IR 05000458/2017003: Difference between revisions

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[[Issue date::November 13, 2017]]
[[Issue date::November 13, 2017]]


Mr. William F. Maguire, Site Vice President Entergy Operations, Inc. River Bend Station 5485 U.S. Highway 61N St. Francisville, LA 70775
Mr. William F. Maguire, Site Vice President Entergy Operations, Inc.
 
River Bend Station 5485 U.S. Highway 61N St. Francisville, LA 707 75


SUBJECT: RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2017003
SUBJECT: RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2017003


==Dear Mr. Maguire:==
==Dear Mr. Maguire:==
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station, Unit 1. On October 11, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report. NRC inspectors documented two findings of very low safety significance (Green) in this report. One of these findings involved a violation of NRC requirements. Further, inspectors documented a licensee-identified violation, which was determined to be of very low safety significance, in this report. The NRC is treating these violations as non-cited violations consistent with Section 2.3.2.a of the NRC Enforcement Policy. If you contest the violations or significance of the non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the River Bend Station. If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the River Bend Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station, Unit 1.
 
On October 11, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
 
NRC inspectors documented two findings of very low safety significance (Green) in this report. One of these findings involved a violation of NRC requirements
. Further, inspectors documented a licensee
-identified violation, which was determined to be of very low safety significance, in this report. The NRC is treating these violations as non-cited violation s consistent with Section 2.3.2.a of the NRC Enforcement Policy.


Sincerely,/RA/ Jason W. Kozal, Chief Project Branch C Division of Reactor Projects Docket No.: 50-458 License No.: NPF-47  
If you contest the violation s or significance of the non-cited violation s, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the River Bend Station.
 
If you disagree with a cross
-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S.
 
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555
-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the River Bend Station. UNITED STATES NUCLEAR REGULATORY COMMISSION REGION IV 1600 E. LAMAR BLVD ARLINGTON, TX 76011
-4511 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading
-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
 
Sincerely,/RA/ Jason W. Kozal, Chief Project Branch C Division of Reactor Projects Docket No.: 50-458 License No
.: NPF-47  


===Enclosure:===
===Enclosure:===
Line 34: Line 53:


===w/Attachments:===
===w/Attachments:===
1.Supplemental Information2.Public Radiation Safety InspectionDocument Request  
1.Supplemental Information 2.Public Radiation Safety InspectionDocument Request  


x SUNSI Review: ADAMS: Non-Publicly Available x Non-Sensitive Keyword: By: JKozal/dll x Yes No x Publicly Available Sensitive NRC-002 OFFICE SRI:DRP/C RI:DRP/C SPE:DRP/C C:DRS/EB1 C:DRS/EB2 C:DRS/OB NAME JSowa BParks CYoung TFarnholtz GWerner VGaddy SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/STG for /RA/ DATE 11/3/2017 11/7/2017 11/3/2017 11/03/2017 11/13/2017 11/6/17 OFFICE C:DRS/PSB2 TL:IPAT BC:DRP/C NAME HGepford THipschman JKozal SIGNATURE /RA/ /RA/ /RA/ DATE 11/6/17 11/6/2017 11/13/2017 Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 05000458 License: NPF-47 Report: 05000458/2017003 Licensee: Entergy Operations, Inc. Facility: River Bend Station Location: 5485 U.S. Highway 61N St. Francisville, LA 70775 Dates: July 1 through September 30, 2017 Inspectors: J. Sowa, Senior Resident Inspector B. Parks, Resident Inspector L. Carson II, Senior Health Physicist N. Greene, PhD, Health Physicist S. Money, Health Physicist J. O'Donnell, CHP, Health Physicist J. Braisted, PhD, Reactor Inspector Approved By: J. Kozal, Chief Project Branch C Division of Reactor Projects 2  
x SUNSI Review: ADAMS: Non-Publicly Available x Non-Sensitive Keyword: By: JKozal/dll x Yes No x Publicly Available Sensitive NRC-002 OFFICE SRI:DRP/C RI:DRP/C SPE:DRP/C C:DRS/EB1 C:DRS/EB2 C:DRS/OB NAME JSowa BParks CYoung TFarnholtz GWerner VGaddy SIGNATURE
/RA/ /RA/ /RA/ /RA/ /RA/STG for
/RA/ DATE 11/3/2017 11/7/2017 11/3/2017 11/03/2017 11/13/2017 11/6/17 OFFICE C:DRS/PSB2 TL:IPAT BC:DRP/C NAME HGepford THipschman JKozal SIGNATURE
/RA/ /RA/ /RA/ DATE 11/6/17 11/6/2017 11/13/2017
 
Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 05000458 License: NPF-47 Report: 05000458/2017003 Licensee:
Entergy Operations, Inc.
 
Facility:
River Bend Station Location:
5485 U.S. Highway 61N St. Francisville, LA 70775 Dates: July 1 through September 30, 2017 Inspectors:
J. Sowa, Senior Resident Inspector B. Parks, Resident Inspector L. Carson II, Senior Health Physicist N. Greene, PhD, Health Physicist S. Money, Health Physicist J. O'Donnell, CHP, Health Physicist J. Braisted, PhD, Reactor Inspector Approved By:
J. Kozal, Chief Project Branch C Division of Reactor Projects
 
2  


=SUMMARY=
=SUMMARY=
IR 05000458/2017003; 07/01/2017 - 09/30/2017; River Bend Station; Heat Sink Performance; Follow-up of Events and Notices of Enforcement Discretion The inspection activities described in this report were performed between July 1 and September 30, 2017, by the resident inspectors at River Bend Station and inspectors from the NRC's Region IV office. Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements. Additionally, NRC inspectors documented one licensee-identified violation of very low safety significance in this report. The significance of inspection findings is indicated by their color (i.e., Green, greater than Green, White, Yellow, or Red), determined using NRC Inspection Manual Chapter 0609, "Significance Determination Process," dated April 29, 2015. Their cross-cutting aspects are determined using NRC Inspection Manual Chapter 0310, "Aspects within the Cross-Cutting Areas," dated December 4, 2014. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," dated July 2016.
IR 05000458/2017003; 07/01/2017  
 
- 09/30/2017; River Bend Station; Heat Sink Performance; Follow-up of Events and Notices of Enforcement Discretion The inspection activities described in this report were performed between July 1 and September 30, 2017, by the resident inspectors at River Bend Statio n and inspectors from the NRC's Region IV office
. Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements
. Additionally, NRC inspectors documented one licensee-identified violation of very low safety significance in this report. The significance of inspection findings is indicated by their color (i.e., Green, greater than Green, White, Yellow, or Red), determined using NRC Inspection Manual Chapter 0609, "Significance Determination Process," dated April 29, 2015. Their cross-cutting aspects are determined using NRC Inspection Manual Chapter 0310, "Aspects within the Cross-Cutting Areas," dated December 4, 2014. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy.
 
The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG
-1649, "Reactor Oversight Process," dated July 2016.


===Cornerstone: Initiating Events===
===Cornerstone: Initiating Events===
: '''Green.'''
: '''Green.'''
The inspectors reviewed a self-revealed finding for the licensee's failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram. Corrective actions included properly installing the tee connection and writing specific procedural guidance on compression fitting inspection, installation, remake, and repair (CR-RBS-2017-02405). The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee's failure to properly install the tee connection caused a steam leak that led to a reactor scram. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, "Initiating Events Screening Questions."  The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5]. (Section 4OA3)  
The inspectors reviewed a self-revealed finding for the licensee's failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram. Corrective actions included properly installing the tee connection and writing specific procedural guidance on compression fitting inspection, installation, remake
, and repair (CR
-RBS-2017-02405). The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee's failure to properly install the tee connection caused a steam lea k that led to a reactor scram
. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, "Initiating Events Screening Questions."  The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5].
  (Section 4OA3)


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," which states, in part, "Measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions."  Specifically, prior to September 28, 2017, the licensee's current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated. This finding was entered into the licensee's corrective action program as Condition Report CR-RBS-2017-06998.
The inspector s identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," which states, in part, "Measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions."  Specifically, prior to September 28, 2017, the licensee's current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30
-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated. This finding was entered into the licensee's corrective action program as Condition Report CR-RBS-2017-06998.


The inspector determined that the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30-day inventory requirement needed to be re-performed to assure that accident analysis requirements were met. In accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding had a cross-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin [H.6].   
The inspector determined that the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30
-day inventory requirement needed to be re-performed to assure that accident analysis requirements were met. In accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding had a cross-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30
-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin [H.6].   
(Section 1R07)
(Section 1R07)


=== Licensee-Identified Violations===
=== Licensee-Identified Violations===
A violation of very low safety significance (Green) that was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and associated corrective action tracking numbers are listed in Section 4OA7 of this report.
 
A violation of very low safety significance (Green) that was identified by the licensee has been reviewed by the inspectors.
 
Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. Th is violation and associated corrective action tracking numbers are listed in Section 4OA7 of this report.


4   
4   


==PLANT STATUS==
==PLANT STATUS==
River Bend Station began the inspection period at 88 percent reactor thermal power. Operators were in the process of returning the plant to full power following a scram that occurred on June 23, 2017. The station returned to 100 percent power on July 3, 2017. On July 28, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak. The station returned to 100 percent power on August 3, 2017. On August 18, 2017, an automatic reactor scram occurred due to equipment issues associated with the feedwater level control system. On August 20, 2017, operators conducted a reactor startup. The station returned to 100 percent power on August 28, 2017. On September 22, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak, but did not identify a new fuel leak. The station returned to 100 percent power on September 28, 2017.
River Bend Station began the inspection period at 88 percent reactor thermal power
. Operators were in the process of returning the plant to full power following a scram that occurred on June 23, 2017. The station returned to 100 percent power on July 3, 2017. On July 28, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak. The station returned to 100 percent power on August 3, 2017. On August 18, 2017, an automatic reactor scram occurred due to equipment issues associated with the feedwater level control system
. On August 20, 2017, operators conducted a reactor startup. The station returned to 100 percent power on August 28, 2017. On September 22, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak, but did not identify a new fuel leak
. The station returned to 100 percent power on September 28
, 2017.


=REPORT DETAILS=
=REPORT DETAILS=
Line 70: Line 124:


====a. Inspection Scope====
====a. Inspection Scope====
On July 19, 2017, the inspectors completed an inspection of the station's readiness to cope with external flooding. After reviewing the licensee's flooding analysis, the inspectors chose three plant areas that were susceptible to flooding:   Residual heat removal train B pump room Low pressure core spray pump room Division I emergency diesel generator The inspectors reviewed plant design features and licensee procedures for coping with flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether credited operator actions could be successfully accomplished. These activities constitute one sample of readiness to cope with external flooding, as defined in Inspection Procedure 71111.01.
On July 19, 2017, the inspectors completed an inspection of the station's readiness to cope with external flooding. After reviewing the licensee's flooding analysis, the inspectors chose three plant areas that were susceptible to flooding:
Residual heat removal train B pump room Low pressure core spray pump room Division I emergency diesel generator
 
The inspectors reviewed plant design features and licensee procedures for coping with flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether credited operator actions could be successfully accomplished.
 
These activities constitute one sample of readiness to cope with external flooding, as defined in Inspection Procedure 71111.01.


====b. Findings====
====b. Findings====
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==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
===.1 Partial Walkdown===
===.1 Partial Walk===
 
down


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial system walkdowns of the following risk-significant systems:  August 14, 2017, Division III 125 VDC system  August 28, 2017, Division II standby service water system September 21, 2017, Division II control building chilled water system The inspectors reviewed the licensee's procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.
The inspectors performed partial system walkdowns of the following risk
-significant systems:  August 14, 2017, Division III 125 VDC system  August 28, 2017, Division II standby service water system September 21, 2017, Division II control building chilled water system The inspectors reviewed the licensee's procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.


These activities constitute three partial system walkdown samples, as defined in Inspection Procedure 71111.04.
These activities constitute three partial system walkdown sample s, as defined in Inspection Procedure 71111.04.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 Complete Walkdown
===.2 Complete Walk===
 
down


====a. Inspection Scope====
====a. Inspection Scope====
On August 14, 2017, the inspectors performed a complete system walkdown inspection of the Division I and Division II 125 VDC system. The inspectors reviewed the licensee's procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, and open condition reports. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration. These activities constitute one complete system walkdown sample, as defined in Inspection Procedure 71111.04.
On August 14, 2017, the inspectors performed a complete system walkdown inspection of the Division I and Division II 125 VDC system. The inspectors reviewed the licensee's procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, and open condition reports
. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.
 
These activities constitute one complete system walkdown sample, as defined in Inspection Procedure 71111.04.


====b. Findings====
====b. Findings====
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{{a|1R05}}
{{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==
===
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
Quarterly Inspection
Quarterly Inspection
Line 102: Line 168:
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the licensee's fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:
The inspectors evaluated the licensee's fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:
July 19, 2017, battery 1A room, fire area C-18  July 19, 2017, ENB inverter charger B room, fire area C-19  August 16, 2017, battery 1B room, fire area C-19  August 28, 2017, standby cooling tower pump B room, fire area PH-2/Z-1 For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions. These activities constitute four quarterly inspection samples, as defined in Inspection Procedure 71111.05.
July 19, 2017, battery 1A room, fire area C-18  July 19, 2017, ENB inverter charger B room, fire area C-19  August 16, 2017, battery 1B room, fire area C-19  August 28, 2017, standby cooling tower pump B room, fire area PH-2/Z-1 For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
 
These activities constitut e four quarterly inspection sample s, as defined in Inspection Procedure 71111.05.


====b. Findings====
====b. Findings====
Line 111: Line 179:


====a. Inspection Scope====
====a. Inspection Scope====
On September 27, 2017, the inspectors completed an inspection of the station's ability to mitigate flooding due to internal causes. After reviewing the licensee's flooding analysis, the inspectors chose one plant area containing risk-significant structures, systems, and components that were susceptible to flooding:   Division I and II standby switchgear rooms The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.
On September 27, 2017, the inspectors completed an inspection of the station's ability to mitigate flooding due to internal causes. After reviewing the licensee's flooding analysis, the inspectors chose one plant area containing risk
-significant structures, systems, and components that were susceptible to flooding:
Division I and II standby switchgear rooms
 
The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.


These activities constitute completion of one flood protection measures sample, as defined in Inspection Procedure 71111.06.
These activities constitute completion of one flood protection measures sample, as defined in Inspection Procedure 71111.06.
Line 123: Line 195:


====a. Inspection Scope====
====a. Inspection Scope====
On September 22, 2017, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors reviewed the data from the most recent internal inspection of the Division II emergency diesel generator jacket water cooler and verified that the licensee adhered to the periodic maintenance method outlined in EPRI NP-7552. Additionally, the inspectors walked down the Division II emergency diesel generator jacket water cooler to observe its material condition and verified that the cooler was correctly categorized under the Maintenance Rule and was receiving proper maintenance.
On September 22, 2017, the inspectors completed an inspection of the readiness and availability of risk
-significant heat exchangers. The inspectors reviewed the data from the most recent internal inspection of the Division II emergency diesel generator jacket water cooler and verified that the licensee adhered to the periodic maintenance method outlined in EPRI NP-7552. Additionally, the inspectors walked down the Division II emergency diesel generator jacket water cooler to observe its material condition and verified that the cooler was correctly categorized under the Maintenance Rule and was receiving proper maintenance.


These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.
These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.
Line 133: Line 206:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed licensee programs to verify heat exchanger performance and operability for the following heat exchangers:   Ultimate Heat Sink Division I Emergency Diesel Generator Jacket Water Heat Exchanger EGT-E1A  Division I Containment Unit Cooler HVR-UC1A  Division I Residual Heat Removal Heat Exchanger E12-EB001A The inspectors verified whether testing, inspection, maintenance, and chemistry control programs are adequate to ensure proper heat transfer. The inspectors verified that the periodic testing and monitoring methods, as outlined in commitments to NRC Generic Letter 89-13, utilized proper industry heat exchanger guidance. Additionally, the inspectors verified that the licensee's chemistry program ensured that biological fouling was properly controlled between tests. The inspectors reviewed previous maintenance records of the heat exchangers to verify that the licensee's heat exchanger inspections adequately addressed structural integrity and cleanliness of their tubes. Specific documents reviewed during this inspection are listed in the attachment. These activities constitute completion of four triennial heat sink inspection samples, as defined in Inspection Procedure 71111.07-05.
The inspectors reviewed licensee programs to verify heat exchanger performance and operability for the following heat exchangers:
Ultimate Heat Sink Division I Emergency Diesel Generator Jacket Water Heat Exchanger EGT
-E1A  Division I Containment Unit Cooler HVR
-UC1A  Division I Residual Heat Removal Heat Exchanger E12
-EB001A The inspector s verified whether testing, inspection, maintenance, and chemistry control programs are adequate to ensure proper heat transfer. The inspectors verified that the periodic testing and monitoring methods, as outlined in commitments to NRC Generic Letter 89-13, utilized proper industry heat exchanger guidance. Additionally, the inspectors verified that the licensee's chemistry program ensured that biological fouling was properly controlled between tests. The inspectors reviewed previous maintenance records of the heat exchangers to verify that the licensee's heat exchanger inspections adequately addressed structural integrity and cleanliness of their tubes. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of four triennial heat sink inspection sample s, as defined in Inspection Procedure 71111.07-05.


====b. Findings====
====b. Findings====


=====Introduction.=====
=====Introduction.=====
The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," involving the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis. Specifically, the analysis did not include loss of inventory from the safety-related standby service water system to the nonsafety-related normal service water system via the normal service water return isolation valves (prior to manual operator action to close the valves), given a loss of coolant accident coincident with a loss of offsite power and the single active failure of an emergency diesel generator to start or run.  
The inspector s identified a Green, non
-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," involving the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis. Specifically, the analysis did not include loss of inventory from the safety
-related standby service water system to the nonsafety
-related normal service water system via the normal service water return isolation valves (prior to manual operator action to close the valves)
, given a loss of coolant accident coincident with a loss of offsite power and the single active failure of an emergency diesel generator to start or run.


=====Description.=====
=====Description.=====
The technical specification bases for Technical Specification 3.7.1, "Standby Service Water (SSW) System and Ultimate Heat Sink (UHS)," describe that safety analyses for long-term containment cooling were performed and that for a loss of coolant accident concurrent with a loss of offsite power, the worst case single failure affecting the performance of the standby service water system is the failure of one of the two standby diesel generators, which would in turn affect one standby service water subsystem. The standby service water system is thus designed to preserve the capability to supply adequate cooling water to equipment required for safe reactor shutdown. Additionally, the bases describe that the ultimate heat sink consists of one 200 percent cooling tower and one 100 percent capacity water storage basin, which is sized such that sufficient water inventory is available to provide heat removal capability to safely shut down the plant and to maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available.
The technical specification bases for Technical Specification 3.7.1, "Standby Service Water (SSW) System and Ultimate Heat Sink (UHS)," describe that safety analyses for long
-term containment cooling were performed and that for a loss of coolant accident concurrent with a loss of offsite power, the worst case single failure affecting the performance of the standby service water system is the failure of one of the two standby diesel generators, which would in turn affect one standby service water subsystem. The standby service water system is thus designed to preserve the capability to supply adequate cooling water to equipment required for safe reactor shutdown. Additionally, the bases describe that the ultimate heat sink consists of one  
 
200 percent cooling tower and one 100 percent capacity water storage basin, which is sized such that sufficient water inventory is available to provide heat removal capability to safely shut down the plant and to maintain it in a cold shutdown condition for a 30
-day period with no external makeup water source available
.
The inspector s requested and reviewed Abnormal Operating Procedure AOP
-0016, "Loss of Standby Service Water," Revision 22, which contained a note that states "Within 20 minutes, actions shall be taken to isolate Division I or Division II standby service water return to normal service water to conserve standby cooling tower inventory per Section 5.1 or Section 5.2."  An additional note states that "With a failure of the Division I diesel to start or load, the Division I powered service water system isolation valves are not able to be closed electrically. With pump SWP
-P2C operating, service water flow from Division I standby service water will pass through the unisolated drywell unit coolers and exit into the Division II standby service water return header back to the standby cooling tower. This return flow will be in excess of the design limits for the Division II portion of the standby cooling tower, thus requiring that SWP
-P2C be secured."
 
The inspector s reviewed calculation PM
-194, "Standby Cooling Tower Performance and Evaporation Losses without Drywell Unit Coolers," Revision 10, whose stated purpos e "is to determine the capacity of the ultimate heat sink to mitigate a design basis accident, using the containment heat loads identified in G13.18.0*19 (Ref.


The inspectors requested and reviewed Abnormal Operating Procedure AOP-0016, "Loss of Standby Service Water," Revision 22, which contained a note that states "Within 20 minutes, actions shall be taken to isolate Division I or Division II standby service water return to normal service water to conserve standby cooling tower inventory per Section 5.1 or Section 5.2."  An additional note states that "With a failure of the Division I diesel to start or load, the Division I powered service water system isolation valves are not able to be closed electrically. With pump SWP-P2C operating, service water flow from Division I standby service water will pass through the unisolated drywell unit coolers and exit into the Division II standby service water return header back to the standby cooling tower. This return flow will be in excess of the design limits for the Division II portion of the standby cooling tower, thus requiring that SWP-P2C be secured."  The inspectors reviewed calculation PM-194, "Standby Cooling Tower Performance and Evaporation Losses without Drywell Unit Coolers," Revision 10, whose stated purpose "is to determine the capacity of the ultimate heat sink to mitigate a design basis accident, using the containment heat loads identified in G13.18.0*19 (Ref. II.2) for a design basis loss of coolant accident coincident with a loss of offsite power and failure of Division II standby diesel generator EGS-EG1B."  The conclusion of the inventory loss case was that a margin of approximately 393,100 gallons would exist in the ultimate heat sink basin after 30 days at technical specification limiting initial conditions. However, the inspector was unable to identify where the calculation accounted for the standby service water system water losses associated with the 20-minute operator action to close the normal service water return isolation valves. Therefore, the inspector requested the analysis of record that demonstrated the loss of standby service water (i.e., ultimate heat sink inventory) to the normal service water system from the affected standby service water train would not be in excess of design limits prior to manual isolation. The licensee provided calculation PM-193, "Standby Service Water - Maximum Flow through Break in Tunnel Piping," Revision 1, as the original basis for the 20-minute operator action. The purpose of PM-193 was to determine the inventory margin and operator action time impact of the assumed break given the scenario in the preceding paragraph, but for a failure of the Division I standby emergency diesel generator instead of the Division II. The postulated break occurred downstream of service water return isolation valve SWP-MOV96A in the nonsafety-related normal service water return header. The conclusion of PM-193 is that 229,500 gallons are potentially lost from the standby service water system to the normal service water system within 30 minutes prior to standby service water system isolation. Based upon these results, the inspector estimated that potentially 153,000 gallons of ultimate heat sink inventory could be lost prior to the 20-minute operator action in AOP-0016 to isolate the nonsafety-related from the safety-related service water systems. Therefore, the inspector concluded that the inventory losses associated with the delayed closure of the normal service water isolation valves were not, but should have been, included in the ultimate heat sink inventory analysis and that the reduction of margin in the inventory analysis was significant. Furthermore, the failure of the Division I standby diesel generator to start or run would result in greater inventory losses through the normal service water return isolation valve than for the same failure on the Division II standby diesel generator due to differences in the design between standby service water system trains; however, PM-194 assumed only a Division II failure.  
II.2) for a design basis loss of coolant accident coincident with a loss of offsite power and failure of Division II standby diesel generator EGS
-EG1B."  The conclusion of the inventory loss case was that a margin of approximately 393,100 gallons would exist in the ultimate heat sink basin after 30 days at technical specification limiting initial conditions. However, the inspector was unable to identify where the calculation accounted for the standby service water system water losses associated with the 20
-minute operator action to close the normal service water return isolation valves. Therefore, the inspector requested the analysis of record that demonstrated the loss of standby service water (i.e., ultimate heat sink inventory) to the normal service water system from the affected standby service water train would not be in excess of design limits prior to manual isolation.
 
The licensee provided calculation PM
-193, "Standby Service Water  
- Maximum Flow through Break in Tunnel Piping
," Revision 1, as the original basis for the 20
-minute operator action. The purpose of PM
-193 was to determine the inventory margin and operator action time impact of the assumed break given the scenario in the preceding paragraph, but for a failure of the Division I standby emergency diesel generator instead of the Division II. The postulated break occurred downstream of service water return isolation valve SWP
-MOV96A in the nonsafety
-related normal service water return header. The conclusion of PM
-193 is that 229,500 gallons are potentially lost from the standby service water system to the normal service water system within 30 minutes prior to standby service water system isolation. Based upon the se results, the inspector estimated that potentially 153,000 gallons of ultimate heat sink inventory could be lost prior to the 20
-minute operator action in AOP
-0016 to isolate the nonsafety
-related from the safety
-related service water systems. Therefore, the inspector concluded that the inventory losses associated with the delayed closure of the normal service water isolation valves were not, but should have been
, included in the ultimate heat sink inventory analysis and that the reduction of margin in the inventory analysis was significant. Furthermore, the failure of the Division I standby diesel generator to start or run would result in greater inventory losses through the normal service water return isolation valve than for the same failure on the Division II standby diesel generator due to differences in the design between standby service water system trains; however, PM-194 assumed only a Division II failure
.  


=====Analysis.=====
=====Analysis.=====
The failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30-day inventory requirement needed to be re-performed to assure that accident analysis requirements were met. In accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding had a cross-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin [H.6].  
The failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30
-day inventory requirement needed to be re
-performed to assure that accident analysis requirements were met.


=====Enforcement.=====
In accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At
Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, prior to September 28, 2017, the licensee failed to assure that the design basis for those structures, systems, and components to which this appendix applies was correctly translated into specifications, drawings, procedures, and instructions. Specifically, the current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated. Because this finding was of very low safety significance (Green) and has been entered into the licensee's corrective action program as Condition Report CR-RBS-2017-06998, it is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:  NCV 05000458/2017003-01, "Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory
-Power," dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non
-technical specification equipment; and did not screen as potentially risk
-significant due to seismic, flooding, or severe weather.
 
This finding had a cross
-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30
-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin
[H.6]. Enforcement
. Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, prior to September 28, 2017, the licensee failed to assure that the design basis for those structures, systems, and components to which this appendix applies was correctly translate d into specifications, drawings, procedures, and instructions. Specifically, the current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated
. Because this finding was of very low safety significance (Green) and has been entered into the licensee's corrective action program as Condition Report CR-RBS-2017-06998, it is being treated as a non
-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:  NCV 05000458/2017003
-01, "Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory


=====Analysis.=====
=====Analysis.=====
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====a. Inspection Scope====
====a. Inspection Scope====
On August 9, 2017, the inspectors observed a portion of an annual requalification test for licensed operators. The inspectors assessed the performance of the operators and the evaluators' critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities. These activities constitute completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.
On August 9, 2017, the inspectors observed a portion of an annual requalification test for licensed operators. The inspectors assessed the performance of the operators and the evaluators' critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities
. These activities constitute completion o f one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed the performance of on-shift licensed operators in the plant's main control room. At the time of the observations, the plant was conducting a reactor startup following a reactor scram. The inspectors observed the operators' performance of the following activities:   August 20, 2017, plant startup, including rod withdrawal to criticality In addition, the inspectors assessed the operators' adherence to plant procedures, including the conduct of operations procedure, and other operations department policies. These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.
The inspectors observed the performance of on
-shift licensed operators in the plant's main control room. At the time of the observations, the plant was conducting a reactor startup following a reactor scram. The inspectors observed the operators' performance of the following activities:
August 20, 2017, plant startup, including rod withdrawal to criticality In addition, the inspectors assessed the operators' adherence to plant procedures, including the conduct of operations procedur e, and other operations department policies.
 
These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectivene==
{{IP sample|IP=IP 71111.12}}
 
ss (71111.12)
 
===.1 Routine Maintenance Effectiveness===
===.1 Routine Maintenance Effectiveness===


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The inspectors reviewed one instance of a degraded performance or condition of safety-significant structures, systems, and components (SSCs):  September 12, 2017, 125 VDC distribution system, functional failure review The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.
The inspectors reviewed one instance of a degraded performance or condition of safety-significant structures, systems, and components (SSCs):  September 12, 2017, 125 VDC distribution system, functional failure review The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.


These activities constitute completion of one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.
These activities constitute completion o f one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
On August 7, 2017, the inspectors reviewed the licensee's quality control activities through a review of their control of safety-related lubricants. The inspectors also reviewed whether quality control verifications were property specified in accordance with the licensee's Quality Assurance Program, and were implemented as specified, during work associated with the addition of oil to safety-related control building chiller HVK-CHL1A.
On August 7, 2017, the inspectors reviewed the licensee's quality control activities through a review of their control of safety
-related lubricants. The inspectors also reviewed whether quality control verifications were property specified in accordance with the licensee's Quality Assurance Program, and were implemented as specified, during work associated with the addition of oil to safety
-related control building chiller HVK-CHL1A.


These activities constitute completion of one quality control sample, as defined in Inspection Procedure 71111.12.
These activities constitute completion of one quality control sample, as defined in Inspection Procedure 71111.12.
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed three risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
The inspectors review ed three risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
July 7, 2017, yellow risk condition during Division I residual heat removal surveillance testing July 12, 2017, green risk condition during preventative maintenance on standby service water cooling tower fan breakers August 14, 2017, yellow risk condition during Division II residual heat removal surveillance testing The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessments and verified that the licensee implemented appropriate risk management actions based on the results of the assessments.
July 7, 2017, yellow risk condition during Division I residual heat removal surveillance testing July 12, 2017, green risk condition during preventative maintenance on standby service water cooling tower fan breakers August 14, 2017, yellow risk condition during Division II residual heat removal surveillance testing The inspectors verified that these risk assessmen ts were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessment s and verified that the licensee implemented appropriate risk management actions based on the result s of the assessment s.


The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.
The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.


These activities constitute completion of three maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.
These activities constitute completion of three maintenance risk assessments and emergent work control inspection sample s, as defined in Inspection Procedure 71111.13.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed four operability determinations that the licensee performed for degraded or nonconforming SSCs:  July 10, 2017, operability determination of missed surveillance test associated with the Division I ENB battery (CR-RBS-2017-04462)  July 10, 2017, operability determination of foreign material intrusion in the standby service water cooling tower basin (CR-RBS-2017-05273)  August 1, 2017, operability determination of Division II standby gas treatment system relay EHS-MCC2D-2B-74 failed to actuate (CR-RBS-2017-05678)  August 30, 2017, operability determination of scram discharge volume level transmitters after found high out of calibration during system functional test (CR-RBS-2017-06031)  The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.
The inspectors review ed four operability determination s that the licensee performed for degraded or nonconforming SSCs:  July 10, 2017, operability determination of missed surveillance test associated with the Division I ENB battery (C R-RBS-2017-04462)  July 10, 2017, operability determination of foreign material intrusion in the standby service water cooling tower basin (CR-RBS-2017-05273)  August 1, 2017, operability determination of Division II standby gas treatment system relay EHS
-MCC2D-2B-74 failed to actuate (CR
-RBS-2017-05678)  August 30, 2017, operability determination of scram discharge volume level transmitters after found high out of calibration during system functional test (CR-RBS-2017-06031)  The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.


These activities constitute completion of four operability and functionality review samples, as defined in Inspection Procedure 71111.15.
These activities constitute completion of four operability and functionality review samples, as defined in Inspection Procedure 71111.15.
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====a. Inspection Scope====
====a. Inspection Scope====
On August 3, 2017, the inspectors reviewed a permanent plant modification of the Division II uninterruptible power supply (ENB-INV01B1) system output frequency meter. The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the SSC as modified. These activities constitute completion of one permanent plant modification inspection sample, as defined in Inspection Procedure 71111.18.
On August 3, 2017, the inspectors reviewed a permanent plant modification of the Division II uninterruptible power supply (ENB
-INV01B1) system output frequency meter.
 
The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post
-modification testing was adequate to establish the operability of the SSC as modified.
 
These activities constitute completion of one permanent plant modification inspection sample, as defined in Inspection Procedure 71111.18.


====b. Findings====
====b. Findings====
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==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}
{{IP sample|IP=IP 71111.19}}
a. Inspection Sco pe The inspectors reviewed five post-maintenance testing activities that affected risk-significant SSCs:
July 14, 2017, work order (WO)00437814, "Division I Battery ENB
-BAT01A Post Maintenance Test," following replacement of Division I battery ENB
-BAT01A  July 27, 2017, WO 00404398-02, "Instrument Air Compressor 2C Post Maintenance Test," following maintenance on instrument air compressor 2C August 28, 2017, WO 52713780, "E22-PC003 - Change Oil and Lubricate the Pump Coupling," retest of E 22-PC003 high pressure core spray line fill pump following oil replacement and lubrication September 2, 2017, WO 00478604, "LSV
-C3A - Perform Operability Test," following cleaning and inspection of compressor strainers, check valves, and orifices September 15, 2017, WO 52652445, "GTS
-FS24B - Calibrate Standby Gas Treatment Exhaust Fan B," operability run of standby gas treatment fan B following calibration of low
-flow switch The inspectors reviewed licensing
- and design
-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post
-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.


====a. Inspection Scope====
These activities constitute completion o f five post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.
The inspectors reviewed five post-maintenance testing activities that affected risk-significant SSCs:  July 14, 2017, work order (WO) 00437814, "Division I Battery ENB-BAT01A Post Maintenance Test," following replacement of Division I battery ENB-BAT01A  July 27, 2017, WO 00404398-02, "Instrument Air Compressor 2C Post Maintenance Test," following maintenance on instrument air compressor 2C  August 28, 2017, WO 52713780, "E22-PC003 - Change Oil and Lubricate the Pump Coupling," retest of E22-PC003 high pressure core spray line fill pump following oil replacement and lubrication  September 2, 2017, WO 00478604, "LSV-C3A - Perform Operability Test," following cleaning and inspection of compressor strainers, check valves, and orifices September 15, 2017, WO 52652445, "GTS-FS24B - Calibrate Standby Gas Treatment Exhaust Fan B," operability run of standby gas treatment fan B following calibration of low-flow switch The inspectors reviewed licensing- and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs. These activities constitute completion of five post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed three risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:
The inspectors observe d three risk-significant surveillance test s and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:
In-service tests:   July 7, 2017, STP-205-6301, "LPCS Pump and Valve Operability Test," performed on July 6, 2017  Other surveillance tests:   August 10, 2017, STP-201-6310, "Standby Liquid Control Pump and Valve Operability Test," performed on July 26, 2017 August 18, 2017, STP-203-1302, "E22-S001BAT Quarterly Surveillance," performed on August 16, 2017 The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the tests satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing. These activities constitute completion of three surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.
 
In-service tests:
July 7, 2017, STP-205-6301, "LPCS Pump and Valve Operability Test," performed on July 6, 2017  Other surveillance tests:
August 10, 2017, STP 6310, "Standby Liquid Control Pump and Valve Operability Test," performed on July 26, 2017 August 18, 2017, STP 1302, "E22-S001BAT Quarterly Surveillance," performed on August 16, 2017
 
The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the tests satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.
 
These activities constitute completion of three surveillance testing inspection sample s, as defined in Inspection Procedure 71111.22.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed an emergency preparedness drill on September 12, 2017, to verify the adequacy and capability of the licensee's assessment of drill performance. The inspectors reviewed the drill scenario, observed the drill from the technical support center and the emergency operations facility, and attended the post-drill critique. The inspectors verified that the licensee's emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.
The inspectors observed an emergency preparedness drill on September 12, 2017, to verify the adequacy and capability of the licensee's assessment of drill performance. The inspectors reviewed the drill scenario, observed the drill from the technical support center and the emergency operations facili ty, and attended the post
-drill critique. The inspectors verified that the licensee's emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post
-drill critique and entered into the corrective action program for resolution.


These activities constitute completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.
These activities constitute completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.
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====a. Inspection Scope====
====a. Inspection Scope====
On July 25, 2017, the inspectors observed simulator-based licensed operator requalification training that included implementation of the licensee's emergency plan. The inspectors verified that the licensee's emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the evaluators and entered into the corrective action program for resolution. These activities constitute completion of one training observation sample, as defined in Inspection Procedure 71114.06.
On July 25, 2017, the inspectors observed simulator
-based licensed operator requalification training that included implementation of the licensee's emergency plan. The inspectors verified that the licensee's emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the evaluators and entered into the corrective action program for resolution.
 
These activities constitute completion of one training observation sample, as defined in Inspection Procedure 71114.06.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the accuracy and operability of the radiation monitoring equipment used by the licensee to monitor areas, materials, and workers to ensure a radiologically safe work environment. This evaluation included equipment used to monitor radiological conditions related to normal plant operations, anticipated operational occurrences, and conditions resulting from postulated accidents. The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance associated with radiation monitoring instrumentation, as described below:  The inspectors performed walkdowns and observations of selected plant radiation monitoring equipment and instrumentation, including portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors. The inspectors assessed material condition and operability, evaluated positioning of instruments relative to the radiation sources or areas they were intended to monitor, and verified performance of source checks and calibrations. The inspectors evaluated the calibration and testing program, including laboratory instrumentation, whole body counters, post-accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors, portable survey instruments, area radiation monitors, electronic dosimetry, air samplers, and continuous air monitors. The inspectors assessed problem identification and resolution for radiation monitoring instrumentation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution. These activities constitute completion of the three required radiation monitoring instrumentation samples, as defined in Inspection Procedure 71124.05.
The inspectors evaluated the accuracy and operability of the radiation monitoring equipment used by the licensee to monitor areas, materials, and workers to ensure a radiologically safe work environment. This evaluation included equipment used to monitor radiological conditions related to normal plant operations, anticipated operational occurrences, and conditions resulting from postulated accidents.
 
The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance associated with radiation monitoring instrumentation, as described below:  The inspectors performed walkdowns and observations of selected plant radiation monitoring equipment and instrumentation, including portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors. The inspectors assessed material condition and operability, evaluated positioning of instruments relative to the radiation sources or areas they were intended to monitor, and verified performance of source checks and calibrations
. The inspectors evaluated the calibration and testing program, including laboratory instrumentation, whole body counters, post
-accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors, portable survey instruments, area radiation monitors, electronic dosimetry, air samplers, and continuous air monitors.
 
The inspectors assessed problem identification and resolution for radiation monitoring instrumentation.
 
The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
 
These activities constitute completion of the three required radiation monitoring instrumentation samples, as defined in Inspection Procedure 71124.05.


====b. Findings====
====b. Findings====
Line 286: Line 461:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated whether the licensee maintained gaseous and liquid effluent processing systems and properly mitigated, monitored, and evaluated radiological discharges with respect to public exposure. The inspectors verified that abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, were controlled in accordance with the applicable regulatory requirements and licensee procedures. The inspectors verified that the licensee's quality control program ensured radioactive effluent sampling and analysis adequately quantified and evaluated discharges of radioactive materials. The inspectors verified the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:   During walkdowns and observations of selected portions of the radioactive gaseous and liquid effluent equipment, the inspectors evaluated routine processing and discharge of effluents, including sample collection and analysis. The inspectors observed equipment configuration and flow paths of selected gaseous and liquid discharge system components, effluent monitoring systems, filtered ventilation system material condition, and significant changes to effluent release points. Calibration and testing program for process and effluent monitors, including National Institute of Standards and Technology traceability of sources, primary and secondary calibration data, channel calibrations, setpoint determination bases, and surveillance test results. Sampling and analysis controls used to ensure representative sampling and appropriate compensatory sampling. Reviews included results of the inter-laboratory comparison program. Instrumentation and equipment, including effluent flow measuring instruments, air cleaning systems, and post-accident effluent monitoring instruments. Dose calculations for effluent releases. The inspectors reviewed a selection of radioactive liquid and gaseous waste discharge permits and abnormal gaseous or liquid tank discharges, and verified the projected doses were accurate. The inspectors also reviewed 10 CFR Part 61 analyses and methods used to determine which isotopes were included in the source term. The inspectors reviewed land use census results, offsite dose calculation manual changes, and significant changes in reported dose values from previous years. Problem identification and resolution for radioactive gaseous and liquid effluent treatment. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution. These activities constitute completion of the six required radioactive gaseous and liquid effluent treatment samples, as defined in Inspection Procedure 71124.06.
The inspectors evaluated whether the licensee maintained gaseous and liquid effluent processing systems and properly mitigated, monitored, and evaluated radiological discharges with respect to public exposure. The inspectors verified that abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, were controlled in accordance with the applicable regulatory requirements and licensee procedures. The inspectors verified that the licensee's quality control program ensured radioactive effluent sampling and analysis adequately quantified and evaluated discharges of radioactive materials. The inspectors verified the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:
During walkdowns and observations of selected portions of the radioactive gaseous and liquid effluent equipment, the inspectors evaluated routine processing and discharge of effluents, including sample collection and analysis
. The inspectors observed equipment configuration and flow paths of selected gaseous and liquid discharge system components
, effluent monitoring systems, filtered ventilation system material condition, and significant changes to effluent release points.
 
Calibration and testing program for process and effluent monitors, including National Institute of Standards and Technology traceability of sources
, primary and secondary calibration data, channel calibrations, setpoint determination bases, and surveillance test results
. Sampling and analysis controls used to ensure representative sampling and appropriate compensatory sampling. Reviews included results of the inter-laboratory comparison program
. Instrumentation and equipment, including effluent flow measuring instruments, air cleaning systems, and post
-accident effluent monitoring instruments.
 
Dose calculations for effluent releases. The inspectors reviewed a selection of radioactive liquid and gaseous waste discharge permits and abnormal gaseous or liquid tank discharges, and verified the projected doses were accurate. The inspectors also reviewed 10 CFR Part 61 analyses and methods used to determine which isotopes were included in the source term. The inspectors reviewed land use census results, offsite dose calculation manual changes, and significant changes in reported dose values from previous years.
 
Problem identification and resolution for radioactive gaseous and liquid effluent treatment. The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
 
These activities constitute completion of the six required radioactive gaseous and liquid effluent treatment samples, as defined in Inspection Procedure 71124.06.


====b. Findings====
====b. Findings====
Line 295: Line 486:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated whether the licensee's radiological environmental monitoring program quantified the impact of radioactive effluent releases to the environment and sufficiently validated the integrity of the radioactive gaseous and liquid effluent release program. The inspectors also verified that the licensee continued to implement the voluntary Nuclear Energy Institute/Industry Ground Water Protection Initiative. The inspectors reviewed or observed the following items:   The inspectors observed selected air sampling and dosimeter monitoring stations, sampler station modifications, and the collection and preparation of environmental samples. The inspectors reviewed calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation, and inter-laboratory comparison program results. The inspectors reviewed selected events documented in the annual environmental monitoring report and significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census. The inspectors evaluated the operability, calibration, and maintenance of meteorological instruments and assessed the meteorological dispersion and deposition factors. The inspectors verified the licensee had implemented a sampling and monitoring program sufficient to detect leakage from structures, systems, or components with credible mechanism for licensed material to reach groundwater and reviewed changes to the licensee's written program for identifying and controlling contaminated spills/leaks to groundwater. Groundwater protection initiative implementation, including assessment of groundwater monitoring results, identified leakage or spill events and entries made into 10 CFR 50.75 (g) records, licensee evaluations of the extent of the contamination and the radiological source term, and reports of events associated with spills, leaks, and groundwater monitoring results. Problem identification and resolution for the radiological environmental monitoring program. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution. These activities constitute completion of the three required radiological environmental monitoring program samples, as defined in Inspection Procedure 71124.07.
The inspectors evaluated whether the licensee's radiological environmental monitoring program quantified the impact of radioactive effluent releases to the environment and sufficiently validate d the integrity of the radioactive gaseous and liquid effluent release program. The inspectors also verified that the licensee continued to implement the voluntary Nuclear Energy Institute/Industry Ground Water Protection Initiative. The inspectors reviewed or observed the following items:
The inspectors observed selected air sampling and dosimeter monitoring stations, sampler station modifications, and the collection and preparation of environmental samples
. The inspectors reviewed calibration and maintenance records for selected air samplers
, composite water samplers, and environmental sample radiation measurement instrumentation, and inter-laboratory compariso n program results
. The inspectors reviewed selected events documented in the annual environmental monitoring report and significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census. The inspectors evaluated the operability, calibration, and maintenance of meteorological instruments and assessed the meteorological dispersion and deposition factors
. The inspectors verified the licensee had implemented a sampling and monitoring program sufficient to detect leakage from structures, systems, or components with credible mechanism for licensed material to reach groundwater and reviewed changes to the licensee's written program for identifying and controlling contaminated spills/leaks to groundwater
. Groundwater protection initiative implementation, including assessment of groundwater monitoring results
, identified leakage or spill events and entries made into 10 CFR 50.75 (g) records
, licensee evaluations of the extent of the contamination and the radiological source term
, and reports of events associated with spills, leaks, and groundwater monitoring results.
 
Problem identification and resolution for the radiological environmental monitoring program. The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
 
These activities constitute completion of the three required radiological environmental monitoring program samples, as defined in Inspection Procedure 71124.07.


====b. Findings====
====b. Findings====
Line 304: Line 509:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the effectiveness of the licensee's programs for processing, handling, storage, and transportation of radioactive material. The inspectors interviewed licensee personnel and reviewed the following items:   Radioactive material storage, including waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition. Radioactive waste system, including walkdowns of the accessible portions of the radioactive waste processing systems and handling equipment. The inspectors also reviewed or observed changes made to the radioactive waste processing systems, methods for dewatering and waste stabilization, waste stream mixing methodology, and waste processing equipment that was not operational or abandoned in place. Waste characterization and classification, including radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult-to-measure radionuclides, and processes for waste classification including use of scaling factors and 10 CFR Part 61 analyses. Shipment preparation, including packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifests. Shipping records for low specific activity (LSA) I, II, III; surface contaminated objects (SCO) I, II; Type A, or Type B radioactive material or radioactive waste shipments. Problem identification and resolution for radioactive solid waste processing and radioactive material handling, storage, and transportation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution. These activities constitute completion of the six required radioactive solid waste processing and radioactive material handling, storage, and transportation samples, as defined in Inspection Procedure 71124.08.
The inspectors evaluated the effectiveness of the licensee's programs for processing, handling, storage, and transportation of radioactive material. The inspectors interviewed licensee personnel and reviewed the following items:
Radioactive material storage, including waste storage areas including containe r labeling/marking and monitoring containers for deformation or signs of waste decomposition.
 
Radioactive waste system, including walkdowns of the accessible portions of the radioactive waste processing systems and handling equipment. The inspectors also reviewed or observed changes made to the radioactive waste processing systems, methods for dewatering and waste stabilization, waste stream mixing methodology, and waste processing equipment that was not operational or abandoned in place
. Waste characterization and classification, including radio
-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult
-to-measure radionuclides, and processes for waste classification including use of scaling factors and 10 CFR Part 61 analyses.
 
Shipment preparation, including packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifests.
 
Shipping records for low specific activity (
LSA) I, II, III; surface contaminated objects (SCO) I, II; Type A, or Type B radioactive material or radioactive waste shipments.
 
Problem identification and resolution for radioactive solid waste processing and radioactive material handling, storage, and transportation. The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
 
These activities constitute completion of the six required radioactive solid waste processing and radioactive material handling, storage, and transportation samples, as defined in Inspection Procedure 71124.08.


====b. Findings====
====b. Findings====
Line 317: Line 538:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data. These activities constitute verification of the mitigating system performance index for heat removal systems, as defined in Inspection Procedure 71151.
The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.
 
These activities constitute verification of the mitigating system performance index for heat removal systems, as defined in Inspection Procedure 71151.


====b. Findings====
====b. Findings====
Line 325: Line 548:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data. These activities constitute verification of the mitigating system performance index for residual heat removal systems, as defined in Inspection Procedure 71151.
The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99
-02, "Regulatory Assessment Performance Indicato r Guideline," Revision 7, to determine the accuracy of the reported data.
 
These activities constitute verification of the mitigating system performance index for residual heat removal systems, as defined in Inspection Procedure 71151.


====b. Findings====
====b. Findings====
Line 333: Line 559:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.
The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99
-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.


These activities constitute verification of the mitigating system performance index for cooling water support systems, as defined in Inspection Procedure 71151.
These activities constitute verification of the mitigating system performance index for cooling water support systems, as defined in Inspection Procedure 71151.
Line 350: Line 577:
No findings were identified.
No findings were identified.


===.2 Annual Follow-up of Selected Issues===
===.2 Annual Follow===
 
-up of Selected Issues


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected one issue for an in-depth follow-up:  On May 21, 2017, following completion of a Division III emergency diesel generator (EDG) 24-hour run performed by operations department personnel, mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. The technician who performed the evolution discovered the error the following the day while updating the lubrication accountability log. Mobilgard 412 oil was added by the technicians instead of the required Mobilgard 450 oil. The addition of the 20 gallons of Mobilgard 412 to the Division III EDG resulted in a zinc concentration of 17.3 ppm in the overall oil volume. The Division III EDG vendor manual states that the allowable concentration for zinc in the lube oil is 0-10 ppm. Since the addition of the Mobilgard 412 oil resulted in a zinc concentration in excess of the vendor recommendation, the station determined that the Division III EDG could not be relied upon to perform its safety function in all conditions and declared it inoperable. The Division III EDG was inoperable for approximately three days while the station pumped out the lube oil and refilled the fuel oil storage tank. The station's adverse conditional analysis determined that technicians added the wrong type of oil because they did not stop and validate the correct oil per procedure GMP-0015, "Lubrication Procedure," Revision 14, as required, but assumed the oil staged in the mechanical shop was the correct oil. GMP-0015, Step 8.1.1, required the technicians to review the lubrication accountability log and verify the correct oil prior to adding it to the EDG.
The inspectors selecte d one issue for an in
-depth follow
-up:  On May 21, 2017, following completion of a Division III emergency diesel generator (EDG) 24
-hour run performed by operations department personnel, mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. The technician who performed the evolution discovered the error the following the day while updating the lubrication accountability log. Mobilgard 412 oil was added by the technicians instead of the required Mobilgard 450 oil. The addition of the 20 gallons of Mobilgard 412 to the Division III EDG resulted in a zinc concentration of 17.3 ppm in the overall oil volume. The Division III EDG vendor manual states that the allowable concentration for zinc in the lube oil is 0
-10 ppm. Since the addition of the Mobilgard 412 oil resulted in a zinc concentration in excess of the vendor recommendation, the  
 
station determined that the Division III EDG could not be relied upon to perform its safety function in all conditions and declared it inoperable. The Division III EDG was inoperable for approximately three days while the station pumped out the lube oil and refilled the fuel oil storage tank. The station's adverse conditional analysis determined that technicians added the wrong type of oil because they did not stop and validate the correct oil per procedure GMP-0015, "Lubrication Procedure," Revision 14, as required, but assumed the oil staged in the mechanical shop was the correct oil. GMP
-0015, Step 8.1.1, required the technicians to review the lubrication accountability log and verify the correct oil prior to adding it to the EDG.


The inspectors assessed the licensee's completed corrective actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition. These activities constitute completion of one annual follow-up sample, as defined in Inspection Procedure 71152.
The inspectors assessed the licensee's completed corrective actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition.
 
These activities constitute completion of one annual follow
-up sample, as defined in Inspection Procedure 71152.


====b. Findings====
====b. Findings====
A licensee-identified violation associated with this inspection sample is documented in Section
A licensee
-identified violation associated with this inspection sample is documented in Section
{{a|4OA7}}
{{a|4OA7}}
==4OA7 of this report.
==4OA7 of this report.==
 
{{a|4OA3}}
{{a|4OA3}}
==4OA3 Follow-up of Events and Notices of Enforcement Discretion==
==4OA3 Follow-up of Events and Notices of Enforcement Discreti==
==
 
{{IP sample|IP=IP 71153}}
on (71153(Closed) Licensee Event Report (LER) 05000458/2017 00, "Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting
(Closed) Licensee Event Report (LER) 05000458/2017-003-00, "Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting"
"


====a. Inspection Scope====
====a. Inspection Scope====
On March 10, 2017, during power ascension testing conducted in the startup after a refueling outage, the reactor operator manually inserted a reactor scram in response to an abnormal increase in steam pressure. Approximately 45 minutes before the scram occurred, a steam leak developed in a tee connection associated with the newly-installed turbine digital electro-hydraulic control (EHC) system. To stop the steam leak, the licensee isolated a piping line that fed two of the three pressure instruments that the digital EHC system used to control turbine valve positions. Given the presence of the leak, those two instruments were already reading pressure erratically, and the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two affected instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading roughly consistent with each other, the system treats their output as the true output. Consequently, with both of the affected instruments sensing pressure at roughly zero pounds, the digital EHC system began to shut the turbine control valves. The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling them based on the two pressure instruments that had been isolated and that were both reading roughly zero pounds. Power was below the 23.8 percent level, above which turbine bypass valves are required to be operable by technical specifications. The steam leak was the result of improper installation of the tee connection. The step that directed the installation of the connection into the transmitter tubing line was not properly carried out and was not sufficiently verified in accordance with its designation as a quality control hold point. When contract maintenance personnel in charge of the installation observed leakage from the connection during power ascension, they tightened down on its compression fitting without notifying the control room or obtaining appropriate permission. This action caused the fitting to dislodge, significantly worsening the leak. The inspectors reviewed the LER associated with the event and determined that the report adequately documented the summary of the event, including the cause of the event and potential safety consequences. The inspectors documented a finding for the licensee's failure to properly complete steps of the work order instruction during the installation and inspection of the tee connection. LER 05000458/2017-003-00 is closed.
On March 10, 2017, during power ascension testing conducted in the startup after a refueling outage, the reactor operator manually inserted a reactor scram in response to an abnormal increase in steam pressure. Approximately 45 minutes before the scram occurred, a steam leak developed in a tee connection associated with the newly-installed turbine digital electro
-hydraulic control (EHC) system. To stop the steam leak, the licensee isolated a piping line that fed two of the three pressure instruments that the digital EHC system used to control turbine valve positions. Given the presence of the leak, those two instruments were already reading pressure erratically, and the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two affected instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading roughly consistent with each other, the system treats their output as the true output. Consequently, with both of the affected instruments sensing pressure at roughly zero pounds, the digital EHC system began to shut the turbine control valves. The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling them based on the two pressure instruments that had been isolated and that were both reading roughly zero pounds. Power was below the 23.8 percent level
, above which turbine bypass valves are required to be operable by technical specifications.
 
The steam leak was the result of improper installation of the tee connection.
 
The step that directed the installation of the connection into the transmitter tubing line was not properly carried out and was not sufficiently verified in accordance with its designation as a quality control hold point. When contract maintenance personnel in charge of the installation observed leakage from the connection during power ascension, they tightened down on its compression fitting without notifying the control room or obtaining appropriate permission. This action caused the fitting to dislodge, significantly worsening the leak
. The inspectors reviewed the LER associated with the event and determined that the report adequately documented the summary of the event, including the cause of the event and potential safety consequences. The inspectors documented a finding for the licensee's failure to properly complete steps of the work order instruction during the installation and inspection of the tee connection.
 
LER 05000458/2017-003-00 is closed.


====b. Findings====
====b. Findings====


=====Introduction.=====
=====Introduction.=====
The inspectors reviewed a Green, self-revealed finding for the licensee's failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram.  
The inspectors reviewed a Green, self-revealed finding for the licensee's failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram.


=====Description.=====
=====Description.=====
On March 10, 2017, a steam leak developed in a tee compression fitting associated with the newly-installed turbine digital EHC system. To stop the steam leak, the licensee isolated a piping line that fed two of three pressure instruments that the digital EHC system used to control turbine valve positions. Prior to this action, the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading consistently with each other, the system treats their output as the true output. Consequently, with both of the affected instruments seeing pressure at roughly zero pounds, the digital EHC system began to close the turbine control valves. The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling their position based on the two pressure instruments that had been isolated and that were reading roughly zero pounds. Power was below the 23.8 percent level above which turbine bypass valves are required to be operable by technical specifications. The steam leak was a result of improper installation of a tee connection in the line that fed the two affected pressure transmitters. Work order 00438386, Task 24, Step 4.3.8 provided instruction for maintenance personnel to install the tee connection into the transmitter tubing line. This action was not properly carried out, with the tee connection incorrectly fitted up to its compression fitting. An adequate seal was not formed, and therefore, when the line was pressurized, a leak developed. The step was identified in the procedure as a quality control hold point, and therefore the deficient craftsmanship should have been identified by supervisor inspection. However, the Quality Control supervisor failed to observe the satisfactory completion of the step, contrary to site expectations. When maintenance personnel identified leakage from the compression fitting during power ascension, they tightened down on the fitting without obtaining appropriate permission from the control room. This action caused the fitting to dislodge, making the leak significantly worse.
On March 10, 2017, a steam leak developed in a tee compression fitting associated with the newly
-installed turbine digital EHC system. To stop the steam leak, the licensee isolated a piping line that fed two of three pressure instruments that the digital EHC system used to control turbine valve positions. Prior to this action, the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading consistently with each other, the system treats their output as the true output. Consequently, with both of the affected instruments seeing pressure at roughly zero pounds, the digital EHC system began to close the turbine control valves.
 
The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling their position based on the two pressure instruments that had been isolated and that were reading roughly zero pounds. Power was below the 23.8 percent level above which turbine bypass valves are required to be operable by technical specifications.
 
The steam leak was a result of improper installation of a tee connection in the line that fed the two affected pressure transmitters. Work order 00438386, Task 24, Step 4.3.8 provided instruction for maintenance personnel to install the tee connection into the transmitter tubing line. This action was not properly carried out, with the tee connection incorrectly fitted up to its compression fitting. An adequate seal was not formed, and therefore, when the line was pressurized, a leak developed. The step was identified in the procedure as a quality control hold point, and therefore the deficient craftsmanship should have been identified by supervisor inspection. However, the Quality Control supervisor failed to observe the satisfactory completion of the step, contrary to site expectations. When maintenance personnel identified leakage from the compression fitting during power ascension, they tightened down on the fitting without obtaining appropriate permission from the control room. This action caused the fitting to dislodge, making the leak significantly worse.


=====Analysis.=====
=====Analysis.=====
The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee's failure to properly install the tee connection caused a steam leak that led to a reactor scram. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, "Initiating Events Screening Questions."  The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5].  
The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee's failure to properly install the tee connection caused a steam leak that led to a reactor scram. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, "Initiating Events Screening Questions."  The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross
-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5].
Enforcement
. This finding does not involve an enforcement action because no regulatory requirement s were violated
. The licensee documented th is finding in their corrective action program as Condition Report CR-RBS-2017-02405. This issue is being characterized as finding FIN 05000458/2017003-02, "Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting
."  These activities constitute completion of one event follow-up sample, as defined in Inspection Procedure 71153.
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
 
===Exit Meeting Summary===
 
On July 28, 2017, the inspectors presented the radiation safety inspection results to Mr. M. Chase, Director of Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


=====Enforcement.=====
On August 25, 2017, the inspectors presented the radiation safety inspection results to Mr. J. Reynolds, Operations Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
This finding does not involve an enforcement action because no regulatory requirements were violated. The licensee documented this finding in their corrective action program as Condition Report CR-RBS-2017-02405. This issue is being characterized as finding FIN 05000458/2017003-02, "Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting."  These activities constitute completion of one event follow-up sample, as defined in Inspection Procedure 71153.
 
{{a|4OA6}}
On September 21, 2017, the inspector presented the triennial heat sink performance inspection results to Mr. M. Chase, Director, Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
==4OA6 Meetings, Including Exit Exit Meeting Summary On July 28, 2017, the inspectors presented the radiation safety inspection results to==


Mr. M. Chase, Director of Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed. On August 25, 2017, the inspectors presented the radiation safety inspection results to Mr. J. Reynolds, Operations Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed. On September 21, 2017, the inspector presented the triennial heat sink performance inspection results to Mr. M. Chase, Director, Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed. On October 11, 2017, the inspectors presented the integrated inspection results to Mr. W. Maguire, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On October 11, 2017, the inspectors presented the integrated inspection results to Mr. W. Maguire, Site Vice President
, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


{{a|4OA7}}
{{a|4OA7}}
==4OA7 Licensee-Identified Violations The following licensee-identified violation of NRC requirements was determined to be of very low safety significance (Green) and meets the NRC Enforcement Policy criteria for being dispositioned as a non-cited violation:==
==4OA7 Licensee-Identified Violations==
Technical Specification 5.4, "Procedures," requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.a of Appendix A to Regulatory Guide 1.33 requires that maintenance that can affect performance of safety-related equipment be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, the station did not properly preplan and perform maintenance that can affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Specifically, on May 21, 2017, following completion of a 24-hour surveillance test run of the Division III emergency diesel generator (EDG), mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. This error resulted in the inoperability of the Division III EDG for approximately three days while the incorrect oil was pumped out of the associated fuel oil storage tank and subsequently refilled. This finding was determined to be of very low safety significance (Green) because the finding did not represent an actual loss of function of one or more trains of safety-related equipment for greater than its technical specification allowed outage time. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2017-04128.


1  
The following licensee
-identified violation of NRC requirements was determined to be of very low safety significance (Green) and meets the NRC Enforcement Policy criteria for being dispositioned as a non-cited violation:
Technical Specification 5.4, "Procedures," requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.a of Appendix A to Regulatory Guide 1.33 require s that maintenance that can affect performance of safety
-related equipment be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, the station did not properly preplan and perform maintenance that can affect the performance of safety
-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Specifically, on May 21, 2017, following completion of a 24
-hour surveillance test run of the Division III emergency diesel generator (EDG), mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. This error resulted in the inoperability of the Division III EDG for approximately three days while the incorrect oil was pumped out of the associated fuel oil storage tank and subsequently refilled. This finding was determined to be of very low safety significance (Green) because the finding did not represent an actual loss of function of one or more trains of safety
-related equipment for greater than its technical specification allowed outage time. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2017-04128.


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 399: Line 670:


===Licensee Personnel===
===Licensee Personnel===
: [[contact::T. Askew]], Manager, Supply Chain  
: [[contact::T. Askew]], Manager, Supply Chain
: [[contact::D. Burnett]], Director, Emergency Planning, Entergy South  
: [[contact::D. Burnett]], Director, Emergency Planning, Entergy South
: [[contact::S. Carter]], Superintendent, Instruments and Controls  
: [[contact::S. Carter]], Superintendent, Instruments and Controls
: [[contact::M. Chase]], Director, Regulatory & Performance Improvement  
: [[contact::M. Chase]], Director, Regulatory & Performance Improvement
: [[contact::B. Cole]], Corporate Radiation Protection  
: [[contact::B. Cole]], Corporate Radiation
: [[contact::R. Conner]], Manager, Nuclear Oversight  
Protection
: [[contact::R. Cook]], Manager, Security  
: [[contact::R. Conner]], Manager, Nuclear Oversight
: [[contact::K. Crissman]], Senior Manager, Production  
: [[contact::R. Cook]], Manager, Security
: [[contact::D. Durocher]], Supervisor, Code Program  
: [[contact::K. Crissman]], Senior Manager, Production
: [[contact::J. Engel]], Superintendent, Radiological Operations, Radiation Protection  
: [[contact::D. Durocher]], Supervisor, Code Program
: [[contact::B. Ford]], Senior Manager, Fleet Regulatory Assurance  
: [[contact::J. Engel]], Superintendent, Radiological Operations, Radiation Protection
: [[contact::C. Foster]], System Engineer  
: [[contact::B. Ford]], Senior Manager, Fleet Regulatory Assurance
: [[contact::D. Guess]], Engineer  
: [[contact::C. Foster]], System Engineer
: [[contact::J. Henderson]], Manager, Systems & Components Engineering  
: [[contact::D. Guess]], Engineer
: [[contact::R. Hilliard]], Supervisor, Chemistry  
: [[contact::J. Henderson]], Manager, Systems & Components Engineering
: [[contact::K. Huffstatler]], Senior Licensing Specialist, Regulatory Assurance  
: [[contact::R. Hilliard]], Supervisor, Chemistry
: [[contact::V. Huffstatler]], Senior Health Physicist/Chemistry Specialist, Chemistry  
: [[contact::K. Huffstatler]], Senior Licensing Specialist, Regulatory Assurance
: [[contact::J. Hurst]], Manager, Emergency Preparedness  
: [[contact::V. Huffstatler]], Senior Health Physicist/Chemistry Specialist, Chemistry
: [[contact::D. Jarnagin]], Supervisor, Instruments and Controls  
: [[contact::J. Hurst]], Manager, Emergency Preparedness
: [[contact::B. Johns]], Licensing Specialist, Regulatory Assurance  
: [[contact::D. Jarnagin]], Supervisor, Instruments and Controls
: [[contact::C. King]], Superintendent, Maintenance Support  
: [[contact::B. Johns]], Licensing Specialist, Regulatory Assurance
: [[contact::G. King]], Specialist, Radiation Protection  
: [[contact::C. King]], Superintendent, Maintenance Support
: [[contact::R. Leasure]], Superintendent, Radiation Protection  
: [[contact::G. King]], Specialist, Radiation Protection
: [[contact::P. Lucky]], Manager, Performance Improvement  
: [[contact::R. Leasure]], Superintendent, Radiation Protection
: [[contact::W. Maguire]], Site Vice President  
: [[contact::P. Lucky]], Manager, Performance Improvement
: [[contact::J. McCoy]], Assistant Manager, Operations  
: [[contact::W. Maguire]], Site Vice President
: [[contact::G. Mermigas]], Engineer  
: [[contact::J. McCoy]], Assistant Manager, Operations
: [[contact::J. O'Connor]], Senior Manager, Maintenance  
: [[contact::G. Mermigas]], Engineer
: [[contact::S. Peterkin]], Manager, Radiation Protection  
: [[contact::J. O'Connor]], Senior Manager, Maintenance
: [[contact::M. Ponzo]], Manager, Chemistry  
: [[contact::S. Peterkin]], Manager, Radiation Protection
: [[contact::M. Reeves]], Supervisor, Radiation Operations  
: [[contact::M. Ponzo]], Manager, Chemistry
: [[contact::J. Rogers]], Supervisor, Engineering  
: [[contact::M. Reeves]], Supervisor, Radiation Operations
: [[contact::T. Venable]], Manager, Operations  
: [[contact::J. Rogers]], Supervisor, Engineering
: [[contact::M. Runion]], Senior Manager, Site Projects and Maintenance Services  
: [[contact::T. Venable]], Manager, Operations
: [[contact::D. Sandlin]], Manager, Design & Program Engineering  
: [[contact::M. Runion]], Senior Manager, Site Projects and Maintenance Services
: [[contact::T. Schenk]], Manager, Regulatory Assurance  
: [[contact::D. Sandlin]], Manager, Design & Program Engineering
: [[contact::W. Spell]], Senior Health Physicist/Chemistry Specialist, Chemistry  
: [[contact::T. Schenk]], Manager, Regulatory Assurance
: [[contact::K. Stupak]], Manager, Training  
: [[contact::W. Spell]], Senior Health Physicist/Chemistry Specialist, Chemistry
: [[contact::S. Vazquez]], Director, Engineering  
: [[contact::K. Stupak]], Manager, Training
: [[contact::S. Vercelli]], General Manager, Plant Operations  
: [[contact::S. Vazquez]], Director, Engineering
: [[contact::J. Vukovics]], Supervisor, Reactor Engineering  
: [[contact::S. Vercelli]], General Manager, Plant Operations
: [[contact::J. Wilson]], Manager, Chemistry
: [[contact::J. Vukovics]], Supervisor, Reactor Engineering
: [[contact::J. Wilson]], Manager, Chemistry


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==


===Opened and Closed===
===Opened and Closed===
: 05000458/2017003-01 NCV Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory Analysis (Section 1R07)  
: 05000458/2017003
: 05000458/2017003-02 FIN Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting (Section 4OA3)   
-01 NCV Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory Analysis
(Section 1R07)  
: 05000458/201700
3-02 FIN Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting
(Section 4OA3)   
===Closed===
===Closed===
: [[Closes LER::05000458/LER-2017-003]]-00 LER Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting (Section 4OA3)   
: 05000458/
: 2017-003-00 LER Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting (Section 4OA3)   
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 1R01: Adverse Weather Protection==
==Section 1R01: Adverse Weather Protection==
: Calculations/Specifications Number Title Revision/Date 8.3.1.32 Design Basis Flood - River Bend Station (West Creek and Grants Bayou) 1 8.3.1.34 PMP in Site Area (Assuming no Berm Around Excavation) 1 8.3.1.37 Determination of Water Surface Elevations in Grants Bayou and West Creek Near Plant Site for PMF and 25-Year Flood + SSE 1 CF8503290006 Peelle Design Calculation for Pressuretight and Watertight Doors March 15, 1985 CI8412200004 Calculations Design & Stress Analysis for Watertight & Pressuretight Doors December 17, 1984
: Calculations/Specifications Number Title Revision/Date 8.3.1.32 Design Basis Flood  
: RBS-210.460 Specification for Missile Protected Doors 2
- River Bend Station (West Creek and Grants Bayou)
: RBS-210.461 Specification for Pressuretight Doors, Watertight Doors, and Special Doors 2
: 8.3.1.34 PMP in Site Area (Assuming no Berm Around Excavation)
: RBS-210.462 Specification for Pressuretight and Watertight Doors 1
: 8.3.1.37 Determination of Water Surface Elevations in Grants Bayou and West Creek Near Plant Site for PMF and 25
-Year Flood + SSE
: CF8503290006
: Peelle Design Calculation for Pressuretight and Watertight Doors March 15, 1985
: CI8412200004  
===Calculations===
: Design & Stress Analysis for Watertight & Pressuretight Doors December 17, 1984
: RBS-210.460 Specification for Missile Protected Doors
: RBS-210.461 Specification for Pressuretight Doors, Watertight Doors, and Special Doors
: RBS-210.462 Specification for Pressuretight and Watertight Doors  
===Condition Reports===
===Condition Reports===
(CRs)
(CRs)
Line 490: Line 776:
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: SOP-0042 Standby Service Water System 043
: SOP-0042 Standby Service Water System
: SOP-0049 125 VDC System (SYS #305) 038
: 043
: SOP-0066 Control Building HVAC Chilled Water System 336  
: SOP-0049 125 VDC System (SYS #305)
: 038
: SOP-0066 Control Building HVAC Chilled Water System
: 336  
===Work Orders===
===Work Orders===
(WOs)
(WOs)
Line 499: Line 788:
: WO 00476553
: WO 00476553
: WO 00479796
: WO 00479796
: WO 00479797 WO 00479800
: WO 00479797
: WO 00479800


==Section 1R05: Fire Protection==
==Section 1R05: Fire Protection==
: Calculation Number Title Revision G13.18.12.2-022 River Bend Station Combustible Loading 005  
: Calculation Number Title Revision G13.18.12.2
-022 River Bend Station Combustible Loading
: 005  
===Condition Reports===
===Condition Reports===
(CRs)
(CRs)
Line 508: Line 800:
: CR-RBS-2017-03519
: CR-RBS-2017-03519
: CR-RBS-2017-04226  
: CR-RBS-2017-04226  
===Procedures===
===Procedure===
: Number Title Revision
s Number Title Revision
: CB-116-133 Battery 1A Room Fire Area C-18 4
: CB-116-133 Battery 1A Room Fire Area C
: CB-116-134 Battery 1B Room Fire Area C-19 4
-18 4
: CB-116-135 ENB Inverter Charger B Room Fire Area C-19 4
: CB-116-134 Battery 1B Room Fire Area C
-19 4
: CB-116-135 ENB Inverter Charger B Room Fire Area C
-19 4
: SP-118-451 Standby Cooling Tower Pump B Room Fire Area
: SP-118-451 Standby Cooling Tower Pump B Room Fire Area
: PH-2/Z-1 3
: PH-2/Z-1 3
Line 519: Line 814:


===Calculations===
===Calculations===
: Number Title Revision G13.18.12.3-15-0 Internal Flooding Screening Analysis 00 G13.18.12.3-16-0 Quantitative Analysis of Internal Flooding 00
: Number Title Revision G13.18.12.3
: PN-317 Max Flood Elevations for Moderate Energy Line Cracks in Cat I Structures 01
-15-0 Internal Flooding Screening Analysis
: G13.18.12.3
-16-0 Quantitative Analysis of Internal Flooding
: PN-317 Max Flood Elevations for Moderate Energy Line Cracks in Cat I Structures


==Section 1R07: Heat Sink Performance==
==Section 1R07: Heat Sink Performance==
 
: Calculation
===Calculations===
s Number Title Revision 228.800-PX-562 WATHAM ANAL With Trapped Air in SSW System
: Number Title Revision 228.800-PX-562 WATHAM ANAL With Trapped Air in SSW System-A-Header & LONSW/LORPCCW & LOOP Events 2 228.800-PX-567 Segment Force Factor for the Components Piping of the SSW System 2 G13.18.2.0*072 E12-EB001A/B/C/D Maximum Tube Throughwall Degradation Limit 0 G13.18.4.0*046 Standby Service Water Pump Capacity Verification without Flow through Drywell Unit Coolers, Including 5% Pumps Degradation 1 G13.18.14.0*166 Heat Rejected by Emergency Diesel Generator Divisions I and II to Cooling Water 0
-A-Header & LONSW/LORPCCW & LOOP Events
: PM-194 Standby Cooling Tower Performance and Evaporation Losses without Drywell Unit Coolers 10
: 228.800-PX-567 Segment Force Factor for the Components Piping of the SSW System
: PM-199 Standby Cooling Tower Basin Volume 7
: G13.18.2.
: 0*072 E12-EB001A/B/C/D Maximum Tube Throughwall Degradation Limit
: G13.18.4.0*046
: Standby Service Water Pump Capacity Verification without Flow through Drywell Unit Coolers, Including 5% Pumps Degradation
: G13.18.14.0*166
: Heat Rejected by Emergency Diesel Generator Divisions I and II to Cooling Water
: PM-194 Standby Cooling Tower Performance and Evaporation Losses without Drywell Unit Coolers
: PM-199 Standby Cooling Tower Basin Volume  
===Condition Reports===
===Condition Reports===
(CRs) Reviewed
(CRs)
: Reviewed
: CR-RBS-1999-00137
: CR-RBS-1999-00137
: CR-RBS-2003-01240
: CR-RBS-2003-01240
Line 556: Line 862:
===Miscellaneous===
===Miscellaneous===
: Number Title Revision/Date
: Number Title Revision/Date
: 204 - Residual Heat Removal - LPCI Q1-2017
: 204 - Residual Heat Removal  
: 309 and 405 - Standby Emergency Diesel Generators - Division I, II, & III and HVAC Q1-2017
- LPCI Q1-2017
: 309 and 405 - Standby Emergency Diesel Generators  
- Division I, II, & III and HVAC
: Q1-2017
: Standby Diesel Generator Division I & II
: Standby Diesel Generator Division I & II
: Diesel Generator Building Ventilation System Design Criteria System Numbers 309 & 405 3 221.432-000-019 RHR Heat Exchanger Calculated Performance January 10, 1990 244.700 Specification for Standby Diesel Generator Systems April 12, 1985 244.700-041-018 Jacket Water Cooler 74039-109 September 1, 1994
: Diesel Generator Building Ventilation System Design Criteria System Numbers 309 & 405
: ER-EB-1999-0592 Replacement Filters for Auxiliary and Containment Unit Coolers 0
: 221.432-000-019 RHR Heat Exchanger Calculated Performance January 10, 1990
: ER-RB-1996-0028 Revise Torqueing Procedure for RHR Heat Exchanger Head from 3224.110-000-031 Requirements 0 P-15854 Continue to Test RHR Heat Exchangers in Accordance with
: 244.700 Specification for Standby Diesel Generator Systems April 12, 1985
: GL 89-13 Supplement 1, Section IID and IIIF October 21, 1998 P-8340 GSU has Developed Inspection Criteria and Requirements which Provide for Scheduled Inspections and Specific Instructions for Maintenance of Service Water Heat Exchangers and Unit Coolers -
: 244.700-041-018 Jacket Water Cooler 74039
-109 September 1, 1994
: ER-EB-1999-0592 Replacement Filters for Auxiliary and Containment Unit Coolers
: ER-RB-1996-0028 Revise Torqueing Procedure for RHR Heat Exchanger Head from 3224.110
-000-031 Requirements
: P-15854 Continue to Test RHR Heat Exchangers in Accordance with
: GL 89-13 Supplement 1, Section IID and IIIF October 21, 1998
: P-8340 GSU has Developed Inspection Criteria and Requirements which Provide for Scheduled Inspections and Specific Instructions for Maintenance of Service Water Heat Exchangers and Unit Coolers  
-
: CMP-9267 Issued to Implement February 2, 1990  
: CMP-9267 Issued to Implement February 2, 1990  
===Procedures===
===Procedure===
: Number Title Revision
s Number Title Revision
: AOP-0016 Loss of Standby Service Water 22
: AOP-0016 Loss of Standby Service Water
: CMP-9267 Heat Exchanger Repairs 13
: CMP-9267 Heat Exchanger Repairs
: CSP-0006 Chemistry Surveillance and Scheduling System 42
: CSP-0006 Chemistry Surveillance and Scheduling System
: EN-DC-159 System and Component Monitoring 9
: EN-DC-159 System and Component Monitoring
: EN-DC-184 NRC Generic Letter 89-13 Service Water Program 4
: EN-DC-184 NRC Generic Letter 89
: EN-DC-316 Heat Exchanger Performance and Condition Monitoring 8,9
-13 Service Water Program
: OSP-0066 Extensive Damage Mitigation Procedure 28
: EN-DC-316 Heat Exchanger Performance and Condition Monitoring
: 8,9
: OSP-0066 Extensive Damage Mitigation Procedure
: SEP-SW-RBS-001 RBS GL89-13 Service Water Heat Exchanger Program 0  
: SEP-SW-RBS-001 RBS GL89-13 Service Water Heat Exchanger Program 0  
===Procedures===
===Procedure===
: Number Title Revision
s Number Title Revision
: STP-403-0301 Containment Unit Cooler
: STP-403-0301 Containment Unit Cooler HVR
: HVR-UC1A Flow Rate Verification 14
-UC1A Flow Rate Verification Thermal Performance Analyses Number Title Date
: Thermal Performance Analyses Number Title Date
: RHR Heat Exchangers E12
: RHR Heat Exchangers E12-EB001A and E12-EB001C Heat Transfer Capacity Verification, March 15, 2005 April 22, 2005
-EB001A and E12
: RHR Heat Exchangers E12-EB001A and E12-EB001C Heat Transfer Capacity Verification, September 30, 2003 December 19, 2003
-EB001C Heat Transfer Capacity Verification, March 15, 2005 April 22, 2005
: RBS-EP-15-00018 RHR Heat Exchangers E12-EB001A and E12-EB001C Heat Transfer Capacity Verification, January 5, 2013 November 23, 2015
: RHR Heat Exchangers E12
-EB001A and E12
-EB001C Heat Transfer Capacity Verification
, September 30,
: 2003 December 19, 2003
: RBS-EP-15-00018 RHR Heat Exchangers E12
-EB001A and E12
-EB001C Heat Transfer Capacity Verification, January 5, 2013
: November 23, 2015
: Vendor Documents Number Title Revision/Date 3244.700-041-082B Special and General Torque Tables,
: Vendor Documents Number Title Revision/Date 3244.700-041-082B Special and General Torque Tables,
: SIM-64 Revision 301
: SIM-64 Revision 301
: NU9-M62 Operating and Maintenance Manual January 14, 1986
: NU9-M62 Operating and Maintenance Manual January 14, 1986
: VTD-T193-0100 Thermxchanger Manual for Installation, Operation & Maintenance of Shell & Tube Heat Exchangers 0
: VTD-T193-0100 Thermxchanger Manual for Installation, Operation & Maintenance of Shell & Tube Heat Exchangers  
===Work Orders===
===Work Orders===
(WOs)
(WOs)
Line 591: Line 918:
: WO 00174873
: WO 00174873
: WO 00174875
: WO 00174875
: WO 00361644
: WO 00361644 WO 00470689
: WO 00470689
: WO 51087021
: WO 51087021
: WO 51695027
: WO 51695027
Line 599: Line 925:
: WO 52654748
: WO 52654748
: WO 52671655
: WO 52671655
: WO 52687800 WO 52703609
: WO 52687800
: WO 52703609


==Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance==
==Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance==
Line 638: Line 965:
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: ADM-0085 Periodic Maintenance Program 7
: ADM-0085 Periodic Maintenance Program
: EN-DC-203 Maintenance Rule Program 3
: EN-DC-203 Maintenance Rule Program
: EN-DC-204 Maintenance Rule Scope and Basis 4
: EN-DC-204 Maintenance Rule Scope and Basis
: EN-DC-205 Maintenance Rule Monitoring 6
: EN-DC-205 Maintenance Rule Monitoring
: EN-DC-206 Maintenance Rule (A)(1) Process 3
: EN-DC-206 Maintenance Rule (A)(1) Process
: EN-LI-118 Cause Evaluation Process 24
: EN-LI-118 Cause Evaluation Process
: EN-WM-105 Planning 18
: EN-WM-105 Planning 18
: Work Order (WO) WO 50032677
: Work Order (WO)
: WO 50032677


==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
Line 651: Line 979:
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: ADM-0096 Risk Management Program Implementation and On-line Maintenance Risk Assessment 325
: ADM-0096 Risk Management Program Implementation and On-line Maintenance Risk Assessment
: EN-WM-104 On Line Risk Assessment 15
: 25
: EN-WM-104 On Line Risk Assessment


==Section 1R15: Operability Determinations and Functionality Assessments==
==Section 1R15: Operability Determinations and Functionality Assessments==
Line 663: Line 992:
: CR-RBS-2017-06075   
: CR-RBS-2017-06075   
: Engineering Request Number Title Revision
: Engineering Request Number Title Revision
: ER-RB-2001-00336 Standby Cooling Tower Basin Cleaning Dive Effort 0
: ER-RB-2001-00336 Standby Cooling Tower Basin Cleaning Dive Effort  
===Miscellaneous===
===Miscellaneous===
: Number Title Revision
: Number Title Revision
: IEEE-308-2012 IEEE Standard Criteria for Class 1E Power Systems for Nuclear Power Generating Stations 0
: IEEE-308-2012 IEEE Standard Criteria for Class 1E Power Systems for Nuclear Power Generating Stations
: IEEE-450-1975 IEEE Recommended Practice for Maintenance, Testing, and Replacement of Large Lead Storage Batteries for Generating Stations and Substations 0
: IEEE-450-1975 IEEE Recommended Practice for Maintenance, Testing, and Replacement of Large Lead Storage Batteries for Generating Stations and Substations
: IEEE-485-1997 IEEE Recommended Practice for Sizing Lead-Acid Batteries for Stationary Applications 0
: IEEE-485-1997 IEEE Recommended Practice for Sizing Lead
-Acid Batteries for Stationary Applications
: QC-RBS-00036504 QC Inspection for
: QC-RBS-00036504 QC Inspection for
: PO 10479021 0
: PO 10479021  
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: ADM-0015 Station Surveillance Test Program 40
: ADM-0015 Station Surveillance Test Program
: EN-LI-108 Event Notification and Reporting 14
: EN-LI-108 Event Notification and Reporting
: EN-MA-125 Troubleshooting Control of Maintenance Activities 20
: EN-MA-125 Troubleshooting Control of Maintenance Activities 20
: EN-OP-104 Operability Determination Process 11
: EN-OP-104 Operability Determination Process
: STP-203-1702 E22-S001BAT Performance Discharge Test 21
: STP-203-1702 E22-S001BAT Performance Discharge Test
: STP-305-1606
: STP-305-1606
: ENB-BAT01A Service Discharge Test 18
: ENB-BAT01A Service Discharge Test
: STP-305-1700
: STP-305-1700
: ENB-BAT01A Performance Discharge Test 25
: ENB-BAT01A Performance Discharge Test
: STP-305-1701
: STP-305-1701
: ENB-BAT01B Performance Discharge Test 26
: ENB-BAT01B Performance Discharge Test  
===Work Orders===
===Work Orders===
(WOs)
(WOs)
Line 694: Line 1,024:
: WO 52628547
: WO 52628547
: WO 52639832
: WO 52639832
: WO 52647337 WO 52647338
: WO 52647337
: WO 52647338


==Section 1R18: Plant Modifications==
==Section 1R18: Plant Modifications==
Line 701: Line 1,032:
: CR-RBS-2015-03808  
: CR-RBS-2015-03808  
===Drawings===
===Drawings===
: Number Title Revision 0244.514-000-005 Schematic 20KVA Inverter 100-140VDC 120VAC 1 60HZ
: Number Title Revision 0244.514-000-005 Schematic 20KVA Inverter 100
: ENB-INV01A1/ENB-INV01B1 0 0244.514-000-006 Schematic 20KVA Inverter 100-140VDC 120VAC 10 60HZ
-140VDC 120VAC 1 60HZ ENB-INV01A1/ENB
: ENB-INV01A1/ENB-INV01B1 0 0244.514-000-031 Schematic Diagram 20KVA Inverter 100-140VDC 120 VAC 0 0244.514-000-032 Schematic Diagram 20KVA Inverter 100-140VDC 120 VAC 0  
-INV01B1 0 0244.514-000-006 Schematic  
: 20KVA Inverter  
: 100-140VDC 120VAC 10 60HZ
: ENB-INV01A1/ENB-INV01B1 0 0244.514-000-031 Schematic Diagram 20KVA Inverter 100-140VDC 120 VAC 0 0244.514-000-032 Schematic Diagram 20KVA Inverter 100
-140VDC 120 VAC 0  
===Miscellaneous===
===Miscellaneous===
: Number Title Revision 4244.514-000-004 Engineering Report Seismic Qualification Evaluation of Frequency Meter Modification 0 S250-0127 Ametek FMR2/1 Weschler Instrument Meter 0
: Number Title Revision 4244.514-000-004 Engineering Report Seismic Qualification Evaluation of Frequency Meter Modification
: S250-0127 Ametek FMR2/1 Weschler Instrument Meter
: EC 65512 Engineering Change:
: EC 65512 Engineering Change:
: FMR2 Model Replacement for
: FMR
: Model Replacement for
: ENB-INV01B1 0  
: ENB-INV01B1 0  
===Procedure===
===Procedure===
: Number Title Revision
: Number Title Revision
: SOP-0048 120 VAC System 328
: SOP-0048 120 VAC System
: Work Order (WO) WO 00414828
: 28
 
: Work Order (WO)
==Section 1R19: Post-Maintenance Testing==
: WO 00414828


==Section 1R19: ==
: Post
-Maintenance Testing
===Condition Report (CR)===
===Condition Report (CR)===
: CR-RBS-2017-03595  
: CR-RBS-2017-03595  
===Drawings===
===Drawings===
: Number Title Revision
: Number Title Revision
: EM-003H Arrangement Instrument Air and Service Compressor Building 1
: EM-003H Arrangement Instrument Air and Service Compressor Building
: FSK-12-01X Flow Diagram Instrument Air System 0
: FSK-12-01X Flow Diagram Instrument Air System
: PID-12-01G Engineering P&I Diagram System 122 Instrument Air 302  
: PID-12-01G Engineering P&I Diagram System 122 Instrument Air 302  
===Miscellaneous===
===Miscellaneous===
: Number Title Revision 3252.15-404-001A Instruction Book for Air Compressors 302
: Number Title Revision 3252.15-404-001A Instruction Book for Air Compressors
: 2
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: EN-WM-107 Post Maintenance Testing 005
: EN-WM-107 Post Maintenance Testing
: STP-000-0201 Monthly Operating Log 311
: 005
: STP-208-6301 Div I MSIV Leakage Control Quarterly Valve Operability Test 008
: STP-000-0201 Monthly Operating Log
: STP-208-6607 Div I MSIV Leakage Control Refuel Position Indication Verification Test 2B
: 311
: STP-257-0202 Standby Gas Treatment System Filter Train B Monthly Operability Test 015
: STP-208-6301 Div I MSIV Leakage Control Quarterly Valve Operability Test
: 008
: STP-208-6607 Div I MSIV Leakage Control Refuel Position Indication Verification Test
: 2B
: STP-257-0202 Standby Gas Treatment System Filter Train B Monthly Operability Test
: 015
: STP-305-1300
: STP-305-1300
: ENB-BAT01A Quarterly Surveillance 28
: ENB-BAT01A Quarterly Surveillance 28
: STP-305-1600
: STP-305-1600
: ENB-BAT01A Inspection 303
: ENB-BAT01A Inspection
: 303
: STP-305-1606
: STP-305-1606
: ENB-BAT01A Service Discharge Test 18
: ENB-BAT01A Service Discharge Test  
===Work Orders===
===Work Orders===
(WOs)
(WOs)
Line 747: Line 1,094:
: WO 52652445
: WO 52652445
: WO 52720726
: WO 52720726
: WO 52732341 WO 52776567
: WO 52732341
: WO 52776567


==Section 1R22: Surveillance Testing==
==Section 1R22: Surveillance Testing==
Line 759: Line 1,107:
===Drawings===
===Drawings===
: Number Title Revision
: Number Title Revision
: PID-04-03C Engineering P&I Diagram System 106 Condensate Makeup Storage and Transfer System 24
: PID-04-03C Engineering P&I Diagram System  
: PID-27-16A Engineering P&I Diagram System 201 Standby Liquid Control System 14
: 106 Condensate Makeup Storage and Transfer System
: PID-27-16A Engineering P&I Diagram System  
: 201 Standby Liquid Control System  
===Miscellaneous===
===Miscellaneous===
: Number Title Revision
: Number Title Revision EC-0000032582
: EC-0000032582 Establish Baseline Reference Valued and Acceptance Limits for IST Pumps C41-PC001A and C41-PC001B 2 Year Comprehensive Tests 0
: Establish Baseline Reference Valued and Acceptance Limits for IST Pumps C
: SEP-RBS-IST-1 RBS Inservice Testing Bases Document 6
: 41-PC001A and C41-PC001B 2 Year Comprehensive Tests
: SEP-RBS-IST-2 RBS Inservice Testing Plan 8
: SEP-RBS-IST-1 RBS Inservice Testing Bases Document
===Procedures===
: SEP-RBS-IST-2 RBS Inservice Testing Plan  
: Number Title Revision
===Procedure===
: ADM-0015 Station Surveillance Test Program 40
s Number Title Revision
: SOP-0028 Standby Liquid Control System 18
: ADM-0015 Station Surveillance Test Program
: STP-201-0201 SLC Valve Continuity and Valve Position Check 9
: SOP-0028 Standby Liquid Control System
: STP-205-6301 LPCS Pump and Valve Operability Test 24
: STP-201-0201 SLC Valve Continuity and Valve Position Check
: STP-201-6310 SLC Pump and Valve Operability Test 311
: STP-205-6301 LPCS Pump and Valve Operability Test
: STP-203-1302 E22-S001BAT Quarterly Surveillance 25
: STP-201-6310 SLC Pump and Valve Operability Test
: 311
: STP-203-1302 E22-S001BAT Quarterly Surveillance  
===Work Orders===
===Work Orders===
(WOs)
(WOs)
: WO 52752999
: WO 52752999
: WO 52756898
: WO 52756898
: WO 52756900 WO 52766017
: WO 52756900
: WO 52766017


==Section 1EP6: Drill Evaluation==
==Section 1EP6: Drill Evaluation==
Line 784: Line 1,137:
===Miscellaneous===
===Miscellaneous===
: Number Title Revision
: Number Title Revision
: RDRL-EP-0803EX Site Drill Scenario 3
: RDRL-EP-0803EX Site Drill Scenario
: RDRL-EP-FD04 Focused Drill Scenario 02
: RDRL-EP-FD04 Focused Drill Scenario


==Section 2RS5: Radiation Monitoring Instrumentation==
==Section 2RS5: Radiation Monitoring Instrumentation==
: Audits and Self-Assessments Number Title Date
: Audits and Self
: LO-RLO-2017-0016 Self-Assessment:
-Assessments Number Title Date
: Pre-NRC Radiation Monitoring Instrumentation (NRC
: LO-RLO-2017-0016 Self-Assessment:  
: IP 71124.05) May 24, 2017  
: Pre-NRC Radiation Monitoring Instrumentation (NRC IP 71124.05)
: May 24, 2017  
===Condition Reports===
===Condition Reports===
(CRs)
(CRs)
Line 808: Line 1,162:
===Miscellaneous===
===Miscellaneous===
: Number Title Date
: Number Title Date
: Evaluation of the Thermo
: Evaluation of the Thermo PM
: PM-7 for use as a Passive Monitor at River Bend Nuclear Plant December 13, 2011 2017 Dry Active Waste Scaling Factors
-7 for use as a Passive Monitor at River Bend Nuclear Plant December 13, 2011
: April 11, 2017 28-8C Gamma Calibration Verifications Data Sheet April 3, 2017 78-2M Gamma Calibration Verifications Data Sheet August 30, 2016
: 2017 Dry Active Waste Scaling Factors April 11, 2017
: Portable Radiation Instrument Calibration Records Number Title Date 2409 Certificate of Calibration for Eberline
: 28-8C Gamma Calibration Verifications Data Sheet April 3, 2017
: ASP-1  (Ludlum Measurements, Inc.) June 9, 2017 6011 Calibration Data Sheet for
: 78-2M Gamma Calibration Verifications Data Sheet August 30, 2016
: BC-4 Scaler (Beta) April 12, 2017 8909 Calibration Data Sheet for
: Portable Radiation Instrument Calibration Records Number Title Date 2409 Certificate of Calibration for Eberline ASP
: LM-177 Frisker January 24, 2017
-1  (Ludlum Measurements, Inc.)
: CHP-C-012 Calibration Data Sheet for iSolo Scaler March 23, 2017
: June 9, 2017
: CHP-DR-525 Calibration Data Sheet for Ludlum Model 9-3 May 17, 2017
: 6011 Calibration Data Sheet for BC
-4 Scaler (Beta)
: April 12, 2017
: 8909 Calibration Data Sheet for LM
-177 Frisker January 24, 2017
: CHP-C-012 Calibration Data Sheet for iSolo Scal er March 23, 2017
: CHP-DR-525 Calibration Data Sheet for Ludlum Model 9
-3 May 17, 2017
: CHP-TEL022 Calibration Data Sheet for WR Telepole December 16, 2016
: CHP-TEL022 Calibration Data Sheet for WR Telepole December 16, 2016
: PM7-395 Calibration Data Sheet for Eberline
: PM7-395 Calibration Data Sheet for Eberline PM
: PM-7 January 6, 2017  
-7 January 6, 2017  
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: EN-RP-106-1 Radiological Survey Guidelines 4
: EN-RP-106-1 Radiological Survey Guidelines
: EN-RP-108 Radiation Protection Posting 19
: EN-RP-108 Radiation Protection Posting
: EN-RP-301 Radiation Protection Instrument Control 8
: EN-RP-301 Radiation Protection Instrument Control
: EN-RP-317-03 Operation and Calibration of Sources and Laboratory Standard Instruments 0
: EN-RP-317-03 Operation and Calibration of Sources and Laboratory Standard Instruments
: MCP-4201 DRMS Low Range Area Monitor Calibration 8, 9
: MCP-4201 DRMS Low Range Area Monitor Calibration
: MCP-4203 DRMS High Range Area Monitor Calibration 301
: 8, 9
: RPP-0010 Operation and Verification of the Shepherd Model 89 Gamma Calibrator 301  
: MCP-4203 DRMS High Range Area Monitor Calibration
: 301
: RPP-0010 Operation and Verification of the Shepherd Model 89 Gamma Calibrator
: 301  
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: RPP-0036 Calibration of DRMS Area Monitors and Determination of Alert and High Alarm Setpoint 302
: RPP-0036 Calibration of DRMS Area Monitors and Determination of Alert and High Alarm Setpoint 302
: RPP-0118 Calibration and Maintenance of Portable Radiological Air Samplers 5
: RPP-0118 Calibration and Maintenance of Portable Radiological Air Samplers
: STP-511-4201 Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test 25, 26
: STP-511-4201 Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test
: STP-511-4203 Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test 26, 27
: 25, 26
: STP-511-4203 Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test
: 26, 27
: STP-511-4209
: STP-511-4209
: RMS-Control Room Fresh Air System Radiation Monitor Local Intake Channel Calibration
: RMS-Control Room Fresh Air System Radiation Monitor Local Intake Channel Calibration RMS
: RMS-RE13A 304
-RE13A 304
: STP-511-4249
: STP-511-4249
: RMS-Primary Containment Area Radiation Monitor, Channel Calibration
: RMS-Primary Containment Area Radiation Monitor, Channel Calibration RMS
: RMS-RE16A 8, 9, 301, 302, 306
-RE16A 8, 9, 301, 302, 306
: Radiation Monitoring System Calibration Records Number Title Date
: Radiation Monitoring System Calibration Records Number Title Date
: WO 52427312
: WO 52427312
Line 846: Line 1,212:
: WO 52548887
: WO 52548887
: STP-511-4209:
: STP-511-4209:
: RMS-Control Room Fresh Air System Radiation Monitor Local Intake Channel Calibration
: RMS-Control Room Fresh Air System Radiation Monitor Local Intake Channel Calibration RMS
: RMS-RE13A June 2, 2016
-RE13A June 2, 2016
: WO 52599307
: WO 52599307
: STP-511-4201: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test November 1, 2016
: STP-511-4201: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test November 1, 2016
: WO 52628624
: WO 52628624
: STP-511-4249:
: STP-511-4249: RMS
: RMS-Primary Containment Area Radiation Monitor, Channel Calibration
-Primary Containment Area Radiation Monitor, Channel Calibration RMS
: RMS-RE16A May 3, 2017
-RE16A May 3, 2017
: WO 52737835
: WO 52737835
: STP-511-4201: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test April 11, 2017
: STP-511-4201: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test April 11, 2017
: WO 52737836
: WO 52737836
: STP-511-4203: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test April 11, 2017
: STP-511-4203: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test April 11, 2017
: Stationary Radiation Instrument Calibration Records Number Title Date 11 Calibration Data Sheet for Eberline
: Stationary Radiation Instrument Calibration Records Number Title Date 11 Calibration Data Sheet for Eberline PM
: PM-7 January 12, 2017
-7 January 12, 2017
: Stationary Radiation Instrument Calibration Records Number Title Date 572 Calibration Data Sheet for PCM 1B Personnel Contamination Monitor September 8, 2016 1011-060 Calibration Data Sheet for CRONOS Contamination Monitor January 31, 2017 11719 Calibration Data Sheet for Small Tool Monitor April 27, 2017 58692 Calibration Data Sheet for
: Stationary Radiation Instrument Calibration Records Number Title Date 572 Calibration Data Sheet for PCM 1B Personnel Contamination Monitor September 8, 2016
: GEM-5 Portal Monitor October 26, 2016 Fast Scan Calibration of the Canberra FastScan WBC System January 18, 2017
: 1011-060 Calibration Data Sheet for CRONOS Contamination Monitor January 31, 2017
: 11719 Calibration Data Sheet for Small Tool Monitor April 27, 2017
: 58692 Calibration Data Sheet for GEM
-5 Portal Monitor October 26, 2016
: Fast Scan Calibration of the Canberra FastScan WBC System January 18, 2017


==Section 2RS6: Radioactive Gaseous and Liquid Effluent Treatment==
==Section 2RS6: Radioactive Gaseous and Liquid Effluent Treatment==
: Audits and Self-Assessments Number Title Date
: Audits and Self
-Assessments Number Title Date
: LO-RLO-2017-0025 Radioactive Gaseous  and Liquid Effluent Treatment and Radiological Environmental Monitoring Program June 24, 2017  
: LO-RLO-2017-0025 Radioactive Gaseous  and Liquid Effluent Treatment and Radiological Environmental Monitoring Program June 24, 2017  
===Condition Reports===
===Condition Reports===
Line 880: Line 1,251:
===Miscellaneous===
===Miscellaneous===
: Number Title Date
: Number Title Date
: 2015 Annual Radioactive Effluent Release Report
: 2015 Annual Radioactive Effluent Release Report May 1, 2016
: May 1, 2016
: 2016 Annual Radioactive Effluent Release Report May 1, 2017
: 2016 Annual Radioactive Effluent Release Report
: Radiological Gaseous and Liquid Effluent Discharge Packages Selected Records
: May 1, 2017
: 2016 and 2017
: Radiological Gaseous and Liquid Effluent Discharge Packages
: 2510628
: Selected Records 2016 and 2017
: 52510628
: STP-402-3602, Inservice Testing of Division II Control Room March 9, 2016
: STP-402-3602, Inservice Testing of Division II Control Room March 9, 2016
: 52535118
: 2535118
: STP-511-4215,
: STP-511-4215, RMS
: RMS-Main Plant Exhaust Duct Noble Gas Activity Channel Calibration
-Main Plant Exhaust Duct Noble Gas Activity Channel Calibration
: RMS-RE126 June 9, 2015
: RMS-RE126 June 9, 2015
: 52597745
: 2597745
: STP-406-3602, Inservice Testing of Division II Fuel Building January 26, 2017
: STP-406-3602, Inservice Testing of Division II Fuel Building January 26, 2017
: 52644279
: 2644279
: STP-257-3602, Inservice Testing of Division II Standby Gas July 24, 2017  
: STP-257-3602, Inservice Testing of Division II Standby Gas July 24, 2017  
===Miscellaneous===
===Miscellaneous===
: Number Title Date
: Number Title Date
: 52644521
: 52644521
: STP-511-4214,
: STP-511-4214, RMS
: RMS-Main Plant Exhaust Duct Noble Gas Activity Channel Calibration
-Main Plant Exhaust Duct Noble Gas Activity Channel Calibration
: RMS-RE125 July 13, 2017
: RMS-RE125 July 13, 2017
: 52661227
: 2661227
: STP-511-5217,
: STP-511-5217, RMS
: RMS-Radwaste BLDG Ventilation Exhaust Duct Noble Gas Activity Monitor Channel Calibration
-Radwaste BLDG Ventilation Exhaust Duct Noble Gas Activity Monitor Channel Calibration RMS
: RMS-RE6B June 24, 2017
-RE6B June 24, 2017
: 525351117
: 25351117
: STP-511-4280,
: STP-511-4280, RMS
: RMS-Liquid Radwaste Effluent Line Radiation Monitor Channel Calibration
-Liquid Radwaste Effluent Line Radiation Monitor Channel Calibration
: RMS-RE107 March 16, 2016
: RMS-RE107 March 16, 2016
: 526132218
: 26132218
: STP-402-3601, Inservice Testing of Division I Control Room January 3, 2017  
: STP-402-3601, Inservice Testing of Division I Control Room January 3, 2017  
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: COP-0046 Sampling Gaseous Effluents Via the Wide Range Gas Monitors 15
: COP-0046 Sampling Gaseous Effluents Via the Wide Range Gas Monitors
: COP-0308 Operation of the Chemistry and Environmental Gamma Ray Spectroscopy Systems Using Apex 2
: COP-0308 Operation of the Chemistry and Environmental Gamma Ray Spectroscopy Systems Using Apex
: COP-0619 Gamma Isotopic Analysis Sample Preparation 6
: COP-0619 Gamma Isotopic Analysis Sample Preparation
: COP-0813 Radioactive Liquid Discharge Permit Process 1
: COP-0813 Radioactive Liquid Discharge Permit Process
: CSP-0110 Radioactive Liquid Effluent Batch Discharge 20
: CSP-0110 Radioactive Liquid Effluent Batch Discharge
: SOP-0113 Liquid Radwaste Processing/Recovery Sample Tank System 26
: SOP-0113 Liquid Radwaste Processing/Recovery Sample Tank System


==Section 2RS7: Radiological Environmental Monitoring Program==
==Section 2RS7: Radiological Environmental Monitoring Program==
: Audits, Self-Assessments, and Surveillances Number Title Date
: Audits, Self
: LO-RLO-2017-00022 Self-Assessment - Compliance with
-Assessments, and Surveillances Number Title Date
: EN-CY-102_Lab Analytical QC February 23, 2017
: LO-RLO-2017-00022 Self-Assessment  
: LO-RLO-2017-0025 Focused Self-Assessment: Radiological Environmental Monitoring Program and Radioactive Gaseous and Liquid Effluent Treatment June 24, 2017 NUPIC #24191 NUPIC Audit: Teledyne Brown Engineering Environmental Services - Audit NUPIC #24191 July 6, 2016  
- Compliance with EN
-CY-102_Lab Analytical
: QC February 23, 2017
: LO-RLO-2017-0025 Focused Self-Assessment:
: Radiological Environmental Monitoring Program and Radioactive Gaseous and Liquid Effluent Treatment June 24, 2017
: NUPIC #24191
: NUPIC Audit: Teledyne Brown Engineering Environmental Services  
- Audit NUPIC #24191
: July 6, 2016
: Calibration and Maintenance Records Number Title Date
: Calibration and Maintenance Records Number Title Date
: WO 52686362 Meteorological Monitoring - Wind Speed Elev. 150 foot (Secondary) Calibration Test September 21, 2016
: WO 52686362 Meteorological Monitoring  
: WO 52686365 Meteorological Monitoring - Wind Direction Elev. 30 foot (Primary) Calibration Test September 21, 2016
- Wind Speed Elev. 150 foot (Secondary)
: WO 52686366 Meteorological Monitoring - Wind Speed Elev. 150 foot (Primary) Calibration Test September 21, 2016
: Calibration Test September
: WO 52717223 Meteorological Monitoring - Wind Speed Elev. 30 foot (Secondary) Calibration Test March 22, 2017
: 21, 2016
: WO 52720478 Meteorological Monitoring - Air Temperature Difference Elev. 30/150 foot (Secondary)
: WO 52686365 Meteorological Monitoring  
- Wind Direction Elev. 30 foot (Primary)
: Calibration Test September 21
, 2016
: WO 52686366 Meteorological Monitoring  
- Wind Speed Elev. 150 foot (Primary)
: Calibration Test September
: 21, 2016 WO 52717223
: Meteorological Monitoring  
- Wind Speed Elev. 30 foot (Secondary)
: Calibration Test March 22, 2017
: WO 52720478 Meteorological Monitoring  
- Air Temperature Difference Elev. 30/150 foot (Secondary)
: Semi-Annual Channel Calibration March 27, 2017
: Semi-Annual Channel Calibration March 27, 2017
: WO 52725318 Meteorological Monitoring - Wind Speed Elev. 150 foot (Secondary) Calibration Test March 23, 2017  
: WO 52725318
: Meteorological Monitoring  
- Wind Speed Elev. 150 foot (Secondary)
: Calibration Test March 23, 2017  
===Condition Reports===
===Condition Reports===
(CRs)
(CRs)
Line 952: Line 1,344:
: TRM 3.12 Radiological Environmental Monitoring
: TRM 3.12 Radiological Environmental Monitoring
: 2016 Groundwater Monitoring Plan: River Bend, Rev. 6 February 8, 2017
: 2016 Groundwater Monitoring Plan: River Bend, Rev. 6 February 8, 2017
: RBG-47682 2015 Annual Radioactive Effluent Release Report
: RBG-47682 2015 Annual Radioactive Effluent Release Report May 2, 2016
: May 2, 2016
: RBG-47753 2016 Annual Radioactive Effluent Release Report May 1, 2017  
: RBG-47753 2016 Annual Radioactive Effluent Release Report May 1, 2017  
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: EN-CY-108 Monitoring of Non-Radioactive Systems 6
: EN-CY-108 Monitoring of Non
: EN-CY-108 Monitoring of Non-Radioactive Systems 6
-Radioactive Systems
: EN-CY-108 Monitoring of Non
-Radioactive Systems  
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: EN-CY-111 Radiological Groundwater Monitoring Program 7
: EN-CY-111 Radiological Groundwater Monitoring Program 7
: EN-EV-100 Environmental Expectations 5
: EN-EV-100 Environmental Expectations
: EN-RP-113 Response to Contaminated Spills/Leaks 9
: EN-RP-113 Response to Contaminated Spills/Leaks
: ESP-8-021 Sampling Of Water For Radiological Environmental Monitoring
: ESP-8-021 Sampling Of Water For Radiological Environmental Monitoring
: 14
: ESP-8-023 Sampling of Airborne Radioiodine and Particulates for Radiological Environmental Monitoring
: ESP-8-023 Sampling of Airborne Radioiodine and Particulates for Radiological Environmental Monitoring
: 15
: ESP-8-042 Radioactive Standard Preparation for Environmental Program
: ESP-8-042 Radioactive Standard Preparation for Environmental Program
: 7
: ESP-8-050 Conduct of the Radiological Environmental Monitoring Program (REMP)
: ESP-8-050 Conduct of the Radiological Environmental Monitoring Program (REMP)
: 15
: ESP-8-052 Inter-laboratory Comparison Program for Radiological Environmental Monitoring
: ESP-8-052 Inter-laboratory Comparison Program for Radiological Environmental Monitoring
: 11
: RSP-0008 Offsite Dose Calculation Manual
: RSP-0008 Offsite Dose Calculation Manual
: 15
: 15
: Section 2RS08:
: Section 2RS08:
: Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation
: Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation Audits and Self
: Audits and Self-Assessments Number Title Date
-Assessments Number Title Date
: Follow-Up to QA Finding (QAF) identified during the performance of the 2015 RP/Radwaste Audit March 15, 2016
: Follow-Up to QA Finding (QAF) identified during the performance of the 2015 RP/Radwaste Audit March 15, 2016
: LO-RLO-2017-0024 Pre-NRC Focused Self-Assessments Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation  (NRC
: LO-RLO-2017-0024 Pre-NRC Focused Self
: IP 71124.08) May 23, 2017
-Assessments Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation  
  (NRC IP 71124.08)
: May 23, 2017
: QA-14/15-2015-RBS-01 Radiation Protection/Radwaste Audit September 1, 2015  
: QA-14/15-2015-RBS-01 Radiation Protection/Radwaste Audit September 1, 2015  
===Condition Reports===
===Condition Reports===
Line 1,003: Line 1,393:
===Miscellaneous===
===Miscellaneous===
: Number Title Revision/Date
: Number Title Revision/Date
: Shipping Logbook 2015
: Shipping Logbook
: Shipping Logbook 2016
: 2015
: Shipping Logbook 2017
: Shipping Logbook
: RBG-47655 Spent Fuel Storage Radioactive Effluent Release Report for 2015 February 25, 2016
: 2016
: RBG-47682 2015 Annual Radioactive Effluent Release Report
: Shipping Logbook
: May 2, 2016
: 2017
: RBG-47739 Spent Fuel Storage Radioactive Effluent Release Report for 2016 February 23, 2017
: RBG-47655 Spent Fuel Storage Radioactive Effluent Release Report for 2015
: RBG-47753 2016 Annual Radioactive Effluent Release Report May 1, 2017
: February 25, 2016
: RLP-RPCT-SHIP DOT HAZMAT RAM Shipping 3 UFSAR Chapter 11 RBS Updates Final Safety Analysis Report 24 UFSAR Chapter 12
: RBG-47682 2015 Annual Radioactive Effluent Release Report May 2, 2016
: RBS Updated Final Safety Analysis Report 24 UFSAR Chapter 9 RBS Updated Final Safety Analysis Report 19
: RBG-47739 Spent Fuel Storage Radioactive Effluent Release Report for 2016
: February 23, 2017
: RBG-47753 2016 Annual Radioactive Effluent Release Report May 1, 201
: RLP-RPCT-SHIP DOT HAZMAT RAM Shipping 3 UFSAR Chapter 11
: RBS Updates Final Safety Analysis Report
: UFSAR Chapter 12  
: RBS Updated Final Safety Analysis Report
: UFSAR Chapter 9
: RBS Updated Final Safety Analysis Report  
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: EN-RP-121 Radioactive Material Control 13
: EN-RP-121 Radioactive Material Control
: EN-RW-101 Radioactive Waste Management 3
: EN-RW-101 Radioactive Waste Management
: EN-RW-102 Radioactive Shipping Procedure 15
: EN-RW-102 Radioactive Shipping Procedure
: EN-RW-104 Scaling Factors 13
: EN-RW-104 Scaling Factors
: EN-RW-105 Process Control Program 5
: EN-RW-105 Process Control Program
: EN-RW-106 Integrated Transportation Security Plan 6
: EN-RW-106 Integrated Transportation Security Plan
: EN-RW-108 Radioactive Shipment Accident Response 3
: EN-RW-108 Radioactive Shipment Accident Response
: RSP-0008 Offsite Dose Calculation Manual (ODCM) 15
: RSP-0008 Offsite Dose Calculation Manual (ODCM)
: RSP-0221 Controls for Storage, Monitoring and Decontamination Areas Outside the Protected Area 8
: RSP-0221 Controls for Storage, Monitoring and Decontamination Areas Outside the Protected Area
: RWS-0304 Radioactive Waste Handling and Control 16
: RWS-0304 Radioactive Waste Handling and Control
: RWS-0336 Set-Up and Operation of the
: RWS-0336 Set-Up and Operation of the RDS
: RDS-1000 Dewatering Unit 11   
-1000 Dewatering Unit 11   
: Radioactive Waste Stream Evaluations Number Title Date
: Radioactive Waste Stream Evaluations Number Title Date 369977001
: 369977001 10
: CFR 61 Dry Active Waste Stream (2015)
: CFR 61 Dry Active Waste Stream (2015) May 5, 2015
: May 5, 2015
: 394211001
: 394211001
: 10
: CFR 61 Liquid Waste Stream (LWS
: CFR 61 Liquid Waste Stream (LWS-CND) Resin April 19, 2016
-CND) Resin April 19, 2016
: 394211003 10
: 394211003
: CFR 61 SFC Waste Stream (2016) February 17, 2017
: CFR 61 SFC Waste Stream (2016)
: 407960001 10
: February 17, 2017
: 407960001
: CFR 61 RWCU Powdex Resin December 5, 2016
: CFR 61 RWCU Powdex Resin December 5, 2016
: RBS-1702-0246 113' Fuel Building February 24, 2017
: RBS-1702-0246 113' Fuel Building February 24, 2017
Line 1,049: Line 1,448:
: RBS-1706-0154 106' Radwaste Liner Bay June 14, 2017
: RBS-1706-0154 106' Radwaste Liner Bay June 14, 2017
: RBS-1706-0221 1408 OS Low Level Radwaste June 21, 2017
: RBS-1706-0221 1408 OS Low Level Radwaste June 21, 2017
: RBS-1706-0313 1419 OS Release Facility June 26, 2017
: RBS-1706-0313 1419 OS Release Facility June 26, 20
: Shipments
: Shipments
: RBS-2015-003
: RBS-2015-003
Line 1,067: Line 1,466:
===Miscellaneous===
===Miscellaneous===
: Number Title Revision/Date Engineering Report
: Number Title Revision/Date Engineering Report
: RBS-SA-06-0001 RBS Mitigating System Performance Index (MSPI) Basis Document 2
: RBS-SA-06-0001 RBS Mitigating System Performance Index (MSPI) Basis Document
: NEI 99-02 Regulatory Assessment Performance Indicator Guideline 7
: NEI 99-02 Regulatory Assessment Performance Indicator Guideline  
===Miscellaneous===
===Miscellaneous===
: Number Title Revision/Date
: Number Title Revision/Date
Line 1,074: Line 1,473:
===Procedure===
===Procedure===
: Number Title Revision
: Number Title Revision
: EN-LI-114 Performance Indicator Process 8
: EN-LI-114 Performance Indicator Process


==Section 4OA2: Problem Identification and Resolution==
==Section 4OA2: Problem Identification and Resolution==
Line 1,082: Line 1,481:
===Procedures===
===Procedures===
: Number Title Revision
: Number Title Revision
: GMP-0015 Lubrication Procedure 14
: GMP-0015 Lubrication Procedure
: GMP-0015 Lubrication Procedure 16
: GMP-0015 Lubrication Procedure Work Order (WO)
: Work Order (WO) WO 52632206
: WO 52632206
 
==Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion==


==Section 4OA3: ==
: Follow
-up of Events and Notices of Enforcement Discretion
===Condition Report (CR)===
===Condition Report (CR)===
: CR-RBS-2017-02405
: CR-RBS-2017-02405
: Work Order (WO)
: Work Order (WO)
: WO 00438386      
: WO 00438386
: The following items are requested for the Public Radiation Safety Inspection at River Bend Station August 21-25, 2017 Integrated Report
: The following items are requested for the Public Radiation Safety Inspection at River Bend Station August 21
: 2017003
-25, 2017 Integrated Report 2017003
: Inspection areas are listed in the attachments below.
: Inspection areas are listed in the attachments below.
: Please provide the requested information on or before July 26, 2017.
: Please provide the requested information on or before July 26, 2017
.
: Please submit this information using the same lettering system as below.
: Please submit this information using the same lettering system as below.
: For example, all contacts and phone numbers for Inspection Procedure 71124.01 should be in a file/folder titled "1- A," applicable organization charts in file/folder "1- B," etc.
: For example, all contacts and phone numbers for Inspection Procedure 71124.0
should be in a file/folder titled  
"1- A," applicable organization charts in file/folder "
: 1- B," etc.
: If information is placed on ims.certrec.com, please ensure the inspection exit date entered is at least 30 days later than the onsite inspection dates, so the inspectors will have access to the information while writing the report.
: If information is placed on ims.certrec.com, please ensure the inspection exit date entered is at least 30 days later than the onsite inspection dates, so the inspectors will have access to the information while writing the report.
: In addition to the corrective action document lists provided for each inspection procedure listed below, please provide updated lists of corrective action documents at the entrance meeting.
: In addition to the corrective action document lists provided for each inspection procedure listed below, please provide updated lists of corrective action documents at the entrance meeting.
Line 1,103: Line 1,507:
: If more than one inspection procedure is to be conducted and the information requests appear to be redundant, there is no need to provide duplicate copies.
: If more than one inspection procedure is to be conducted and the information requests appear to be redundant, there is no need to provide duplicate copies.
: Enter a note explaining in which file the information can be found.
: Enter a note explaining in which file the information can be found.
: If you have any questions or comments, please contact Louis Carson at (817) 817-200-1221 or Louis.Carson@nrc.gov.
: If you have any questions or comments, please contact Louis Carson at (817) 817-200-1221 or Louis.Carson@nrc.gov
: PAPERWORK REDUCTION ACT STATEMENT This letter does not contain new or amended information collection requirements subject to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.).
.
: Existing information collection requirements were approved by the Office of Management and Budget, control number 3150-0011.
: PAPERWORK
: 5. Radiation Monitoring Instrumentation (71124.05) Date of Last Inspection: December 7, 2015
: REDUCTION ACT STATEMENT
: A. List of contacts and telephone numbers for the following areas: 1. Effluent monitor calibration 2. Radiation protection instrument calibration
: This letter does not contain new or amended information collection requirements subject to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.).  
: 3. Installed instrument calibrations 4. Count room and Laboratory instrument calibrations
: Existing information collection requirements were approved by the Office of Management and Budget, control number 3150
: B. Applicable organization charts C. Copies of audits, self-assessments, vendor or NUPIC audits for contractor support and LERs, written since date of last inspection, related to:
-0011.
: 1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, or whole body counters 2. Installed radiation monitors
: 5. Radiation Monitoring Instrumentation (71124.05)
: D. Procedure index for: 1. Calibration, use and operation of continuous air monitors, criticality monitors, portable survey instruments, temporary area radiation monitors, electronic dosimeters, teledosimetry, personnel contamination monitors, and whole body counters. 2. Calibration of installed radiation monitors E. Please provide specific procedures related to the following areas noted below.
: Date of Last Inspection:
: December 7, 2015
: A. List of contacts and telephone numbers for the following areas:
: 1. Effluent monitor calibration
: 2. Radiation protection instrument calibration
: 3. Installed instrument calibrations
: 4. Count room and Laboratory instrument calibrations  
: B. Applicable organization charts
: C. Copies of audits, self
-assessments, vendor or NUPIC audits for contractor support and LERs, written since date of last inspection
, related to:  
: 1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, or whole body counters
: 2. Installed radiation monitors
: D. Procedure index for:
: 1. Calibration, use and operation of continuous air monitors, criticality monitors, portable survey instruments, temporary area radiation monitors, electronic dosimeters, teledosimetry, personnel contamination monitors, and whole body counters.
: 2. Calibration of installed radiation monitors
: E. Please provide specific procedures related to the following areas noted below
.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Calibration of portable radiation detection instruments (for portable ion chambers) 2. Whole body counter calibration
: 1. Calibration of portable radiation detection instruments (for portable ion chambers)
: 2. Whole body counter calibration  
: 3. Laboratory instrumentation quality control
: 3. Laboratory instrumentation quality control
: F. A summary list of corrective action documents (including corporate and sub-tiered systems) written since date of last inspection, related to the following programs: 1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, whole body counters, 2. Installed radiation monitors, 3. Effluent radiation monitors 4. Count room radiation instruments NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: F. A summary list of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection, related to the following programs:
: 1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, whole body counters,
: 2. Installed radiation monitors,
: 3. Effluent radiation monitors
: 4. Count room radiation instruments
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. Offsite dose calculation manual, technical requirements manual, or licensee controlled specifications which lists the effluent monitors and calibration requirements. H. Current calibration data for the whole body counters. I. Primary to secondary source calibration correlation for effluent monitors.
: G. Offsite dose calculation manual, technical requirements manual, or licensee controlled specifications which lists the effluent monitors and calibration requirements.
: H. Current calibration data for the whole body counter
s. I. Primary to secondary source calibration correlation for effluent monitors.
: J. A list of the point of discharge effluent monitors with the two most recent calibration dates and the work order numbers associated with the calibrations.
: J. A list of the point of discharge effluent monitors with the two most recent calibration dates and the work order numbers associated with the calibrations.
: K. Radiation Monitoring System health report for the previous 12 months
: K. Radiation Monitoring System health report for the previous 12 months
: 6. Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
: 6. Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
: Date of Last Inspection: December 7, 2015
: Date of Last Inspection:
: A. List of contacts and telephone numbers for the following areas: 1. Radiological effluent control
: December 7, 2015
: A. List of contacts and telephone numbers for the following areas:
: 1. Radiological effluent control
: 2. Engineered safety feature air cleaning systems
: 2. Engineered safety feature air cleaning systems
: B. Applicable organization charts C. Audits, self-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to: 1.
: B. Applicable organization charts
: Radioactive effluents 2.
: C. Audits, self
: Engineered Safety Feature Air cleaning systems D. Procedure indexes for the following areas 1. Radioactive effluents 2. Engineered Safety Feature Air cleaning systems E. Please provide specific procedures related to the following areas noted below.
-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to:
: 1.
: Radioactive effluents
: 2.
: Engineered Safety Feature Air cleaning systems
: D. Procedure indexes for the following areas
: 1. Radioactive effluents
: 2. Engineered Safety Feature Air cleaning systems
: E. Please provide specific procedures related to the following areas noted below
.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Sampling of radioactive effluents 2. Sample analysis 3. Generating radioactive effluent release permits 4. Laboratory instrumentation quality control 5. In-place testing of HEPA filters and charcoal adsorbers 6. New or applicable procedures for effluent programs (e.g., including ground water monitoring programs) F. List of corrective action documents (including corporate and sub-tiered systems) written since date of last inspection, associated with: 1.
: 1. Sampling of radioactive effluents
: Radioactive effluents 2.
: 2. Sample analysis
: Effluent radiation monitors 3.
: 3. Generating radioactive effluent release permits
: Engineered Safety Feature Air cleaning systems NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: 4. Laboratory instrumentation quality control
: Please provide in document formats which are "searchable" so that the inspector can perform word searches. G. 2015 and 2016 Annual Radioactive Effluent Release Report or the two most recent reports. H. Current Copy of the Offsite Dose Calculation Manual. I. Copy of the 2015 and 2016 inter-laboratory comparison results for laboratory quality control performance of effluent sample analysis, or the two most recent results.
: 5. In-place testing of HEPA filters and charcoal adsorbers
: J. Effluent sampling schedule for the week of the inspection.
: 6. New or applicable procedures for effluent programs (e.g., including ground water monitoring programs)
: F. List of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection, associated with:
: 1.
: Radioactive effluents
: 2.
: Effluent radiation monitors
: 3.
: Engineered Safety Feature Air cleaning systems
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. 2015 and 2016
: Annual Radioactive Effluent Release Report or the two most recent reports. H. Current Copy of the Offsite Dose Calculation Manual
. I. Copy of the 2015 and 2016
inter-laboratory comparison results for laboratory quality control performance of effluent sample analysis, or the two most recent results.
: J. Effluent sampling schedule for the week of the inspection
.
: K. New entries into 10
: K. New entries into 10
: CFR 50.75(g) files since date of last inspection. L. Operations department (or other responsible dept.) log records for effluent monitors removed from service or out of service. M. Listing or log of liquid and gaseous release permits since date of last inspection. N. A list of the technical specification-required air cleaning systems with the two most recent surveillance test dates of in-place filter testing (of HEPA filters and charcoal adsorbers) and laboratory testing (of charcoal efficiency) and the work order numbers associated with the surveillances. O. System Health Report for radiation monitoring instrumentation.
: CFR 50.75(g) files since date of last inspection
: Also, please provide a specific list of all effluent radiation monitors that were considered inoperable for 7 days or more since the last inspection.
. L. Operations department
: If applicable, please provide the relative Special Report and condition report(s).
(or other responsible dept.) log records for effluent monitors removed from service or out of service
: P. A list of all radiation monitors that are considered §50.65/Maintenance Rule equipment. Q. A list of all significant changes made to the Gaseous and Liquid Effluent Process Monitoring System since the last inspection.
. M. Listing or log of liquid and gaseous release permits since date of last inspection
. N. A list of the technical specification
-required air cleaning systems with the two most recent surveillance test dates of in
-place filter testing (of HEPA filters and charcoal adsorbers) and laboratory testing (of charcoal efficiency) and the work order numbers associated with the surveillances
. O. System Health Report for radiation monitoring instrumentation.
: Also, please provide
a specific list of all effluent radiation monitors that were considered inoperable for 7 days or more since the last inspection
.
: If applicable, please provide the relative Special Report and condition report(s).  
: P. A list of all radiation monitors that are considered §50.65/Maintenance Rule equipment.
: Q. A list of all significant changes made to the Gaseous and Liquid Effluent Process Monitoring System since the last inspection.
: If applicable, please provide the corresponding UFSAR section in which this change was documented.
: If applicable, please provide the corresponding UFSAR section in which this change was documented.
: R.
: R.
: A list of any occurrences in which a non-radioactive system was contaminated by a radioactive system.
: A list of any occurrences in which a non
-radioactive system was contaminated by a radioactive system.
: Please include any relative condition report(s).
: Please include any relative condition report(s).
: 7. Radiological Environmental Monitoring Program (71124.07)
: 7. Radiological Environmental Monitoring Program (71124.07)  
: Date of Last Inspection: December 7, 2015
: Date of Last Inspection:
: A. List of contacts and telephone numbers for the following areas: 1. Radiological environmental monitoring
: December 7, 2015
: 2. Meteorological monitoring B. Applicable organization charts. C. Audits, self-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to: 1. Radiological environmental monitoring program (including contractor environmental laboratory audits, if used to perform environmental program functions) 2. Environmental TLD processing facility 3. Meteorological monitoring program D. Procedure index for the following areas: 1. Radiological environmental monitoring program 2. Meteorological monitoring program E. Please provide specific procedures related to the following areas noted below.
: A. List of contacts and telephone numbers for the following areas:
: 1. Radiological environmental monitoring
: 2. Meteorological monitoring
: B. Applicable organization charts
. C. Audits, self
-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to:
: 1. Radiological environmental monitoring program (including contractor environmental laboratory audits, if used to perform environmental program functions)
: 2. Environmental TLD processing facility 3. Meteorological monitoring program
: D. Procedure index for the following areas:
: 1. Radiological environmental monitoring program
: 2. Meteorological monitoring program
: E. Please provide specific procedures related to the following areas noted below
.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Environmental Program Description 2. Sampling, collection and preparation of environmental samples 3. Sample analysis (if applicable)
: 1. Environmental Program Description
: 4. Laboratory instrumentation quality control 5. Procedures associated with the Offsite Dose Calculation Manual.
: 2. Sampling, collection and preparation of environmental samples
: 6. Appropriate QA Audit and program procedures, and/or sections of the station's QA manual (which pertain to the REMP) F. A summary list of corrective action documents (including corporate and sub-tiered systems) written since date of last inspection, related to the following programs: 1. Radiological environmental monitoring 2. Meteorological monitoring NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: 3. Sample analysis (if applicable)  
: Please provide in document formats which are "searchable" so that the inspector can perform word searches. G. Wind Rose data and evaluations used for establishing environmental sampling locations.
: 4. Laboratory instrumentation quality control
: 5. Procedures associated with the Offsite Dose Calculation Manual
.
: 6. Appropriate QA Audit and program procedures, and/or sections of the station's QA manual (which pertain to the REMP)
: F. A summary list of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection, related to the following programs:
: 1. Radiological environmental monitoring
: 2. Meteorological monitoring
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. Wind Rose data and evaluations used for establishing environmental sampling locations
.
: H. Copies of the 2 most recent calibration packages for the meteorological tower instruments.
: H. Copies of the 2 most recent calibration packages for the meteorological tower instruments.
: I. Copy of the 2015 and 2016 Annual Radiological Environmental Operating Report and Land Use Census, and current revision of the Offsite Dose Calculation Manual, or the two most recent reports.
: I. Copy of the 2015 and 2016
: J. Copy of the environmental laboratory's inter-laboratory comparison program results for 2015 and 2016, or the two most recent results, if not included in the annual radiological environmental operating report. K. Data from the environmental laboratory documenting the analytical detection sensitivities for the various environmental sample media (i.e., air, water, soil, vegetation, and milk). L. Quality Assurance audits (e.g., NUPIC) for contracted services. M. Current NEI Groundwater Initiative Plan and status. N.
: Annual Radiological Environmental Operating Report and Land Use Census, and current revision of the Offsite Dose Calculation Manual, or the two most recent reports.
: Technical requirements manual or licensee controlled specifications which lists the meteorological instruments calibration requirements.
: J. Copy of the environmental laboratory's inter
-laboratory comparison program results for  
: 2015 and 2016, or the two most recent results, if not included in the annual radiological environmental operating report
. K. Data from the environmental laboratory documenting the analytical detection sensitivities for the various environmental sample media (i
.e., air, water, soil, vegetation, and milk)
. L. Quality Assurance audits (e.g., NUPIC) for contracted services.
: M. Current NEI Groundwater Initiative Plan and status
. N.
: Technical requirements manual or licensee controlled specifications which lists the meteorological instruments calibration requirements
.
: O. A list of Regulatory Guides and/or NUREGs that you are currently committed to relative to the Radiological Environmental Monitoring Program.
: O. A list of Regulatory Guides and/or NUREGs that you are currently committed to relative to the Radiological Environmental Monitoring Program.
: Please include the revision and/or date for the committed item and where this can be located in your current licensing basis/UFSAR.
: Please include the revision and/or date for the committed item and where this can be located in your current licensing basis/UFSAR.
: P. If applicable, per
: P. If applicable, per NEI 07
: NEI 07-07, provide any reports that document any spills/leaks to groundwater since the last inspection.
-07, provide any reports that document any spills/leaks to groundwater since the last inspection
: 8. Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)
.
: Date of Last Inspection: December 7, 2015
: 8. Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)  
: A. List of contacts and telephone numbers for the following areas: 1. Solid Radioactive waste processing 2. Transportation of radioactive material/waste B. Applicable organization charts (and list of personnel involved in solid radwaste processing, transferring, and transportation of radioactive waste/materials).   
: Date of Last Inspection:
: C. Copies of audits, department self-assessments, and LERs written since date of last inspection related to: 1. Solid radioactive waste management 2. Radioactive material/waste transportation program D. Procedure index for the following areas: 1. Solid radioactive waste management 2. Radioactive material/waste transportation
: December 7, 2015
: E. Please provide specific procedures related to the following areas noted below.
: A. List of contacts and telephone numbers for the following areas: 1. Solid Radioactive waste processing
: 2. Transportation of radioactive material/waste
: B. Applicable organization charts (and list of personnel involved in solid radwaste processing, transferring, and transportation of radioactive waste/materials)
.   
: C. Copies of audits, department self
-assessments, and LERs written since date of last inspection related to:
: 1. Solid radioactive waste management
: 2. Radioactive material/waste transportation program
: D. Procedure index for the following areas:
: 1. Solid radioactive waste management
: 2. Radioactive material/waste transportation  
: E. Please provide specific procedures related to the following areas noted below
.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Process control program 2. Solid and liquid radioactive waste processing
: 1. Process control program
: 3. Radioactive material/waste shipping
: 2. Solid and liquid radioactive waste processing
: 4. Methodology used for waste concentration averaging, if applicable 5. Waste stream sampling and analysis F. A summary list of corrective action documents (including corporate and sub-tiered systems) written since date of last inspection related to: 1. Solid radioactive waste 2. Transportation of radioactive material/waste NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: 3. Radioactive material/waste shipping  
: Please provide in document formats which are "searchable" so that the inspector can perform word searches. G. Copies of training lesson plans for 49CFR172 subpart H, for radwaste processing, packaging, and shipping. H. A summary of radioactive material and radioactive waste shipments made from date of last inspection to present. I. Waste stream sample analyses results and resulting scaling factors for 2015 and 2016, or the two most recent results. J. Waste classification reports if performed by vendors (such as for irradiated hardware). K. A listing of all onsite radwaste storage facilities.
: 4. Methodology used for waste concentration averaging, if applicable
: Please include a summary or listing of the items stored in each facility, including the total amount of radioactivity and the highest general area dose rate. Although it is not necessary to compile the following information, the inspector will also review: L. Training, and qualifications records of personnel responsible for the conduct of radioactive waste processing, package preparation, and shipping.
: 5. Waste stream sampling and analysis
: F. A summary list of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection related to:
: 1. Solid radioactive waste
: 2. Transportation of radioactive material/waste
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. Copies of training lesson plans for 49CFR172 subpart H, for radwaste processing, packaging, and shipping.
: H. A summary of radioactive material and radioactive waste shipments made from date of last inspection to present
. I. Waste stream sample analyses results and resulting scaling factors for 2015 and 2016
, or the two most recent results.
: J. Waste classification reports if performed by vendors (such as for irradiated hardware)
. K. A listing of all onsite radwaste storage facilities.
: Please include a summary or listing of the items stored in each facility, including the total amount of radioactivity and the highest general area dose rate.
: Although it is not necessary to compile the following information, the inspector will also review:
: L. Training, and qualifications records of personnel responsible for the conduct of radioactive waste processing, package preparation, and shipping.
}}
}}

Revision as of 10:11, 29 June 2018

River Bend Station - NRC Integrated Inspection Report 05000458/2017003
ML17318A189
Person / Time
Site: River Bend Entergy icon.png
Issue date: 11/13/2017
From: Kozal J W
NRC/RGN-IV/DRP/RPB-C
To: Maguire W F
Entergy Operations
JASON KOZAL
References
IR 2017003
Download: ML17318A189 (54)


Text

November 13, 2017

Mr. William F. Maguire, Site Vice President Entergy Operations, Inc.

River Bend Station 5485 U.S. Highway 61N St. Francisville, LA 707 75

SUBJECT: RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2017003

Dear Mr. Maguire:

On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station, Unit 1.

On October 11, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report. One of these findings involved a violation of NRC requirements

. Further, inspectors documented a licensee

-identified violation, which was determined to be of very low safety significance, in this report. The NRC is treating these violations as non-cited violation s consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violation s or significance of the non-cited violation s, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the River Bend Station.

If you disagree with a cross

-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555

-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the River Bend Station. UNITED STATES NUCLEAR REGULATORY COMMISSION REGION IV 1600 E. LAMAR BLVD ARLINGTON, TX 76011

-4511 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading

-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."

Sincerely,/RA/ Jason W. Kozal, Chief Project Branch C Division of Reactor Projects Docket No.: 50-458 License No

.: NPF-47

Enclosure:

Inspection Report 05000458/2017003

w/Attachments:

1.Supplemental Information 2.Public Radiation Safety InspectionDocument Request

x SUNSI Review: ADAMS: Non-Publicly Available x Non-Sensitive Keyword: By: JKozal/dll x Yes No x Publicly Available Sensitive NRC-002 OFFICE SRI:DRP/C RI:DRP/C SPE:DRP/C C:DRS/EB1 C:DRS/EB2 C:DRS/OB NAME JSowa BParks CYoung TFarnholtz GWerner VGaddy SIGNATURE

/RA/ /RA/ /RA/ /RA/ /RA/STG for

/RA/ DATE 11/3/2017 11/7/2017 11/3/2017 11/03/2017 11/13/2017 11/6/17 OFFICE C:DRS/PSB2 TL:IPAT BC:DRP/C NAME HGepford THipschman JKozal SIGNATURE

/RA/ /RA/ /RA/ DATE 11/6/17 11/6/2017 11/13/2017

Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 05000458 License: NPF-47 Report: 05000458/2017003 Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station Location:

5485 U.S. Highway 61N St. Francisville, LA 70775 Dates: July 1 through September 30, 2017 Inspectors:

J. Sowa, Senior Resident Inspector B. Parks, Resident Inspector L. Carson II, Senior Health Physicist N. Greene, PhD, Health Physicist S. Money, Health Physicist J. O'Donnell, CHP, Health Physicist J. Braisted, PhD, Reactor Inspector Approved By:

J. Kozal, Chief Project Branch C Division of Reactor Projects

2

SUMMARY

IR 05000458/2017003; 07/01/2017

- 09/30/2017; River Bend Station; Heat Sink Performance; Follow-up of Events and Notices of Enforcement Discretion The inspection activities described in this report were performed between July 1 and September 30, 2017, by the resident inspectors at River Bend Statio n and inspectors from the NRC's Region IV office

. Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements

. Additionally, NRC inspectors documented one licensee-identified violation of very low safety significance in this report. The significance of inspection findings is indicated by their color (i.e., Green, greater than Green, White, Yellow, or Red), determined using NRC Inspection Manual Chapter 0609, "Significance Determination Process," dated April 29, 2015. Their cross-cutting aspects are determined using NRC Inspection Manual Chapter 0310, "Aspects within the Cross-Cutting Areas," dated December 4, 2014. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG

-1649, "Reactor Oversight Process," dated July 2016.

Cornerstone: Initiating Events

Green.

The inspectors reviewed a self-revealed finding for the licensee's failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram. Corrective actions included properly installing the tee connection and writing specific procedural guidance on compression fitting inspection, installation, remake

, and repair (CR

-RBS-2017-02405). The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee's failure to properly install the tee connection caused a steam lea k that led to a reactor scram

. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, "Initiating Events Screening Questions." The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5].

(Section 4OA3)

Cornerstone: Mitigating Systems

Green.

The inspector s identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," which states, in part, "Measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions." Specifically, prior to September 28, 2017, the licensee's current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30

-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated. This finding was entered into the licensee's corrective action program as Condition Report CR-RBS-2017-06998.

The inspector determined that the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30

-day inventory requirement needed to be re-performed to assure that accident analysis requirements were met. In accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding had a cross-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30

-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin [H.6].

(Section 1R07)

Licensee-Identified Violations

A violation of very low safety significance (Green) that was identified by the licensee has been reviewed by the inspectors.

Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. Th is violation and associated corrective action tracking numbers are listed in Section 4OA7 of this report.

4

PLANT STATUS

River Bend Station began the inspection period at 88 percent reactor thermal power

. Operators were in the process of returning the plant to full power following a scram that occurred on June 23, 2017. The station returned to 100 percent power on July 3, 2017. On July 28, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak. The station returned to 100 percent power on August 3, 2017. On August 18, 2017, an automatic reactor scram occurred due to equipment issues associated with the feedwater level control system

. On August 20, 2017, operators conducted a reactor startup. The station returned to 100 percent power on August 28, 2017. On September 22, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak, but did not identify a new fuel leak

. The station returned to 100 percent power on September 28

, 2017.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness to Cope with External Flooding

a. Inspection Scope

On July 19, 2017, the inspectors completed an inspection of the station's readiness to cope with external flooding. After reviewing the licensee's flooding analysis, the inspectors chose three plant areas that were susceptible to flooding:

Residual heat removal train B pump room Low pressure core spray pump room Division I emergency diesel generator

The inspectors reviewed plant design features and licensee procedures for coping with flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether credited operator actions could be successfully accomplished.

These activities constitute one sample of readiness to cope with external flooding, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walk

down

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk

-significant systems: August 14, 2017, Division III 125 VDC system August 28, 2017, Division II standby service water system September 21, 2017, Division II control building chilled water system The inspectors reviewed the licensee's procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constitute three partial system walkdown sample s, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

.2 Complete Walk

down

a. Inspection Scope

On August 14, 2017, the inspectors performed a complete system walkdown inspection of the Division I and Division II 125 VDC system. The inspectors reviewed the licensee's procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, and open condition reports

. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.

These activities constitute one complete system walkdown sample, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensee's fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:

July 19, 2017, battery 1A room, fire area C-18 July 19, 2017, ENB inverter charger B room, fire area C-19 August 16, 2017, battery 1B room, fire area C-19 August 28, 2017, standby cooling tower pump B room, fire area PH-2/Z-1 For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constitut e four quarterly inspection sample s, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

On September 27, 2017, the inspectors completed an inspection of the station's ability to mitigate flooding due to internal causes. After reviewing the licensee's flooding analysis, the inspectors chose one plant area containing risk

-significant structures, systems, and components that were susceptible to flooding:

Division I and II standby switchgear rooms

The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.

These activities constitute completion of one flood protection measures sample, as defined in Inspection Procedure 71111.06.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

.1 Annual Review

a. Inspection Scope

On September 22, 2017, the inspectors completed an inspection of the readiness and availability of risk

-significant heat exchangers. The inspectors reviewed the data from the most recent internal inspection of the Division II emergency diesel generator jacket water cooler and verified that the licensee adhered to the periodic maintenance method outlined in EPRI NP-7552. Additionally, the inspectors walked down the Division II emergency diesel generator jacket water cooler to observe its material condition and verified that the cooler was correctly categorized under the Maintenance Rule and was receiving proper maintenance.

These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.

b. Findings

No findings were identified.

.2 Triennial Review

a. Inspection Scope

The inspectors reviewed licensee programs to verify heat exchanger performance and operability for the following heat exchangers:

Ultimate Heat Sink Division I Emergency Diesel Generator Jacket Water Heat Exchanger EGT

-E1A Division I Containment Unit Cooler HVR

-UC1A Division I Residual Heat Removal Heat Exchanger E12

-EB001A The inspector s verified whether testing, inspection, maintenance, and chemistry control programs are adequate to ensure proper heat transfer. The inspectors verified that the periodic testing and monitoring methods, as outlined in commitments to NRC Generic Letter 89-13, utilized proper industry heat exchanger guidance. Additionally, the inspectors verified that the licensee's chemistry program ensured that biological fouling was properly controlled between tests. The inspectors reviewed previous maintenance records of the heat exchangers to verify that the licensee's heat exchanger inspections adequately addressed structural integrity and cleanliness of their tubes. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four triennial heat sink inspection sample s, as defined in Inspection Procedure 71111.07-05.

b. Findings

Introduction.

The inspector s identified a Green, non

-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," involving the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis. Specifically, the analysis did not include loss of inventory from the safety

-related standby service water system to the nonsafety

-related normal service water system via the normal service water return isolation valves (prior to manual operator action to close the valves)

, given a loss of coolant accident coincident with a loss of offsite power and the single active failure of an emergency diesel generator to start or run.

Description.

The technical specification bases for Technical Specification 3.7.1, "Standby Service Water (SSW) System and Ultimate Heat Sink (UHS)," describe that safety analyses for long

-term containment cooling were performed and that for a loss of coolant accident concurrent with a loss of offsite power, the worst case single failure affecting the performance of the standby service water system is the failure of one of the two standby diesel generators, which would in turn affect one standby service water subsystem. The standby service water system is thus designed to preserve the capability to supply adequate cooling water to equipment required for safe reactor shutdown. Additionally, the bases describe that the ultimate heat sink consists of one

200 percent cooling tower and one 100 percent capacity water storage basin, which is sized such that sufficient water inventory is available to provide heat removal capability to safely shut down the plant and to maintain it in a cold shutdown condition for a 30

-day period with no external makeup water source available

.

The inspector s requested and reviewed Abnormal Operating Procedure AOP

-0016, "Loss of Standby Service Water," Revision 22, which contained a note that states "Within 20 minutes, actions shall be taken to isolate Division I or Division II standby service water return to normal service water to conserve standby cooling tower inventory per Section 5.1 or Section 5.2." An additional note states that "With a failure of the Division I diesel to start or load, the Division I powered service water system isolation valves are not able to be closed electrically. With pump SWP

-P2C operating, service water flow from Division I standby service water will pass through the unisolated drywell unit coolers and exit into the Division II standby service water return header back to the standby cooling tower. This return flow will be in excess of the design limits for the Division II portion of the standby cooling tower, thus requiring that SWP

-P2C be secured."

The inspector s reviewed calculation PM

-194, "Standby Cooling Tower Performance and Evaporation Losses without Drywell Unit Coolers," Revision 10, whose stated purpos e "is to determine the capacity of the ultimate heat sink to mitigate a design basis accident, using the containment heat loads identified in G13.18.0*19 (Ref.

II.2) for a design basis loss of coolant accident coincident with a loss of offsite power and failure of Division II standby diesel generator EGS

-EG1B." The conclusion of the inventory loss case was that a margin of approximately 393,100 gallons would exist in the ultimate heat sink basin after 30 days at technical specification limiting initial conditions. However, the inspector was unable to identify where the calculation accounted for the standby service water system water losses associated with the 20

-minute operator action to close the normal service water return isolation valves. Therefore, the inspector requested the analysis of record that demonstrated the loss of standby service water (i.e., ultimate heat sink inventory) to the normal service water system from the affected standby service water train would not be in excess of design limits prior to manual isolation.

The licensee provided calculation PM

-193, "Standby Service Water

- Maximum Flow through Break in Tunnel Piping

," Revision 1, as the original basis for the 20

-minute operator action. The purpose of PM

-193 was to determine the inventory margin and operator action time impact of the assumed break given the scenario in the preceding paragraph, but for a failure of the Division I standby emergency diesel generator instead of the Division II. The postulated break occurred downstream of service water return isolation valve SWP

-MOV96A in the nonsafety

-related normal service water return header. The conclusion of PM

-193 is that 229,500 gallons are potentially lost from the standby service water system to the normal service water system within 30 minutes prior to standby service water system isolation. Based upon the se results, the inspector estimated that potentially 153,000 gallons of ultimate heat sink inventory could be lost prior to the 20

-minute operator action in AOP

-0016 to isolate the nonsafety

-related from the safety

-related service water systems. Therefore, the inspector concluded that the inventory losses associated with the delayed closure of the normal service water isolation valves were not, but should have been

, included in the ultimate heat sink inventory analysis and that the reduction of margin in the inventory analysis was significant. Furthermore, the failure of the Division I standby diesel generator to start or run would result in greater inventory losses through the normal service water return isolation valve than for the same failure on the Division II standby diesel generator due to differences in the design between standby service water system trains; however, PM-194 assumed only a Division II failure

.

Analysis.

The failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30

-day inventory requirement needed to be re

-performed to assure that accident analysis requirements were met.

In accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At

-Power," dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non

-technical specification equipment; and did not screen as potentially risk

-significant due to seismic, flooding, or severe weather.

This finding had a cross

-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30

-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin

[H.6]. Enforcement

. Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, prior to September 28, 2017, the licensee failed to assure that the design basis for those structures, systems, and components to which this appendix applies was correctly translate d into specifications, drawings, procedures, and instructions. Specifically, the current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated

. Because this finding was of very low safety significance (Green) and has been entered into the licensee's corrective action program as Condition Report CR-RBS-2017-06998, it is being treated as a non

-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy: NCV 05000458/2017003

-01, "Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory

Analysis.

"

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On August 9, 2017, the inspectors observed a portion of an annual requalification test for licensed operators. The inspectors assessed the performance of the operators and the evaluators' critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities

. These activities constitute completion o f one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

The inspectors observed the performance of on

-shift licensed operators in the plant's main control room. At the time of the observations, the plant was conducting a reactor startup following a reactor scram. The inspectors observed the operators' performance of the following activities:

August 20, 2017, plant startup, including rod withdrawal to criticality In addition, the inspectors assessed the operators' adherence to plant procedures, including the conduct of operations procedur e, and other operations department policies.

These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectivene

ss (71111.12)

.1 Routine Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed one instance of a degraded performance or condition of safety-significant structures, systems, and components (SSCs): September 12, 2017, 125 VDC distribution system, functional failure review The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constitute completion o f one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

.2 Quality Control

a. Inspection Scope

On August 7, 2017, the inspectors reviewed the licensee's quality control activities through a review of their control of safety

-related lubricants. The inspectors also reviewed whether quality control verifications were property specified in accordance with the licensee's Quality Assurance Program, and were implemented as specified, during work associated with the addition of oil to safety

-related control building chiller HVK-CHL1A.

These activities constitute completion of one quality control sample, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors review ed three risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:

July 7, 2017, yellow risk condition during Division I residual heat removal surveillance testing July 12, 2017, green risk condition during preventative maintenance on standby service water cooling tower fan breakers August 14, 2017, yellow risk condition during Division II residual heat removal surveillance testing The inspectors verified that these risk assessmen ts were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessment s and verified that the licensee implemented appropriate risk management actions based on the result s of the assessment s.

The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.

These activities constitute completion of three maintenance risk assessments and emergent work control inspection sample s, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors review ed four operability determination s that the licensee performed for degraded or nonconforming SSCs: July 10, 2017, operability determination of missed surveillance test associated with the Division I ENB battery (C R-RBS-2017-04462) July 10, 2017, operability determination of foreign material intrusion in the standby service water cooling tower basin (CR-RBS-2017-05273) August 1, 2017, operability determination of Division II standby gas treatment system relay EHS

-MCC2D-2B-74 failed to actuate (CR

-RBS-2017-05678) August 30, 2017, operability determination of scram discharge volume level transmitters after found high out of calibration during system functional test (CR-RBS-2017-06031) The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.

These activities constitute completion of four operability and functionality review samples, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

On August 3, 2017, the inspectors reviewed a permanent plant modification of the Division II uninterruptible power supply (ENB

-INV01B1) system output frequency meter.

The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post

-modification testing was adequate to establish the operability of the SSC as modified.

These activities constitute completion of one permanent plant modification inspection sample, as defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Sco pe The inspectors reviewed five post-maintenance testing activities that affected risk-significant SSCs:

July 14, 2017, work order (WO)00437814, "Division I Battery ENB

-BAT01A Post Maintenance Test," following replacement of Division I battery ENB

-BAT01A July 27, 2017, WO 00404398-02, "Instrument Air Compressor 2C Post Maintenance Test," following maintenance on instrument air compressor 2C August 28, 2017, WO 52713780, "E22-PC003 - Change Oil and Lubricate the Pump Coupling," retest of E 22-PC003 high pressure core spray line fill pump following oil replacement and lubrication September 2, 2017, WO 00478604, "LSV

-C3A - Perform Operability Test," following cleaning and inspection of compressor strainers, check valves, and orifices September 15, 2017, WO 52652445, "GTS

-FS24B - Calibrate Standby Gas Treatment Exhaust Fan B," operability run of standby gas treatment fan B following calibration of low

-flow switch The inspectors reviewed licensing

- and design

-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post

-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constitute completion o f five post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observe d three risk-significant surveillance test s and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:

In-service tests:

July 7, 2017, STP-205-6301, "LPCS Pump and Valve Operability Test," performed on July 6, 2017 Other surveillance tests:

August 10, 2017, STP 6310, "Standby Liquid Control Pump and Valve Operability Test," performed on July 26, 2017 August 18, 2017, STP 1302, "E22-S001BAT Quarterly Surveillance," performed on August 16, 2017

The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the tests satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constitute completion of three surveillance testing inspection sample s, as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

Cornerstone:

Emergency Preparedness

1EP6 Drill Evaluation

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on September 12, 2017, to verify the adequacy and capability of the licensee's assessment of drill performance. The inspectors reviewed the drill scenario, observed the drill from the technical support center and the emergency operations facili ty, and attended the post

-drill critique. The inspectors verified that the licensee's emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post

-drill critique and entered into the corrective action program for resolution.

These activities constitute completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

.2 Training Evolution Observation

a. Inspection Scope

On July 25, 2017, the inspectors observed simulator

-based licensed operator requalification training that included implementation of the licensee's emergency plan. The inspectors verified that the licensee's emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the evaluators and entered into the corrective action program for resolution.

These activities constitute completion of one training observation sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS5 Radiation Monitoring Instrumentation

a. Inspection Scope

The inspectors evaluated the accuracy and operability of the radiation monitoring equipment used by the licensee to monitor areas, materials, and workers to ensure a radiologically safe work environment. This evaluation included equipment used to monitor radiological conditions related to normal plant operations, anticipated operational occurrences, and conditions resulting from postulated accidents.

The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance associated with radiation monitoring instrumentation, as described below: The inspectors performed walkdowns and observations of selected plant radiation monitoring equipment and instrumentation, including portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors. The inspectors assessed material condition and operability, evaluated positioning of instruments relative to the radiation sources or areas they were intended to monitor, and verified performance of source checks and calibrations

. The inspectors evaluated the calibration and testing program, including laboratory instrumentation, whole body counters, post

-accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors, portable survey instruments, area radiation monitors, electronic dosimetry, air samplers, and continuous air monitors.

The inspectors assessed problem identification and resolution for radiation monitoring instrumentation.

The inspectors reviewed audits, self

-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the three required radiation monitoring instrumentation samples, as defined in Inspection Procedure 71124.05.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

a. Inspection Scope

The inspectors evaluated whether the licensee maintained gaseous and liquid effluent processing systems and properly mitigated, monitored, and evaluated radiological discharges with respect to public exposure. The inspectors verified that abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, were controlled in accordance with the applicable regulatory requirements and licensee procedures. The inspectors verified that the licensee's quality control program ensured radioactive effluent sampling and analysis adequately quantified and evaluated discharges of radioactive materials. The inspectors verified the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:

During walkdowns and observations of selected portions of the radioactive gaseous and liquid effluent equipment, the inspectors evaluated routine processing and discharge of effluents, including sample collection and analysis

. The inspectors observed equipment configuration and flow paths of selected gaseous and liquid discharge system components

, effluent monitoring systems, filtered ventilation system material condition, and significant changes to effluent release points.

Calibration and testing program for process and effluent monitors, including National Institute of Standards and Technology traceability of sources

, primary and secondary calibration data, channel calibrations, setpoint determination bases, and surveillance test results

. Sampling and analysis controls used to ensure representative sampling and appropriate compensatory sampling. Reviews included results of the inter-laboratory comparison program

. Instrumentation and equipment, including effluent flow measuring instruments, air cleaning systems, and post

-accident effluent monitoring instruments.

Dose calculations for effluent releases. The inspectors reviewed a selection of radioactive liquid and gaseous waste discharge permits and abnormal gaseous or liquid tank discharges, and verified the projected doses were accurate. The inspectors also reviewed 10 CFR Part 61 analyses and methods used to determine which isotopes were included in the source term. The inspectors reviewed land use census results, offsite dose calculation manual changes, and significant changes in reported dose values from previous years.

Problem identification and resolution for radioactive gaseous and liquid effluent treatment. The inspectors reviewed audits, self

-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the six required radioactive gaseous and liquid effluent treatment samples, as defined in Inspection Procedure 71124.06.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program

a. Inspection Scope

The inspectors evaluated whether the licensee's radiological environmental monitoring program quantified the impact of radioactive effluent releases to the environment and sufficiently validate d the integrity of the radioactive gaseous and liquid effluent release program. The inspectors also verified that the licensee continued to implement the voluntary Nuclear Energy Institute/Industry Ground Water Protection Initiative. The inspectors reviewed or observed the following items:

The inspectors observed selected air sampling and dosimeter monitoring stations, sampler station modifications, and the collection and preparation of environmental samples

. The inspectors reviewed calibration and maintenance records for selected air samplers

, composite water samplers, and environmental sample radiation measurement instrumentation, and inter-laboratory compariso n program results

. The inspectors reviewed selected events documented in the annual environmental monitoring report and significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census. The inspectors evaluated the operability, calibration, and maintenance of meteorological instruments and assessed the meteorological dispersion and deposition factors

. The inspectors verified the licensee had implemented a sampling and monitoring program sufficient to detect leakage from structures, systems, or components with credible mechanism for licensed material to reach groundwater and reviewed changes to the licensee's written program for identifying and controlling contaminated spills/leaks to groundwater

. Groundwater protection initiative implementation, including assessment of groundwater monitoring results

, identified leakage or spill events and entries made into 10 CFR 50.75 (g) records

, licensee evaluations of the extent of the contamination and the radiological source term

, and reports of events associated with spills, leaks, and groundwater monitoring results.

Problem identification and resolution for the radiological environmental monitoring program. The inspectors reviewed audits, self

-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the three required radiological environmental monitoring program samples, as defined in Inspection Procedure 71124.07.

b. Findings

No findings were identified.

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation

a. Inspection Scope

The inspectors evaluated the effectiveness of the licensee's programs for processing, handling, storage, and transportation of radioactive material. The inspectors interviewed licensee personnel and reviewed the following items:

Radioactive material storage, including waste storage areas including containe r labeling/marking and monitoring containers for deformation or signs of waste decomposition.

Radioactive waste system, including walkdowns of the accessible portions of the radioactive waste processing systems and handling equipment. The inspectors also reviewed or observed changes made to the radioactive waste processing systems, methods for dewatering and waste stabilization, waste stream mixing methodology, and waste processing equipment that was not operational or abandoned in place

. Waste characterization and classification, including radio

-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult

-to-measure radionuclides, and processes for waste classification including use of scaling factors and 10 CFR Part 61 analyses.

Shipment preparation, including packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifests.

Shipping records for low specific activity (

LSA) I, II, III; surface contaminated objects (SCO) I, II; Type A, or Type B radioactive material or radioactive waste shipments.

Problem identification and resolution for radioactive solid waste processing and radioactive material handling, storage, and transportation. The inspectors reviewed audits, self

-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the six required radioactive solid waste processing and radioactive material handling, storage, and transportation samples, as defined in Inspection Procedure 71124.08.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Mitigating Systems Performance Index: Heat Removal Systems (MS08)

a. Inspection Scope

The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for heat removal systems, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index: Residual Heat Removal Systems (MS09)

a. Inspection Scope

The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99

-02, "Regulatory Assessment Performance Indicato r Guideline," Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for residual heat removal systems, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index: Cooling Water Support Systems (MS10)

a. Inspection Scope

The inspectors reviewed the licensee's mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99

-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for cooling water support systems, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensee's corrective action program and periodically attended the licensee's condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensee's problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Annual Follow

-up of Selected Issues

a. Inspection Scope

The inspectors selecte d one issue for an in

-depth follow

-up: On May 21, 2017, following completion of a Division III emergency diesel generator (EDG) 24

-hour run performed by operations department personnel, mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. The technician who performed the evolution discovered the error the following the day while updating the lubrication accountability log. Mobilgard 412 oil was added by the technicians instead of the required Mobilgard 450 oil. The addition of the 20 gallons of Mobilgard 412 to the Division III EDG resulted in a zinc concentration of 17.3 ppm in the overall oil volume. The Division III EDG vendor manual states that the allowable concentration for zinc in the lube oil is 0

-10 ppm. Since the addition of the Mobilgard 412 oil resulted in a zinc concentration in excess of the vendor recommendation, the

station determined that the Division III EDG could not be relied upon to perform its safety function in all conditions and declared it inoperable. The Division III EDG was inoperable for approximately three days while the station pumped out the lube oil and refilled the fuel oil storage tank. The station's adverse conditional analysis determined that technicians added the wrong type of oil because they did not stop and validate the correct oil per procedure GMP-0015, "Lubrication Procedure," Revision 14, as required, but assumed the oil staged in the mechanical shop was the correct oil. GMP

-0015, Step 8.1.1, required the technicians to review the lubrication accountability log and verify the correct oil prior to adding it to the EDG.

The inspectors assessed the licensee's completed corrective actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition.

These activities constitute completion of one annual follow

-up sample, as defined in Inspection Procedure 71152.

b. Findings

A licensee

-identified violation associated with this inspection sample is documented in Section

4OA7 of this report.

4OA3 Follow-up of Events and Notices of Enforcement Discreti

on (71153) (Closed) Licensee Event Report (LER) 05000458/2017 00, "Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting

"

a. Inspection Scope

On March 10, 2017, during power ascension testing conducted in the startup after a refueling outage, the reactor operator manually inserted a reactor scram in response to an abnormal increase in steam pressure. Approximately 45 minutes before the scram occurred, a steam leak developed in a tee connection associated with the newly-installed turbine digital electro

-hydraulic control (EHC) system. To stop the steam leak, the licensee isolated a piping line that fed two of the three pressure instruments that the digital EHC system used to control turbine valve positions. Given the presence of the leak, those two instruments were already reading pressure erratically, and the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two affected instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading roughly consistent with each other, the system treats their output as the true output. Consequently, with both of the affected instruments sensing pressure at roughly zero pounds, the digital EHC system began to shut the turbine control valves. The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling them based on the two pressure instruments that had been isolated and that were both reading roughly zero pounds. Power was below the 23.8 percent level

, above which turbine bypass valves are required to be operable by technical specifications.

The steam leak was the result of improper installation of the tee connection.

The step that directed the installation of the connection into the transmitter tubing line was not properly carried out and was not sufficiently verified in accordance with its designation as a quality control hold point. When contract maintenance personnel in charge of the installation observed leakage from the connection during power ascension, they tightened down on its compression fitting without notifying the control room or obtaining appropriate permission. This action caused the fitting to dislodge, significantly worsening the leak

. The inspectors reviewed the LER associated with the event and determined that the report adequately documented the summary of the event, including the cause of the event and potential safety consequences. The inspectors documented a finding for the licensee's failure to properly complete steps of the work order instruction during the installation and inspection of the tee connection.

LER 05000458/2017-003-00 is closed.

b. Findings

Introduction.

The inspectors reviewed a Green, self-revealed finding for the licensee's failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram.

Description.

On March 10, 2017, a steam leak developed in a tee compression fitting associated with the newly

-installed turbine digital EHC system. To stop the steam leak, the licensee isolated a piping line that fed two of three pressure instruments that the digital EHC system used to control turbine valve positions. Prior to this action, the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading consistently with each other, the system treats their output as the true output. Consequently, with both of the affected instruments seeing pressure at roughly zero pounds, the digital EHC system began to close the turbine control valves.

The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling their position based on the two pressure instruments that had been isolated and that were reading roughly zero pounds. Power was below the 23.8 percent level above which turbine bypass valves are required to be operable by technical specifications.

The steam leak was a result of improper installation of a tee connection in the line that fed the two affected pressure transmitters. Work order 00438386, Task 24, Step 4.3.8 provided instruction for maintenance personnel to install the tee connection into the transmitter tubing line. This action was not properly carried out, with the tee connection incorrectly fitted up to its compression fitting. An adequate seal was not formed, and therefore, when the line was pressurized, a leak developed. The step was identified in the procedure as a quality control hold point, and therefore the deficient craftsmanship should have been identified by supervisor inspection. However, the Quality Control supervisor failed to observe the satisfactory completion of the step, contrary to site expectations. When maintenance personnel identified leakage from the compression fitting during power ascension, they tightened down on the fitting without obtaining appropriate permission from the control room. This action caused the fitting to dislodge, making the leak significantly worse.

Analysis.

The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee's failure to properly install the tee connection caused a steam leak that led to a reactor scram. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, "Initiating Events Screening Questions." The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross

-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5].

Enforcement

. This finding does not involve an enforcement action because no regulatory requirement s were violated

. The licensee documented th is finding in their corrective action program as Condition Report CR-RBS-2017-02405. This issue is being characterized as finding FIN 05000458/2017003-02, "Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting

." These activities constitute completion of one event follow-up sample, as defined in Inspection Procedure 71153.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On July 28, 2017, the inspectors presented the radiation safety inspection results to Mr. M. Chase, Director of Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On August 25, 2017, the inspectors presented the radiation safety inspection results to Mr. J. Reynolds, Operations Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On September 21, 2017, the inspector presented the triennial heat sink performance inspection results to Mr. M. Chase, Director, Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On October 11, 2017, the inspectors presented the integrated inspection results to Mr. W. Maguire, Site Vice President

, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

4OA7 Licensee-Identified Violations

The following licensee

-identified violation of NRC requirements was determined to be of very low safety significance (Green) and meets the NRC Enforcement Policy criteria for being dispositioned as a non-cited violation:

Technical Specification 5.4, "Procedures," requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.a of Appendix A to Regulatory Guide 1.33 require s that maintenance that can affect performance of safety

-related equipment be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, the station did not properly preplan and perform maintenance that can affect the performance of safety

-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Specifically, on May 21, 2017, following completion of a 24

-hour surveillance test run of the Division III emergency diesel generator (EDG), mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. This error resulted in the inoperability of the Division III EDG for approximately three days while the incorrect oil was pumped out of the associated fuel oil storage tank and subsequently refilled. This finding was determined to be of very low safety significance (Green) because the finding did not represent an actual loss of function of one or more trains of safety

-related equipment for greater than its technical specification allowed outage time. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2017-04128.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Askew, Manager, Supply Chain
D. Burnett, Director, Emergency Planning, Entergy South
S. Carter, Superintendent, Instruments and Controls
M. Chase, Director, Regulatory & Performance Improvement
B. Cole, Corporate Radiation

Protection

R. Conner, Manager, Nuclear Oversight
R. Cook, Manager, Security
K. Crissman, Senior Manager, Production
D. Durocher, Supervisor, Code Program
J. Engel, Superintendent, Radiological Operations, Radiation Protection
B. Ford, Senior Manager, Fleet Regulatory Assurance
C. Foster, System Engineer
D. Guess, Engineer
J. Henderson, Manager, Systems & Components Engineering
R. Hilliard, Supervisor, Chemistry
K. Huffstatler, Senior Licensing Specialist, Regulatory Assurance
V. Huffstatler, Senior Health Physicist/Chemistry Specialist, Chemistry
J. Hurst, Manager, Emergency Preparedness
D. Jarnagin, Supervisor, Instruments and Controls
B. Johns, Licensing Specialist, Regulatory Assurance
C. King, Superintendent, Maintenance Support
G. King, Specialist, Radiation Protection
R. Leasure, Superintendent, Radiation Protection
P. Lucky, Manager, Performance Improvement
W. Maguire, Site Vice President
J. McCoy, Assistant Manager, Operations
G. Mermigas, Engineer
J. O'Connor, Senior Manager, Maintenance
S. Peterkin, Manager, Radiation Protection
M. Ponzo, Manager, Chemistry
M. Reeves, Supervisor, Radiation Operations
J. Rogers, Supervisor, Engineering
T. Venable, Manager, Operations
M. Runion, Senior Manager, Site Projects and Maintenance Services
D. Sandlin, Manager, Design & Program Engineering
T. Schenk, Manager, Regulatory Assurance
W. Spell, Senior Health Physicist/Chemistry Specialist, Chemistry
K. Stupak, Manager, Training
S. Vazquez, Director, Engineering
S. Vercelli, General Manager, Plant Operations
J. Vukovics, Supervisor, Reactor Engineering
J. Wilson, Manager, Chemistry

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000458/2017003

-01 NCV Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory Analysis

(Section 1R07)

05000458/201700

3-02 FIN Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting

(Section 4OA3)

Closed

05000458/
2017-003-00 LER Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting (Section 4OA3)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Calculations/Specifications Number Title Revision/Date 8.3.1.32 Design Basis Flood

- River Bend Station (West Creek and Grants Bayou)

8.3.1.34 PMP in Site Area (Assuming no Berm Around Excavation)
8.3.1.37 Determination of Water Surface Elevations in Grants Bayou and West Creek Near Plant Site for PMF and 25

-Year Flood + SSE

CF8503290006
Peelle Design Calculation for Pressuretight and Watertight Doors March 15, 1985
CI8412200004

Calculations

Design & Stress Analysis for Watertight & Pressuretight Doors December 17, 1984
RBS-210.460 Specification for Missile Protected Doors
RBS-210.461 Specification for Pressuretight Doors, Watertight Doors, and Special Doors
RBS-210.462 Specification for Pressuretight and Watertight Doors

Condition Reports

(CRs)

CR-RBS-2016-06807
CR-RBS-2017-00399
CR-RBS-2017-04694 CR-RBS-2017-05292

Section 1R04: Equipment Alignment

Condition Reports

(CRs)

CR-RBS-2015-05695
CR-RBS-2015-06913
CR-RBS-2015-07827
CR-RBS-2016-02450
CR-RBS-2016-03137
CR-RBS-2016-03870
CR-RBS-2016-04083
CR-RBS-2016-05088
CR-RBS-2016-05560
CR-RBS-2016-07064
CR-RBS-2017-00886
CR-RBS-2017-00891
CR-RBS-2017-01783
CR-RBS-2017-03315
CR-RBS-2017-03805
CR-RBS-2017-04163
CR-RBS-2017-04635
CR-RBS-2017-04727
CR-RBS-2017-05292
CR-RBS-2017-05811
CR-RBS-2017-06831
CR-RBS-2017-06832
CR-RBS-2017-06841

Procedures

Number Title Revision
SOP-0042 Standby Service Water System
043
SOP-0049 125 VDC System (SYS #305)
038
SOP-0066 Control Building HVAC Chilled Water System
336

Work Orders

(WOs)

WO 00408444
WO 00458738
WO 00476553
WO 00479796
WO 00479797
WO 00479800

Section 1R05: Fire Protection

Calculation Number Title Revision G13.18.12.2

-022 River Bend Station Combustible Loading

005

Condition Reports

(CRs)

CR-RBS-2017-00491
CR-RBS-2017-03519
CR-RBS-2017-04226

Procedure

s Number Title Revision

CB-116-133 Battery 1A Room Fire Area C

-18 4

CB-116-134 Battery 1B Room Fire Area C

-19 4

CB-116-135 ENB Inverter Charger B Room Fire Area C

-19 4

SP-118-451 Standby Cooling Tower Pump B Room Fire Area
PH-2/Z-1 3

Section 1R06: Flood Protection Measures

Calculations

Number Title Revision G13.18.12.3

-15-0 Internal Flooding Screening Analysis

G13.18.12.3

-16-0 Quantitative Analysis of Internal Flooding

PN-317 Max Flood Elevations for Moderate Energy Line Cracks in Cat I Structures

Section 1R07: Heat Sink Performance

Calculation

s Number Title Revision 228.800-PX-562 WATHAM ANAL With Trapped Air in SSW System

-A-Header & LONSW/LORPCCW & LOOP Events

228.800-PX-567 Segment Force Factor for the Components Piping of the SSW System
G13.18.2.
0*072 E12-EB001A/B/C/D Maximum Tube Throughwall Degradation Limit
G13.18.4.0*046
Standby Service Water Pump Capacity Verification without Flow through Drywell Unit Coolers, Including 5% Pumps Degradation
G13.18.14.0*166
Heat Rejected by Emergency Diesel Generator Divisions I and II to Cooling Water
PM-194 Standby Cooling Tower Performance and Evaporation Losses without Drywell Unit Coolers
PM-199 Standby Cooling Tower Basin Volume

Condition Reports

(CRs)

Reviewed
CR-RBS-1999-00137
CR-RBS-2003-01240
CR-RBS-2009-05083
CR-RBS-2009-05399
CR-RBS-2015-07358
CR-RBS-2016-00078
CR-RBS-2016-01168
CR-RBS-2016-02077
CR-RBS-2016-04289
CR-RBS-2017-02330
CR-RBS-2017-02798
CR-RBS-2017-03705
CR-RBS-2017-04086
CR-RBS-2017-04275
CR-RBS-2017-04674
CR-RBS-2017-06488
CR-RBS-2017-06686

Condition Reports

(CRs) Issued

CR-RBS-2017-06830
CR-RBS-2017-06856
CR-RBS-2017-06858
CR-RBS-2017-06859
CR-RBS-2017-06998

Miscellaneous

Number Title Revision/Date
204 - Residual Heat Removal

- LPCI Q1-2017

309 and 405 - Standby Emergency Diesel Generators

- Division I, II, & III and HVAC

Q1-2017
Standby Diesel Generator Division I & II
Diesel Generator Building Ventilation System Design Criteria System Numbers 309 & 405
221.432-000-019 RHR Heat Exchanger Calculated Performance January 10, 1990
244.700 Specification for Standby Diesel Generator Systems April 12, 1985
244.700-041-018 Jacket Water Cooler 74039

-109 September 1, 1994

ER-EB-1999-0592 Replacement Filters for Auxiliary and Containment Unit Coolers
ER-RB-1996-0028 Revise Torqueing Procedure for RHR Heat Exchanger Head from 3224.110

-000-031 Requirements

P-15854 Continue to Test RHR Heat Exchangers in Accordance with
GL 89-13 Supplement 1, Section IID and IIIF October 21, 1998
P-8340 GSU has Developed Inspection Criteria and Requirements which Provide for Scheduled Inspections and Specific Instructions for Maintenance of Service Water Heat Exchangers and Unit Coolers

-

CMP-9267 Issued to Implement February 2, 1990

Procedure

s Number Title Revision

AOP-0016 Loss of Standby Service Water
CMP-9267 Heat Exchanger Repairs
CSP-0006 Chemistry Surveillance and Scheduling System
EN-DC-159 System and Component Monitoring
EN-DC-184 NRC Generic Letter 89

-13 Service Water Program

EN-DC-316 Heat Exchanger Performance and Condition Monitoring
8,9
OSP-0066 Extensive Damage Mitigation Procedure
SEP-SW-RBS-001 RBS GL89-13 Service Water Heat Exchanger Program 0

Procedure

s Number Title Revision

STP-403-0301 Containment Unit Cooler HVR

-UC1A Flow Rate Verification Thermal Performance Analyses Number Title Date

RHR Heat Exchangers E12

-EB001A and E12

-EB001C Heat Transfer Capacity Verification, March 15, 2005 April 22, 2005

RHR Heat Exchangers E12

-EB001A and E12

-EB001C Heat Transfer Capacity Verification

, September 30,

2003 December 19, 2003
RBS-EP-15-00018 RHR Heat Exchangers E12

-EB001A and E12

-EB001C Heat Transfer Capacity Verification, January 5, 2013

November 23, 2015
Vendor Documents Number Title Revision/Date 3244.700-041-082B Special and General Torque Tables,
SIM-64 Revision 301
NU9-M62 Operating and Maintenance Manual January 14, 1986
VTD-T193-0100 Thermxchanger Manual for Installation, Operation & Maintenance of Shell & Tube Heat Exchangers

Work Orders

(WOs)

WO 00099363
WO 00174873
WO 00174875
WO 00361644 WO 00470689
WO 51087021
WO 51695027
WO 52499665
WO 52556202
WO 52654748
WO 52671655
WO 52687800
WO 52703609

Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance

Condition Reports

(CRs)

CR-RBS-2017-05934
CR-RBS-2017-06122 CR-RBS-2017-06139

Section 1R12: Maintenance Effectiveness

Condition Reports

(CRs)

CR-RBS-2016-02450
CR-RBS-2016-06408
CR-RBS-2016-06691
CR-RBS-2016-07181
CR-RBS-2016-07227
CR-RBS-2016-07409
CR-RBS-2016-08136
CR-RBS-2016-08562
CR-RBS-2017-00043
CR-RBS-2017-00323
CR-RBS-2017-00373
CR-RBS-2017-00629
CR-RBS-2017-00645
CR-RBS-2017-00713
CR-RBS-2017-00714
CR-RBS-2017-00886
CR-RBS-2017-00891
CR-RBS-2017-00958
CR-RBS-2017-02409
CR-RBS-2017-02677
CR-RBS-2017-04128
CR-RBS-2017-04470
CR-RBS-2017-05201
CR-RBS-2017-05908

Procedures

Number Title Revision
ADM-0085 Periodic Maintenance Program
EN-DC-203 Maintenance Rule Program
EN-DC-204 Maintenance Rule Scope and Basis
EN-DC-205 Maintenance Rule Monitoring
EN-DC-206 Maintenance Rule (A)(1) Process
EN-LI-118 Cause Evaluation Process
EN-WM-105 Planning 18
Work Order (WO)
WO 50032677

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

Number Title Revision
ADM-0096 Risk Management Program Implementation and On-line Maintenance Risk Assessment
25
EN-WM-104 On Line Risk Assessment

Section 1R15: Operability Determinations and Functionality Assessments

Condition Reports

(CRs)

CR-RBS-1997-01293
CR-RBS-1997-01314
CR-RBS-2016-07675
CR-RBS-2017-06075
Engineering Request Number Title Revision
ER-RB-2001-00336 Standby Cooling Tower Basin Cleaning Dive Effort

Miscellaneous

Number Title Revision
IEEE-308-2012 IEEE Standard Criteria for Class 1E Power Systems for Nuclear Power Generating Stations
IEEE-450-1975 IEEE Recommended Practice for Maintenance, Testing, and Replacement of Large Lead Storage Batteries for Generating Stations and Substations
IEEE-485-1997 IEEE Recommended Practice for Sizing Lead

-Acid Batteries for Stationary Applications

QC-RBS-00036504 QC Inspection for
PO 10479021

Procedures

Number Title Revision
ADM-0015 Station Surveillance Test Program
EN-LI-108 Event Notification and Reporting
EN-MA-125 Troubleshooting Control of Maintenance Activities 20
EN-OP-104 Operability Determination Process
STP-203-1702 E22-S001BAT Performance Discharge Test
STP-305-1606
ENB-BAT01A Service Discharge Test
STP-305-1700
ENB-BAT01A Performance Discharge Test
STP-305-1701
ENB-BAT01B Performance Discharge Test

Work Orders

(WOs)

WO 00480183
WO 52471441
WO 52471442
WO 52487137
WO 52487622
WO 52628405
WO 52628547
WO 52639832
WO 52647337
WO 52647338

Section 1R18: Plant Modifications

Condition Report (CR)

CR-RBS-2015-03808

Drawings

Number Title Revision 0244.514-000-005 Schematic 20KVA Inverter 100

-140VDC 120VAC 1 60HZ ENB-INV01A1/ENB

-INV01B1 0 0244.514-000-006 Schematic

20KVA Inverter
100-140VDC 120VAC 10 60HZ
ENB-INV01A1/ENB-INV01B1 0 0244.514-000-031 Schematic Diagram 20KVA Inverter 100-140VDC 120 VAC 0 0244.514-000-032 Schematic Diagram 20KVA Inverter 100

-140VDC 120 VAC 0

Miscellaneous

Number Title Revision 4244.514-000-004 Engineering Report Seismic Qualification Evaluation of Frequency Meter Modification
S250-0127 Ametek FMR2/1 Weschler Instrument Meter
EC 65512 Engineering Change:
FMR
Model Replacement for
ENB-INV01B1 0

Procedure

Number Title Revision
SOP-0048 120 VAC System
28
Work Order (WO)
WO 00414828

Section 1R19:

Post

-Maintenance Testing

Condition Report (CR)

CR-RBS-2017-03595

Drawings

Number Title Revision
EM-003H Arrangement Instrument Air and Service Compressor Building
FSK-12-01X Flow Diagram Instrument Air System
PID-12-01G Engineering P&I Diagram System 122 Instrument Air 302

Miscellaneous

Number Title Revision 3252.15-404-001A Instruction Book for Air Compressors
2

Procedures

Number Title Revision
EN-WM-107 Post Maintenance Testing
005
STP-000-0201 Monthly Operating Log
311
STP-208-6301 Div I MSIV Leakage Control Quarterly Valve Operability Test
008
STP-208-6607 Div I MSIV Leakage Control Refuel Position Indication Verification Test
2B
STP-257-0202 Standby Gas Treatment System Filter Train B Monthly Operability Test
015
STP-305-1300
ENB-BAT01A Quarterly Surveillance 28
STP-305-1600
ENB-BAT01A Inspection
303
STP-305-1606
ENB-BAT01A Service Discharge Test

Work Orders

(WOs)

WO 00404398
WO 00462213
WO 00478238
WO 00478604
WO 52639832
WO 52652445
WO 52720726
WO 52732341
WO 52776567

Section 1R22: Surveillance Testing

Condition Reports

(CRs)

CR-RBS-2008-06244
CR-RBS-2012-06631
CR-RBS-2017-05271
CR-RBS-2017-06022

Drawings

Number Title Revision
PID-04-03C Engineering P&I Diagram System
106 Condensate Makeup Storage and Transfer System
PID-27-16A Engineering P&I Diagram System
201 Standby Liquid Control System

Miscellaneous

Number Title Revision EC-0000032582
Establish Baseline Reference Valued and Acceptance Limits for IST Pumps C
41-PC001A and C41-PC001B 2 Year Comprehensive Tests
SEP-RBS-IST-1 RBS Inservice Testing Bases Document
SEP-RBS-IST-2 RBS Inservice Testing Plan

Procedure

s Number Title Revision

ADM-0015 Station Surveillance Test Program
SOP-0028 Standby Liquid Control System
STP-201-0201 SLC Valve Continuity and Valve Position Check
STP-205-6301 LPCS Pump and Valve Operability Test
STP-201-6310 SLC Pump and Valve Operability Test
311
STP-203-1302 E22-S001BAT Quarterly Surveillance

Work Orders

(WOs)

WO 52752999
WO 52756898
WO 52756900
WO 52766017

Section 1EP6: Drill Evaluation

Miscellaneous

Number Title Revision
RDRL-EP-0803EX Site Drill Scenario
RDRL-EP-FD04 Focused Drill Scenario

Section 2RS5: Radiation Monitoring Instrumentation

Audits and Self

-Assessments Number Title Date

LO-RLO-2017-0016 Self-Assessment:
Pre-NRC Radiation Monitoring Instrumentation (NRC IP 71124.05)
May 24, 2017

Condition Reports

(CRs)

CR-RBS-2015-08749
CR-RBS-2015-08881
CR-RBS-2016-00195
CR-RBS-2016-07951
CR-RBS-2016-08138
CR-RBS-2016-08593
CR-RBS-2017-00982
CR-RBS-2017-02906
CR-RBS-2017-03210
CR-RBS-2017-03334
CR-RBS-2017-04676
CR-RBS-2017-07545

Miscellaneous

Number Title Date
Evaluation of the Thermo PM

-7 for use as a Passive Monitor at River Bend Nuclear Plant December 13, 2011

2017 Dry Active Waste Scaling Factors April 11, 2017
28-8C Gamma Calibration Verifications Data Sheet April 3, 2017
78-2M Gamma Calibration Verifications Data Sheet August 30, 2016
Portable Radiation Instrument Calibration Records Number Title Date 2409 Certificate of Calibration for Eberline ASP

-1 (Ludlum Measurements, Inc.)

June 9, 2017
6011 Calibration Data Sheet for BC

-4 Scaler (Beta)

April 12, 2017
8909 Calibration Data Sheet for LM

-177 Frisker January 24, 2017

CHP-C-012 Calibration Data Sheet for iSolo Scal er March 23, 2017
CHP-DR-525 Calibration Data Sheet for Ludlum Model 9

-3 May 17, 2017

CHP-TEL022 Calibration Data Sheet for WR Telepole December 16, 2016
PM7-395 Calibration Data Sheet for Eberline PM

-7 January 6, 2017

Procedures

Number Title Revision
EN-RP-106-1 Radiological Survey Guidelines
EN-RP-108 Radiation Protection Posting
EN-RP-301 Radiation Protection Instrument Control
EN-RP-317-03 Operation and Calibration of Sources and Laboratory Standard Instruments
MCP-4201 DRMS Low Range Area Monitor Calibration
8, 9
MCP-4203 DRMS High Range Area Monitor Calibration
301
RPP-0010 Operation and Verification of the Shepherd Model 89 Gamma Calibrator
301

Procedures

Number Title Revision
RPP-0036 Calibration of DRMS Area Monitors and Determination of Alert and High Alarm Setpoint 302
RPP-0118 Calibration and Maintenance of Portable Radiological Air Samplers
STP-511-4201 Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test
25, 26
STP-511-4203 Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test
26, 27
STP-511-4209
RMS-Control Room Fresh Air System Radiation Monitor Local Intake Channel Calibration RMS

-RE13A 304

STP-511-4249
RMS-Primary Containment Area Radiation Monitor, Channel Calibration RMS

-RE16A 8, 9, 301, 302, 306

Radiation Monitoring System Calibration Records Number Title Date
WO 52427312
RMS-RE192 - Clean, Check Calibration, and Functionally Test Fuel Building Refueling Platform Radiation Monitor June 24, 2014
WO 52548887
STP-511-4209:
RMS-Control Room Fresh Air System Radiation Monitor Local Intake Channel Calibration RMS

-RE13A June 2, 2016

WO 52599307
STP-511-4201: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test November 1, 2016
WO 52628624
STP-511-4249: RMS

-Primary Containment Area Radiation Monitor, Channel Calibration RMS

-RE16A May 3, 2017

WO 52737835
STP-511-4201: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test April 11, 2017
WO 52737836
STP-511-4203: Main Steam Line Radiation High High Channel Calibration and Logic System Functional Test April 11, 2017
Stationary Radiation Instrument Calibration Records Number Title Date 11 Calibration Data Sheet for Eberline PM

-7 January 12, 2017

Stationary Radiation Instrument Calibration Records Number Title Date 572 Calibration Data Sheet for PCM 1B Personnel Contamination Monitor September 8, 2016
1011-060 Calibration Data Sheet for CRONOS Contamination Monitor January 31, 2017
11719 Calibration Data Sheet for Small Tool Monitor April 27, 2017
58692 Calibration Data Sheet for GEM

-5 Portal Monitor October 26, 2016

Fast Scan Calibration of the Canberra FastScan WBC System January 18, 2017

Section 2RS6: Radioactive Gaseous and Liquid Effluent Treatment

Audits and Self

-Assessments Number Title Date

LO-RLO-2017-0025 Radioactive Gaseous and Liquid Effluent Treatment and Radiological Environmental Monitoring Program June 24, 2017

Condition Reports

(CRs)

CR-RBS-2015-08948
CR-RBS-2015-09149
CR-RBS-2016-02260
CR-RBS-2016-05180
CR-RBS-2016-06545
CR-RBS-2016-08014
CR-RBS-2017-04312
CR-RBS-2017-05005
CR-RBS-2017-05479
CR-RBS-2017-05590

Miscellaneous

Number Title Date
2015 Annual Radioactive Effluent Release Report May 1, 2016
2016 Annual Radioactive Effluent Release Report May 1, 2017
Radiological Gaseous and Liquid Effluent Discharge Packages Selected Records
2016 and 2017
2510628
STP-402-3602, Inservice Testing of Division II Control Room March 9, 2016
2535118
STP-511-4215, RMS

-Main Plant Exhaust Duct Noble Gas Activity Channel Calibration

RMS-RE126 June 9, 2015
2597745
STP-406-3602, Inservice Testing of Division II Fuel Building January 26, 2017
2644279
STP-257-3602, Inservice Testing of Division II Standby Gas July 24, 2017

Miscellaneous

Number Title Date
52644521
STP-511-4214, RMS

-Main Plant Exhaust Duct Noble Gas Activity Channel Calibration

RMS-RE125 July 13, 2017
2661227
STP-511-5217, RMS

-Radwaste BLDG Ventilation Exhaust Duct Noble Gas Activity Monitor Channel Calibration RMS

-RE6B June 24, 2017

25351117
STP-511-4280, RMS

-Liquid Radwaste Effluent Line Radiation Monitor Channel Calibration

RMS-RE107 March 16, 2016
26132218
STP-402-3601, Inservice Testing of Division I Control Room January 3, 2017

Procedures

Number Title Revision
COP-0046 Sampling Gaseous Effluents Via the Wide Range Gas Monitors
COP-0308 Operation of the Chemistry and Environmental Gamma Ray Spectroscopy Systems Using Apex
COP-0619 Gamma Isotopic Analysis Sample Preparation
COP-0813 Radioactive Liquid Discharge Permit Process
CSP-0110 Radioactive Liquid Effluent Batch Discharge
SOP-0113 Liquid Radwaste Processing/Recovery Sample Tank System

Section 2RS7: Radiological Environmental Monitoring Program

Audits, Self

-Assessments, and Surveillances Number Title Date

LO-RLO-2017-00022 Self-Assessment

- Compliance with EN

-CY-102_Lab Analytical

QC February 23, 2017
LO-RLO-2017-0025 Focused Self-Assessment:
Radiological Environmental Monitoring Program and Radioactive Gaseous and Liquid Effluent Treatment June 24, 2017
NUPIC #24191
NUPIC Audit: Teledyne Brown Engineering Environmental Services

- Audit NUPIC #24191

July 6, 2016
Calibration and Maintenance Records Number Title Date
WO 52686362 Meteorological Monitoring

- Wind Speed Elev. 150 foot (Secondary)

Calibration Test September
21, 2016
WO 52686365 Meteorological Monitoring

- Wind Direction Elev. 30 foot (Primary)

Calibration Test September 21

, 2016

WO 52686366 Meteorological Monitoring

- Wind Speed Elev. 150 foot (Primary)

Calibration Test September
21, 2016 WO 52717223
Meteorological Monitoring

- Wind Speed Elev. 30 foot (Secondary)

Calibration Test March 22, 2017
WO 52720478 Meteorological Monitoring

- Air Temperature Difference Elev. 30/150 foot (Secondary)

Semi-Annual Channel Calibration March 27, 2017
WO 52725318
Meteorological Monitoring

- Wind Speed Elev. 150 foot (Secondary)

Calibration Test March 23, 2017

Condition Reports

(CRs)

CR-RBS-2016-06844
CR-RBS-2016-07079
CR-RBS-2016-07383
CR-RBS-2016-07790
CR-RBS-2017-01030
CR-RBS-2017-01122
CR-RBS-2017-03997
CR-RBS-2017-06201

Miscellaneous

Number Title Date
Wind Rose Data Charts: 10 and 50 Meter March 1979
2015 Land Use Census Results May 2, 2016
2016 Land Use Census Results May 1, 2017
Annual Radiological Environmental Operating Report May 1, 2017
TRM 3.12 Radiological Environmental Monitoring
2016 Groundwater Monitoring Plan: River Bend, Rev. 6 February 8, 2017
RBG-47682 2015 Annual Radioactive Effluent Release Report May 2, 2016
RBG-47753 2016 Annual Radioactive Effluent Release Report May 1, 2017

Procedures

Number Title Revision
EN-CY-108 Monitoring of Non

-Radioactive Systems

EN-CY-108 Monitoring of Non

-Radioactive Systems

Procedures

Number Title Revision
EN-CY-111 Radiological Groundwater Monitoring Program 7
EN-EV-100 Environmental Expectations
EN-RP-113 Response to Contaminated Spills/Leaks
ESP-8-021 Sampling Of Water For Radiological Environmental Monitoring
ESP-8-023 Sampling of Airborne Radioiodine and Particulates for Radiological Environmental Monitoring
ESP-8-042 Radioactive Standard Preparation for Environmental Program
ESP-8-050 Conduct of the Radiological Environmental Monitoring Program (REMP)
ESP-8-052 Inter-laboratory Comparison Program for Radiological Environmental Monitoring
RSP-0008 Offsite Dose Calculation Manual
15
Section 2RS08:
Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation Audits and Self

-Assessments Number Title Date

Follow-Up to QA Finding (QAF) identified during the performance of the 2015 RP/Radwaste Audit March 15, 2016
LO-RLO-2017-0024 Pre-NRC Focused Self

-Assessments Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation

(NRC IP 71124.08)

May 23, 2017
QA-14/15-2015-RBS-01 Radiation Protection/Radwaste Audit September 1, 2015

Condition Reports

(CRs)

CR-RBS-2015-08815
CR-RBS-2015-08867
CR-RBS-2016-00328
CR-RBS-2016-00354
CR-RBS-2016-00810
CR-RBS-2016-01038
CR-RBS-2016-02462
CR-RBS-2016-03202
CR-RBS-2016-03865
CR-RBS-2016-03986
CR-RBS-2016-05442
CR-RBS-2016-05858
CR-RBS-2016-08057
CR-RBS-2017-00144
CR-RBS-2017-00347
CR-RBS-2017-03332

Miscellaneous

Number Title Revision/Date
Shipping Logbook
2015
Shipping Logbook
2016
Shipping Logbook
2017
RBG-47655 Spent Fuel Storage Radioactive Effluent Release Report for 2015
February 25, 2016
RBG-47682 2015 Annual Radioactive Effluent Release Report May 2, 2016
RBG-47739 Spent Fuel Storage Radioactive Effluent Release Report for 2016
February 23, 2017
RBG-47753 2016 Annual Radioactive Effluent Release Report May 1, 201
RLP-RPCT-SHIP DOT HAZMAT RAM Shipping 3 UFSAR Chapter 11
RBS Updates Final Safety Analysis Report
UFSAR Chapter 12
RBS Updated Final Safety Analysis Report
UFSAR Chapter 9
RBS Updated Final Safety Analysis Report

Procedures

Number Title Revision
EN-RP-121 Radioactive Material Control
EN-RW-101 Radioactive Waste Management
EN-RW-102 Radioactive Shipping Procedure
EN-RW-104 Scaling Factors
EN-RW-105 Process Control Program
EN-RW-106 Integrated Transportation Security Plan
EN-RW-108 Radioactive Shipment Accident Response
RSP-0008 Offsite Dose Calculation Manual (ODCM)
RSP-0221 Controls for Storage, Monitoring and Decontamination Areas Outside the Protected Area
RWS-0304 Radioactive Waste Handling and Control
RWS-0336 Set-Up and Operation of the RDS

-1000 Dewatering Unit 11

Radioactive Waste Stream Evaluations Number Title Date 369977001
CFR 61 Dry Active Waste Stream (2015)
May 5, 2015
394211001
CFR 61 Liquid Waste Stream (LWS

-CND) Resin April 19, 2016

394211003
CFR 61 SFC Waste Stream (2016)
February 17, 2017
407960001
CFR 61 RWCU Powdex Resin December 5, 2016
RBS-1702-0246 113' Fuel Building February 24, 2017
RBS-1704-0303 186' Reactor Building April 27, 2017
RBS-1706-0085 1407 OS Anco Warehouse June 7, 2017
RBS-1706-0154 106' Radwaste Liner Bay June 14, 2017
RBS-1706-0221 1408 OS Low Level Radwaste June 21, 2017
RBS-1706-0313 1419 OS Release Facility June 26, 2017
Radiological Surveys Number Title Date
RBS-1702-0246 113' Fuel Building February 24, 2017
RBS-1704-0303 186' Reactor Building April 27, 2017
RBS-1706-0085 1407 OS Anco Warehouse June 7, 2017
RBS-1706-0154 106' Radwaste Liner Bay June 14, 2017
RBS-1706-0221 1408 OS Low Level Radwaste June 21, 2017
RBS-1706-0313 1419 OS Release Facility June 26, 20
Shipments
RBS-2015-003
RBS-2016-004
RBS-2016-012
RBS-2016-033
RBS-2016-060
RBS-2016-111
RBS-2016-112
RBS-2016-113
RBS-2017-012
RBS-2017-062
RBS-2017-073 RBS-2017-074

Section 4OA1: Performance Indicator Verification

Miscellaneous

Number Title Revision/Date Engineering Report
RBS-SA-06-0001 RBS Mitigating System Performance Index (MSPI) Basis Document
NEI 99-02 Regulatory Assessment Performance Indicator Guideline

Miscellaneous

Number Title Revision/Date
RBF1-17-0084 Electronic Submittal of Second Quarter 2017 NRC Performance Indicator Information July 21, 2017

Procedure

Number Title Revision
EN-LI-114 Performance Indicator Process

Section 4OA2: Problem Identification and Resolution

Condition Report (CR)

CR-RBS-2017-04128

Procedures

Number Title Revision
GMP-0015 Lubrication Procedure
GMP-0015 Lubrication Procedure Work Order (WO)
WO 52632206

Section 4OA3:

Follow

-up of Events and Notices of Enforcement Discretion

Condition Report (CR)

CR-RBS-2017-02405
Work Order (WO)
WO 00438386
The following items are requested for the Public Radiation Safety Inspection at River Bend Station August 21

-25, 2017 Integrated Report 2017003

Inspection areas are listed in the attachments below.
Please provide the requested information on or before July 26, 2017

.

Please submit this information using the same lettering system as below.
For example, all contacts and phone numbers for Inspection Procedure 71124.0

should be in a file/folder titled

"1- A," applicable organization charts in file/folder "

1- B," etc.
If information is placed on ims.certrec.com, please ensure the inspection exit date entered is at least 30 days later than the onsite inspection dates, so the inspectors will have access to the information while writing the report.
In addition to the corrective action document lists provided for each inspection procedure listed below, please provide updated lists of corrective action documents at the entrance meeting.
The dates for these lists should range from the end dates of the original lists to the day of the entrance meeting.
If more than one inspection procedure is to be conducted and the information requests appear to be redundant, there is no need to provide duplicate copies.
Enter a note explaining in which file the information can be found.
If you have any questions or comments, please contact Louis Carson at (817) 817-200-1221 or Louis.Carson@nrc.gov

.

PAPERWORK
REDUCTION ACT STATEMENT
This letter does not contain new or amended information collection requirements subject to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.).
Existing information collection requirements were approved by the Office of Management and Budget, control number 3150

-0011.

5. Radiation Monitoring Instrumentation (71124.05)
Date of Last Inspection:
December 7, 2015
A. List of contacts and telephone numbers for the following areas:
1. Effluent monitor calibration
2. Radiation protection instrument calibration
3. Installed instrument calibrations
4. Count room and Laboratory instrument calibrations
B. Applicable organization charts
C. Copies of audits, self

-assessments, vendor or NUPIC audits for contractor support and LERs, written since date of last inspection

, related to:

1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, or whole body counters
2. Installed radiation monitors
D. Procedure index for:
1. Calibration, use and operation of continuous air monitors, criticality monitors, portable survey instruments, temporary area radiation monitors, electronic dosimeters, teledosimetry, personnel contamination monitors, and whole body counters.
2. Calibration of installed radiation monitors
E. Please provide specific procedures related to the following areas noted below

.

Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
1. Calibration of portable radiation detection instruments (for portable ion chambers)
2. Whole body counter calibration
3. Laboratory instrumentation quality control
F. A summary list of corrective action documents (including corporate and sub

-tiered systems) written since date of last inspection, related to the following programs:

1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, whole body counters,
2. Installed radiation monitors,
3. Effluent radiation monitors
4. Count room radiation instruments
NOTE: The lists should indicate the significance level of each issue and the search criteria used.
Please provide in document formats which are "searchable" so that the inspector can perform word searches.
G. Offsite dose calculation manual, technical requirements manual, or licensee controlled specifications which lists the effluent monitors and calibration requirements.
H. Current calibration data for the whole body counter

s. I. Primary to secondary source calibration correlation for effluent monitors.

J. A list of the point of discharge effluent monitors with the two most recent calibration dates and the work order numbers associated with the calibrations.
K. Radiation Monitoring System health report for the previous 12 months
6. Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
Date of Last Inspection:
December 7, 2015
A. List of contacts and telephone numbers for the following areas:
1. Radiological effluent control
2. Engineered safety feature air cleaning systems
B. Applicable organization charts
C. Audits, self

-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to:

1.
Radioactive effluents
2.
Engineered Safety Feature Air cleaning systems
D. Procedure indexes for the following areas
1. Radioactive effluents
2. Engineered Safety Feature Air cleaning systems
E. Please provide specific procedures related to the following areas noted below

.

Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
1. Sampling of radioactive effluents
2. Sample analysis
3. Generating radioactive effluent release permits
4. Laboratory instrumentation quality control
5. In-place testing of HEPA filters and charcoal adsorbers
6. New or applicable procedures for effluent programs (e.g., including ground water monitoring programs)
F. List of corrective action documents (including corporate and sub

-tiered systems) written since date of last inspection, associated with:

1.
Radioactive effluents
2.
Effluent radiation monitors
3.
Engineered Safety Feature Air cleaning systems
NOTE: The lists should indicate the significance level of each issue and the search criteria used.
Please provide in document formats which are "searchable" so that the inspector can perform word searches.
G. 2015 and 2016
Annual Radioactive Effluent Release Report or the two most recent reports. H. Current Copy of the Offsite Dose Calculation Manual

. I. Copy of the 2015 and 2016

inter-laboratory comparison results for laboratory quality control performance of effluent sample analysis, or the two most recent results.

J. Effluent sampling schedule for the week of the inspection

.

K. New entries into 10
CFR 50.75(g) files since date of last inspection

. L. Operations department

(or other responsible dept.) log records for effluent monitors removed from service or out of service

. M. Listing or log of liquid and gaseous release permits since date of last inspection

. N. A list of the technical specification

-required air cleaning systems with the two most recent surveillance test dates of in

-place filter testing (of HEPA filters and charcoal adsorbers) and laboratory testing (of charcoal efficiency) and the work order numbers associated with the surveillances

. O. System Health Report for radiation monitoring instrumentation.

Also, please provide

a specific list of all effluent radiation monitors that were considered inoperable for 7 days or more since the last inspection

.

If applicable, please provide the relative Special Report and condition report(s).
P. A list of all radiation monitors that are considered §50.65/Maintenance Rule equipment.
Q. A list of all significant changes made to the Gaseous and Liquid Effluent Process Monitoring System since the last inspection.
If applicable, please provide the corresponding UFSAR section in which this change was documented.
R.
A list of any occurrences in which a non

-radioactive system was contaminated by a radioactive system.

Please include any relative condition report(s).
7. Radiological Environmental Monitoring Program (71124.07)
Date of Last Inspection:
December 7, 2015
A. List of contacts and telephone numbers for the following areas:
1. Radiological environmental monitoring
2. Meteorological monitoring
B. Applicable organization charts

. C. Audits, self

-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to:

1. Radiological environmental monitoring program (including contractor environmental laboratory audits, if used to perform environmental program functions)
2. Environmental TLD processing facility 3. Meteorological monitoring program
D. Procedure index for the following areas:
1. Radiological environmental monitoring program
2. Meteorological monitoring program
E. Please provide specific procedures related to the following areas noted below

.

Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
1. Environmental Program Description
2. Sampling, collection and preparation of environmental samples
3. Sample analysis (if applicable)
4. Laboratory instrumentation quality control
5. Procedures associated with the Offsite Dose Calculation Manual

.

6. Appropriate QA Audit and program procedures, and/or sections of the station's QA manual (which pertain to the REMP)
F. A summary list of corrective action documents (including corporate and sub

-tiered systems) written since date of last inspection, related to the following programs:

1. Radiological environmental monitoring
2. Meteorological monitoring
NOTE: The lists should indicate the significance level of each issue and the search criteria used.
Please provide in document formats which are "searchable" so that the inspector can perform word searches.
G. Wind Rose data and evaluations used for establishing environmental sampling locations

.

H. Copies of the 2 most recent calibration packages for the meteorological tower instruments.
I. Copy of the 2015 and 2016
Annual Radiological Environmental Operating Report and Land Use Census, and current revision of the Offsite Dose Calculation Manual, or the two most recent reports.
J. Copy of the environmental laboratory's inter

-laboratory comparison program results for

2015 and 2016, or the two most recent results, if not included in the annual radiological environmental operating report

. K. Data from the environmental laboratory documenting the analytical detection sensitivities for the various environmental sample media (i

.e., air, water, soil, vegetation, and milk)

. L. Quality Assurance audits (e.g., NUPIC) for contracted services.

M. Current NEI Groundwater Initiative Plan and status

. N.

Technical requirements manual or licensee controlled specifications which lists the meteorological instruments calibration requirements

.

O. A list of Regulatory Guides and/or NUREGs that you are currently committed to relative to the Radiological Environmental Monitoring Program.
Please include the revision and/or date for the committed item and where this can be located in your current licensing basis/UFSAR.
P. If applicable, per NEI 07

-07, provide any reports that document any spills/leaks to groundwater since the last inspection

.

8. Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)
Date of Last Inspection:
December 7, 2015
A. List of contacts and telephone numbers for the following areas: 1. Solid Radioactive waste processing
2. Transportation of radioactive material/waste
B. Applicable organization charts (and list of personnel involved in solid radwaste processing, transferring, and transportation of radioactive waste/materials)

.

C. Copies of audits, department self

-assessments, and LERs written since date of last inspection related to:

1. Solid radioactive waste management
2. Radioactive material/waste transportation program
D. Procedure index for the following areas:
1. Solid radioactive waste management
2. Radioactive material/waste transportation
E. Please provide specific procedures related to the following areas noted below

.

Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
1. Process control program
2. Solid and liquid radioactive waste processing
3. Radioactive material/waste shipping
4. Methodology used for waste concentration averaging, if applicable
5. Waste stream sampling and analysis
F. A summary list of corrective action documents (including corporate and sub

-tiered systems) written since date of last inspection related to:

1. Solid radioactive waste
2. Transportation of radioactive material/waste
NOTE: The lists should indicate the significance level of each issue and the search criteria used.
Please provide in document formats which are "searchable" so that the inspector can perform word searches.
G. Copies of training lesson plans for 49CFR172 subpart H, for radwaste processing, packaging, and shipping.
H. A summary of radioactive material and radioactive waste shipments made from date of last inspection to present

. I. Waste stream sample analyses results and resulting scaling factors for 2015 and 2016

, or the two most recent results.

J. Waste classification reports if performed by vendors (such as for irradiated hardware)

. K. A listing of all onsite radwaste storage facilities.

Please include a summary or listing of the items stored in each facility, including the total amount of radioactivity and the highest general area dose rate.
Although it is not necessary to compile the following information, the inspector will also review:
L. Training, and qualifications records of personnel responsible for the conduct of radioactive waste processing, package preparation, and shipping.