ML20206D280: Difference between revisions

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#REDIRECT [[IR 05000324/1987003]]
{{Adams
| number = ML20206D280
| issue date = 03/26/1987
| title = Safety Insp Repts 50-324/87-03 & 50-325/87-03 on 870201-28, 0303-04.Violation Noted:Failure to Maintain Unit 2 PWR Fuel Storage Capacity
| author name = Fredrickson P, Garner L, Ruland W
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =
| addressee affiliation =
| docket = 05000324, 05000325
| license number =
| contact person =
| document report number = 50-324-87-03, 50-324-87-3, 50-325-87-03, 50-325-87-3, NUDOCS 8704130291
| package number = ML20206D205
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 11
}}
See also: [[see also::IR 05000324/1987003]]
 
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                                                        ~
            .                                              .,,
e
  **
                                                                        s                          ;
                                                                                            '
        p Ktog                                UNITE 3 STATES                                        l
                Do
                                                                  .
                '
                                    NUCLEAR REGULATORY COMMISSION                                  !
  ,8          -
                  ,                            REGION 11                                          I
  g              ,j                    101 MARIETTA STREET.N.W.        .
  *                t                      ATLANTA, GEORGIA 30323 a
  \, * * * * /
    Report Nos. 50-325/87-03 and 50-324/87-03
    Licensee: Carolina Power and Light Company
                    P. O. Box 1551
                    Raleigh, NC 27602
    Docket Nos.: 50-325 and 50-324                        License Nos.: DPR-71 and DPR-62
    Facility Name: Brunswick 1 and 2
    Inspection Conducted: February 1 - 28, 1987 and March 3-4, 1987
    Inspectors:
                g
                      .I. N &
                      , H. Ruland
                                                                                3/16/f7
                                                                                Date Signed
                    9.6.d
                @ LM W. Garner ,
                                                                                slu tt?
                                                                                Date Signed      ,
    Approved by:        .  .                                                  3 /2(> [87
              g P4 Division
                      E. Fredrickson,  Section Chief                            Date Signed
                              of Reactor Projects
                                              SUMMARY
    Scope:      This routine safety inspection involved the areas of maintenance
    observation, surveillance observation, operational safety verification, onsite
    Licensee Event Reports (LER) review, in-office LER review, followup on
    inspector identified and unresolved items, Limitorque Operators, spent fuel
    storage capacity, and refueling activities.
    Results: One violation - failure to maintain Unit 2 PWR spent fuel storage
    capacity, paragraph 11,
                                                                                                  1
        0704130291 870330
        PDR      ADOCK 0D000324
        0                      PDR
 
                                            ,          _ _ .                                                  _ _ _ _ - _ _ _ _ .
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        .
    *
  .
!
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                                    REPORT DETAILS
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i
    1. Persons Contacted
      Licensee Employees
      P. Howe, Vice President - Brunswick Nuclear Project
l      C. Dietz, General Manager - Brunswick Nuclear Project
'
      T. Wyllie, Manager - Engineering and Construction
      J. Holder, Manager - Outages
      R. Eckstein, Manager - Technical Support
      E. Bishop, Manager - Operations
l      L. Jones, Director - Quality Assurance (QA)/ Quality Control (QC)-
      R. Helme, Director - Onsite Nuclear Safety - BSEP
      J. Chase, Assistant to General Manager
      J. O'Sullivan, Manager - Maintenance
      G. Cheatham, Manager - Environmental & Radiation Control
      J. Smith, Manager - Administrative Support
      K. Enzor, Director - Regulatory Compliance
      A. Hegler, Superintendent - Operations
,      W. Hogle, Engineering Supervisor
l      B. Wilson, Engineering Supervisor
l      B. Parks, Engineering Supervisor
      R.Creech,I&C/ElectricalMaintenanceSupervisor(Unit 2)
      R. Warden, ISC/ Electrical Maintenance Supervisor (Unit 1)
      W. Dorman, Supervisor - QA
      W. Hatcher Supervisor - Security
      R. Kitchen,MechanicalMaintenanceSupervisor(Unit 2)
!      C. Treubel, Mechanical Maintenance Supervisor (Unit 1)
      R. Poulk, Senior NRC Regulatory Specialist
      W. Murray, Senior Engineer - Nuclear Licensing Unit
;      Otiler licensee employees contacted included construction craftsmen,
'
      engineers, technicians, operators, office personnel, and security force
      members.
1
    2. ExitInterview(30703)
l      The inspection scope and findings were summarized on March 3,1987, with
'
      the general manager and vice-president. The violation, excess capacity in
      the Unit 2 spent fuel pool (paragraph 11), was discussed in detail. The
i      inspector stated that the item was unresolved pending inspector discussion
      with regional management.    On March 4, 1987, the licensee was informed by
'
      the inspector that the spent fuel pool issue was a violation.                                        The
i      licensee agreed to address the issue of board walkdowns/ reviews
      (paragraph 6) along with the response to the violation. The licensee
l      acknowledged the findings without exception. The licensee did not
l      identify as proprietary any of the materials provided to or reviewed by
      the inspectors during the inspection.
                                                                      _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .
 
        .
    -
  .
,
                                            2
    3. Followup on Previous Enforcement Matters (92702)
      Not inspected.
;  4. Maintenance Observation (62703)
      The inspectors observed maintenance activities and reviewed records to
      verify that work was conducted in accordance with approved procedures,
      Technical Specifications, and applicable industry codes and standards. The
      inspectors also verified that:      redundant components were operable;
      administrative controls were followed; tagouts were adequate; personnel
      were qualified; correct replacement parts were used; radiological controls
      were proper; fire protection was adequate; quality control hold points
      were adequate and observed; adequate post-maintenance testing was
      performed; and independent verification requirements were implemented.
      The inspectors independently verified that selected equipment was properly
      returned to service.
      Outstanding work requests were reviewed to ensure that the licensee gave
      priority to safety-related maintenance.
.
      The inspectors observed / reviewed portions of the following maintenance
      activities:
            MP-09          Dryer / Separator, Cattle Chute, and Fuel Pool Gates
                            Removal and Installation.
              OLP-NVT001    Topaz Static Inverter and Lambda Power Supply.
              WR&A-87-AGEB1 Repair of Unit 2 Annunciation Horn Circuit.
      During performance of work request 87-AGEB1, the inspector observed a
      communication problem between operations and maintenance personnel. At
'
      first, the annunciator horn being repaired, could not be silenced. Later,
j      the horn stopper' continuously sounding and would not sound when another
!      annunciator came in. Operations was aware of this and took proper
      compensatory actions, e. g., assigned sections of the board to individuals
      to note when a new annunciator came in. The first problem was correctly
      conmunicated to maintenance; however, the change in symptoms was not.
      Operations assumed the change was due to Instrumentation and Control (I&C)
      trouble shooting activities.      The inspector informed the maintenance
      personnel of the second item approximately 30 minutes after it happened.
      Although the inspector was confident that the problem would have been
      fixed, the failure of operations personnel to recognize that a new
      condition existed versus a condition induced by I&C personnel performing
      trouble shooting or repair, was a concern. Inadequate communication can
      noticeably increase the length of time an unsatisfactory condition exists.
      This matter was discussed with cognizant supervision.
      No violations or deviations were identified.
 
                                                                                                            <
                                    .
                  ,
                    ..
                                                                                      3
                      5.    SurveillanceObservation(61726)
                            The inspectors observed surveillance testing required by Technical
                            Specifications. Through observation and record review, the inspectors
                            verified that: tests conformed to Technical Specification requirements;
                            administrative controls were followed; personnel were qualified;
                              instrumentation was calibrated; and data was accurate and complete.                        The
                              inspectors independently verified selected test results and proper return
                            to service of equipment.
                            The inspectors witnessed / reviewed portions of the following test
                            activities:
                                                        IMST-DG12R    Diesel Generator DG-2 Loading Test.
                                                        2MST-APRM12    Average Power Range Monitor (APRM), (Ch. 8, D & F)
                                                                      Channel Functional Test (Reactor Protection System
                                                                      (RPS) Inputs].
                                                        2MST-ATWS22M  Anticipated Transcient Without Scram (ATWS) Reactor
                                                                      High Pressure Trip Instrument Channel Calibration.
                                                        2MST-RHR21M    Residual Heat Removal (RHR) - Low Pressure Coolant
                                                                      Injection (LPCI), Core Spray System (CSS) and HPCI Hi
                                                                      Drywell Pressure Trip Unit Channel Calibration.
                                                        PT-12.8        Electrical Power Systems Operability Test.
                              During performance of IMST-DG12R on February 17, 1987, the licensee
                                identified that step 7.4.30 had not been performed correctly. The step
                              requires stopping of the core spray pump while supplying rated flow to
                              verify that the DG does not trip.                          This is a surveillance requirement
                              specified in Technical Specification (TS) .4.8.1.1.2.d.2. The operator
                                reduced the flow prior to stopping the pumb. This is the method normally
                              used to stop the pump as required by either the quarterly required
                              Surveillance Test Procedure PT-07.2.4b, or the Operating Procedure OP-18.
                              The licensee verified that during another performance of MST-DG12R, the
                                step was satisfactorily performed. This item meets all the requirements
                                to be considered as a licensee identified violation. The licensee is
                                preparing an Operating Experience Report (0ER) to address the root cause
                                of the communication failure between the I&C personnel in charge of the
                                test and the control operator. The inspector plans to review the OER when
                                issued.                    This is an Inspector Followup Item:      Review of IMST-DG12R
                                ProcedureViolationOER(325/87-03-03).
                              One licensee identified violation and no deviations were identified.
                      6.      Operational Safety Verification (71707)                                                          )
                                                                                                                              T
. _ - _ _ - _ _ _        _ _ - _ _ _ _ _ _ _ _ _ _ - _
 
        - .        .. .      - ..          .            -        - - . . .      .      - - .
k
                .
      .
            ..
)
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                                                      4
1-
l-
:              The inspectors verified conformance with regulatory requirements by direct
,
              . observations of activities, facility tours, discussions with personnel,
                reviewing of records and independent-verification.of safety. system status.
1
!              The inspectors verified that control room manning requirements of 10 CFR
<
                50.54 and the Technical Specifications were-met. . Control room, shift
<
                supervisor, and clearance logs were reviewed to obtain information-
j              concerning operating trends and out of service safety systems to ensure
'
                that there were no conflicts with Technical Specifications Limiting
:              Conditions for Operations. Direct observations were conducted of control
'
                room panels, instrumentation and recorder traces important to safety to
a              verify operability and that parameters were within~ Technical Specification
]              limits. The inspectors observed shift turnovers to verify that continuity
;.              of system status was maintained. :The' inspectors verified the status of
                selected control room annunciators.
1
i              Operability of ' a selected Engineered ' Safety Feature (ESF) train was -
i              verified by insuring that:      each accessible valve in the flow path was in
;              its correct position; each power supply' and breaker,. including control
                room fuses, were aligned for components that must activate upon initiation
;              signal; removal of power from those - ESF motor-operated valves, so
                identified by Technical Specifications, was completed; there was. no
                                                                  ~
1
1
                leakage of major components; there was proper lubrication and cooling
i              water available; and a condition did. not exist which might prevent
.
                fulfillment of the system's functional requirements. Instrumentation
i              essential to system actuation or performance was. verified operable by
                observing on-scale indication and proper instrument valve lineup, if
'
j              accessible.
                The    inspectors verified    that the licensee's health physics
J              policies / procedures were followed.      This includod a review of area
,
                surveys, radiation work permits, posting, and instrument calibration.
j- '
    .
                The inspectors verified that:        the security. organization was properly
{              manned and security personnel were capable of performing their assigned
4
                functions; persons and packages were checked prior to entry into the
!              protected area (PA); vehicles were properly authorized, searched and
;              escorted within the PA; persons within the PA ~ displayed photo
:              identification badges; personnel in vital areas were authorized; and
                effective compensatory measures were employed when required.
!
i              On February 1, -1987, the inspector found a vital area door closed but            !
'
                unlatched.      While an unauthorized person could have opened the door, the    l
i
                security computer would have detected the intrusion, enabling the security        j
>              force to respond. The inspector reported the condition to security. A
{              security member responded in a timely manner, verified the condition and
                took action as required.
                                                                                                  .
i              The inspectors also observed plant housekeeping controls, verified
!              position of certain containment isolation valves, and verified ' the
i              operability of onsite and offsite emergency power sources.-
1
                                                                                  4
i
i
                                                                              '
k                                                                                h
 
        .
,
  ..
                                              5
        On February 2,1987, the inspector observed the Unit 2 A and 6 trains of
        Standby Gas Treatment (SBGT) system with loose blower and motor pedestal
        mounting rubber bushing retaining bolts. The licensee issued work
        requests 87-ADJIl and 87-ADJJ1 to correct the deficiency. The licensee
        inspected Unit I and issued work requests ADJK1 and ADJL1 to correct
        similar deficiencies on Unit 1 SBGT trains A and B. Technical support
        reviewed the "as found" condition and determined that the condition had
        not rendered the SBGT trains inoperable.
        On February 12, 1987, at 7:50 a.m., the inspector found valve 1-E11-F007B,
        the Division II RHR minimuni flow valve, open instead of closed. The valve
        had remained open after the licensee had performed OP-17, RHR Operating
        Procedure    Section 8.7, draining the suppression pool to radwaste.
        Valve]-Ell F007B auto-opened when the RHR pump was started, but no
        procedure step existed to manually reshut the valve. Thus, the valve was
        in the position required by the last procedure performed on the RHR
        system.    However, the licensee reported that the evolution had occurred
        two shifts prior to discovery.      Therefore, three shifts and two shift
        turnovers failed to identify the mi:; positioned valve.  The Plant General
        Manager agreed to address this issue, weakness in board walkdowns and
        board review after valve manipulations, when responding to the violation
        issued with this report.    This is an Inspector Followup Item: Inadequate
        Board Walkdown and Review (325/87-03-04).
        No violations or deviations were identified.
    7. Onsite Review of Licensee Event Reports (92700)
        The listed Licensee Event Reports (LERs) were reviewed to verify that the
        inforr.ation provided met NRC reporting requirements. The verification
        included adequacy of event description and corrective action taken or
        planned, existence of potential generic problems and the relative safety
        significance of the event.      Onsite inspections were performed and
        concluded that necessary corrective actions have been taken in accordance
        with existing requirements, licensee conditions and commitments.
        (CLOSED)    LER 1-86-13, Control Building Emergency Air Filtration System
        Start Due to Corrosion on Radiation Monitor Sensor Converter. The
        inspector verified that the applicable Maintenance Procedure, MI-26-11A,
        was revised July 29, 1986, to include inspection for corrosion as
        comitted to in the LER.    A sign-off on the data sheet was also provided
        to document the review.
        (OPEN)    LER 1-87-01, Failure of Unit 1 HPCI System Turbine Steam Supply
        Valve E41-F002 to Open. The licensee discovered a failed auxiliary
        contact adder block assembly during the followup to the valve failure.
        The auxiliary contact block assemblies are attached to the main contactor
        in each breaker compartment, with from one to six auxiliary blocks per
        breaker. There are over 3000 auxiliary contact blocks on site in both Q
        and non Q app'eications. The licensee sent several auxiliary contact
        blocks to General Electric (GE) for failure analysis. GE reported to the
                                                                                    .
 
        '
,
  .-
                                            6
      licensee that the supplied blocks (CR205X100E) failed because dimensional
      problems caused excess wear of the movable plunger, allowing the plunger
      to eventually stick inside the block, preventing the contact and thus the
      valve from moving.
      Further licensee investigation revealed a potential generic problem with
      the auxiliary cor. tact adder block. Maintenance record searches by the
      licensee turned up over 50 potential auxiliary contactor problems since
      1982. GE has redesigned the auxiliary contact adder block (new part No.
      CR305X100E) and it appears that the new design is not susceptible to the
      binding problem. Further inspection of this item will be conducted after
      the licensee issues an LER supplement due May 22, 1987.
      (CLOSED)    LER 2-86-13, Failure to Prcperly Verify Reactor Protection
      System (RPS) Shorting Links Installed During Testing Causes Full RPS Trip
      During Refueling. The in5pector verified via the training report that
      members of the I&C crews were trained on proper verification of
      installation of the RPS shorting links.      The training class syllabus
      adequately addressed the item. It required class participants to field
      verify that the shorting links were in place.
      (CLOSED)                                          . Level Scram During Pipe
      Flushing Due LER
                      to 2-86-16,
                        PersonnelAutomatic
                                    Error. TheLowinspect
                                                  Water,'or verified that the lesson
      plan associated with the committed real time training satisfactorily
      discussed the circumstances surrounding the event and the lessons which
      can be learned.
        (CLOSED)  LER 2-86-24, Inadvertent Emergency Core Cooling System (ECCS)
      Actuation During Refueling Outage Due to Personnel Error. The inspector
      reviewed the documentation which demonstrated that new tags were
        installed. The inspector visually verified that the tags were in place on
      the Unit 1 Division ECCS inverters and power supplies on February 24,
      1987.
      No violations or deviations were identified.
    8.  In Office LER Review (90712)
      The listed LERs were reviewed to verify that the information provided met
      NRC reporting requirements. The verification included adequacy of event
      description and corrective action taken or planned, existance of potential
      generic problems and the relative safety significance of the avent.
        (CLOSED) LER 1-86-17, Late Performance of Required Hourly Fire Watches.
        (CLOSED)    LER 1-86-18, Output Breaker EPA-2, Reactor Protection System
        (RPS) Motor Generator 1A, Tripped Unexpectedly to De-energize RPS Bus A;
      Cause - Undetermined.
 
        .
,
  .-
                                              7
        (CLOSED)    LER 1-86-23, Technical Specification (TS) 3.0.3 Entered Due to
        Inoperability of the Unit 1 Reactor Core Spray Subsystem B and RHR Low
        Pressure Coolant Injection Loop.
        (CLOSED)    LER 1-86-32, Failure to Functionally Test Relay TR/2 in Logic
        Channels A2, A4, B2 and B4 Primary Containment Isolation Instruments
        B21-TS-3229-3232; Procedure Deficiency.
        (CLOSED)    LER 2-86-04, Primary Containment Group 6 Isolation / Automatic
        Isolation of Reactor Building Ventilation System and Automatic Starting of
        Standby Gas Treatment System Occurred; Cause - Electrical Shorting.
        (CLOSED)    LER 2-86-07, High Radiation Alarm Trip of Reactor Building
        Ventilation Exhaust Radiation Monitor D12-RM-N010B; Due to Electrical
        Grounding of the Monitor Power Lead.
        (CLOSED)    LER 2-86-09, Upscale Trip of Instrument Trip Unit to Reactor
        Building Exhaust Ventilation Monitor D12-RM-N010B: Cause Could Not Be
        Determined.
        (CLOSED)    LER 2-86-11, Reactor Water Cleanup System Inlet Primary
        Containment Outboard Isolation Valve, Automatically Closed; Cause - Fuse
        F18 Blew.
        (CLOSED)    LER 2-86-14, Upscale Trip of Reactor Power Intermediate Range
        Monitor D Occurred When Control Rod 02-19 Was Selected in Reactor Manual
        Control System While Performing PT-18.1; Cause - Electronic Noise Spike.
        (CLOSED)  LER 2-86-22, Unit 2 Shutdown in Accordance With TS 3.4.1.1 Due
        to a Lockout / Trip of the Recirculation Pump Motor Generator Set.
        No violations or deviations were identified.
    9. Followup on Inspector Identified and Unresolved Items (92701)
        (OPEN) Inspector Followup Item, (325/84-04-01 and 324/84-04-01), Licensee
        to Identify and Repair Cab *ie Tray Raceway Z Clamps Problems. The I clamps
        secure the tray to the horizontal tray support.      The inspector reviewed
        completed work requests 1-E84-1658 and 2-E84-2009 which documented
        completion of this particular inspection and repair. The inspector          '
        performed an inspection of safety related cable trays 50F/DA and 50M/DA in
        the Unit 2 control room on February 22. Of twenty four Z clamps installed
        on these trays, five were bent such that they were not engaged with the
        tray top, four others had loose I clamp nuts, and three others were turned
        to the side. In addition, two Z clamps were missing. The inspector also
        observed several tray covers which were not in their proper place. Based
        on discussions with the architect / engineer, the licensee determined that
        the "as found" condition of these two trays would not render the raceway
        inoperble or adversely effect the cables in the trays.
 
                                                                                      _ _ _ _ _ _ - _ _ _ _ _ _ _ .
            .
  .
    .-
                                                  8
            Discussion with Quality Assurance (QA) personnel revealed that an
            outstanding non-conformance report (NCR), number E-86-002, involving cable
            tray covers had been issued on July 1,1986, but a review of the NCR
            responses by the QC supervisor and the inspector showed that poor work
            control practices which allowed the 2 clamp problems to occur had not been
            specifically addressed. Hence, both the licensee and the inspector have
            determined that the responses were inadequate. On February 27, 1987,
            licensee QA issued a Notice of Deficiency against this NCR in accordance
            with QA procedure 0QA-104, which required correction of the inadequate
            response within seven days.
            This item will remain open pending final resolution of NCR E-86-002 and
            the Notice of Deficiency and subsequent review by the inspector.
            No violations or deviations were identified.
      10. LimitorqueOperators(71707)
            The licensee has recently procured information from Limitorque Corporation
            concerning actuator sizing and settings on both safety and non-safety
            related valves. The data was recently reviewed (December - January) and
            compiled from original design documents into a new format at the
            licensee's request. Review of the data sheets showed that Limitorque was
            now recommending upgrade of some actuator motors to a larger size.
            Apparently, Limitorque had used 100% full voltage to size the motors,
            instead of the currently specified degraded supply of 85%. Reviews of
            documents between the licensee, the valve manufacturer and the valve
            manufacturer's subcontractor (Limitorque), has not been able to determine
            what was specified to Limitorque (or by whom) when the original plant
            equipment was procured. The licensee has evaluated this condition on the
            applicable safety related valves and has determined that these valves
            would function under design conditions.        The affected valves are:
            E41-F002, High Pressure Coolant Injection (HPCI) inboard steam line
            isolation valve; E41-F004, HPCI condensate storage tank suction valve;
            E41-F008, HPCI full flow test isolation valve; E11-F017A and B, RHR system
            outboard isolation valves; and E11-F024A and B, suppression pool test
            return isolation valve. The inspector has reviewed the justification for
            continued operation for Unit 2 contained in Engineering Evaluation
            EER-87-0088. In summary, the evaluation concludes that no safety problem
            exists based upon either application and/or electrical distribution
            voltage studies. The voltage studies determined that the degraded voltage
            of some of the valves would not drop below 85%. Under these anticipated
            voltages, there is no motor sizing concern. In addition, contact with the
            applicable valve vendors, Anchor Darling and Rockwell, revealed that they
            perfonn their own sizing and setting calculations.      Of three valves.
            reviewed by Anchor Darling, a degraded voltage of 85% was used. A list of
            the other valves has been supplied to the vendors to verify exactly what
,
            value was used.
            The licensee has contracted with B&W to review the Limitoroue data sheets,
            calculations and generally assist in resolving the concerns. Their review
                                                                      - . _ - , . _ -
 
                                                                                      _ - _ _ _
          .
.
  .-
                                                9
          has indicated potential problems with Limitorque data sheets.        Two DC
          motor powered actuators had been treated as AC powered.    In addition, one
          of these had the wrong pull-out efficiency used for the overall unit ratio
          (motor design speed-RPM / actuator speed RPM). Apparently the wrong value
          had been taken from the Limitorque Gate and Globe Valve Efficiency Chart.
          The actuators involved were SMB-3 and SMB-000. Another valve with an
          SMB-5T actuator also had the wrong pull-out efficiency used in the torque
          switch calculation. This was attributed to using the wrong motor speed
          when obtaining values from the Gate and Globe Valve Efficiency Chart.
          The licensee is continuing his review. This is an Inspector Followup
          Item: Potential Problems with Limitorque Data Sheets (324/87-03-02).
          No violations or deviations were identified.
    11. Spent Fuel Storage Capacity (59095)
          The inspectors reviewed the available storage capacity in the Unit 1 and
          Unit 2 spent fuel storage pools to determine if full core offload
          capability existed for each unit.      Based on discussions with licensee
          personnel and review of the licensee's fuel map, full offload capability
          (560 assemblies) existed. Unit 2 Spent Fuel Pool (SFP) has room for 566
          more BWR assemblies:
                          1839      allowed by TS
                        -
                            36      displaced by a PWR rack
                        - 36        rack not installed
                        -
                              I      contains stuck blade guide
                        -
                              2      boral sample stations
                        - 442      not yet installed
                          1322      available spaces
                        - 756      assemblies in pool
                          ~566      BWR spaces available
          Unit 1 SFP has room for 925 more BWR assemblies:
                          1803      allowed by TS
                        -  36      rack not installed
                        -    2      boral sample stations
                          T7EE      available spaces
                        - 840      assemblies in pool
                            975      BWR spaces available
          The above data is as of February 15, 1987.
          The inspector noted that each SFP contained 10 PWR spent fuel modules each
          capable of storing 16 assemblies for a PWR capacity in each pool of 160
          PWR assemblies. The Unit 1 SFP contained 160 assemblies while the Unit 2
          pool contained 144 assemblies. However, Unit 2 Technical Specification
          5.6.3 states that, "the fuel storage pool is designed and shall be
          maintained with a storage capacity limited to no more than 144 PWR fuel
 
,_                                                                                                ,
            .
              ..
                                                          10
I
                    assemblies and 1839 BWR fual assemblies.    The extra 16 storage locations
                      in the Unit 2 SFP pose no safety problem since the Unit 1 SFP has been
                    reviewed and approved by NRR, contains 160 PWR assemblies and locations,
                    also contains additional high density racks, and is essentially identical
                    to the Unit 2 SFP. The excess storage capacity in the Unit 2 SFP is a
                    violation of TS 5.6.3: Failure to Meet TS 5.6.3 Regarding Spent Fuel Pool
l                    PWR Capacity (324/87-03-01).
!
j                    One violation and no deviations were identified.
                12. RefuelingActivities(60705)
                    Selected refueling activities were witnessed and reviewed by the
                      inspector. These included verification that:
                      -    The fuel pool gates were removed per MP-09.
l                    -
                            Surveillance requirements of Technical Specification 4.9.6 associated
l
                            with refueling bridge interlocks were performed prior to fuel
                            movement.
                      -    Number of operable SRM's per Technical Specification 3.9.2.a. and b.
                            were maintained.
                      -    Continues communications between the refueling bridge and the control
                            room were established per Technical Specification 3.9.5.
                      -
                            Fuel movements were conducted in accordance with operating procedures
                            and the Fuel Movement Sheets.
                      The last activity was performed during a two hour inspection conducted on
                      the refueling bridge during fuel movements.
                      No violations or deviations were identified.
l
i
.
                                                                                                    l
                                                                                                    1
  _ _ _ _ _
}}

Latest revision as of 23:21, 19 December 2021

Safety Insp Repts 50-324/87-03 & 50-325/87-03 on 870201-28, 0303-04.Violation Noted:Failure to Maintain Unit 2 PWR Fuel Storage Capacity
ML20206D280
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 03/26/1987
From: Fredrickson P, Garner L, Ruland W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20206D205 List:
References
50-324-87-03, 50-324-87-3, 50-325-87-03, 50-325-87-3, NUDOCS 8704130291
Download: ML20206D280 (11)


See also: IR 05000324/1987003

Text

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p Ktog UNITE 3 STATES l

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NUCLEAR REGULATORY COMMISSION  !

,8 -

, REGION 11 I

g ,j 101 MARIETTA STREET.N.W. .

\, * * * * /

Report Nos. 50-325/87-03 and 50-324/87-03

Licensee: Carolina Power and Light Company

P. O. Box 1551

Raleigh, NC 27602

Docket Nos.: 50-325 and 50-324 License Nos.: DPR-71 and DPR-62

Facility Name: Brunswick 1 and 2

Inspection Conducted: February 1 - 28, 1987 and March 3-4, 1987

Inspectors:

g

.I. N &

, H. Ruland

3/16/f7

Date Signed

9.6.d

@ LM W. Garner ,

slu tt?

Date Signed ,

Approved by: . . 3 /2(> [87

g P4 Division

E. Fredrickson, Section Chief Date Signed

of Reactor Projects

SUMMARY

Scope: This routine safety inspection involved the areas of maintenance

observation, surveillance observation, operational safety verification, onsite

Licensee Event Reports (LER) review, in-office LER review, followup on

inspector identified and unresolved items, Limitorque Operators, spent fuel

storage capacity, and refueling activities.

Results: One violation - failure to maintain Unit 2 PWR spent fuel storage

capacity, paragraph 11,

1

0704130291 870330

PDR ADOCK 0D000324

0 PDR

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REPORT DETAILS

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1. Persons Contacted

Licensee Employees

P. Howe, Vice President - Brunswick Nuclear Project

l C. Dietz, General Manager - Brunswick Nuclear Project

'

T. Wyllie, Manager - Engineering and Construction

J. Holder, Manager - Outages

R. Eckstein, Manager - Technical Support

E. Bishop, Manager - Operations

l L. Jones, Director - Quality Assurance (QA)/ Quality Control (QC)-

R. Helme, Director - Onsite Nuclear Safety - BSEP

J. Chase, Assistant to General Manager

J. O'Sullivan, Manager - Maintenance

G. Cheatham, Manager - Environmental & Radiation Control

J. Smith, Manager - Administrative Support

K. Enzor, Director - Regulatory Compliance

A. Hegler, Superintendent - Operations

, W. Hogle, Engineering Supervisor

l B. Wilson, Engineering Supervisor

l B. Parks, Engineering Supervisor

R.Creech,I&C/ElectricalMaintenanceSupervisor(Unit 2)

R. Warden, ISC/ Electrical Maintenance Supervisor (Unit 1)

W. Dorman, Supervisor - QA

W. Hatcher Supervisor - Security

R. Kitchen,MechanicalMaintenanceSupervisor(Unit 2)

! C. Treubel, Mechanical Maintenance Supervisor (Unit 1)

R. Poulk, Senior NRC Regulatory Specialist

W. Murray, Senior Engineer - Nuclear Licensing Unit

Otiler licensee employees contacted included construction craftsmen,

'

engineers, technicians, operators, office personnel, and security force

members.

1

2. ExitInterview(30703)

l The inspection scope and findings were summarized on March 3,1987, with

'

the general manager and vice-president. The violation, excess capacity in

the Unit 2 spent fuel pool (paragraph 11), was discussed in detail. The

i inspector stated that the item was unresolved pending inspector discussion

with regional management. On March 4, 1987, the licensee was informed by

'

the inspector that the spent fuel pool issue was a violation. The

i licensee agreed to address the issue of board walkdowns/ reviews

(paragraph 6) along with the response to the violation. The licensee

l acknowledged the findings without exception. The licensee did not

l identify as proprietary any of the materials provided to or reviewed by

the inspectors during the inspection.

_ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .

.

-

.

,

2

3. Followup on Previous Enforcement Matters (92702)

Not inspected.

4. Maintenance Observation (62703)

The inspectors observed maintenance activities and reviewed records to

verify that work was conducted in accordance with approved procedures,

Technical Specifications, and applicable industry codes and standards. The

inspectors also verified that: redundant components were operable;

administrative controls were followed; tagouts were adequate; personnel

were qualified; correct replacement parts were used; radiological controls

were proper; fire protection was adequate; quality control hold points

were adequate and observed; adequate post-maintenance testing was

performed; and independent verification requirements were implemented.

The inspectors independently verified that selected equipment was properly

returned to service.

Outstanding work requests were reviewed to ensure that the licensee gave

priority to safety-related maintenance.

.

The inspectors observed / reviewed portions of the following maintenance

activities:

MP-09 Dryer / Separator, Cattle Chute, and Fuel Pool Gates

Removal and Installation.

OLP-NVT001 Topaz Static Inverter and Lambda Power Supply.

WR&A-87-AGEB1 Repair of Unit 2 Annunciation Horn Circuit.

During performance of work request 87-AGEB1, the inspector observed a

communication problem between operations and maintenance personnel. At

'

first, the annunciator horn being repaired, could not be silenced. Later,

j the horn stopper' continuously sounding and would not sound when another

! annunciator came in. Operations was aware of this and took proper

compensatory actions, e. g., assigned sections of the board to individuals

to note when a new annunciator came in. The first problem was correctly

conmunicated to maintenance; however, the change in symptoms was not.

Operations assumed the change was due to Instrumentation and Control (I&C)

trouble shooting activities. The inspector informed the maintenance

personnel of the second item approximately 30 minutes after it happened.

Although the inspector was confident that the problem would have been

fixed, the failure of operations personnel to recognize that a new

condition existed versus a condition induced by I&C personnel performing

trouble shooting or repair, was a concern. Inadequate communication can

noticeably increase the length of time an unsatisfactory condition exists.

This matter was discussed with cognizant supervision.

No violations or deviations were identified.

<

.

,

..

3

5. SurveillanceObservation(61726)

The inspectors observed surveillance testing required by Technical

Specifications. Through observation and record review, the inspectors

verified that: tests conformed to Technical Specification requirements;

administrative controls were followed; personnel were qualified;

instrumentation was calibrated; and data was accurate and complete. The

inspectors independently verified selected test results and proper return

to service of equipment.

The inspectors witnessed / reviewed portions of the following test

activities:

IMST-DG12R Diesel Generator DG-2 Loading Test.

2MST-APRM12 Average Power Range Monitor (APRM), (Ch. 8, D & F)

Channel Functional Test (Reactor Protection System

(RPS) Inputs].

2MST-ATWS22M Anticipated Transcient Without Scram (ATWS) Reactor

High Pressure Trip Instrument Channel Calibration.

2MST-RHR21M Residual Heat Removal (RHR) - Low Pressure Coolant

Injection (LPCI), Core Spray System (CSS) and HPCI Hi

Drywell Pressure Trip Unit Channel Calibration.

PT-12.8 Electrical Power Systems Operability Test.

During performance of IMST-DG12R on February 17, 1987, the licensee

identified that step 7.4.30 had not been performed correctly. The step

requires stopping of the core spray pump while supplying rated flow to

verify that the DG does not trip. This is a surveillance requirement

specified in Technical Specification (TS) .4.8.1.1.2.d.2. The operator

reduced the flow prior to stopping the pumb. This is the method normally

used to stop the pump as required by either the quarterly required

Surveillance Test Procedure PT-07.2.4b, or the Operating Procedure OP-18.

The licensee verified that during another performance of MST-DG12R, the

step was satisfactorily performed. This item meets all the requirements

to be considered as a licensee identified violation. The licensee is

preparing an Operating Experience Report (0ER) to address the root cause

of the communication failure between the I&C personnel in charge of the

test and the control operator. The inspector plans to review the OER when

issued. This is an Inspector Followup Item: Review of IMST-DG12R

ProcedureViolationOER(325/87-03-03).

One licensee identified violation and no deviations were identified.

6. Operational Safety Verification (71707) )

T

. _ - _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _

- . .. . - .. . - - - . . . . - - .

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4

1-

l-

The inspectors verified conformance with regulatory requirements by direct

,

. observations of activities, facility tours, discussions with personnel,

reviewing of records and independent-verification.of safety. system status.

1

! The inspectors verified that control room manning requirements of 10 CFR

<

50.54 and the Technical Specifications were-met. . Control room, shift

<

supervisor, and clearance logs were reviewed to obtain information-

j concerning operating trends and out of service safety systems to ensure

'

that there were no conflicts with Technical Specifications Limiting

Conditions for Operations. Direct observations were conducted of control

'

room panels, instrumentation and recorder traces important to safety to

a verify operability and that parameters were within~ Technical Specification

] limits. The inspectors observed shift turnovers to verify that continuity

. of system status was maintained.
The' inspectors verified the status of

selected control room annunciators.

1

i Operability of ' a selected Engineered ' Safety Feature (ESF) train was -

i verified by insuring that: each accessible valve in the flow path was in

its correct position; each power supply' and breaker,. including control

room fuses, were aligned for components that must activate upon initiation

signal; removal of power from those - ESF motor-operated valves, so

identified by Technical Specifications, was completed; there was. no

~

1

1

leakage of major components; there was proper lubrication and cooling

i water available; and a condition did. not exist which might prevent

.

fulfillment of the system's functional requirements. Instrumentation

i essential to system actuation or performance was. verified operable by

observing on-scale indication and proper instrument valve lineup, if

'

j accessible.

The inspectors verified that the licensee's health physics

J policies / procedures were followed. This includod a review of area

,

surveys, radiation work permits, posting, and instrument calibration.

j- '

.

The inspectors verified that: the security. organization was properly

{ manned and security personnel were capable of performing their assigned

4

functions; persons and packages were checked prior to entry into the

! protected area (PA); vehicles were properly authorized, searched and

escorted within the PA; persons within the PA ~ displayed photo
identification badges; personnel in vital areas were authorized; and

effective compensatory measures were employed when required.

!

i On February 1, -1987, the inspector found a vital area door closed but  !

'

unlatched. While an unauthorized person could have opened the door, the l

i

security computer would have detected the intrusion, enabling the security j

> force to respond. The inspector reported the condition to security. A

{ security member responded in a timely manner, verified the condition and

took action as required.

.

i The inspectors also observed plant housekeeping controls, verified

! position of certain containment isolation valves, and verified ' the

i operability of onsite and offsite emergency power sources.-

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On February 2,1987, the inspector observed the Unit 2 A and 6 trains of

Standby Gas Treatment (SBGT) system with loose blower and motor pedestal

mounting rubber bushing retaining bolts. The licensee issued work

requests 87-ADJIl and 87-ADJJ1 to correct the deficiency. The licensee

inspected Unit I and issued work requests ADJK1 and ADJL1 to correct

similar deficiencies on Unit 1 SBGT trains A and B. Technical support

reviewed the "as found" condition and determined that the condition had

not rendered the SBGT trains inoperable.

On February 12, 1987, at 7:50 a.m., the inspector found valve 1-E11-F007B,

the Division II RHR minimuni flow valve, open instead of closed. The valve

had remained open after the licensee had performed OP-17, RHR Operating

Procedure Section 8.7, draining the suppression pool to radwaste.

Valve]-Ell F007B auto-opened when the RHR pump was started, but no

procedure step existed to manually reshut the valve. Thus, the valve was

in the position required by the last procedure performed on the RHR

system. However, the licensee reported that the evolution had occurred

two shifts prior to discovery. Therefore, three shifts and two shift

turnovers failed to identify the mi:; positioned valve. The Plant General

Manager agreed to address this issue, weakness in board walkdowns and

board review after valve manipulations, when responding to the violation

issued with this report. This is an Inspector Followup Item: Inadequate

Board Walkdown and Review (325/87-03-04).

No violations or deviations were identified.

7. Onsite Review of Licensee Event Reports (92700)

The listed Licensee Event Reports (LERs) were reviewed to verify that the

inforr.ation provided met NRC reporting requirements. The verification

included adequacy of event description and corrective action taken or

planned, existence of potential generic problems and the relative safety

significance of the event. Onsite inspections were performed and

concluded that necessary corrective actions have been taken in accordance

with existing requirements, licensee conditions and commitments.

(CLOSED) LER 1-86-13, Control Building Emergency Air Filtration System

Start Due to Corrosion on Radiation Monitor Sensor Converter. The

inspector verified that the applicable Maintenance Procedure, MI-26-11A,

was revised July 29, 1986, to include inspection for corrosion as

comitted to in the LER. A sign-off on the data sheet was also provided

to document the review.

(OPEN) LER 1-87-01, Failure of Unit 1 HPCI System Turbine Steam Supply

Valve E41-F002 to Open. The licensee discovered a failed auxiliary

contact adder block assembly during the followup to the valve failure.

The auxiliary contact block assemblies are attached to the main contactor

in each breaker compartment, with from one to six auxiliary blocks per

breaker. There are over 3000 auxiliary contact blocks on site in both Q

and non Q app'eications. The licensee sent several auxiliary contact

blocks to General Electric (GE) for failure analysis. GE reported to the

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licensee that the supplied blocks (CR205X100E) failed because dimensional

problems caused excess wear of the movable plunger, allowing the plunger

to eventually stick inside the block, preventing the contact and thus the

valve from moving.

Further licensee investigation revealed a potential generic problem with

the auxiliary cor. tact adder block. Maintenance record searches by the

licensee turned up over 50 potential auxiliary contactor problems since

1982. GE has redesigned the auxiliary contact adder block (new part No.

CR305X100E) and it appears that the new design is not susceptible to the

binding problem. Further inspection of this item will be conducted after

the licensee issues an LER supplement due May 22, 1987.

(CLOSED) LER 2-86-13, Failure to Prcperly Verify Reactor Protection

System (RPS) Shorting Links Installed During Testing Causes Full RPS Trip

During Refueling. The in5pector verified via the training report that

members of the I&C crews were trained on proper verification of

installation of the RPS shorting links. The training class syllabus

adequately addressed the item. It required class participants to field

verify that the shorting links were in place.

(CLOSED) . Level Scram During Pipe

Flushing Due LER

to 2-86-16,

PersonnelAutomatic

Error. TheLowinspect

Water,'or verified that the lesson

plan associated with the committed real time training satisfactorily

discussed the circumstances surrounding the event and the lessons which

can be learned.

(CLOSED) LER 2-86-24, Inadvertent Emergency Core Cooling System (ECCS)

Actuation During Refueling Outage Due to Personnel Error. The inspector

reviewed the documentation which demonstrated that new tags were

installed. The inspector visually verified that the tags were in place on

the Unit 1 Division ECCS inverters and power supplies on February 24,

1987.

No violations or deviations were identified.

8. In Office LER Review (90712)

The listed LERs were reviewed to verify that the information provided met

NRC reporting requirements. The verification included adequacy of event

description and corrective action taken or planned, existance of potential

generic problems and the relative safety significance of the avent.

(CLOSED) LER 1-86-17, Late Performance of Required Hourly Fire Watches.

(CLOSED) LER 1-86-18, Output Breaker EPA-2, Reactor Protection System

(RPS) Motor Generator 1A, Tripped Unexpectedly to De-energize RPS Bus A;

Cause - Undetermined.

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(CLOSED) LER 1-86-23, Technical Specification (TS) 3.0.3 Entered Due to

Inoperability of the Unit 1 Reactor Core Spray Subsystem B and RHR Low

Pressure Coolant Injection Loop.

(CLOSED) LER 1-86-32, Failure to Functionally Test Relay TR/2 in Logic

Channels A2, A4, B2 and B4 Primary Containment Isolation Instruments

B21-TS-3229-3232; Procedure Deficiency.

(CLOSED) LER 2-86-04, Primary Containment Group 6 Isolation / Automatic

Isolation of Reactor Building Ventilation System and Automatic Starting of

Standby Gas Treatment System Occurred; Cause - Electrical Shorting.

(CLOSED) LER 2-86-07, High Radiation Alarm Trip of Reactor Building

Ventilation Exhaust Radiation Monitor D12-RM-N010B; Due to Electrical

Grounding of the Monitor Power Lead.

(CLOSED) LER 2-86-09, Upscale Trip of Instrument Trip Unit to Reactor

Building Exhaust Ventilation Monitor D12-RM-N010B: Cause Could Not Be

Determined.

(CLOSED) LER 2-86-11, Reactor Water Cleanup System Inlet Primary

Containment Outboard Isolation Valve, Automatically Closed; Cause - Fuse

F18 Blew.

(CLOSED) LER 2-86-14, Upscale Trip of Reactor Power Intermediate Range

Monitor D Occurred When Control Rod 02-19 Was Selected in Reactor Manual

Control System While Performing PT-18.1; Cause - Electronic Noise Spike.

(CLOSED) LER 2-86-22, Unit 2 Shutdown in Accordance With TS 3.4.1.1 Due

to a Lockout / Trip of the Recirculation Pump Motor Generator Set.

No violations or deviations were identified.

9. Followup on Inspector Identified and Unresolved Items (92701)

(OPEN) Inspector Followup Item, (325/84-04-01 and 324/84-04-01), Licensee

to Identify and Repair Cab *ie Tray Raceway Z Clamps Problems. The I clamps

secure the tray to the horizontal tray support. The inspector reviewed

completed work requests 1-E84-1658 and 2-E84-2009 which documented

completion of this particular inspection and repair. The inspector '

performed an inspection of safety related cable trays 50F/DA and 50M/DA in

the Unit 2 control room on February 22. Of twenty four Z clamps installed

on these trays, five were bent such that they were not engaged with the

tray top, four others had loose I clamp nuts, and three others were turned

to the side. In addition, two Z clamps were missing. The inspector also

observed several tray covers which were not in their proper place. Based

on discussions with the architect / engineer, the licensee determined that

the "as found" condition of these two trays would not render the raceway

inoperble or adversely effect the cables in the trays.

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Discussion with Quality Assurance (QA) personnel revealed that an

outstanding non-conformance report (NCR), number E-86-002, involving cable

tray covers had been issued on July 1,1986, but a review of the NCR

responses by the QC supervisor and the inspector showed that poor work

control practices which allowed the 2 clamp problems to occur had not been

specifically addressed. Hence, both the licensee and the inspector have

determined that the responses were inadequate. On February 27, 1987,

licensee QA issued a Notice of Deficiency against this NCR in accordance

with QA procedure 0QA-104, which required correction of the inadequate

response within seven days.

This item will remain open pending final resolution of NCR E-86-002 and

the Notice of Deficiency and subsequent review by the inspector.

No violations or deviations were identified.

10. LimitorqueOperators(71707)

The licensee has recently procured information from Limitorque Corporation

concerning actuator sizing and settings on both safety and non-safety

related valves. The data was recently reviewed (December - January) and

compiled from original design documents into a new format at the

licensee's request. Review of the data sheets showed that Limitorque was

now recommending upgrade of some actuator motors to a larger size.

Apparently, Limitorque had used 100% full voltage to size the motors,

instead of the currently specified degraded supply of 85%. Reviews of

documents between the licensee, the valve manufacturer and the valve

manufacturer's subcontractor (Limitorque), has not been able to determine

what was specified to Limitorque (or by whom) when the original plant

equipment was procured. The licensee has evaluated this condition on the

applicable safety related valves and has determined that these valves

would function under design conditions. The affected valves are:

E41-F002, High Pressure Coolant Injection (HPCI) inboard steam line

isolation valve; E41-F004, HPCI condensate storage tank suction valve;

E41-F008, HPCI full flow test isolation valve; E11-F017A and B, RHR system

outboard isolation valves; and E11-F024A and B, suppression pool test

return isolation valve. The inspector has reviewed the justification for

continued operation for Unit 2 contained in Engineering Evaluation

EER-87-0088. In summary, the evaluation concludes that no safety problem

exists based upon either application and/or electrical distribution

voltage studies. The voltage studies determined that the degraded voltage

of some of the valves would not drop below 85%. Under these anticipated

voltages, there is no motor sizing concern. In addition, contact with the

applicable valve vendors, Anchor Darling and Rockwell, revealed that they

perfonn their own sizing and setting calculations. Of three valves.

reviewed by Anchor Darling, a degraded voltage of 85% was used. A list of

the other valves has been supplied to the vendors to verify exactly what

,

value was used.

The licensee has contracted with B&W to review the Limitoroue data sheets,

calculations and generally assist in resolving the concerns. Their review

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has indicated potential problems with Limitorque data sheets. Two DC

motor powered actuators had been treated as AC powered. In addition, one

of these had the wrong pull-out efficiency used for the overall unit ratio

(motor design speed-RPM / actuator speed RPM). Apparently the wrong value

had been taken from the Limitorque Gate and Globe Valve Efficiency Chart.

The actuators involved were SMB-3 and SMB-000. Another valve with an

SMB-5T actuator also had the wrong pull-out efficiency used in the torque

switch calculation. This was attributed to using the wrong motor speed

when obtaining values from the Gate and Globe Valve Efficiency Chart.

The licensee is continuing his review. This is an Inspector Followup

Item: Potential Problems with Limitorque Data Sheets (324/87-03-02).

No violations or deviations were identified.

11. Spent Fuel Storage Capacity (59095)

The inspectors reviewed the available storage capacity in the Unit 1 and

Unit 2 spent fuel storage pools to determine if full core offload

capability existed for each unit. Based on discussions with licensee

personnel and review of the licensee's fuel map, full offload capability

(560 assemblies) existed. Unit 2 Spent Fuel Pool (SFP) has room for 566

more BWR assemblies:

1839 allowed by TS

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36 displaced by a PWR rack

- 36 rack not installed

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I contains stuck blade guide

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2 boral sample stations

- 442 not yet installed

1322 available spaces

- 756 assemblies in pool

~566 BWR spaces available

Unit 1 SFP has room for 925 more BWR assemblies:

1803 allowed by TS

- 36 rack not installed

- 2 boral sample stations

T7EE available spaces

- 840 assemblies in pool

975 BWR spaces available

The above data is as of February 15, 1987.

The inspector noted that each SFP contained 10 PWR spent fuel modules each

capable of storing 16 assemblies for a PWR capacity in each pool of 160

PWR assemblies. The Unit 1 SFP contained 160 assemblies while the Unit 2

pool contained 144 assemblies. However, Unit 2 Technical Specification 5.6.3 states that, "the fuel storage pool is designed and shall be

maintained with a storage capacity limited to no more than 144 PWR fuel

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assemblies and 1839 BWR fual assemblies. The extra 16 storage locations

in the Unit 2 SFP pose no safety problem since the Unit 1 SFP has been

reviewed and approved by NRR, contains 160 PWR assemblies and locations,

also contains additional high density racks, and is essentially identical

to the Unit 2 SFP. The excess storage capacity in the Unit 2 SFP is a

violation of TS 5.6.3: Failure to Meet TS 5.6.3 Regarding Spent Fuel Pool

l PWR Capacity (324/87-03-01).

!

j One violation and no deviations were identified.

12. RefuelingActivities(60705)

Selected refueling activities were witnessed and reviewed by the

inspector. These included verification that:

- The fuel pool gates were removed per MP-09.

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Surveillance requirements of Technical Specification 4.9.6 associated

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with refueling bridge interlocks were performed prior to fuel

movement.

- Number of operable SRM's per Technical Specification 3.9.2.a. and b.

were maintained.

- Continues communications between the refueling bridge and the control

room were established per Technical Specification 3.9.5.

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Fuel movements were conducted in accordance with operating procedures

and the Fuel Movement Sheets.

The last activity was performed during a two hour inspection conducted on

the refueling bridge during fuel movements.

No violations or deviations were identified.

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