ML20216B174

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Insp Repts 50-324/97-15 & 50-325/97-15 on 971228-980131. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support
ML20216B174
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 03/02/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20216B149 List:
References
50-324-97-15, 50-325-97-15, NUDOCS 9803120431
Download: ML20216B174 (27)


See also: IR 05000324/1997015

Text

U.-S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-325. 50-324

License Nos: DPR-71. DPR-62

Report No: 50-325/97-15. 50-324/97-15-

Licensee: Carolina Power & Light (CP&L)

Facility: Brunswick Steam Electric Plant. Units 1 & 2

Location: 8470 River Road SE

Southport. NC 28461

Dates: December 28. 1997 - January 31. 1998

Inspectors: C. Patterson, Senior Resident Inspector

E. Brown. Resident Inspector

E. Guthrie.. Inspector in Training

J. Coley, Reactor Inspector (Section M1.2 - M2.2)

Approved by: M. Shymlock. Chief. Projects Branch 4

Division of Reactor Projects

9903120431 980302

PDR ADOCK 05000324

0 PDR _

Enclosure 2

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EXECUTIVE SUMMARY  ;

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Brunswick Steam Electric Plant. Units 1 & 2 1

NRC Inspection Report 50-325/97-15. 50-324/97-15

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This integrated inspection included asrects of licensee operations. J

engineering, maintenance, and plant support. The report covers a 6-week 4

period of resident inspection: in addition it includes the results of a

maintenance inspection by a regional inspector.

Doerations

. A recirculation pump trip occi rred as a result of an electrical fault on

a transmission line. The transmission line was promptly restored and

the recirculation pump was satisfactorily ret"rned to service. Operator

response to the resultant transient was good (Section 01.1).

. The inspector concluded that the site alarms were being tested in

accordance with procedure requirements (Section 02.1). j

Maintenance l

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. The inspector concluded, from observation of routine maintenance l

activities, that the licensee was continuing to upgrade the material '

condition of plant equipment and equipment spaces (Section M1.1).

  • Corrective and predictive maintenance activities observed were conducted

in a thorough and effective manner (Section M1.2).

  • Technicians observed performing maintenance surveillance tests were  ;

skillful, experienced, and knowledgeable of their assigned tasks I

(Section M2.1).

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. Discrepancies identified by maintenance technicians during a

< surveillance test indicated weaknesses in foreign material exclusion

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controls test fixture traceability controls and the handling and l

storage of internally contaminated test equipment (Section M2.1).

  • Numerous examples of inadequate control of special processes were

identified by the licensee of vendor examination activities for the

Unit 2. H6B reactor core shroud weld (Section M2.2).

  • Extensive effort was subsequently expended by the licensee to identify

vendor examination problems and to implement corrective actions

necessary to compare ultrasonic data taken during refueling outages 12

and 13 for the Unit 2. H6B reactor core shroud weld (Section M2.2).

. The ECCS Response Time Testing was being conducted as a group of tests

at different times. This methodology requires further review

Section M3.1).

2

e Multiple failures of the Plant Process Computer (PPC) occurred during

the months of December 1997 and January 1998. A violation was issued

for failing to initiate Condition Reports for repetitive failures of the

PPC (Section M4.1).

Enaineerino.

  • Instrument setpoint changes, deemed more conservative than existing TS

requirements, were being made in preparation for converting to Improved

Standard Technical Specifications. The inspector concluded that the

implementing instructions and changes needed additional clarification

and license review (Section E2.1).

  • Inspector's review determined that the logic testing for the reactor

core isolation cooling condensate storage tank low water level automatic

transfer and the generation of the isolation signal on high turbine

exhaust diaphragm pressure were completed satisfactorily in accordance

with Technical Specifications (Section E3.1),

Plant Sucoort

. The inspector' concluded that Health Physics technician daily walkthrough

procedures lacked guidance to ensure continuity of walkthroughs

(Section R4.1).

  • Twenty-eight doors in the Diesel Building were modified defeating the 3

hour fire rating of the doors. An unresolved item was issued to allow

additional review for the failure of the licensee to perform an adequate 1

- engineering review prior to modifying required fire protection quality

hardware (Section F4 1).

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Report Details

Sammary of Plant Status

Unit 1 operated continuously during this report period. At the end of -

this report period the unit had'been on-line continuously for 78 days. '

Unit 2 operated continuously during this report period. A recirculation

pump trip occurred on January 27. 1998, following the loss of an offsite

power feeder line. The transient, which occurred due to an electrical

fault, caused 6 loss of the 2B reactor recirculation pump motor

generator set. Reactor power decreased to around 55 percent due to the

loss of the recirculation pump. At the end of the report period, the

unit had been on-line continuously for 101 days.

Due to concerns about the control room dose. the licensee imposed an

administrative limit on Iodine until a Technical Specification (TS)

amendment submitted was approved. The licensee made a procedure change

to Administrative Procedure OAI-81. Water Chemistry Guidelines, setting

the limit at 0.1 microcurie per gram dose equivalent Iodine 131 comparod

to the TS value of 0.2 microcurie per gram. Also, the licensee has bmi

providing weekly water chemistry data to NRR and the Resident Inspector

for review. None of the data reviewed has exceeded the administrative l

limit. ]

Due to a reconstitution of the Environmental Qualification (E0) program

and items identified, there are 9 of 24 Justification for Continued

0)eration (JCO) that remain open for both units. The following provides

t1e status of the EQ JC0s and associated Engineering Service Requests ,

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(ESRs)-

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Closed i

1) ESR 97-00087. E0-Type JC0 for Improperly Configured Conduit Seal.

2) ESR 97-00574. Greyboot' Connectors. l

3) ESR 97-00329 (old ESR 96-00625). EQ Type JC0 for E0 Fuses Without

a Qualification Data Package (0DP).

4) ESR 97-00289. Post Accident Sampling System (PASS) Valve Limit l

Switch Panel Wiring.

5) ESR 97-00238. JC0 for Standby Gas Treatment Motor Operated Valve

(MOV) Position Indicator Rheostat.

6) ESR 97-00534. GE EB-5 Type Terminal Strips.

7) ESR 97-00513. In-Board Drywell Electrical Penetrations.

8) ESR 97-00535. Target Rock Solenoids Terminal Block Spray.

9) ESR 97-00449. Degraded Junction Boxes.

10) ESR 97-00250. Conduit Union in E0 Boundary.

11) ESR 96-00425. Evaluation of E0 sealants.

12) ESR 97-00523. High Pressure Coolant Injection (HPCI) Auxiliary Oil ,

Pump Motor Unit 1. '

13) ESR 97-00446. GE Radiation Detectors.

14) ESR 96-00587 PASS Valves. ,

15) ESR 97-00229. JC0 for GE Type 151 B Terminal Blocks.

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DEG 4

16) ESR 96-00503. Associated Circuit E0. closure date To Be Determined. l

(TBD).

.17) ESR 97-00330 (old ESR 96-00501). Motor Control Center (MCC) E0 was

closed by the licensee, but was reopened - closure date TBD.

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18) ESR 96-00426. . Evaluation Quality class and E0 classification of'

PASS valves was scheduled for completion June 6.1997, but closure

date is TBD.

19) ESR 97-00529. Failure of Unit 1 Drywell Motor. closure date TBD.

20) ESR 96-00627. ODP.for Marathon 300 Terminal Blocks was scheduled

for completion December 31. 1997 but revised to August 1. 1997,

but closure date is now TBD.

21) ESR 97-00206. Main Steam Isolation Valve (MSIV) Hiller Actuator 1

JCO. was scheduled for completion September 2.1997, but closure

date.is now TBD.

22) ESR 97-00343. Qualification of Kulka Model 500 Terminal Blocks was

scheduled for completion September 1. 1997, but closure date is

now TBD.

23) ESR 97-00435. MCC Fittinas, closure date TBC

'24 ) ESR 97-00602. Solenoid Vilve Field Wiring closure date TBD.

In summary Unit 1 and 2 operated continuously despite a trip of the

Unit 2 ~B" recirculation pump. However, there were 9 outstanding JC0s

in the E0 area for both units.

I. Operations

01 Conduct of Operations

01.1 Unit 2 ~B" Recirculation Pumo Trio

a. Insoection Scooe (71707)

The inspector reviewed the circumstances surrounding the January 27,

1998, trip of the 2B recirculation pump.

b. Observations and Findinas

-On January 27, 1998, both units were operating at 100 percent power. At

10:22 a.m. the 2B recirculation Jump tripped. The resultant decrease in

core flow caused entrance into t1e 5 percent thermal hydraulic

instability (THI) buffer region. The o)erators, in accordance with

Engineering Procedure OENP-24. Reactor Engineering Guidelines, inserted

rods to exit the 5 percent buffer region. Upon loss of the

recirculation pump. Unit 2 entered Abnormal Operating Procedure 2A0P-4.

Low Core Flow and Technical ' Specification (TS) Action 3.4.1.1.

Recirculation System, which required the power level reduced or core

flow increased until the limits established in TS Figure 3.4.1.1-1 were

met. The plant was stabilized at approximately 55 percent . cower with no

-indications of THI observed. The trip of the 2B recirculat. , pump was

attributed to an undervoltage trip as a result of an electrical fault on

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l a transmission line due to a damaged insulator which caused the loss of

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the Whiteville offsite feeder. The inspector verified that two

physically independent circuits were available throughout the transient.

This event was recorded in Conditior Reports (CR)98-181. 2B

Recirculation Pump Trip.98-185. Loss of 2B Recirculation Pump, and

98-184. Insulator Damage - Whiteville Line.

The licensee further reduced power to approximately 33 percent to

establish proper temperature and flow conditions for restart of the

tripped recirculation pump. At 1:50 p.m. the licensee attempteo to

restart the 2B recirculation pump: however, the 4160 volt drive motor

breaker had tripped when the internal drive motor temperature switch

stuck in the tripped position. The switch was removed and a new switch

installed. This event was recorded in CR 98-186. Failure of the 28 to

Start. The licensee successfully restarted the recirculation pump, thus

returning to two-loop operation at 9:05 p.m. The inspector observed

good operator response to the transient, procedure usage by the

operators and oversight by Operations supervision. The inspector

verified that the actions prescribed in 2A0P-4 were properly conducted

and TS properly applied.

The licensee questioned why the 2B recirculation pump received an

undervoltage trip and the 2A did not. Licensee review has not

definitively established the root cause for one pump tripping and not

the other. The inspector noted that this trip was similar to a

recirculation Jump trip on June 25. 1996, which resulted from a l

lightning stri ce as documented in NRC Inspection Report (IR) 50- j

325(324)/96-10. Licensee investigation into the cause of the  !

recirculation pum) trip for the 2B pump and not the 2A pump, and the i

cause of the stucc temperature switch were underway.

c. Conclusion

A recirculation pump trip occurred as a result of an electrical fault on

a transmission line. The transmission line was promptly restored and

the recirculation pump was satisfactorily returned to service. Operator

response to the resultant transient was good.

02 Operational Status of Facilities and Equipment  !

02.1 Weekly Test of Emeraency Alcrms

a. Insoection Scone (71707)

On January 9.1998, the inspector reviewed the weekly test of the plant

emergency alarms.

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b .- Observation and Findinas

l< During.a routine tour of the Unit 2 Reactor _ Building, the inspector

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noticed that.no other person was in the area while the site alarms were

being tested. The site evacuation alarm, fire alarm. and building

l evacuation alarm are tested every Friday at 9:00 a.m. Each building

evacuation alarm is tested, such as Unit 2 Reactor Building Radwaste

. Building, etc.

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-The inspector questioned the control room operators that perform the

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test whether anyone was placed in the various buildings during the test.

No one was placed in the buildings during the test and it was not-

required by plant procedure. The alarms were tested by procedure 001-

01.04, Communications. The inspector reviewed this procedure. but it

only provided the public address system announcement used during

testing. The licensee stated that this test was done weekly to

familiarize personnel with the alarms.

The licensee stated that full volume testing was being performed by

procedure OPT-4.8.2.3. Public Address System Volume Level Bypass. The

inspector reviewed this procedure. This test requires placement of a

Jerson in the area being tested. The acceatance criteria was that the

Juilding/ area alarm was audible and that t1e warning lights were

visible.  !

c. Conclusions

The inspector concluded that the site alarms were being tested in

accordance with procedure requirements.

02.2 Soecial UFSAR Review

A recent discovery of a licensee operating the facility in a manner

contrary to the' Updated Final Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

practices, procedures, and/or parameters to the UFSAR descri)tions. l

dhile performing the inspections discussed in this report. tie-

inspectors reviewed the applicable portions of the UFSAR that related to

the areas inspected. The inspectors verified that the UFSAR wording was

consistent with the observed plant' practices, procedures, and/or

parameters.

The inspector reviewed the UFSAR Section 13.3, Emergency Planning, to

- review any alarm testing requirements. This section of the UFSAR

contains only a short paragraph that plans for coping with emergencies

are contained in the Radiological Emergency Res.?onse Plan. No

requirements are contained for alarm testing.

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II. Maintenance

M1 Conduct of Maintenance I

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M1.1 General Comments

a. Insoection Scooe (62707)

The inspector observed a portion of the following work activities:

. Diesel Generator (DG) 3 Scheduled Maintenance outage

. DG Building Ventilation Filter Upgrade

. Control Room Cable Sealing

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b. Observations and Findinos

The inspector observed maintenance activities in the DG building on 1

January 12. 1998. Cylinder liner replacements were being conducted for j

four cylinders on DG 3. The inspector checked various clearance tags

for the work under clearance CL 2-97-00975. The work around the diesel

was controlled as a Foreign Material Exclusion (FME) area. i

The inspector observed the material upgrade of the building ventilation

filters. The old filters had been removed and support housing freshly

painted. One end of the building was completed with new filters

installed. This corrected the degraded material condition discussed in j

NRC IR 97-08. Section M1.1.

The licensee was conducting additional sealing of cable penetrations in

the floor of the control room cabinets. The cabinets were initially

sealed with a putty- type substance, but testing using a gas tracer

revealed leakage. The new sealing material was being' poured into the

cabinet floor area to provide a better seal. Another test was planned

once all cabinets were sealed.

c. Conclusions

The inspector concluded, from observation of routine maintenance

activities, that the licensee was continuing to upgrade the material

condition of plant equipment and equipment spaces.

M1.2 Observation of On Line Maintenance Activities

a. Insoection Scooe (62700)

The inspector examined the following on-line maintenance activities to

verify that mainteaance activities were being conducted in a manner that

resulted in reliable and safe operation of the plant.

  • WR/JO 97-AIXP1 Unit 2 Repair Rad-Waste Floor Drain Sample Pump (2-

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G16-C021A) Mechanical Seal (seal was leaking).

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. WR/JO 98-AABU1 Unit 2. 2B Motor Generator (MG) Set Outboard Motor

Bearing was Making an Abnormal Noise Indicative of a Problem.

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b. Observations and findinas

The aboie work was performed with the work package present and in active

use. Technicians were skillful, experienced, and knowledgeable of- their

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assigned tasks. The mechanical seal was successfully replaced on the

radwaste pump. Excessive vibration readings from the Unit 28 MG set

l resulted in the outboard motor bearing and the outboard generator

bearing being classified in the alert status. The licensee planned to

monitor the 2B MG set weekly until the bearings are changed out.

Tentative schedule will be to replace the bearings during the week of

February 16, 1998.

c. Conclusions

Maintenance activities observed were ccnducted in a thorough and )

effective manner.

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M2 Maintenance and Material Condition of Facilities and Equipment j

M2.1 Observation of Maintenance Surveillance Test (MST)

a. Insoection Scone (62700)

The inspectors observed the following surveillance calibration tests on

Unit 2:

. 2MST-RHR250, Residual Heat Removal (RHR) Pump Pressure Automatic

Depressurization' System. (ADS) Permissive Instrument Channel

Calibration.

Channel Calibration.

b. Observations and Findinas

Maintenance Eurveillance Test 2MST-RHR250 verified that all eight-

pressure switches were in calibration. The inspector also verified that

test equipment was properly calibrated. test procedures were followed

and testing was adequately performed. )

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-On January 7. 1998, the inspector observed a technician filling a test

hose to remove entrapped air in order to perform liaintenance  ;

Surveillance Test 2MST-RHR27Q on the RHR Shutdown Cooling Reactor  !

Pressure Instrument B32-PS-N018A-1. when an unexpected fluid slurry of  !

resin came out of the hose and onto the floor. Further investigation by  !

a health physics technician revealed that the resin we> contaminated. 2

The comparator pump and hose had been stored in a Unit 2 gang box marked

for contaminated storage. However, neither_the comparator pump nor the I

high pressure hose had been packaged to prevent the spread of  !

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contamination after 'ts previous use. The comparator pump and hose were

i subsequently packageJ and transported to a decontaminated area and {

replaced with other equipment from an equipment storage area within the 1

l reactor building. The inspector questioned the technician concerning

i the contaminated test equ pment and discovered that neither the ,

comparator pump nor the h gh pressure hose had serial numbers on them in

order to trace their previous use to determine if contaminated foreign

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material had entered other systems. In addition, the practice of

! storing internally contaminated test equipment in gang boxes was 4

L discussed. The technician subsequently notified his supervisor and CR

98-00029. Contaminated Test Equipment was issued to address the lack of j

! traceability of the test equipment, possible violation of foreign  !

material exclusion requirements. and storage of internally contaminated

l equipment. Since previous we of the test equipment had not been i

! determined at the conclusion of the ins)ection, the inspector identified ,

l this item as Inspection Followup Item 1:1 50-325(324)/97-15-01. Test

l Fixture Discrepancies. Subsequent to the inspection, on January 12,

1998, the licensee not,fied the inspector that (1) all contaminated i

equ pment had been. removed from gang boxes and stored in a contaminated

l too room inside the plant. (2) an inspection had been conducted of the

, internals of dead weight testers and hoses, and the problem of cross J

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contamination was determined to be confined to hoses. (3) the previous

use of the hose which would have allowed the RHR system to be cross

centaminated was found to have occurred on January 2,1998, during work

activities implemented by Work Request / Job Order (WR/J0) 96-AG0K1 which

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directed maintenance technicians to unclog a rad-waste sample line, and

l that the hose had not been used since, and (4) programmatic controls

were planned to be instituted to identify and control test equipment.

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l c. Conclusion

Technicians observed performing maintenance surveillance tests were

skillful, experienced, and knowledgeable of their assigned tasks.

However, discrepancies were identified by technicians which indicated

weaknesses in foreign material exclusion controls test fixture

traceability controls and the handling and stora;p of internally j

contaminated test equipment.

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M2.2 Unit 2 Shroud Weld H6B Ultrasonic Data Review

a. Insoection Scooe (737531

On January 9.1998, representatives from the licensee, the Electrical

Power Research Institute (EPRI), and the inspector reviewed automated '

ultrasonic data taken of reactor core shroud Weld No. H6B. during the

Brunswick Unit 2. 12th and 13th refueling outages. This review was

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conducted at the EPRI Nondestructive Examination (NDE) Center in

Charlotte. North Carolina. The review was necessary to confirm the

licensee's analyses of the differences in data, and the actions taken by

the licensee when the crack depths reported by an ultrasonic vendor were

consistently less in 1997 than those reported by the same vendor in

1996.

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b. ' Observations and Findinas

The licensee notified the inspector on October 9,1997. that there were

differences between the 1996 and the 1997 data and that crack depths on

core. shroud Weld No. H6B were consistently less in 1997. The licensee

stated that the raw data for 1996 and 1997 had been sent to'the EPRI NDE

center for their review. The licensee recuested that the EPRI NDE

center review the analysis process. procecures, tooling hysteresis,

tooling start positions, scan patterns, etc., to hel) the licensee

understand the effects these items may have had on tie differences in

the 1996 and 1997 crack depths. The licensee provided the inspector

with spreadsheets of the initial results of both inspections.

Arrangements were made at that time to review the results of the

CP&L/EPRI evaluations at the EPRI Center in order to verify the

subsequent conclusions using the raw ultrasonic data from both outages.

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The licensee issued CR 97-03902. Unit 2 Core Shroud Weld H6B. and with

assistance from EPRI conducted an extensive review of the problem.

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L On January 6 and 7.1998, the inspector reviewed documentation including

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the licensee's and EPRI's shroud examination findings delineated in CR

L 97-03902 in preparation for the inspection to be conducted at the EPRI

L NDE Center on January 9. Initial discrepancies reported by the licensee

l- in the CR consisted of the following: (1) the 1996 flaw depths were

reported as being taken in one inch increments when the ultrasonic data

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disks indicated the data was taken in 0.775 inch increments. (2) the

1997 data was not interpreted in areas where the data overlapped with

other ultrasonic scans resulting in some data being missed. (3) the

azimuthal locations of the data shifted causing flaws to be reported in

l areas that were reported as unflawed areas in 1996. (4) the tooling

i location error may be outside that used for analysis of the ultrasonic

results, and (5) the depths of the flaws in 1997 were significantly less

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than those determined in 1996 without any substantiated reason.

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l In the CR root cause analyses. the licensee captured the above reported

l problems in three central issues:

(1) The depths and lengths of the flaws were reported inaccurate:

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  • The cause of the depth difference was attributed to the j

difference in rasper scan size between the 1996 and 1997

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examinations: the one inch ras)er scans were too large to  ;

produce comparable crack growt1 results each outage: .and  ;

impurities in the weld sometimes were included in the 1996 .

interpretation of crack depth.  !

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. The cause of the lateral displacements was attributed to

failure of the analyst to sufficiently review overlap data.

Therefore, when start point errors in scanning were made

they were not compensated for in the analysis.

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(2) The data collection and analysis process discrepancies with

respect to tool location, data collection location validation, and

analyses of the results:

. Review of the inspection data revealed three known instances

where the 1997 data collected was not at the stated

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location.

. Additionally, the positioning tool was not precisely placed

against the lug.

  • One instance was found where the licensee believes the

offset specified in the examination plan was not used for

the scan.

  • Review of the 1996 data revealed that scans did not begin at

the location stated in the report, but were separated by

several degrees.

. Examples of discrepancies made by the analyst were that not

all of the data collected was evaluated. This was due to

the analyst's failure-to perform comparison of overlap data

for matching flaw profiles. In addition, independent review i

of the final report for accuracy and completeness was not I

satisfactorily performed.

Review of the inspection procedures by the licensee determined that

these procedures lacked controls to prevent the above instances from

occurring. Examples of inadequate controls for data collection

included: verification of correct scan location, verification that tool

start positions are correct, verification that the correct location and )

identifiers-are entered into the data collection computer, and

verification that any offsets used were applied.

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-(3) The vendors quality assurance process was ineffective in detecting

these errors.

  • The vendor cuality assurance process lacked steps to detect

the items icentified in this event report.

The CR also noted under immediate corrective action that EPRI had

concluded, based on re-evaluation of the ultrasonic data, that the flaw

depth analysis for both years was accurate.

On January 9. 1998, representatives from CP&L and EPRI. and the

i inspector selected 17 crack depth reflectors reported in the 1996

examinations for re-inspection. These cracks represented crack defect

differences between inspections of at least twice the ultrasonic root

mean square error band established by the vendor when demonstrating

their procedure techniques at EPRI on Boiling Water Reactor Vessel

Internal Program Mockup Blcck 16.

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The examination of the 1996 data revealed the following: (1) of the 17

crack reflectors.10 were single indications ana the analyst made the

o correct call. (2) of the remaining seven crack reflectors five appeared

l to be two separate indications one crack and the other possibly

involving a metallurgical condition in or near the weld which the  ;

analyst had conservatively included in the crack length. (3) the two J

remaining crack indications appeared as two' separate indications but

both EPRI and the inspector interpreted the total presentation as one

l crack. The review of the 1997 data revealed that although this data was

documented as being two decibels more sensitive than the 1996 data, the

test sensitivity and noise level was actually much higher.in the 1996

l data. This resulted in single reflector type A-scan data presentations

on the screen in 1997, where in 1996, due to the higher sensitivity, the

analyst had to deal with signals and facets of signals that were not

present in the 1997 data. The inspector concluded from this review

that both the 1996 analyst and the 1997 analyst had made the correct

crack depth calls based on the data they were presented. Differences

noted in the evaluation of defect signals between 1996 and 1997 were not

significant and did not account for the significant depth differences i

encountered in the 17 reflector chosen for review. Therefore the

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differences encountered in crack depth could only be attributed to the

difference in the rasper scans (0.775 inch in 1996 verses one inch in

1997) between inspections and the fact that the one inch rasper scan was

too large to verify crack growth differences between refuelings. This

was demonstrated by the overall negative difference value obtained of

(-) 0.071 inch for the 1997 ultrasonic data of Weld No. H6B from the

data taken in 1996, which is anomalous; defect growth should htue been

encountered with time.

10 CFR 50. Appendix B. Criteria IX. Control of Special Processes,

requires that measures shall be established to assure that special

processes, including nondestructive testing are controlled. CR 97-

03902, delineated inspection procedure weaknesses and numerous vendor

examination discrepancies, as described above, which resulted in

documentation of ultrasonic data that was incorrect and was not

comparable to previous data to determine defect growth. This

nonrepetitive. licensee-identified and corrected violation is identified

as a Non-Cited Violation, consistent with Section VII.B.1 of the NRC

Enforcement Policy and i.s designated NCV 50-324/97-15-02. Inadequate

Control of Special Processes,

c. Conclusions

Numerous examples of inadequate control of special processes were

identified by the licensee of vendor examination activities for the

Unit 2, H6B reactor core shroud weld. These discrepancies required the

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licensee to expend extensive time and effort to identify the cause and

( im)lement necessary corrective actions in order that ultrasonic data

tacen of the reactor core shroud H6B weld during the Unit 2.12th and

13th refueling outages could be compared.

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M3 -Maintenance Procedures and Documentation

M3.1 Emeraency Core Coolina System (ECCS) Response Time Testina

L a. Insoection Scoce (61726)

On January 9. 1998, the inspector reviewed the test data for a new

surveillance test performed on Unit 2.

I b. Observations and Findinas

The inspector reviewed Periodic Test OPf-08.2.7, Low-Pressure Coolant

Injection / Residual Heat Removal (LPCI/RHR) Pump Response Time Test. The

L test was performed to determine the operability of the LPCI/RHR pumps in

conformance with the requirements specified in TS 4.5.3.2.d. This

section of TS states that each LPCI subsystem shall be demonstrated

operable at least Once per 18 months by verifying the ECCS Response Time

for each LPCI subsystem is within its limit. The definition for ECCS

Response Time is in TS Section 1-0. Definitions.

The definition is as follows:

"The ECCS Response T'me shall be that time interval from

,~ when the monitored parameter exceeds its ECCS actuation

setpoint at the channel sensor until the ECCS equiament is

capable of Jerfcrming its safety function (i.e., t1e valves

travel to t1eir required positions, pump discharge pressures

l'

reach their required values. etc.). Times shall include

diesel generator starting and sequence loading delays where

applicable."

The inspector reviewed the procedure and test data. ~he test data

,

indicated that the response time of each of the two RHR pumps in Loop A

l and Loop B was about 2 seconds. The acceptance criteria stated that

when each pump was started the RHR heat exchanger inlet pressure should

be greater than or equal to 215 pounds per square inch gauge (psig) in

less than.or equal to 4.0 seconds.

l Thus, each pump tested met the acceptance criteria. However, the

inspector questioned the definition that times shall include diese'

generator-(DG) ' starting and sequence loading delays where aiolicole.

l The new test was written to greatly simplify the old test tiat was

L performed with the unit off-line.

i

The inspector reviewed ESR 97-00508, ECCS Response Time Testing Methods,

p which 3rovided the basis for the testing change.. This ESR indicates

that L)CI response time was 53 seconds. A discussion of this time is

broken into several intervals. -The first time interval of 15 seconds

allows for DG start and energizing of the emergency bus. The next time

interval is 12.5 seconds for LPCI load sequence delay. This is followed

by 4 seconds for the pump response time.

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However, this new test only checks the pump response time of 4 seconds

and not the other times specified in the sequence above. The complete

l testing of all times could not be verified using this test. The

'

licensee stated that other times are tested using a different procedure

but at different times in the 18 month time requirement. This test

methodology and generic implications requires further review. This will

be identified as Inspection Followup Item IFI 325(324)/97-15-03. ECCS

Response Time Testing.

c. Conclusions

The ECCS Response Time Testing was being conducted as a group of tests

at different times. This methodology requires further review.

M4 Maintenance Staff Knowledge and Performance

M4.1 Process Comouter Failures

a. Insoection Scooe (62707. 37551)

The inspector reviewed recent failures of the )lant process computer and

the corrective actions taken in accordance wit 1 the maintenance rule and

the corrective action program.

b. Observ6tions and Findinos

On December 22. 1997, during routine review, the inspector noted that at

3:49 a.m. on December 20. 1997. the /lant Process Computer (PPC) ceased

producing the heat 'oalance for Unit 2. This malfunction was aromptly

corrected by 5:50 a.m. on December 20. On January 5. 1998, t1e

inspector noted that the PPC had gone down again at 8:48 p.m. on

January 4. 1998, and was restored at 7:42 a.m. on January 5. 1998.

During the January 4.1998. failure, the control room operators were

instructed not to increase recirculation flow or perform any evolutions

that could potentially increase core thermal power and engineering '

.

support was required to perform core thermal power calculations using

Periodic Test OPT-1.80. Core Tht mal Power Calculation. These actions

were consistent with a previous failure on November 18. 1997, as

recorded in CR 97-4004 Queue Manager Failure-U2 PPC. A Standing

Instruction (SI) 97-76 was initiated-for the November 18, 1997, to l

inform operations personnel to limit reactor power to less than 99.5

percent if the PPC fails. The SI also established frequencies for the

Nuclear Engineers to monitor thermal power indication and other

procedures to satisfy TS 4.2.1.a-c. 4.2.2.la-c. and Table 4.3.1-1

Note (e) surveillance requirements. The inspector verified that the

licensee took appropriate actions and no limits were exceeded.

The inspector questioned the licensee, after the December 20 and

January 4 failures, concerning the absence of CRs for the failures. The

licensee indicated that since the PPC performance criteria had not been

,

exceeded, no CR was required. After further licensee review. CR 98-012. l

j Unit 2 PPC Data Acquisition System failures was issued on January 6. 1

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1998. The CR recorded the increasing trend in PPC failures during

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December 1997 and January 1998 for Unit 2. Plant Program Procedure

OPLP-04. Corrective Action Management, requires the initiatioc of a CR

for repetitive equipment failures. The inspector identified that no CRs

were generated until questioned by the NRC about the failures on

December 3 and 30, 1997 for Unit 1 and December 3. 10 and 20. 1997 and

January 4. 1998 for Unit 2. The failure to initiate CRs for repetitive

failures of the PPC is a violation. This violation is identified as VIO

50-325(324)/97-15-04, No CRs for Plant Process Computer Failures.

The inspector reviewed the Maintenance Rule PPC Scoping and Performance

Criteria. The performance criteria for the system was based upon an

expectation of 99 percent availability over a three year period minus

time for two scheduled refueling outages. This translated into an

unavailability goal of 274 hours0.00317 days <br />0.0761 hours <br />4.530423e-4 weeks <br />1.04257e-4 months <br /> per 36 months. The licensee scoping

report-indicated that this time was sufficient to permit development of

a trend toward unsatisfactory system performance. The inspector

questioned whether the established performance criteria was adecuate in

assessing degrading performance of the PPC. since the 36 month curation

of the allowable unavailability time masked observed degradation over

short periods of time. The inspector was also concerned that due to not

initiating a CR the long duration of the allowable unavailability time

would not prompt the performance of a cause determination for the

functional failures in accordance with the guidance 3rovided in Section

9.4.4 of Nuclear Management and Resources Council (NJMARC' 43-01.

Industry Guideline for Monitoring the Effectiveness of KJntenance at

Nuclear Power Plants. Review of the sco)ing report, indicated no

recorded unavailability for Unit 2 from rebruary 1995 through October

1997. However, from November 1997 to January 1998, the report stated

that the PPC had been unable to provide its intended function in excess

of 45 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br />. The inspector determined that this sudden increase in

unavailability was evidence of system degradation. After further

licensee review, the PPC performance criteria was modified to require no

less than 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> per quarter of unavailability for the PPC. Under the

new criteria, the Unit 2 PPC exceeded the established performance

requirements.

t Conclusion

Multiple failures of the Plant Process Computer occurred during the

months of December 1997 and January 1998. A violation was issued for-

failing to initiate Condition Reports for repetitive failures of the

PPC,

M8 Hiscellaneous Maintenance Issues (92902)

M8.1 (Closed) Violation VIO 50-324/96-18-02: Testing Using Uncalibrated

Gauges

While observing the performance of Periodic Test OPT-8.2.2c LPCI/RHR

,

Sys'w Operability Test - Loop A for Unit 2. the inspector identified

! that the test was being performed using uncalibrated pressure gauges on

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the RHR pumps A and C discharge side. The licensee was using temporary

gauges due to an existing drift problem affecting the calibration of the

permanently installed gauges (2-E11-R003A(C)). The. failure to

, incorporate test requirements into the testing procedure and to properly

l identi.fy the out-of-calibration gauges in the Automated Maintenance

l -Management System (AMMS) resulted in the use of those gauges during the

! operability test.

Violation VIO 50-324/96-18-02 was issued to address this failure. The

licensee reperformed OPT-8.2.2c with properly calibrated gauges.

Subsequently, the 2C RHR ) ump was.placed in the alert range which

, required an increase in t le testing frequency. The licensee revised-

!

Plant Program Procedure OPLP-24. Work Management Process, to require

identification of each deficient item either by a separate WR/JO or by

listing each component in the secondary equipment field on a single

WR/JO to ensure all nonconforming gauges are appro)riately captured.

Training was provided to the Operations staff on tie correct fields to

access to determine deficient components, based on a finding by the

licensee that many staff personnel were not aware of a secondary

function in AMMS needed to be accessed to perform an adequate search for

outstanding components. During this event, the requirement to use

temporary gauges for this periodic test were improperly located in a

Standing Instruction. The licensee performed a review to determine

,

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whether.other procedural requirements were being controlled outside of I

an approved procedure. Several deficiencies were discovered and I

promptly corrected.

The licensee responded to the Violation issued in IR 50-325(324)/96-18

in a letter dated March 17, 1997. The inspector reviewed the root cause

analysis, revised procedures, and assigned corrective actions. The

corrective actions instituted were adequate to prevent recurrence.

Based on adequate completion of the corrective actions. this item is

closed.

M8.2 LClosed) Insoection Followuo Item IFT 50-325(324)/97-02-03: PM

Frequencies Based on Appropriate Plant Fuel Cycle

Review of the Transmission Substation Maintenance Procedures Manual

revealed that the frequency for performing preventive maintenance (PM)

procedures on components which require the unit to be in an outage in

order to perform the PM had not been updated to reflect the new 24-month 1

-fuel cycle for. Unit 1. The licensee had issued CR 97-01670. IFI 97-02.  !

( PM Frequencies, on this issue. However, the offsite System Reliability

L 'and Power Quality (SRPQ) group which is responsible for revising these

procedures, had not done so to date. The primary reason SRP0 had not

revised the proceAres was due to Unit 1 not actually being in the 24-

month fueling cyca until the year 2000 and Unit 2 until 2001. However. !

the licensee had requested that SRPQ revise the appropriate procedures  ;

by June 1. 1998. The inspector held discussions with the licensee's l

cognizant engineer, reviewed the schedule for Units 1 and 2 refueling l

cycles and determined that the licensee had control of this corrective

action and no additional inspection was necessary. This item is closed.

15

III. Enaineerina

-E2. Engineering Support of Facilities and Equipment

E2.1 Drywell Pressure Setooint Chanae

a. Insoection Scoce (37551)

The inspector reviewed the reason why the Unit 1 Reactor Protection

System (RPS) Hign Drywell Pressure Trip Setpoint was being changed on an

operating unit.

'b. Observations and Findinas

On January 8,1998, the inspector learned, by attending the morning

meeting. that a setpoint change was being made for Unit 1 RPS High

Drywell Pressure. This parameter is monitored because it provides

indication of a Loss of Coolant Accident. The setpoint was being

changed from 1.8 to 1.7 psig; the TS limit is 2.0 psig. The basis for

the change was due to Improved Standard Technical S

However. ITSs have not been approved for Brunswick.pecification (ITS).

-

The setpoints were being changed per ESR 97-0025. Implement Unit 1

Instrument Setpoint Changes. The ins)ector. reviewed the ESR that i

discussed implementation of some of tie ITS instrument setpoint changes.

The purpose of the ESR was to implement the instrument setpoint and TS

Allowable Value-(AV) changes-that result from ITS and'24 month refueling

project.

From the ESR there were 18 setpoint changes that were called "More

Restrictive Changes", which were determined to be more conservative than

the existing setpoint. The licensee determined that these could be

implemented prior to NRC approval. There were 11 setpoint changes that

were called "Less Restrictive Changes" which could only be made after

NRC ap3roval of ITS. The drywell pressure setpoint change was a change

that t1e licensee called "More Restrictive".

The inspector noted that on the cover sheet for the approval of the ESR

was a block checked._ "NRC Before Implement:ition." However, the ESR

itself allowed partial implementation. The inspector noted a statement

on page 3 that ITS had been-reviewed by Nuclear Assessment Section (NAS)

and Plant Nuclear Safety Committee (PNSC) and will be reviewed by the

NRC prior to implementation.

-The inspector questioned the licensee concerning implementation of these

changes prior to NRC approval and the lack of PNSC review prior to

implementation. A conference call with NRR was held on January 13.

L 1998, to discuss these issues. It was discussed that ITS had not been

approved yet, but maing more conservative changes prior to NRC ap3roval

had been an approach taken by other licensees. The review of whic1

items were conservative and non-conservative was discussed by the NRC as

something PNSC should review.

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The licensee was responsive to these issues and revised the ESR to

clarify the implementation process. The setpoint changes were discussed

l in a PNSC meeting February 3. 1998.

c. Conclusions

l

Instrument setpoint changes, deemed more conservative than existing TS

requirement, were being made in preparation for converting to Improved

Standard Technical Specifications. The inspector concluded that the

implementing instructions and changes needed additional clarification

and license review.

E3 Engineering Procedures and Documentation

E3.1 Testina of Safety-Related Loaic Circuits

a. Insoection Scoce (37551)

As a result of continuing industry problems to correct previously {

identified problems in logic circuit testing, the NRC issued Generic

Letter (GL) 96-01. Testing of Safety-Related Logic Circuits, in GL 96-

01, the NRC requested that the licensee review the plant surveillance

test procedures to verify adequate testing of all logic circuit

components. If testinc discrepancies were identified, the licensee was

instructed to modify the surveillance procedures to comply with the iS.

The inspector performed a review of selected TS required functioris for

the Reactor Core Isolation Cooling (RCIC) system.

b. Observations and Findinas

The inspector revi >wed the adequacy of the surveillance logic testing

for the RCIC suction automatic transfer on low-level in the condensate

storage tank (CST). Harmally, upon reaching the low-level setpoint, the .

CST suction valve receives a close signal unless one of the two I

suppression pool suction valves are not open. When in standay, the

opening of both suppression pool suction valves causes the automatic )

closure of the CST suction valve.

The ins)ector reviewed the adequacy of the surveillance logic testing

for tur)ine exhaust diaphragm's high pressure isolation function. This

function isolates RCIC u)on sensing a high pressure condition between

the turbine exhaust diapiragms.

The inspector reviewed Maintenance Surveillance Test (1)2MST-RCIC41R.

RCIC Auto-Actuation and Isolation Logic System Functional Test.

Maintenance Surveillance Test 2MST-RCIC230. RCIC Turbine Exhaust

Diaphragm High Pressure Instrument Channel Calibration, and the

associated elementary and control wiring diagrams. Based on inspector

review, the inspector determined that surveillance testing of relay

contacts. interlocks, and bypass was sufficient to provide adequate

logic testing for those functions reviewed.

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c. Conclusions

Inspector's review determined that surveillance procedures testing of

the logic for the RCIC CST low water level automatic transfer and the

! generation of the isolation signal on high turbine exhaust diaphragm

pressure were being conducted in accordance with TS.

E8 Miscellaneous Engineering Issues (92903)

E8.1 (Closed) Violation VIO 50-325/96-16-01: Improper Work Planning Resulted

in a Loss of Shutdown Cooling

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( (Closed) Licensee Event Reoort LER 50-325/96-14: Loss of Shutdown

l Cooling During Instrument Rack Repair

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On October 11. 1996, with Unit 1 in Mode 5 for refueling. a grour 8

isolation was received. The isolation signal closed the 1-E11-F008-

Shutdown Cooling (SDC) suction valve resulting in the loss of the

primary loop used for decay heat removal. Prompt identif.ication and

l restoration of the system by the control room operator resulted in

! minimalization of the coolant heatup to less than 1 degree Fahrenheit

l ( F). The licensee subsequently reported this event in LER 50-325/

l_ 96-14.

l The inspector reviewed the violation response. LER 50-325/96-14.

. associated CRs and root cause analysis 96-3166. The inspector verified

! that the corrective actions.were completed. Hov?ver, the inspector

l noted that an issue identified in the root cause was not addressed by

any of the corrective actions. .During this event it was determined that

multiple root cause barriers were broken. The ESR failed to adequately

address the scope of the modification: scheduling personnel by)assed the

administrative controls in place to make a schedule change witlout

understanding the impact the change would have on the unit
and the work

l instructions were not adhered to by the maintenance workers. However,

the' corrective actions addressed the specific inadequacy of the system

!

impact evaluation contained in the ESR. proper adherence to work ticket

instructions, and counseling for those involved. The corrective actions

l~ were not assigned to the root cause which identified that scheduling

[ personnel bypassed the administrative controls.

Several' modifications were made to the process of making an outage scope I

change after the outage risk assessment had been performed. These  !

changes were incorporated into Administrative Procedure 0AP-22. BNP

Outage Risk Management. The inspector discussed the adequacy of the

procedure changes and other modifications made to the outage scheduling

process with the licensee. The inspector observed that the addition of

extra supervisory approval before permitting a scope change to the

outage schedule provides extra op)ortunities to catch errors. The  !

inspector identified that the lacc of checks and balances for l

unauthorized schedule changes, before the schedule is issued / worked.

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could allow the same event to reoccur. .This conclusion was based on the

scope change process allowing an individual who initiates a change

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request to be the same individual who makes the change. After further

review by the licensee, the licensee stated that the process changes

provided adequate checks and balances to prevent bypassing the required

administrative approval the corrective actions taken are adequate to

prevent recurrence. Based on completion of those items committed to in

the LER and the violation these items are closed.

E8.2 (Closed) Violation VIO 50-325(324)/96-181-1013: Inadequate Design

l Control for Material Selection in Service Water Pump

l

-(Closed) Licensee Event ReDort LER 50-325(324)/96-03-00. 01. 02: Dual

l Unit Shutdown Due to Service Water Pump Inoperability

1

l This violation was due to the wrong material selection for some bolts in

Service Water pumps. Because of a pump failure and inspecti_on of other

pumps which revealed a common mode failure mechanism, both units were

! shutdown. Each service water pump had the bolts replaced with a new

material. Hastelloy, which was less susceptible to galvanic corrosion.

I

The licensee responded to this violation on August 9.1996. The

i licensee completed a number of corrective actions to address the

l violation. A procedure was developed to provide guidance for material

l selection. Follow-up inspections were conducted on 2A Nuclear Service

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Water Pump in December 1996 and 2B Conventional Service Water Pum) in

January 1997. The results of these inspections were reported in _ER 50-

325(324)/96-03-02. No corrosion of the Hastelloy bolts was found. The

pump inspections completed the corrective action for this violation.

These items are closed.

E8.3 (Closed) Licensee Event Reoort LER 50-325(324)/96-015-00. 01: Technical

Specification Required Suppression Chamber Water Volume Discrepancy

l The licensee identified that the suppression chamber water volumes, as

stated in TS and the Updated Final Safety Analysis Report (UFSAR) were

l incorrect. The licensee took prompt action to control torus water

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level, within the correct band, using site administrative controls until

a change was made to the TS. The licensee evaluated the necessary

-

! corrective actions satisfactorily and implemented a T5 change and a

UFSAR update to incorporate the correct water volumes. The TS

l

amendments, number 186 to license number DPR-71, and number 217 to

I license number DPR-62, were approved on August 28, 1997. This LER is

closed.

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IV. Plant Support

R4 Staff Knowledge and Performance in Radiological Protection and Control

l R4.1 Health Physics Technician Work ~ Practices

a. Insoection Scoce (71750)

The inspector observed radiological controls and procedural compliance

during a tour of the radiologically controlled area with a Health

Physics (HP) technician.

!

i b. Observations and Findinas-

On January 2,1998, the inspector observed a-HP technician perform a

L- . daily Unit 2 Reactor Building walkthrough. The performance of this

. walkthrough was governed by Environmental and Radiological Control

! (E&RC) procedure OE&RC-0100. Routine /Special Dose Rate Survey.

e

[ The inspector observed the technician perform general area radiation ,

I surveys in various locations on each elevation of the Reactor Building.

l fhe technician observed the condition of eculpment on the tours, looking J

L for water and steam leaks. The inspector cetermined that the tour by, I

the technician was adequate. No deficiencies were noted by the .

J

l ' inspector. The inspector questioned the technician as to whether there

were specific locations at which they were expected to perform surveys, j

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check general conditions in rooms and components, or check radiation and j

l high radiation boundaries, etc. The technician exalained that there

were no specific guidelines given to conduct walkt1 roughs. The

inspector verified that no guidance was given in the procedure.

!

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The -inspector questioned licensee management whether minimum walkthrough

l guidance was deemed necessary to ensure that management expectations

l were met during the performance of the procedural requirement. E&RC

i management agreed with the necessity to have minimal guidance for HP

technician walkthroughs. Further discussion with E&RC management

,

confirmed that corrective actions were being addressed to formulate

l guidance.

c. Conclusions

l

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The inspector determined that the tour by the technician was adequate.

The inspector concluded that HP technician daily walkthrough procedures

lacked guidance to ensure continuity of walkthroughs.

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F4 Fire Protection Staff Knowledge and Performance

l

F4.1 Diesel Generator Buildina Doors Imoaired

a. Insoection Scoce (71750. 37551) )

The inspector reviewed the circumstances surrounding a maintenance

activity which was subsequently determined to have degraded the 3-hour

fire rating of 28 fire doors in the DG building. This )roblem was

identified by the licensee in.CR 98-074. Fire Doors Loccset.

b.~ Observations and Findinas )

i

On January 13. 1998. the licensee determined that modifications to the j

latching mechanism on 28 doors in the DG building had defeated their  !

3-hour fire rating. The modification performed, beginning in August

1996 and completed in December of 1997, removed an internal component

which 3revented the crash bar from opening the door in the event of a

fire w1ere the temperature exceeds 600 F. This function prevents the

door from opening if the crash bar is struck with debris. These doors i

are designed to restrict the s) read of flames when exposed to a d

predetermined fire exposure. Jpon recognition of the loss of the 3-hour

fire rating the licensee established a fire arotection impairment until

all the locksets could be replaced with the lardware needed to maintain

the 3-hour rating. The licensee initiated CR 98-074 to address this i

problem. The licensee's root cause review indicated that inadequate

documentation of the basis for the 3-hour fire rating existed. An

additional issue included the failure to perform a review for a

modification to fire. protection equipment.

l

The inspector reviewed UFSAR section 9.5.1.4.3, CR 98-074 and the

associated root cause, CR 96-3928. Configuration of Fire Doors. ESR 98-

00023 Evaluation of Yale Mortise Modifications associated WR/J0s, and

Nuclear Generation Group Standard Procedure EGR-NGGC-005 Engineering

Service Requests. Review of these CRs revealed a history-of incomplete

documentation for the fire doors and hardware problem. The lack of

documentation of the fire door basis was previously identified in

section F2.3 as a URI in IR 50-325(324)/97-13.

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The inspector reviewed WR/J0s'97-ADHR1 and 97-ADHS1 required for

implementation of the corrective action CR 96-3929, No Followup on UL

Report. The WR/J0s referenced ESR_"97-XXXX." The inspector questioned

if the designation of ESR "97-XXXX was an ESR referenced by CR 96-3929.

CR 96-3929 referenced ESR-97-571. Fire Door Problem. The inspector

determined that ESR 97-571 was still in review but the WR/J0s had been

completed. The inspector could not determine if an ESR had been  ;

completed prior to the work performed by the WR/J0s. Due to the

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licensee's review into this problem being incomplete at the close of

inspection report period, this item is unresolved. This unresolved item

is identified as URI 50-325(324)/97-15-05, Inoperable Fire Doors. '

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c'. Conclusion

~

Twenty-eight doors in the DG Buildin were modified defeating the 3-hour

l fire rating of the doors. An unreso ved~ item was issued to allow

additional review for the failure of the licensee to perform an adequate

engineering review prior to modifying required fire protection quality

l hardware.

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V- Manaoement Meetinos

L. XI Exit Meetina Summary

l

l~ The inspector presented the inspection results to members of licensee

management at the conclusion'of the inspection on February 9.1998.

Post inspection briefings were conducted on January 8 and 12,1998. The-

licensee acknowledged the findings presented.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

A. Brittain, Manager Security

M. Christinziano, Manager Environmental and Radiation Control

W. Dorman. Supervisor Licensing and Regulatory Programs

N. Gannon, Manager Maintenance

J.'Gawron. Manager Nuclear Assessment Section

S. Hinnant. Vice President. Brunswick Steam Electric Plant

K. Jury. Manager Regulatory Affairs

J. Langdon., Supervisor NDE Services

B. Lindgren. Manager Site Support Services

J. Lyash Plant General Manager

G. Miller. Manager Brunswick Engineering Support Section

~

R. Mullis, Manager Operations

D. Ouidley. Superintendent, Electrical /I&C i

S. Tabor, Regulatory Affairs j

Other licensee employees or contractors included office, operation,

maintenance, chemistry, radiation, and corporate personnel. j

E. Brown

J. Coley j

E. Guthrie {

C. Patterson

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INSPECTION PROCEDURES USED

l IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62700: Maintenance Implementation

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 73753: Inservice Inspection

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

ITEMS OPENED, CLOSED AND DISCUSSED

'

Ooened

'

50-325(324)/97-15-01 IFI Test Fixture Discrepancies (paragraph M2.1)

i

50-324/97-15-02 NCV Inadequate Control of Special Processes

(paragraph M2.2) {

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50-325(3?4)/97-15-03 IFI ECCS Response Time Testing (paragraph M3.1)

50-325(324)/97-15-04 VIO No CRs for Plant Process Computer Failures

(paragraph M4.1)

i

50-324/97-15-05 URI Inoperable Fire Doors (paragraph F4.1)

Closed

50-324/97-15-02 NCV Inadequate Control of Special Processes

(paragraph M2.2)

50-324/96-18-02 VIO Testing Using Uncalibrated Gauges (paragraph

M8.1)

50-325(324)/97-02-03 IFI PM Frequencies Based on Appropriate Plant Fuel

Cycle (paragraph M8.2)

50-325/96-16-01 VIO Improper Work Planning Resulted in a Loss of

Shutdown Cooling (paragraph E8.1)

50-325/96-14 LER Loss of Shutdown Cooling During Instrument Rack

Repair (paragraph E8.1)

, 50-325(324)/96-181-1013 VIO Inadequate Design Control for Material Selection ,

j in Service Water Pump (paragraph E8.2) I

50-325(324)/96-03-00 LER Dual Unit Shutdown Due to Service Water Pump

f Inoperability (paragraph E8.2)

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50-325(324)/96-03-01 LER Dual Unit Shutdown Due to Service Water Pump

Inoperability (paragraph E8.2)

50-325(324)/96-03-02 LER Dual Unit Shutdown Due to Service Water Pump

Inoperability (paragraph E8.2)

50-325(324)/96-015-00 LER Technical Specification Required Suppression

Chamber Water Volume Discrepancy (paragraph

E8.3)

i

50-325(324)/96-015-01 LER Technical Specification Required Suppression

Chamber Water Volume Discrepancy (paragraph

E8.3)

Discussed

50-325(324)/97-13-05 URI UFSAR Discrepancy Fire Doors (paragraph F4.1)

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