IR 05000458/2017003

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NRC Integrated Inspection Report 05000458/2017003
ML17318A189
Person / Time
Site: River Bend Entergy icon.png
Issue date: 11/13/2017
From: Jason Kozal
NRC/RGN-IV/DRP/RPB-C
To: Maguire W
Entergy Operations
JASON KOZAL
References
IR 2017003
Download: ML17318A189 (54)


Text

November 13, 2017

SUBJECT:

RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2017003

Dear Mr. Maguire:

On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station, Unit 1. On October 11, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

One of these findings involved a violation of NRC requirements. Further, inspectors documented a licensee-identified violation, which was determined to be of very low safety significance, in this report. The NRC is treating these violations as non-cited violations consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violations or significance of the non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the River Bend Station.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the River Bend Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Jason W. Kozal, Chief Project Branch C Division of Reactor Projects Docket No.: 50-458 License No.: NPF-47 Enclosure:

Inspection Report 05000458/2017003 w/Attachments:

1. Supplemental Information 2. Public Radiation Safety Inspection Document Request

x SUNSI Review: ADAMS: Non-Publicly Available x Non-Sensitive Keyword:

By: JKozal/dll x Yes No x Publicly Available Sensitive NRC-002 OFFICE SRI:DRP/C RI:DRP/C SPE:DRP/C C:DRS/EB1 C:DRS/EB2 C:DRS/OB NAME JSowa BParks CYoung TFarnholtz GWerner VGaddy SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/STG for /RA/

DATE 11/3/2017 11/7/2017 11/3/2017 11/03/2017 11/13/2017 11/6/17 OFFICE C:DRS/PSB2 TL:IPAT BC:DRP/C NAME HGepford THipschman JKozal SIGNATURE /RA/ /RA/ /RA/

DATE 11/6/17 11/6/2017 11/13/2017

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000458 License: NPF-47 Report: 05000458/2017003 Licensee: Entergy Operations, Inc.

Facility: River Bend Station Location: 5485 U.S. Highway 61N St. Francisville, LA 70775 Dates: July 1 through September 30, 2017 Inspectors: J. Sowa, Senior Resident Inspector B. Parks, Resident Inspector L. Carson II, Senior Health Physicist N. Greene, PhD, Health Physicist S. Money, Health Physicist J. ODonnell, CHP, Health Physicist J. Braisted, PhD, Reactor Inspector Approved By: J. Kozal, Chief Project Branch C Division of Reactor Projects Enclosure

SUMMARY

IR 05000458/2017003; 07/01/2017 - 09/30/2017; River Bend Station; Heat Sink Performance;

Follow-up of Events and Notices of Enforcement Discretion The inspection activities described in this report were performed between July 1 and September 30, 2017, by the resident inspectors at River Bend Station and inspectors from the NRCs Region IV office. Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements. Additionally, NRC inspectors documented one licensee-identified violation of very low safety significance in this report. The significance of inspection findings is indicated by their color (i.e., Green, greater than Green, White, Yellow, or Red), determined using NRC Inspection Manual Chapter 0609,

Significance Determination Process, dated April 29, 2015. Their cross-cutting aspects are determined using NRC Inspection Manual Chapter 0310, Aspects within the Cross-Cutting Areas, dated December 4, 2014. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, dated July 2016.

Cornerstone: Initiating Events

Green.

The inspectors reviewed a self-revealed finding for the licensees failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram. Corrective actions included properly installing the tee connection and writing specific procedural guidance on compression fitting inspection, installation, remake, and repair (CR-RBS-2017-02405).

The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine electro-hydraulic control system was a performance deficiency.

The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.

Specifically, the licensees failure to properly install the tee connection caused a steam leak that led to a reactor scram. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions. The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5]. (Section 4OA3)

Cornerstone: Mitigating Systems

Green.

The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, which states, in part, Measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. Specifically, prior to September 28, 2017, the licensees current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated. This finding was entered into the licensee's corrective action program as Condition Report CR-RBS-2017-06998.

The inspector determined that the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30-day inventory requirement needed to be re-performed to assure that accident analysis requirements were met. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather. This finding had a cross-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin [H.6].

(Section 1R07)

Licensee-Identified Violations

A violation of very low safety significance (Green) that was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and associated corrective action tracking numbers are listed in Section 4OA7 of this report.

PLANT STATUS

River Bend Station began the inspection period at 88 percent reactor thermal power. Operators were in the process of returning the plant to full power following a scram that occurred on June 23, 2017. The station returned to 100 percent power on July 3, 2017.

On July 28, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak. The station returned to 100 percent power on August 3, 2017.

On August 18, 2017, an automatic reactor scram occurred due to equipment issues associated with the feedwater level control system. On August 20, 2017, operators conducted a reactor startup. The station returned to 100 percent power on August 28, 2017.

On September 22, 2017, operators reduced power to 65 percent for suppression testing to find and suppress a suspected fuel leak, but did not identify a new fuel leak. The station returned to 100 percent power on September 28, 2017.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness to Cope with External Flooding

a. Inspection Scope

On July 19, 2017, the inspectors completed an inspection of the stations readiness to cope with external flooding. After reviewing the licensees flooding analysis, the inspectors chose three plant areas that were susceptible to flooding:

  • Division I emergency diesel generator The inspectors reviewed plant design features and licensee procedures for coping with flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether credited operator actions could be successfully accomplished.

These activities constitute one sample of readiness to cope with external flooding, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • August 14, 2017, Division III 125 VDC system
  • September 21, 2017, Division II control building chilled water system The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constitute three partial system walkdown samples, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

.2 Complete Walkdown

a. Inspection Scope

On August 14, 2017, the inspectors performed a complete system walkdown inspection of the Division I and Division II 125 VDC system. The inspectors reviewed the licensees procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, and open condition reports. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.

These activities constitute one complete system walkdown sample, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:

  • July 19, 2017, battery 1A room, fire area C-18
  • July 19, 2017, ENB inverter charger B room, fire area C-19
  • August 16, 2017, battery 1B room, fire area C-19
  • August 28, 2017, standby cooling tower pump B room, fire area PH-2/Z-1 For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constitute four quarterly inspection samples, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

On September 27, 2017, the inspectors completed an inspection of the stations ability to mitigate flooding due to internal causes. After reviewing the licensees flooding analysis, the inspectors chose one plant area containing risk-significant structures, systems, and components that were susceptible to flooding:

  • Division I and II standby switchgear rooms The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.

These activities constitute completion of one flood protection measures sample, as defined in Inspection Procedure 71111.06.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

.1 Annual Review

a. Inspection Scope

On September 22, 2017, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors reviewed the data from the most recent internal inspection of the Division II emergency diesel generator jacket water cooler and verified that the licensee adhered to the periodic maintenance method outlined in EPRI NP-7552. Additionally, the inspectors walked down the Division II emergency diesel generator jacket water cooler to observe its material condition and verified that the cooler was correctly categorized under the Maintenance Rule and was receiving proper maintenance.

These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.

b. Findings

No findings were identified.

.2 Triennial Review

a. Inspection Scope

The inspectors reviewed licensee programs to verify heat exchanger performance and operability for the following heat exchangers:

  • Division I Containment Unit Cooler HVR-UC1A
  • Division I Residual Heat Removal Heat Exchanger E12-EB001A The inspectors verified whether testing, inspection, maintenance, and chemistry control programs are adequate to ensure proper heat transfer. The inspectors verified that the periodic testing and monitoring methods, as outlined in commitments to NRC Generic Letter 89-13, utilized proper industry heat exchanger guidance. Additionally, the inspectors verified that the licensees chemistry program ensured that biological fouling was properly controlled between tests. The inspectors reviewed previous maintenance records of the heat exchangers to verify that the licensees heat exchanger inspections adequately addressed structural integrity and cleanliness of their tubes. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four triennial heat sink inspection samples, as defined in Inspection Procedure 71111.07-05.

b. Findings

Introduction.

The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, involving the failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis. Specifically, the analysis did not include loss of inventory from the safety-related standby service water system to the nonsafety-related normal service water system via the normal service water return isolation valves (prior to manual operator action to close the valves), given a loss of coolant accident coincident with a loss of offsite power and the single active failure of an emergency diesel generator to start or run.

Description.

The technical specification bases for Technical Specification 3.7.1, Standby Service Water (SSW) System and Ultimate Heat Sink (UHS), describe that safety analyses for long-term containment cooling were performed and that for a loss of coolant accident concurrent with a loss of offsite power, the worst case single failure affecting the performance of the standby service water system is the failure of one of the two standby diesel generators, which would in turn affect one standby service water subsystem. The standby service water system is thus designed to preserve the capability to supply adequate cooling water to equipment required for safe reactor shutdown. Additionally, the bases describe that the ultimate heat sink consists of one 200 percent cooling tower and one 100 percent capacity water storage basin, which is sized such that sufficient water inventory is available to provide heat removal capability to safely shut down the plant and to maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available.

The inspectors requested and reviewed Abnormal Operating Procedure AOP-0016, Loss of Standby Service Water, Revision 22, which contained a note that states Within 20 minutes, actions shall be taken to isolate Division I or Division II standby service water return to normal service water to conserve standby cooling tower inventory per Section 5.1 or Section 5.2. An additional note states that With a failure of the Division I diesel to start or load, the Division I powered service water system isolation valves are not able to be closed electrically. With pump SWP-P2C operating, service water flow from Division I standby service water will pass through the unisolated drywell unit coolers and exit into the Division II standby service water return header back to the standby cooling tower. This return flow will be in excess of the design limits for the Division II portion of the standby cooling tower, thus requiring that SWP-P2C be secured.

The inspectors reviewed calculation PM-194, Standby Cooling Tower Performance and Evaporation Losses without Drywell Unit Coolers, Revision 10, whose stated purpose is to determine the capacity of the ultimate heat sink to mitigate a design basis accident, using the containment heat loads identified in G13.18.0*19 (Ref. II.2) for a design basis loss of coolant accident coincident with a loss of offsite power and failure of Division II standby diesel generator EGS-EG1B. The conclusion of the inventory loss case was that a margin of approximately 393,100 gallons would exist in the ultimate heat sink basin after 30 days at technical specification limiting initial conditions. However, the inspector was unable to identify where the calculation accounted for the standby service water system water losses associated with the 20-minute operator action to close the normal service water return isolation valves. Therefore, the inspector requested the analysis of record that demonstrated the loss of standby service water (i.e., ultimate heat sink inventory) to the normal service water system from the affected standby service water train would not be in excess of design limits prior to manual isolation.

The licensee provided calculation PM-193, Standby Service Water - Maximum Flow through Break in Tunnel Piping, Revision 1, as the original basis for the 20-minute operator action. The purpose of PM-193 was to determine the inventory margin and operator action time impact of the assumed break given the scenario in the preceding paragraph, but for a failure of the Division I standby emergency diesel generator instead of the Division II. The postulated break occurred downstream of service water return isolation valve SWP-MOV96A in the nonsafety-related normal service water return header. The conclusion of PM-193 is that 229,500 gallons are potentially lost from the standby service water system to the normal service water system within 30 minutes prior to standby service water system isolation. Based upon these results, the inspector estimated that potentially 153,000 gallons of ultimate heat sink inventory could be lost prior to the 20-minute operator action in AOP-0016 to isolate the nonsafety-related from the safety-related service water systems. Therefore, the inspector concluded that the inventory losses associated with the delayed closure of the normal service water isolation valves were not, but should have been, included in the ultimate heat sink inventory analysis and that the reduction of margin in the inventory analysis was significant. Furthermore, the failure of the Division I standby diesel generator to start or run would result in greater inventory losses through the normal service water return isolation valve than for the same failure on the Division II standby diesel generator due to differences in the design between standby service water system trains; however, PM-194 assumed only a Division II failure.

Analysis.

The failure to account for delayed closure of isolation valves in the ultimate heat sink inventory analysis was a performance deficiency. The performance deficiency was more-than-minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in a condition where the current analysis to determine the acceptability of the ultimate heat sink with respect to the 30-day inventory requirement needed to be re-performed to assure that accident analysis requirements were met.

In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated July 19, 2012, the finding screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of operability or functionality; did not represent an actual loss of safety function of the system or train; did not result in the loss of one or more trains of non-technical specification equipment; and did not screen as potentially risk-significant due to seismic, flooding, or severe weather.

This finding had a cross-cutting aspect in the area of human performance associated with design margins because the failure to account for delayed closure of isolation valves in the 30-day ultimate heat sink inventory analysis resulted in a significant reduction in the available margin [H.6].

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, prior to September 28, 2017, the licensee failed to assure that the design basis for those structures, systems, and components to which this appendix applies was correctly translated into specifications, drawings, procedures, and instructions. Specifically, the current calculation for assuring adequate ultimate heat sink inventory did not support the acceptability of the timing of a critical operator action in the abnormal operating procedure for the loss of standby service water. The potential safety consequence is that sufficient ultimate heat sink inventory might not be available to safely shut down the plant and maintain it in a cold shutdown condition for a 30-day period with no external makeup water source available. In response to this finding, the licensee performed an initial analysis and determined that the ultimate heat sink had sufficient inventory to account for the losses associated with the delayed closure of the normal service water return isolation valves and that the losses would likely be less than those previously calculated.

Because this finding was of very low safety significance (Green) and has been entered into the licensees corrective action program as Condition Report CR-RBS-2017-06998, it is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy: NCV 05000458/2017003-01, Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory

Analysis.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On August 9, 2017, the inspectors observed a portion of an annual requalification test for licensed operators. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities.

These activities constitute completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

The inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was conducting a reactor startup following a reactor scram. The inspectors observed the operators performance of the following activities:

  • August 20, 2017, plant startup, including rod withdrawal to criticality In addition, the inspectors assessed the operators adherence to plant procedures, including the conduct of operations procedure, and other operations department policies.

These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed one instance of a degraded performance or condition of safety-significant structures, systems, and components (SSCs):

  • September 12, 2017, 125 VDC distribution system, functional failure review The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constitute completion of one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

.2 Quality Control

a. Inspection Scope

On August 7, 2017, the inspectors reviewed the licensees quality control activities through a review of their control of safety-related lubricants. The inspectors also reviewed whether quality control verifications were property specified in accordance with the licensees Quality Assurance Program, and were implemented as specified, during work associated with the addition of oil to safety-related control building chiller HVK-CHL1A.

These activities constitute completion of one quality control sample, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed three risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:

  • August 14, 2017, yellow risk condition during Division II residual heat removal surveillance testing The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the results of the assessments.

The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.

These activities constitute completion of three maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed four operability determinations that the licensee performed for degraded or nonconforming SSCs:

The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.

These activities constitute completion of four operability and functionality review samples, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

On August 3, 2017, the inspectors reviewed a permanent plant modification of the Division II uninterruptible power supply (ENB-INV01B1) system output frequency meter.

The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the SSC as modified.

These activities constitute completion of one permanent plant modification inspection sample, as defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed five post-maintenance testing activities that affected risk-significant SSCs:

  • July 14, 2017, work order (WO) 00437814, Division I Battery ENB-BAT01A Post Maintenance Test, following replacement of Division I battery ENB-BAT01A
  • July 27, 2017, WO 00404398-02, Instrument Air Compressor 2C Post Maintenance Test, following maintenance on instrument air compressor 2C
  • September 2, 2017, WO 00478604, LSV-C3A Perform Operability Test, following cleaning and inspection of compressor strainers, check valves, and orifices
  • September 15, 2017, WO 52652445, GTS-FS24B Calibrate Standby Gas Treatment Exhaust Fan B, operability run of standby gas treatment fan B following calibration of low-flow switch The inspectors reviewed licensing- and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constitute completion of five post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed three risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:

In-service tests:

  • July 7, 2017, STP-205-6301, LPCS Pump and Valve Operability Test, performed on July 6, 2017 Other surveillance tests:
  • August 10, 2017, STP-201-6310, Standby Liquid Control Pump and Valve Operability Test, performed on July 26, 2017
  • August 18, 2017, STP-203-1302, E22-S001BAT Quarterly Surveillance, performed on August 16, 2017 The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the tests satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constitute completion of three surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on September 12, 2017, to verify the adequacy and capability of the licensees assessment of drill performance.

The inspectors reviewed the drill scenario, observed the drill from the technical support center and the emergency operations facility, and attended the post-drill critique. The inspectors verified that the licensees emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.

These activities constitute completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

.2 Training Evolution Observation

a. Inspection Scope

On July 25, 2017, the inspectors observed simulator-based licensed operator requalification training that included implementation of the licensees emergency plan.

The inspectors verified that the licensees emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the evaluators and entered into the corrective action program for resolution.

These activities constitute completion of one training observation sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS5 Radiation Monitoring Instrumentation

a. Inspection Scope

The inspectors evaluated the accuracy and operability of the radiation monitoring equipment used by the licensee to monitor areas, materials, and workers to ensure a radiologically safe work environment. This evaluation included equipment used to monitor radiological conditions related to normal plant operations, anticipated operational occurrences, and conditions resulting from postulated accidents. The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance associated with radiation monitoring instrumentation, as described below:

  • The inspectors performed walkdowns and observations of selected plant radiation monitoring equipment and instrumentation, including portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors. The inspectors assessed material condition and operability, evaluated positioning of instruments relative to the radiation sources or areas they were intended to monitor, and verified performance of source checks and calibrations.
  • The inspectors evaluated the calibration and testing program, including laboratory instrumentation, whole body counters, post-accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors, portable survey instruments, area radiation monitors, electronic dosimetry, air samplers, and continuous air monitors.
  • The inspectors assessed problem identification and resolution for radiation monitoring instrumentation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the three required radiation monitoring instrumentation samples, as defined in Inspection Procedure 71124.05.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

a. Inspection Scope

The inspectors evaluated whether the licensee maintained gaseous and liquid effluent processing systems and properly mitigated, monitored, and evaluated radiological discharges with respect to public exposure. The inspectors verified that abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, were controlled in accordance with the applicable regulatory requirements and licensee procedures. The inspectors verified that the licensees quality control program ensured radioactive effluent sampling and analysis adequately quantified and evaluated discharges of radioactive materials. The inspectors verified the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:

  • During walkdowns and observations of selected portions of the radioactive gaseous and liquid effluent equipment, the inspectors evaluated routine processing and discharge of effluents, including sample collection and analysis.

The inspectors observed equipment configuration and flow paths of selected gaseous and liquid discharge system components, effluent monitoring systems, filtered ventilation system material condition, and significant changes to effluent release points.

  • Calibration and testing program for process and effluent monitors, including National Institute of Standards and Technology traceability of sources, primary and secondary calibration data, channel calibrations, setpoint determination bases, and surveillance test results.
  • Sampling and analysis controls used to ensure representative sampling and appropriate compensatory sampling. Reviews included results of the inter-laboratory comparison program.
  • Instrumentation and equipment, including effluent flow measuring instruments, air cleaning systems, and post-accident effluent monitoring instruments.
  • Dose calculations for effluent releases. The inspectors reviewed a selection of radioactive liquid and gaseous waste discharge permits and abnormal gaseous or liquid tank discharges, and verified the projected doses were accurate. The inspectors also reviewed 10 CFR Part 61 analyses and methods used to determine which isotopes were included in the source term. The inspectors reviewed land use census results, offsite dose calculation manual changes, and significant changes in reported dose values from previous years.
  • Problem identification and resolution for radioactive gaseous and liquid effluent treatment. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the six required radioactive gaseous and liquid effluent treatment samples, as defined in Inspection Procedure 71124.06.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program

a. Inspection Scope

The inspectors evaluated whether the licensees radiological environmental monitoring program quantified the impact of radioactive effluent releases to the environment and sufficiently validated the integrity of the radioactive gaseous and liquid effluent release program. The inspectors also verified that the licensee continued to implement the voluntary Nuclear Energy Institute/Industry Ground Water Protection Initiative. The inspectors reviewed or observed the following items:

  • The inspectors observed selected air sampling and dosimeter monitoring stations, sampler station modifications, and the collection and preparation of environmental samples. The inspectors reviewed calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation, and inter-laboratory comparison program results. The inspectors reviewed selected events documented in the annual environmental monitoring report and significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census. The inspectors evaluated the operability, calibration, and maintenance of meteorological instruments and assessed the meteorological dispersion and deposition factors. The inspectors verified the licensee had implemented a sampling and monitoring program sufficient to detect leakage from structures, systems, or components with credible mechanism for licensed material to reach groundwater and reviewed changes to the licensees written program for identifying and controlling contaminated spills/leaks to groundwater.
  • Groundwater protection initiative implementation, including assessment of groundwater monitoring results, identified leakage or spill events and entries made into 10 CFR 50.75
(g) records, licensee evaluations of the extent of the contamination and the radiological source term, and reports of events associated with spills, leaks, and groundwater monitoring results.
  • Problem identification and resolution for the radiological environmental monitoring program. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the three required radiological environmental monitoring program samples, as defined in Inspection Procedure 71124.07.

b. Findings

No findings were identified.

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation (71124.08)

a. Inspection Scope

The inspectors evaluated the effectiveness of the licensees programs for processing, handling, storage, and transportation of radioactive material. The inspectors interviewed licensee personnel and reviewed the following items:

  • Radioactive material storage, including waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition.
  • Radioactive waste system, including walkdowns of the accessible portions of the radioactive waste processing systems and handling equipment. The inspectors also reviewed or observed changes made to the radioactive waste processing systems, methods for dewatering and waste stabilization, waste stream mixing methodology, and waste processing equipment that was not operational or abandoned in place.
  • Waste characterization and classification, including radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult-to-measure radionuclides, and processes for waste classification including use of scaling factors and 10 CFR Part 61 analyses.
  • Shipment preparation, including packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifests.
  • Shipping records for low specific activity (LSA) I, II, III; surface contaminated objects (SCO) I, II; Type A, or Type B radioactive material or radioactive waste shipments.
  • Problem identification and resolution for radioactive solid waste processing and radioactive material handling, storage, and transportation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the six required radioactive solid waste processing and radioactive material handling, storage, and transportation samples, as defined in Inspection Procedure 71124.08.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Mitigating Systems Performance Index: Heat Removal Systems (MS08)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for heat removal systems, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index: Residual Heat Removal Systems (MS09)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for residual heat removal systems, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index: Cooling Water Support Systems (MS10)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of July 2016 through June 2017 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for cooling water support systems, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors selected one issue for an in-depth follow-up:

  • On May 21, 2017, following completion of a Division III emergency diesel generator (EDG) 24-hour run performed by operations department personnel, mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. The technician who performed the evolution discovered the error the following the day while updating the lubrication accountability log.

Mobilgard 412 oil was added by the technicians instead of the required Mobilgard 450 oil. The addition of the 20 gallons of Mobilgard 412 to the Division III EDG resulted in a zinc concentration of 17.3 ppm in the overall oil volume.

The Division III EDG vendor manual states that the allowable concentration for zinc in the lube oil is 0-10 ppm. Since the addition of the Mobilgard 412 oil resulted in a zinc concentration in excess of the vendor recommendation, the station determined that the Division III EDG could not be relied upon to perform its safety function in all conditions and declared it inoperable. The Division III EDG was inoperable for approximately three days while the station pumped out the lube oil and refilled the fuel oil storage tank. The stations adverse conditional analysis determined that technicians added the wrong type of oil because they did not stop and validate the correct oil per procedure GMP-0015, Lubrication Procedure, Revision 14, as required, but assumed the oil staged in the mechanical shop was the correct oil. GMP-0015, Step 8.1.1, required the technicians to review the lubrication accountability log and verify the correct oil prior to adding it to the EDG.

The inspectors assessed the licensees completed corrective actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition.

These activities constitute completion of one annual follow-up sample, as defined in Inspection Procedure 71152.

b. Findings

A licensee-identified violation associated with this inspection sample is documented in Section 4OA7 of this report.

4OA3 Follow-up of Events and Notices of Enforcement Discretion

(Closed) Licensee Event Report (LER) 05000458/2017-003-00, Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting

a. Inspection Scope

On March 10, 2017, during power ascension testing conducted in the startup after a refueling outage, the reactor operator manually inserted a reactor scram in response to an abnormal increase in steam pressure. Approximately 45 minutes before the scram occurred, a steam leak developed in a tee connection associated with the newly-installed turbine digital electro-hydraulic control (EHC) system. To stop the steam leak, the licensee isolated a piping line that fed two of the three pressure instruments that the digital EHC system used to control turbine valve positions. Given the presence of the leak, those two instruments were already reading pressure erratically, and the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two affected instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading roughly consistent with each other, the system treats their output as the true output.

Consequently, with both of the affected instruments sensing pressure at roughly zero pounds, the digital EHC system began to shut the turbine control valves. The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling them based on the two pressure instruments that had been isolated and that were both reading roughly zero pounds. Power was below the 23.8 percent level, above which turbine bypass valves are required to be operable by technical specifications.

The steam leak was the result of improper installation of the tee connection. The step that directed the installation of the connection into the transmitter tubing line was not properly carried out and was not sufficiently verified in accordance with its designation as a quality control hold point. When contract maintenance personnel in charge of the installation observed leakage from the connection during power ascension, they tightened down on its compression fitting without notifying the control room or obtaining appropriate permission. This action caused the fitting to dislodge, significantly worsening the leak.

The inspectors reviewed the LER associated with the event and determined that the report adequately documented the summary of the event, including the cause of the event and potential safety consequences. The inspectors documented a finding for the licensees failure to properly complete steps of the work order instruction during the installation and inspection of the tee connection. LER 05000458/2017-003-00 is closed.

b. Findings

Introduction.

The inspectors reviewed a Green, self-revealed finding for the licensees failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system. Specifically, the licensee failed to properly install a tee connection in a steam supply line to turbine pressure transmitters in the system, creating conditions for an eventual steam leak that led to a reactor scram.

Description.

On March 10, 2017, a steam leak developed in a tee compression fitting associated with the newly-installed turbine digital EHC system. To stop the steam leak, the licensee isolated a piping line that fed two of three pressure instruments that the digital EHC system used to control turbine valve positions. Prior to this action, the system was controlling turbine valve positions based on the output of the unaffected instrument. When the licensee isolated the piping line, the pressure readings of the two instruments were brought into congruence with each other at roughly zero pounds. The system is designed such that when two instruments are reading consistently with each other, the system treats their output as the true output. Consequently, with both of the affected instruments seeing pressure at roughly zero pounds, the digital EHC system began to close the turbine control valves.

The reactor operator saw the turbine control valves going shut and inserted a manual scram. The plant responded to the scram as designed, without complications. Because the scram occurred from a low power condition, no safety relief valves lifted. The turbine bypass valves did not open because the digital EHC system was controlling their position based on the two pressure instruments that had been isolated and that were reading roughly zero pounds. Power was below the 23.8 percent level above which turbine bypass valves are required to be operable by technical specifications.

The steam leak was a result of improper installation of a tee connection in the line that fed the two affected pressure transmitters. Work order 00438386, Task 24, Step 4.3.8 provided instruction for maintenance personnel to install the tee connection into the transmitter tubing line. This action was not properly carried out, with the tee connection incorrectly fitted up to its compression fitting. An adequate seal was not formed, and therefore, when the line was pressurized, a leak developed. The step was identified in the procedure as a quality control hold point, and therefore the deficient craftsmanship should have been identified by supervisor inspection. However, the Quality Control supervisor failed to observe the satisfactory completion of the step, contrary to site expectations. When maintenance personnel identified leakage from the compression fitting during power ascension, they tightened down on the fitting without obtaining appropriate permission from the control room. This action caused the fitting to dislodge, making the leak significantly worse.

Analysis.

The failure to properly complete steps of an approved procedure during the installation of a modification to the turbine EHC system was a performance deficiency.

The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensees failure to properly install the tee connection caused a steam leak that led to a reactor scram. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions. The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a loss of mitigation equipment relied upon to transition the plant from the onset of a trip to a stable shutdown condition. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority [H.5].

Enforcement.

This finding does not involve an enforcement action because no regulatory requirements were violated. The licensee documented this finding in their corrective action program as Condition Report CR-RBS-2017-02405. This issue is being characterized as finding FIN 05000458/2017003-02, Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting.

These activities constitute completion of one event follow-up sample, as defined in Inspection Procedure 71153.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On July 28, 2017, the inspectors presented the radiation safety inspection results to Mr. M. Chase, Director of Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On August 25, 2017, the inspectors presented the radiation safety inspection results to Mr. J. Reynolds, Operations Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On September 21, 2017, the inspector presented the triennial heat sink performance inspection results to Mr. M. Chase, Director, Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On October 11, 2017, the inspectors presented the integrated inspection results to Mr. W. Maguire, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

4OA7 Licensee-Identified Violations

The following licensee-identified violation of NRC requirements was determined to be of very low safety significance (Green) and meets the NRC Enforcement Policy criteria for being dispositioned as a non-cited violation:

  • Technical Specification 5.4, Procedures, requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.a of Appendix A to Regulatory Guide 1.33 requires that maintenance that can affect performance of safety-related equipment be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, the station did not properly preplan and perform maintenance that can affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Specifically, on May 21, 2017, following completion of a 24-hour surveillance test run of the Division III emergency diesel generator (EDG), mechanical maintenance technicians added 20 gallons of the wrong type of oil to the Division III EDG. This error resulted in the inoperability of the Division III EDG for approximately three days while the incorrect oil was pumped out of the associated fuel oil storage tank and subsequently refilled. This finding was determined to be of very low safety significance (Green) because the finding did not represent an actual loss of function of one or more trains of safety-related equipment for greater than its technical specification allowed outage time. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2017-04128.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Askew, Manager, Supply Chain
D. Burnett, Director, Emergency Planning, Entergy South
S. Carter, Superintendent, Instruments and Controls
M. Chase, Director, Regulatory & Performance Improvement
B. Cole, Corporate Radiation Protection
R. Conner, Manager, Nuclear Oversight
R. Cook, Manager, Security
K. Crissman, Senior Manager, Production
D. Durocher, Supervisor, Code Program
J. Engel, Superintendent, Radiological Operations, Radiation Protection
B. Ford, Senior Manager, Fleet Regulatory Assurance
C. Foster, System Engineer
D. Guess, Engineer
J. Henderson, Manager, Systems & Components Engineering
R. Hilliard, Supervisor, Chemistry
K. Huffstatler, Senior Licensing Specialist, Regulatory Assurance
V. Huffstatler, Senior Health Physicist/Chemistry Specialist, Chemistry
J. Hurst, Manager, Emergency Preparedness
D. Jarnagin, Supervisor, Instruments and Controls
B. Johns, Licensing Specialist, Regulatory Assurance
C. King, Superintendent, Maintenance Support
G. King, Specialist, Radiation Protection
R. Leasure, Superintendent, Radiation Protection
P. Lucky, Manager, Performance Improvement
W. Maguire, Site Vice President
J. McCoy, Assistant Manager, Operations
G. Mermigas, Engineer
J. OConnor, Senior Manager, Maintenance
S. Peterkin, Manager, Radiation Protection
M. Ponzo, Manager, Chemistry
M. Reeves, Supervisor, Radiation Operations
J. Rogers, Supervisor, Engineering
T. Venable, Manager, Operations
M. Runion, Senior Manager, Site Projects and Maintenance Services
D. Sandlin, Manager, Design & Program Engineering
T. Schenk, Manager, Regulatory Assurance
W. Spell, Senior Health Physicist/Chemistry Specialist, Chemistry
K. Stupak, Manager, Training
S. Vazquez, Director, Engineering
S. Vercelli, General Manager, Plant Operations
J. Vukovics, Supervisor, Reactor Engineering
J. Wilson, Manager, Chemistry

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000458/2017003-01 NCV Failure to Account for Delayed Closure of Isolation Valves in the Ultimate Heat Sink Inventory Analysis (Section 1R07)
05000458/2017003-02 FIN Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting (Section 4OA3)

Closed

05000458/2017-003-00 LER Manual Reactor Scram Initiated in Response to Increase in Steam Pressure during Steam Leak Troubleshooting (Section 4OA3)

LIST OF DOCUMENTS REVIEWED