ML20094A998: Difference between revisions

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This precautionary statement in conjunction with the proposed technical specification to limit the loads during testing, responds to the NRC request to prevent unnecessary loading of the engines above 185 psig BMEP. The proposed technical specifications were transmitted as PCOL-84/17 (MPAL letter, dated July 20,1984).
This precautionary statement in conjunction with the proposed technical specification to limit the loads during testing, responds to the NRC request to prevent unnecessary loading of the engines above 185 psig BMEP. The proposed technical specifications were transmitted as PCOL-84/17 (MPAL letter, dated July 20,1984).
: 2. Training on the above precautionary statement - Training on the procedure change will be included in the training package for Amendment 13 to the Facility Opercting License. This amendment is expected to include related technical specification revisions. The training package will be initiated following receipt of the amendment.
: 2. Training on the above precautionary statement - Training on the procedure change will be included in the training package for Amendment 13 to the Facility Opercting License. This amendment is expected to include related technical specification revisions. The training package will be initiated following receipt of the amendment.
: 3.      Confirmatory walkdown of the engine fuel oil lines - As noted in the letter dated July 26, 1984, a confirmatory walkdown has been completed. Several areas of concern were noted on the Division 11 engine fuel lines. Corrections of these conditions have been completed.      The corrections were performed by replacing or rerouting the affected lines.
: 3.      Confirmatory walkdown of the engine fuel oil lines - As noted in the {{letter dated|date=July 26, 1984|text=letter dated July 26, 1984}}, a confirmatory walkdown has been completed. Several areas of concern were noted on the Division 11 engine fuel lines. Corrections of these conditions have been completed.      The corrections were performed by replacing or rerouting the affected lines.
8408060189 840803 gDRADOCK 05000416 PDR                                                              ^
8408060189 840803 gDRADOCK 05000416 PDR                                                              ^
mumua. Niiddle South Utilities System                      i U i
mumua. Niiddle South Utilities System                      i U i
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AECM-84/0392 MIZIL3IPPI POWER & LIGHT COMPANY                    Page 2
AECM-84/0392 MIZIL3IPPI POWER & LIGHT COMPANY                    Page 2
: 4. Inclusion of fuel oil inspection in the plant surveillance program - As noted in the July 26, 1984 letter, a visual inspection of the engine fuel oil lines has been incorporated in the Augmented Maintenance / Surveillance Program.
: 4. Inclusion of fuel oil inspection in the plant surveillance program - As noted in the {{letter dated|date=July 26, 1984|text=July 26, 1984 letter}}, a visual inspection of the engine fuel oil lines has been incorporated in the Augmented Maintenance / Surveillance Program.
Should you need additional information please contact this office.
Should you need additional information please contact this office.
,                                                  Sincerely, L. F. Dale Director, Nuclear Licensing & Safety
,                                                  Sincerely, L. F. Dale Director, Nuclear Licensing & Safety

Latest revision as of 20:38, 24 September 2022

Confirms Completion of Listed 840720 & 26 Commitments Re Tdi Diesel Generators.Correction of Deficiencies Noted During Confirmatory Walkdown of Engine Fuel Oil Lines Completed
ML20094A998
Person / Time
Site: Grand Gulf  Entergy icon.png
Issue date: 08/03/1984
From: Dale L
MISSISSIPPI POWER & LIGHT CO.
To: Harold Denton
Office of Nuclear Reactor Regulation
References
ACEM-84-0392, ACEM-84-392, NUDOCS 8408060189
Download: ML20094A998 (2)


Text

..

N MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi P. O. B OX 1640 J AC K S O N, MIS SIS SIP PI 3 9 2 05 August 3,1984 NUCLEAR LICEN$ LNG & SAFETY DEPARTMENT Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commissien Washington, D.C. 20555 Attention: Mr. Harold R. Denton, Director

Dear Mr. Denton:

SUBJECT:

Grand Gulf Nuclear Station Units I and 2 Docket Nos. 50-416 & 50-417 License No. NPF-13 File: 0260/L-860.0 Additional Informaton - TDI Diesel Generators AECM-84/0392 Various commitments related to the TDI diesel generators were made in the Mississippi Power & Light Company (MP&L) letters dated July 20,1984 and July 26, 1984. This letter provides confirmation of the completion of these commitments,

l. Addition of precautionary statement in the " loss of offsite power" procedure - A statement has been added to the subject Off-Normal Event Procedure by change notice dated July 20, 1984. This note specifies the 5740 kw (equivalent to 185 psig BMEP) limit on diesel generator loading during this off-normal event. The statement advises the operator that the Division I and Division 11 diesel generator may, if necessary, be used to carry additional plant loads.

This precautionary statement in conjunction with the proposed technical specification to limit the loads during testing, responds to the NRC request to prevent unnecessary loading of the engines above 185 psig BMEP. The proposed technical specifications were transmitted as PCOL-84/17 (MPAL letter, dated July 20,1984).

2. Training on the above precautionary statement - Training on the procedure change will be included in the training package for Amendment 13 to the Facility Opercting License. This amendment is expected to include related technical specification revisions. The training package will be initiated following receipt of the amendment.
3. Confirmatory walkdown of the engine fuel oil lines - As noted in the letter dated July 26, 1984, a confirmatory walkdown has been completed. Several areas of concern were noted on the Division 11 engine fuel lines. Corrections of these conditions have been completed. The corrections were performed by replacing or rerouting the affected lines.

8408060189 840803 gDRADOCK 05000416 PDR ^

mumua. Niiddle South Utilities System i U i

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AECM-84/0392 MIZIL3IPPI POWER & LIGHT COMPANY Page 2

4. Inclusion of fuel oil inspection in the plant surveillance program - As noted in the July 26, 1984 letter, a visual inspection of the engine fuel oil lines has been incorporated in the Augmented Maintenance / Surveillance Program.

Should you need additional information please contact this office.

, Sincerely, L. F. Dale Director, Nuclear Licensing & Safety

LFD /sad cc
Mr. J. B. Richard Mr. R. B. McGehee Mr. N. S. Reynolds 1

Mr. G. B. Taylor Mr. Richard C. DeYoung Office of Inspection & Enforcement U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. J. P. O'Reilly Regional Administrator U.S. Nuclear Regulatory Commission Region ll 101 Marietta Street, N.W., Suite 2900 Atlanto, GA 30323 r

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