found in the reactor building

(see paragraphs 3.2.4 and 4.2.2.4) were not logged but

i were recorded in another plant record, a work request, to

initiate repair action.

1 The safety rod out limit interlock prevents movement of

reactor control rod groups 5 to 7. The operational

actions taken to correct the problem were not recorded.

When this was brought to the plant operations manager's

attention, he had a " late entry" placed in the shift

foreman's log. Considering other log entries during this

period and previous inspection periods, the inspector

i stated that the above log entry discrepancies were not

characteristic of the past performance by the' operator.

'

The inspector also stat 4d that this area will be trended

during subsequent routine NRC reviews. The safety rods

i

out interlock problem is unresolved pending further review

(289/85-25-01).

.

3.2.2 Rod Exercise Surveillance

A shift inspector witnessed portions of surveillance

procedure 1303-3.1, " Control Rod Drive Movement"

(see paragraph 2.2.6). The procedure successfully

,

demonstrated the operability of all safety rods as

required by Technical Specification (TS) 4.7.1, but the '

'

shift inspector questioned how the surveillance would be

current for startup when TS 4.7.1 requires the rod

exercising only during power operations. P

1

The resident inspector reviewed the surveillance data

records and confirmed the shift inspector's findings. The

TS 4.7.1 surveillance is performed to ensure that a stuck

rod does not exist prior to returning to power operation

or that a stuck rod does not go undetected for long

periods of time while at power. There were no

,

provisions in the licensee's startup procedure to perform

! this surveillance during or after an extended period at

. hot shutdown. The licensee was aware of the problem and

l was manually tracking this type of surveillance to assure

its completion prior to startup. The inspector discussed

the possibility that this should be part of the reactor

l startup checklist. Licensee representatives' acknowledged

this and stated it would be considered. The inspector

it em W. a.c.r.p'. r *

i

.a ! n .. .: o -
. ' .4 ...  :

4.7.1 and nad no further comments.

3.2.3 Calibration Stickers

During tours in the turbine and intermediate buildings,

shift inspectors noted various instrument sages with

,

calibration stickers that indicated the gages were past

due for calibration. When challenged, the licensee

i

i

! '

L

-- - ---- - - - - . - _ _ . . .. . . . . - - , - - . - - . . . - - . - - - - - - - , - - - - - . . , - - . . .

-

- ~ . . . . - . . - . . .

16

provided sufficient records, on a sampling basis, to

demonstrate the calibration of gages within the specified

intervals.

,

The resident inspector queried licensee representatives as

to why the calibration stickers were not updated.

Licensee representatives indicated that the calibration

stickers were to be phased out and replaced with

individual gage records that are now being used to assure

proper calibration. The problem is that many calibration

procedures still require the use of stickers and it is a

low priority administrative effort to change these

procedures. Based or. this review and review of data

related to testing in past inspection reports, the

inspector concluded that operators used calibrated gages

for regulatory required functional testing and control

room parameter monitoring. However, the inspector stated

that calibration stickers indicating past due calibration

were confusing from an op.:stor's viewpoint in that the

reliability of the instrument could be questioned when

data was needed for operations or testing. Licensee

management acknowledged the problem and stated that the

calibration sticker problem would be resolved on a higher

priority basis. The inspector had no further comments in

j this area.

3.2.4 NRC Review of "Furmanite" Process

!

The restart staff reviewed the licensee's repairs to the

leaking components found during the reactor building

inspection (see paragraph 4.2.2.4). A sealant compound

"Furmanite" was injected into the leaking area and formed

,

a new gasket thus stopping the leaks. In the case of the

flange leak, a machined sealing ring was bolted over the

outer surfaces of the two flanges to form a void that was

filled with Furmanite. ants void formed a new pressure

boundary and the injected Furmanite then sealed the

boundary. In the case of the leaking valve the Furmanite

was injected between the body and the bonnet and formed a

new gasket.

,

The licensee's plant engineering group prepared a safety

evaluation (10 CFR 50.59 review). No. 85-250-M, to

determine the acceptability of Furmanite for this

  • *

i -

,

  • , :At * *ryf ,

. *' * *

,a*g ,e rs

"...No new unreviewed safety questions.... The flange

injection clamp adds [approximately) 15 lbs. to the

existing flange assembly...[which was] determined to be

, insignificant from a dead weight concern...[the added]

mass does not degrade any previous seismic

classification...."

While the work was in progress, the inspectors queried the

licensee as to whether or not stresses on the flange bolts

had been considered in the safety evaluation and the

- .- - - - ---- - - - - . . - - . - _ - - , . - - - - - - - - - - - . . .--

1

. 17

inspector determined that it was not. The vendor's

engineering group was contacted to perform such a

calculation. Furmanite provided an analysis which  ;

indicated the bolts would not be overstressed. This was  !

based on normal operating pressure of 900 psig leaking and

being sealed by the Furmanite. The inspectors determined

that, by applying higher pressures than the 900 psig, the

bolts would not be overstressed.

The inspectors and licensee representatives discussed the

effects of Furmanite injection during a telephone

conversation with tne vendor engineering representative.

The vendor representative noted that although Furmanite

was injected under pressure, this pressure tended to

relieve itself. The vendor representative stated that tha

last segment of Furmanite installed might place some

stress on the flange bolts but it should not be signifi-

cant. The vendor representative also stated that, from

their experience, stress analyses were not required for

similar design rated flanges.

The inspectors reviewed the licensee safety evaluation.

Based on this review, discussions with the licensee,

discussions with Furmanite, and review of the Furmanite

safety analysis for bolt stresses, the inspectors

determined that the licensee's initial safety evaluation

was acceptable. While the evaluation could have been more

thorough and included an analysis of flange stresses,

their not being included did not constitute a serious

review deficiency. The inspector noted that safety

evaluation (85-250-M) also included a review of the

specific procedure for applying Furmanite to this flange. -

The licensee's generic procedure 1410-Y-44, "Use of

Furmanite," was used in this process.

The staff concluded that the flange bolts would not be

overstressed and the Furmanite process is an acceptable

temporary repair method. The licensee committed to repair

the joints prior to returning to power after the

completion of the Spring 1986 eddy current outage. This

matter is unresolved pending completion of licensee action

as committed to above and subsequent NRC Region I review

(289/85-25-02). -

3.2.5 D-r !~~ ce-* ci

During witnessing of a surveillance in a radiation

monitoring system (RMS) cabinet located in control room

console panel right front, the shift inspector observed

circuit drawings and typed procedural notes posted on the

inner cabinet door (see paragraph 2.2.6). Further

inspection revealed that uncontrolled and unapproved

.

'

drawings and procedural notes were posted to the inside of

all eight RMS panel access doors and reactor protection

system subassembly cabinet "C."

- . _ _ - __ _ . _ _ . _ . _ _ _ _ _ - _ _ _ - _ ____

18

Administrative procedure (AP) 1001H, " Drawing Utiliza-

tion," states that the use of drawings and notes are not

authorized on plant panels. All drawings and procedures

observed on the cabinet doors were removed by the

instrument and controls supervisor.

The posting of uncontrolled and unapproved drawings and

procedures on cabinet doors is contrary to 10 CFR 50,

Appendix B, Criterion VI and licensee procedure AP 100lH

and constitutes an apparent violation (289/85-25-03).

3.2.6 H2/02Storage

A shift inspector tour of the intermediate building

revealed that hydrogen and oxygen gas cylinder bottles

were stored side by side. The gases were used as calibra-

tion gases for the reactor building hydrogen monitors.

The TMI-l Restart Staff determined that, although the

bottles were in seismically designed storage racks, this

situation was not strictly in accordance with the

licensee's occupational safety and health manual. Later

review by licensee representatives in consultation with

the Harrisburg OSHA (Occupational Safety and Health

Administration) office determined that the storage aspects

were acceptable. Plant engineering personnel also re-

viewed the situation and they concluded that no fire

hazard existed. The adequacy of the licensee's hazard

analysis for this area is unresolved pending a subsequent

inspection (289/85-25-04).

3.3 Conclusion

Licensee management continued their detailed attentiveness and

involvement in daily activities. In general, highly motivated

managers appear to be instilling that same motivation in plant

personnel,

i

There may be a need for more detailed recording of events or

abnormal conditions in the control room logs when plant personnel

! make observations or conduct activities. A licensee decision is

needed on whether or not to use and/or rely on calibration stickers

l on instruments in the plant. Apparently, this decision was being

held up because numerous facility procedures are affected by that

'

decision.

l

The licensee's post-trip review met the intent of the Salem AWS

(anticipated transient without scram) corrective actions. However,

! there could have been more plant engineering review and involvement

on the stress analysis for the flange bolts during the planning

l phase for the "Furmanite Repairs." The licensee's 10 CFR 50.59

l evaluation nevertheless was adequate to meet the requirements of

l that rule.

i

L

. 19

The drawing control problem was an apparent violation of regulatory

requirements. However, it was not characteristic of the licensee's

overall program since drawings and procedures available for use

inside and outside the control room were verified to be controlled

copies when checked during previous inspections since the program

problem was identified in this area in 1981.

4. Startup and Power Escalation Testing

4.1 Scone of Review

4.1.1 Test Witnessing

At various times during the inspection period, the inspec-

tors witnessed testing in progress on a sampling basis.

However, test procedure (TP) 800/2, " Trip on Loss of

Feedwater," and TP 800/8, "RCS Overcooling Test," were

witnessed in their entirety by the THI-1 Restart Staff.

The tests were observed to verify that:

--

tests were conducted in accordance with

appropriate test procedures;

--

prior to performing tests, an adequate briefing

was conducted for operations personnels

--

test prerequisites and initial conditions were

met;

--

applicable technical specifications were

complied with;

--

operator actions were correct;

--

test engineers were knowledgeable in their

,. duties; and.

--

test results were acceptable.

In addition to TP 800/2 and TP 800/8 witnessing, the

following tests were observed and/or their test results

independently reviewed by the TMI-1 Restart Staff during

this inspection period. -

-- Tr c?C/*, "" 't 'es! ' Str:^ r:r-

-

ce*"

--

TP 836/1, "Feedwater System Operation and

, Tuning"

-- TP 849/1, "ICS Tuning at 40% Power"

--

TP 846/1, "Incore Thermocouple Operations Test"

--

TP 885/2, " Turbine Bypass Valve Test"

_ _ _ - - -- -. __.

. 20

--

TP 800/2, " Trip on Loss of Feedwater"

.

--

TP 800/8, "RCS Overcooling Test"

--

OP 1105-14. " Loose Parts Vibration Monitoring

Data"

--

RP 1550-01, "Incore Detector Checkout"

--

RP 1550-04, " Power Imbalance Detector

Correlation"

4.1.2 Test Results Review

Test results from the testing program for the 40% power

plateau were reviewed by the inspector to verify that:

--

test changes were approved and implemented in

accordance with administrative procedures;

--

changes did not impact the basic objectives of

the test;

--

test deficiencies and exceptions were identified

and resolved and resolutions were acceptables

--

the cognizant engineering group has evaluated

the test results and signified that testing

demonstrated that design conditions were mets

and.

--

test results vere within established acceptance

criteria or properly resolved.

4.2 Licensee Test Results and NRC Findings

,

Licensee performance of key tests is described in this section. The

discussion includes a summary of key test objectives and test

results: test performance including operators, test engineers and

equipments and pertinent findings and outstanding problem areas

-

identified and/or NRC findings as a result of testing.

4.2.1 Reactor Trip on Loss of Feedwater/ Turbine Trip (TP 800/2)

.: ..

' ~

_; 'r' --

Restart condition 2.b requires that prior to operation

above 48% power, the licensee demonstrate automatic

initiation of emergency feedwater (EFW) pumps upon loss of

both main feedwater pumps. This test was performed on

October 21, 1985, in accordance with TP 800/2, " Reactor

Trip on Loss of Feedwater/ Turbine Trip," during which both

main feedwater pumps were tripped. Following the trip of

, 21

1

the feedwater pumps, the following events were expected to

occur.

--

reactor trip on anticipatory loss of feedwater

--

turbine bypass setpoint transfers to 1010 psig

--

turbine trip coincident with loss of main

feedwater pumps

--

containment isolation on reactor trip

--

OTSG levels control at 30 inches using EFW flow

--

all three EFW pumps start automatically.

Operations and test personnel were stationed in the

control room, at the remote shutdown panel, at the two

motor driven and one steam driven EFW pumps, and outside

the plant to visually monitor which main steam relief

valves actually opened. Recorder charts were connected at

the EFW pumps and remote shutdown panel for data

recording.

Personnel were stationed at all three EFW pumps to assure

proper operation of the pumps. To temporarily rectify a

previous problem in which the steam supply relief valves

to EFP-1 lifted during pump startup, one steam supply

valve from the "A" OTSG (MS-V-13A) was shut and disabled

from automatic actuation to reduce steam flow and preclude

actuation of the relief valves. The previous actuation of

these relief valves was detailed in inspection report

50-289/85-22.

The operator stationed at EF-P-1 was also tasked with

opening of MS-V-13A manually, 11 necessary. MS-V-13B was

allowed to operate automatically to supply steam to

EF-P-1. In accordance with TP 800/2, after automatic

actuation of EF-P-1 was demonstrated, EF-P-1 was secured

from further operation so that motor driven pumps EF-P-2

A&B could control OTSG 1evel.

4.2.1.2 Observations and Findinas -

Tr -!- ~~ e n r cf r?r-t c~ e r s. r ~ .- * : ~ * t r o. --*-r? w--

observec in the control room ano in the interracciate

building at the emergency feedwater pumps. The following

observations of operators and plant equipment were noted.

Control Room

Overall, operator performance appeared to be good.

Operators were attentive, maintained their stations,

monitored appropriate instrumentation, and reported

.

.

23

important readings and alarms. Plant operations for

this test were directed by the plant operations

manager. Test direction was formal, and operators

were kept informed of overall plant status, test

concerns, and impending actions. Procedures were

followed completely.

Since a reactor trip took place, the immediate

actions of ATP 1210-1, " Reactor Trip / Turbine Trip,"

were followed. A shift foreman read the procedure

actions aloud and received formal responses from

operators concerning completed actions.

Communications during performance of post-trip

actions were good. In general, annunciators were

properly acknowledged.

Proper communications between the control room and

plant stations, such as the EFW pumps and the outside

safety valve watch, were maintained. The test was

conducted according to procedures test prerequisites

were satisfied and test limitations were observed.

Intermediate Buildina

The motor driven EFW pumps (EF-P-2 A&B) and the

turbine driven EFW pump (EF-P-1) were manned by

operations personnel who wc e in direct communica-

tions with the control room. Test engineering

persennel were present to take data for the test, and

plant engineering personnel were present to monitor

inservice test parameters.

All three EFW pumps started on loss of main feedwater

within the required time frame. As noted previously,

one steam supply valve was shut to EF-P-1. This did

not affect proper operation of EF-P-1, and the steam

supply safety valves did not lift. The operator

stationed at EF-P-1 was available to open the other

steam supply valve if it had been required. However,

as noted in inspection report 50-289/85-22, a

satisfactory permanent resolution to the lifting of

EF-P-1 safety valves on normal pump starts is

required. As required by the test procedure, EF-P-1

was secured after approximately 12 minutes of

y . . ,

1 . . : . c. 3 ;; . . . 3 7,. . .. t . e .,

maintain 0T56 levels ano for tne natural circulation

test, TP 800/8.

. 23

Test Results

The test results indicated that actuation times for

all three EFW pumps met the test acceptance criteria.

For comparison, the results from the previous test as

conducted per TP 700/2 as well as the results of TP

800/1 are included in the following table.

Acceptance

Actuation Time Criteria

(seconds) (seconds)

TP 700/2 TP 800/2

Turbine Driven Pump

(EF-P-1) 15 20 <40

Motor Driven Pump

(EF-P-2A) 3 1.8 <15

Motor Driven Pump

(EF-P-2B) 3 2.0 <15

In addition to the automatic start of the EFW pumps

after shutting off both main feedwater pumps the

reactor tripped: the turbine tripped; partial

containment isolation on reactor trip functioned and

OTSG 1evels were controlled at approximately 30

inches using EFW pumps. Another test objective, that

the turbine bypass valve function at a turbine header

pressure of 1010 1 10 psig, did not appear to be

proven by the test. Although the turbine bypass

setpoint was found to be in calibration, the turbine

bypass valves did not control turbine header steam

pressure as expected. This problem is further

detailed in paragraph 4.2.3 below.

4.2.2 RCS Overcoolina Test (TP 800/8)

4.2.2.1 Test Performance

The licensee prepared test TP 800/8, "RCS Overcooling

Test," to further demonstrate plant operation in a natural

circulation mode and to gain additional real plant data

cenectr.ing this operatien. The barie ch,4ectiva ef the

test was to demonstrate that the control rocm operators

could properly throttle EFW flow to prevent overcualing

the reactor coolant system (RCS) while feeding the OTSGs

following loss of the reactor coolant pumps (RCPs). The

OTSGs were to be fed from an initial level of 30 inches in

the startup range to a level of 50% (245 inches) in the

operating range. During this transition, it was desired

to start and maintain natural circulation.

- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ _ - _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .

24

TP 800/8 was not part of the restart test program

committed to the NRC for the startup of 'INI-1 and

satisfactory completion of all aspects of this test were

not required for satisfactory completion of the startup

test program. TP 800/8 was scheduled following the trip

during performance of TP 800/2 since the reactor would be

shut down at this time. The driving force for natural

circulation was to be an expected decay heat of 0.5 to

0.7% of rated power based on two to three days of

operation at 40% of rated power.

Since this test was to take place immediately following

the reactor trip, the operator and test engineer manning

as stated for TP 800/2 was also in place for this test.

The RCPs were stopped approximately 25 minutes after the

reactor scram and after plant conditions had stabilised.

The motor driven EFW pumps were already running and

maintaining OTSG 1evels at approximately 30 inches.

Because of transients experienced on the restart of RCPs

during performance of natural circulation test TP 700/2,

an engineering evaluation had been done for TP 800/2.

This resulted in a major revision to TP 800/2 which

included setting a limit for reactor coolant system hot

leg temperature (Th) prior to restart of the RCPs and

manually controlling steam generator pressure just prior

to and immediately after the starting of RCPs to minimize

the secondary side pressure transient. An extensive two

hour briefing was given to the operating crew which was to

perform TP 800/2 and TP 800/8. This briefing included

test performance, operator actions, possible problems, and

expected plant responses in natural circulation and return

to forced circulation. NRC inspectors attended and

verified the acceptability of this briefing.

4.2.2.2 General Observations - RCS Overcoolina Control Test

Since this test was done immediately following the reactor

trip per TP 800/2, the observations concerning operator

actions for TP 800/2 also apply to the performance of TP

800/8. As noted previously, the objective of the test was

to raise the level in both OTSGs equally from 30 inches to

245 inches using EFW flow, raise OTSG 1evels without

overcooling the RCS, and establish and maintain natural

tir d.stion.

Apparently, because there was insufficient decay heat, the

licensee was not able to raise the OTSGs to the 50% level

(operating range) and maintain natural circulation.

However, a fundamental objective of the procedure was met

in that the operators were able to throttle EFW to the

OTSGs without overcooling of the RCS. It appears that

__ _ _ _ _ . - _ _ _ _ - _._ _ __. _ -_ _ _ _ ._ __ _ _ _ .

25

approximately 20 minutes after tripping of the RCPs,

4 natural circulation was achieved for a short period of

time in that a 30 degrees F temperature difference was

obtained between Th and Tc; and Th and incore thermocouple  :

temperatures were tracking. Th increased initially,

reached a peak temperature of 556 degrees F at

i approximately 15 minutes then decreased in a continuous

manner. The behavior of Th followed closely with the .

'

analytically predicted model (GPU study TDR-410. "RETRAN

Analysis of the 'INI-140% LOFW & Transition to Natural

Circulation Startup Test") with the differences only in

absolute peak Th value and the timing of reaching the

peak.

Although Tc followed MSG pressure, because of very low

decay heat and possible excessive steaming in MSG "A",

the desired OTSG level of 50% operating range was not

i accomplished before OTSG "A" pressure dropped below 750

psig. The 750 psig OTSG pressure was one of the criteria

,

to restart the RCPs per test procedure. The RCPs were

subsequently restarted to establish the forced circula-

'

tion.

!

!

The possibility of the depressurization in OTSG pressure

below 750 psig during, the test had been analyzed in the

licensee's study (TDR-410). This was discussed in the

briefing prior to the test. The inspector also noted that

smooth natural circulation had been lost before forced

, circulation was established. Although, all test objec-

tives were not completely met, licensee engineers stated

l they considered the test a success because sufficient

information was obtained. The licensee is in the process

j of evaluating the test results. Appropriate information

, derived from this test will be issued for future plant

operation Ruidelines.

I 4.2.2.3 Licensee Post-Trio Data Review

i

l'

The resident inspector attended the licensee's post trip

review of the trip test on October 21, 1985. The licensee

review was required by Administrative Procedure 1063,

" Reactor Trip Review Process." This was the first time

that the licensee performed this review since the licenses

significantly revised the procedure. As a result, it took

.,
.  ;,,,, .

.e.

.

. . . , . -

.

,.<;.-  : ...,,..s .i

respect to gathering and properly reviewins tr.e cata.

a The licensee noted several minor administrative

i inconsistencies in the procedure that will be corrected.

l The post trip review identified the problem associated ,

with turbine bypass control valves and main steam safety I

'

valves interaction which are described further in para-

i graphs 4.2.1.2 and 4.2.3 of this report. Subsequent to

t

the post trip review, licensee representatives required

that an independent safety review be conducted addressing,

specifically, the safety valve-turbine bypass valve >

interaction problem.

!

l

. _ - _ . , _ , . _ _ - . . _ _ . _ _ . _ _ _ _ _ _ _ _ _ _ . _

. _ _ _ _ _ . _ _ _ _ _ . _

_ _ _ _

26

The inspector independently reviewed the completed

enclosure 1. " Post Trip Review of AP 1063," and the

recorder strip charts and verified that the data required

by enciesure 1 was retrieved with no significant ,

deficiencies noted. The inspector also reviewed the i

minutes of the independent safety review noted above.

This review concluded that the manner in which the

secondary system responded was not a safety concern and

the plant could be safely returned to power. The

inspector concluded that the procedure adequately

evaluated plant performance to the extent necessary to

reach a decision related to startup. In addition, the

inspector confirmed the licensee's conclusion.

4.2.2.4 Post-Trio Reactor Buildina Inspection

Immediately following the loss of feedwater

reactor / turbine trip on October 21, 1985, a shift

inspector accompanied licensee representatives into the

reactor building for a post-trip inspection. Two leaks ,

'

were identified during the licensee's walkdown of the

reactor building. The leaks were a flange leak on an

emergency feedwater spray ring header on once through

steam generator (OTSG) 1A and a valve body-to-bonnet leak l

on a steam generator level transmitter root valve,

FW-V-1093. Both leaks were repaired by using a process

known as "Furmaniting," as described in paragraph 3.2.4.

The licensee's inspection of the reactor building was

thorough and adverse conditions were properly identified

to the operating shift.

4.2.2.5 Effect of 40% Reactor Trio on RCS and OTSG Leak Rates

Based on data review of surveillance procedure (SP)

1301-1, " Shift and Daily Checks," and SP 1303-1.1,

" Reactor Coolant System Leak Rate," the inspector noted

i

that both RCS and OTSG 1eak rates on the day following the

trip test (October 22, 1985) remained well within the l

technical specification's limits and were consistent with

'

1

the previous day's result. No abnormal conditions were

< observed. ,

,

4.2.3 Turbine Bypass Valve Testina (TP 885/2) -

n ..,a er '

7- ee-t- "..;.,.....,..,,,,...4.

.

, ' in

conjunction witn it ELL,2 "heactor 1 rip Test." The tes.

objective was to verify that the six turbine bypass valves

opened fully within three seconds after trip of the

turbine, and that the turbine bypass valve functioned at '

i

1010 psis i 10 psig. During performance of TP 800/2, the

main feedwater pumps tripped causing both a reactor trip

!

and turbine trip. During the pressure increase in the

steam headers, the turbine bypass control setpoint is

expected to move to 1010 psig and attempt to control steam

i

'

i

h

- - _ _ _ . _ _ _ _ . _ _ , _ __,_ _ _.___. _ . _ ___ _ _ _ _. _ _ _ _ _ . -

.. 27

.

pressure at this level. All the turbine bypass valves

should fully open in less than three seconds. Since the

bypass valves alone may not control the full header

pressure transient, some of the main steam safety valves

would then open to relieve further increases in header

pressure.

Although the turbine bypass valves are not safety related,

the results of this test warrant further review. During

the test, the bypass valves failed to fully open. Since

the valve indication limit switches are set at 5% and 95%

the actual amount that the bypass valves opened was not

known. However, post-test graphs indicated that

integrated control system (ICS), turbine bypass "B" loop

demand (valves MS-V-3A, 38, and 3C) received an 30% open

demand signals and "A" loop demand (valves MS-V-3D, 3E,

and 3F) received a 30% open demand signal. Hence, the

bypass valve opening times could not be measured.

The failure of the turbine bypass valves to fully open was

explained by the fact that the main steam safety relief

valves opened before the turbine bypass valves. Based on

visual observations of an operator stationed for this

purpose, it appears that all eighteen mai steam safety

relief valves lifted. The lifting of the relief valves

apparently took pressure control away from the turbine

bypass valves.

Subsequent to the test, based on review of test graphs,

calibration of steam pressure instruments, and the reac-

tion of the ICS, the licensee initially concluded that

some main steam relief valve set points may be set too

low. The inspector reviewed test data for the setpoint

test of six safety relief valves performed April 15, 1985,

which were tested in pince while the plant was at normal

operating temperature. This data indicated that relief

valves were properly set.

The licensee committed tos (1) document a test exception

for the test results, with a test to be reaccomplished

during the 100% trip test, (2) test the set points of the

main steam safety valves and evaluate the need to set them

at a higher pressure prior to going beyond the 75% power

plateau (an NRC hold point), and (3) document this

cm f et ; in a. Ie*ter :: the P.neten 7 84-tetrtr: ur.

Also, Tp 800/2 will be accomplished at 100% power, which

tests the ability of the turbine bypass valves control

setpoint to transfer and control pressure at 1010 psis

following a reactor trip. This test problem is unresolved

pending completion of licensee action as stated above'and

subsequent NRC review (289/85-25-05).

28

4.2.4 Unit Load Steady State Test (TP 800/5)

The steady state plant parameters as measured per TP 800/5

at 40% power plateau continuously showed good agreement

with the predicted values. As noted in inspection report

50-289/85-24, at the 15% power level these values showed

some deviation. Tave was expected to be 579 degrees F and

actually was found to be 568 degrees F. However, Th and

Tc measurements correlated well to expected values. Near

the 15% power level the relationship of Tave to reactor

powar level makes the transition from an increasing linear

relationship to a constant Tave relationship. Tave

measurements at 25% and 40% power levels were as

predicted.

The licensee again performed the test at 15% power during

the startup after the 40% trip test. The test results

were approximately the same as before. Discussions with

B&W indicate that a Tave of 579 degrees F could be

achieved if OTSG water levels were reduced from 30" to 25"

or 26". However, the plant operators are reluctant to

steam down to these low levels.

Test engineers are evaluating a test exception for this

data point since the Tave data at higher power levels is

as expected and the plant does not normally operate for

lengthy periods at 15% power.

4.2.5 Loose Parts Monitoring (OP 1104.14)

The licensee continued to record loose parts monitoring

base line data at each power level plateau. Sound levels

were recorded at 40% power both before and after the

reactor trip at 40%. A B&W technician was on hand to

racntd data and to parannally monitor andin channela. Nn

loose parts or significant unusual noises were detected.

4.2.6 Core Power Distribution Verification (RP 1550-08)

The detailed core power distribution at the 40% power

plateau was measured by the licensee per procedure RF

1550 08, " Core Power Distribution Verification " using the

~

incere detector system. The incore detector system

contains fifty-two incore flux detector assamblies with

'. . :. s . .. ,.

.: . .

. . . .

following results:

-- The readings from symmetrical location detectors

were within 10% of the symmetrical group average

values.

-- The measured radial peaking factor for each fuel

assembly was consistent with the analytically

predicted value. The comparison of the highest

measured radial peaking f actor (1.291) at core

29

location K-11 agreed closely with the predicted

value of 1.298.

--

The measured total peaking factor in each fuel

assembly also agreed consistently well with the

predicted value. The highest measured total

peaking factor of 1.585 agreed well with the

predicted value of 1.462 and was within the

established acceptance range of 12%.

--

The measured linear heat rates accounting for

various uncertainty factors were within TS 3.5.2.7 limits, as indicated in the following

table.

Axial Location From Measured Maximum Maximum Allowable

Bottom of Core Linear Heat Rate Linear Heat Rate

(ft) (kw/ft) (kw/ft)

11.14 2.490 15.20

9.43 4.496 16.26

7.71 4.942 17.10

6.00 4.756 17.50

4.29 4.422 16.31

2.57 4.311 14.37

0.86 3.159 11.48

All results were acceptable.

4.2.7 Power Imbalance Detector Correlation Test (RP 1550-04)

Power imbalances from power range channels (NI-5 through

8) were fed to the reactor protection system to provide

the power-flow-imbalance trip. The licensee performed an

out-of-core imbalance calibration using information from

the incore detector system per test procedure RF 1550-04,

" Power Imbalance Detector Correlation Test," Revision 9.

Through test data review, the inspector noted that an

excellent linear relationship exists between the indicated

out-of-core power distribution and the actual measured

incore values. The slopes of measured out-of-core

imbalance to incore imbalance were 1.22, 1.23, 1.12, and

1.15 for NI-5, NI-6, NI-7, and NI-8, respectively. The

acceptance criterion for this correlation slope was

grrater ths- 1.'5. Uren cert?etien of *kir tc5*. the

reactor protection system channel C c1116rtr.ca amplifier

gain from NI-7 input was adjusted by instrument and

controls technicians in accordance with procedure SP

1303-4.1 Appendix B. " Procedure for Changing Scaled

Difference Amplifier (Delta Flux) Gain," on October 21,

1985. The inspector verified that the actual " difference

amplifier" sain setting K value of 5.035 (corresponding to

an imbalance slope of 1.15 as described above) was

properly implemented in the calibration. The inspector

-__ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -

30

also noted that during this test the quadrant power tilt

values which ranged from 2.01 to 2.71 were all within the

TS 3.5.2.4 limit of 3.52.

4.2.8 Restart Condition Verification

Restart condition 2.b stated the following:

" Prior to operation above 48% power, GPU

Nuclear Corporation shall demonstrate

automatic initiation of EFW pumps upon

loss of both feedwater pumps."

As discussed in paragraph 4.2.1, this was demonstrated by

performance of TP 800/2. The inspectors verified

satisfactory perforinance of TP 800/2 and that the required

restart condition was met.

4.3 Conclusion

Testing for the 40% power plateau was accomplished in accordance

with procedures, data were acceptable, and test objectives were met

or proper test exceptions taken. Licensee management was responsive

to inspector observations. Problem areas were quickly corrected and

actions were taken to preclude their recurrence. Overall, licensee

performance in the test area can be considered acceptable and, to

date, test results are acceptable to proceed with the startup

program. The adequacy of the OTSG safety valve settings needs to be

resolved.

5. Pressurizer Power Operated Relief Valve (PORV) Setpoint Check

5.1 Discussion

on October 25, 1985 the NRC shift inspector witne==ad portions of

surveillance procedure 1303-11.45, "PORV Setpoint Check," Revision

5, September 3, 1985, from the control room. Two instrument and

control (I&C) technicians performed this test at the module cabinet

located in the relay room one floor below the control room. The

first portion of the test required that the fuses be pulled on the

electrical control power to the PORV making it inoperable. This

action invoked Technical Specification 3.1.12.3 requirements that

the associated block valve be closed within one hour of the PORV

being declared inoperable. This one hour time clock requirement was

; ;, b ;. t r. t; i ..;

! m ..r.'r 4 ct I t 4 5 r. . r~ .

As one of the technicians was increasing the test voltage setting on

the equipment used in conjunction with this surveillance the control

room operator and the NRC shift inspector noted an unexpected low

spike on pressurizer level channel 1 in the control room. The low

spike was sufficiently large to cause the low pressuriser level

annunciator to actuate. The shift supervisor and the technicians

reviewed the wiring logic diagrams and determined that the

prescribed test sequence should not affect pressurizer level

_ _ _ _ _

.

31

.

,

instrumentation. The IEC technicians per'formel the steps again and

were able to repeat the spike on the pressurizer level channel 1

instrument. The shift supervisor,then directed that pressurizer

level channel 3 be selected. The technicians performed the steps

again and this tine they had no effect on the pressurizer level

channel that was selected. The shift supervisor then gave

permission to continue with the surveillance test. The effect of

the PORV-calibration check on pressurizer level was not completely

resolved at that time, only to the point of licensee supposition.

that a loose wire existed in the'same cabinet that was being worked

on.

The I&C technicians successfully parformed the surveillance

procedure up to the point of checking the trip (opening pressure)

setpoint, which was found to be within technical specification

tolerance (2450 1 25 psig). Before starting the portion of the

procedure associated with checking the reset (closing pressure)

setpoint, the technicians determined that the procedure could not be

performed as written and generated an exception sheet. The

technicians discussed the exception sheet with the shift supervisor

who concurred with the noted exception. He gave them permission to

perform the steps in the corrected sequence as described on the

exception sheet. Later, senior day shift I&C technicians determined

that the two technicians had misread the procedure.

The two technicians then obtained reset setpoint voltage readings.

The value (2438 psig) obtained was out of tolerance high (2400 1

6.25 psig). This value would allow the PORV to be able to ressat

after lifting at a high pressure, but the setting would cause the

PORV blowdown time to be shortur. The technicians generated a

deficiency sheet addressing the noted out-of-tolerance value for the

PORV reset pressure. The technicians brought the deficiency to the

shif t supervis or's attention, 'and af ter discussing the findings,

permission van given to recalibrate the setpolat.

In the meantime the shift supervisor, because of the technical

specification one-hour time clock requirement, directed the block

valve (RC-V-2) to be shut. This was logged in the shift foreman's

log as occurring at 2:37 a.m.

The I&C technicians, however, were unable to recalibrate the reset

setpoint, and they discussed this problem with the shift supervisor.

The shift supervisor directed them to return all calibrated

adjustment device values back to where they had found them prior to

,

,,

. . *

. . "r , , , g ; g

  • J ., c # g( .=

/- r s,( g,;

test equipment ano close the cabinets., Tne surveillanct was

terminated and would be turned over to the day shift and more

experienced I&C technicians. At 2:52 a.m., as recorded in the shift

foreman's log, the PORV fuses were installed and the block valve was

opened. The shift supervisor declared the PORV to be operable at

'

that time.

At approximately 7:30 a.m., the NRC inspectors requested to see the

documents associated with the surveillcnce. The NRC inspectors were

__ _ . _ . - _ - _ - - - .- ._- - .-- . _ - _ , - - - ___ . -, _ -

._

.

32

directed to the senior day shift I&C technician who was following up

on this matter. At that time, the original surveillance procedure

could not be found, but the original exception and deficiency sheets

were found in a trash can in the I&C shop by the I&C technician and

the NRC inspectors.

Based on preliminary assessment of the information known of this

matter, the inspector questioned the operability of the PORV. The

inspector discussed his concern with the plant operations manager

who stated that he considered the PORV operable; however, he

directed a bench test of the module in question to be performed

immediately to resolve the inspector's concern. The bench test

determined that both the trip and reset setpoint values were within

the allowable tolerances. The inspector acknowledged that the PORV

was operable and had no further questions about the operability of

the valve.

While performing the bench test, the licensee contacted one of the

two technicians to determine the location of the original

surveillance procedure. At 10:30 a.m. the licensee was able to

locate the original surveillance procedure and reported that it was

on a desk in the I&C shop. In addition, later that day, SP

1303-11.45 was properly performed and reconfirmed that the PORV

t setpoints were correct.

The dayshift I&C technicians reported that the surveillance was

performed in error during the midshift because the technicians did

not correctly perform step 8.1.8.1 of the procedure which clarified

where voltages were to be read for a proper calibration check.

5.2 Scope of Review

The inspectors reviewed the incident on the apparent improper

performance of the PORV surveillance and the licensee's review of

this matter to determine the following items.

-- details regarding the cause of the incident and the

chronology

-- consistency of licensee actions with license requirements,

approved procedures, and the nature of the incident

-- proposed licensee actions to correct the cause of the

incident

Tne inspectors' review of the surveillance activity incAudes

discussions with cognizant licensee personnel and review of the

following documents.

-- Surveillance procedure (SP) 1303-11.45, Revision 5,

September 3,1985, "PORV Setpoint Check"

-- SP 1303-11.45, partially completed procedure from the

midshift on October 25, 1985

- - - _ _ _ - - - - _. . _ - . _ _ -

-- _

_ . _. . - ___-- - - _ . . - . _ _

. -

33

s

--

Exception Sheet E-1 to SP 1303-11.45, dated October 25,

1985

--

Deficiency Sheet D-2 to SP 1303-11.45, dated October 25,

1985

--

(Draf t) Plant' Incident Report No.1-85-13

--

Shift foreman log and control room operator log for

October 25, 1985 -

The inspectors also accompanied licensen personnel while they

performed the bench test of the PORV reset value. ,

5.3 Licensee's Review / Findings

During the morning of October 25, 1985, the TMI-1 Restart Staff

expressed concern regarding the apparent poor document control

practice of the exception and deficiency forms being thrown away and

the relatively poor performance on the completion of an apparently

routine calibration check. The licensee immediately dedict.ted two

senior knowledgaable individuals to independently review the event

and resolve the staff's concerns. Their review included interviews

with personnel involved and a review of the applicable logs.

reconstruction of the event chronology was generated as part oi i.ne

review. In addition, the licensee convened the Plant Review Group

to review the data to determine if the licensee was proceeding in a

correct manner with respect to the operability question of the PORV.

Although plant management had already concluded that the PORV was

operable, as an independent verification the licensee stopped

scheduled maintenance testing and performed a bench test of the PORV '

module in order to be responsive to the NRC concerns. The bench

test was quickly able to determine the operability of the PORV. In

addition, the licensee conducted an immediate search to locate the

missing surveillance procedure.

Subsequently, the licensee decided to develop a plant incident

report (PIR) as the mechanism to capture the information and to

disseminate lessons learned. Based on their review, as stated in

the PIR, the licensee' concluded the actions of the shift supervisor

were correct and in accordance with the technical specifications.

The shift supervisor" properly directed and controlled the events in

accordance with applicable facility procedures. All independent

reviews performed, including the Plant Review Group review and

' *

r e:1 - - ? t ' i m.- - .-hnt r.r : -r : u u- ' -

---.'

responsibilities, aid not uncover any significant safety concern.

The PORV was considered operable by the licensee at all times during

this event, except during actual surveillance testing.

With respect to discarding the exceptica and deficiency sheets, the

licensee's review was unable to determine how this occurred or who

discarded them. The licensee, however, concluded e. hat there was

(

>

,

k

1

34

l

y i

l

in place, as part of their administrative controls program, various

checks and balances that would have identified that the sheets were

missing. The surveillance procedure coordinator is specifically

tasked with reviewing all surveillance packages for completeness.

In addition, the noted deficiency and exception were described on

the shift turnover sheet which would trigger identification of the

problem to I&C personnel from the operations department.

Also, the licensee concluded that surveillance packages should

,

remain together at all times.

3

The licensee found that the shift supervisor could have asked more

'

probing questions associated with the noted exception sheet

-

generated by the two technicians. It was determined that the two

' technicians had never performed this test before and had misread the

procedure. If the shift supervisor had asked more questions,

misreading of the procedure may have teen identified. The procedure

as written was correct and properly obtained the required data. The

data obtained by the technicians for the PORV reset pressure setting

was not actually the required reading due to improper test

connections being used. These test connections were not the

g

+

required test connections specified in the written surveillance

g procedure. The surveillance that was performed on the dayshift

verified that the procedure could be performed as written and that

the PORV was operable.

The licensee plans to review the event with all personnel who may be

involved with official facility surveillance records. The

requirement to maintain and preserve legal records will be restated.

5.4 NRC Staff Findings

The licensee was responsive to NRC concerns and their actions were

timely and provided sufficient information to permit the concerns

associated with PORV operability to be resolved immediately.

I Although the shift supervisor could have been more inquisitive,

l especially on the rather routine surveillance, the shift

supervisor's action on the operability of the PORV was technically

correct and he complied with technical specifications. The shift

,

supervisor could have better substantiated by documentation his

reasoning on the operability of the PORV. Also, the inspector

reviewed and concurred with the findings in the licensee's plant

incident report.

!

l With respect to the documentation control problen, licensee

personnel did not maintain control of the surveillance package in

that the exception and deficiency forms were separated from the

! surveillance procedure, contrary to AP 100lJ provisions, and

j personnel were careless by either discarding the forms or not

l providing enough attention to detail to assure the completed package

l was retained.

!

l

l

t

l

!

!

_

35

It is merely speculative as to whether or not Technical Specification 6.10 requirements to maintain original plant records

would have been adhered to since that issue was dependent on whether

or not the licensee's review process would have identified the

missing records (E&D forms). Since the surveillance procedure had

not been discarded, it is likely that the exception and deficiency

sheets would have been identified as missing. However, this may not

have occurred in time for the records to be retrieved from the

trash. The licensee then would have had to reproduce a

reconstructed record which would be a violation of TS 6.10.

From our independent review of this matter, the inspector concluded

there was no apparent motive to cover up the event. The E&D forms

were in an obvious place -- the trash can in the I&C shop, which was

not a place one would discard a record if one were trying to cover

up the event. Further, three other records of the event were

retained, i.e., the completed procedure and the control room

narrative logs. Further the apparently adverse test results did not

reflect an immediate need to shut down the facility.

A review of the exception and deficiency sheets (required by AP

1001J) indicated that the questions on the form were not clear as to

the intent of each question. In response to one of the questions on

the deficiency D-2. the shift supervisor marked "yes" indicating

that the deficiency (lack of proper reset value for the PORV)

reflected a failure to meet TS acceptance criteria. However, the

shift foreman's log reflected that the shift supervisor determined

that the PORV was operable without details of how he came to that

conclusion. (It is well recognized that a specific TS LCO alone

does not determine operability because the specific TS must be

reviewed in conjunction with the TS definition of operability, TS 1.3.) Licensee managers reported that shift supervisors were

instructed to mark yes to the above noted question when the more

restrictive criteria of the applicable surveillance procedure could

not be met. The inspector noted that no provisions then exist on

the E&D form to determine operability of the surveillance component

and that it would appear that the shift supervisor did not

adequately resolve the deficiency before declaring the component

operable.

The problem was evident upon review of the computerized outstanding

E&D list in which a number of deficiencies were listed; but, upon

closer review, one found procedural, editorial, or updating

problems; not TS compliance or operability problems. The licensee

acknow'cdref

. this situt i:e c.f aprerf :: reciew * .i st a tier.;

with submitting a report on this matter to NRC Region 1. Inis is

unresolved pending completion of licensee action to assure that

surveillance test exceptions / deficiencies are appropriately reviewed

for operability, TS compliance, reportability, and pending the

submittal of a report to the NRC on the incident. Further licensee

corrective action for this incident will be reviewed in a future

inspection (289/85-25-06).

- -_ _ -

36

5.5 Conclusions

The licensee's initial and followup actions were responsive to the

NRC concerns. The PORV was always operable. Licensee operators

maintained the plant in the mode which they considered to be safest.

No motive for wrongdoing in discarding the deficiency and exception

sheet was noted. Existing documentation and handling measures for

surveillance test exceptions and deficiencies were considered to be

poor and warrant improvement.

6. Nuclear Safety and Compliance Committee Performance

6.1 Review

By Commission Memorandum and Order CLI-85-2, dated February 25,

1985, the licensee was required to maintain an expanded Board of

,

Directors and a Nuclear Safety and Compliance Committee (NSCC). The

committee is to have a staff of its own and is designated to monitor

the operation and maintenance of the GPU systems nuclear units with

specific attention to adherence to procedures and license

requirements. This requirement was restated a2 restart condition

1.t by NRC letter dated October 2, 1985.

The NSCC of the GPU Board of Directors was established on February

23, 1984. The committee consists of three outside members of the

GPU Nuclear Board of Directors. This committee has established on

the TMI-1 site a staff consisting of a staff director and three

members. This staff has been established to assist the NSCC in

accomplishing its mandate. The staff activities are governed by

NSCC staff guidelines.

During this inspection, the activities of the TMI-1 NSCC site staff

were reviewed. The on-site staff performs evaluations in accordance

with a six-month activity schedule which has been approved by the

NSCC. The current activity' schedule (July to December 1985)

,

provides for monitoring in the following areas.

Operations

-- monitor conduct of operations by ongoing in-plant

observations

-- evaluate normal and emergency operating procedures

-- r r ".: r c : . . . I r ,cc v. d i t c r e u 3

-- operations surveillance

-- radioactive waste operations

Maintenance

-- control of heavy loads

-- system maintenance and testing, including:

_ - _ _

. . _ .

37

--

containment

--

reactor pr<ssure boundary

--

maintenance of EQ components

--

restart activities

--

Davis-Besse lessons learned

--

control of maintenance

--

corrective maintenance reports to )(C

--

planning and scheduling (evaluate outage p-eparations)

--

response to NRC and INPO findings

Training

--

maintenance training

--

STA training

--

simulator instructors

--

INPO accreditation

Licensing

--

evaluate LER/ PRE (Licensee Event Report /Potentially

Reportable Evnnt Reports)

--

action item t~acking

--

preliminary safety cencerns

Radiological Control

--

contaminction control

--

radiation awareness reports

-

Chemistry

--

monitor enemistry dcpartment operations

--

chemistry procedures

Technical Functions

--

operating experience and assessment overview

- -. - - .

-_

..

- .- - . .. - - _ _ . -

38

Safety Committees

-- GORB

--

plant review group

--

10SRG

--

other

Quality Assurance

-- evaluate corrective action systems (QDRs, MNCRs, Audits.

LER followup, etc.)

Emergency Preparedness

--

monitor exercises and drills

Plant Engineering

-- overview of organization and responsibilities

NSCC Requests

-- observations meeting

--

Davis-Besse incident

-- biennial procedure review followup

--

plant incident reports

--

procedure standardization

-- MORT training

-- NSCC semi-ennual report

l

i

l

The following evaluation reports of evaluations conducted as

described in the activity schedule have been issued since January 1,

l 1985. -

! -- THI-R-85.001, Instructor Training and Qualification, April

. ??e-

l

l

-- TMI-R-85.002, Evaluation of Control Room Audits, March 15,

1985

-- TMI-R-85.003, Procurement and Control of Parts, Materials,

and Services, March 15, 1985

-- TMI-R-85.004, Processing of Design Change Packages, March

25, 1985

-- THI-R-85.005, Control of Special Processes, March 29, 1985

l

__

39

--

TMI-R-85.006, Investigation into the Use of Inappropriate i

Welding Procedures  !

-- TMI-R-85.007, Instrument Calibration Stickers, May 21,

1985

-- TMI-R-85.008, Training Document Control, Records and

Records Retention, April 17, 1985

--

THI-R-85.009. Training Examination Control Process, April

30, 1985

--

THI-R-85.010, Normal and Emergency Operating Procedures,

May 6, 1985

--

TMI-R-85.011, Control of Measuri.g and Test Equipment, May

21, 1985

-- THI-R-85.012, Evaluation of the Control of Equipment

Status, May 23, 1985

-- TMI-R-85.013, Evaluation of Emergency Preparedness, June

20, 1985

--

THI-R-85.014, Review of Independent Onsite Safety Review

Group (10SRG), July 29, 1985

-- TMI-R-85.015, Review of Potential Safety Concerns and

Potential Reportable Events, September 5, 1985

--

TMI-R-85.016, Evaluation of Training Program Development

Approval and Review

The inspector also reviewed the following NSCC documentation.

--

monthly reports of NSCC staff activities for the months of

July and September 1985

-- minutes of NSCC-NSCC staff meeting conducted July 23, 1985

- --

Nuclear Safety and Compliance Committee report No. I to

the GPU Nuclear Board of Directors, October 15, 1984

--

Nuclear Safety and Compliance Committee Report No. 2 to

  • '

the C7. %::1. .ir  ! . irc :: - s.  : *'. :~

.

--

draft Nuclear Safety and Compliance Committee staff

semi-annual report for the period April 1, 1985, through

September 30, 1985

A number of questions developed during the review of the above

documents. These were discussed with NSCC staff members as follows.

-. . ._

40

- --

The activity schedule provides for a significant amount of

time to be spent evaluating operations and maintenance,

yet no evaluation reports are issued which discuss these

areas.

The staff stated this time is devoted to the routine

observations of operations and maintenance. If matters

which require further staff evaluation were identified,

results of these evaluations would be documented in

evaluation reports.

--

The monthly reports discuss matters in which the staff is

involved which are not documented in evaluation reports.

These are activities in which the staff has been involved

during routine observations but not to the extent that an

evaluation report is appropriate. The monthly report does

provide the committee with some information on these

topics. If the committee feels more information is

necessary, they would request it from the staff.

--

It appears not all findings and recommendations which

appear in evaluation reports are included in the NSCC's

+

semi-annual report to the board. How are these

transmitted to the site or sites?

One method by which these are transmitted is during

scheduled observation meetings with the committee, the

committee staff and senior GPU management. There may be

other methods of which the staff is not aware.

--

Is there routine followup to implementation of findings

and recommendations?

There is no formally established planned followup to

findings and recommendations known to the NSCC staff.

--

Monthly reports discuss trending of certain data. What is

being trended by the staff?

The following is being trended:

--

unit availability -

--

' .11 r-te

.

--

audit findings (QA)

--

radiological data

--

injury rates

--

iodine ratio

-- - - - __

- . . - . _ . . . -

41

--

open job tickets

--

Are activities at Parsippany also evaluated?

Activities at Parsippany are also evaluated by the staff.

--

How frequently are NSCC and NSCC s.aff meetings held?

These meetings are held monthly and generally last over

six hours each. These meetings provide far a major

exchange of information between the committee and the

staff.

6.2 NRC Findinas

The requirement that an NSCC with an independent staff be maintained

to monitor the operation and maintenance of TMI-1, with specific

attention to adherence to procedures and licensee requirements is

being met. Staff guidelines have been prepared which describe the

staff activities which are to be performed in order for the

committee to perform its task. These guidelines are being adhered

to. A staff, which has appror.imately 80 man years of nuclear

experience in various disciplines, has been established at the THI-l

site to perform evaluations. Based on discussions with staff

members the committee appears to stay well informed of site

activities and staff findings both through the receipt of staff

reports (semi-annual report to NSCC, monthly report to NSCC, and

specific evaluation reports) and through monthly meetings with the

staff.

Staff evaluation reports and semi-annual reports to the committee

are detailed and reflect adherence to a preplanned schedule. The

committee, in addition to approving a staff activity schedule,

frequently makes specific requests for evaluations or other actions

from the staff. There does not appear to be any formal followup by

the staff as to the disposition of evaluation findings and

recommendations.

The committee's evaluation and disposition of staff findings and

recommendations other than those formally transmitted by reports to

the GPU Nuclear Board of Directors is beyond the scope of this site

inspection. This area is unresolved pending NRC Region I additional

~

review of NSCC activities (289/85-25-07).

t.1 C an ?us i c-

The licensee is meeting the requirements of restart condition 1.t to

retain the NSCC. Additional NRC staff review will be needed to

evaluate the effectiveness of the NSCC.

42

7. Administrative Control Implementation

7.1 Review

The inspectors reviewed selected TMI-1 Administrative Control

Procedures to verify that APs were properly implemented by licensee

personnel.

The selected procedures reviewed included:

-- AP 1002, Revision 36, October 14, 1985, " Rules for the

Protection of Employees Working on Electrical and

Mechanical Apparatus";

--

AP 1036, Revision 6 February 104 1985, " Instrument

Out-of-Service Control";

--

AP 1037, Revision 4, January 3, 1985, " Control of Caution

and DNO Tags"; and,

--

AP 1063, Revision 4, August 19, 1985, " Reactor Trip Review

Process."

The specific scope and findings related to each of these areas are

addressed below.

7.2 Rules for the Protection of Employees Working on Electrical and

Mechanical Apparatus

The stated purpose of AP 1002 is to provide methods to insure the

safety of personnel who may be required to work on or around

electrical and mechanical apparatus under the jurisdiction of TMI-1.

The apparatus covered by the procedure may or may not be

radioactive. The procedure is also intended to help assure that

equipment tagging and alignments are consistent with nuclear and

equipment safety concerns. As stated further in AP 1002, the

,

detailed procedure provides a step-by-step method for the electrical

and/or mechanical isolation and control of equipment of which

maintenance, inspection, troubleshooting or testing is to be

performed.

The inspector reviewed the detailed procedures specified in AP 1002

and verified that adequate controls were in place for-awitching and

tagging operations including appropriate requirements for proper

rmz ' n to be ccr.fu::ed p:ic:  : rcr ~irr ( r.'; r .: frer e.rvitt. r

however, the inspector noted that the control room operator assigned

to switching and tagging activities could approve a tag even though

he may not be certified as a switching and tagging initiator. The

inspector noted that this apparent inconsistency was allowed by

procedure and the number of control room operators not qualified as

switching and tagging initiators was minimal. Licensee

.

e- -g--, . ~ - . - - - . - ,,r . ,.-. .._ , , . , - - _ - . , . -, -.

. _

43

.

representatives stated that their certification practices would be

reviewed for appropriate followup actions, and the inspector had no

i further questions regarding this matter.

In addition to the above procedure review, the inspector randomly

selected several active switching and tagging sheets and verified

their accuracy. The inspector also determined that the switching

and tagging sheets correctly reflected what tags were posted in the

plant.

The inspector concluded, based on this review, that the licensee's

switching and tagging prcgram and procedures were properly

controlling the removal and return of equipment that was required to

be tagged out. The comments noted by the inspector were considered

to be of a minor nature.

7.3 Control of Caution and Do-Not-Operate Taas

The AP 1037 describes the purpose and control of caution and

do-not-operate (DNO) tags. Caution tags are used as an information

tag only; not.as safety tags for protection of personnel. A caution

tag is to be attached to a component, control switch or other device

to indicate an off normal condition or to caution personnel to a

specific condition which must be satisfied prior to using the

component or device. A do-not-operate tag, which is primarily used

for equipment protection may be used in place of a caution tag

particularly when used in environments where the caution tag may

easily deteriorate under extended use.

The inspector reviewed the requirements related to caution and

do-not-operate tags, as specified in AP 1037, and determined that

the guidance appeared to provide effective administrative controls

for using these tags. In addition, the inspector reviewed the

caution and do-not-operate tag log books and selected tags in use,

i Based on this review, the inspector noted only minor potential

administrative problems. The procedure established no policy on

when to consolidate caution tag log sheet entries, and the operator

cannot tell whether a log sheet is removed or lost from the note-

book. Also, AP 1037 states that upon removal of a do-not-operate

tag, the time (as well as other items) is to be filled in on the log

,

I

! sheet; however, the log sheet does not include a place for recording

time. The inspector discussed these observations with licensee

representatives and had no further comments regarding-this matter.

r_

-

l

,4 y e - -, - _- q . . . - r - - - ; - r.

___

The stated purpose of AP 1036 is to describe the method of control

of read out devices which become inoperable or are strongly

! suspected of being inoperable such that they are marked, documented

! and controlled until repair is affected. The procedure applies

principally to the control of out-of-service instruments and read

out devices which are required by the technical cpecifications. It

applies to meters, gauges, amplifiers and recorders when they become

i

1

-

, , . - _ . , _

. - . .--

,

44

-f

inoperative or are displaying what appears to be incorrect

information.

The inspector reviewed this procedure and verified that a log was

being maintained of out-of-service devices, the log reflected actual

equipment status, and out-of-service equipment did not or would not

have an adverse affect on safe plant operations.

The inspector noted that the number of pieces of equipment

out-of-service was minimal. Equipment that has been out of service

for extended periods generally was minimal and had no effect on

plant operation. Several old out-of-service stickers were still in

effect; two since 1977, two since 1981, five since 1983 and five

since 1984. However, the average length that a major piece of

equipment would remain out of service was short. From the review of

the log entries and selected stickers the inspector determined that

the lictusee's program for control of out-of-service instruments was

being implemented.

'

7.5 Reactor Trip Review Process

The inspector reviewed AP 1063 to ensure that the procedure required

the gathering and retaining of key plant parameters and plant

records that would identify significant changes and trends of plant

parameters that may be indicative of plant performance problems and

that the procedure required the necessary safety review and analysis

to be performed to ensure the plant could properly restart. In

addition, the procedure was reviewed to ensure that noted problems,

if any, were properly characterized, tracked and resolved, if

necessary, prior to restart.

Implementation of this procedure was verified as noted in paragraph

3.4. The inspector reviewed the data generated to support the post

trip review. The inspector determined that the major and

significant parameters were being retrieved and recorded. The

procedure was structured in a manner that allowed the review group

to smoothly move through the checklist in a timely manner. The -

'

licensee did note several minor administrative problems that need to

be reviewed but which had no significant impact on the overall

' '

objective of the procedure. The checklist had the necessary

provisions to cause independent reviews to be performed to resolve

identified inconsistencies in plant response. Overall, the

'

procedure was determined to be adequate.

'

.. .

The administrative procedures described above were technically

adequate although they could be improved to enhance effectiveness.

In general, these procedures were properly implemented.

.

- , - . , . , , - - . - - - - - - - - , - - - - - - - - - -r- - - , - - - , - , , - - , - - - -- -

, - , - -

- - - - - -- - m. .- ,n n- . - , . - , - - -

__

'

45

8. Exit Interview

The inspectors discussed the overall inspection scope and findings with

licensee management at the exit interview conducted on October 25, 1985.

The following licensee personnel attende1 the final exit meeting.

D. Carl, Review Program Coordinator, TMI-1

J. Colitz, Plant Engineering Director TMI-1

S. DiVito, Supervisor Design and Drafting - THI, Technical Functions

T. Hawkins, Manager, TMI-1 Startup and Test, Technical Functions

H. Hukill, Vice President and Director, TMI-1

C. Incorvati, TMI-1 Audit Supervisor, Nuclear Assurance

M. Nelson, Supervisor, Review Program, THI-1

S. Otto, TMI-1 Licensing Engineet. Technical Functions

L. Ritter, Administrator II, Plant Operations, TMI-1

M. Ross, Manger, Plant Operations, TMI-1

C. Shorts, Manager Technical Functions THI-1. Technical Functions

D. Shovlin, Manager, Plant Maintenance, TMI-1

P. Sinegar, Administrator II - Maintenance, THI-1

H. Snyder, Preventive Maintenance Manager, THI-1

R. Toole, Operations and Maintenance Director, THI-1

The exit meeting was also attended by Ajit Bhattacharyya, a nuclear

engineer representing the Commonwealth of Pennsylvania. As discussed at

the meeting, the inspection results are summarized in the cover page of

the inspection report. Licensee representatives indicated that none of

the subjects discussed contained proprietary information.

There was an interim exit on October 24, 1985, with the Nuclear Safety

.

'

and Compliance Committee Staff members (Mr. E. Hammond, et. al.) to

discuss the results of the inspection on their activities.

Unresolved items are matters about which information is required in order

to ascertain whether they are acceptable items, violations or deviations.

Unresolved item (s), discussed during the exit meeting, are documented in

paragraphs 3.2.1, 3.2.4, 3.2.5, 3.2.6, 4.2.3, 5.4, and 6.2.

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EDO PRINCIPAL CORRESPONDENCE CONTROL

- ------------- - - - - - -

FROM: DUE: 12/27/85 EDO CONTROL: 001245

DOC DT: 10/22/85

JANE LEE FINAL REPLY:

ETTERS, PA.

TO:

COMM. ASSELSTINE

FOR SIGNATURE OF: ** GREEN ** SECY NO:

DESC: ROUTING:

TMI " COOLING TOWER DRIFT"

DATE: 12/11/85

ASSIGNED TO: M

'

CONTACT: M ANYIT U

i

SPECIAL~ INSTRUCTIONS OR REMARKS:

A SHORT ANSWER IS IN ORDER.

TAREHM

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NRR RECEIVED: 12/11/85

ACTION: egGPL4: MIRAGLIA_ p[de7 4-

ROUTING: DENTON/EISENHUT

PPAS

M0SSBURG

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