05-09-2017 | On March 10, 2017, at approximately 7:14 a.m. CST, the reactor operator manually actuated a reactor scram in response to an abnormal increase in steam pressure. Reactor power was approximately 15 percent at the time. The turbine generator had been synchronized to the grid at 5:13 a.m. on March 10, and was being closely monitored by engineers and operators since a major modification to the turbine electro-hydraulic control ( EHC) system had been installed during the recent refueling outage.
Approximately 45 minutes prior to the manual scram, a main control room alarm actuated indicating a problem with the EHC system.
A few minutes later, it was reported from the turbine building that there was a steam leak in the area of the EHC steam pressure transmitters. Shortly thereafter, reactor pressure began to increase with no demand signal present, at which time the reactor operator initiated the scram. The main feedwater system remained in service, and reactor water level control performed normally as designed. No reactor safety-relief valves actuated. The main turbine bypass valves did not open following the shutdown, and engineering review determined this condition was consistent with the response to the abnormal configuration of the EHC system pressure transmitters created by efforts to isolate the leak locally. Approximately five minutes after the scram, the outboard main steam isolation valves were manually closed to limit the reactor cooldown rate. This event resulted from the incorrect installation of a new compression fitting in the steam pressure instrumentation tubing for the main turbine control system. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as a manual actuation of the reactor protection system. |
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Category:Letter
MONTHYEARIR 05000458/20240102024-10-31031 October 2024 Design Basis Assurance Inspection (Programs) Inspection Report 05000458/2024010 IR 05000458/20240032024-10-31031 October 2024 Integrated Inspection Report 05000458/2024003 RBG-48315, Reply to a Notice of Violation, NRC Inspection Report 05000458/2023003 Supplement2024-09-24024 September 2024 Reply to a Notice of Violation, NRC Inspection Report 05000458/2023003 Supplement RBG-48306, Report of Changes and Errors to 10CFR50.462024-09-24024 September 2024 Report of Changes and Errors to 10CFR50.46 ML24263A2712024-09-19019 September 2024 Application to Revise Technical Specifications to Adopt TSTF-592, Revise Automatic Depressurization System (ADS) Instrumentation Requirements ML24255A1192024-09-16016 September 2024 Notification of NRC Follow Up Inspection for One Severity Level (SL) III and Two SL IV or Three or More SL IV Violations and Request for Additional Information RBG-48311, Reply to a Notice of Violation, NRC Inspection Report 05000458/20240022024-08-28028 August 2024 Reply to a Notice of Violation, NRC Inspection Report 05000458/2024002 IR 05000458/20240052024-08-22022 August 2024 Updated Inspection Plan for River Bend Station (Report 05000458/2024005) ML24220A2642024-08-20020 August 2024 Entergy Operations, Inc. - Entergy Fleet Project Manager Assignment ML24185A1522024-08-13013 August 2024 Issuance of Amendment Nos. 334, 235, and 215, Respectively, to Revise TSs to Adopt TSTF-205 ML24214A2752024-08-0202 August 2024 Acknowledgement of Readiness for Supplemental Inspection RBG-48308, Notification of Readiness for Supplemental Inspection2024-07-31031 July 2024 Notification of Readiness for Supplemental Inspection IR 05000458/20240022024-07-30030 July 2024 Integrated Inspection Report 05000458/2024002 and Notice of Violation ML24164A0862024-06-12012 June 2024 Notification of Commercial Grade Dedication Inspection (05000458/2024010) and Request for Information 05000458/LER-2023-005-01, Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String2024-06-0404 June 2024 Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String ML24060A2192024-05-30030 May 2024 Authorization of Alternative to Use EN-RR-01 Concerning Proposed Alternative to Adopt Code Case N-752 ML24081A0072024-05-16016 May 2024 Issuance of Amendment No. 213 Revision to Technical Specifications to Adopt TSTF 505, Revision 2, Provide Risk-Informed Extended Completion Times – RITSTF Initiative 4b ML24093A0892024-05-16016 May 2024 Issuance of Amendment No. 214 Adoption of 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components for Nuclear Power Reactors IR 05000458/20240012024-05-14014 May 2024 Integrated Inspection Report 05000458/2024001 ML24128A0422024-05-0707 May 2024 License Amendment Request to Remove Obsolete License Conditions ML24102A2842024-05-0707 May 2024 Summary of Regulatory Audit in Support of LARs to Revise Technical Specifications to Adopt Risk-Informed Completion Times and Implement the Provisions of 10 CFR 50.69 RBG-48276, 2023 Annual Radioactive Effluent Release Report2024-04-23023 April 2024 2023 Annual Radioactive Effluent Release Report RBG-48288, Louisiana Pollutant Discharge Elimination System Permit Renewal2024-04-15015 April 2024 Louisiana Pollutant Discharge Elimination System Permit Renewal IR 05000458/20244022024-04-15015 April 2024 Security Baseline Inspection Report 05000458/2024402 (Full Report) ML24106A0432024-04-11011 April 2024 June 2024 Emergency Preparedness Exercise Inspection Request for Information ML24101A3882024-04-10010 April 2024 Response to Request for Confirmation of Information by the Office of Nuclear Reactor Regulation Proposed Alternative Request EN-RR-22-001 Risk-Informed Categorization and Treatment for Repair RBG-48277, 2023 Annual Radiological Environmental Operating Report2024-04-10010 April 2024 2023 Annual Radiological Environmental Operating Report IR 05000458/20243012024-04-0202 April 2024 Notification of NRC Initial Operator Licensing Examination 05000458/2024301 ML24089A2262024-03-29029 March 2024 Entergy Response to Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Exams ML24075A1712024-03-15015 March 2024 Nuclear Onsite Property Damage Insurance (10 CFR 50.54(w)(3)) IR 05000458/20240402024-03-15015 March 2024 – 95001 Supplemental Inspection Report 05000458/2024040 and Follow-Up Assessment ML24074A2892024-03-14014 March 2024 Proof of Financial Protection (10 CFR 140.15) ML24066A1802024-03-0707 March 2024 Notification of NRC Follow-Up Inspection for Any Severity Level I or II Traditional Enforcement Violation IR 05000458/20230062024-02-28028 February 2024 Annual Assessment Letter for River Bend Station - Report 05000458/2023006 RBG-48278, 2023 Spent Fuel Storage Radioactive Effluent Release Report2024-02-27027 February 2024 2023 Spent Fuel Storage Radioactive Effluent Release Report RBG-48286, Revision to Owners Activity Report Form (OAR) for Cycle 222024-02-27027 February 2024 Revision to Owners Activity Report Form (OAR) for Cycle 22 ML24031A0042024-02-21021 February 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0052 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) 05000458/LER-2023-006, Automatic Reactor Scram Due to a Turbine Trip Following a Disconnect Failure at Switchyard2024-02-0808 February 2024 Automatic Reactor Scram Due to a Turbine Trip Following a Disconnect Failure at Switchyard RBG-48274, Notification of Readiness for Supplemental Inspection2024-02-0505 February 2024 Notification of Readiness for Supplemental Inspection IR 05000458/20230042024-01-30030 January 2024 Integrated Inspection Report 05000458/2023004 IR 05000458/20230402024-01-18018 January 2024 – 95001 Supplemental Inspection Supplemental Report 05000458/2023040 and Follow-Up Assessment Letter 05000458/LER-2023-005, Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String2024-01-16016 January 2024 Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String RBG-48271, Supplement to License Amendment Request to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times – RITSTF Initiative 4b and Application to Adopt 10 CFR 50.69, Risk2024-01-12012 January 2024 Supplement to License Amendment Request to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times – RITSTF Initiative 4b and Application to Adopt 10 CFR 50.69, Risk ML24012A1962024-01-12012 January 2024 Response to 2nd Round Request for Additional Information Concerning Relief Request Number EN-RR-22-001 – Proposed Alternative to Use ASME Code Case N-752, Risk-Informed Categorization and ML24011A1742024-01-11011 January 2024 Security Baseline Inspection Report (Cover Letter) 05000458/LER-2023-004, Drywall Post Accident Radiation Monitor Inoperable Due to Unrecognized Surveillance Failure2023-12-28028 December 2023 Drywall Post Accident Radiation Monitor Inoperable Due to Unrecognized Surveillance Failure ML23349A1672023-12-21021 December 2023 Request for Withholding Information from Public Disclosure ML23348A3572023-12-14014 December 2023 Application to Revise Technical Specifications to Use Online Monitoring Methodology – Slides and Affidavit for Pre-Submittal Meeting ML23352A0292023-12-13013 December 2023 Entergy - 2024 Nuclear Energy Liability Evidence of Financial Protection ML23340A1592023-12-13013 December 2023 Entergy Operations, Inc. - Entergy Fleet Project Manager Assignment 2024-09-24
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000458/LER-2023-005-01, Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String2024-06-0404 June 2024 Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String 05000458/LER-2023-006, Automatic Reactor Scram Due to a Turbine Trip Following a Disconnect Failure at Switchyard2024-02-0808 February 2024 Automatic Reactor Scram Due to a Turbine Trip Following a Disconnect Failure at Switchyard 05000458/LER-2023-005, Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String2024-01-16016 January 2024 Manual Reactor Scram Due to Lowering Feedwater Temperature Following an Automatic Isolation of Feedwater Heater String 05000458/LER-2023-004, Drywall Post Accident Radiation Monitor Inoperable Due to Unrecognized Surveillance Failure2023-12-28028 December 2023 Drywall Post Accident Radiation Monitor Inoperable Due to Unrecognized Surveillance Failure 05000458/LER-2023-003-01, Drywell Atmosphere Radiation Monitor Particulate and Gaseous Channels Inoperable Due to Out of Tolerance Conversion Factors2023-11-15015 November 2023 Drywell Atmosphere Radiation Monitor Particulate and Gaseous Channels Inoperable Due to Out of Tolerance Conversion Factors 05000458/LER-2022-004-01, High Pressure Core Spray Inoperable Due to Transformer Failure2023-11-15015 November 2023 High Pressure Core Spray Inoperable Due to Transformer Failure 05000458/LER-2023-003, Drywell Atmosphere Radiation Monitor Particulate and Gaseous Channels Inoperable Due to Out of Tolerance Conversion Factors2023-09-14014 September 2023 Drywell Atmosphere Radiation Monitor Particulate and Gaseous Channels Inoperable Due to Out of Tolerance Conversion Factors 05000458/LER-2023-002-01, Division I and II Diesel Generators Inoperable Due to Exceeding Load Sequence Times2023-09-13013 September 2023 Division I and II Diesel Generators Inoperable Due to Exceeding Load Sequence Times 05000458/LER-2023-001-01, Ultimate Heat Sink Inoperable Due to Boundary Valve Leakage2023-08-17017 August 2023 Ultimate Heat Sink Inoperable Due to Boundary Valve Leakage 05000458/LER-2023-002, Division I and II Diesel Generators Inoperable Due to Exceeding Load Sequence Times2023-06-29029 June 2023 Division I and II Diesel Generators Inoperable Due to Exceeding Load Sequence Times 05000458/LER-2023-001, Ultimate Heat Sink Inoperable Due to Boundary Valve Leakage2023-05-23023 May 2023 Ultimate Heat Sink Inoperable Due to Boundary Valve Leakage 05000458/LER-2022-004, High Pressure Core Spray Inoperable Due to Transformer Failure2022-11-17017 November 2022 High Pressure Core Spray Inoperable Due to Transformer Failure 05000458/LER-2022-003, Division 1 Standby Diesel Generator Speed Sensor Power Supply Failure2022-09-0101 September 2022 Division 1 Standby Diesel Generator Speed Sensor Power Supply Failure 05000458/LER-2022-002, Condition Prohibited by Technical Specifications Due to Reactor Scram and Turbine Trip Level 8 Trip Setpoint Deviation2022-06-0909 June 2022 Condition Prohibited by Technical Specifications Due to Reactor Scram and Turbine Trip Level 8 Trip Setpoint Deviation 05000458/LER-2022-001, Condition Prohibited by Technical Specifications Due to Residual Heat Removal B Pump Motor Bearing Oil Leak2022-05-17017 May 2022 Condition Prohibited by Technical Specifications Due to Residual Heat Removal B Pump Motor Bearing Oil Leak 05000458/LER-2021-005, Potential Loss of Safety Function Due to Inoperable Reactor Core Isolation Cooling Steam Flow Transmitter2021-12-16016 December 2021 Potential Loss of Safety Function Due to Inoperable Reactor Core Isolation Cooling Steam Flow Transmitter 05000458/LER-2017-0092017-11-13013 November 2017 Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door, LER 17-009-00 for River Bend, Unit 1 Regarding Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door 05000458/LER-2017-0072017-08-21021 August 2017 Automatic Reactor Scram due to Failure of Main Generator Voltage Regulator Mode Transfer Relay, LER 17-007-00 for River Bend Station - Unit 1 Regarding Automatic Reactor Scram due to Failure of Main Generator Voltage Regulator Mode Transfer Relay 05000458/LER-2017-0062017-07-13013 July 2017 Potential Loss of Safety Function of Onsite Power Sources due to Inadvertent Inoperability of Control Building Chiller, LER 17-006-00 for River Bend, Unit 1 re Potential Loss of Safety Function of Onsite Power Sources due to Inoperability of Control Building Chiller 05000458/LER-2016-0032017-06-0808 June 2017 Operations Prohibited by Technical Specifications Due to Reactor Control Rod Drift During Core Alterations, LER 16-003-01 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Control Blade Drift During Core Alterations 05000458/LER-2017-0052017-06-0505 June 2017 1 OF 3, LER 17-005-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Inoperable Main Control Room Filter Train 05000458/LER-2017-0042017-05-22022 May 2017 Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve, LER 17-004-00 for River Bend Station, Unit 1, Regarding Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve 05000458/LER-2017-0032017-05-0909 May 2017 Manual Reactor Scram Initiated in Response to Increase in Steam Pressure During Steam Leak Troubleshooting, LER 17-003-00 for River Bend Station, Unit 1, Regarding Manual Reactor Scram Initiated in Response to Increase in Steam Pressure During Steam Leak Troubleshooting 05000458/LER-2017-0022017-04-18018 April 2017 Loss of Safety Function of Onsite Electrical Distribution Due to Malfunction of Control Building HVAC System, LER 17-002-00 for River Bend Station, Unit 1, Regarding Loss of Safety Function of Onsite Electrical Distribution Due to Malfunction of Control Building HVAC System 05000458/LER-2017-0012017-04-0303 April 2017 Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open), LER 17-001-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open) 05000458/LER-2016-0072016-07-25025 July 2016 1 Operations Prohibited by Technical Specifications Due to Failure to Implement Required Actions Within Completion Time, LER 16-007-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Failure to Implement Required Actions Within Completion Time 05000458/LER-2016-0062016-07-12012 July 2016 Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers, LER 16-006-00 for River Bend Station re: Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers 05000458/LER-2016-0042016-03-29029 March 2016 Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power, LER 16-004-00 for River Bend, Unit 1, Regarding Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power 05000458/LER-2016-0012016-03-0707 March 2016 Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System, LER 16-001-00 for River Bend, Unit 1, Regarding Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System 05000458/LER-2016-0022016-03-0707 March 2016 Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient, LER 16-002-00 for River Bend, Unit 1, Regarding Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient 05000458/LER-2015-0102016-02-0808 February 2016 Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller, LER 15-010-00 for River Bend Station, Unit 1, Regarding Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller 05000458/LER-2015-0092016-01-26026 January 2016 1 OF 3, LER 15-009-00 for River Bend Station, Unit 1 Regarding Automatic Reactor Scram Due to Partial Loss of Offsite Power Caused by Fault in Local 230K Switchyard 05000458/LER-2015-0082016-01-18018 January 2016 Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller, LER 15-008-00 of River Bend Station, Unit 1, Regarding Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller 05000458/LER-2015-0072016-01-18018 January 2016 Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller, LER 15-007-00 for River Bend Station - Unit 1 Regarding Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller RBG-47473, Special Report for NEI 07-07 Notification2014-06-0404 June 2014 Special Report for NEI 07-07 Notification ML0627100382006-05-16016 May 2006 Final Precursor Analysis - River Bend Station, LER-458/04-005-01, Automatic Reactor Trip Due to Loss of Non-Vital 120V Instrument Bus 2024-06-04
[Table view] |
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
05000-458 2017 003 00
REPORTED CONDITION
On March 10, 2017, at approximately 7:14 a.m. CST, the reactor operator manually actuated a reactor scram in response to an abnormal increase in steam pressure. Reactor power was approximately 15 percent at the time, and the turbine generator was on line. The reactor had been taken critical at 4:39 p.m. on March 8 following a refueling outage, and power ascent was in progress. The turbine generator had been synchronized to the grid at 5:13 a.m. on March 10, and was being closely monitored by engineers and operators since a major modification to the turbine electro-hydraulic control (EHC) system [JI] had been installed during the outage.
Approximately 45 minutes prior to the manual scram, a main control room alarm actuated indicating a problem with the EHC system. A few minutes later, it was reported from the turbine building that there was a steam leak in the area of the steam pressure transmitters. The operations shift manager held a briefing with the operators on potential effects of the field observations, the single-point vulnerability of the transmitter configuration, and the possibility of a main turbine trip. Shortly thereafter, reactor pressure began to increase with no demand signal present. This response likely resulted from efforts to isolate the steam leak.
The main feedwater system remained in service, and reactor water level control was performed normally. No reactor safety-relief valves actuated. The main turbine bypass valves did not open following the shutdown, and engineering review determined this condition was consistent with the response to the abnormal configuration of the EHC system pressure transmitters created by efforts to isolate the leak locally. Approximately five minutes after the scram, the outboard main steam isolation valves were manually closed to limit the reactor cooldown rate.
Other than scheduled testing on the Division 1 diesel generator, no safety-related systems were out of service at the time of the scram.
This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as a manual actuation of the reactor protection system
INVESTIGATION
During the recent refueling outage, a digital control system had been installed on the main steam turbine bypass / pressure regulation system. Part of that modification involved the installation of a new main turbine steam throttle pressure transmitter (**PT**) near the high pressure turbine. The transmitter was to be installed adjacent to two existing steam pressure transmitters by adding a tee fitting into an existing run of tubing (**TBG**). One of the newly- installed tubing compression fittings separated during efforts to isolate the leak. Examination of the components concluded that the ferrule in the fitting was not fully inserted, and did not compress adequately to engage the surface of the tubing when the nut was tightened.
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
05000-458 2017 003 00 The tee fitting was installed by two qualified pipefitters who were contracted for the refueling outage, with oversight provided by a contract pipefitter foreman. The field work to complete the fit-up of the tee connection was specified as Quality Control (QC) Hold Point. The contract foreman stated that he was present during the fit-up of the tee connection and that the technicians performed the work as required, fitting each of the three connections and tightening them one at a time starting with the top compression fitting and ending with the bottom connection. When the fittings were tight, he observed the technicians use a gap tool to verify proper gap and engagement of the compression nut on the tee connection body.
CAUSAL ANALYSIS
This event resulted directly from the incorrect installation of the tee compression fitting for the new steam pressure transmitter. A contributing cause was the lack a standard process on how to properly verify compression tubing and fitting engagement is maintained during the tightening process.
CORRECTIVE ACTION TO PREVENT RECURRENCE
A maintenance procedure will be developed to address the proper installation of compression fittings. This action will be tracked in the corrective action program.
PREVIOUS OCCURRENCE EVALUATION
RBS has reported no similar events in the last three years.
SAFETY SIGNIFICANCE
The plant responded as designed to the transient. The response of the main turbine bypass valves resulted from the efforts to isolate the steam leak, and was, by itself, of no consequence to the operators' response to the event. The steam leak was isolated by closure of an instrument valve. The outboard main steam isolation valves were manually closed in accordance with procedures to manage reactor cooldown rate. There were no injuries as a result of the steam leak. This event was, thus, of minimal significance to the health
- and safety of the public.
(NOTE: Energy Industry Identification System component function identifier and system name of each component or system referred to in the LER are annotated as (**XX**) and [XX], respectively.)
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05000458/LER-2017-001 | Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open) LER 17-001-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000458/LER-2017-002 | Loss of Safety Function of Onsite Electrical Distribution Due to Malfunction of Control Building HVAC System LER 17-002-00 for River Bend Station, Unit 1, Regarding Loss of Safety Function of Onsite Electrical Distribution Due to Malfunction of Control Building HVAC System | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000458/LER-2017-003 | Manual Reactor Scram Initiated in Response to Increase in Steam Pressure During Steam Leak Troubleshooting LER 17-003-00 for River Bend Station, Unit 1, Regarding Manual Reactor Scram Initiated in Response to Increase in Steam Pressure During Steam Leak Troubleshooting | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000458/LER-2017-004 | Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve LER 17-004-00 for River Bend Station, Unit 1, Regarding Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000458/LER-2017-005 | 1 OF 3 LER 17-005-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Inoperable Main Control Room Filter Train | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000458/LER-2017-006 | Potential Loss of Safety Function of Onsite Power Sources due to Inadvertent Inoperability of Control Building Chiller LER 17-006-00 for River Bend, Unit 1 re Potential Loss of Safety Function of Onsite Power Sources due to Inoperability of Control Building Chiller | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000458/LER-2017-007 | Automatic Reactor Scram due to Failure of Main Generator Voltage Regulator Mode Transfer Relay LER 17-007-00 for River Bend Station - Unit 1 Regarding Automatic Reactor Scram due to Failure of Main Generator Voltage Regulator Mode Transfer Relay | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000458/LER-2017-009 | Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door LER 17-009-00 for River Bend, Unit 1 Regarding Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material |
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