ML20198F410

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Insp Repts 50-324/97-08 & 50-325/97-08 on 970525-0705. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20198F410
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 08/01/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20198F382 List:
References
50-324-97-08, 50-324-97-8, 50-325-97-08, 50-325-97-8, NUDOCS 9708130035
Download: ML20198F410 (43)


See also: IR 05000324/1997008

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U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50 325, 50 324

License Nos:

DPR 71, DPR 62

Report No:

50 325/97 08, 50 324/97 08

Licensee:

Carolina Power & Light (CP&L)

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-Facility:

Brunswick Steam Electric Plant, Units 1 & 2

Location:

8470 River Road SE

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Southport, NC 28461

Dates:

May 25

July 5,1997

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Inspectors:

C. Patterson, Senior Resident Inspector

E. Brown, Resident Inspector

J. Lenahan, Reactor Inspector (Sections E1.2, E1.3,

E3.1, E3.2, E5.1)

J. Coley, Reactor Inspector-(Section M1.3)

J. Canady, Resident Inspector-(Plant Hatch)

Approved by:

M. Shymlock, Chief. Projects Branch 4

Division of Reactor Projects

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Enclosure 2

9708130035 970901

ADOCK 050

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EXECUTIVE SUMMARY

Brunswick Steam Electric P1 ant, Units 1 &-2-

NRC Inspection Report 50 325/97 08, 50 324/97 08

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This integrated inspection included aspects of licensee operations

maintenance, engineering, and plant support. The report covers a 6 week

period of resident inspection; in addition, it includes the results of an

engineering inspection and maintenance inspection by regional inspectors.

Ooerations

The inspector concluded that operator performance was excellent during

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an unplanned dual unit downpower maneuver.

(Section 01.1)

The inspector concluded that the licensee's response to an issue

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potentially affecting operability of the Standby Gas Treatment (SBGT)

and Environmental Qualification (EQ) components was poor. This problem

occurred due to the licensee living with a known deficiency with a

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alugged drain. The inspector identified water leakage a second time

3ecause of inadequate controls to prevent the problem from recurring.

(Section 02.1)

The inspector concluded that the licensee activities of dredging the

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intake canal and maintenance activities on the diversion structure were

maintaining the intake structure free of debris.

(Section 02.2)

The inspector concluded that the operator's res>onse to an unexpected

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recirculation pump speed transient was good. T1e aroblem was quickly

recognized and action taken to prevent further pro)1 ems. (Section 02.3)

One example of a violation for failure to enter a Limiting Condition for

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Operation (LCO) was identified.

(Section 08.2)

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Maintenance

The inspector observed good electrical safety precaution while

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performing preventive maintenance on circuit breakers.

The inspector

noted that the diesel generator (DG) building ventilation intake filter

structure was degraded. A missed opportunity to verify EQ components in

the motor control center (MCC) occurred when the MCC was tagged out and

opened.

(Section M1.1)

The inspectors concluded that two violations were identified.

Following

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' work on the emergency bus.-no post maintenance. testing (PMT) was

conducted to insure operability. An intent change to a procedure was

made changing the undervoltage relay operating range as a pen and ink

change.

(Section M1.2)

Verification of the licensee's corrective maintenance activities

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revealed three noticeable in process-maintenance' strengths. These-

strengths consisted of: 1) knowledgeable and technically confident

maintenance technicians performing the work: 2) formation of a site

investigation team which used formal fault tree analysis techniques to

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identify equipment and human performance problems, determine their

direct cause, and implement appropriate corrective action, and (3)

aggressive engineering and supervision oversight to assure work

activities proceeded effectively.

However, one NCV for Failure to

-Follow Work Instructions During the Previous Installation of Solenoid

Valves 2 CAC SV 4410 26 & 27. and one unresolved item for Failure to

Obtain an EQ Disposition on Extension of Vendor Recommended EQ Life for

Thermo Electric Cooler were also identified. (Section Hl.3)

Enaineerina

The inspector concluded that a questioning attitude and conservative

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decision making led to the discovery of a problem in the number two DG.

The preplanned systematic approach to problem solving was beneficial to

an orderly timely resolution of the issue.

(Section E1.1)

Upon exceeding the tracking LC0 covering the hydrogen / oxygen thermo-

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electric qualified life operability review, an extension was not

obtained until questioned by the inspector. This was a violation-of the

plant operating instruction.

(Section E4.1)

A noncited violation (NCV) was identified for failure to perform an

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adecuate 50.59 review for downgrading the control building air-

concitioning qualify classification.

(Section E8.2)

A violation was identified for failure to initiate condition reports

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when nonconforming . EQ hardware installations were identified. An

unresolved item was identified for concerns related to moisture

-intrusion into EQ equipment. A weakness was identified for failure to

train contract engineering personnel in the requirements of the

corrective action program.

(Section E1.2, E5.1)

The licensee's arogress to correct the EQ program deficiencies was

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satisfactory. -

Equipment operability issues were aapropriately evaluated

through JCOs although closure of the JC0s has not aeen timely. (Section

E1.2)

Engineering response to address equipment operability issues were

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conservative and prompt. Engineering support to plant operations is

rated as a strength.

(Section E1.3)

The inspectors concluded that the licensee's Phase I UFSAR was performed

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in accordance with their procedure and was an effective program for

identification of errors. The licensee is considering various o)tions

for performance of additional UFSAR reviews to assure that the U:SAR

accurately reflects the design. operation, and licensing basis of the

plant. (Section E3.1)

The licensee's corrective actions for the EQ program will address the-

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insufficient detail in DBD 100.

Further review will be performed by NRC

to determine the adequacy of other DBDs. (Section E3.2)

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Plant Support

A lack of ccwprehensive procedural guidance or standard site practice

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contributed to the inconsistent posting of radioactive material within

the radioactive controlled area.

(Section R2.1)

The inspector concluded that plant management made a conservative

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decision to perform a dual unit shutdown based on the untimely and

erroneous test results provided by the LPU. An ongoing NAS audit

identified several issues in this area.

Two non cited violations were

identified for failure to promptly take corrective action when flow test

performance did not meet acceptance criteria and for an inadequate fire

protection flow test procedure. A weakness was identified-in trending

and monitoring of the fire protection water suppression system

performance. (Section F1.1)

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The inspector concluded that there was a violation of the fire

protection procedure for having transient combustibles in a fire

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separation zone.

Designation of fire separation zones was unresolved

recuiring further review.

Implementing procedures for the establishment

anc maintenance of fire protection separation zones were weak. This was

evident by the discovery of transient combustibles in separation zones.

(Section F1.2)

An NCV was identified for the mispositioning of a hydrant isolation

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valve.

(Section F3.1)

Poor attention to detail resulted in the inadvertent water spraying on

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an energized high voltage Unit Auxiliary Transformer.

No personnel were

injured and no equipment damage or malfunction was observed.

(Section

F4.1)

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Report Details

Summary of Plant Status

Unit 1 operated continuously during this period. On June 21, 1997,

>ower was decreased to 22 percent until concerns about the fire main

leader were resolved as discussed in this report. Two control rods

remain inserted around an identified fuel pin leaker. At the end of the

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period the unit had been on line 240 days.

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Unit 2 operated continuously during this period. On June 21, 1997,

)ower was decreased to 22 percent until concerns about the fire main

leader were resolved as discussed in the re

At the end of the

period the unit hr.d been on line 295 days. port.

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The mechanical facuum pumps remained tagged out on both units due to

concerns about centrol room dose in the event of a Rod Drop Accident.

The licensee, in a letter to the NRC dateo February 13, 1997, committed

to upgrade the mechanical vacuum pump trip function to implement a

vacuum pump trip from the main steam line radiation monitor prior to the

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next startup.

Due to an identified discrepancy between TS required suppression chanber

water level and water volume, the licensee has issued Standing

Instruction (SI), SI 97 031. to maintain a more conservative water level

band until a TS amendment is approved. The SI directs o ' rations to

maintain level between 27.5 inches and 29.5 inches compared to TS

values of 27 inches to 31 inches. The inspectors have observed

compliance with this SI during routine tours of the control room.

Due to concerns about the control room dose the licensee imposed an

administrative limit on Iodine until a TS amendment is approved. The

licensee made a procedure change to Administrative Procedure OAI 81,

Water Chemistry Guidelines, setting the limit at 0.1 microcurie per gram

dose equivalent Iodine 131 com)ared to a TS value of 0.2 microcurie per

gram. Also, the licensee has

3een providing weekly data to NRR and the

resident inspector for review.

None of the data reviewed has exceeded

the administrative limit.

Nine of thirteen Justification for Continued Operation (JCO) in the

Environmental Qualification (EQ) of equipment area remain open for both

units. The following provides the status of the EQ JCOs and associated

Engineering Service Requests (ESRs):

1)

ESR 96 00425, Evaluation of EQ sealants was closed by the

licensee.

2)

ESR 97 00331 (old ESR 96 00503), Associated Circuit EQ was

scheduled for completion May 31, 1997, but revised to July 18,

1997.

3)

ESR 96 00426. Evaluation Quality class and EQ classification of

PASS valves was scheduled for completion June 6,1997, but revised

to October 31, 1997,

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4)

ESR 97 00330 (old ESR 96 00501), MCC EQ was scheduled for -

completion June 6, 1997, but was revised to July 18, 1997.

5)

ESR 97 00329 (old ESR 96 00625), EQ Type -JC0 for EQ Fuses Without

a Qualification Data Package (QDP) was closed by the licensee.

6)

ESR 97 00340 (old ESR 96 00627), QDP for Marathon 300 Terminal

Blocks was scheduled for completion December 31, 1997 but revised

to August 1, 1997.

7)

ESR 97 00087, EQ Type JC0 for Improperly Configured Conduit Seal

was closed by the licensee.

8)

ESR 97 00229, JC0 for GE CR 151 B Terminal Blocks was scheduled to

be completed July 15, 1997.

9)

ESR 97 00238, JC0 for SBGT Motor Operated Valve (MOV) Position

Indicator Rheostat, was closed by the licensee.

10)

ESR 97 00250, Conduit Union in EQ Boundary, was scheduled for

completion December 31, 1997

11)

ESR 97 00256, Main Steam Isolation Valve (MSIV) Hiller Actuator

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JCO, was scheduled for completion July 17, 1997.

12)

ESR 97 00289, Pass Valve Limit Switch Panel Wiring, scheduled for

completion September 15, 1997,

13)

ESR 97 00343, Qualification of Kulka Model 600 Terminal Blocks was

scheduled for completion September 1,1997.

In summar

However, y, both units operated continuously during this report period.

there were nine outstanding JCOs in the EQ area.

The

mechanical vacuum pump remained tagged out due to concerns related to

Rod Drop Accident analysis.

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I. Operations

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Conduct of Operations

01.1 Dual Unit Downoower

a.

l!1soection Scone (71707)

The inspector periodically observed operator performance during the dual

unit downpower and return to full power during June 20 21, 1997.

b.

Observations and Findinas

The inspector observed that operator performance during the downpower

was controlled and deliberate. Good pre job briefings were conducted at

major evolutions. The downpower was staggered between the units to

- provide more control in the Control Room.

c.

Conclusions

The inspector concluded that operator performance was excellent during

an unplanned dual unit downpower maneuver.

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02

Operational Status of Facilities and Equipment

02.1 Water Leak onto Standby Gas Treatment (SBGT) System

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a.

Insoection Scone (71707)

The inspector reviewed the activities associated with a unit 1 weekend

downpower and associated water leak on the SBGT system,

b.

Observations and Findinas

On June 1,1997, the inspector reviewed the operator logs concerning

activities associated with the Unit I weekend down>ower.

Noted in the

logs on May 31, 1997, was an event where water lea (ed onto the Unit 1

SBGT. This occurred due to a plugged floor drain on the upper elevation

resulting in water running down onto the SBGT. This caused a ground on

the 1B 250 volt battery bus and anntmciator "RX BLDG SBGT UNITS TEMP

HIGH" alarm.

Later, the alarm and ground cleared.

The inspector toured the Unit 1 reactor building on June 1, 1997, to

inspect the condition of the 1B SBGT.

Noted above the control panel and

other instrumentation was a tem)orary protective cover to divert water

from going onto the IB SBGT. T1e inspector noted that the control panel

was labeled as EQ. The inspector questioned the control room operators

as to whether the adequacy of EQ component sealing had been considered

since the water intrusion caused the grounds and annunciator alarms and

if the operability of the SBGT train had been affected. A Condition

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Report (CR) 97 01940. Water Leaking on 1B SBGT, had been written but it

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only addressed the drain problem. The CR addressed that the drain had

been plugged for scme time but was not corrected.

The licensee reviewed the EQ question and determined that SBGT was EQ

for radiation only for a loss of coolant accident (LOCA) in the drywell.

It was not sealed for a high energy line break (HELB) in the reactor

building. Also, the licensee did an additional walkdown of the SBGT on

June 1,1997, to identify water leakage paths. No evidence of water

intrusion into the control

)anel was found. The top of the panel was

dry with dust on it. Opera)ility tests were conducted on both SBGT

trains in accordance with OPT 15.6. Standby Gas Treatment System and

were completed satisfactorily. On June 2, 1997, the licensee opened the

panel and found half an inch of water in the bottom of the panel.

On June 13, 1997, during a routine tour of the Unit I reactor building,

the inspector observed water running out from underneath the door (door

402) to the Southwest Swamp Ventilation Room on the 80 foot elevation.

The inspector immediately contacted the control room and stayed in the

area until plant aersonnel arrived. A health physics technician

responded and too( swipes of the water. The water was not contaminated.

It was determined that the water was from condensation due to running

the air conditioning.

In addition, the inspector told a plant operator

that water was running down onto the 50 foot elevation and was wetting

electrical junction box 45A/DA.

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The inspector also notified plant management because this was the second

time that water had run out of this area. The licensee inspected the

junction box and found no water inside the box. The licensee initiated

CR 97 02121 to document the problem. Also, management directed that the

Unit I reactor building temporary cooling system operation be stopped

until a way was developed to handle the condensation drainage due to the

floor drain being plugged.

c.

Conclusions

The inspector concluded that the licensee's response to an issue

potentially affecting operability of the SBGT and EQ components was

poor. This problem occurred due to the licensee living with a known

31ugged drain. The inspector identified water leakage a second time

3ecause of inadequate controls to prevent the problem from recurring.

02,2 Intake Canal

a,

inspection Scope (71707)

On June 25, 1997, an inspection of the intake canal was performed.

b.

Qbservations and Findinas

The inspector observed the main circulating water and service water

intake structures at the traveling screens from the intake canal.

Both

structures were found to be free of debris.

During several months in

the Spring of 1997.-the licensee conducted dredging of the entire intake

canal to ensure reliable operation prior to the vegetation growth

season,

Also, the diversion structure at the beginning of the intake canal at

the mouth 01' the Cape Fear River was inspected. The licensee was in the

process of installing coarse mesh screens, called turtle blockers, on

the-river side of the structure outside of fine mesh diversion screens.

These blocker screens would prevent any sea turtles from entering the

canal if a blowout occurred at the fine mesh screen. A maintenance crew

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was assigned to the diversion structure-seven days a week during this

time of year for cleaning vegetation, etc. from the fine mesh screens,

c.

Conclusions

The inspector concluded that the licensee activities of dredging the

intake canal and maintenance activities on the diversion structure were

maintaining the intake structure free of debris.

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02.3 Recirculation PumD SDeed Increan

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a.

InsDeCtion SCoDe (71707)

The ins)ector reviewed the transient that occurred on Unit 1 on July 1,

1997, w1en the 1A recirculation pump speed increased unexpectedly,

b.

OhservationsandFindinas

During routine operations, without any indication of an annunciator

alarm or other warning, the control room operator observed a step

increase in power on a monitor display.

Power was at 97 percent due to

a limiting control rod pattern and then unexpectedly increased to an

indicated power of 101.6 percent. The operator went to the

recirculation pump speed controller and noticed that the 1A speed

indication was pegged high.

The operator took manual control of the 1A

recirculation pump and reduced the speed.

The licensee, after reducing speed, locked the scoop tube preventing any

further inadvertent transient. The controller was replaced and the old

controller checked for defects. The licensee determined, by

calculation, that the step increase in power had occurred about five

minutes early until observed by the operator. The calculated power was

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100.3 percent.

The inspector observed the response to the pump speed increase. Good

communication and supervisory oversight was present.

Due to the

transient, operations promptly restored the out of service Diesel

Generator as a precautionary measure. The inspector noted that

engineering res;>onse was prompt and provided good support in determining

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the effect of the transient on core safety parameters.

c.

Conclusions

The inspector concluded that the operator's res)onse to the unexpected

recirculation pump speed transient was good. T1e aroblem was quickly

recognized and action taken to prevent further proalems.

08

Miscellaneous Operations issues (92901)

08.1

(Closed) VIO 50 325(324)/96 04 02:

Croldown Menitoring Not Followed

This violation, with two examples, was issued as a result of exceeding

the cooldown rate on February 3, 1996 following the Unit 2 shutdown for

refueling and a failure to record Unit 1 bottom head temperature during

a )lant cooldown on March 18, 1996. The event that occurred on

Fe>ruary 3.1996 was identified as URI 50 324/96 01 01. This URI was

closed in Inspection Report (IR) 50 325(324)/96 04 and opened as another

example of Violation 50 324/96 04 02 for not following plant shutdown

procedure OGP 05.

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The licensee responded to this violation in a letter dated May 29, 1996.

The immediate corrective actions included counseling of the involved

operating crew regarding management's expectations, training of licensed

operators during requalification training on the circumstances

surrounding the events, and training of licensed operators on a new

periodic test procedure that was developed for the monitoring of heatup

and cooldown limits.

The corrective actions to be taken, as stated in the licensee's res>onse

of May 29,1996, included the development of a unit shutdown plan tlat

would be integrated into the outage plan: the revision of appropriate

operations procedures to interface with the newly developed periodic

test procedure for monitoring heatup and cooldown limits; and an

evaluation of the scram discharge volume surveillance test to identify

siternatives to the testing method.

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The inspectors reviewed Brunswick Site Procedure BSP 35, Outage

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Planning, Revision 5, to verify that a Unit Shutdown Plan was integrated

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into the Outage Planning procedure. Additionally, the inspectors

reviewed the Unit Shutdown Plan for refueling outage B111R1 that began

October 4,1996, and the planned B213R1 refueling outage scheduled for

September 12, 1997.

The ins

Operating Procedures OGP 02,pectors verified that General Plant

Approach to Criticality and Pressurization

of the Reactor, Revision 56 and 0GP 05, Unit Shutdown, Revision 73 were

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revised to interface with the new Periodic Testing Procedures 1(2)PT-

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01.7, Heatup/Cooldown Monitoring, Revision 0.

The inspectors reviewed

Periodic Testing (surveillance) procedures OPT 14 1.1b, ASME Section XI

Functional /N498 Hydrostatic Pressure Test of the Class 2 Control Rod

Drive (CRD) System and Scram Discharte Volume Piping, Revision 3: and

OPT 14,1,2, Scram Discharge Voluma Visual Inspection Revision 5.

It

was noted from this review that procedure OPT 14 1 lb was revised to

include inspection of the scram discharge volume (SDV) piping whic1 was

removed froni procedure OPT 14.1.2. This revision resulted from on

evaluation of the SDV surveillance to identify alternatives to the

existing test method. The inspectors noted that heatup and cooldown

cautions and response ex>ectations were listed in the procedural

revisions. Based upon tiese reviews, this violation is closed.

08.2 (Closed) URI 50 325(324)/97 07 01:

Failure to Enter TS ACTION Statement

During the April performance of Haintenance Surveillance Test OMST-

CLDETIIH, Chlorine Detection System Channel Functional Test the response

of the Control Building Heating, Ventiletion and Air Conditioning

(CBHVAC) System, to a chlorine isolation signal was tested.

This

isolation rendered the control room radiation and smoke protection

functions inoperable due to these signals being blocked when the

chlorine isolation mode was actuated,

The inspector determined that the

licensee failed to enter the ACTION statement for TS 3.7.2 Control Room

Emergency Ventilation System (CREVS) since the smoke and control room

radiation protection modes were inoperable. TS 6,8,1.a. requires that

written procedures shall= be established, im)1emented, and maintained

covering the activities in Appendix "A" of Regulatory Guide (RG) 1.33,

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November 1972.

Section I, requires administrative procedures for log

entries and equipment control.

Operating Instruction 001 01.08, Control of Equipment and System Status,

requires that for limiting condition for oxrations (LCOs) an entry

describing the condition be entered into tie LCO tracking system. The

failure to log entrance into the 15 3.7.2 ACTION statement upon loss of

the smoke and radiation modes is a violation. This is the first example

of VIO 50 325(324)/97 08 01, TS/LC0 Administration.

The licensee addressed not only this missed LC0 entry, but four

additional-instances as captured in the following CRs:

CR 97 815, Log Entry Clarity

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CR 97 1017, Missed Technical Specification Applicability

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CR 97 1028, CAC Honitor Filter Changeout

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CR 97 1242, LC0 Not Written for Both Units

The inspector reviewed the licensee common cause evaluation. The

inspector was concerned with the number and the repetitive nature of

these failures. Four out of the five reports stated the Control Room

supervisor failed to correctly recognize and log TS LC0 conditions.

The inspector noted that many of these events were for LCOs of short

duration and that 12 events in 18 months were identified.

Four out of

12 events reported were related to inaccuracies, errors, or oversights

with the LCOs concerning the Control Building Emergency Filtration

System. Two others dealt with errors regarding the containment

radiation monitors. The licensee root cause attributed the failures to

not having formal second verification. Operations management conducted

a standdown to address this adverse trend, among the causes identified

were inadequate validation and verification, wrong assum)tions, and

inadequate supervision. The inspector determined that tle licensee root

cause evaluation was deficient since the root cause did not acknowledge

or address those specific additional items identified.

In addition, the

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inspector noted a deficiency in the procedural guidance.

Procedure 001

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1.0.8 does not require nor suggest referencing the specific Technical

Specification requirements.

This URI was closed with issuance of the violation.

08.3 Corrective Action Program

The conclusion statement in paragraph 07.1.c of NRC Inspection Renort

50 325.324/97 07 was re reviewed by the inspectors. The statement which

inferred that senior management training on the Corrective Action

Program (CAP) and Condition Reports (CRs) was behind the scheduled NRC

commitment should be revised to indicate that management training on CAP

and CRs was behind the NRC. commitment.-

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II. Maintenante

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Conduct of Maintenance

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M1.1 General Comments

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a.

Inspection Scope (62707. 61726)

The inspectors observed all or portions of the following work

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activities:

e

WR/JO 97 ACFH1

Rebuild standby liquid control-(SLC) pump 2B

discharge check valve C41 F033B

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WR/JO 97 ADCX1

Investigate cause for point 7 indicating error

for the containment atmosphere control system

torus /drywell temperature recorder

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WR/JO 97 ABTW 01 4160 volt breaker PMS

b.

Observations and Findinas

All work observed was performed with the work Jackage present and in

active use. Technicians were experienced and (nowledgeable of their

assigned tasks.

The inspectors also observed the use of foreign

material exclusion practices where appropriate.

The insactors noted, during a subsequent review of the operation daily

logs, t1at the SLC pump discharge check valve rebuilt under WR/JO 97

ACFM1 had failed its post maintenance functional test (0PT 06.1).

Based

upon O wrations. discussions with Engineering, the check valve did not

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meet tie full stroke closed criteria of OPT 061.

It would be tracked

as increased frequency testing under Inservice Testing deviation report

number 97 016.

On May 28, 1997, the inspector observed work activities associated with

the Unit 2 Residual Heat Removal (RHR) Loop A outage. The inspector

observed preventive maintenance on 4160 volt breakers for RHR pump A and

RHR pump 2A wrformed under WR/JO ABTW 01. The work was performed per

procedure OPi BKR001, ITE 4KV Breaker and Compartment Checkout. The

inspector verified that revision 17 dated July 29, 1996, was the correct

revision of the procedure. The insactor observed good use of safety

_ equipment.

The technicians used ru)ber gloves, a face shield, and a

safety man with a hot stick. The inspector also verified that the

-megger and other test equipment were in calibration.

Each breaker compartment was dusted off using a paint brush. A handful

of dust was taken out of each com)artment. Although the general area

was very clean, the inspector looted for possible sources of-dust or

dirt. The 4160 volt class 1E breaker com)artments are located on the

upper elevation of the Diesel Generator (JG) building. The DG building

ventilation intake filters were in poor material condition. The filters

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were dirty and the structures holding the filters in place were degraded

which allowed unfiltered air entry into the DG buildirg.

Also, the inspector observed breaker work in the Unit 2 reactor building

on MCC 2XA, The inspector observed that the MCC was t6

circuit breaker preventive maintenance was in arogress.99ed out and

The inspector

questioned if any EQ walkdowns as part of the

EQ 3rogram reconstitution

were being performed to verify components in the 4C0 but none were being

conducted. The EQ walkdown was not planned,

c.

Conclusions

The inspector observed good electrical safety precaution while

performing preventive maintenance on circuit breakers,- The inspector

noted that the DG building ventilation intake filter structure was

degraded. A missed opportunity to verify EQ com

occurred when the MCC was tagged out and opened.ponents in the MCC

M1.2 Loss of E 2 bus and Diesel Generator

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a.

Insoection Scoce (62707)

The inspector reviewed the circumstances concerning a loss of the E 2

emergency bus due to the off site power supply breakers tripping and

subsequent loss of DG 2 due to a fuel oil leak that occurred on June 8,

1997,

b,

Observations and Findinas

- On June 8,1997, the licensee was_ preparing for a scheduled outage of

DG 4.

Preparation involved quick start testing of the other three DGs

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to ensure operability prior to taking the DG 4 out of service, When

preparing to start DG 2, the operator placed the DG 2 selector switch in

the " Local Manual" position to allow personnel in the DG building to

start the DG. The master and slave breakers supplying the normal off-

site power to the emergency 4160 VAC bus E P. tripped de energizing

emergency bus E 2.

DG 2 auto started and W ed onto the emergency bus

per design. The loss of the E 2 bus resulted in a half scram and

several half isolations of containment group-isolations. The half scram

and group isolations were reset without complications.

Since no

apparent cause for the breaker trip could be determined, the licensee

declared off site power inoperable. A four hour notification was made

to the NRC at.6:05 p.m,

Later, at 7:13 p.m.. DG 2 was manually tripped due to a fuel oil leak

caused by a 1/4 inch fuel oil line to a pressure gauge breaking.- The-

-licensee entered TS 3.0.3 due to a loss of off site power and DG 2 being

inoperable.

After identifying the most- probable cause of the breaker tripping to E 2

was a relay failure, and with DG 2 in AUTO but mechanically locked out,

the E 2 bus was_re energized from off site power at 7:26 p.m. and TS

_

%.m

-

--

_ . . .

.

.

10

3.0.3 exited. A four hour notification was made to the NRC at 10:30

p.m. concerning the second loss of E 2.

At 11:30 p.m. it was determined

'

that the 27 PK relay contacts were in the tri> ped condition with no trip

signal present.

The relay was replaced and t1e trip condition was no

longer present. The mechanical lockout for DG 2 was roset.

l

The licensee formed an event review team once the E 2 tius was lost to

investigate the problem. The licensee determined that the loss of E 2

due to tripping of the master and slave breakers was because one of the

trip contacts of 27 PK relays three colls failed to opon when the relay

was energized. This was due to an incorrect operating arm / armature

assembly adjustment.

There are three protective relaym in parallel

connected to the E 2 bus between the master and slave breaker. Any one

of the three relays or nine contacts could cause this same trip

condition.

The 27 PK relay is an under voltage relay designed to sense

an under voltage condition on off site power allowing the DG to be the

sole electrical source. The 27 PK relay is normally energized when

installed but only in the trip circuit when the select switch is not in

the "AUT0" mode of operation and the master and slave breakers are

closed.

The failed relay had been successfully calibrated and tested on a relay

tester on May 27, 1997.

Upon examination of the failed rniay, one of

the three contact assemblies had limited contact travel. The licensee's

'

root cause evaluation stated that it was believed that the as found

condition existed since initial installation. Adjustment of these

contacts was addressed in the vendor manual which indicated that the

contact gap to checked to be .005 inches prior to installation.

Further, the inspector questioned if post maintenance testing (PMT) had

been performed to ensure operability of the emergency (E) bus components

following maintenance and after separating electrical connections or

contacts. The PM was performed under WR/JO AELB 001 that specified no

aost maintenance test requirement. The relay test procedure was OPIC-

lLY026. Relay Calibration using Pulsemaster Software and Pulsar Relay

Tester. This procedure was a bench test of the relay atter removal from

service and did not cover any PMT.

The inspector also reviewed procedure 0PLP 20. Post Maintenance Testing

Program.

Stated in the procedure, under section 6.1. Scope of the

Program, was that post maintenance testing verifies the tatisfactory

completion of maintenance activities and the technical specification

operability of the equipment, if applicable.

No post maintenance test to verify the E 2 bus operability or continuity

of relays after replacement was performed.

Vendor recommendations to

verify relay contact point ga) prior to installation was not

)erformed.

This was a violation of TS 6.3.1.a. written procedures shall

)e

established, implemented, and maintained covering the activities in

A)pendix "A" of RG 1.33. November 1972.

RG 1.33. Section 1. requires

tlat maintenance which can affect performance of safety related

equipment should be properly preplanned and performed in accordance with

o

.

.

11

written procedures, documented instructions, or drawings a

opriate to

the circumstances. This violation will be treated as VIO

325(324)/97 08 02, Failure to Verify / Check E Bus Relay Operability.

Additionally, the inspector reviewed the completed procedura (0PIC-

RLY026) for PK 27 relay calibration.

The data sheets used in the

procedure were completed on May 27, 1997. The "as left" pickup voltage

range was specified as 52.25 to 57.75. The picku

was denoted as not being in the correction range.p voltage was_50.60 end

The technicians

performing the work made a pen and ink change to the procedure to change

the range from 50.0 to 55.0 which would agree with the technical manual.

The inspector reviewed how a wn and ink change could be made on a

protective relay in a safety

aus.

Procedure OAP 004, Temporary Changes

to Procedures, gives the guidance for making a temporary change within

14 days as discussed in TS. -Temporary changes generally are classified

as changes that do not alter the intent of a procedure. One of the

examples given in Section 3.2, Intent of a Procedure, was one that

alters or deletes setroints or required operating parameter ranges.

This type change was an intent change.

This was a violation of PS 6.8.1 for maintaining procedures. TS 6.8.2

provides that a temporary change can be made in 14 days if the intent of

the procedure was not chan]ad. This violation was identified as

50 325(324)/97 08 03, Safety Relay Setting Change Made as Pen and Ink

Changes to Procedure.

Additionally, the inspector reviewed how the information in the

Equipment Data Base System (EDBS) was initially reviewed in relay test

3rocedure OPIC RLY026 and the relay setpoint change made in EDBS.

-

3rocedure step 7.2.11.6 requires entry of EDBS settings.

From

discussion with the licensee it was learned that the fields in EDBS in

this case were color coded as "information only". They were not to be

used until verified as the correct design data.

Also, the inspector reviewed how the EDBS data was changed and this also

was done with a computer generated form and not the form in the

3rocedure. The licensee initiated CR 97 02400 concerning non validated

EDBS information. The CR stated that non validated EDBS data had been

routinely used to determine settings for the following components:

balance of plant instruments with non specific data sheets in

o

' applicable procedures -

e

4160 volt protective relays

molded case circuit breakers magnetic trip settings

e

Limitorque motor operated valve torque and limit switch settings

e

Control of EDBS information will be unresolved pending further review.

This will be tracked as URI 50 325(324)/97 08 04. Control of EDBS

Information.

_ _ _ _ _ _ _ _ _ _ _

_

a

.

.

12

c.

Conclusigns

The inspectors concluded that two violations were identified.

Following

work on the E bus, no PHT was conducted to insure operability. An

intent change to a procedure was made changing the undervoltage relay

operating range as a pen and ink change.

M1.3 Maintenance Imolementation

a.

Inspection Scope. Corrective Maintenance (62700)

l

The inspector reviewed documentation and observed work activities

consisting of troubleshooting and corrective maintenance of components

in the Unit 2, 4410 containment atmosphere control (CAC) analyzer

cabinet. These activities were examined to verify that maintenance

activities were being conducted in a manner which would result in the

reliable and safe operation of the plant,

b.

Observations and Findinal

The installed system for measuring the oxygen and hydrogen gas

concentration in the primary containment was the Teledyne CAC 4410

monitor. This system was qualified as a Class 1E nuclear safety related

system. The system was designed to measure hydrogen and oxygen

concentration in the primary containment under normal or accident

conditions. Even under containment conditions of 50 pounds per square

j

inch gauge and 445 degrees Fahrenheit the system would continue to

lL

provide accurate measurements of hydrogen and oxygen concentrations.

The Brunswick Unit 2 -CAC 4410 monitor failed after five hours of

operation following preventive maintenance performed on May 28 29. 1997.

A trouble alarm was received, caused by actuation of the sample flow

switch, and water was observed in the rotameter and found in the sample

lines. An investigation revealed that the solenoid valves previously

installed in April 1996, for 2 CAC SV 4410 26 and 2 CAC SV 4410 27 were

improperly installed. A normally closed valve was installed where the

drawing required a normally open valve and a normally open valve was

installed where a normally closed valve was indicated. The installation

and maintenance instruction that accompanied each valve stated that the

valves were not interchangeable.

The inspector observed the licensee's troubleshooting and corrective

maintenance activities from the point where the-licensee thought the

improperly installed valves were identified as the cause of the failure

to the resolution of the problem. This work was performed in accordance

with WR/JO ADLP 1.

Maintenance-performed

replaced the flow switch and the CAC pump. prior to this point had

On June 2, 1997, the pro >er

valves were installed, correct valve installation was verified for tie

other train-and Unit 1, and the monitor was run. On June 2 3, after

five hours of o>eration the same failure symptoms were observed, On

June 2. 1997, tie licensee also assigned an investigation team to

develop an equipment problem action plan and identify the cause of the

_

__.

.

.

13

monitor failure using formal failure analysis methods, and to establish

appropriate corrective :ction.

During the investigation team's development of a fault tree the vendor

was contacted. The vendor immediately attributed the current problem to

a problem identified in an August 13, 1993. 10 CFR Part 21 notice on the

monitor's-thermo electric cooler.

However, the licensee was not

convinced that this was their )roblem.

Both of the failures re>orted in

the Part 21, resulted in a hig1 temperature alarm to indicate tie

failure (current drop).

This had not been encountered during the

Brunswick Unit 2 monitor failure.

But, the licensee proceeded at this

point to obtain a new thermo electric cooler from another utility since

the vendor could not support the Unit 2 schedule in a timaly manner.

Troubleshooting continued on other fault tree issues and two other

problems were identified.

The first was that terminal block 28 in the

lower solenoid valve trough-had a broken thermal shield barrier between

points 11 & 12. This problem apparently occurred during the replacament

of the solenoid valves. The licensee Q d not have a spare terminal

block or thermal shield barriers. Therefore, an ESR 97 00321 was issued

to evaluate the problem and restore the cabin.t wiring to an analyzed E0

configuration. This was accomplished by relocating the wire on terminal

TB 11 to terminal TB28 3.

During the engineering review a second

problem was also identified in that, the 2 CAC AT 4410 logic print was

in error. The vendor was again notified and the licensee was informed

that the vendor drawing had been changed. This change was not

incorporated into the vendor drawing issued to CP&L as a foreign print

drawing. The ESR made the appropriate drawing changes but, the vendor

was requested to provide the correct revised drawing.

On June 5,1997, the new thermo electric cooler arrived on site, and

work immediately proceeded to replace the cooler.

Prior to its removal

maintenance technicians found particles of copper and insulation on a

ledge in the cooler, During further disassembly, the connector on the

thermal plate in the back of the cooler fell off.

The licensee sent

these parts to be analyzed to determine the direct cause of the failure.

On June 5 and 6 the CAC 4410 monitor was successfully tested.

Documentation was O so initiated to trouble shoot' the cooler on the

other Unit 2 monitor (CAC 4409) and the coolers on both monitors for

Unit 1.

- With the exception of the improperly installed valves, the problems

experienced on the CAC 4410 monitor were the result of the cooler

failure.

The licensee also determined during their investigation that

the improperly installed solenoid valves did not affect the monitor's

o>eration.

The valves tested and operated satisfactory because flow was

t1 rough the same valve ports, whether the valve was open or closed and

the differential 3ressure on the valve seat was insufficient to open the

seat even under tie most extreme conditions.

=-_

,

___ ___

1

.

.

1

I

'

14

i

The licensee issued two condition reports on findings identified during

investigation of the CAC 4410 Honitor failure. The first (CR 97 01946)

!

dealt with the previous improper installation of the two CAC AT 4410

solenoid valves.

The inspector reviewed documentation of the April 16,

'

1996 installation, and found that although visual inspection or testing

of the valves would not determine which valve was open or closed. valve

parts numbers were correct for proper valve installation. Therefore,

the cause was due to personnel error during the valve replacement

'

process. The inspector considered the improper valve installation to be

,-

caused by a technician's failure to follow work instructions. This

!

failure constitutes a violation of minor si

i

treated as an NCV, consistent with Section gnificance and is being

IV of the NRC Enforcement

'

4

]

Policy.

It was reported as NCV 50 324/97 08 05, Failure to Follow Work

'

Instructions During Previous Installation of Solenoid Valves 2 CAC SV.

l

,

4410 26 & 27.

'

'

The second CR (CR 97 02005) issued by the licensee involved the Part 21

!

issued by Teledyne.

Based on this reported failure Teledyne shortened

'

'

the EQ life of this compoaent from 40 years to two years. The

,

- licensee's system engineer believed the vendor's recommendation was

!

overly conservative based on licensee's operating history and performing

!

>

i

the vendor recommended testing to verify operability.

Hcwever, an EQ

j

review of the disposition was not obtained. The immediate corrective

i

actions for this CR notified EQ and 001 1.0.8 LC0 was written to obtain

an operability assessment by engineering for both units.

The inspector

4

i-

was informed of CR 96 02005 late in the inspection and insufficient time

was available to

Therefore, follow up

will be required, properly review this problem.

and this item will be identified as Unresolved Item

~L

50 325(324)/97 08 06. Failure to Obtain Engineering Disposition on

Extension of Vendor Recommended EQ Component Life.

l

c.

Conclusions

<

During verification of the licensee's corrective maintenance activities

three noticeable in process maintenance strengths were observed. Th9se

strengths consisted of: 1) knowledgeable and technically confident

-

maintenance technicians performing the work: 2) formation of a site

4

investigation team which used formal _ fault tree analysis techniques to

.

- identify equipment and human performance problems, determine their

direct cause, and implement appropriate corrective action, and 3)

'

,.

i

aggressive engineering and supervision oversight to assure work

!

activities proceeded effectively. However, one NCV Failure to follow

i

Work Instructions During the Previous Installation of Solenoid Volves 2-

'

CAC SV 4410 26 & 27, and one unresolved item Failure to Obtain an EQ

Disposition on Extension of Vendor Recommended EQ Life for Thermo-

.

Electric Cooler were also identified,

a

.

M1.4 Special UFSAR Review

A recent discovery of a licensee o wrating the facility in a manner

- contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures, and/or

,

,

4

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15

!

arameters to the UFSAR descriptions. While performing the inspections

discussed in this re) ort, the inspectors reviewed the applicable

,

portions of the UFSAl that related to the areas inspected.

The

'

inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures, and/or parameters.

,

W

'

The inspector reviewed the UFSAR Section 8.3, Onsite Power Systems, to

review the 27 PK relay setting. There are specific relay settings

listed in Table 8.3.1 17 but not the 27 PK relay.

This was due to this

',

relay only being in the circuit when the DG was run in manual.

MB

Miscellaneous Maintenance Issues (92902)

i

M8,1

(Closed) LER 50 324/96 01: Control Rod Average 5 percent Insertion Time

Exceeds Technical Specification Requirements

.'

(Closed) LER 50 324/96 01 01: Control Rod Average 5 percent Insertion

l

Time Exceeds Technical Specification Requirements

Based on the closure of this item for Unit 2 in IR 50 325(324)/97 02

.

Section E8.2 and no degradation of scram times as discussed in IR 50-

325(324)/97 07 Section M3.1, these LERs are closed,

'

i

III. Enaineerina

!

El

Conduct of Engineering

i

E1.1 Diesel Generator Slow Start

a.

Inspection SCoDe (37551)

4

The inspector reviewed the circumstances concerning a slow start of DG 2

'

that occurred on June 20, 1997,

.

i

b.

Observations and Findinas

On July 1,1997, the DG 3 scheduled outage was delayed because DG 2

.

l

start time was longer than expected.

In

outage, each of the other DGs were quick _ preparation for the DG 3

started to ensure they were

operable prior to removing the DG scheduled for maintenance. DG 2

experienced a start time of about 9.5 seconds compared to a normal start

of 8.5 seconds.

The TS allowed start tiine is 10 seconds or less. The

licensee implemented a preplanned slow DG start time trouble shooting

plan,

This plan was developed as part of a site wide systematic

approach to problem solving.

By implementing the trouble shooting plan

4

it was found that a pressure regulator in the air start system was not

functioning correctly. The DG was still operable due to the capability

.

to start from the redundant side of the air start system. After

replacement of the regulator, DG 2 start time was about 8.5 seconds, the

normal starting time.

.a.

_

,

. . -

- _ -

-

--.-

. - - -

~ . - . . - . - .-

.....;...

- - - .

. - - . - , - - .

___ . _ _ _

___._

_____

__

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e

,

4

h

16

4

i

j

c.

Conclusions

The inspector concluded that a questioning attitude and conservative

i

decision making led to the discovery of a problem with DG 2.

The

,

-preplanned systematic approach to problem solving was beneficial to an

i

orderly timely resolution of the issue.

El.2 Environmental Oualification

!

.,

a.

Inspection Scope (37550)

,

J

The inspectors reviewed the licensee's corrective actions for the EQ

program, in res3onse to findings identified during Self Assessment

1

95 0041 and 96 0271 and the violations identified in NRC IR 50 325(324)/

j

96 14,

i

j_

b.

Observations and Findinas

a

.

1)

Status of EQ Justifications for Continued Operation

!

The licensee has issued 13 JCOs in response to deficiencies

!

identified in their EQ program.

Four of the JCOs have been closed

and nine remain open. The requirements for JCOs are specified in

i

Section 6 of Attachment 2 to CP&L procedure EGR NGGC 0156,

i

Environmental Qualification of Electric Equipment Important to

Safety. The procedure requires that a CR be initiated and that a

4

JC0 be prepared to address the problem. The-instructions for

,

!

preparation of the JC0 references NRC Generic Letter 9118.

Subject: Information to Licensees Regarding Two NRC Inspection

Manual Sections on Resolution of Degraded and Nonconforming

l

Conditions and on Operability, dated November 7, 1991. The JC0s

were reviewed by the inspectors during previous inspections and

!

were found to be technically adequate.

However, closure of the

JCO's has not been timely.

,

i

The JC0s and controlling procedures have been reviewed by the NAS

j

in November,1996, and during a self assessment conducted in June,

1997. CR 96 3799 was issued on November 15, 1997, as a result of

the NAS review,' which determined that the site procedures used to

prepare JCOs did not reference the appropriate regulatory

'

requirements. -These requirements were incorporated into EGR NGGC-

'

0156.- A finding from the self assessment concerned the lack of

consistency in the JC0s and the fact that the ESRs written for the

!

JCOs were not processed as design change ESRs.~ CR 97 2008 was

initiated on June 5, 1997 to document and disposition this

-

finding.

2)

EQ Equipment Inspection

The licensee's corrective action program to address the EQ program

deficiencies identified in NRC IR 50 325(324)/96 14 included a

<

_

commitment to perform a walkdown inspection of all EQ equipment to

4

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.

.

17

verify the equipment was installed in accordance with the

requirements specified in QDPs. The inspectors reviewed CP&L

Special Procedure OSP 96 014 EQ Equipment Field Verification,

Revision 1 dated April 18, 1997. This procedure specifies the

requirements for performance of walkdown inspections which are

being performed to determine if EQ equipment was installed in

accordance with the configurations required by the ODPs.

The

procedure contains a three page data sheet for recording and

review of the field inspection data.

Pages one and two of the

o ta sheets are used fo, recording the results of the field

inspections.

Page 3 of the data sheet is completed by a _ qualified

EQ engineer to document disposition of the field inspection

results, including deficiencies in the installed equipment.

The inspectors accompanied members of the EQ Task Force ad

witnessed these individuals in performance of walkdown

i

inspections.

Equipment examined during the walkdowns included the

l

following:

Unit 2 Post Accident Sampling System (PASS) valve numbers 2-

-

4183, 4186, 4188,

4189, and 4192.

Unit 2 Containment Atmospheric Control valve numbers 2 CAC-

-

SV 4540 and 213A.

Unit 1 motor control center (MCC) 1XDA

-

The purpose for examining the MCCs was to identify the type of

equipment (e.g., breakers, resistors, overload relays, etc.)

installed in the MCCs and the location installed in the MCCs. The

MCC walkdown data will be compared to the EDBS. The EDBS will be

corrected to reflect the information from the field walkdowns.

When equipment is identified which is not listed in EDBS, and for

which has not been qualified by a ODP, a CR will be issued, and if

appropriate, a JC0 will be written. The inspectors noted that

during inspection of the MCCs, the gasket materials around the MCC

doors were examined to determine if the gaskets were intact and

were performing their function to seal the HCCs. These gasket

materials had been replaced in 1996 as part of the corrective

actions for CR 96 02545. The replacement gasket materials were

qualified under ESR 96 00659.

A JC0 was issued under ESR 96 00501

to resolve concerns regarding qualification of equipment in the

MCCs. Discussions with licensee engineers and review of the

ESR/JC0 disclosed that two additional ESRs had been issued to

"

address replacement of gasket materials which were inaccessible

and could not be replaced in 1996. These gaskets were the ones

originally supplied with the MCCs by the vendor, Ger,eral Electric,

and had been qualified for the life of the plant. However tests

which were performed on the original gasket materials disclosed

that the gaskets had been fabricated from different materials

which had a life of only approximately 30 years and will require

replacement in the years 2003

2005. This problem had not been

._

.

..

.

-

- -.

..

.

.

18

documented in a CR as required by the licensee's corrective action

program specified in CP&L procedure OPLP 04.

Failure to initiate

a CR to document and disposition this issue was identified to the

licensee as violation item 50 325(324)/97 08 07. Failure to

Initiate Condition Reports to Document EQ Equipment Installation

Deficiencies. The licensee initiated CR 97 02262 on June 26, 1997

to document this problem after this violation was identified.

During the walkdowns licensee engineers identified unmarked wires

on PASS valves 4188 and 4189. Review of original construction

documentation identified the type of wire which had been installed

during plant construction, a description of the wires, and the

reason for installation. CR 97 02143 was initiated to document

the fact that unidentified and/or potentially unqualified wiring

was found on the PASS valves.

'

The inspectors also observed portions of the installation of new

EQ seals for ASCO Tripoint pressure switches N010 and N027.

The

seals were installed adjacent to the instruments. The seals had

been originally installed at the junction box, with a piece of

flexible conduit between the junction box and instrument.

Since

the flexible conduit was not EQ qualified it was necessary to

-install new seals adjacent to the instrument to comply with the

QDP. This problem was documented on CR 9700508 which was

!

initiated on February 3, 1997, and a JC0 issued under ESR

97 00087.

3)

Review of EQ Equipment Inspection Data Sheets

The inspectors reviewed the EQ Component Field Verification Data

Sheets for walkdown inspections completed between February 1

through 15, 1997, and other randomly selected components which had

been field inspected through March 15, 1997. The data sheets were

completed in accordance with OSP 96 014.

Information on the data

sheet pages 1 and 2 included field walkdown data, identified

deficiencies and included comments on potential EQ concerns.

Sheet 3 of the data sheets contains a summary of a review of the

walkdown data by a qualified EQ engineer and lists deficiencies

which require repair.

Review of the data sheets disclosed that

the field inspectors identified numerous potential deficiencies in

installation of EQ equipment where the installed equipment did not

comp /or manufacturer's requirements.ly with the requirements of the qualificatio

and

As discussed below, some

potential deficiencies had not been addressed on page 3 of the

data sheet by the EQ engineers when they reviewed the data sheets.

The inspectors noted comments in the data sheets regarding lack of

weep holes in junction boxes, potentially damaged gaskets on

junction boxes, and other comments regarding possible effect of

moisture intrusion on EQ equipment.

However, these comments /

concerns had not been addressed in the review of the EQ field

,

.

19

inspection notes as documented on page 3 of 3 of the field

inspection data sheets. The inspectors noted that CRs 97 1841,

97 2017, and 97 2025 had been initiated between May 23 and June 6,

1997, to document and disposition some of these problem.

In .ome

cases the data sheets (page 3 of 3) were signed off several wr.eks

prior to initiation of the condition reports.

Pending further

review by NRC of the various issues concerning the effect oi

moisture on EQ equipment, and identification of corrective actions

and the affected equipment, this problem was identified to the

licensee as URI 50 325(324)/97 08 08. Control of Moisture in

Installation of EQ Components.

Review of the data sheets also disclosed comments on the possible

incorrect installation of Raychem splices. These comments

indicated that some Raychem splice installations may not comaly

with the manufacturer's recommendations or the licensee's QD) for

Raychem splices.

Discussions with EQ task force personnel and

review of licensee documentation disclosed that licensee

engineers, in review of Operating Experience report OE 8238, noted

that non conforming configurations had been identified for some

Raychem splices installed at BNP. However, this )roblem was not

documented on a condition report as required by tie licensee's

corrective action program.

The failure to initiate a CR to

document and disposition the potentially defective Raychem splices

was identified as another example of violation item VIO 50-

325(324)/97 08 07, Failure to Initiate Condition Reports to

Document EQ Equipment Installation Deficiencies,

c.

Conclusions

The licensee is making progress in addressing the previously

identified deficiencies in the EQ program. However, the failure

to initiate CRs to document nonconforming items when they are

identified continues to be a 3roblem which resulted in a violation

which was identified during tie inspection. An unresolved item

was identified for concerns related to moisture intrusion into EQ

equipment.

E1.3 Followuo on Service Water System Reoairs

a.

Inspection Scooe (37550)

The inspectors reviewed the licensee's actions to evaluate

corroded bolts in a support on a service water booster pump motor

cooler pipe su) port and two through wall leaks in the vital

service water leader.

b.

Findinas and Observations

On June 23. 1997, two of four anchor bolts on pipe support number

1 SW 148PG248 on the Unit 1 IB RHR service water booster pump

motor cooler inlet line 1 SW 1481417A were found to be severely

J

.

.

20

corroded. The bolts, when measured using ultrasonic testing (UT),

were found to have no measurable embedment length in the concrete.

This aroblem was documented on CR 97 02213. The UT inspections

were :eing performed in response to corroded anchor bolts

identified on the Unit I nuclear service water header in

January, 1997. This issue was discussed in NRC IR 50 325(324)/

97 02.

Review of the results of the NDE showed that while two bolts were

corroded and had no embedment length in the concrete, the

remaining two anchor bolts were in acceptable condition to carry

their design loads. The licensee performed an operability review

,

of the degraded bolts in accordance with CP&L procedure EGR.NGGC.

0320. Civil / Structural Operability Reviews, Revision 0, dated

i

'

May 8, 1996. The inspectors reviewed ESR 97 0351. Revision 1.

l

which documents the operability review.

The operability review

was performed by assuming only two bolts were remaining to carry

the piping loads.

The analysis showed that the supports were

operable until the next refueling outage.

The licensee identified two leaks in a section of piping on the

Division 1 vital service water header.

These-

documented on CR numbers 97 02013 and 02108. problems were

Each leak was

estimated to be approximately one drop per minute.

Based on the

results of NDE ultrasonic testing, licensee engineers determined

that the leaks were of the " pinhole" type.

The inspectors

reviewed ESR 97 00326, Revisions 0 and I which evaluated the

)iping wall thickness using the guidance provided in Generic

.etter 90 05. The conclusion of the ESR was that the piping was

operable until the next refueling outage.

.c.

Conclusions

The 11censee's actions to evaluate the corroded-anchor bolts on

the service water system booster pump pipe support and the pinhole

leaks in the vital header were conservative and completed

promptly. Engineering response to these issues is rated as a

strength and a continuing example of good engineering support to

plant operations. The inspectors concurred with the results of.the

licensee's operability evaluations.

E3

Engineering Procedures and Documentation

E3.1 UFSAR Review

a.

Inspection Scooe (37550)

The inspector examined the licensee's-program for review of the UFSAR.

_

.

.

i

21

b.

Observations and Findings

l

Theinspectorsreviewedthelicensee'sUFSARreviewproject, The

l

purpose of the review is to provide reasonable assurance that the UFSAR

properly reflects the current plant configuration, plant processes and

procedures, and operating oarameters.

The inspectors reviewed CP&L

S>ecial Procedure OSP 96 0)3, Revision 0, dated June 28, 1996. UFSAR

P1ase I Review, This procedure provides instructions for aerformance of

the review, As a result of the review, approximately 250 CRs have been

initiated to document discrepancies identified in the UFSAR during the

review. The discrepancies include the following: Administrative errors

such as typos and incorrect references; errors in the original FSAR

which were carried over into the current UFSAR: and errors resulting

from implementation of modifications which were not considered when

updating the UFSAR. The inspectors reviewed the CRs and concluded that

I

none of the UFSAR errors affected operability of any safety related

systems,

c.

Conclusions

l

The inspectors concluded that the licensee's Phase 1 UFSAR was

!

performed in accordance with their procedure and was an effective

i

program for identification of errors, The licensee is considering

various options for aerformance of additional UFSAR reviews to

assure that the UFSAR accurately reflects the design, operation,

and licensing basis of the plant,

E3.2 Review of Design Basis Documents (DBD)

a,

Insoection Scope (375501

The inspectors reviewed two DBDs to determine their content and

accuracy pertaining to documentation of the design basis for the

Brunswick Plant.

b,

Observations and Findinas

The inspectors performed a review of DBD 09, Neutron Monitoring,

Revision 1, dated May 29, 1997, and DBD 100 Equipment Qualification,

Revision 0, dated December 6, 1993.

DBD 09 was recently revised to

include design information on the power u) rate project.

However the

inspectors noted that the references in tie DBD were incomplete

regarding the response to Generic Letter 82 33, Sup lement No. I to

NUREG 0737

Requirements for Emergency Response Ca ability Regarding

Post Accident Neutron Monitoring Instrumentation,

eferences not

included in the DBD included the licensee's letter dated August 30,

1993, Serial: BSEP 93 0142, and a letter from NRC to CP&L dated

February 15, 1993. These letters concerned the licensee's

implementation of the BWR owners group position on Regulatory Guide 1.97, documented in NED0 31588 regarding qualification of the neutron

monitoring system. The NED0 31588 report

neutron monitoring system instrumentation, proposed criteria for the

in lieu of the Category 1

.

.

22

criteria fn:1uded in RG 1.97. The proposed criteria, which was accepted

by NRC in o Safety Evaluation Report attached to an NRC letter to CP&L

dated April 7. 1993, does not require the neutron monitoring

instrumentation to be included in the EQ program.

Review of DBD 100 showed that this DBD was incomplete and contained

references to procedures which had been recently deleted / superseded by

new procedures.

Also, numerous NRC documents, such as Information

Notices relating to EQ issues were not referenced in the DBD.

However,

as part of the corrective actions to the EQ violations discussed above,

the licensee is in the process of reviewing and updating the DBD. The

inspectors reviewed ESR 97 00055. EQ NRC Docum ntation Identification.

This ESR. which has been partially completed, will include a review of

NRC documents such as circulars, generic letters, bulletins, and

information notices, and verify they have been included in the BNP EQ

program,

c.

Conclusions

The licensee's corrective actions for the EQ program will address the

insufficient detail in DBD 100.

Further review will be performed by NRC

to determine the adequacy of other DBDs.

E4

Engineering Staff Knowledge and Performance

E4.1 Thermo electric Cooler Oper3bility Timeliness

(

a.

Inspection Scope 137551)

The inspector reviewed the timeliness of the operability assessment for

the Hydrogen /0xygen Analyzer Thermo electric coolers,

b.

Qblenations and Findinas

In 1993 a 10 CFR Part 21 evaluation was issued concerning a reduction of

the qualified life of the hydrogen / oxygen analyzer thermo electric

cooling units from 40 to two years due to galvanic corrosion. The

licensee reviewed the Part 21 notification and decided not to decrease

the qualified life of the component.

Upon discovery, the licensee

initiated tracking LC0 for both units in accordance with Operating

Instruction 001 1.08 Control of Equipment and System Status. Tracking

LCOs TI 97 542 and TI 97 543 were initiated ai. 1:00 p.m. on June 5,

1997, with a 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> duration causing the LCOs to expire June 7, 1997,

at 1:00 p.m.

On June 7. 1997, around 2:15 p.m., the inspector questioned the shift

superintendent (SS) on the status of the operability assessment.

The SS

stated verbal acceptance had been given at 12:17 p.m. but an approved

ESR would not be completed in accordance with the established duration.

The inspector questioned why an extension was not requested in

accordance with 001 1.0.8.

The SS subsequently requested and received

-

.

.

23

>ermission for an extension at 3:00 p.m.

CR 97 2028, Untimely

)ocumentation for LCO, was initiated documenting this occurrence.

TS 6.8.1 requires that written procedures be implemented for eg2.pment

ul

control as recommended in Appendix "A" of RG 1.33, November 19

001-

1.0.8 required that the Manager 0perations and the manager of the

assisting organization approve any extension of the initially

established time frame.

The inspector noted that the acting manager of

the assisting organization was a member of the team performing the

operability assessment.

The failure to properly obtain an extension in

accordance with 001 1.08 until questioned by the inspector was

identified as a violation.

This violation is the second example of VIO

50 325(324)/97 08 01, TS/LCO Administration,

c.

Conclusions

Upon exceeding the tracking LC0 covering the hydrogen / oxygen thermo-

i

electric qualified life operability review, on extension was not

obtained until questioned by the inspector.

This was a violation of the

i

plant operating instruction.

E5

Engineering Staff Knowledge and Qualification

E5.1 Trainina and Qualification of Svjtem Enaineers

a.

IDSpection Scope (37550)

The inspactor reviewed the licensee's program for training and

qualification of personnel in the EQ task force including both

I

CP&L and contract engineers,

b.

Observations and Findinas

The inspe';ars reviewed Training Administrative Procedure (TAP)

6.04, Revision 1. dated January 14, 1997 Engineering Support

Personnel Job Specific Training Guide for Plant Engineers. This

procedure specifies the licensee's arogram for training and

qualification of engineers within tie Brunswick Engineering

Support Section (BESS). The ins)ectors also reviewed the

qualifications of engineers in tie EQ task force. These included

CP&L direct employees and contract engineers employed temporarily

in the EQ task force. The records indicated that the 3ersonnel

involved in the EQ program were well

With the exce) tion of one individual, qualified in the

EQ area.

all CP&L direct employees

involved in tie EQ program have completed training and are fully

qualified as modification engineers as specified in TAP 6.04. The

contract engineers, with the exception of a recently hired

individual, were all fully qualified as EQ engineers in accordance

with Attachment 9 of TAP 6.04.

However the inspectors noted that

contract engineers did not require training in the licensee's

corrective action program, CP&L procedure OPLP 04

The TAP 6.04

training program requires self study (reading for understanding)

,

.

.

24

of procedure OPLP.04.

Failure to include this recuirement as part

of the contract engineers' training was identificc to the licensee

as a weakness. CR 97 01927 was recently initiated to document an

issue that engineers in the EQ group were concerned that

nonconformances were not being addressed appropriately.

A finding

was also identified during the recently completed self assessment

in the EQ group that the threshold for when a CR should be written

was inconsistent among personnel in the EQ task force,

c.

CODelusions

The inspector concluded that the licensee's program for training

and qualification of EQ engineers meets NRC requirements. A

weakness was identified for failure to require that the contract

engineers receive training on the licensee's corrective action

program.

E8

Hiscellaneous Engineering Issues (92903)

E8.1 (Closed) VIO 50 324/96 04 03:

Inadequate Work Instructions for Main

Steam Line Radiation Trip Modification

This violation was issued as a result of inadequate work instructions

for deleting the Main Steam Line High Radiation Trip function for

Unit 2.

A similar violation occurred during installation of the same

modification on Unit 1 dlaing the Spring 1995 Refueling Outage.

The licensee responded to this violation in a letter dated May 29, 1996.

The licensee's corrective actions included a work stoppage, a design

package review, disciplinary action for the persons involved and

establishing procedural direction to require independent verification of

modification implementation packages by appropriate technical personnel.

The inspectors reviewed CR 96 00594: Action Item Assignment Project 10

96 00594.1: and Engineering Request EGR NGGC 005, " Engineering Service

Requests, Revision 4. The inspectors verified through these reviews that

the ap3ropriate corrective actions were taken by the licensee. Based

upon t1ese reviews, this violation is closed.

E8.2 (Closed) URI 50 325(324)/95 22 01: Control Building Ventilation Problems

(Closed) llR 50 325/95 020: Control Building Emergency Air Filtration

System (CBEAF), Unable to Maintain Positive Pressure

(Closed) LER 50 325/95 020 01: Control Building Emergency Air Filtration

System (CBEAF), Unable to Maintain Positive Pressure

The problem was identified during testing of the control room pressure

envelo)e on October 25, 1995. The control room pressure is required by

TS to >e positive to minimize radioactive material intrusion into the

control room during accident conditions. The licensee immediately

established compensatory measures once the problem was identified.

The

!

_

.

.

25

most probable cause of the negative pressure condition was the

cumulative degradation of control room cable seals and ductwork.

Following completion of trouble shooting activities, system repairs, and

a satisfactory surveillance test, the control building ventilation

system was declared operable with no compensatory measures on

December 4, 1995.

The licensee Supplement 1 to LER 195 20, committed to 1) a development

and implementation plan which establishes periodic functional testing of

control building HVAC system and components: 2) develop and implement a

preventive maintenance inspection procedure to evaluate the condition of

and repair as required the control building access door seals: and

3) complete a safety system functional inspection (SSFI) for the control

building HVAC system.

The inspector reviewed the plan for periodic testing.

This plan listed

all current periodic tests and surveillance tests required by TS.

Several preventive maintenance items were added to the required tests to

formalize the plan. The inspector reviewed the preventive maintenance

check list developed for doors and seals. The licensee conducted an

SSFI during April 29

May 31, 1996. A significant issue was found in

the SSFI concerning the Q list downgrade to non-Q of the control

building air conditioning units. This downgrade was done without a 10 CFR 50.59 safety evaluation being perf e ed. This item will be reviewed

to determine why a 10 CFR 50.59 review was not aerformed. This is

identified as URI 50 325(324)/ 97 08 09, 50.59 leview for Control

Building Air Conditioning Quality Classification Downgrade.

Additionally, after submittal of the power uprate license amendment

request, several cuestions concerning control building ventilation

system were raisec. The licensee committed in a letter to the NRC dated

February 15, 1997, to two commitments to be completed by the end of the

Unit 1 twelf th refueling outage scheduled to start in April 1998. The

first commitment was to evaluate the sealing and pressurization

capabilities of the existing CREVS and to implement imarovements to

increase pressurization of the control room while in tie smoke / radiation

protection mode. The second commitment was a part of a comprehensive

plan to resolve all remaining open items associated with the SSFI.

The inspector reviewed the licensee's project plan for the issues

committed to by the licensee to resolve all control room ventilation

issues.

It is a comprehensive plan with a dedicated project manager.

The programmatic review of the licensee committed corrective actions

will be tracked as IFI 50 325(324)/97 08 10 Review of Control Room

Ventilation Issues. The URI and LERs associated with these issues are

closed and completion of the corrective actions will be tracked as part

of the IFI review.

E8.3 10pftn) VIO 50 32E(324)/96 15 06:

Repeat Failure to Take Adequate

Corrective Action; for Chlorine Detector Failures

j

.

.

26

1 Closed) VIO 50 325(324)/96 05 01:

Failure to Take Corrective Actions

for Chlorine Sensors

(Closed) LER 50325(324)/9612:

Five of 8 Chlorine Detectors Inoperable

(Closed) LER 50 325(324)/96 05.1 Six of 8 Chlorine Sensors Used for

Control Building Isolation Logic Were Found Inoperable

(Closed) LER 50 325(324)/95 021 Multi)1e Chlorine Sensors used for

Control Buildin Logic Were Found to )e Outside Technical Specification

Tolerance Durin Routine Calibration

Based on the corrective actions for the repeated failures of the

chlorine detectors as described in IR 50 325(324)/96 15 being the same,

the closure of these issues will be tracked under the associated

violation 50 325(324)/96 15 06, Repeat Failure to Take Adequate

Corrective Action for Chlorine Detector Failures.

E8.4 1 Closed) LER 50 325/96 02 01: Unit 1 Hanual Reactor Scram Due to Main

Turbine Vibration

Based on NRC review as documented in IR 50 325(324)/96 01 and 50-

325(324)/97 02 this item is closed.

IV. Plant Sunoort

R2

Status of RP&C Facilities and Equipment

R2.1 Radioactive Material Postina

,

a.

Inspection Scope (71750)

The inspector reviewed the posting of radioactive material area (RMA),

b.

Dh gr_gtions and Findinas

On June 20, 1997, the licensee extended the radiation control area (RCA)

to include the transformer switchyard, Auxiliary Off Gas, Diesel and

Water Treatment Building, the Condensate Storage, Deniineralized Water

Tanks for both units, as well as the Diesel Fuel Oil Storage Tanks.

During routine inspections of the RCA on June 24 25, 1997, the inspector

noted inconsistencies in the posting of radioactive material areas. At

-the north end of the RCA, between the Unit 1 Turbine Building and the

Radioactive Haterial Control Storage Building, the inspector observed

several metal containers and other equipment. All equi) ment observed

was labeled, however only the metal containers were wit 11n the posted

roped off RHA. Additional review of the RCA revealed numerous

inconsistencies in RMA posting.

Some radioactive material is located

within roped off areas

other material was not, the outside areas of

the RCA encompassing half the plant site are considered one continuous

RMA. -Therefore, areas used to store RMA are not always posted. One

area the inspector noted was behind the Radwaste loading dock. This

.

.

27

area contains several high integrity containers which served as a

temporary storage arec until the waste can be moved to its designated

storage location. The area was posted as a radiation area, but not a

RMA despite the presence and storage of radioactive material.

The inspector discussed these inconsistencies with the licensee and

reviewed Nuclear Generation Group Standard Procedure HPS NGGC 0003,

Radiological Posting, Labeling and Surveys.

Discussions with the

licensee revealed a dichotomy concerning how radioactive material should

be posted. The inspector could not locate a comprehensive standard site

practice or expectation for the posting of RM within the RCA.

Section

9.1.8 Radioactive Materials Area of HPS NGGC 003, provided adequate

instruction for the establishment cf RMA outside of the RCA.

However,

no comprehensive instructions for the establishment of RMA's within the

RCA could be located.

The lack of comprehensive instructions for the

l

establishment of posted RMAs within the RCA was seen as a weakness.

l

'

c.

fanclusions

A lack of comprehensive procedural guidance or standard site practice

contributed to the inconsistent posting of radioactive material within

the radioactive controlled area.

R8

Miscellaneous RP&C Issues

R8.1

(Closed) Violaijpn 50 325(324)/96 04 04:

Failure to Conduct CAT

This violation was issued as a result of individuals being allowed

unescorted access to contaminated areas of the plant without the

required contamination area training.

The licensee responded to this violation in a letter dated May 29, 1996.

The licensee's cor rective actions included a review of Contaminated Area

Training (CAT) records to identify those individuals required to work in

restricted areas who had not received CAT instruction, the conduct of

special training classes for those individuals identified as not having

.

CAT, and implementation of an electrcnic flagging feature to ensure that

'

only >ersons who have completed CAT ate allowed to sign on a Radiation

Work Jermit and an assessment of the programs implement to ensure

adequate barriers exist to prevent the performance of work without the

required CAT.

The inspectors reviewed Action Item Assignment Project ID 96 00823.9 and

96.00823.11 through 96 00823.17. Each of these Action Item Assignment

packages contained a Self Assessment Report that described the

effectiveness of the barrier designed to provent the performance of work

without the required training. The inspectors identified no

deficiencies during the review of the Self Assessment Reports.

Based

upon these reviews, this violation is closed.

.

.

1

,

.

28

F1

Control of Fire Protection Activities

F1,1 Qual Unit Downoower Due to Fire Suppression System Declared Inonerable

a.

Inspection Scope (71750)

The inspector reviewed the dual unit downpower that occurred on June 20,

1997, following declaration that the fire suppression water system was

inoperable,

b,

Observations and Findinas

On June 20, 1997, at 6:00 p.m., the fire suppression water system was

declared inoperable. The system was declared inoperable because during

a flow test performed by 0PT 34,7,10, Fire Suppression Water System Flow

Test, the test results did not meet the acceptance criteria. The test

results were logged into the Loss Prevention Unit (LPU) Shift Supervisor

log on June 19, 1997, at 6:00 p.m.

but were not adequately communicated

to Hanagement.

Plant Procedure OPLP 01.2 Fire Protection System Operability. Action,

and Surveillance Requirements, required that, with the fire suppression

water system inoperable, a backup fire suppression water system must be

established within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or be in at least HOT SHUTDOWN within the

next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in COLD SHUTDOWN within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Plant Management concluded that 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> had elapsed prior to

establir,hing a backup fire suppression water system and proceeded to

initiate a dual unit shutdown. This was a conservative decision. The

sequence of events was as follows:

llE

EYff

Jslie_12

6:00 p.m.

Fire Suppression System Test Does Not Meet

Acceptance Criteria Logged into LPU Shift

Supervisor Log.

June 20

6:00 p.m.

Licensee starts 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> to hot shutdown LCO.

10:10 p.m.

Unit 2 started power reduction.

11:00 p.m.

Unit I started power reduction.

11:02 p.m.

Licensee made 10 CFR 50.72 one hour report to

NRC,

June 21-

2:45 a.m.

_ Licensee re performs test which again did not

meet acceptance criteria.

_ _

_ _ _ _ - - . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ ___ _ __ _ _ _ _ __.

.

.

29

4:15 a.m.

Fire watches established as compensatory

measures for portion of fire main loop that

was believed to be partially blocked or had

reduced flow.

5:38 a.m.

Units stop shutdown both units around 22

percent power based on compensatory actions

for portion of fire main loop that had reduced

flow.

6:00 a.m.

Power increase started.

4:20 p.m.

ESR 97 000348 determined that an error was

made in the calculation of test date.

June 22

Test date for last performance of test in 1995

found to be questionable.

The inspector reviewed the test procedure, OPT 34.7.10. The purpose of

the test was to determine the water flow capability of the Fire

Suppression Water System underground loop piping. This surveillance

test was required by OPLP 01.2, step 6.1.3.1.f.

At least once per three

years a flow test was required to be performed in accordance with

Chapter 5, Section 11. of the Fire Protection Handbook,14th edition,

published by the National Fire Protection Association.

This procedure

performs three flow tests and calculates a "C", friction loss co-

efficient for each flow test. The acceptance criteria was a C factor

greater than or equal to 100. The test takes pressure readings at

various locations under static conditions and then takes pressure.and

nozzle flow readings under dynamic conditions.

This data is then used

to perform a fluid flow calculation to determine the C factor.

1

The reason the test was performed on June 19, 1997, was because of CR

97 02142. Suspect Flow in the Fire Header.

During fire drills in recent

weeks LPU personnel noticed an apparent drop in pressure at the hose

nozzles. The test data taken on June 19, 1997, indicated a C factor

greater then 100 for test one and test two but test three was 83. The

test was re performed on June 21, 1997, and determined to give similar

results with a value of 84 for test three. They concluded that there

was a partial system blockage or reduced flow in a portion of the fire

main loop.

The licensee performed a technical review of the test data and

determined there was an error in the calculation. This analysis was

' documented in ESR 97 00348, Evaluation of OPT 34.7.1.0. Fire Protection

Flow Test Data.

The licensee concluded that there was an error in the

calculation and the static differential pressure should be applied as a

correction factor when measuring differential pressure under dynamic

conditions. This data was. collected as cart of the test but was not

specified as to how the C factor was to oe applied in the calculation.

Once this correction was made, the test data for test three indicated

valves greater than 100. The licensee concluded that there was no

system blockage and the test data was acceptable.

.

.

30

The inspector reviewed the test procedure OPT 34.7.1.0 and ESR 97 00348.

The inspector concluded that using the )rocedure as written would not

provide accurate results. TS 6.8.1,f,

rire Protection Implementation,

requires that written procedures shall be established, implemented, and

maintained covering the Fire Protection Program.

The test procedure was

not adequately maintained and was identified as a violation of TS 6.8.1.f.

The licensee identified and corrected violation is being

treated as a Non Cited Violation (NCV), consistent with Section VII.B.1

of the NRC Enforcement Policy. This will be tracked as NCV 50 325(324)/

-97 08 11,- Inadequate Fire Protection Flow Test Procedure.

Additionally, the inspector questioned how the system flow data compared

to the last >erformance of the three year test in 1995.

The licensee

determined t1at the C factor was not calculated in 1995. As a result of

an audit finding, the procedure was changed to put the C factor

determination back into the procedure, liowever, taking the pressure and

flow date from 1995 and calculating a C factor determined that the data

was not reasonably close to the expected values. The C factor values

ranged from 576 to 303.

Data taken from a Fire Protection Handbook

indicated the following C. factor valves:

._ip.e

G.fAC10C

P

Jnlined Cast Iron, new

120

Unlined Cast Iron,10 years mildly corrosive water

110

Unlined Cast Iron, 20 years mildly corrosive water

90

Unlined Cast Iron, 30 years mildly corrosive water

80

Cast Iron, cement lined

140

Steel Pipe, new

140

Therefore, the data in 1995 was erroneous and was not questioned until

the inspector requested a comparison. The purpose of these flow tests

being performed every three years was to monitor system performance and

possible problems.

The inspector determined that the failure to identify a trend in the

1995 test results and establish a baseline data for OPT 34.7.1.0 was a

weakness in trending and monitoring of the fire protection water

suppression system performance.

The inspector reviewed the licensee's Corporate Quality Assurance

Program (CQAP) Hanual

Section 15. QAS Program for Fire Protection

Systems.

Section 15.8, Conditions Adverse to Quality (CATO), states

that CATQ for fire protection related items shall be identified,

reported, dispositioned, and corrected in accordance with Section 12.

Conditions Adverse to Quality and Correction Action. Section 12 of the

CQAP manual implements 10 CFR Appendix B. Criterion XVI, Corrective

' Action.

Accordingly, a violation of 10 CFR Appendix B. Criterion XVI, Corrective

Action, as committed to by the licensee's CQAP for fire protection

related items was identified.

_ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ -

_ _ _ _ _ _ _ _ _ _ _

_ _ _ _ - _ _ _ _

__

_ - _ _ _ _ _-__________ _ _______ -__-__-- ___

.

.

31

,

A violation was identified for failure to promptly take corrective

1

action for a flow test >erformed on June 19, 1997, that did not meet the

1

acceptance criteria. T1e results for the test were not adequately

communicated to Hanagement until the next day. This licensee identified

and corrected violation is being treated as a NCV consistent with

Section VII.B.1 of the NRC Enforcement Policy. This will be tracked as

NCV 50 325(324)/97 08 12. Failure to Take Corrective Action for Abnormal

Fire System Flow Data.

Additionally, there was a comunir.ations interface problem with

Operations. The licensee had taken the approach to fire protection as

not being part of TS and placed control of the systems out of

Operations.

For example, in IR 50 325(324)/97 07 the inspector

discussed a compensatory fire protection problem with Operations but was

told that LPU had control over this issue and all discussion should be

with LPU.

In fact, in LPU shift supervisor's log, there is an LC0

statement to indicate when a fire protection LC0 was initiated or

canceled. The LCOs are not logged or tracked by Operations.

In the

past few months, the fire )rotection engineer was taken out of

engineering and placed in

_PU.

The inspector discussed with licensee management that licensed operators

must maintain control of the LCOs for fire protection equipment. The

facility operating license requires that the fire protection program be

maintained. The TSs require that the fire protection program procedures

be established, implemented, and maintained.

The inspector attended a debrief on July 2.1997, of an NAS audit of the

fire protection program.

Several issues were identified by NAS. The

NAS team assessment concluded that the program was ineffective based on

a number of program elements being below acceptable standards,

c.

Conclusions

The inspector concluded that plant management made a conservative

decision to perform a dual unit shutdown based on the untimely and

erroneous test results provided by the LPU. An ongoing NAS audit

identified several issues in this area.

Two non cited violations were

identified for failure to promptly take corrective action when flow test

performance did not meet acceptance criteria and for an inadequate fire

protection flow test procedure. A weakness was identified in trending

and monitoring of the fire protection water suppression system

performance.

F1.2 Transient Combustible in Seoaration Zone

a.

Inspection scope (71750)

The inspector, during routine inspection activities, observed the

improper storage of combustibles in the Unit I reactor building.

.

.

32

b.

Observations and Findinas

The Safe Shutdown Analysis defines separation zones as areas " intended

to provide separation between redundant trains in lieu of three hour

barriers," Keeping these zones free of combustibles is required to

prevent a fire from damaging redundant safe shutdown equipment on either

side of the zone.

The requirement was established as part of the fire

protection requirements in a Safety Evaluation Report dated December 30,

1984.

During routine inspection activities on June 23, 1997, the inspector

observed transient combustible material stored within a separation zone

located on the 50 foot elevation in Unit 1.

The inspector questioned a

nearby worker regarding the material. The material was immediately

removed and the LPU supervisor was notified.

The separation area was

posted indicating that no transient combustibles were allowed.

The failure to maintain the Unit 150 foot elevation separation zone

free of transient combustibles is a violation of TS 6.8.1.f.

This

violation is identified as examples one of VIO 50 325(324)/97 08 13.

Failure to follow Fire Protection Program procedures.

The inspector reviewed the UFSAR section and discussed this event with

the licensee. The inspector reviewed 0FPP 13. Transient Fire Load

Evaluation and 0FPP 14, Control of Combustible. Transient Fire Loads,

and Ignition Sources. These procedures were weak in providing guidance

concerning the maintenance and inspection of fire separation zones.

On June 24, 1997, during routine inspection activities the inspector

observed combustible material in a separation area. This area was

located in the Unit 1 ECCS Mini Steam Tunnel.

The control room was

notified and the items removed.

The entrance to the ECCS Mini Steam Tunnel has a sign on the door

stating that no transient combustibles were allowed to be stored-in the

separation area in accordance with 0FPP 13.

However, from discussion

with the licensee, the actual separation zone was thought to be above

the tunnel and the posting was mislead 61

This item will be-identified

as an unresolved item pending further review and tracked as URI 50-

325(324)/97 08 14 Designation of Fire Separation Zones.

In addition, on July 2.1997, the licensee initiated CR 97 02331,

Combustibles in Separation Zone.

This CR identified that a computer and

desk had been placed in the Separation Zone in the DG building south

end. This area was designated by the Alternate Shutdown Capabilities

Assessment Report as an Alternate Safe Shutdown Separation Zone.

c.

Conclusions

The inspector concluded that there was a violation of the fire

protection procedure for having transient combustibles in a fire

separation zone.

Designation of fire separation zones was unresolved

_

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33

requiring further review.

Implementing-procedures for the establishment

and maintenance of fire protection separation zones were weak. This was

evident by the discovery of transient combustibles in separation zones.

F3

Fire Protection Procedures and Documentation

i

F3,1 Hydrant Isolation Valve Misoositioned

a.

Insoection SCoDe (71750)

The inspector reviewed the circumstances surrounding an out of position

hydrant isolation valve.

g

b.

Observations and Findinas

On June 19, 1997, during the performance of OPT 34.7.1.0, Fire

Sup)ression Water System Flow Test, the isolation valve for hydrant

num)er 5 was found closed. This clocad valve prevented flow from this

section of the fire suppression loop. However, flow was still available

to the other hydrants in the loop via another flow path.

The inspector reviewed the appropriate procedures, associated prints,

and discussed the issue with the licensee.

00P 41 Fire Protection and

Well Water System, required the valve to be open. A review of the last

,'

performance of tir; valve line up in 1995 indicated that the valve was

verified open. Subsequent licensee review has not determined the reason

for the mispositioning. TS 6.8.1.a requires that procedures shall be

implemented and maintained for the Fire Protection System as required by

Appendir iof Regulatory Guide 1.33 November 1972. The failure to

maintain the. valve in accordance with 00P 41, is a violation of TS 6.8.1.a. This licensee identified anti corrected violation is being

treated as an NCV consistent with Section VII.B.1 of the NRC Enforcement

,

Policy. This violation is identified as NCV 50 325(324)/97 08 15.

Hydrant IV Mispositioned,

c.

Conclusions

An NCV was. identified for the mispositioning of a hydrant isolation

valve.

F4

Fire Protection Staff Knowledge and Performance

F4.1 Inadvertent Actuation of Deluae Vah q

'

a.

Insoection Scope (71750)

The inspector reviewed the circumstances surrounding the actuation of

the transformer fire protection deluge system on June 22, 1997.

I

1

m

. _ _ - _ _ _ ___ _ _ _ _ - - -

.

.

34

b.

Observations and Findings

On June 11, 1997, the LPU 3erformed Periodic Test 1PT 34.13.3.3,

Transformer Deluge System runctional Test.

This surveillance

demonstrated the operability of the deluge system for the Unit 1

transformers. The 3rocedure isolated the water source to prevent

spraying water on t1e 230 kV transformer.

System alarm and Control Room

annunciation are verified from the manual pull station and by simulation

of a heat source by use of a heat gun.

The alarms and annunciators are

reset and cleared and then the water source is restored.

During the performance of 1PT 34.13.3.3 on the Unit 1 Startup

Transformer (SAT), the technician halted performance of the test and

left tne work site. U

the wrong transformer,pon the technician's return, work was resumed on

the unit auxiliary transformer (UAT). Upon use

of the heat gun on the UAT heat detector, the UAT fire protection deluge

system actuated spraying water on the energized 24/4.16 kV UAT. The

ins)ector reviewed the procedure, work site, and discussed the event

wit 1 licensee personnel. The procedure indicated under precaution 4.2

that high voltage exists in the transformer area, EXERCISE caution.

Also, precaution 4.4 requires communications must be ESTABLISHED and

MAINTAINED between personnel at the deluge valve, transformer spray

,

l

headers, and the Control Room while performing the test. The inspector

determined that similar labeling on the heat detectors for both

transformers, poor procedural equipment identification, and the

technician's lack of attention to detail were contributing factors to

this event. No personnel were injured nor was any equipment damage or

malfunction noted. The licensee wrote CR 97 02196, Inadvertent Deluge

Actuation, to document this problem.

TS 6.8.1.f requires that written procedures shall be implemented for the

Fire Protection Program.

The failure to implement the test in

accordance with IPT 34.13.3.3 is a violation. This violation is

identified as example two of VIO 50 325/97 08 13, Failure to follow Fire

Protection Program procedures.

c.

Conclusions

Poor attention to detail resulted in the inadvertent spraying of water

on an energized high voltage Unit Auxiliary Transformer.

No personnel

were injured and no equipment damage or malfunction was observed.

'

F8

Miscellaneous Fire Protection Issues (92904)

F8.1

(Closed) VIO 50 325(324)/96 04 06:

Failure to Follow Fire Protection

Procedure

This violation, with two examples, was issued as a result of contractor

painters not implementing the procedural requirements for transient

combustibles and the lack of a valid transient loading evaluation for

combustibles found in both units. Also, the material found on both

~

- _ _ _ ________-___ __ - __ -

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.

.

.

35

units was not properly tracked in accordance with procedural

- requirements.

The licensee responded to this violation in a letter dated May 29, 1996.

The immediate corrective actions included the conduct of a stand.down by

the involved painting contractor and a field verification of the

- transient load evaluation log book by the licensee,

The corrective actions to be taken, as stated in the licensee's response

of May 29, 1996. included a procedural revision to ensure combustible

,

load evaluation requirements are clearly defined and easily understood.

The inspectors reviewed Fire Protection Procedure 0FPP 014. Control of

Combustible Transient Fire Loads, and Ignition Sources, Revision 15.

The inspectors observed during the procedural review that a detailed

l

definition section was 'in the revised procedure and the organization of

the procedure was clear and straightforward. The inspectors also

l

,

observed that training on the procedural revision was presented to

facility personnel to include contractors.

Based upon this review, this violation is closed.

V.

Manaaement Meetinos

,

XI

Exit Meetina Summary

- The inspector presented the inspection results to mcmbers of licensee

management at the conclusion of the inspection on Jaly 10. 1997. Post

inspection triefings were conducted on' June 6 and Juie 27, 1997. The

licensee acknowledged the findings pressated.

PARTIAL-LIST OF PERSONS CONTACTED-

Licensee-

'

G. Barnes. Manager Training

A. Brittain, Manager Strurity

4

M. Christinziano, Manager Environmental and Radiation Control

'

N. Gannon, Manager Maintenance

J. Gawron, Manager Nuclear Assessment

S. Hinnant, Vice President, Brunswick Steam Electric Plant-

K.- Jury, Manager Regulatory Affairs

W. Levis, Director Site Operations

B. Lindgren, Manager Site Support Services

R. Lopriore, General Plant Manager

J. Lyash, Brunswick Engineering Support Section

R. Mullis, Manager Operations

H. Turkal, Supervisor Licensing and Regulatory Programs

,

4

.

.

36

Other licensee employees or contractors included office, operation,

maintenance, chemistry, radiation, and corporate personnel.

E. Brown

J. Canady

J. Coley

J. Lenahan

C. Patterson

H. Shymlock

,

N

.

.

'

37

INSPECTION PROCEDURES USED

IP 37550:

Engineering

IP 37551:

Onsite Engineering

4

IP 61726:

Surveillance Observations

IP 62700:

Maintenance Implementatien

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92901:

Followup

Operations

IP 92902:

Followup

Maintenance

IP 92903:

Followup

Engineering

IP 92904:

Followup

Plant Support

ITEMS OPENED, CLOSED, AND DISCUSSED

l-

Ooened

50 325(324)/97 08 01

VIO

TS/LC0 Administration (paragraphs 08.2. E4.1)

50 325(324)/97 08 02

VIO

Failure to Verify / Check E Bus Relay Operability

(paragraph M1.2)

50 325(324)/97 08 03

VIO

Safety Relay Setting Change Made as Pen and Ink

Changes to Procedure (paragraph M1.2)

50 325(324)/97 08 04

URI

Control of EDBS Information (paragraph Hl.2)

50 324/97 08 05

NCV

Failure to Follow Work Instructions uuring

Previous Installation of Solenoid Valves 2 CAC-

SV 4410 26 & 27 (paragraph Hl.3)

-50 325(324)/97 08 06

URI

Failure to Obtain an EQ Disposition on Extension

of Vendor Recommended EQ Life for Thermo-

Electric Cooler (paragraph Hl.3)

50 325(324)/97 08 07

VIO

Failure to Initiate Condition Reports to

Document Nonconforming EQ Items (Paragraph E1.2)

50 325(324)/97 08 08

URI

Control of Moisture in Installation of EQ

Components (Paragraph E1.2)

50-325(324)/97 08 09

URI

10 CFR 50.59 Review for Control Building. Air-

'

Conditioning Quality Classification Downgrade

(paragraph E8.2)

50 325(324)/97-08 10

IFI

Review of Control Room Ventilation Issues

(paragraph E8.2)

50 325(324)/97-08-11

NCV

Inadequate Fire Protection Flow Test Procedure

(paragraph F1.1)

,

.

..

....

.. . . .

.

.

38

50 325(324)/97 08 12

NCV

Failure to Take Corrective Action for Abnormal

Fire System Flow Data-(paragraph F1.1)

50 325(324)/97 08 13

VIO

Failure to follow Fire Protection Program

procedures (paragraphs F1.2 and F4.1)

50 325(324)/97 08 14

URI

Designation of Fire Separation Zones (paragraph

F1.2)

50 325(324)/97 08 15

NCV

Hydrant IV Mispositioned (paragraph F3.L)

l

Closed

50 325(324)/96 04 02

VIO.

Cooldown Monitoring Not Followed (paragraph

08.1)

i

50 325(324)/97 07 01

URI

Failure to Enter TS ACTION Statement (paragraph

08.2)

50 324/97 08 05

NCV

Failure to Follow Work Instructions During

Previous Installation of Solenoid Valves. ? CAC.

SV 4410 26 & 27 (paragraph M1.3)

50 324/96 01

LER

Control Rod Average 5 percent Insertion Time

Exceeds Technical Specification Requirements

(paragraph M8.1)

50 324/96 01 01

LER

Control Rod Average 5 percent Insertion Time

exceeds Technical Specification Requirements

(paragraph M8.1)

50 324/96 04 03

VIO

Inadequate Work Instructions for Main Steam Line

Radiation Trip Modification (paragraph E8.1)

50 325(324)/97 08 09

NCV

Failure to Perform 50.59 for Control Building.

Air Conditioning Quality Classification

Downgrade (paragraph E8.2)

50 325(324)/95 22 01

URI

Control Building Ventilation Problems (paragraph

E8.2)

50 325/95 020

LER

Control Building Emergency Air Filtration System

(CBEAF). Unable to Maintain Positive Pressure

(paragraph E8.?)

50 325/95 020 01-

LER

Control Building Emergency Air Filtration System

(CBEAF). Unable to Maintain Positive Pressure

(paragraph E8.2)

,

50 325(324)/96 05-01

VIO

Failure to Take Corrective Actions for Chlorine

Sensors (paragraph E8.3)

.

. .

. . . . . . . . . .

..

.

.

.

.

,

___

_

,

...

39

50 325(324)/96 12

LER

Five of 8 Chlorine Detectors Inoperable

(paragraph E8,3)

50 325(324)/96 05

LER

Six of 8 Chlorine Sensors Used for Control

Building Isolation Logic Were Found Inoperable

(paragraph E8.3)

50 325(324)/95 02

LER

Multiple Chlorine Sensors used for Control

Building Logic Were Found to be Outside

Technical Specification Tolerance During Routine

Calibration (paragraph E8.3)

50 325/96 02 01

LER

Unit 1 Manual Reactor Scram Due to Main Turbine

Vibration (paragraph E8.4)

50 325(324)/96 04 04

VIO

Failure to Conduct CAT (paragraph R8.1)

50 325(324)/97 08 11

NCV

Inadequate Fire Protection Flow Test Procedure

(paragraph F1,1)

50 325(324)/97 08 12

NCV

Failure to Take Corrective Action for Abnormal

Fire System Flow Data (paragraph F1.1)

50 325(324)/97 08-15

NCV

Hydrant IV Mispositioned (paragraph F3.1)

50 325(324)/96 04 06

VIO

Failure to Follow Fire Protection Procedure

(paragraph F8.1)

Discussed

50 325(324)/96 15 06

VIO-

Repeat Failure to Take Adequate Corrective

Action for Chlorine Detector Failures (paragraph

E8.3)

i

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...

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