ML20140D178

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Insp Repts 50-324/97-05 & 50-325/97-05 on 970302-0412. Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support
ML20140D178
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 05/12/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20140D165 List:
References
50-324-97-05, 50-324-97-5, 50-325-97-05, 50-325-97-5, NUDOCS 9706100280
Download: ML20140D178 (31)


See also: IR 05000324/1997005

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION II ,

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Docket Nos: 50 325, 50 324

License Nos: DPR 71 DPR 62  ;

' Report No: 50 325/97 05, 50 324/97-05 f

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Licensee: Carolina Power & Light (CP&L)

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Facility: Brunswick Steam Electric Plant, Units 1 & 2  !

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Location: 8470 River Road SE -

Southport NC 28461

Dates: March 2 April 12, 1997

Inspectors: C. Patterson, Senior Resident Inspector

E. Brown, Resident Inspector

W. Rankin, Regional ' Inspector (Section R1)

Approved by: M. Shymlock, Chief, Projects Branch 4 j

Division of Reactor Projects-  !

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Enclosure 2

9706100280 970512 "

PDR ADOCK 05000324

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, EXECUTIVE SUMMARY

Brunswick Steam Electric Plant, Units 1 & 2

NRC Inspection Report 50-325/97-05, 50 324/97-05

This integrated inspection included aspects of licensee operations,

engineering,' maintenance, and plant support. The report covers a 6 week ,

period of resident inspection: in addition, it includes the results of a ~

radiological protection and chemistry controls by a regional inspector.

l Ooerations

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The present method of conducting an operation shift crew post turnover '

meeting was not effective to make the operators fully aware of plant

changes and problems prior to assuming the shift responsibilities. .

(Section 01.1). The licensee was responsive to this concern and

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initiated changes to the shift turnover process for in coming crews that l

had been off site for several days.

The licensee recalibrated the unit 1 feedwater flow instrumentation

resulting in a power decrease due to conflicting test data.

(Section 08.2). The instruments were recalibrated to the more

conservative of ultrasonic flow test data and feed flow tracer data.

Maintenance

A violation was identified for failure to properly perform a

surveillance test for the core spray sparger leak detector system.

(Section M3.1). The normal range was defined in the procedure.

However, the normal range had actually changed in the plant.

An inspection followup item was opened to review why the core spray

sparger leak detection system normal differential pressure had shifted.

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(Section M3.1). This will be accomplished during the next refueling

outage. The licensee's operability assessment concluded that the

instrumentation would still be functional during a line break. ,

Good coverage of maintenance activities by maintenance line supervision

and the health physics technician was observed during RCIC system

maintenance activities. (Section M1.4). Adequate supervisory oversight

and procedural use was observed during monthly diesel testing.

Maintenance activities with regards to securing wheeled equiament has

improved. (Section M2.1). Further attention is needed in t1e area of

foreign material exclusion around the spent fuel pool. '

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Enoineerina

A violation was identified for failure to take corrective action once

notified of an error in the rod withdrawal accident analysis. (Section

E2.1). A condition report was not initiated for this issue, that was

subsequently determined reportable, until questioned by the inspector.

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An unresolved item was identified covering issuance of a Notification of

Enforcement Discretion concerning deletion of certain response time

testing requirements. (Section E3.1)

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L Plant Sucoort i

Chemistry parameters were maintained well within TS and licensee

administrative limits. The licensee's water chemistry control program

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for monitoring water quality at specified surveillance frequencies had

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been implemented in accordance with the licensee's TS requirements.

(Section R1.1)

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The licensee had maintained an effective program to monitor and control

liquid and gaseous radioactive effluents and thereby limit doses to

members of the public to a small percentage of regulatory limits.

(Section R1.2)

The release of radioactive material to the environment from liquid and

gaseous effluents for 1995 and 1996 was a small fraction of the

10 CFR 20, Appendix B and 10 CFR 50, Appendix I limits. (Section R1.2)

The projected offsite dose commitments which resulted from plant liquid

and gaseous effluents were well within limits specified in the TSs and ,

the Offsite Dose Calculation Manual (0DCM). (Section R1.2) I

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The results of planned licensee activities to reduce tritium in the

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stabilization pond will be reviewed in the future and tracked as an

inspector followup item. (Section R1.2)

Radwaste minimization efforts were successfully reducing radwaste volume ,

with a .significant reduction in the rate of radwaste generation evident )

from 1996 to 1997 year to date. (Section R1.2) j

The radiological controls program was being effectively implemented with

generally good occupational exposure controls observed during normal

plant operating conditions. (Section R1.3)

Good radiological control performance was apparent in specific work

activities observed by the inspectors. (Section R1.3)

The licensee was effectively controlling operational site exposures to

low levels during the period of inspection although sitewide dose

performance for 1996, at 702 person rem, remained relatively high.

(Section R1.3)

An unresolved Item was identified concerning the movement valve to a

radioactive material storage area. (Section R1.3)

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The licensee had implemented an effective program for packaging,

preparation, and transport of radioactive material in accordance with

regulatory requirements. (Section R1.4)

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An unresolved item was identified to review licensee documentation to

demonstrate compliance with 10 CFR Part 71.137 audit requirements. .

(Section R1.4)

~ An inspector followup item was opened for an audit finding concerning

plant access searches. (Section S1.1) <

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Report Details

Summary of Plant Status '

Unit 1 operated continuously during this period without any significant

problems. A power adjustment was )erformed due to calibration of

feedwater flow instrumentation. T11s is discussed in paragraph 08.2.

At the end of the inspection period the unit had been on line 156 days.

On November 1, 1996, the NRC approved amendments to the Brunswick

operating licensee for a five percent increase in maximum licensed power

level. Prior to operation at u) rated )ower levels on Unit 1 the

licensee identified errors in t1eir su3mittals. The licensee committed

to hold power at the previous maximum licensed aower level until all

issues were resolved. On March 18,1997, the N1C completed its review '

of these problems and in a letter to the licensee did not object to

operation of Brunswick to the uprate licensed maximum power. Power

increase to the maximum power was contingent upon scheduling and

completion of power ascension tests. At the end of this report period,

testing had not been completed. Unit 1 remained at 95% power.

Unit 2 operated continuously during this period without any significant

problems. At the end of the inspection period, the unit had been on-

line 211 days.

The mechanical vacuum pumps remained tagged out on both units due to

concern about control room dose in the event of a Rod Drop Accident.

The licensee, in a letter to the NRC dated February 13, 1997, committed

to upgrade the mechanical vacuum pump trip function to implement a

vacuum pump trip from the main steam line radiation monitor prior to the

next startup.

Seven of eight Justification for Continued Operation (JCO) in the

Environment Qualification (EQ) of equipment area remain open for both

units. The following provides the status of the EQ JCOs and associated

Engineering Service Requests (ESRs):

1) ESR 96 00425, Evaluation of EQ sealants was considered closed by

the licensee.

2) ESR 96 00503, Associated Circuit EQ was scheduled for completion

May 31, 1997.

3) ESR 96 00426. Evaluation Quality class and EQ classification of

Post Accident Sample System valves was scheduled for completion

June 6, 1997.

4) ESR 96 00501, Motor Control Center (MCC) EQ was scheduled for

completion June 6,1997.

5) ESR 96-00625, EQ Type JC0 for EQ Fuses Without a Qualification

Data Package (QDP) was scheduled for completion June 6,1997.

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6) ESR 96 00627, ODP for Marthon 300 Terminal Blocks was scheduled 4

for completion December 31, 1997.

7) ESR 97 00087, EQ Type JC0 for Improperly Configured Conduit Seal -

was scheduled to be completed June 30, 1997.

8) ESR 97 00229. JC0 for GE CR 151 B Terminal Blocks was scheduled to

be completed July 15, 1997.

In addition, a JC0 and an Operations Standing Instruction SI 97 016,

remains in effect 3roviding guidance and allowed out of service time for  !

the three control auilding air conditioning units. During a Safety

System Functional Inspection conducted in May June 1996, it was

identified that the units were incorrectly downgraded from safety  :

related or Q list to non safety related. ESR 96 00366. Evaluation of

Using Existing Control Room Air Conditioners, provided a JC0 evaluation

until the issue was resolved. The issue remains open and the licensee

committed in their February 15, 1997, letter to resolve all open issues  :

by the completion of the Unit I refueling outage 12, scheduled to begin ,

in the second quarter of 1998.

In summary, both units operated continuously during this report period.  !

However, there are seven outstanding JCOs in the EQ area and one JC0 for

the non-Q control building air-conditioning units. Mechanical vacuum

pumps due to concerns related to Rod Drop Accident analysis remain

tagged out.

I. Doerations

02 Operational Status of Facilities and Equipment

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02.1 Shift Turnover Meetinas

a. Insoection Scope (71707)

The inspector reviewed the operation crew shift turnover meeting and

discussion held on March 4, 1997.

b. Observations and Findinos

On March 4, 1997, the inspector observed at 7:10 a.m. the crew (that had

just assumed the shift responsibilities) conduct a turnover meeting in

the control room, The shift turnover meetings are conducted different

from what the inspector had encountered at other facilities. Although

called a shift turnover meeting, the meeting was a post turnover '

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meeting. Each operator conducted a one on one turnover and assumed the

shift. The off going crew left the control room and left the site.

Each unit SR0 gave a status of the unit, etc. The crew (assigned to the

day shift) had been off several days prior to the meeting and was off -

work when the recirculation aump transients occurred on March 1,1997.

The crew stated that the pro)lems had occurred but that someone later in

the shift would give them the details.

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The inspector noted that the crew did not have a good pers)ective of

plant problems which had occurred since being off work. T1ese problems 1

were not discussed with the crew prior to them assuming the watch. The l

inspector discussed this concern with lant management. Also, the j

inspector discussed that at the other icensees' facilities shift ,

turnover was conducted in a more conventional way with a turnover l

meeting prior to assuming the shift responsibilities. l

In response to this issue, the licensee implemented a pre shift turnover

meeting for the on coming crews that had been off work for several

shifts. As the crews are on 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts, the licensee concluded that

the last 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> off shift could quickly be reviewed for plant changes j

and a pre shift turnover was not necessary. i

The inspector attended the pre shift turnover meeting on April 8, 1997.

The meeting was conducted by the off going shift supervisor. Changes

for the several days the shift was off work were reviewed.  ;

c. Conclusions i

The inspector. concluded that the present method of conducting a post '

turnover was not effective to make operators fully aware of plant

changes and problems prior to assuming the shift responsibilities. The

licensee was responsive to this concern and initiated changes to the i

shift turnover process for on coming crews that had been off site for  ;

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08 Miscellaneous Operations Issues (92901) f

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08.1 (Closed) LER 50 324/96 04: Jet Pump Surveillance Not Performed Prior to

Exceeding 25% Reactor Power. l

This licensee event report (LER) reported the events surrounding the  !

discovery that the jet pump surveillance was not performed prior to ,

exceeding 25% reactor power. During power ascension from 153 to 30%, (

the licensee failed to perform Periodic Test OPT 13.1 Reactor  ;

Recirculation Jet Pump Operability. Satisfactory performance of OPT.

13.1 would have satisfied the surveillance requirements stated in TS j

4.4.1.2.1. The licensee, upon recognizing the failure, reduced power -

below 25% and entered the Limiting Condition for Operation (LCO) for TS '

3.4.1.2. The jet pump surveillance was satisfactorily performed and the  ;

LCO exited.

The inspector reviewed the LER, associated condition report, and l

corrective action program action items. TS 4.0.4 requires that entry  ;

into an operational condition or other specified applicable state shall

not be made unless the surveillance requirements associated with the LC0

have been performed within the applicable surveillance interval or as

otherwise specified. The inspector concluded that the failure to

perform surveillance testing to satisfy jet pump operability

requirements prior to exceeding 25% rated thermal power was a violation

of TS 4.0.4. This licensee identified and corrected violation is being

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treated as a Non Cited Violation, consistent with section VII.B.1 of the  !

NRC Enforcement Policy and is identified as NCV 50 324/97 05 01, Missed ,

Jet Pump Surveillances. Based on satisfactory completion of the '

licensee corrective actions and issuance of the above NCV, this item is

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08.2 (00en) LER 50-324/96 03 01: Operation in Excess of Maximum Power Level  !

Specified in Operating License.

In this LER the licensee committed to test and calibrate the reactor

feedwater flow venturis by March 31, 1997. The licensee stated

additional time was needed to complete this action and revised the  ;

commitment date to May-30, 1997.

On April 2,1997, the licensee initiated CR 97 1293 titled

Nonconservative Feedwater Flow Indication. Ultrasonic flow testing on i

the feedwater water flow venturis revealed that the plant indicated i

feedwater flow for Unit I was nonconservative by about 1.6 percent.

Feedwater flow inputs into the reactor power level calculation. If the

new data was accurate, actual reactor power was 2479 MW thermal when

indicated power was 2436 MW thermal. Data for Unit 2 indicated the

valves were conservative. This data was in conflict with feedwater flow

tracer testing performed in 1994. Present steam plant data supported i

that the latest data was correct. However, questions remained as to why l

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The licensee took action to reduce reactor power by 43 MW thermal (93%

power), and controlled the APRM gain adjustment factors and thermal

limits equal to 0.98.

On April 7,1997, the licensee recalibrated the Unit 1 feedwater flow

transmitters with new scaling factors which the licensee considers

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conservation. Unit 1 power was increased from 93% to 95% power. Power

increase to 100% was contingent upon completion of the power ascension

tests associated with the recently NRC approved increase in maximum

thermal power.

This LER will remain open pending completion of the commitment and

further NRC review.

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08.3 (Ocen) URI 50 325(324)/97-02 02: Recirculation Pump Transients.  !

The inspector reviewed the licensee's root cause report for CR 97-00926 j

and CR 97-00923 concerning work in the switchyard on power circuit i

breaker, PCB 31A. Following maintenance the breaker was closed but a l

grounding strap had been left installed. This caused the breaker to

immediately open and a trip of the 2B recirculation motor generator set.

The licensee formed an event review team to assess the problem. The

licensee determined that the cause was due to poor worker practice, .

improper verification techniques, and insufficient administrative

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controls for maintaining status and accountability of materials. ,

Corrective action included personnel disciplinary action, training on '

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lessons learned, development of a ground tagging program, and general

review of transmission department work activities.

The inspector reviewed the licensee's event assessment team report and

concluded it was thorough. The inspector inspected the switchyard

around the PCB 31A breaker on March 5, 1997. There was no evidence of

any physical damage in the switchyard. This event was caused by

additional work outside the original job scope to remove a rag stuck in

the switch mechanism. The rag could not be easily removed. Two ground

straps were installed to allow removal of the rag. Only one ground

strap was removed and the procedure controls used initially were not  !

followed. The procedures used were Transmission Services 3rocedures and 1

not governed by the plant operating requirements. Althoug1 this event )

occurred on the owner controlled property the same problem could have  !

occurred off-site. l

Additionally, the inspector held discussions with the licensee regarding

the runbacks. Additional questions remain and this will remain open l

pending resolution of the questions. 1

II. Maintenance

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M1 Conduct of Maintenance j

M1.1 RHR Time Delay Relay Calibration

a. Inspection Scope (61726)

The inspector observed the performance of Maintenance Surveillance Test

Procedure IMST RHR28R, Time Delay Relays Channel Calibration.

b. Observations and Findinns

On March 5, 1997, the inspector observed the performance of IMST-RHR28R

for loop "A". This surveillance test performs calibrations of the time

delay relays associated with the 1 E11 F007A, Residual Heat Removal

(RHR) Minimum Flow Valve, 1-E11 F017A, LPCI Outboard Injection Valve. l

and 1 E11 F0048A, RHR Heat Exchanger IA Bypass Valve. Successful l

completion of the test partially satisfied the TS 4.3.3.2 requirement to '

calibrate the time delay relays for the RHR system.

The inspector verified that the required administrative approvals and

equipment tagouts were performed prior to beginning the testing. All

test instrumentation was verified to be within the current calibration

cycle. The test procedure was referred to at each step and the

inspector observed good procedural use, self-checking, and independent

verification. The inspector reviewed the test data and verified that

the values recorded were accurate and complete.

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Hl.2 Diesel Generator Monthly

a. Insoection Scooe (61726)

The inspector observed the performance of the monthly load test for

diesel generator (DG) 2.

b. Ebservations and Findinas

On March 31, 1997, the inspector observed the performance of Periodic

Test OPT-12.28, No. 2 Diesel Generator Monthly Load Test. OPT 12 2B was

performed to satisfy TS requirements 3.8.1.1.b and 4.8.1.1.2.a. The

test verified full level in the engine mounted and four day fuel tanks,

the diesel started and accelerated to rated speed in 10 seconds, the

generator could be successfully loaded and run for at least 15 minutes,

and the DG was properly aligned to provide power to the associated

emergency bus.

During the performance and review of the test the inspector observed

that testing was accomplished by qualified personnel, procedural

precautions and limitations were followed, and acceptance criteria met.

Inspector review determined that the procedure conformed to the TS

requirements. -The inspector independently verified selected parameters

during the surveillance

the required frequency. The performance and thatadequate

inspector observed the test supervisory

was completed at

oversight and procedure use.

H1.3. RCIC Maintenance Activities '

a. Inspection Scooe (62707)

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The inspector observed several maintenance activities during the Unit 1

Reactor Core Isolation Cooling (RCIC) System Outage.

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b. Observations and Findinas

On March 19, 1997, the inspector observed the installacion of

environmentally qualified (EQ) seals and mechanical valve lube

inspection on the RCIC system on Unit 1. The EQ seal installation was

performed to address EQ concerns with the position of the seal for

selected safety related instrumentation. During seal replacement on the

IE51 PSH N012A, RCIC Turbine Exhaust Diaphragm High Pressure Switch, the

ins actor observed adequate communication and coordination between the

war (ers, procedures had been properly approved and in use. The

inspector noted a good practice in the inclusion of relevant

administrative procedures in the work packages. Inspector observations

of mechanical valve lubrication inspections identified no concerns or

deficiencies.

The inspector verified that all applicable limiting conditions for

operation were appropriately entered and exited and that operability

testing after the EQ seal installation was completed satisfactorily.

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In addition the inspector noted good coverage of the activities by line 1

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supervision and the health physics technician.

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l M1.4 Maintenance Conclusions

i Good coverage of maintenance activities by maintenance line supervision

and the health physics. technician was observed during RCIC system

j maintenance activities. Adequate supervisory oversight and procedural

i use was observed during monthly diesel testing.

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M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 Maintenance Practices

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a. Insoection Scone (62707)

The inspector performed observations of maintenance practices during

!- routine tours on April 8 9, 1997.

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b. Observations and Findinas

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During a routine tour of the Unit I reactor building on April 8, the 1

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inspector discovered a large cart of . scaffolding material on the 20 foot )

elevation without a wheel clamp. The lack of a clama could have allowed l

. the cart to roll and potentially impact nearby High )ressure Coolant

! Injection, Standby Gas Treatment, or RHR piping. The inspector notified

licensee personnel and a clamp was promptly applied.

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During a routine plant tour of the Unit I reactor building on April 9,

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the inspector discovered a clear plastic bag containing yellow

decontamination towels. This clear plastic bag was located less than 5

feet from the spent fuel pool. The clear translucent material would not

have been readily visible should it have fallen in the spent fuel pool.

The inspector promptly notified the control room and the bag was removed

from the floor.

Despite the discovery of one wheeled cart the inspector observed that

overall licensee performance with regards to the securing of wheeled

carts has improved. The licensee had recently improved the marking and

signs on the refuel floor to raise the level o c awareness with regards

to foreign material exclusion. The clear plas'ic bag left near the

spent fuel pool demonstrates that further attenPn is needed in this

area,

c. Conclusions

Maintenance activities with regards to securing wheeled equipment has  ;

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improved. Further attention is needed in the area of foreign material

exclusion around the spent fuel pool.

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H3 Maintenance Procedures and Documentation

H3.1 Core Soray Soarcer Channel Calibration Procedure

a. Inspection Scone (61726)

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The inspector reviewed the actions associated with an abnormal  ;

differential pressure reading on the Unit 1 Core Spray Sparger Break l

Detector.

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b. Observations and Findinas

On March 9,1997, an auxiliary operator was verifying instrumentation

indications and observed that the reading displayed for 1 F21 POS-N004A,

Core Spray Line Break Indicator, was not within specifications. This l

pressure switch functions to detect a break in the core spray (CS)

piping' located between the vessel and the shroud. The differential

pressure (dP) sensor measures the pressure across the core.

The inspector reviewed the associated instrumentation, Engineering

Service Requests (ESR) 95 238 and 97 181, CR 97 1053, and LER 50 325/

97 02, Core Spray Header Differential Pressure Instrumentation

Inoperable. In LER 97 02, the licensee stated that the safety

significance was minimal since an actual break in the core spray line

would have actuated the alarm. Immediate corrective actions included

recalibration of the 1 E21 PDS N004A which confirmed that the pressure

sensor was within tolerances. Additional action included backfilling

both sensing lines with no change in the readings. After completion of

the review of the existing documentation and discussions with the

licensee the cause for the abnormal indication has not been definitively

determined. The licensee surmises that the dP may have been affected by

voiding of the sparger nozzles. The CS dP nozzles may be empty or full

depending on local hydraulic / thermodynamic conditions.

Pending completion of the NRC's review of the licensee's corrective

actions and further investigation of the problem, this item will be

tracked as Inspector Follow up Item IFI 50-325/97 05-02, Abnormal CS

Sparger Break Detector Indication.

TS surveillance operability requirement 4.5.3.1.c.2 required the

performance of a channel calibration for dP instrumentation every three

months and verification that the setpoint is 5 i 1.5 psid greater than

normal dP. The setpoint was set at +31 i 7 inches of water back in 1985

was based on a normal value of 108 inches of water. Upon determining

that the actual normal value was 154 inches of water, the licensee

concluded that the dP instrument had not been in compliance with TS

surveillance requirements. The 154 inches of water value was

determined as recorded in the system engineer's walkdown notes. ESR

97 205, and LER 50 325/97-02 Core Saray Header Differential Pressure

Instrumentation Inoperable, to have 3een the normal condition since the

start of the current Unit 1 operating cycle.

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The inspector reviewed the last three performances of Maintenance ,

Surveillance Procedure IMST CS210, CS Sparger High dP Chan Cal. This I

test was'3erformed to assure CS sparger break detection instrumentation I

was opera)le in accordance with TS 4.5.3.1.c.2. In the December 4, 1996 j

and February 2E, 1997 tests, the inspector determined that the indicated  ;

dP routinely exceeded normal expectations, therefore the alarm setpoint

was not verified to be within 5 i 1.5 psid of normal which was

identified as -154 inches of water. The inspector determined that if

the procedure had required actual verification of the alarm setpoint in I

relation to the indicated instrument pressure this nonconformance would

have been identified earlier.

TS 6.8.1.c requires that written procedures shall be established,

implemented, and maintained covering TS surveillance test activities of I

safety related equipment. The failure to have a procedure that

correctly implemented the TS 4.5.3.1.c.2 requirement that the CS Sparger

Break Detection alarm setpoint be within 5 1.5 psid greater than the

normal indicated pressure of 154 inches of water was identified as a

violation. This violation is identified as VIO 50 325/97 05 03,

Inadequate CS Surveillance Verification.

c. Conclusion

An Inspector Follow up Item was identified pending completion of NRC's

Review of licensee corrective actions and further investigation of the

problem. A violation was identified for the failure to verify the CS

sparger break detector alarm setpoint as required by TS.

MB Miscellaneous Maintenance Issues (92902)

M8.1 (Closed) LER 50 325/96 04: Standby Gas Treatment System Charcoal

Testino.

This voluntary LER was issued on April 19, 1996, to document the finding

that charcoal filters for the standby gas treatment system were not

tested in accordance with Regulatory Guide 1.52, Revision 1. as

specified in TS 4.6.6.1.b.2. This issue was identified on March 21,

1996, during the dual unit shutdown to repair problems with the service

water pumps. The Unit 1 startup was placed on hold by licensee

management pending resolution of this issue.

The issue was identified following information received by the NRC from

another utility who had identified this problem. Subsequent

investigation determined that vendor testing performed on the charcoal

for the Unit 1 standby gas treatment system was not in accordance with

Regulator Guide 1.52. Revision 1. The testing was conducted with pre-

loading, oading, and post loading temperatures of 80 degrees centigrade

(C) versus the required 25 degrees C pre and post load temperatures.

The vendor had provided the licensee certification that the testing was

performed in accordance with the requirements based on their  ;

determination that the testing was equivalent. The performance of  ;

believed equivalent testing by the vendor resulted in non compliance l

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with the requirements of TS 4.6.6.1.b.2, which was a violation. This

violation was identified as NCV 50 325/97 05 04, Charcoal Testing Not .

Performed in Accordance with TS Requirements. This non compliance

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constitutes a violation of minor significance, and is being treated as a ;

Non Cited Violation, consistent with Section IV of the NRC Enforcement

Policy.  ;

On identification, the licensee had new samples of the Unit 1 charcoal

tested in accordance with the requirements of Regulatory Guide 1.52.

Revision 1. Successful testing was completed on March 23, 1996, prior

to the restart of Unit 1. Charcoal from Unit 2, which was still within

its 18 month surveillance window from installation, was sampled and

successfully tested. In addition to these immediate corrective actions,  !

the licensee revised testing procedures for both the Unit 1 and Unit 2 l

standby gas treatment trains and control building emergency air l

filtration system charcoal filters, to specifically incorporate the l'

temperatures required in Regulatory Guide 1.52, Revision 1. These same

i changes were incorporated into the testing requests accompanying the

charcoal samples sent to the testing vendor. The inspector has reviewed I

this event and the completed corrective actions, and finds that with the

issuance of the above noted NCV, this issue is closed.

III. Enaineerina

E2 Engineering Support of Facilities and Equipment

E2.1 Rod Withdrawal Error Analysis  !

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a. Inspection Scooe (37551) i

The inspector reviewed the issues concerning notification by the fuel

vendor that an inconsistency existed between the rod withdrawal error

(RWE) analysis assumptions and the TS operability requirements.

b. Observations and Findinas

The licensee was notified in a letter dated February 24, 1997, by the  !

Boiling Water Reactor (BWR) vendor of a situation at another facility  !

that could have similar implications at Brunswick. The letter indicated '

that the vendor had failed to notify another reactor licensee of the

need to issue a TS change request to control those conditions for which ,

the continuous withdrawal of a high worth control rod may cause fuel i

damage by exceeding the 1% plastic strain criteria. In a letter dated

March 10, 1997, the licensee was notified by the BWR vendor of the

results of a review of the Supplemental Reload Licensing Report (SRLR)

specific to Brunswick. This review indicated that a similar condition ,

existed at Brunswick for Cycle 10 on Unit 1. No discrepancies were

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identified for Unit 2 or the current Unit 1 operating cycle.

The Rod Block Monitor (RBM) suspends movement of a control rod in the

event of the im)royer withdrawal of that rod from an area of high

, density during liga power. The improper withdrawal of a high worth rod

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at high power would lead to fuel damage if the cladding plastic strain

exceeds 1% or if the safety limit minimum critical power ratio (MCPR)

was surpassed. The existing RBM TS 3rovided protection of the fuel from

exceeding the safety limit MCPR in tie operational condition by

requiring both RBM channels operable when greater than or equal to 90%

rated thermal power. No requirement existed in the Brunswick TS's to

maintain RBM operability to prevent exceeding the 1% plastic strain

criteria, despite the BWR vendor analysis taking credit for that  ;

condition, i

The inspector reviewed the associated correspondence, CR 97 1277, RWE

analysis and TS. The licensee determined that on May 24, 1995, movement

of control rods while the RBM was inoperable was in accordance with TS.

During this occurrence the licensee contends that, despite movement of

the rods with the RBM ino)erable, conservatism built into the

calculation showed that t1e 1% plastic strain criteria was not exceeded.

The letter indicating the potential Brunswick discrepancy was received

by the licensee Nuclear Fuels Section and forwarded to site engineering

organization for concurrent review the day after receipt on March 10, 1

1997. Annotated on the letter was an indication dated March 11, 1997 l

that the Nuclear Fuels Section would initiate a CR. The inspector could

not locate a CR recording the nonconformance. The nonconformance was

finally entered into the corrective action program after discussions

between the inspector and the licensee on March 31, 1997, at 1:00 p.m.

concerning performance of an evaluation for reportability. Subsequently

the CR was evaluated and a reportability determination made. At

6:54 p.m. on March 31, the licensee made a four hour report to the NRC

in accordance with 10 CFR 50.72(b)(2)(iii)(D).

Plant Program Procedure OPLP-04, Corrective Action Management implements

the Corrective Action Management Policy for Brunswick. The procedure  !

required consultation with the supervisor and initiation of a CR upon  ;

identification of an operability concern or potential reportable event. '

The CR would serve to document the condition and actions taken, and the

possibility of an operability concern or reportable event. Potential

o)erability concerns or reportable events would then be evaluated by the i

S11ft Superintendent. Additionally, the CR served to provide proper I

classification and correction of adverse conditions, deficiencies, or

deviations by management processes based upon importance.

The inspector determined that a CR was not written promptly upon

identification of a potential operability concern or reportable event.

10 CFR 50 Appendix B, Criterion XVI Corrective Action, requires that

measures shall be established to assure that conditions adverse to

quality such as deficiencies, deviations, and nonconformances are

promptly identified and corrected. The failure to promptly initiate a

CR upon identification of a potential o)erability concern or reportable

event was identified as a violation. T11s violation will be identified

as VIO 50 325(324)/97 05 05, Timeliness of Operability and Reportability

Determination.

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c. Conclusions

The inspector reviewed the actions associated with the BWR vendor's

notification of an error in the SRLR for Unit 1. Licensee review

indicates that although rods were moved during RBM inoperability no i

safety limits were exceeded. The failure to promptly identify a l

nonconformance delayed evaluation of a potential operability concern or i

reportable event was identified as a violation.  !

E3 Engineering Procedures and Documentation

E3.1 Improper Removal of Instrument Response Time Testing Requirements 1

a. Inspection Scone (37551)

The inspector reviewed the actions surrounding the deletion of

instrumentation response time testing requirements from the Updated

Final Safety Analysis Report (UFSAR) and subsequent notice of l

enforcement discretion. I

b. Observatiers i

In December 1993, the NRC issued Generic Letter (GL) 93 08 Relocation

of Technical Specification Tables of Instrument Response Time Limits.

The GL provided guidance for the relocation of instrument response time

limits from the TSs to the UFSAR. The licensee submitted a TS change

request in a letter dated April 14, 1994 which was supplemented on

May 16, 1994. The letters requested relocation of the instrument

response times to the UFSAR in accordance with GL 93 08. The request

was reviewed and subsequently approved by the NRC by Amendments 171 and i

202 to the operating license for Units 1 and 2 with the NRC Safety i

Evaluation Report included in a letter dated May 31, 1994.

The NRC, in a letter dated December 28, 1994 to the Boiling Water

Reactors Owners Group (BWROG) Chairman, concluded that selected

instrumentation response time testing (RTT) as identified in BWROG

Licensing Topical Report NED0-32291 A, System Analysis for Elimination

of Selected Response Time Testing Requirements could be deleted. The NRC

would accept the topical report as a reference in license amendments for '

those licensees adopting the NEDO recommendation to eliminate selected

instrumentation RTT, based on the conclusion that significant

degradation could be detected during the performance of other 1

surveillance tests, principally calibration tests. On February 14,

1995, the licensee, citing the NRC's approval of the NED0

recommendations deleted the RTT requirements for certain instruments

under the control of a 10 CFR 50.59 safety evaluation.

c. Findinas l

On March 21, 1997, the licensee was notified of a potential

noncompliance with the TSs. On March 20, 1997, Washington Nuclear Power

Station Unit 2 (WNP-2) entered into a TS 3.0.3 required shutdown due to l

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not performing RTT of selected Reactor Protection System (RPS),

Emergency Core Cooling System (ECCS), and Containment Isolation

Instrumentation. The noncompliance at WNP 2 resulted from the improper

deletion of those RTT requirements, which were previously located in TSs

from the UFSAR without NRC a> proval. Subsequent NRC review determined

that Brunswick had deleted tie RTT requirements located in the UFSAR in

the same manner as WNP 2. The licensee inappropriately made these i

changes based on NRC approval of the NED0 document, but did not make  !

corresponding changes to the plant TS to indicate actual testing  !

methods. I

The licensee reviewed the last performances of the RTT for those

instruments deleted from the UFSAR. The licensee determined that RTT

for selected instruments in the RPS, ECCS, and those used for

containment isolation had not been performed within the TS allotted

time. The licensee stated in their request for discretion that the

affected instrumentation was verified functional during the period of ,

nonconformance by the performance of channel functional, calibration and I

logic system functional tests. At 8:30 pm on March 21, 1997 in a i

telephone conversation with the NRC, the licensee requested the NRC i

exercise discretion in the enforcement of compliance with the 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

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requirement to shutdown both units in TS Limiting Condition for i

Operation (LCO) for Sections 3.3.1, Reactor Protection System i

Instrumentation, 3.3.2. Isolation Actuation Instrumentation, and 3.3.3, l

Emergency Core Cooling System Actuation Instrumentation. In a letter to

the licensee dated March 25, 1997, the NRC staff acknowledged that the

equipment operability was assured by qualitative RTT performed on the l

deleted instruments in accordance with the NRC-anroved NEDO topical  ;

report. Based on evaluation of the request the RC staff was satisfied

that granting the request involved minimal or no safety impact on public

health and safety. Therefore, the NRC staff exercised discretion not to

enforce compliance with the applicable TS sections. The Notice of

Enforcement Discretion was granted by the NRC staff by telephone at

9:36 p.m. and documented by the March 25, 1997 letter.

The inspector reviewed the TS, associated Engineering Service Requests,

TSs, unit log entries, and correspondence. The inspector verified that

the licensee approved the deletion of selected instrumentation RTT under

a 10 CFR 50.59 safety evaluation. UFSAR Change Request 94FSAR 100,

Deletion of RTT Requirements Per NED0 32291, documents this deletion.

The change analysis cites NRC approval of the NEDO topical report in the

10 CFR 50.59 evaluation. This issue is unresolved pending further NRC

review. This issue is identified as URI 50 325(324)/97 05 06, Deletion

of RTT Requirements.

d. Conclusions

The licensee as a result of a BWROG topical report deleted TS RPS, ECCS,

and Isolation Actuation response time testing. Subsequently, a notice

of enforcement discretion was issued due to the failure to perform

several response time test as required by TS. This issue is unresolved

pending further NRC review.

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E3.2 Soecial UFSAR Review

A recent discovery of a licensee o)erating the facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures, and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspectors reviewed the applicable

portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures, and/or parameters.

The inspectors reviewed the UFSAR change associated with instrument

response time testing requirements in paragraph E3.1. No additional

issues were identified.

IV. Plant Support

R1 Radiological Protection and Chemistry Controls

R1.1 Water Chemistry Controls

a. Inspection Scoce (84750)

The inspectors evaluated implementation of the licensee's water

chemistry program for control of primary system water quality. The

inspectors reviewed the specific plant chemistry and operational

controls affecting plant water chemistry. TS 3.4.4 specifies that the

concentration of chloride and the conductivity level in the Reactor

Coolant System (RCS) be maintained below 0.50 ppm and 2.0 mhos/cm,

respectively. TS 3.4.5 specifies that the specific activity of reactor

coolant be limited to less than or equal to 0.2 Ci/g dose equivalent

iodine (DEI).

b. Observations and Findinos

The inspectors reviewed the licensee's Procedure OAI 81, Water Chemistry

Guidelines, Revision No. 18, dated January 14, 1997, and determined that

it included provisions for sampling and analyzing reactor coolant at the

prescribed frequency for the parameters required to be monitored by TSs.

Action levels and responses for out of limit chemistry parameters were

also reviewed as described in 0AI 81. This procedure included provisions

for monitoring water quality based on established industry guidelines

and standards. The inspectors noted that the referenced licensee

procedure specified the sampling frequency and ty)1 cal values for each

parameter to be monitored. Action levels applica)le to various

operational modes were given where appropriate. Guidance was also

provided for actions to be taken if analytical results exceeded

prescribed limits. The inspectors determined that the above guidance

and procedures were consistent with applicable TS requirements.

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The inspectors reviewed chemistry statistical analysis reports, primary

chemistry data, related data trend plots, and records of analytical l

results for selected Unit 1 and Unit 2 parameters at power operations

and at shutdown during the period January 1, 1995 through March 4, 1997.

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The parameters selected included conductivity, chlorides, sulfates,

boron, zinc, and dose equivalent Iodine 131. A review of chemistry data

disclosed that the licensee exceeded water chemistry TS limits for

1

conductivity on April 20 and 21,1995 but the Unit 1 reactor vessel was l

defueled, the unit was in an outage, and the licensee was conducting a

full system chemical decon. The licensee was able to provide ,

documentation that verified an exemption had been granted to exceed TS  :

limits by the NRC's Office of Nuclear Reactor Regulation based on the

licensee's amendment submittal approved by the NRC for these specific

conditions only. The licensee also entered administrative action levels

in accordance with 0AI 81 on numerous occasions during the period of

review indicating a parametric variance from normal values during power  !

operations. In each case the inspector reviewed, the licensee was able l

to explain the variance in terms of an anomaly such as a reactor water

cleanup (RWCU) system trip, expended RWCU filters, or an evolution such l

as a reduction in the hydrogen water chemistry (HWC) injection rate.

c. Conclusions

Chemistry parameters were maintained well within TS and licensee

administrative limits. The licensee's water chemistry control program i

for monitoring water quality at specified surveillance frequencies had

been implemented in accordance with the licensee's TS requirements. l

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R1.2 Semiannual Radioactive Effluent Release Reoort l

a. Insoection Scope (84750)

TS 6.9.1.8 requires the licensee to submit a Semiannual Radioactive

Effluent Release Report covering licuid and gaseous effluent releases

resulting from facility operations curing each six months period of

prior operation. The report provided required estimates of radiation

doses to members of the public from effluents released to unrestricted  :

areas. Data on solid radwaste shipments was also provided in the report

and evaluated. The licensee's program to monitor and control radiation

,

doses associated with effluent releases within TS 3.11 limits was

evaluated. The inspectors also evaluated effluent data to identify

adverse effluent trends, increases in estimated doses to the public from

effluents, if any, and explain these variances in the context of

operational experience,

b. Observations and findinos

Liquid and gaseous effluent data was developed from the licensee's

effluent release reports for the years 1994, 1995, and 1996. The

inspectors evaluated sup)orting raw data for effluent release reports

covering these years wit 1 emphasis on identifying elevated release

trends or data anomalies. As shown in the effluent release summary

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below, the amount of activity released during 1994, 1995, and 1996 in

liquid effluent streams remained relatively stable, at low levels, and

well within regulatory release limits. The amounts of activity released

during 1996 as fission gases, iodides, and particulates in gaseous

effluents was also at low levels and within release limits. Minor

variances in gaseous effluent parameters within operational limits were

identified between 1995 and 1996 indicative of normal steady state power

operations. No abnormal releases were identified during the period.

Brunswick Radioactive Effluent Release Summary

1994 1995 1996

Abnormal Releases

Liquid 0 0 0

Gaseous 0 0 0

Activity Released (curies)

a. Liquid

1. Fission and 0.045 0.415 0.04

Activation Products

2. Tritium 69.6 55.2 47.2

b. 'iaseous

1. Noble Gases 477 4330 713

2. Iodine 131 2.13E-03 5.32E-03 2.12E 02

3. Particulates 2.12E 02 2.24E 02 6.36E 03

4. Tritium 2.26E 01 3.66E 01 2.70E-01

As indicated above the curies of mixed fission and activation products I

were significantly elevated for 1995 in liquid releases due primarily to ]

the high activity from s)ent fuel shipping casks. The licensee

addressed this problem t1 rough improved control over cask washdown water

and the installation of a filter on the refuel floor to remove activity

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prior to introduction into the radwaste system. During 1996, the

i licensee achieved low levels of liquid effluents due to a liquid

l effluent reduction initiative that included the recovery of the floor

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drain collector filter system and cleanout of radwaste tanks and piping.

Accumulated sludge and debris from radwaste processing systems was

successfully removed. As a result of this radwaste processing system

upgrade project, a majority of floor and equipment drain quality water

was reclaimed resulting in a great reduct1on in liquid effluent volume

and curies. Less than three million gallons of radioactive liquid

effluents were released from radwaste (only 800,000 gallons released

from April through December 1996) as a result of this 3roject which

represents a record low release volume for the site (Tle site released

4.4 millirem gallons in 1995.)

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4.- M 4 62 m .r-u. om ,+,+ r 5' nu, A4h 46 asAman,2,- a b mu- 4 e, =D , 46 S

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During 1995, noble gases released were elevated due to the 3resence of a

fuel leak in Unit 2 and problems associated with bypass leacage of a

Unit 2 offgas by) ass . valve. Successful licensee efforts to mitigate the

bypass valve pro)1em pending outage work precluded a significantly

greater gaseous release volume.

The inspectors evaluated 1994,1995, and 1996 hypothetical maximum

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annual dose estimates to the public from radioactive materials in

! gaseous and liquid effluent streams. Dose limits for the total body

from liquid effluents are given in TS 3.11.1.2. and limits for, doses

from gaseous effluents are provided'in TS 3.11.2.2 and TS 3.11.2.3.

Doses are calculated in accordance with the methodology in the Offsite

Dose Calculation Manual (0DCM) and are a function of the release point,

the isotopic mix, total curies released, and exposure pathways. All

calculated doses from liquid and gaseous releases were determined to be

less than 1 percent of the applicable TS dose limits and were calculated

to be in a range of 0.03 percent to 0.4 percent of applicable TS limits.

! The inspectors evaluated current tritium concentrations in the

licensee's storm drain stabilization pond based on recent licensee

condition reports which identified an increasing trend in tritium

concentration in the pond. One sample well, ESS 2C., averaged monthly

, tritium concentrations during a recent twelve month period of

approximately 84,000 picocuries/ liter. The average tritium

concentration in the pond water from 1991 to the present was 8E-5

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microcuries/cc which was below the 10 CFR Part 20 limit of IE-3

microcurie /cc. However, in that the pond is unlined and elevated, there

is a hypothetical potential paMsay for tritium migration. Monitored

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releases within regulatory limits are currently made from.the pond

routinely via a ditch to the intake canal. To address the issue of

recent elevated tritium concentrations in the pond, the licensee plans

an upgrade which would route turbine building condensate containing

) tritium to the plant's normal radwaste system for )rocessing instead of

the storm drain system which discharges to the sta)111zation pond.

Additional licensee actions contemplated include increased water

sam) ling and additional monitoring wells in potential migration

pat 1 ways. The inspectors evaluation of current licensee studies and

monitoring results identified no regulatory concerns. The inspectors

informed the licensee that the planned licensee activities which address

this issue will be further reviewed upon completion and the issue will

- be tracked as an Inspector Followup Item (IFI). IFI 50 325(324)/

97 05 07. Actions to Reduce Tritium in the Stabilization Pond.

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The licensee had undertaken initiatives to reduce solid radwaste volume

during 1996 and 1997. Efforts ongoing in radwaste generation

minimization include increased education and communication programs and

radwaste volume reduction / minimization initiatives. The licensee was

storing onsite all radwaste generated, including post processing

radwaste, due to the unavailability of offsite low level radwaste

storage. During 1996, the licensee generated 60,655 cubic feet of

radwaste, which was less than projected. During 1997, the licensee had

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generated 4825 cubic feet through February. The 1997 goal was 49,300

cubic feet (a one outage year).

c. Conclusions

The inspectors concluded that the licensee had maintained an effective  !

program to monitor and control liquid and gaseous radioactive effluents '

and thereby limit doses to members of the public to a small percentage

of regulatory limits. The release of radioactive material to the .

environment from liquid and gaseous effluents for 1995 and 1996 was a  !

small fraction of the 10 CFR 20, Appendix B and 10 CFR 50, Appendix I

limits. The projected offsite dose commitments which resulted from

plant liquid and gaseous effluents were well within limits specified in j

the TSs and the Offsite Dose Calculation Manual (0DCH). The results of

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planned licensee activities to reduce tritium in the stabilization pond

will be reviewed in the future and tracked as an inspector followup

item. Radwaste minimization efforts were successfully reducing radwaste

volume with a significant reduction in the rate of radwaste generation i

evident from 1996 to 1997 year to date. '

R1.3 External Occupational Exoosure Control and Personal Dosimetry

a. Insoection Scope (837501

The inspectors evaluated the adequacy of licensee radiological. controls

with emphasis on external occupational exposure controls during normal

power operations. The inspectors made tours of the radiation controlled  ;

areas, observed compliance of licensee personnel with radiation  !

protection procedures for routine work evolutions, and conducted

interviews with licensee personnel with respect to knowledge of ,

radiological controls and working conditions. The inspectors evaluated

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the adequacy of licensee commitnents to upgrade site dosimetry and l

wrsonnel monitoring programs to address NRC concerns identified in i

3runswick Unresolved Items 50 325(324)/96 16 03 for Lack of Accurate

Dose Tracking and Dose Assignment Practices and Related Procedures.

b. Observations and Findinas

The inspectors observed controls for external occupational ex osures  ;

l which met applicable regulatory requirements and were designed to i

l maintain exposures As Low As Reasonably Achievable (ALARA). The '

l inspectors reviewed select radiation work permits (RWPs) utilized to I

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control ongoing work within the radiation controlled area (RCA) and 1

noted that the rad controls observed were appropriate for the described - i

tasks and radiological conditions. Interviews were conducted with '

radiation workers in order to determine the level of understanding of

radiation work permit requirements from a re3resentative cross section

of plant workers. The inspectors observed tlat the workers interviewed

had signed onto an RWP. were wearing dosimetry appropriate to their work

activities within the RCA in accordance with plant 3rocedures, and were

performing specific work activities on appropriate RWPs. The workers

demonstrated an adequate knowledge of RWP requirements and of

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radiological working conditions. The ins)ectors continued to note ,

upgraded radiological posting practices tiroughout the plant. Pre job l

RWP work planning and ALARA briefings for observed ongoing work

evolutions were found to be conducted in an effective manner. During i

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tours of the plant, the inspectors observed RC technicians performing

radiation and contamination surveys in accordance with procedure. 1

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During a routine facility inspection walkdown on the morning of l

March 26, 1997, the inspectors toured the Radioactive Material Storage

Container Building (RMSCB) and identified a standard size five gallon

bucket that had the appearance of a new, unopened container. The

container was labelled " Activated Charcoal." With no radioactive  ;

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material label evident. During questioning of licensee personnel in the

area, it was determined the bucket had alarmed the small article monitor

and measured approximately 1.3 million dpm. The inspectors requested I

that the contents be surveyed. Licensee personnel appropriately affixed i

a radioactive material label to the container as an immediate corrective

action necessary to identify the hazard. It was later determined that

the bucket contained highly contaminated components including a valve

which surveyed at 474,000 dpm and a bag of nuts and bolts that surveyed I

at 681,000 dpm. In addition to a radiological safety concern with

radioactive material found not controlled in accordance with labeling j

and storage procedures, the inspectors were additionally concerned that i

radiation workers had apparently not properly released the contaminated  !

materials from a contaminated area prior to placement of the bucket in I

the RMSCB. Although not observed by the inspectors, the apparent i

improper transfer of highly contaminated material out of a contamination l

area (masked in what appeared to be a new container of activated

charcoal) indicated a disregard for contamination control procedures.

Upon discussion of these concerns with licensee management the licensee

indicated full agreement and initiated prompt and thorough corrective

actions. These actions included documentation of the findings as

condition reports requiring root cause analysis, proper disposition of

the improperly controlled container and its contents, initiation of an

investigation to determine the circumstances / origins of the bucket, and

a sitewide standdown with all site personnel regarding compliance with

the basic radiation protection principles violated. The circumstances

surrounding the movement of this highly contaminated valve from the work

area to the RMSCB are identified as an Unresolved Item pending ,

completion of the licensee's investigation. URI 50 325(324)/97 05 08.

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Movement of Unlabeled Container of Radioactive Material from Work Area

to RMSCB.

During inspection activity conducted during the period December 2 6,

1996, the inspector's evaluation of the licensee's dosimetry,

monitoring, and general radiation control procedures indicated the

licensee did not treat dose to occupational workers in buildings outside i

the RCA as occupational dose and that licensee procedures and practices

were generally deficient in this regard. Details of the issue are i

contained in Brunswick Inspection Report 96 16, dated January 2, 1997, l

in Paragraph R1.4 External Occupational Control and Personal Dosimetry. i

The licensee was unable to demonstrate adequately during the prior  !

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inspection that occupational dose received by workers outside the RCA ,

(restricted area) was being considered .in the prospective analysis used

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to determine if workers required monitoring in accordance with the

requirements of 10 CFR 20.1502. In response to these findings the  ;

licensee documented the issues in condition reports, identified root  !

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causes, and initiated significant corrective actions sufficient to

remedy the inspector's concern. These actions included: 1) Expansion of

the population of workers who will be issued a TLD to encompass all

permanently assigned personnel at the site. This will involve the ,

assignment of approximately 200 additional TLDs: 2) Revised plant

, practices and related procedures to permit all workers assigned a TLD to i

take them home and wear at all times while on site: and 3) Revise the  !

practice of 100 percent " background radiation" subtraction as detected

at a RCA access point to a practice of subtracting natural background as  :

detected at a remote point not influenced by turbine building radiation  :

shine. Although planned corrective actions adequately address the

regulatory concerns identified during the prior inspection URI 50-

325(324)/96 16 03 will remain open pending licensee completion and l

implementation of needed dosimetry upgrades. ,

c. Conclusions

The radiological controls program .was being effectively implemented with

i generally good occupational exposure controls observed during normal

plant operating conditions. Good radiological control performance was

apparent in specific work activities observed by the inspectors. The .

licensee was effectively controlling operational site exposures to low

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levels during the period of inspection although sitewide dose  !

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acrformance for 1996, at 702 person rem, remained relatively high. An  !

Jnresolved Item was identified concerning the movement of a contaminated  !

valve to a radioactive material storage area.

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R1.4 Transoortation of Radioactive Materials t

I a. Inspection Scope (86750)  ;

The inspectors evaluated the licensee *s program for the preparation and

shipment of packages of radioactive materials in accordance with  ;

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regulatory requirements and the licensee's radioactive material receipt l

and shi) ping procedure, HPS NGGC-0001, Rev. 4. dated February 17, 1997.  !

10 CFR ) art 71 established the requirements for packaging, preparation 1

for shipment, and transportation of licensed material. 10 CFR Part 71,  !

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Subpart H, established the quality assurance (QA) program requirements

applicable to transportation of radioactive materials. 10 CFR Part

71.137 required the licensee to perform comarehensive, planned and  :

periodic audits to verify compliance with t1e QA program and to  ;

determine the effectiveness of the program.

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b. Observations and Findinas  !

The inspectors evaluated the licensee's preparation of packages for

transport including vendor services used for preparation and transport

of radwaste. Also reviewed were detailed checklists completed by the

licensee and vendors at the time of shipments to ensure proper l

packaging, labeling, and placarding of vehicles prior to shipping i

radioactive material offsite. The inspectors' determined that licensee's i

procedure for shipping radioactive materials included provisions for i

performing the required surveys and for assuring that the radiation and

contamination limits were met for each package offered for shipment.

Licensee's records for several shipments of radioactive material were

reviewed and it was found that the required surveys had been performed  ;

and that radiation and contamination limits had been met. The inspectors '

determined that the licensee's procedures included provisions for

preparing shipping papers and manifests in accordance with requirements '

and for recording the required information thereon. The~ inspectors also

reviewed shipping papers for selected shipments of radioactive materials

and determined that they had been prepared in accordance with 3rocedure.

The inspectors determined that the licensee's procedures for slipping

radioactive materials included provisions for providing drivers with the

required instructions and that the shipping papers for selected

shipments included a copy of those instructions. The inspectors

determined that the licensee's procedures for shipping radioactive

materials included provisions for making recuired advance notifications  !

and that the licensee's records for selectec shipments included copies

of the forms used to make the recuired notifications. The inspectors

reviewed selected shipping recorcs and determined that needed

information was being retained as required. The inspector's evaluated a  :

1995 E&RC program assessment to determine if the licensee had met the ,

audit requirements of 10 CFR Part 71.137. The assessment was provided )

in response to the inspector's request to see an audit that met the I

s)ecific requirements of Part 71.137. The inspectors determined that l

tie assessment was broad in scope, covered multiple E&RC areas, but had i

very limited coverage of Part 71, Subpart H requirements, and did not

meet the regulatory intent of Part 71.137. The licenste stated that

despite the limited scope of the assessment reviewed they believed they

were in compliance when other audits in other quality assurance areas ,

were considered that could be tied to packaging and trans>ortation of I

radioactive material requirements. The licensee stated t1ey could i

demonstrate compliance and needed time to prepare a response. Review of

licensee documentation for compliance with 10 CFR Part 71.137 was

identified as an Unresolved Item URI 50 325(324)/97 05 09. Review  !

Licensee Documentation for Compliance with Transportation of Rad

Material Audit Requirements.

c. Cpnclusions

Based on the above reviews and observations, it was concluded that the

licensee had implemented an effective program for packaging,

preparation, and transport of radioactive material in accordance with

regulatory requirements. One Unresolved Item was identified based on the

. . . .- . - . . ._- . . - . -. -. . . -

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need of the licensee to demonstrate compliance with 10 CFR Part 71.137

audit requirements.

P8 Miscellaneous Emergency Planning (EP) Issues (92904) '

!

P8.1 (Closed) LER 50-325/96 08: Hurricane Bertha at Brunswic h )

-

.

ThisLERwasissuedonAugust8,1996,torekorteventswhichoccurred

onsite due the impact of Hurricane Bertha, he site entered an Unusual

l Event (UE) on July 10, 1996, following the issuance of a hurricane

warning for the Brunswick County area by the National Weather Service.

Pre)arations were made to ready the site for the storm. In accordance

wit 1 site procedures, both units were taken to Cold Shutdown in

preparation for the storm's arrival. Due to power losses caused by the

storm, 29 of the 34 off site emergency notification sirens became

inoperable. A one hour notification was made in accordance with 10 CFR

50.72(b)(1)(v) when greater than seven sirens were determined to be l

inoperable. Additionally, a one hour event notification was made to  ;

'

report the suspension of the roving security watches pursuant to 10 CFR

, 50.54(x). While the roving watches were suspended, additional measures

were established to maintain the requirements of the security plan. A

subsequent review of the event identified that the suspension of the

security watches and establishment of other measures constituted a 1

loggable event in accordance with 10 CFR 73.71. However, this did not

<

require invoking the provisions of 10 CFR 50.54(x). This issue, as well

as the actions taken were discussed with and reviewed by the Region II

security specialist inspector, and determined to be acceptable. The

issuance of this voluntary LER documenting this issue is considered

acceptable for closure of this item.

, P8.2 (Closed) LER 50-325/96-11: Hurricane Fran at Brunswick.

This LER was issued on October 4, 1996, to report events which occurred

d

onsite due the impact of Hurricane Fran. The site entered an Unusual

Event on September 4, 1996, following the issuance of a hurricane

,

warning for the Brunswick County area by the National Weather Service.

.

Pre)arations were made to ready the site for the storm. In accordance

'

wit 1 site procedures, both units were taken to Cold Shutdown in ,

preparation for the storm's arrival. Due to power losses caused by the  !

'

storm, 31 of the 34 off site emergency notification sirens became

inoperable. A one hour notification was made in accordance with 10 CFR

50.72(b)(1)(v) when greater than 7 sirens were determined to be

inoperable. Additionally, a one hour event notification was made to

1

report the suspension of the roving security watches pursuant to 10 CFR

50.54(x). .When the roving watches were suspended, additional measures

were taken to meet the requirements of the security plan. Despite these

efforts, a security alert was declared on September 5,1996, following

i the inability of two security cameras to monitor two protected area

, zones. For approximately 25 minutes, the requirements of security plan

i were unable to be met due to the immediate threat to personnel safety in

l posting compensatory guards to monitor the areas covered by the two

cameras. Ca'nera coverage was restored approximately 25 minutes later.

.

. . - - -- - _

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This uncompensated degradation of a safeguards system is a loggable

security event and meets the reportability requirements specified in 10 ,

CFR 73.71. This issue, as well as the actions taken were discussed with

and reviewed by the Region II security specialist inspector, and

determined to be acceptable. The issuance of this voluntary LER

documenting this issue is considered acceptable for closure of this '

item.

,

S1 Conduct of Security and Safeguards Activities

'

S1.1 Annual Security Assessment

'

a. Inspection Scone (71750)

The inspector reviewed the annual assessment relating to protected area

personnel access measures including equipment or pat-down searches for

illegal contraband.

b. Observations and Findinas  ;

The inspectors reviewed the circumstances of CR 97-00794, dated

February 20, 1997, resulting from a Nuclear Assessment Section (NAS)

findings during the February 17-28, 1997, annual self assessment of the

security program. The NAS team conducted performance drills during the

evaluation and noted that the security officers responsible for .

conducting personnel and package searches prior to allowing access to I

the protected area (PA) failed to identify or aroperly handle devices l

introduced as contraband during two of the eig1t drills. As a result a l

potential existed for a weapon and explosive device to be introduced l

into the arotected area. However, these events were part of a drill and '

none of t1e devices were introduced into the PA. 1

i

Paragraph 7.0 of the Physical Security Plan (PSP), Revision 0, dated

March 15, 1996, requires "all )ersonnel, materials, packages (including

hand carried packages), shall 3e searched for firearms, explosives and 1

incendiary devices, prior to entry into the protected area." Paragraph

7.1 (3), of the PSP requires that a hands on search of any individual be

conducted when the search officer has a well founded suspicion that the .

individual may be carrying firearms, ' explosives, or incendiary devices.

Security procedure OSI 9 Personnel Access Authorization, Control and  !

Identification, Revision 74, dated July 25, 1996, requires that " hand

held metal detector units and/or a pat-down search shall be performed to

the degree necessary to ensure detection of explosives, firearms, or

'

incendiary devices on these individuals who are not successfully

screened by the walk through detectors."

As noted above on two seaarate occasions during performance testing the

'

search officers responsi)le for ensuring that contraband was not

I introduced into the protected area failed to perform duties according to

regulatory requirements. Licensee management was responsive to this

issue and initiated action to upgrade training in this area. j

l

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24

c. Conclusions

'

The security personnel responsible for searching personnel and packages

! entering the protected area failed to properly identify and control .

l contraband. Additionally, work practices at the Primary and Secondary  !

Access portals was not consistent with approved procedures and )lans.

This will be an inspector follow up item 50 325(324)/97-05 10 )ersonnel ,

Access Search Training.

V. Manaoement Meetinas i

l

l XI Exit Meetina Summary

The inspector presented the inspection results to members of licensee

management at the conclusion of the ins)ection on April 21, 1997. Post

inspection briefings were conducted on ,iarch 27, 1997. The licensee

acknowledged the findings presented.

,

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!

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25  ;

PARTIAL LIST OF PERSONS CONTACTED

Licensee

G. Barnes, Manager Training '

C. Barnhill, Dosimetry Supervisor, E&RC

A. Brittain, Manager Security

.

W. Campbell, Vice President, Brunswick Steam Electric Plant

1

R. Crate, Superintendent, Radiation Protection

B. Deacy. Outage Planning Manager

N. Gannon, Manager Maintenance

J. Gawron, Manager Nuclear Assessment

D. Holder, Supervisor, Radwaste Programs

K. Jury, Manager Regulatory Affairs

'

W. Levis, Director Site Operations

B. Lindgren, Manager Site Support Services

R. Lopriore, General Plant Manager ,

.J. Lyash, Brunswick Engineering Support Section

i B. Nurnburger, Superintendent, Environmental and Chemistry

C. Pardee Manager Operations

G. Raker, Senior Analyst. Environmental and Chemistry -

D. Pacini, Radiation Control Supervisor

"

i P. Sawyer, Radiation Control Supervisor '

R. Schlichter, Manager Environmental and Radiation Control

S. Tabor, Senior Specialist. Regulatory Affairs

J. Terry, Program Analyst E&RC

M. Turkal, Supervisor Licensing and Regulatory Programs

Other licensee employees or contractors included office, operation, '

maintenance, chemistry, radiation, and corporate personnel.

E. Brown

C. Patterson

W. Rankin

D. Thompson

K. Barr

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26 L

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations -

IP 62707: Maintenance Observations

, IP 71707: Plant Operations

IP 71750
Plant Support Activities

IP 83750: Occupational Radiation Exposure

IP 84740: Radwaste Treatment Effluent & Environmental Mon.

IP 86750: Transportation of Radioactive Material ,

IP 92901: Followup Operations '

IP 92902: Followup Maintenance

IP 92904: Followup - Plant Support

ITEMS OPENED, CLOSED, AND DISCUSSED l

Ooened

50 324/97 05 01 NCV Missed Jet Pump Surveillance (paragraph 08.1)

50 325/97 05 02 IFI Abnormal CS Sparger Break Detector Indication .

(paragraph M3.1)  !

50 325/97 05 03 VIO Inadequate CS Surveillance Verification

(paragraph M3.1)

50-325/97 05 04 NCV Charcoal Testing Not Performed in Accordance

with TS Requirements (paragraph M8.1)

50 325(324)/97-05-05 VIO Timeliness of Operability and Reportability

Determination (paragraph E2.1) l

l

l

50-325(324)/97 05 06 URI Deletion of RTT Requirements (paragraph E3.1)

50 325(324)/97 05 07 IFI Actions to Reduce Tritium in Stabilization Pond

(paragraph R1.2)

50 325(324)/97-05 08 URI Movement of Highly Contaminated Valve from Work

Area to Storage (paragraph R1.3) ,

50 325(324)/97 05 09 URI Review Licensee Documentation for Compliance .;

with Transportation of Rad Material Audit  ;

Requirements per 10 CFR 71.137 (paragraph R1.4)

'

50 325(324)/97-05-10 IFI Personnel Access Search Training (paragraph ,

S1.1)

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27

Closed  :

50 324/97 05-01 NCV Missed Jet Pump Surveillance (paragraph 08.1)

50 324/96 04 LER Jet Pump Surveillance Not Performed Prior to

Exceeding 25% Reactor Power (paragraph 08.1)

50 325/96 04 LER Standby Gas Treatment System Charcoal Testing

(paragraph M8.1)

50-325/97 05-04 NCV Charcoal Testing Not Performed in Accordance  :

with TS Requirements (paragraph M8.1)  !

50-325/96 08 LER Hurricane Bertha at Brunswick (paragraph P8.1)

50 325/96 11 LER Hurricane Fran at Brunswick (paragraph P8.2)

!

'

Discussed

50-324/96-03 01 LER Operation in Excess of Maximum Power Level ,

Specified in Operating License (paragraph 08.2)

50-3?5(324)/97 02 02 URI Recirculation Pump Transients (paragraph 08.3)

50 325(324)/96-16 03 URI Unresolved Item for Lack of Accurate Dose

Tracking and Dose Assignment Practices and

Related Procedures (paragraph R1.3)

50 325/97 02 LER Core Spray Header Differential Pressure ,

Instrumentation Inoperable (paragraph H3.1) l

,

1

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