ML20244C982

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Insp Repts 50-324/89-05 & 50-325/89-05 on 890201-0315. Violations Noted.Major Areas Inspected:Maint Observation, Surveillance Observation,Operational Safety Verification,Esf Sys Walkdown & Onsite Licensee Event Repts Reviews
ML20244C982
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 04/06/1989
From: Dance H, Levis W, Madden P, David Nelson, Ruland W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20244C969 List:
References
50-324-89-05, 50-324-89-5, 50-325-89-05, 50-325-89-5, IEB-88-007, IEB-88-7, NUDOCS 8904210087
Download: ML20244C982 (25)


See also: IR 05000324/1989005

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION '

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Report >o. 50-325/89-05 and 50-324/89-05

Licensee: Carolina Power and Light Company

P. O. Box 1551

Raleigh, NC 27602

Docket No. 50-325 and 50-324 License No. DPR-71 and DPR-62

Facility Name: Brunswick I and 2

Inspection Conducted: February 1 - March 15,1989

Inspectors: (- '

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Date Signe'd

Approved By: b dNL ,/N

Fl. C. Daned, Section Chief Dat6 Signed

Division of Reactor Projects

SUMMARY

Scope: This routine safety inspection by the resident inspectors involved the

areas of maintenance observation, surveillance observation, operational safety

verification, Engineered Safety Feature System walkdown, onsite Licensee Event

Reports review, in office Licensee Event Reports review, handling of emergency

diesel generator fuel oil, implementation of requested actions of NRC Bulletin

88-07, installation and testing of modifications, drawing system verification,

and action on previous inspection findings.

Results: In the areas inspected three violations were identified. The first

violation involved the hanging of an improper clearance on certain Unit 1 SLC

valves, which led to the inadvertent draining of the SLC tank. Accordingly,

increased management attention is required over clearance control,

paragraph 12.g. The second violation, which is not being cited, involved a

failure to document a valve position change (locked open to open) on an

exception form. The third violation resulted from failure to adequately verify

correct pressure in stored pressure dry chemical fire extinguishers,

8904210087 890406 ^

PDR ADOCK 05000324

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paragraph 4.b. All three violations occurred in the operations area,

indicating that continued management attention is required over that work

group.

The licensee made an interpretation of the definition of " core alteration"

that is not supported by the current language of the Technical Sepcifications.

The licensee plans to submit an amendment request to NRR, paragraph 4.a.

Housekeeping remains a strength. However, system walkdowns still show that

minor leaks and other discrepancies are not being documented and corrected by

the plant staff, paragraph 5.b.

The licensee satisfactorily implemented Bulletin 88-07, but certain

discrepancies still require resolution, paragraph 9.

Plant drawings satisfactorily supported operations in the control room and

technical support center. A previous problem with timely delivery of aperture

cards to the control room was resolved through third party /QA in"olvement.

P&ID hard copies in the control room were well controlled with virtually no

plant modification outstanding. The licensee's complete yearly ' inventory of

CR/ Operations drawings should keep the aperture card file updated. Two system

descriptions were not adequately maintained current. Excessive plant

modifications remained outstanding against two SDs, paragraph 11.

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REPORT DETAILS

1. Persons Contacted j

Licen see . Employee s

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  • K. Altman, Engineering Supervisor i

W. Biggs, Engineering Supervisor i

  • F. Blackmon, Manager - Operations

J. Brown, Resident Engineer

  • S. Callis, On-Site Licensing Engineer

T. Cantebury, Mechanical Maintenance Supervisor (Unit 1)

  • G. Cheatham, Manager - Environmental & Radiation Control i
  • M. Ciemnicki, Security

R. Creech, I&C/ Electrical Maintenance Supervisor (Unit 2)  ;

  • W. Dorman, Supervisor - QA i
  • K. Enzor, Director - Regulatory Compliance i

R. Groover, Manager - Project Construction

  • V. Grouse, Employee Relations
  • J. Harness, General Manager - Brunswick Nuclear Project

W. Hatcher, Supervisor - Security

a. Hegler, npervisor - Radwaste/ Fire Protection

n. Helme, Manager - Technical Support

J. Holder, Manager - Outages -l

L. Jones, Director - Guality Assurance (QA)/ Quality Control (QC)

M. Jones, Director - On-Site Nuclear Safety - BSEP )

R. Kitchen, Mechanical Maintenance Supervisor (Unit 2)

G. Oliver, Manager - Site Planning and Control

  • J. O'Sullivan, Manager - Training
  • B. Parks, Engineering Supervisor
  • M. Pastva, Senior Specialist

R. Poulk, Project Specialist - NRC

  • J. Smith, Director - Administrative Support j

S. Smith, I&C/ Electrical Maintenance Supervisor (Unit 1) '

  • R. Starkey, Project Manager - Brunswick Nuclear Project ,
  • R. Warden, Manager - Maintenance i'

B. Wilson, Engineering Supervisor

  • T. Wyllie, Manager - Engineering and Construction

Other licensee employees contacted included construction craftsmen,

engineers, technicians, operators, office personnel, and security force

members.

  • Attended the exit interview.

Note: Acronyms and initialisms used in the report are iisted in

paragraph 14. l

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2. Maintenance Observation (62703)

The inspectors observed maintenance activities, interviewed personnel, and

reviewed records to verify that work was conducted in accordance with

approved procedures, Technical Specifications, and applicable industry

codes and ~ standards. The inspectors also verified that: redundant

components were operable; administrative controls were followed; tagouts

were adequate; personnel were qualified; correct replacement parts were

used; . radiological controls were proper; fire protection was adequate;

quality control hold points were adequate and observed; adequate

post-maintenance testing was performed; and independent verification

requirements were implemented. The inspectors independently verified that

selected equipment was properly returned to service.

The inspectors observed / reviewed portions of the following maintenance

activities:

87-AGDD1 Diesel Generator Centrol Panel Termination Connection

Inspection and Repair.

88-AXGN1 Service Water Valve SW-V18 Replacement of Valve Actuator

Grease.

88-BFMA1 Replacement of Emergency Control Room Ventilation Fan Motor  !

Bearings.

89-AAWJ1 RSCS Card Inspection.

89-AfiIR1 Diesel Generator Building Basement Fire Retardant Cable

Coatings. ]

89-ADKE1 Diesel Generator No. 1, No. 7 Cylinder Valve Cover Gasket

Replacement.

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89-AFQC1 HPCI Injection Valve Testing.

89-DBF011 Breaker Compartment Inspection for 2-E11-F016A.

No violations or deviations were identified.

3. Surveillance Observation (61726)

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The inspectors observed surveillance testing required by Technical l

Specifications. Through observation, interviews, and record review, the i

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inspectors verified that: tests conformed to Technical Specification

requirements; administrative controls were followed; personnel were l

qualified; instrumentation was calibra;ed; and data was accurate and l

complete. The inspectors independently verified selected test results and I

proper return to service of equipment.

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The inspectors witnessed / reviewed portions of the following test

activities:

1MST-BATT14W Batteries, Spare, Weekly Operability Test.

IMST-PCIS24M PCIS High Condenser Pressure Trip Unit Channel Calibration.

2MST-APRM21Q APRM A and LPRM Group A Channel Calibration Functional

Test.

2MST-RHR27R RHR and CS Time Delay Relays Channel Calibration.

OI-3.1- Unit 2 C0 Daily Surveillance' Requirements.

PT-14.1.29 CRD System Charging Water Check Valve C11/C12-115,

Operability Test.

SRM Channel Functional Test Adequacy

AsL detailed' in inspection rsport 89-02, the inspector' questioned the

adequacy Lof the licensee's channel functional test performed on the SRMs-

prior to core alterations. Specifically, the inspector questioned why the

licensee's ' test did not detect a preamplifier problem on one SRM and a

control room-indicator problem on another SRM which occurred shortly after

commencing core load.

Channel Functional Test is defined in the Technical Specificai"sns as "the' 1

injection of a simulated signal into the channel as close to the primary

sensor as practicable to verify OPERABILITY, including alarm and/or trip

functions." The- licensee used 1/2 MST-SRM11W, SRM Channel Functional

Test, to meet this requirement. In the test, a square wave output is

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supplied from a ' function generator to the SRM input signal cable at the

SRM drawer. A counter is also connected to the drawer to measure the-

count rate. The frequency of the function generator is varied to

obtain the necessary count rates to check the alarm and trip functions of

the SRM. The associated count rate for the alarm and trip function is  !

measured and recorded from the counter.

With this test configuration, the problems with the preamplifier and the i

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control room log count rate meter would not be detected. However, the

channel functional test does comply with the Technical Specification

requirements. A ~ simulated signal is inserted into the channel and- the

alarm and trip functions are verified. The preamplifier and log rate

count meter are verified on another surveillance test which is verified to

be current prior to core alterations. Also, after loading fuel around the

SRMs to establi sh sufficient' count rate, the licensee checks the

discrimination circuitry and high voltage power supply. The licensee has

agreed, however, to perform a two point check of their control room log

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l rate count meter during their channel functional test. The test signal

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will be supplied from a function generator and will check two points to

. ensure that the -control room indicator is' tracking properly. The' .

inspectors had no further questions concerning this issue.

No violations.or deviations were identified.

4. Operational Safety Verification (71707)

The inspectors verified that Unit I and Unit 2 were operated in compliance

with Technical Specifications and other regulatory requirements by direct

observation of activities, facility tours, discussions with personnel,

reviewing of records and independent verification of safety system status.

The' inspectors verified that control room manning requirements of

10 CFR 50.54 and the Technical Specif. cations were met. Control operator,

shift supervisor, clearance, STA, daily and standing instructions, and

jumper / bypass logs were reviewed to. obtain .information concerning-

operating trends and out of service safety systems to- ensure that there

were no conflicts with Technical Specification Limiting. Conditions for

Operations. Direct observations were conducted of control room panels,

instrumentation, and recorder traces important to safety in order to

verify operability and that operating parameters were within -Technical

Specification limits. The inspectors observed shift turnovers to verify

that continuity of system status was maintained. The inspectors also

verified the status of selected control room annunciators.

Operability of a selected Engineered Safety Feature division was verified

weekly by ensuring that: each accessible valve in the flow path was in

its correct position; each power supply and breaker was closed .for

components that must activate upon initiation signal; the RHR subsystem

cross-tie valve for each unit was closed with the power' removed from the

valve operator; there was no leakage of major components; there was proper

lubrication and cooling water availabie; and a condition did not exist

which might prevent fulfillment of the system's functional requirements.

Instrumentation essential to system actuation or performance was verified

operable by observing on-scale indication and proper instrument valve

lineup, if accessible.

Tha inspectors verified that the licensee's health physics

poiicies/ procedures were followed. This included observation of HP

practices and a review of area surveys, radiation work permits, postings,

and instrument calibration.

The inspectors verified that; the security organization was properly I

manned and security personnel were capable of performing their assigned

functions; persons and packages were checked prior to entry into the

'PA; vehicles were properly authorized, searched and escorted within the

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! PA; persons within the PA displayed photo identification badges; personnel

in vital areas were authorized; and effective compensatory measures were

employed when required.

i The inspectors also observed plant housekeeping controls, verified

l position of certain containment isolation valves, checked several

clearances, and verified the operability of onsite and offsite emergency  !

power sources.

a. Shutdown Margin and Core Alteration Requirements l

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During a tour of the control room, the inspectors noted that the

licensee was removing Unit 1 control rods one at a time in order to 4

rebuild the associated control rod drive. Technical Specification 3.9.10.1, states the requirements that the licensee must meet. to

remove a single control rod evolution. Some of the requirements are:

SRMs are operable per TS 3.9.2. '

Shutdown margin specified in TS 3.1.1 satisfied. l

All other rods are inserted or have adjacent fuel removed.

Surrounding rods in a 5 x 5 matrix electrically disarmed.

The inspector questioned whether the SDM requirements were satisfied

since the core had been recently refueled and no SDM demonstration

specified by TS 3.1.1 had been performed. The licensee stated that

the SDM requirements were satisfied by analytical means and referenced

their Cycle 7 Core Management Report dated January 3, 1989, which 1

calculated a SDM of 1.89% delta K/K. The licensee did suspend all

further rod withdrawal until the question was resolved.

The inspectors examined Technical Specifications of other BWR

facilities and discussed the SDM requirement and core alterations

definition with regional and headquarters personnel. The inspectors

determined that NRC has accepted a calculation of SDM as an adequate

means of determining SDM at other facilities under certain

circumstances. However, the inspectors could find no information to

support the licensee's interpretation of core alterations.

During the inspection, the inspectors learned that the licensee did

not consider the insertion or withdrawal of control rods by their

normal means as a core alteration. Technical Specifications states

that " CORE ALTERATION shall be the addition, removal, relocation, or

movement of fuel, sources, incore instruments, or reactivity controls

in the reactor core with the vessel head removed and fuel in the

vessel. Suspension of CORE ALTERATIONS shall not preclude completion

of the movement of a component to a safe, conservative location."

The licensee felt that their definition was justified since the

original Unit 2 Technical Specifications specifically stated that  ;

movement of control rods by normal means was not a core alteration.

Clearly, the current Technical Specifications have no such provision.

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The inspector found that no t tolation of Technical Specifications

occurred as a result of the licensee's incorrect definition of core

alterations. The inspector examined the time pe.riod .that the

shorting links were ~ installed during this reporting period. -

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f: inspector. noted - that, during this time, control rods were being

. withdrawn, their: respective control ' rod drive removed, rebuilt and -

reinserted, and the rod was timed to verify proper operation. These

actions were performed in accordance with procedure 0WP 7/1, Rev. 3,

Control Rod Drive Mechanism Removal With Fuel.in Vessel, and met ~the.

requirements of.TS 3.9.10.1. The inspector found no cases where the-

licensee violated TS 3.9.2 governing core alterations. during this

reporting. period as a result of their definition of core alterations.

.The licensee: plans to submit a TS amendment request to clarify the

definition of core ' alterations, and the SDM requirements. The

licensee will also submit a letter to NRR. explaining their position

on SDM and .the' adequacy of a calculation to' satisfy TS requirements

.for single or multiple control rod withdrawal and removal. This will

be an Inspector Followup Item: Submission and Approval of Clarifi-

cation of SDM and Core Alterations Amendment ' Request, (325/89-05-04

and 324/89-05-04).

b. Undercharged Fire Extinguishers

The inspector informed the control room of two fire extinguishers

that were inadequately ' charged on February 27, 1989. The two dry

chemical fire extinguishers were located on elevation 23' of the

Control Building, in the Unit 2 cable spreading room at fire

extinguisher station CB-2-2, and in the ' Unit 2 Reactor Building on

elevation - 80', west, at fire extinguisher station RX-2-26. On

March 8, 1989, the inspector found the undercharged extinguishers

still in place., Additionally, the inspector noted that the

extinguisher in the Unit 2 cable spreading room, according to the

inspection tag on the extinguisher, was inspected on March 8,1989,

and found to be acceptable in its' current under pressurized

condition.

Surveillance procedure OPT-34.11.2.1, Portable Fi re Extinguisher

Inspection . Reactor Building 1 and 2, Revision 6, section 6,

acceptance criteria 6.0.1.7 requires, for hand held stored pressure

dry chemical extinguishers, that the pressure gauge indicator must

fall within the acceptable range and, for those extinguishers that do

not meet this criteria, that they be replaced. The licensee did not

fully implement the requirements of this procedure and, therefore,

this is identified as a Violation: Inadequate Surveillance of Stored

Pressure Dry Chemical Fire Extinguishers (324/89-05-03).

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The licensee replaced the extinguishers on March 8, 1989.

c. RHR Valve Not Adequately Controlled

During a walkdown of the -17' elevation of the Unit 2 Reactor

' Building on March'14, 1989, the' inspector,1at 11:45 a.m., noted that'

-the.RHR pump D minimum flow isolation valve E11-F018D had the locking

chain and locking seal removed for maintenance without a clearance

being issued. No work was:in progress and the . work, replacement. of

the handwheel, appeared complete. The inspector. notified the control

room that the valve should be locked open.

Since the valve was not under a clearance and was not in the locked

open position required by the system operating procedure, the

position of.this valve should be controlled under 01-13, Revision.29,

Valve and Electrical Lineup Administrative. Controls. The shift .

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foreman -indicated that a valve lineup exception form was not

initiated as required by 01-13, section 4.8.3. The licensee

subsequently locked the valve in the open position. This is

identified as a Violation: Failure to Complete Valve / Breaker

Exception Form for an Unlocked Valve (324/89-05-02).

This violation meets the criteria specified in Section V of the NRC

Enforcement Policy for not issuing a Notice of Violation and is not

' cited.

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Two violations were identified.

5. Engineered Safety Feature System Walkdown (71710)

a. Duplex Strainer Position

During a walkdown of the Emergency Diesel Generator fuel oil system, ,

the inspector found the selecting lever on fuel oil discharge duplex

strainer mispositioned. The selecting lever can be placed in one of

three positions; to place either strainer element in service or to

place both in service. Interruption of flow is not possible,

however, by use of the selecting lever alone. The inspector found j

both elements in service, which defeats the purpose of a duplex j

strainer. No . element is kept clean to permit cleaning of a fouled i

element. With both elements in service, both would become fouled and -i

interruption of flow would be necessary to clean the strainer and {

return it to service. )

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The inspector notified the licensee of this condition. The licensee

agreed that a single strainer element should be in service and

returned the duplex strainer to the correct position. The licensee

could not determine when the incorrect lineup was made. This

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condition had no effect on EDG operability since the strainers were

not fouled. The inspector verified correct strainer alignment on the

remaining EDGs. The licensee determined that a misaligned strainer

could occur elsewhere in the plant because these strainer levers are

not identified on system drawings or by tagging. The licensee

initiated Surveillance Field Report 89-010 to address this concern.

The inspectors will review the licensee's actions during future

routine inspections.

b. Core Spray System Walkdown

The inspectors conducted a detailed assessment of the Unit 1 and

Unit 2 Core Spray Systems. The assessment included a review of

outstanding work orders, plant walkdowns to verify valve positions

and material conditions, and a check of selected core spray

surveillance procedures to determine their adequacy.

Physical verification of local and remote valve positions revealed no

discrepancies with actual position versus the required valve position

operating procedure valve lineup. However,'a review of the operating

system valve lineup for the Unit 2 A loop, OP-18, Revision 35, showed

three valves in a different position than shown on the P&ID, D-02524,

Sheet 2, Revision 22. The discrepancies are shown below:

E21-V4 indicates closed on P&ID, open on OP-18 valve lineup.

E21-V72 and E21-V81, indicate open on P&ID, closed on OP-18

valve lineup.

Physical inspection of the core spray systems revealed numerous

material deficiencies. None of the items found by the inspector

posed an operability concern. However, these type of items should be

detected and corrected by existing licensee programs. Examples of

items found by the inspector for which no existing trouble ticket or

work order could be found include:

Fluid leaking from low pressure vent fitting from

2-E21-FS-N006A.

Small grease leak from 2-E21-F031A, F031B, and 1-E21-F031B motor

actuators.

2-E21-F030 leaking.

Pipe caps missing f rom 2-E21-IV-783, IV-728, IV-726, IV-781,

F0218, V12, V11.

Junction box located behind pump 2A not secured (screws not

tightened) and upper conduit fitting taped to junction box.

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2-E21-V13 mi ssing handwh'e el .

Grease leaking from.1-E21-F001A.

Packing _ leak from 1-E21-F004B.

Grease ' dripping from motor T ' drain for 1-E21-F004B, _ and

2-E21-F0018.

Small oil leak at the bottom fill connection'for all four pumps.

These and other discrepancies were discussed with the system et.gineer.

The system engineer inspected the items 'and initiated work requests

as necessary to correct the discrepancies.

The licensee continues to develop the system engineers and organiza-

tional changes are. still in progress. Based on a comparison of the

Core Spray inspection and the RHR inspection in November, 1988, no

changes have occurred relative to system conditions. The inspectors

' will continue to inspect safety systems to monitor ' the licensee's

progress.

The inspector also checked PT-7.1.8, . Core Spray System Component

Test, - to determine its adequacy. The inspector noted that ' the 4

minimum flow valve, F031A(B), a valve in the flow path that is not 1

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locked, sealed, or otherwise secured in position, is not checked in.

its . proper position as required by TS 4.5.3.1.6.2. This valve is

normally open during no flow or low flow conditions and shuts when

core spray flow reaches a -specified value. The licensee stated that

this valve is not included in the PT because the position noted

during standby operati.on (0 pen) differs from the valve ' position i

expected when the core spray system operates! (Closed). When core

spray is injecting to the vessel, the minimum flow valve is a flow-

path boundary valve. The licensee also stated that the valve

position indicator on the RTBG is checked during shift turnover. The

inspector concluded that this valve position should - be checked as

part of the monthly PT. The issue of what constitutes a flow path

valve was raised in inspection report 88-38 and resulted in URI 325,

324/88-38-02. This item will be referred to the Region /NRR for

further clarification. This issue, the requirement to check the

position of the F031A(B) during the monthly PT, will be included with

the previous unresolved item.

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No violations or' deviations were identified.

6. Onsite Review of Licensee Event Reports (92700)

The below listed LERs were reviewed to verify that the information

provided met NRC reporting requirements. The verification included

adequacy of event description and corrective action taken or planned,

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existence of potential generic problems, and the relative safety

significance of the event. Onsite inspections were performed and

concluded that necessary corrective actions have been taken in accordance

with existing requirements, license conditions, and commitments.

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(CLOSED) LER 1-88-07, Primary Containment Group 1 Isolation Following

Reset of Main Turbine Trip Signal. The licensee revised Operating

Procedures 1-0P-26 and 2-0P-26, Turbine Operating Procedure, to require

that the "All Valves Closed" and the " Emergency Trip Reset" push buttons

be pushed and held until the mechanical and emergency reset lights come

on. This prccedural action should preclude the changing of the main

turbine speed logic selection from " Valves Closed" to "1800 RPM" whenever

the main turbine trip signal is reset. The inspector reviewed the

licensee's corrective ' actions associated with this event and found them

appropriate. 4

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(CLOSED) LER 2-87-10, Inoperability of Reactor Building Fire Hose Station  !

2-RB-23 Resulting from Personnel Error During/Following Fire Drill. The

inspector reviewed the licensee's corrective actions associated with this

event. The licensee revised operating instruction OI-36, Shift Fire

Drills, to require that the equipment utilized during the drill be

identified on the drill evaluation sheet and verified that the equipment

is restored to an operable status. In addition, real time training on

this event was conducted for the radwaste/ fire protection operating

shifts. The inspector verified 0I-36 had been appropriately revised and

that the training was conducted as a part of the fifth quarter fire

brigade training session, course No. 88-1-5, completed on February 15,

1988. Based on the inspector's review of this event and the licensee's

corrective actions, the inspector found the licensee's response

satisfactory.

(CLOSED) LER 2-88-07, Pinhole Leaks and Linear Indications in the Insert  ;

and Withdraw Lines of Unit 2 Control Rod Drives. The licensee, during the

Unit 21988 refueling outage, conducted a visual and liquid penetrant

inspection of the control rod insert / withdraw lines. The licensee found

pinhole and linear indications on 21 lines. The licensee replaced

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sections of 11 withdraw and 4 insert lines and performed a base metal

repair to one insert line. The remaining seven lines with indications

were evaluated and found acceptable by the licensee per the guidance of 4

ASME, Section X1 requirements. The licensee performed the inspection and  !

repairs under plant modification PM-87-128, Unit 2 Refueling Outage Weld l

Overlays, Field Revisions 30, 31, 32, 35 and 39. In addition, the

licensee inspected the withdraw and insert CRD lines on Unit I under 1

PM-88-040, CRD Pipe Repairs. No unacceptable indications were identified  !

using visual and liquid penetrant inspection techniques. The inspector j

reviewed the licensre's corrective actions associated with the repairs

made on Unit 2 and the results of the CRD line inspection conducted on

Unit 1 and found them acceptable. .

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(CLOSED) LER 2-88-12, . Inability of High Pressure Coolant Injection System

Auxiliary 011 Pump Motor Termination Splices to Meet Environmental

Qualification Criteria. The inspector reviewed the documentation package

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and other inspection reports' dealing with the :HPCI Auxiliary 011 Pump

Mctor Splices. Previous insoection in this . area are documented in

inspection reports 88-24 and 88-39. Based on these previous inspections

and the information provided in the- LER, the inspector had ro further

questions.

No~ violations or deviations were identified.

7. In Office Licensee Event Report Review (90712)

The below listed LER was reviewed to verify that the information provided

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met NRC reporting requirements. The verification included adequacy of

event . description and corrective action taken or planned, existence of

potential generic problems, and the relative safety significance of the

event.

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(CLOSED) LER 1-88-21, Primary Containment Group 6 Isolation, Reactor i

Building Ventilation Isolation- and Standby Gas Treatment System

Auto-Starting During Cancellation of 48 VDC Battery Clearance.

No violations or deviations were identified.

8. TI 2515/100 (25020)

(OPEN) TI 2515/100, Proper Receipt, Storage and Handling of Emergency

Diesel Generator Fue, 011.

Events at other operating reactor sites involving problems' with DG fuel

oil and fuel oil systems prompted the NRC to issue the above Temporary

Instruction. This TI provides inspection guidance to NRC . inspectors to

evaluate the likelihood of similar events occurring at individual reactor

sites. The inspector conducted a portion of this TI during this reporting

period. This inspection consisted of collecting specific information

regarding the licensee's diesel fuel oil system with emphasis on fuel oil

sampling and analysis. The inspector noted discrepancies between NRC

Regulatory Guide 1.137, Revision 1, Fuel Oil Systems for Standby Diesel

Generators, an FSAR commitment, and actual programs and practices of the

licensee. For example, the licensee is not cleaning and inspecting all

fuel oil storage tanks at a 10 year minimum interval per Regulatory

Guide 1.137. These discrepancies were also noted by the licensee's site

QA/QC and are being dispositioned in accordance with the licensee's-QA/QC

program. None of these discrepancies appear to affect the operability of

the Emergency Diesel Generators. However, the inspectors will monitor the

licensee's action to ensure all issues are properly resolved.

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The inspector also noted a problem with a fuel oil system strainer that

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may be generic to many strainers / filters at the site. This is. discussed '

in detail in paragraph'5.a of this report.

No violations or deviations were identified.

9. TI.2515/99 (25599)

(CLOSED) TI 2515/99, Implementation of Requested Actions of NRC

Bulletin 88-07, Power Oscillations in Boiling Water Reactors.

The Bulletin describes a double recirculation pump trip event at 'LaSalle

Unit 2 where significant thermal-hydraulic instabilities occurred in the

reactor. . After the recirculation pumps tripped, feedwater heating

automatically isolated and core flow was due to natural circulation.

Under those power to flow conditions, peak-to peak oscillations were from

. 25?; to 50?4 power every two to three seconds as indicated on the. Average

Power Range Monitors. Seven minutes after the dual pump trip, the unit

scrammed automatically on high neutron flux. The Bulletin - and its

supplement requests BWR licensees, including Brunswick, to take certain

actions in response to the LaSalle event.

The inspector interviewed personnel, reviewed procedures and training

materials, and examined instrumentation ' to verify that the licensee.

completed the committed actions from the Bulletin.

a. Briefing on LaSalle Event

The inspector interviewed 12 operations personnel (SR0s, R0s, STA),

about the LaSalle event. Twenty-five percent of the operators

interviewed recalled. few event details. All operators interviewed

recalled the new procedural required actions for thermal-hydraulic

instability.

b. Procedure Changes

l The inspector verified that the licensee revi scri the appropriate

procedures to:

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Require a manual scram if both recirculation pumps trip when

the mode switch is in RUN (A0P-4.3, Rev. 8, February 6,1989,

Recirculation Pump Trip and Others).

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Require a manual scram, if region A of the power to flow map,

was entered.

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Require a manual scram if indications of instability occur.

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Identify indications of thermal-hydraulic instability - 10% peak

to peak APRM oscillations or LPRM upscale-downscale alarms. I

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The inspector reviewed . the below listed procedures, which also

.contain revised-guidance per above, for thermal-hydraulic instability:

0-A0P-4.0,' Rev. 6, Recirculation Flow Control Failure - Decreasing

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Flow

0-A0P-4.1, Rev. 4, Recirculation Flow Control. Failure - Increasing

Flow

.1/2-0P-02, Rev. 17 & 62, Reactor Recirculat' ion System Operating.

Procedure

GP-04', Rev. 14, Increasing. Turbine Load to Rated Power

GP-05, Rev. 30, Unit Shutdown

1-APP-A-06, Rev. 6,' Annunciator Response Procedure

2-APP-A-06, Rev. 7, Annunciator Response Procedure

The inspector.noted these problems:

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In the above annunciator procedures, window 1-7, LPRM Downscale,

requires a reactor scram if power is i 15%. This criterion

differs from the 10% peak to peak ( Sis) interim , corrective

actions published by.GE. All other procedures used the 10f, peak

-to peak criterion as required.

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During a procedure walk through using A0P-4.3 with a control

operar.or, the inspector noted.that the procedure caution refers

to the 8094 rod line but the power to flow map with the rod line

is not included with the procedure.

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No guidance for using Select Rod Insert on Unit 2 was provided i

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to the operators, either in procedures or training. The . SRI

button allows, on Unit 2 only, the operator to scram

pre-determined rods to rapidly reduce power. A0P-4.3 instructs

the operator to use SRI if above 5094 power, if desired. 1

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Most operators interviewed did not completely recall the pro-

hibitions in OP-2 not to intentionally enter thermal-hydraulic j

instability regions A&B, J

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1/2-APP-A-06, window 1-7, refers the operator to Technical i

Specifications, but not the AOPs, which require operator actions

sooner than TS.

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c. Instrumentation

The licensee verified that'LPRM/APRM instrumentation had no filtering

that could mask thermal-hydraulic instabilities. All APRM chart

recorders in the control room were checked by the licensee to verify.

.that the full scale deflection setting was one second. Maintenance

did find one recorder set at 5 second ' full scale deflection and

corrected it. The inspector reviewed the procedure . revision request-

88-2094 for new procedure OPIC-UR008, which will incorporate . the

maintenance requirement to verify the setting of recorder response

time.

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The licensee identified no deficiencies- in instrumentation that-

required procedural. compensation.

d. Technical Specifications

The ' licensee addressed thermal-hydraulic instability in TS .3.4.1.1

through amendments 114. and 142.-approved December 30, 1987. Those

amendments incorporated the recommendations of GE Service Information

Letter SIL-380, Rev. 1, dated February 10,.1984. Current procedures.

are more restrictive than the TS, thus the procedures are consistent-

with TS'.

,e. Training Programs

The licensee has integrated thermal-hydraulic instability and the

LaSalle event into their licensed operator training program. The

inspector reviewed updated training materials and observed a

simulator exercise to verify implementation. The simulator staff

demonstrated their simulation of instability using their current BWR

model.during a dual recirculation pump trip. LPRM indication did not

show the swings as soon as expected. APRM response was all in unison

and the indicators moved in a jerky fashion. In spite of the

indi. cation-problems, the inspector believes that the general behavior

of the reactor during conditions of instability was reasonably

demonstrated to the operators. The licensee does not . routinely

demonstrate instability to all operators during training. No

specific training syllabus requires simulation to the operators of

instability. under 2 pump, single pump, and natural circulation

conditions.

The inspector concluded that the licensee's response to the bulletin was

sati sf actory. However, the problems found by the inspector require

resolution by the licensee.

No violations or deviations were identified.

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10. Installation and Testing of Modifications (37828)

The licensee is currently implementing on Unit 1 a HPCI Reliability

Improvement Plant Modification, PM-88-051. The purpose of this

modification is to improve system reliability by: (1) the addition of an

oil bypass line around the Woodward EGR Actuator; (2) rerouting tubing

between the Woodward EGR Actuator and the remote servo; (3) deletion of

the opening rate control valve and bypass tubing on the HPCI Turbine Stop

Valve (E51-V8), and; (4) the addition of a 10 second time delay to the low

suction pressure pump trip.

The EGR bypass portion of this modification allows hydraulic oil pressure

developed from the auxiliary oil pump to move the control valve prior to

HPCI turbine startup. This, in conjunction with a reduced idle voltage

setting on the ramp generator signal converter, will allow the control

valve to open, then partially close prior to the opening of the stop

valve. Thus, this portion of the modification, along with the rerouting ,

of the tubing between the EGR actuator and the remote servo, will allow

the control valve to absorb the majority of the initial steam differential

pressure during the turbine quick start transient, reduce the initial

quick start turbine speed peak, and reduce the turbine exhaust line

pressure transient.

In addition, the licensee, under this modification, installed a 10 second

time delay relay in the low pressure pump suction logic. The intention of l

this delay is to prevent the pump from tripping due to pressure spikes

experienced during pump startup.

The licensee had confirmed that a low suction pressure trip was the cause

of a Unit 2 HPCI turbine trip on November 16, 1988. (see inspection

report 88-39), by conducting a full flow injection test on January 28,

1989. The test showed that a turbine low suction pressure alarm occurred

upon initial HPCI injection into the reactor vessel . Since the low

suction pressure trip had been previously bypassed, HPCI did not trip.

The. inspector reviewed the licensee's HPCI Reliability Improvement Plant

Modification, verified that the specified suction pressure trip time delay

relay was installed and wired into the HPCI logic in accordance with the

drawings and instructions provided in the modification package, and

confirmed that Acceptance Test No. 6 of the PM properly tested the changes

to the suction pressure trip logic. However, the inspector found that the

PM did not identify that u revision to MST-HPCI41R was required.

Currently MST-HPCI41R, Revision 5, Section 7.0, Step 7.8.124 tests the low

pressure suction trip function. However, the procedure was not revised to

test and calibrate the time delay function of the circuit. The licensee

said they will issue a field revision to the PM to include a draf t

revision to MST-HPCI41R.

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In addition, the licensee plans to perform a HPCI vessel injection test )

upon Unit I restart to evaluate the improvements in system reliability. l

The test results, the licensee's evaluation of these test results, and the i

overall assessment of the improvements in reliability will be evaluated

during a subsequent NRC inspection.

No violations or deviations were identified.

11. Drawing System Verification (71707) a

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The inspector conducted a review of the licensee's drawing control in the

control room arid Technical Support Center. The review attempted to

determine whether the licensee's drawing control efforts and programs

satisfactorily supported operators in a meaningful way. The inspection

included review and verification of a biased sample of drawings. The

inspector reviewed about 30 control room / operations aperture cards and

drawings, over 30 hard copy Unit 1 P& ids, and about 30 aperture cards in

the TSC. That review included verification of:

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Drawings present where distribution required.

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Drawing or aperture card legibility.

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Drawing list revision number matched drawing revision.

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No outstanding plant modifications against the drawing that made the

true status of a system difficult to determine.

The inspector found:

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Six missing drawings:

FP-55109, SH 1, 7, 8, Primary Containment Isolation System

elementary logic, located in the Operations aperture collection

in the back panel area of the control room. (Those same

drawings were in the control room aperture card file.)

FP-F5109, SH 12, PCIS elementary logic, located in the control

room aperture collection.

FP-50015 SH 1, Reactor Protection System, Unit 2, in the TSC.

D2020, SH 1, a Unit i hard copy drawing that was non-safety

related.

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FP-55109, SH 12, Operations - was difficult to read. (Note that the

j same sheet was missing from the control room.)

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D-7029, SH 2A, Unit 2 Instrument Air System P&ID, was still stamped

as requiring an update per PM-82-288FF. The inspector and an

operator walked through the drawing verification process using this

drawing. The drawing had already been updated and thus was

incorrectly marked.

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Two binders of hard copy P& ids were in the training library. The i

library becomes part of the TSC when an alert or higher is declared.

The Accident Assessment Team uses the information in the library to

evaluate an event. No uncontrolled documents should be available for

their use.

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Less than 1% of hard copy P& ids for Unit I had outstanding plant

modifications against them, thus requiring little additional work by

the operators.

Other observations:

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Per 0I-29, Operations Internal Audit, the licensee had just completed

(early 1989) a complete inventory of all control room operations

aperture cards and hard copy P& ids. Several lists of missing

drawings were sent to document control to complete the control room

collection. The licensee had not, by the close of the inspection,

verified whether the missing drawings identified by the inspector had

also been identified by the operations staff.

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The inspector also found that certain System Descriptions, or SDs,

had too many plant modifications not incorporated in the document.

Specifically, 50-18, Rev. 12, Core Spray System, had 8 plant

modifications not incorporated and SD-19, Rev. 12, HPCI System, had 5

plant modifications not incorporated. While the SDs are not

operating procedures, they do describe the system and are available

in the control room.

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The licensee corrects drawings using ENP-25, Rev. 6, Plant Drawing

Correction Procedure. The procedure controls any corrections to

drawings and requires a technical review of the drawing change with

project engineer approval. The appropriate engineering document for

safety reviews, an EER, is referenced in ENP-25.

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A previous audit by a third party found that as-built P& ids had not

been available to operations prior to, nor at the time the plant ]

modification was declared operable. It took about two weeks before 1

the updated aperture card was transmitted and made available to {

operations. QA issued SFR-88-042 on September 26, 1988, to track the l

resolution of the issue. By meno, on March 14, 1989, the licensee ]

intends to issue a second " original" aperture card drawing directly

to operations as an advance copy prior to declaration of operability.

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A P&ID comparison was made with the as-built plant condition as part.

of module 71710 (see paragraph 7 of this inspection report for Core

Spray and paragraph 6 in inspection report' 88-38 for RHR). The plant.

configuration matched the P& ids. However, as noted, the operating

procedure did not- match the P&ID indicated position , in rare

instances. The OP governs valve position at Brunswick. However, the

licensee still plans to correct the drawings.

The . inspectors concluded . that -the system for maintaining control room

drawings was satisfactory and usable.

No violations or deviations were identified.

12. Action on Previous Inspection Findings (92701) (92702)

a. (CLOSED) Violation 325/86-11-03 and 324/86-12-03, Failure to Install

Standby: Liquid Control Relief Valves With Discharge . Flooded. The

licensee. has co'mpleted a plant modification that installed vent

valves in the SLC relief valve discharge piping. Appropriate changes

were made to, operating procedure OP-5, SLC System, to provide for-

filling and venting the discharge piping. The inspector reviewed the

procedure and inspected the vent valves. They cbtermined to be y

adequate .to ensure' that the discharge piping is flooded to prevent i

boron precipitation within the valves, as . committed" to in FSAR  !

Section 9.3.4.2. Additionally, the licensee reviewed the i FSAR - to I

-ensure that plant procedures properly implement other =FSAR  ;

commitments for the SLC system. No additional discrepancies were .i

found. I

b. (CLOSED)- Violation (325/87-02-05 and 324/87-02-05), Failure to

Follow Maintenance Procedure When Installing Motor-0perated Valve

Anti-Rotation Devices. The inspector reviewed the results .of; the

licensee's anti-rotation device inspection which they . conducted .in'

response to this violation. This inspection was conducted under 4

Special . Procedure SP-87-002, . Inspection of Anchor Darling i

Anti-Rotation Devices. The licensee inspected 41 pressure seal-globe '

valves on Units 1 and 2. They found six valves with problems

associated with the installation / maintenance of the anti-rotation

device. Based on this review, the inspector determined that the 1

licensee's assessment as to the cause of this violation is correct. I

To prevent recurrence, the licensee revised the applicable procedure

to require that the lead mechanic sign off on the data sheet that the

work has been done properly. The inspector. reviewed corrective

procedure CM-VGB509, " Anchor Darling Pressure Seal Globe Valves",

Revision 0, dated September 27, 1988, and verified that section 7.9.2'

and 7.9.3 requires that the lead mechanic verify and sign off on the

data sheet that the anti-rotation device installation / maintenance

work activities were performed in accordance with the procedure.

This had also been inspected in inspection report 88-01.

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-c. (CLOSED)- Violation 325/88-14-03, ~ Failure to Perform 10 CFR 50.59

.

Evaluation on~ Service Water System. .The inspector. reviewed the

circumstances of the event and the licensee's response-to the. Notice

of.' Violation dated June 3,1988. The inspector verified that the

actions committed to by the licensee were' accomplished. The

inspector did note that the licensee missed' the commitment date of .

September 1,1988, for the. development 'of improved policy guidance

concerning conditions which constitute-potential deviations from the

facility as described in the FSAR. The. failure to meet this

commitment date was identified by .the licensee and result.ed in the

issuance.of an.NCR. The guidance was subsequently provided. in .a

memorandum dated September 7, 1988.'

d .' -(CLOSED) Unresolved- Item 325/87-36-05 and 324/87-37-05.- MSIV Pit

Openings Not on Q-List; Reactor Building EQ Envelope May be Affected.

This issue involved the potential for unsealed penetrations from'the'

MSIV pit'to the Reactor Building which, in the event of a MSLB in the .

pit, could possibly result.in higher peak temperatures and pressures l

in the. Reactor Building than previously. analyzed in the licensee's EQ ,

program. The largest of the penetrations, one ventilation exhaust .

line and two ventilation supply lin~ es, are designed to automatically

close in the event of a MSLB due to the pressure surge. However,

.these' dampers are not on the Q-List and, therefore, no credit can be

taken for them to perform their safety function.

The licensee performed an initial assessment - of the issue and

concluded that continued operation of both units was justified. This

conclusion was reached principally upon a comparison of the energy

releases into the general areas of the Reactor Building associated

with the previously analysed 10" HPCI DEGB versus that from the

various postulated short lived MSL critical crack / double ended ..

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guillotine scenarios. Subsequent to the initial assessment, the

licensee has performed additional analysis to show that the harsh

environment in the Reactor Building (excluding the MSIV pit) due to a ,

MSLB in the pit, is bounded by their previous Reactor Building j

analysis.

The additional analysis was presented in EER 89-0020, dated

January 24, 1989. The evaluation uses Reactor Building temperature /

pressure response data from UE&C Study Report 7992-303-S-W-048, dated

January 31, 1989. The report evaluated certain break sizes, time

response and damper positions, and the effect on the EQ envelope. '

The evaluation further states that a DEGB was not considered because

stress analysis results and the configuration of pipe whip restraints

preclude an assumption of a DEGB in the pit

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,The. pressure and ' temperature transients resulting from. each of the -

cases examined, show that'the licensee's previous Reactor Building-

environmental profile is still the limiting case for'all-' areas in the

Reactor Building except for: the MSIV. pit. 'The previous MSIV peak-

temperature was '297 degrees F. The 'new profile, based on case 1

above, . shows a peak temperature of ' 375 degrees. F. The licensee

evaluated this condition and concluded that this profile did not

, impact on the qualification of FQ equipment' installed in the MSIV

pit. This conclusion was based on the short lived nature of the

profile and that the EQ equipment located in the pit had been

previously -qualified for conditions ' representative of drywell

accident environments. Although the licensee considers this new

profile to be acceptable for existing equipment in the pit, they will

update their Reactor Building environmental report to snow these new

parameters.

e. (CLOSED) Unresolved Item 325/88-18-06 and 324/88-18-06, Control Room

Fire Detectors' Affect on CBEAF Operability. In response to the

inspection item, the licensee re-examined the operability' of CBEAF

with the loss of the automatic initiation function due to smoke

detection in the control room area. The licensee determined that the

smoke detection function was required for. the CBEAF system to be

considered operable. To clarify this information for the operators,

a Memorandum, BSEP/89-0110, was sent to the operations manager

explaining - the requirement for the . smoke detection function for

CBEAF. In addition, the licensee has modified PT-34.4.1.3 Control

Building Fire Detection Instrumentation Operability Test, .to

discontinue the use of the disconnect switch.

The inspector then reviewed completed copies of PT-34.4.1.3, to

determine if any violations of the plant's TS occurred. The time

that' the disconnect switch for the alarm panel was taken to

disconnect was not recorded during the performance of the test,

however, a caution was placed in the procedure which requires that

the system be aligned for normal operation if a break of greater than

15 minutes were to oct.ur during the performance of the test. Based

on this information and the inspector's observation during the

performance of the test, the TS time limit was not exceeded.

f. (OPEN) Unresolved Item 325/88-38-02 and 324/88-38-02, Failure to

Include All LPCI and Suppression Pool Cooling Flow Path Boundary

Valves in Their Surveillance Program. Further questions were raised

by the inspectors concerning flow path boundary valves and the

necessity to verify their valve position as part of the required

monthly surveillance check. Specifically, the core spray minimum

l flow valve, F031A/B, is not checked monthly for proper position, The

1 licensee has stated that this valve is not in the flow path when core

spray would be performina its safety function, namely, injecting

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water to the reactor vessel. This' item will remain unresolved- i

pending Region /NRR response to clari.fy requirement to check flow path

boundary valves. (See paragraph 5.b.)

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g. '(CLOSED) . Unresolved Item 325/89-02-03, Inadvertent Draining' of SLC

Tank. The inspector reviewed the' licensee's operability assessment

of the -SLC system during the inadvertent draining event. The

licensee concludedLin their evaluation that the SLC remained operable

during the' time that water Ws inadvertent 1y' drained from the SLC

tank through the F010/F014 valve bonnets. The licensee's conclu,lon

was based on the volume / concentration of the tank at the time of toe

event, the leak rate caused by the work, the injection requirements

of SLC had it been required, and the NPSH'available to'the SLC pumps.

The inspector had no other questions concerning the operability of

the SLC system.

, As noted in inspection report 89-02, the lean from the SLC tank

resulted from inadequate clearance / work control:,. The work involved

repairs to valves .the F010 and F014 which were contributing to

demineralized water leakage into the SLC tank. The-clearance which

established the work boundaries was not adequate for work on the F010

and F014 valves. Even if the work had been only on the F010 valve as

thought-by the SF authorizing the clearance, the boundary still would'

not .have been sufficient; however, no leakage would have occurred.

Maintenance personnel also removed the locking devices'-from both the

valves (with operation's permission), operated the' valves, and then

proceeded to loosen the bonnet bolts. The manipulation of valves by

maintenance personnel is permitted by- plant procedures proviaed the

~ valves are within the established work boundaries and the valves are

listed in Attachment C, BSEP. Clearance Tag Sheet. Attachment C of

clearance 1-189A,. which established the boundaries, did not list the

F010 or .the F014 as valves to be manipulated. The inspector also

noted that the maintenance personnel had accepted clearance 1-189A,

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signifying that they agreed the clearance was adequate for the work.

I The failure of plant personnel to follow plant procedures concerning

equipment clearances. is listed as a Violation: Failure to Follow

Equipment Clearance Procedures (325/89-05-01).

One violation was identified,

l 13. Exit Interview (30703)

The inspection scope and findings were summarized on March 15, 1989, with

those persons indicated in paragraph 1. The inspectors described the i

areas inspected and discussed in detail the inspection findings listed '

below and those addressed in the report summary. Dissenting comments were

l not received from-the licensee. Proprietary information is not contained

in this report.

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-Item Number Description / Reference Paragraph

325/89-05-01 VIOLATION - Failure to Follow Equipment

Clearance Procedures, (paragraph 12.g).

324/89-05-02 VIOLATION - Failure to Complete Valve / Breaker

Exception Form for an Unlocked Valve,

(paragraph 4.c).

324/89-05-03 ;IOLATION - Inadequate Surveillance of Stored

Pressure Dry Chemical Fire Extinguishers,

(paragraph 4.b).

325, 324/89-05-04 IFI - Submission and Approval of Clarification

of SDM and Core Alterations, (paragraph 4.a).

14. List of Abbreviations for Unit 1 and 2

AI Administrative; Instruction

A0 Auxiliary Operator

AOP Abnormal Operating Procedure

APRM Average Power Range Monitor

ASME American Society for Mechanical Engineers

BSEP Brunswick Steam Electric Plant

BWR Boiling Water Reactor

CBEAF Control Building Emergency Air Filtration

C0 Control Operator

CP Corrective Procedure

CR Control Room I

CRD Control Rod Drive

CS Core Spray

DEGB Double Ended Guillotine Break

DG Diesel' Generator

EDG Emergency Diesel Generator

EER Engineering Evaluation Report

ENP Engineering Procedure

EQ Environmental Qualification

ESF Engineered Safety Feature

F Degrees Fahrenheit

FSAR Final Safety Analysis Report

HP Health Physics

HPCI High Pressure Coolant Injection

I&C Instrumentation and Control

IFI Inspector Followup Item

IPBS Integrated Planning Budget System

LER Licensee Event Report

LPRM Local Power Range Monitor

MSIV Main Steam Isolation Valve

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MSLB Main Steamline Break-

MST' Maintenance Surveillance Test

.NCR. .Non-Conformance Report

NPSH- Net. Positive Suction Head-

'NRC Nuclear Regulatory Commission

0I Operating Instruction

0F Operating Procedure-

OWP Operations Work Permit

P&ID Piping & Instrumentation Data

PA Protected Area

PCIS Primary Containment Isolatien System

'PM . Plant Modification

PNSC  : Plant Nuclear Safety Committee

PT- ' Periodic Test

-QAL . Quality Assurance

QC- Quality Control

RHR Residual Heat Removal

RPS Reactor Protection System

RSCS Rod Sequence Contro1' System

'RTGB Reactor Turbine Gauge Board

SD System Description

SDM' _ Shutdown. Margin

SF Shift Foreman

SIL Service Information Letter

SLC Standby Liquid Control

SRI Select Rod Insert

SRM Source Range Monitor.

STAE Shift Technica1' Advisor

ETI . Temporary Instruction

TS Technical Specification

TSC . Technical Support Center

UF&C United Engineers & Constructors

.URI' Unresolved Item

VDC Volts Direct Current

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