ML20197H188

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Insp Repts 50-324/97-12 & 50-325/97-12 on 970928-1108. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20197H188
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 12/08/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20197H167 List:
References
50-324-97-12, 50-325-97-12, NUDOCS 9712310215
Download: ML20197H188 (54)


See also: IR 05000324/1997012

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' U, S.c NUCLEAR REGULATORY: COMMISSION:  !

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' Docket Nos': 50 325',-50 324:  ;^

License Nos: .-0PR 71, DPR-62

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LReport'No:- -50s325/97-12, 50-324/97-12

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-Licensee: -Carolina-Power =& Light.(CP&L)-

facility: Brunswick! Steam Electric Plant, Units 1-& 2 '

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, 'Locationi 8470 R1'ver Road'SE

Southport, NC- 28461 t

Dates: September 28 November 8, 1997 -

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Inspectorsi C. Patterson. Senior Resident-Inspector

E.-. Brown, Resident: Inspector-

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. E. Guthrie. Inspector in Training

J. Coley. Reactor Inspector (Section-M2.2-2.3)

J. Lenahan, Reactor.-Inspector (Section El.1-El.2) .;

F. Jape Reactor Inspector (Section M1.1)

< . Approved by: M.~ Shymlock, Chief. Projects Branch 4

Division of-Reactor Projects

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EXECUTIVE SUMMARY .

Brunswick Steam Electric Plant, Units 1 & 2

NRC Inspection Report 50-325/97-12. 50-324/97-12

This integrated inspection included aspects of licensee ope ations.

engineering, maintenance, and plant support. The report cc- rs a 6-week

period of resident inspection: in addition, it includes the results of an

engineering and in-service inspection by regiona! inst actors.

Operations

e lhe torus was found very clean and absent of foreign material during an

inspection prior to final torus closeout. (3ection 02.1)

. During an inspection, the drywell was founc to be free of foreign

material and ready for closecut. (Section 02.2)

. One example of a violation of the plant clearance procedure occurred

because the torus master clearance was not adequate to protect plant

personnel and equipment. (Section 02.3)

. Operator response to a plant transient resulting from a mechanical

problem on a reactor feed pump was good. (Section 02.4)

. An inadvertent diesel generator start occurred due to an operator error

while performing the procedure to restore system lineup. This was

because of a lack of understanding of the procedure step required

actions and the procedure step did not provide clear guidance.

(Section 04.1)

. A weakness was identified in ti.e direction provided for reactivity

manipulation cortrol. A Non-Cited Violation occurred due to the failure

to follow procedure for control rod movement. (Section 04.2)

. During removal of Reactor Feed Pumps from service as aart of a planned

shutdown, two recirculation aump runbacks occurred. )ending further

licensee investigation and NRC review this item is unresolved.

(Section 04.3)

. During maintenance on an electrical bus a diesel generator automatic

start circuit was defeated as part of a clearance without Operations

recognition. This is an unresolved item pending further review.

(Section 04.4)

. The restart affirmation conducted by the Plant Nuclear Safety Committee

was determined to be thorough and effective in the evaluation of the

overall site organization's readiness to restart Unit 2. (Section 07.1)

. Outage planning and control continues to be a strength. (Section 07.2)

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Maintenangg

. Maintenance activities were 3erformed satisfactorily. The inspector

noted good controls of houseceeping and good supervisor oversight of

work activities. (Section M1.1)

3 The conduct of testing during the PT-1/ .:.1 Single Rod Scram Insertion

Time testing was satisfactory, no discrepancies were noted by the

inspector. (Section M1.2)

  • The licensee took appropriate actions to ;ecure the surveillance test

when a discrepancy was identified, and they took the appropriate actions

to correct the procedures and drawings. (Section M1.3)

  • The failure to pro)erly develop and implement a clearance for the

isolation of the 23 recirculation pump motor resulted in racking out the

incorrect breaker and the replacement of the pump seals due to damage

from excessive temperatures. These were identified as two examples of a

clearance violation. Prior licensee review of operating experience for

torquing motor oil coolers was erroneous. (Section M2.1)

. In-vessel visual inspections on the Core Spray annulus piping and the

jet pump riser welds were performed by skillful vendor technicians.

Clarity of examination surface resolution, detail, and contrast of

indica.tions when using the GE color camera was excellent. Crack like

indications on the outside diameter surface of the piping would be

properly identified by the enhanced visual examinations observed

(Section M2.2).

  • Examination results from the 1996 and 1997 core shroud inspections

revealed very little crack growth for Weld H4. Weld H6B however, gave

conflicting information, crack depth was actually measured much less

during the 1997 examinations than during the 1996 examinations. The

licensee requested EPRI's help in determining the reason for these

examination differences (Section M2.3).

  • Maintenance measuring and test equiament located within the plant was

found properly labeled and within t1e current calibration interval.

Revie*' of several surveillance tests determined that the acceptance

criteria and frequency were within Technical Specification allowances.

(Section M6.1)

Enoineerino

. Two violations were identified. The licensee's progress in addressing

the previously identified deficiencies in the environmental

qualification (E0) program has required extensive NRC review. The

violations identified are indicative of a lack of progress and failure

to address the previously identified issue regarding inadequate

corrective actions. The licensee has also failed to document

operability of rquipment for which F0 is indeterminate. (Section El.1)

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  • The inspectors concluded that the modifications for USI A-46 were

adequately implemented in accordance with design requiremerits.

(Section El.2)

  • Excellent planning and decision making led to the successful completion

of a major phnt modification. This was a significant strength in

project management. (Section E2.1)

. An apparent corrective action violation occurred because no action was

taken once the drywell temperatures exceeded their limit bounded by an

engineering analysis. This problem occurred due to a known deficiency

that was allowed to exist. The deficiency was routinely red circled in

operations daily logs as an out-of-specification condition and above the

UFSAR limit. (Section E2.2)

  • Brunswick conducted activities, since original procedural approvals in

1974, which could have potentially exceeded the containment design

pressure in the event of a LOCA. The licensee had missed two

opportunities to recognize and take prompt action. A third opportunity

was initiated by the Resident Inspector, and only after questions from

the inspector did the licensee recognize the problem existed. Once the

licensee recognized the problem, corrective action was taken to correct

the problem via a procedural change. This issue was identified as the

second example of an apparent violation for failure to take corrective

action. (Section E2.3)

  • Inadecuate design review during laitial comaosition allowed errors to be

introcuced into the database which establisled the Option B minimum

critical power ratio limits. A violation was issued for the failure to

assure that corrective actions taken upon discovery of an error in the

minimum critical power ratios database precluded repetition.

(Section E3.1)

a The NAS assessments were adequate in evaluating the licensee's onsite

engineering pro 0 ram. However the results of the assessments showed that

the licensee's corrective actions in response to previously identified

assessment findings have been ineffective. An additional violation was

identified regarding failure to implement the corrective action program.

(Section E7.1)

  • During review of operating experience at another facility in response to

NRC Bulletin 96-02, the licensee determined that movement of the spent

fuel shipping cask with a non-single failure proof lift with the valve

box covers removed constituted an unreviewed safety question. The

failure to perform an adequate 10 CFR 50.59 screening to identify the

Unreviewed Safety Question was identified as an apparent violation.

(Section E8.1)

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Plant Suonort

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e Improved suaervisory oversight of radiation control practices was noted

during the Jnit 2 refueling outage. (Section RI.1)

  • Corrective actions for a generic event identified at another facility

were found to be incomplete. Security personnel failed to secure

protected area access on two occasions which could have resulted in the

entrance of an unauthorized individual into the protected area. These

failures were identified as a violation. (Section S4.1)

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Bmprt Details

Summary of Plant Status

Unit 1 operated continuously durir.g this period until November 5. 1997,

completing 364 days of operation before starting a mid-cycle outage to

remove leaking fuel assemblies. A reactor feed pump tri) occurred on

October 24. 1997, when the feed pump oil pumas failed. ollowing

repairs. the unit returned to full power on October 27. 1997. On

October 29, 1997, the IB reactor feed pump mechanical linkage failed

resulting in a loss of the feed pump and subsequent downpower maneuvers.

The linkage was repaired and the unit returned to full power. During

the planned downpower on November 5.1997, te recirculation pump

runbacks occurred while removing reactor feed pumps.

Unit 2 completed a refueling outage and the reactor was taken critical

on October 13, 1997. The scheduled outage work was essentially

completed on October 15. 1997. but synchronizing to the grid was delayed

due to a problem with a recirculation pump motor oil cooler. The unit

was taken to hot shutdown on October 16. 1997, for repair of motor oil

cooler leaks. However, cooling water flow was erroneously secured to

the shaft seal resulting in exceeding the temperature limit of the seal.

The unit was then taken to cold shutdown for seal replacement.

Following repairs. the unit was taken critical on October 21, 1997. and

synchronized to the grid on October 22, 1997, ending the refueling

outage in 39 days. A five percent power uprate was implemented on the

unit. At the end of the report period the unit had been on-line

continuously for 17 days.

The licensee in a letter to the NRC dated February 13, 1997. committed

to upgrade the mechanical vacuum pumps trip function to include a vacuum

pump trip from the main steam line radiation monitor prior to the next

startup. This modification was completed for Unit 2 during this

refueling outage. During the Unit 1 mid-cycle outage in November 1997.

the modification was also completed. This completed the commitment that

was made because of a concern about control room dose in the event of a

Rod Drop Accident. The inspector inspected the installation of this

modification and no prc'lems

a were identified.

Due to concerns about the control room dose, the licenset. imposed an

administrative limit on Iodine until a Technical Specification (TS)

amendment submitted was approved. The licensee made a procedure change

to Administrative Procedure 0Al-81. Wcter Chemistry Guidelines, setting

the limit at 0.1 microcurie per gram dose equivalent Iodine 131 compared

to the TS value of 0.2 microcurie per gram. Also, the licensee has been

providing weekly water chemistry data to NRR and the Resident Insp ator

for review. None of the data reviewed has exceeded the administrative

limit.

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Due to a reconstitution of- the Environmental'Oualification (E0) program

and items identified, there are-12 of 24 Justification's for Continued 3

0)eration (JCO) that~ remain open for both units. The following provides '

t1e status of the EQ JC0s and associated Engineering Service Requests

-(ESRs):

Closed

1) ESR 97-00087. E0 Type JC0 for Improperly Configured Conduit Seal.

2) ESR 97-00574. Greyboot Connectors.

3)' ESR 97-00329 (old ESR 96 00625). E0 Type JC0 for E0 Fuses Without

a Qualification Data Package (0DP).

4) f*:' 07-00289, Post Accident Sampling System (PASS) Valve Limit

bwitch Panel Wiring,

5) ESR 97-00238, JC0 for Standby Gas Treatment Motor Operated Valve

(MOV) Position Indicator Rheostat.

6) ESR 97-00534, GE EB-5 Type Terminal Strips.

7)- ESR 97-00513,- In-Board-Drywell Electrical-Penetrations.

8) ESR 97-00535. Target Rock-Solenoids TB Spray.

9) ESR 97-00449. Degraded Junction Boxes.

10) ESR 97-00250. Conduit Union in E0 Boundary.

11) ESR 97-00446, GE Radiation Detectors.

12) ESR 96-00503, Associated Circuit E0.

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13) ESR 96-00425. Evaluation of E0 sealants was initially closed by

the licensee but was reopened - closure date to be determined

(TBD).

14) ESR 97-00330 (old ESR 96-00501). Motor Control Center (MCC) E0 was

closed by the licensee, but was reopened - closure date TBD.

15) ESR 96-00426. Evaluation Quality class and E0 classification of

PASS valves was scheduled for completion June 6,1997. but closure

date is TBD.

16) ESR 97-00529. Failure of Unit 1 Drywell Motor, closure date TBD.

17) ESR 97-00523, High Pressure Coolant Injection (HPCI) Auxiliary 011

Pump Motor Unit 1, closure date TBD.

18) ESR 96-00587. PASS Valves, closure date TBD.

19) ESR 96-00627. ODP for Marathon 300 Terminal Blocks was scheduled

for completion December 31, 1997 but revised to August 1. 1997.

but closure date is ncw TBD.

20) ESR 97-00229. JC0 for GE Condition Report (CR) 151 B Terminal

Blocks was scheduled to be completed September 1. 1997 but

closure date is now TBD.

21) .ESR 97-00256. Main Steam Insulation Valve (MSIV) Hiller Actuator

JCO..was scheduled for completion September 2, 1997. but closure-

date is now TBD.

22). ESR 97-00343, Qualification of Kulka Model 600 Terminal Blocks was

scheduled for completion September 1. 1997, but closure date is

now TBD.

23) -ESR 97-00435. MCC Fittings, closure date TBD.

24) _ESR_97-00602, Soleno_id Valve Field Wiring, closure date TBD.

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In sumary, Unit 1 operated continuously during this report period until

a mid-cycle outage was started on November 5. 1997. Unit 2 completed- a

refueling outage and operated continuously once returned to service on

October 22, 1997 after a refueling outage. There are 12 outstanding

'JCOs in the E0 area for both units.

I. Operations

02 Operational Status of Facilities and Equipment

02.1 Torus Closecut Insoettion

a. Inspection Scoce (71707)

On September 29, 1997. the inspector inspected the Unit 2 torus in

preparation for torus closecut.

b. @servations and Findinas

The inspector toured the Unit 2 torus while it was dry and after

completion of work activities. The torus had been drained for

modification work to install new suction strainers for the core spray

(CS) system and residual heat removal (RHR) system. Each strainer

installation was inspected with emphasis on support clearances and

fastener attachments. No deficiencies were found.

The inspector also checked to see that all fcreign material had been

removed from the torus. The torus was completely dry and had been

recently vacuumed.- No foreign material was found. The torus was very

clean and no dust was present.

The inspector, with permission from the licensee, opened each torus to

drywell vacuum breaker and looked inside for any foreign material and

found none.

c. Conclusions

The torus was found very clean and absent of foreign material during an

inspection prior to final torus closecut.

02.2 Drywell Closecut Insoection

a. Inspection Scope (71707)

On October 12, 1997, the inspector inspected tne condition of Unit 2

drywell just prior to final closecut.

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b, Observations and Findinas

The inspector, along with the outage l manager, inspected all elevations

of the drywell. At the five foot ekvation the inspector looked inside

- each downcomer and found them free of any obstruction and foreign

material. The inspector observed that several pieces of grating were

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stored underneath the vessel and not tied down.

Each of the other elevations were generally clean with no foreign

material present. The inspector checked to see that junction boxes were

closed and sealed. Several safety relief valves were checked for proper

mechanical assembly and installation of-lock wires. No deficiencies

were noted.

Following the inspection the licensee determined that the loose grating

identified was properly secured. This was based on a review of the

acceleration valves and inertial forces. The storage requirements for

the grating were originally in Administrative' Instruction 0Al-105.

Under-vessel Ins)ection and Access Control, however, this procedure had

been deleted. T1e licensee issued a temporary revision to procedure

0Al-127. Primary Containment inspection and Closeout, to document this

inspection item.

c. Conclusions

During an inspection, the drywell was found to be free of foreign

material and ready for closeout.

02.3 Inadvertent Drainino of Water Into a Dry Torus

a. Insnection Scone (71707)

The inspector inspected the inadvertent draining of about 1000' gallons

of water into Unit 2 torus while in a dry condition. These occurred on

September 23 -1997, while work activities associated with the torus

suction strainer modification _we, a in progress.

b. Observations and Findinos

. While securing RHR from the shutdown cooling mode of operation in

accordance with plant procedures. water was introduced into the dry

torus:when the combined torus suction valve. 2-E11-F020A was opened.

This valve is normally opened providing the RHR pump suction path from

the torus except when closed for shutdown cooling operation. The

control room was notified that water was introduced into the torus and

the valve was closed. The licensee initiated CR 97-03292. Water in

Torus, to document this problem. The licensee conducted a Level 2 Root

Cause Review of the event.

The licensee's review determined that water trapped.between the combined

torus suction valve. 2-E11-F020A and the closed individual pump suction

valves. 2-E11-F004A and 2-E11-F004C. drained into the torus when the

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combined torus suction valve was opened. The torus master clearance.

2-97-555. used to isolate the torus used the indivi. dual pump suction

valves instead of-the combined torus suction valve because of planned

preventive maintenance on the valve. It was not recognized that the

time that the sequence of scheduling-activities would lead to'a

situation where water could be trapped between the valves.

No personnel safety problems or )ersonnel contamination events occurred

when water was introduced into tie torus. However, due to the fact that

-welding work was scheduled and being performed in the area. the

potential for a personnel safety risk was possible. Electrical power

cords welding supplies, and other tools were wetted. ,

Operating Instruction 001-01.09. Equipment Tagging, requires that

clearance activities be used to provide for the safety of personnel and

plant equipment during operation, maintenance, and modification

activities.

The licensee initiated clearance 2-97-01461 for valve 2-E11-F020A in the

closed position. Other corrective action included a review of other

potential areas where water could be introduced. The torus water was

drained. Any affected tools and equipment were replaced prior to work

re-start. This event was captured in the outage lessons-learned

database reviewed with clearance preparers and ) laced in operator

training. The licensee review of this event in t1e level 2 CR was

thorough,

TS 6.8.1 requires procedures for activities as equipment control covered

in Regulatory Guide (RG) 1.33. Plant Operating Instruction 00I-1.09.

Equipment Control, established requirement for equipment tagging to

protect personnel and plant equipment. This was the first example of a

violation against the plant clearance procedure. Clearance 2-97-00559,

was not adequate to protect )lant personnel and equipment. This

violation is identified as t1e first example of VIO 50-324/97-12-01.

Clearance Errors.

c. Conclusions

One example of a violaticn of the plant clearance procedure occurred

because the torus master clearance was not adequate to protect plant

personnel and equipment.

-02.4 Unit l~ Reactor Feed Pumo (RFP) Linkaoe

a. Insoection Scone (71707)

The-ins)ector reviewed the Unit 1 transient that occurred on October 29,

1997, w1en_the IB RFP. control linkage failed.

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b. Observations and Findinos

While Unit I was operating at 92 3ercent power, a. reactor vessel low

water level alarm was received. )lant operators promptly observed low

flow on the 1B RFP. To avoid a unit trip, power was reduced to 55

percent power by manually reducing recirculation pump speed which

stabilized the transient. Later, the licensee determined that the IB

RFP speed control linkage became disconnected resulting in the speed of

the pump reducing to an idle condition. This was slower than a normal

feed pump trip and thus, no alarms were received to indicate a problem

with the pump.

A lock nut on the feed pum) linkage was found to have come loose. The

linkage was repaired and t1e feed pump returned to service.

c. Conclusions

Operator response to a plant transient resulting from a mechanical

problem on a RFP was good.

04 Operator Knowledge and Performance

04.1 Inadvertent Diesel Generator (DG) Start

a. Inspection Scone (71707)

The inspector reviewed the cause of the number 3 DG start on October 10.

1997

b. Observations and Findinas

Following maintenance on the E3 and E7 buses, power was being restored

to the E3 4160 volt bus when the number 3 DG automatically started.

Operators were performing Operating Procedure 00P-50.1. Energizing 4160v

Buses. Procedure step 5.3.5 required that the operator ensure the DG

was in the Auto mode on Panel XU-2. The operator thought the only way

to ensure completion of this step was to verify proper control

indication lights were illuminated. The operator closed the switch for

the DG control panel. This activated the control power circuitry and

.the DG automatically started as designed, because the circuitry sensed a

de-energized emergency bus. An error occurred in manipulation of the

control power switch, since the procedure sequenced the switch to be

closed last in step 5.3.13. The operators immediately secured the

running DG. The licensee initiated CR 97-03072 to document the problem.

The inspector went to the Control Room after the inadvertent start and

reviewed the procedure with the Shift Superintendent. The inspector

also reviewed clearance 2-97-01281 for de-energizing the E3 bus. The

inspector questioned how the error was made when performing the

procedure. The procedure ste)s to close the control power switch were

performed.out of sequence. T1e procedure step did not provide clear

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guidance as to how to verify the diesel was in automatic without control

power available for indications.

c. Conclusions

The inspector concluded that an inadvertent diesel generator start

occurred due to an operator error while performing the procedure to

restore the system lineup. This was because of a lack of understanding

of the procedure step required actions and the procedure step did not

provide clear guidance.

04.2 Reactor Feed Pumo Trio

a. Insoection Scope (71707).

The inspector reviewed the operator response to a RFP trip that occurred

on Unit 1.

b. Observations and Findinas

On October 24, 1997, the IB RFP tripped due to a loss of oil pressure.

Unit 1 power decreased from 100 percent to 50 percent power following

the pump trip. Several hours earlier the running feed pump oil pump

tripped due to an electrical short. The standby oil pump was designated

to emergency use due to a high vibration condition. The standby pump

ran for several hours but -subsequently failed. The loss of both oil

pumps resulted in the IB RFP trip.

The feed pump trip occurred at 6:33 a.m. The inspector entered the

control room around 6 45 a.m. as part of the normal daily routine and

observed stable plant conditions.

Reactor water level had decreased to a level of 173 inches. The scram

setpoint was at 166 inches. A recirculation pump runback occurred as

designed. The unit entered region 'B' of the thermal hydraulic

instability region. The operators inserted control rods to exit the

region.

Following the transition, the licensee determined that three control

rods were driven to position 'O' instead of the specification position

'12', The licensee initiated CR 97-03833. Control Rod Pattern, to

document'this problem. A reactor engineer verified no thermal limits

were exceeded. Due to the leaking fuel in Unit 1. the licensee provided

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direction to the operator for power changes in Standing Instruction (SI)97-053. This SI provided direction for a rapid power reduction use

procedure OENP-24.0 Reactor Engineering Guidelines. Form 2. This

procedure was not followed when three control rods were driven from

position '24' to position 'O' instead of the required position '12'.

As part of the licensee's corrective action, the reactor operator was

removed from duty pending a review of this event. SI 97-067 was issued

October 24, 1997, which provided direction to use procodure OGP-12.

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Power Changes, for immediate power reductions. This procedure requires

that a second licensed operator or other qualified member of the '

technical staff shall monitor control rod movement and shall document

correct selection and placement of control rods on the procedure

controlling rod movement.

The inspector reviewed SI 97-053. SI 07-067. OENP-24.0, and 0GP-12. The

inspector notad that 0ENP-24.0 was a " Reference Use" procedure intended

for the reactt,r engincer's use. 0GP-12 was a " Continuous Use" procedure

intended for the control room o)eratcr's use. The direction given by SI

97-053 to use OENP 24.0. gave t1e operator latitude for control rod

manipaletion outside the normal operations procedure. This was

considered a weakness in direction provided for reactivity manipulation

control.

1he operator's failure to follow arocedure for moving control rods was a

violation of plant procedures. T11s non-repetitive, licensee identified

and corrected violation is being treated as a Non-Cited Violation,

consistent with Section VII.B.1 of the NRC Enforcement Policy. This

Non-Cited Violation (NCV) was identified as NCV 50-325/97-12-02. Control

Rod-Movement Error,

c. Conclusinns

The inspector concluded that a weakness in direction provided for

reactivity manipulation control. An NCV occurred due to the failure to

follow procedure for control rod movement.

04.3 Unit 1 Recirculation Pumo Runbacks

a. Insoection Scone (71707)

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The inspector reviewed the circumstances surrounding the November 5-6,

1997, recirculation pump runbacks. These events were captured in CR 97-

3917.1B RFP induced transients,

b. Observations and Findinas

On November 5. 1997, the licensee began a controlled shutdown for the

Unit 1 forced outage in order to replace leaking fuel bundles. At

11:54 p.m.. while at 65 percent, the licensee started removing the IB

RFP from service. While securing the pump, unexpected level transients

were observed. As a result, the licensee ceased actions to secure the

IB RFP and restored the IB RFP. Attempts to secure the 1A RFP resulted

in larger than expected level changes, reactor water level dropped below

182 inches and due to feedwater flow on one pump being less than 20

percent, a recirculation pump runback on the IB recirculation pump to

the 45 percent limiter occurred. As efforts continued to secure the 1A

pump at 12:02 a.m. on November 6. 1997, level transients were

encountered for a third time and both the 1A and IB recirculation pumps

- received a runt'ack to the 45 percent limiter. During both runbacks

Abnormal Operating Procedure 1A0P-4.0. Low Core Flow was entered. The 5

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percent buffer region was entered and exited in accordance with

procedures. Subsequently, no other transients or runbacks were-

encountered while removing the RFPs from service.

The licensee has preliminarily attributed the first runback to a

malfunction of the IB discharge check valve causing diversion of the IA-

RFP flow through the IB discharge valve to the main condenser. Pending

licensee completion of. the event investigation and further NRC review

this item is unresolved. This unresolved item is identified as URI

50-325/97-12-03, Recirculation Pump Runbacks.

In addition, a previous weakness in training and 3rocedural guidance for

removal of an RFP from service was discussed in NRC IR 97-02.

c. Conclusion

During removal of RFPs from service as aart of a planned shutdown, two

recirculation pump runbacks occurred. Pending further licensee

investigation and NRC review this item is unresolved.

04.4 Diesel Generator low Voltaae Auto Start Defeat 0d

a. Insnection Scone (71707)

The inspector reviewed the low voltage auto start feature being defeated

on the number 4 DG.

b Observations and Findinos

The ins)ector reviewed the operator logs dated October 11. 1997, and

found tie following. At approximately 6:15 a.m., clearance 2-97-01038

was processed on the 4.16KV bus 2C. This war. a planned maintenance

activity on the 2C bus. TS 3.8.1,1 was entered at this time as part cf

the planned maintenance activity. The logs stated that the TS action

statement required the offsite power sources be restored in 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

.At 6:47 a.m. the number 4 DG was aligned to provide power to the E4 bus

as part of the same planned maintenance activity on the 2C bus. Use of

the number 4 DG to supply power to the E4 bus was necessary because the

2C bus is the normal power supply to the E4 bus. Without the number 4

DG supplying power the E4 bus would have been inoper6ble.

The inspector determined, by reviewing CR 97-03683. that the operators,

subsequent to establishing the required plant lineup to perform the

maintenance on the 2C bus, questioned why the number 4 DG was operating

in a control room manual status instead of automatic on the isolated E4

bus. This question arose because a similar maintenance activity on the

20 bus had established a-lineup with the-number 3 DG in automatic.

- After investigation, by the operators, into why the diesels were in

different lineups for the same kind of maintenance activity, it was

determined that the clearance for the 2C bus had defeated the low

voltage auto start for the number 4 DG.

-

- . ._ _ _ _ _ _ _ _ _ . _ _

_. _ _ _ _ _ _ . _ _ . _ _ -

1

1

10

The. logs stated that at 8:35 a.m. the number 4 DG was declared .

i

xinoperable. The inspector determined; following discussion with the- i

licensee. that this was done because it is required by TS 3,0.3 action l

'

statement. The action statement requires that when the 4.16KV emergency

bus undervoltage relay is inoperable. then the diesel which supplies

that emergency bus.-must be declared inoperable. The operator logged at j

this time. 8:35 a.m., that TS 3.0.3 was entered because two offsite

power sources to E4 and the number 4 DG were' inoperable, which placed

the unit outside a condition addressed in TS 3.8.1.1.  ;

The inspector identified that the operators, to resolve the problem.

determined that the low voltage relay was disabled in a manner that i

could be prevented. The clearance was changed and the low voltage relay

was' restored at 9:45 a.m. The clearance originally chose terminal

points dt junctions before and after two parallel path relays. The  ;

wires were restored at those locations and then removed at the other i

relay in the parallel path circuit. thus restoring the low voltage relay

and providing a sufficient clearance condition to perform the

maintenance on the 2C bus. The operator logs stated that the number 4

DG was declared operable at 9:45 a.m. and that TS 3.0.3 was exited.

Following a review of the clearance 2-97-1038, the inspector noted that

in the special instruction.section, page three of the document, a

caution statement directed toward operations stated that three wire

lifts were necessary to perform the clearance. The caution statement

s)ecified that one of the wire lifts would prevent the DG from starting

w1en the emergency bus was de-energized. However, since the licensee

did not complete their root cause investigation at the conclusion of

this inspection report period, this is an unresolved item. URI 50-325 '

(324)/97-12-04 Diesel Generator Low Voltage Auto Start Defeated.

pending review of the completed investigation.

c. Conclusions

During maintenance on an electrical bus a diesel generator automatic

start circuit was defeated as part of a clearance without Operations

recognition. This is an unresolved item pending further review.

07 Quality Asst.rance in Operations

07.1 Startuo Plant Nuclear Safety Review Meetina

a. . Ins 9ection Scoce (71707)

The inspector observed startup assessment activities conducted in

accordance with Plant Programs OPLP-29. Self-Assessment for Readiness to

Startup Following an Outage.

b. Observations and Findinas

20n October 11. 1997. the ins)ector observed the Startup Plant Nuclear

Safety Committee (PNSC) for Jnit 2. The readiness of each organization

, . - - - --

11

to support restart activities was discussed by the PNSC and affirmed by

the appropriate supervisor. The affirmations observed by the inspector

were performed in accordance with Attachment 3 of OPLP-29. Areas

, addressed during the meeting included adequecy of stiffing and

housekeeping, completion of regulatory compliance items, and outstanding

engineering service requests. Any activities not ready for restart

where flagged as exceptions and a duration for resolution was discussed.

The meeting generated eight action items for completion. These items

-did not -include the OPLP-29 exception.

The inspector determined that the meeting was comprehensive and adequate

to assess restart readiness.

c. Conclusions

The restart affirmation conducted by the PNSC was determined to be

thorough and effective in the evaluation of the overall site

organization's readiness to restart Unit 2.

07.2 Outane Plannina

a. Insoection Scone (71707)

The inspector reviewed the control of Unit 2 outage activities.

b. Observations and Findinas

The planned work activities for the Unit 2 refueling outage were

completed without dif ficulty. This included completion of a major plant

modification as discussed in section E2.1. The planned 35 day outage

was completed in approximately 32-33 days. Com]letion of the outage was

delayed several days because of problems with t1e recirculation pump

motor oil cooler and shaft seals.

Contributing to this success was the 11censee's detailed and thorough

planning for the outage. Numerous milestones were reviewed prior to the

start of the outage. Lessons learned from previous outages were

formally incorporated into the outage planning. Once the outage

started, outages meetings were conducted twice a day with shift outages

managers. The licensee used a unified outage log to integrate all

important log entries into one document.

c. Conclusions

Outage planning and control continues to be a strength.

08 Hiscellaneous Operations Issues

08.1 (Onen) Violation VIO 50-325(324)/97-02-07: Failure to Initiate CR for

HPCI Valve Time Discrepancy

. __

12

This l item was inadvertently closed in 50 325(324)/97-09 and, remains

open pending completion of licensee corrective actions and further NRC

review.

11. Maintenance

M1 Conduct of Haintenance

Ml.1 Maintenance Proaram

a. Insoection Scone (62707)

The inspector reviewed / observed portions of the maintenance related work

and reviewed the associated documentation control rod drive (CRD)

rebuilding.

b. Observations and Findinos

The inspector observed that these activities were performed by personnel

who were experienced and knowledgeable of their assigned tasks.

Procedures were present at the work location and were being followed.

The procedure for rebuilding the control rod drives provided sufficient

detail and guidance for the intended activities. Activities were

properly authorized und coordinated with operations. Test and

maintenance equipment in use was calibrated, procedure prerequisites

were met, and replacement components were obtained through an acceptable

vendor.

The maintenance supervisor in ch_ of these safety related jobs was

observed frequently at the job lota , .. and aroviding good oversight of

work activities. Good control of area house (eeping was maintained

during the work. The inspector noted that when the old, replaced

components were removed from the CRD. they were immediately placed in a

shielded container to reduce the radiation level in the work area.

The rebuilt CRDs were stored in a container for installation in Unit 1

at a later date. Therefore the rebuilt CRDs were not leak tested at

this time. The licensee's plan is to leak test the drives shortly

before installation. The work activity was well controlled and

coordinated,

c. Conclusions

The inspector concluded that the maintenance activities were performed

satisfactorily. The inspector noted good controls of housekeeping and

good supervisor oversight of work activities.

. - .. - - -

1

13

M1.2 Control Rod Drive Scram Time Surveillance Testina (Unit 2)

al Insoection Scooe (61726)

The ins)ector observed the perforniance of Periodic Test PT-14.2.1. ,

Single Rod Scram Insertion Time 7esting,

b. Observations and Findinas

On October 23. 1997, the ins)ector observed the licensee perform

PT-14.2.1. The purpose of t11s test was to measure control rod scram

-insertion times on a single rod basis, following the Unit 2 Refueling

-Outage. Several TS requirements are verified by completion of the

surveillance.

The test evolution required personnel to perform portions of the testing

at three different locations. Auxiliary 0.perators were stationed at the

Hydraulic Control Units (HCU) in the Reactor Building, a Licensed

-Operator was stationed at the Reactor Protection System (RPS) scram test

panel, and the Reactor Operator was in the Control Room. The inspector

observed the conduct of the test from all three locations, observing

multiple control rods being tested at each location.

The inspector observed the Aux 111ary Operators in the Reactor Building

first. The Auxiliary Operators were dressed in full protective

clothing. in a contaminated area, while performing the surveillance.

-They were given direction by the Reactor Operator via hand held

communications. As the Auxiliary Operators received the next control

rod number to be tested they used good self checking practices to ensure

the correct HCU was located. The Auxiliary Operators were required to

operate the Charging Valve on each HCU and ensure proper nitrogen

accumulator pressures upon valve mani)ulction. Satisfactory

communications were used throughout t1e observed portion of the testing

evolution. Satisfactory independent verification was conducted for each

charging valve operation, also the verification check sheet was

initialed after each manipulation.

The inspector observed two operators at the RPS scram test panel. At

this panel the test switch is manipulated to cause individual scramming

of the control rods. The Reactor Operator directed the I.icensed-

Operator at the test panel, via the sound powered phone system, when to

, manipulate the test switch and when and where to move the test leads.

Satisfactory communications were used throughout the observed portion of

the evolution. Satisfactory continuous dual verification was performed

by both individuals at the RPS test Janel during the )ortion of the

testing' observed. -Adequate use of tle verification cleck sheet was

observed as the inspector noted that. contrary to the Auxiliary Operator

and the Reactor Operator, they were using a check mark'on the check

sheet vice double verification initials. The inspector observed testing

in the Control Room and noted satisfactory procedural compliance and

communications between the Senior Control Operator, the Reactor

Operator, and the Reactor. Engineer and, as stated previously, between

. .

. . .- . - - . ._- .

14

'the remote stations. The inspector noted when the test was complete

that. individuals performing activities-in the remote locations initialed

the master verification check sheet in the Control Room.

-

,

c. -Conclusiong

The conduct of testing during the PT-14.2.1 Single Rod Scram insertion

Time testing was satisfactory, no discrepancies were noted oy the

inspector.

M1.3 Main Stack Radiation Monitor Surveillance Testina - Unit 1 ,

a. JnspectionScone(61726)

The ins]ector observed the performance of Maintenance Surveillance Test

IMST-RGE31R. Main Stack Radiation Monitor High Radiation Isolation

Response Time,

b. Observations and Findinas

On November 5, 1997, the inspector observed the licensee perform IMST-

RGE31R. The )urpose of this test was to determine the response times of

the Main Stact High Radiation Function of the Primary Containment

Isolaticn System (PCIS) for group six valves that are primary

containment purge and vent valves on Unit 1. Perforrance of this test

was in conformance with requirements specified in-TS 4.3.2.3 and UFSAR

Table-7,3.1-3A. item 1.g.

The inspector observed the pre-evolution brief which was conducted in

the Control Room. Al' the personnel necessary to conduct the test were

3 resent. The brief was conducted by a Control Operator. The use of a

]riefing check sheet resulted in a thorouqh brief by the Control

Operator who encouraged participation. The brief discussed actions for

expected and unexpected test results.

The test was performed with both Unit 1 and Unit 2 at 100 percent. The

Unit'2 Containment Atmospheric Control (CAC) Purge Vent Isolation System

was placed in override, per orocedure, to prevent isolation trips on

Unit 2. The test was performed by inserting a simulated Hi-H1 radiation

condition to the Main Stack Radiation Monitor system, which causes the

Reactor l Building Ventilation System to isolate, the Standby Gas

Treatnent System Trains' A and B to initiate, and PCIS group six valves

to-isolate.

The inspector noted that the proper TS Limiting Condition for Operations

(LCOs) were entered upon conmencement of the test. As the Hi-Hi

radiation signal was raised to the Hi-H1 setpoint, a graphic recorder

recorded five channel ctuations. The inspector observed that channel

five recorded no change of state. which would normally indicate that the

'

relay being. monitored did not actuate. However, upon investigation by

the technicians, it was determined that the test jacks, which were being

used.to monitor the signal, did not have wires hooked up to them. The

.

,e--e

. _ _ . _ _ . ___ ._ __

15

technicians notified operations of the problem. The test was secured

and the Unit 1 and Unit 2 systems were restored according to the

-procedure.-

The MST was considered by the licensee to be an invalid test. The PCIS

system was considered operable since the wires that were missing were

for test monitoring only and did not affect system operation.

Subsequent review by the licensee verified this evaluation to be

correct. CR 97-03919 was generated November 6, 1997.

Upon further investigation. the licensee found that the wires had been

removed in an effort to divide Division I and Division II logic

circuitry. The last time this response time testing had been performed

was August 25, 1995. The licensee identifjed a discrepancy in the

wiring diagram that was used to perform the test. The Main Stack

Radiation Monitor test procedure was a new procedure which became

effective October 17, 1997. This procedure was written referencing

drawing F-97083. The drawing showed that the test panel points 3B1-

11/12 were active. This drawing, entitled Unit No. 1 Division II

Terminal Cabinet XU-56 front Side - JXI Interconnection Wiring Diagram,

was revised October 5, 1994. The licensee identified another drawing.

LL-90046 entitled Unit 1 CAC System Outboard LOCA Signal Trip Control

Wiring and Cable Diagram, that showed terminals 3B1-11/12 as spares.

This drawing was revised October 20, 1994. The licensee generated CR-

97-3919 to document the problem, with a recommended action to determine

the cause of the wiring revision error and correct the drawing

discrepancy.

Procedure IMST-RGE31R has been revised to perfora the test using test

points on the relay via the test aanel. The inspector determined that

the change was performed via the 3runswick temporary revision procedure.

c. Conclusions

The inspector concluded that the licensee took appropriate actions to

secure the surveillance test when a discrepancy was identified, and they

took the appropriate actions to correct the procedures and drawings.

,

H2 Maintenance-and Material Condition of Facilities and Equipment

H2.1 2B Recirculation Pumn Errors

a. Insoection Scone (62707)

The inspector reviewed the circumstances surrounding the discovery of

water from the Reactor Building Closed Cooling Water (RBCCW) Sy; tem in

the 2B recirculation. pump motor lower oil reservoir and the clearance- ,

errors during the repair which resulted in damage to the recirculation

-pump seals. The repair of the motor cooler and recirculation sm) seals

resulted in a delay of startup activities for approximately a weet. The

recirculation pump seals serve as a pressure boundary between the

reactor coolant and the drywell atmosphere.

. , _ ._

-- _. _ _ _ _ , _ _

,

-16

.

b. Observations and Findincs

t

On October 2.- 1997. Unit 2 was in Mode 5 when the licensee identified

that the 2B recirculation Jump motor had indications of an oil leak at

the coupling of the lower RBCCW cooling water piping to the-laver oil

reservoir. Work request / job order (WR/J0) 97-AGJS1 for the-repair of

the oil leak was planned and issued. On October 4. connections on the

. cooling water piping for the Jump motor were tightened. No additional

oil leakage was identified. iowever, during startup activities on

October:15. the licensee received the Recirculation Pump Motor B Lower

Bearing High Level annunciator.  :

Motor 011 Cooler Problem Timeline

Octohar 2 4:24 p.m. Mode 5 - Refuel . WR/JO 97-

AGJS1 initiated for observed

recirculation notor reservoir ,

oil leakage

1

October 3 5:19 p.m. Clearance 2 97-1531 initiated

for repair of oil leak

-October 4 5:00 p.m. Maintenance completes work and

closes WR/JO 97-AGJS1

OctcLer 7- Clearance 2-97-1531 retracted

and ticket deleted

October 15 12:56 p.m. Mode Switch to Run

6:43 p.m. Mode 1 - 13.5 percent power

8:43 p.m. High oil level annunciator for

the B recirculation pump lower

bearing

October 16 12:59 p.m. Mode 3 - Hot Shutdown:

Inserted a manual scram to

repair the motor oil reservoir

cooler leak

,

The licensee determined that the 2B recirculation pump motor still was

leaking fluid. The identification of excessive water in the lower oil

reservoir.was recorded in CR 97 3783. Recirc. 011/ Water Cooler Leak.

Another WR/JO was initiated and samples taken to identify the source of

the water. Chemistry sample results revealed RBCCW water in the oil.

.The licensee indicated in CR 97-3782. Improper Response to SIL 484. that

vendor guidance regarding damage to the oil cooler reservoir of a motor

due to torquing.had not been properly dispositioned. The operating

experience review had indicated that no motors for either unit contained

internal cooling coils mounted in the oil reservoir. However, both

units had this cooling configuration. As a result. the vendor

.

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g yy

. ._. .

l

17

recommendations were not integrateo into the cautions on the work

ticket. The cause of the RBCCW leak was not definitively identified.

hawever the licensee indicated that maintenance activities in or around

the damaged line could have contributed to the RBCCW leak.

-

Motor Oil Cooler RBCCW Leak

October 16 2:16 p.m. Clearance 2-97 1622 written to

drain oil-in the pump.

4i45 p.m. Clearance implementation error

for 2-97-1623 incorrect

breaker racked out- 2B bus

versus 2B recirculation motor

(CR 97-3765)

5:00 p.m. Increasing temperature seen on

recirculation pump seals (CR

97-3766)

11:32 p.m. Repair during hot shutdown

unsuccessful initiated

clearance 2-97-1623 to repair *

motor oil cooler leak and

replace damaged recirculation

seals

While isolating the 28 pump. two clearance errors were made. During

initial hanging of clearance 2-97-1623. the operator racked out the 4160

volt feed from the Unit Auxiliary Transformer (UAT) which isolated the

entire 2B bus instead of just racking out the 2B recirculation drive -

motor breaker. No injuries resulted and no required components were

damaged. The failure to implement the clearance in accordance with 001-

1.09 is a violation. This violation is identified as the second example

of VIO 50-324/97-12-01. Clearance Errors. After completing the correct

alignment to isolate the 2B recirculation pump, temperature was seen to

increase on the #1 seal. The licensee restored the system to the pre-

clearance alignment and reestablished seal injection. CR 97-3766.

Recirc. Seal Temp increase. Ws initiated to record the increased

temperature problem. = Tem)erature recorded for the seal exceeded the

graphical bounds of the clart recorder of 300 degrees Fahrenheit.

Inspector review of the vendor manual revealed that the seals were rated

for 200 degrees Fahrenheit. Subsequently, the licensee had to replace

both seals during'the motor cooler replacement.

The inspector reviewed the associated clearances, work tickets,

procedures, and CRs. Discussions with the licensee revealed substantial

damage to the #1 seal and a minor crack or the #2 seal as a result of

the temperature excursion. The licensee indicated that the #1 seal

would not have been capable of holding pressure had the pump been

returned to service. lhe inspector determined that the clearance

preparer did not consider the effects of attempting the repair for the

,

__ _ _ _ . _ _ . _ _ .

18

cooler while in hot shutdown. The failure to maintain the status and

integrity of important plant components and systems in accordance with

001-1.09 was a violation. This violation was identified as the third

example of V10 50-324/97-12 01. Clearance' Errors. The inspector

concluded that this errer constituted a lack of sensitivity by the '

clearance preparer and reviewer to activities affecting the pressure

boundary.

Preliminary review of the motor cooler RBCCW 1eak attributes the failure

to possibly maintenance activities on or around the cooler ai)ing.

During-inspector review of the failure mode determination ( M)) for CR ,

97-3766, errors in clearance development and review resulted in seal

degradation where classified in accordance with the corrective act:on

program as a level 3 or of minor significance, while the positioning of

the wrong breaker and the RBCCW motor cooler leak was assigned a

-level 2. important. Plant Program Procedure OPLP-4. Corrective Action

Management. describes the type of investigation to be 3erformed.

Level 1 and 2 CRs require a root cause determination w11ch is a

comprehensive review in accordance with Plant Program Procedure OPLP-

4.3' Foot Cause Investigations. Tha FMD reviewed identified the errors,

but not the root cause for the inadequate reviews. The inspector

discussed with the licensee the. lack of a comprehensive review of the

multiple human 3erformance errors associated with this event. The

licensee has su)sequently included the clearance errors in the root

cause review of CR 97-3765. Incorrect Breaker Racked Out. Discussion

with licensee management determined that a comprehensive review was

planned and the multiple CRs were rolled into one level two CR.

c. Conclusions

The failure to pro)erly develop and implement a clearance for the

isolation of the 23 recirculation pump motor which resulted in racking

out the incorrect breaker and the replacement of the pump seals due to

damage from excessive temperatures was identified as two examples of a

clearance violation. Prior licensee review of operating experience for

torquing motor oil cooler was' erroneous.

M2.2 Observation of Unit 2 In-Vessel Visual Insoections (TVVI)

a. InsnectionScoce(73751).

The inspector reviewed video taped visual examinations of the CS thermal

sleeve to shroud weld, the thermal sleeve to CS pipe weld and the CS

lower )iping downcomer elbow weld on loop "A" @ 10 degrees azimuth and

,

loop "3" @ 350 degrees azimuth. The weld Nos associated with these

examinations were Weld Nos. 1.-2 & 3 on loop "A" and Weld Nos. 21. 20

and 19 on loop "B". The welds were examined in accordance with NRC

Bulletin 80-13 and the industry's-BWRVIP standards. The inspector also -

reviewed video data for the visual examinations of the "F" Recirculation

System Jet Pump-Riser elbow welds and the pup piece to thermal sleeve

weld. The jet pump riser piping welds were examined as recommended by

the vendor in Service Information Letter (SIL) No. 605 Revision 1. To

_ _. , .

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1

l

19

~ determine the effectiveness of the enhanced visual examinations. the

' inspector evaluated camera resolution quality. examination surface i

detail; and contrast of visual indications.

b. Observations and Findinas

The enhanced visual examinations of the CS piping and thermal sleeves

were performed utilizing GE's underwater color comera. The ins)ection

sensivity was based on clear resolution of a 0.5 Mil wire. T1e

inspector determined that the camera work for these examinations was

excellent, cleaning of the examination surface was very good and

examination surface contrast, detail, and resolution was also excellent.

The inspector concluded that crack like indications on the outside

diameter (00) surface of the CS piping would be identified by the visual

examinations observed.

The inspector also selected the jet pump riser welds to examine. The

observed visual examinations of the jet pump elbow to riser, elbow to

pup piece, and pup piece to thermal sleeve (including draw beads) were

aerformed to the same examination sensitivity as the CS piaing above.

iowever, most of the jet pump welds were examined using a ) lack and

white camera because its smaller size allowed it access to the t@ter

clearances around the jet pumps. Surface contrast and resolution was

not as good as those provided by the color camera, but the same test

sensitivity was achieved and the welds were adequately examined,

c. Conclusions

In-vessel visual inspections were conducted by skillful technicians.

Examination surfaces were brush cleaned, examination sensitivity was a

0.5 Mil wire and surface contrast resolution was excellent es)ecially

with the vendor color camera. Crack like indications on the 0D surface

of the )iping would be identified by the visual examinations observed.

No cracts were identified during the examinations reviewed by the

inspector.

M2.3 Connarison of 1996 and 1997 Unit 2 Core Shroud Ultrasonic Data for

Select Welds

a. Insoection Scone (73753)

The inspector reviewed analysts' resolution sheets and spread sheet

presentations of ultrasonic (UT) data comparison for defect growth for

core shroud welds. This review was performed to determine the rate of

defect growth on selected welds.

b. Observations and Findinas

The inspector selected two core shroud welds to compare defect growth:

(1) Weld H-4 because it was in the high fluence area of the reactor core

shroud and would be expected to see the highest crack growth rate; and

(2) Weld H68 because it had the largest amount of crack recorded on any

,

r ,

_ . . _ _ _ _ _ . _ . _ . - _ . - , _ . _ _ _ _ _

,

i

g-

20 ~ j

~

unrepaired: Unit 2 shroud weld. Review of the~H4 shroud weld data f

< revealed very little change in crack 1 length or death. The change

. . recorded was:found-within-the 0.108" UT-depth tec1nique error band. .-

.;

y

Subsecuent to the inspection. the inspector reviewed the comparison  ;

--

spreac sheets-for_ H6B. which revealed that the crack depth ~was actually  ;

measured much less.during the-1997 examinations than during the 1996  :

-

examinations. -The licensee stated that the Electric' Power Research:

Institute (EPRI) Nondestructive Examination (NDE) Center reviewed the- -!

analysis processes for the 1997 crack d4ths while onsite, as discussed- -l

in NRC IR 50-325(324)/97-11. and concurred with the analysis process.  ;

The licensee was sending the-1996 raw UT data to the EPRI NDE Center-for-

their' review.. The' intent was for EPRI to review the actual analysis

process. procedures, tooling hysterisis, tooling start >ositions-. scan  ;

'

patterns.. etc. to hel) the licensee better understand tie effects. if-

any. these-items-may lave had on the differences in the 1996 and 1997 *

crack depths. 4

c. Conclusions ,

Examination results from the 1996 and 1997 cor. shroud inspections '

.

-revealed very little crack growth for Weld H4. .

conflicting-information. crack depth was actually?id aeasuredH6B muchhowever.

less gave

during the 1997-examinations than during the 1996 examinations.. The

' licensee requested EPRI's help in determining the reason for these

examination differences. ,

M6 Maintenance Organization and Administration

n

M6.1- knprino and Test Eauioment

,

a. Insoettion Scone (62707)

The inspector reviewed installed CS instrumentation data to verify

calibration activities were properly performed in accordance with TS '

requirements. Calibration of in-plant test ecuipment was reviewed as

well as standards located in the measuring anc test equipment- (M&TE)

facility.

b. Observations and Findinas

1The-inspector performed a verification of proper channel calibration

activities for CS trip functions -la - c as recorded in TS Table 3.3.3-2.

Emergency Core Cooling System Actuation Instrumentation Setpoints. The

, " inspector:reviewedi

,e' ~ Maintenance Surveillance Test OMST :RHR210. RHR-LPCI. CSS and HPCI -

6 -High Drywell Pressure Trip Unit Channel Calibration

~

e- Maintenance Surveillance Test.1(2)MST-RHR220. RHR-LPCI ADS CS LL3.

HPCI RCIC LL2 01 vision I Trip Unit Channel Calibration

_

L

6-

k _- _ -- l_ --

~

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21

. Maintenance Surveillance Test 1(2)MST RHR260. RHR CS Low Reactor

Pressure Permissive Trip Unit Channel Calibratica

All instruments were found to be within the prescribed calibration

frequency. Proceducal acceptance criteria and frequency were found to

be within TS allowances.

Throughout the inspection period the inspector reviewed labeling and

prescribed calibration frequency for test equipment located within the

M&TE facility end the plant. With one exception, the test equipment

reviewed was properly labeled in accordance with Maintenance Management

Manual 0MMM 006. Control of Measuring cnd Test Equipment and no

equipment was found beycnd the calioration due date. The inspector

during inspection activities within the M&TE facility identified a

temperature component of a shop standard which was beyond the

calibration due date. The inspector reviewed the last calibration for

all the test ecuipment calibrated by the standard. All equipment

calibration hac been performed prior to the calibration due date. No

discrepancies or concerns were identified.

c. Conclusions

Maintenance measuring and test equiament located within the plant was

found properly labeled and within t1e current calibration interval.

Review of several surveillance tests determined that the acceptance

criteria and frequency were within TS allowances.

M8 Hiscellaneous Maintenance Issues (92902)

M8.1 (Onen) Licensee Event Reoort 97-008-00: Main Stack Radiation Monitor

Surveillance Interval Exceeded.

Licensee Event Report (LER) 97-008-00. dated August 19. 1997, re)orted

that on August 19. 1997, the licensee identified that an UFSAR clange.

implemented on February 12,186. inappropriately eliminated the

requirement to perform Main Stack Radiation Monitor res)onse time

testing. Consequently, the Unit 1 and Unit 2 Main Stacc Radiatioc.

Monitor surveillance tests were not performed prior to the required

dates of July 12. 1997, and August 15. 1996. respectively. On

August 19, 1997, the licensee declared the Main Stack Radiation Monitor

inoperable and actions per TSs were implemented for both units. Test

procedures were developed by August 23, 1997, and performed to satisfy

the surveillance requirements of portions of the logic which had not

been performed within the required surveillance interval. Upon

satisfactory completion, the Main Stack Radiation Monitor was declared

operable. The licensee attributed the cause of this event to inadequate

review and basis verification related to the UFSAR change that

eliminated the response time testing requirement. This LER remains open

pending completion of a corrective action item to assess the UFSAR

change review process.

22

III. Enaineerina

El Conduct of Engineering

El.1 Environmental Qualification (37550. 929031

a. Insoection Scoce

The inspectors reviewed the licensee's corrective actions for the

Environmental Qualification (EO) program, in response to findings

identified during Self-Assessment numbers 95-0041 and 96-0271 and

the violations identified in NRC Inspection Report number 50-

325(324)/96-14.

b. Observations and Findinas

1) Review of Modifications to Drywell Terminal Boxes to Resolve

E0 Moisture Issues

The inspectors, accompanied by licensee E0 engineers,

performed walkdown inspections in the Unit 2 drywell and

examined modifications to electrical terminal boxes to

address moisture intrusion issues identified in CR number

97-02408. The modificationa, which were completed under ESR

97-00519, it.volved drilling of weepholes in the terminal

boxes to preclude the possibility of excessive moisture from

accumulating in the boxes during various accident scenarios.

The inspectors examined the electrical terminal boxes for

the following penetrations and verified the weep holes had

been drilled per the design requirements specifled in the

ESR: penetration numbers 102C 102H. 105D. 105G. and 105J.

The inspectors also examined the conduits located at

radiation monitors and verifier that they had been sealed as

s]ecified in the ESR to prevent intrusion of moisture from

t1e drywell spray headers. Conduits at the following

monitors were examined: 2-D22-RM-4195, 2-D22-RM-4196. 2-D22-

RM-4197 & 2-022-RM-4198.

Additional modifications are required to terminal boxes in

the Units 1 & 2 Reactor Buildings and the Uait I drywell to

resolve this issue. The scope of work for the modifications

required in the reactor buildings to close CR 97-02408 has

not yet been established. Additional comments on the

licensee's corrective actions program to resolve CR 97-02408

and other CRs is discussed in the paragraphs below. The

work in the Unit 1 drywell will be completed during the

Spring 1998 refueling outage.

_ - _ _ __- _ _. _ _ _ . _ . .

23 ,

2) Review of Environmental Qualification Condition Reports

The inspectors reviewed a random sample of CRs initiated by

the licensee to document and disposition nonconforming items

which were identified during the ongoing-E0 reconstitution

project. The nonconforming items were identified as a

result of E0 equipmcnt walkdowns. rev1ew and updating of EQ

ODPs, omissions from the original program, or changes to the

-

operating environment. The inspectors also reviewed the

status of corrective actions to resolve the nonconforming -

conditions. The CRs reviewed, the date the CR was

-identified, and the title / description are listed in the

-

Table below.

lAELE

E0 CONDITION REPORTS

CR Number Date CR Title /Descriotion

Initiated

96-03641 11/3/96 Exceeding qualified life of

ASCO pressure switches.

97-00189 1/9/97 Lack of documentation for

qualification of MSIV pilot

valve components.

97-01841 5/23/97 Affect of fire protection

system initiated by HELB on E0

equipment.

97-02015 6/6/97 Operator training concerns

relative to HELB.

97-02016 6/6/97 Painting of NAMCO limit

switches.

97-02017 6/6/97 Control wires for transmitter

below flood levels.

97-02025 6/6/97 Leakage through stranded wire

condtG ors / seals.

97-02074 6/11/97 Unknown qualified life of some

NAMCO limit switches.

97-02094' 6/12/97 Failure to document open items

in EQ references.

97-02103 6/13/97 Failure to identify E0

documents affected by ESRs.

. - . _

_ _ . . . _ _ _ _ . ~ . _- _ _ _ _ . _ _ .._ _ _ _ _ _ _ _ _

24

CR Number Date CR -Title /Descriotion-

Ront'd)

97 02193 6/20/97 Use of incorrect wiring on

Valcor solenoid valves.

97 02257 6/27/97 Review of Level 2 CR action

items.

97-02333 7/2/97 Failure to perform safety

reviewsforchangestoEDdata

in the equipment data base.

'

97 02408 7/9/97 Effects of moisture intrusion

in electrical boxes.

97 02428 7/10/97 Qualification of radiai. ion

detectors.

97 02465 7/15/97 Questions regarding

operability determinations for

EQ related CRs.

CP&L Procedure PLP-04, Corrective Action Management.

implements the requirements of 10 CFR 50, Ap>endix 8.

Criterion XVI. Procedure PLP 04 specifies tie requirements

for identifying, evaluating, and correcting deficiencies,

,

'

defective equipment, programs, procedures, and other

nonconforming conditions. When a CR is identified, an

invest.igation is performed to determine the cause and

corrective actions are specified to resolve the problem.

The corrective actions are identified as Action items which-

are assigned to a work grou) with a due date. The Action

items (Als) are controlled )y CP&L Procedure PLP-4.1. Site

Action item Management. The CR is closed when all the

assigned Als for the CR are completed.

During review of the status of the corrective actions to

resolva the above listed CRs. the inspectors determined that

18 Als associated with 11 CRs had not been completed by the

assigned due dates. These included the following Al

,, numbers: Al 2 for CR 96 03941 which was due on 9/1/97: Al 6

for CR 97 00189 which was due on 9/2/97: Al 3 & 5 for CR 97-

01841-which were due on 9/8 & 9/24/97, respectively: Al 2.

3 & 4 for CR 97 02017 which were due on 9/30/97: Al 2 for

CR 97-02074 which was due on 9/1/97: Al-2 for CR 97-02103

which was due on 9/30/97: Al 1 & 2 for CR 97-02193 which

were due on 9/22 & 9/15/97, respectively: Al 2. 3. & 4 for

CR 97-02257 which were due on 9/22, 9/22, & 9/15,

respectively AI 4 for CR 97-02333 which was due on

9/12/97: Al 1 &-2 for CR 97 02408 which were due on 8/15 &

9/26/97, respectively; and Al 2 for CR 97-02428 which was

.

- . - -

7

25

due on 8/22/97. The due dates for many of these Als had

already been extended two or more times. -S)ecific examples

are Al 2 for CR 06 03641. Al 6 for CR 97 0139. Al 3 & 5 for

CR 97 01841. Al 2 for CR 97 02074. Al 1 & 2 for CR 97 02193,

and Al 2 for CR 97-02408.

On October 8. 1997 the licensee completed a detailed review

of the E0 related CRs and determined that approximately 100

Als related to 25 CRs were nyerdue from 8 to 53 days. The

licensee also determined that Als related to 18 E0 CRs (nine

from 1996 and nine from 1997) had been extended two or more

times. The Action items related to one 1996 CR had been

extended seven times.

Paragraph 4.2.7 of CP&L Procedure PLP-04. Corrective Action

Management, requires managers / superintendents to ensure that

assigned corrective actions required to resolve CRs are

implemented. Paragraph 5.4 of PLP-04 states that corrective

dctions for CRs shall be tracked per CP&L Procedure PLP-

04.1. Site Action item Management. Paragraph 4.2 of PLP-

04.1 requires supervisors and superintendents to ensure

assigned Al responses adequately addresses the item and are

completed by the due assigned date, if an extension of the

due date is recuired the extension is required to be

justifiable anc documented on the Action item Assignment

form in accordance with Procedure PLP-04.1. The failve of

licensee managers to ensure corrective actions were

implemented as required by Procedure PLP 04, and the failure

to complete the Als in accordance with the schedules

established by Procedure PLP-04.1 is identified as Violation

examples one and twe of V10 325(324)/97-12-05. Failure to

implement Corrective Actions in Accordance with Corrective

Action Program Requirements. Additional revi w will be

performed by NRC to followup on the corrective actions for

the above listed CRs.

3) Review of Justifintions for Continued Operation

The inspectors reviewed the licensee's procedures which

control determination of ecuipment operabit 'v when

deficiencies are identifiec in the environm6 mal

qualification program. Guidance issued by NRC in this area

and the licensee s program (procedures) which implements NRC

guidance are summarized below.

On April 7,1988, the NRC issued Generic Letter (GL) 88 07.

Subject: Modified Enforcement Policy Relating to 10 CFR

50.49. Environmental Qualification:of Electrical Equipment

Important to Safety. The GL provided guidance to licensees

regarding actions to be taken when potential deficiencies

are identified in the environmental qualification of-

. equipment. The guidance specifies that the licensee is

. . . . . - - . . .- . - - _ - - - - . - ~ . - . . - -. -..--.-

b

U

26

9

expected to make a prom)t determination of operability, take

immediate steps to esta)lish a plan with a reasonable

schedule to correct the deficiency. and have written a JCO.

On November 7, 1991, NRC issued GL 91 18. Subject: ,

Information to Licensees Regarding Two NRC Inspection Manual  :

Sections on Resolution of Degraded and Nonconforming

Conditions and Operability. GL 91-18 provided licensees

with the written guidance used by the NRC staff regarding

resolution of degraded and nonconforming conditions and

performance of operability determinations, j

The licensee has-implemented the GL 88-07 guidance for

determination of operability (operability evaluations),

corrective actions, and preparation of JC0s in the following

CP&L Procedures: PLP-04. Corrective Action Management: EGR- i

NGGC 0005, Engineering Service Requests; and EGR NGGC-0156.

Environmental Qualification of Electrical Equipmen+ '

Important to Safety.

CP&L ]rocedure PLP 04, which implements the requirements of

10 CFl 50 Appendix B, Criterion XVI. specifies the

requirements for identifying, evaluating and correcting

deficiencies, defective equipment, or nonconformances.

Procedure EGR NGGC 0156 provides instructions for ,

establishing maintaining, and implementing the requirements

of 10 CFR 50.49 Environmental Qualification of Electric

Equipment Important to Safety for Nuclear Power Plants.

Section 9.3.2 of Procedure EGR-NGGC 0156, provides

instructions for performing E0 operability determinations

and ) reparation of JCOs. Paragraph 9.3.2.3 of procedure

EGR-4GGC 0156 requires preparation of an ESR to document

operability determinations and JCOs. Procedure EGR-NGGC-

0005 specifies recuirements for performance of engineering

work. This procecure implements the requirements of 10 CFR

50, Appendix B, and licensee commitments pertaining to

engineering activities. Paragraph 9.3.7 and Attachment 4 to

Procedure EGR-NGGC-0005, which provide instructions for

performance of engineering evaluations in support of system

operability, require preparation of ESRs to document

operability.

The inspectors reviewed the status of the 23 previously

identified JCOs which were initiated to address potential

. equipment operability issues. Nine of the JCOs were closed,  ;

two were comoleted except for closecut of documentation, <

while the remaining 12 were still open pending completion of -

corrective actions. The inspectors noted that the ESR for

the o)erability determination of solenoid valves due to

possi)le incorrect ty]e of field wiring on the valves

(documented in CR 97-)2193 on June 20, 1997) had not been

approved (completed) until October 11, 1997 for Unit 2 and

October 21,.1997 for Unit 1.

,

, , . - m.,_ - _

_ , _ . . , . . _ . ._

.,,,..__.<,,.,,..n_ , --v..,--- .

.-.y,... .., ,

- - - - . . - - - . - - - . - - - -

4

27

The inspectors performed an additional review the CRs listed

above to determine if potential Equipment operability issues

were ,vidressed with a JC0 per the requirements of licensee

procedures. The following~ problems were identified:

- CR 96 03641 - This CR addressed a discrepancy in the

qualified service life of 88 tripoint pressure switches

manufacturer by the Automatic Switch Company (ASCO). The

manufacturer's original test reports, which were based on a

service temperature of 104 degrees Fahrenheit. indicated

that these switches had a ten year service life, lhis

service life was documented in ODP 77. ASCO Tri-point

Pressure Switches. The ODP was based upon data from DR

77.1. ASCO Test Re

ASCO Test Report # port #Revision

A0R-51785. A0R-10183. 0. TheRevision 1. and DR 77.2,

switches had

been installed in-1985 in Unit I and .986 in Unit 2. In

'

the early 1990's a licensee engineer rt 1culated to service

life to be 36.67 years by using an incoi ect value for the

activation energy in the Arrhenius equation. CR 96 03641

was initiated on November 3. 1996, when this error was

discovered. Per licensee records, based on the original

manufacturer's test report the service life for the Unit I

switches expired on October 2. 1995, while the service life

of the Unit 2 switches expired on April 24, 1996.

Discussions with licensee engineers disclosed that a preliminary

operability review had been performed in November,1996 when this

problem had been initially identified. The review consisted of a

prc'iminary calculation which was based on some actual historical

reactor building temperature data. The preliminary calculation

showed the service life of the ASCO switches was approximately 14

years. However the calculation had not been properly documented.

checked, reviewed, or approved. Also, the licensee failed to 1

prepare a JC0/ESR. During the current inspection the licensee was

in the process of preparing ESR 9700483, to document the revised

service life of the switches. The inspectors reviewed a draft of

the ESR and noted that the only environmental factor reviewed by

the ESR was the service temperature of the switches. Other

environmental factors such as switch wear. radiation, or frequency

of switch operation were not considered in the ESR. The liccnsee

informed the inspectors that they had determined that operating

temperature was the controlling design parameter. However this

had not been documented in the ESR. The inspectors noted that the

Al which addressed the completion of the ESR had been extended

twice and was overdue when the ins)ectors reviewed the draft co)y

of the ESR. 'The current due date lad been Se)tember 1. 1997. io

JC0 (ESR) had been prepared to document opera)1lity of the

pressure switches.

ESR 97 00483 was completed and approved on October 11. 1997.

The inspectors reviewed the completed ESR. The licensee,

based on a review of ODP-77 concluded that thermal aging was

l

,

_ . _ . _ __ _ ___ . . _ _ _ . _ _ _ _ . _ _ _

26

the limiting factor in the life of the switchet.. The

qualified life calculation in the ESR which was based on

actual operating temperature data showed the switches have a

qualified life of 14 years. The Unit I switches will

require replacement in 1999, and the Unit 2 switches will

require replacement in the year 2000

CR 97-02017 - This CR. initiated on June 6, 1997, addressed

t1e possible installation of an environmental seal for a

Rosemount transmitter below the flood (water) level during

some accident conditions OiELB) in the Unit i reactor

building north core spray room. Further review of the

problem disclosed that the seal would not be affected by

water but the wiring for the transmitters, which is covered

with a Kapton insulation, was not qualified for submergence,

The transmitter in question is installed in the core spray

system pump and is covered under RG 1.97. The supervisor's

comments on the CR stated that the transmitter is required

for LOCA but not HELB. when the conduit seal may be

submerged. Review of UFSAR Cha)ter 15 disclosed that the CS

system is required during a HEL 3. Therefore the comment on  ;

the CR.-which apparently was a basis for not requiring an i

operability determination, was incorrect. No JC0/ESR had  !

been prepared to document operability of the Rosemount

transmitter. The Action item for this issue had been

extended once. The new due date had been September 30.

1997.

The licensee determined that only one transmitter had been  !

installed with the wiring and seal in an orientation to be l

affected by submergence. The inspectors performed walkdowns in

the north and south RHR room, north and south CS rooms..and HPCI

rooms in both Units 1 & 2 and verified that no other transmitter .

had been installed in locations where the lead wires or  !

transmitters would be subjected to submergence. During the

inspection. the licensee was in the process of pre)aring an ESR to l

evaluate the existing installed configuration of tie '

transmitter / wiring. The licensee determined, based on data

'

provided by the manufacturer, that the lead wiring from the

transmitters were covered with a Raychem type protective jacket .

which was qualified for submergence. The inspector examined the l

installed transmitter and lead wires and verified that a Raychem l

Jacket had been 1.nstalled over the Kapton insulation to provide i

for resistance to moisture penetration.

CR 97-01841. 97-02025. & 97-02403 These CRs documented

various issues regarding possible effects of moisture on E0

equipment. The inspectors reviewed ESR 97-00391 which

documents an operability review of the problem (effect of

spray from the fire protection system on E0 equipment)

documented in CR 97 01841. This ESR was not issued until

July 22, 1997. 60 days after the CR was initiated. However.  ;

,- ,. _ _ _ __ __ - . _ - . _ _ _ _ . _ . _ . _ _ _ - _ _

29

some other operability issues such as effect of deteriorated

junction box gaskets on E0 equipment were not evaluated in

the ESR, The inspectors concluded that no JC0/ESR had been

prepare to evaluate operability of this issue. The )roblem

documented in CR 97 02025 concerned a problem which 1ad been

a subject of IE Circular 79 05. Moisture Leakage in Stranded

Wire Conductors, which was issued by NRC on March 20, 1979.

The current concern at Brunswick involved primarily the effect .of

moisture intrusion through stranded wire conductors which could

result in leakage currents in instiument circuits. Patel seals

were used to seal some stranded wire conductors in instrument

circuits. A recommended action stated in the CR was to prepare a

JCO. However none was prepared. CR 97-02408 documents numerous

potential moisture intrusion issues. The i mediate corrective

action taken to resolve these issues, as documented in the CR was

to hire an outside consultant to address the issues. A

recommended action listed in the CR was to prepare a JCO. However

none was prepared. The consultant has reviewed many of the issues

documented ir '9 97-01841. 97-02025. and 97 02408 and made

recommendav% W of which have been implemented. The

consultant u TW,1y addressing the current leakage issues and

possible impact ou OOPS and E0 of equipment in ESR 9700440 for the

120 AC volt circuits and ESR 9700441 for DC volt circuits. The

current leakage issue is also anlicable to cuestions raised

regarding the NAMC0 limit switches, discussec below.

CR 97-07016 & 97 02074 - These CRS documented issucs

involving NAMCO limit switches for which the environmental

qualification was indeterminate due to inability to identify

the date of manufacture and a possible issue regarding

leakage currents due to moisture. Although the CRs were

identified as potential operability concerns, no JC0/ESR was

prepared. The licensee subsequently determined that the

switches were still within their qualified life. The

current leakage issue is presently being evaluated.

The above examples of failure to prepare JCOs and document

equipment operability on ESR when environmental

qualification was indeterminate is identified as violation

V10 50-325(324)/97-12 06. Failure to Prepare ESRs/JCOs to

Evaluate Equipment Operability Problems.

4) Qualification / Operability of Post Accident Sampling System

Valves

The inspectors reviewed the status of the operability of the-

R. G. Laurence valves in the post-accident sampling system

'(PASS). Two issues were identified which affected

environmental qualification of these valves and the

associated limit switches. The first issue, which was

. discussed in NRC Inspection Report number 50-325(324)/96-14

_ _ _ _

.

I

30

involved the EQ of the valves. The second issue involved EQ

-of PASS limit switch wiring. The JC0 for this issue was

documented in ESR 97 00289. This JC0 was closed when the

limit switch wires were replaced.

'

Operability of the PASS valves was originally addressed in

ESR 9600426. However this ESR (JCO) has been suaerseded by

ESR 9600587. The inspectors reviewed ESR 96 00537. Evaluate

Re)lacement Coils for R. G. Laurence Solenoid Valves. This

ES1 provided the evaluation that replaced non mtallic

components in the valves with components which were

environmentally qualified. The non metallic components

included the following: a body / bonnet 0 ring seal, a rotary

shaft 0-ring seal, ard the solenoid coil. The licensee

performed testing of the replacement components and verified

that the replacement materials met the requirements for the

service environment (temperature, radiation, humidity). The

18 PASS valves were then rebuilt under WR/J0s using new

materials / parts to replace all non metallic comaonents. The

inspectors randomly selected the WR/J0s listed selow and

reviewed the completed maintenance records (WR/J0s) which

documented the rebuilding of the valves. Records reviewed

were as follows: WR/JO 96 AHFZ1 for valve 1-Ell-F079A.

WR/JO 96 NIGA1 & 2 for valve 1 E11-F079B. WR/JO 96-AIFR1 for

valve 2 RXS-S64180.- and WR/JO 96-AIFS1 for valve 2 RXS SV-

4181. The inspectors concluded that the valves were

operable in their present configuration.

The licensee is in the process of updating ESR 96-00587 to

clarify documentation regarding environmental qualification

of the valves. A ODP is being prepared which will provide

the basis for documentation of the environmental

qualification of the PASS valves. This is part of the

licensee's corrective actions to resolve the violations

identified in NRC Inspection Report 50 325(324)/96-14.

c. Conclusions

Two violations were identified. The licensee's progress in

addressing the previously identified deficiencies in the EQ

program has required extensive NRC review. The violations

1dentified are indicative of a lack of progress and failure to

address the previously identified issue regarding inadequate

corrective actions. The licensee has also failed to document

operability of equipment for which environmental qualification is

indeterminate.

-

' '

n . . .. . . .. .. . . . , . . . . _ _ _ _ , . _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ _

31

El.2 Ilown Inspectiot, for USI A-46 Unit 1 Modifications. Seismic

ification of {ouinment (92903)

a. Inspection Scope

The inspectors inspected modifications to various components in the

Unit 1 Control Building, Reactor Building, and drywell implemented to

resolve deficiencies identified during the US! A 46 walkdowns.

b. Observations and Findinns

The inspectors randomly selected the components listed below for

insSection and verified the modifications were implemented in accordance

wit 1 design requirements specified in ESR 96 00597. Seismic

Qualification - Unit 2 Outage Issues - SOUG. Revisions 0 through 14.

The following modifications were examined:

Location * ESR Pane Ogitr_ int _lon

CB-49 12,12A Connection of 2 EHC-XY-644 to 2-XU-

50.

CB 49 13, 14 Connection of 2-XU-62 to 2-XU 60.

CB 49 20. 21 Connection of 2-H12-P624 to 2 CAC.

TY-4426-1.

CB 49 22, 23 Connections of 2-XU 77 to 2 XU 65 &

-79: 2-XU-66 to 2 XV 65 & -67: and

2-XV 68 to 2-XU-67.

CB-23 32, 33 Connection of 2 2A UPS to concrete

column.

CB 23 34 38 Battery chargers.

CB 49 - 60. 61 HVAC interaction with XU 29.

RB 20 125 135 Seismic Interaction Resolution

2-2-H21 P003

RB-50 94 Add missing bolt to 2-Cl2-CV-

F010

RB 50 95, 96 Add new support. 2Cl2-CV-F010

RB-20 145, 146 Reroute ground cable. 2

IR RB+4

  • Note: Location designated CB 23 refers to control building

elevation 23, CB-49 refers to Control Building elevation 49: RB 20

refers to Reactor Building elevation 20: and RB-50 refers to

Reactor Building elevation 50.

The inspectbrs also examined the two A 46 modifications

implemented in the Unit 2 drywell. These modifications included

relocation and-repair to an HVAC duct under WR/JO 97-ACBR2 and

correction of an interaction between a conduit and valve under

WR/JO 97-ACBR3.

32

The following attributes were examined by the ins)ectors during

the walkdowns: bolt s Res. thread engagement mem)er sizes.

installation tolerances, and location / orientation of

modifications. and where applicable, use of proper type hardware

to implement the modifications. No deficiencies were identified

by the inspectors,

c. Conclusions

The inspectors concluded that the modifications for USl A 46 were

adequately implemented in accordance with design requirements.

s

E2 Engineering Support of Facilities and Equipment

E2.1 Emeraency Core Coolina System Suction Strainer Pro.iect

a. Insnection Scone (37551)

The inspector reviewed the project activities associated with the

installation of new RHR and CS system strainers,

b. Observations and Findinas

The inspector noted excellent planning and decision makina associated

with the ECCS suction strainer project. The decision to drain the torus

early in the project decreased the complexity of the task. Underwater

installation and welding were avoided. The development of a rigging

plan using a full scale mock-up to perform a dry run of moving the

strainers along the heavy load path inside the reactor building led to

ease of installation.

The licensee used an engineering services company for design and

procurement of the strainers. A third party review of the engineering

work was performed. The review concluded that the strainers had been

correctly design in accordance with NRC requirements.

The inspector observed the installation of the strainers in the torus as

c discussed in Section 02.1. The task was accomplished according to the

outage schedule. The total job was performed only using 1? man rem.

The inspector reviewed the project implementation plan. This plan was

very detailed and thorough. It contained pre outage milestones,

schedules, project organization. ALARA plan, assessment of risks. and

many other topic discussions. This thorough implementation plan

resulted in a large modification being completed without difficulty,

c. Conclusions

The inspector concluded that excellent planning and decision making led

to the successful com)letion of a major plant modification. This was a

signification strengt1 in project management.

. . _- -. - - - .. - . - . _-.- - - -.-. -

I

f

33~

E2.2 peak Drywell Temneratures l

a. Insnection Scone (37551)

The inspectors reviewed the events surrounding the declaration of  ;

several snubbers inoperable in Unit 1 drywell inoperable as a result of  ;

high drywell temperatures. .

i

b. Observations ,

,

The inspector reviewed a time line of events leading up to declaring the.

snubbers inoperable. The time line was as follows:

IjE fJrD1 -

June 6, 1996 NRC IR 96-05 documented high drywell

temperatures above the UFSAR limit of 200

degrees Fahrenheit. This was part of URI 96 05-  :

02. Discreaancies, to document NRC special

review of JFSAR problems. The licensee issued

CR 96-1388. ,

December 19, 1996 ESR 96 397 issued to address CR 96-1388

concerning exceeding UFSAR drywell temperatures

which determines new drywell temperature limits

for Unit 1 of 221.7 degrees Fahrenheit and Unit

2 of 240 degrees Fahrenheit.

'

June 4. 1997 Drywell Cooling Fan 10-1 tripped.

Note: Unit 1 drywell tem)eratures were running

above 200 degrees Fahrenleit as documented by

Operations routinely red circling an out-of-

specification reading on the daily logs but were

below 221.7 degrees Fahrenheit per ESR 96 397

until the cooler tripped. Temperatures then

took a step jump to around 230 degrees '

Fahrenheit.

September 19, 1997 Licensee entered 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LC0 for TS 3.7.5 for i

snubbers due to temperatures as high as 249-

degrees Fahrenheit in the upper elevations of

the drywell.

September 21, 1997 Licensee declared that seven out of ten snubbers-

on the reactor head vent line were inoperable

due to exceeding their. seal life due to elevated

-temperatures in the drywell. Licensee prepared

ESR 97-532 to document that the pipe was-

qualified even with the inoperable snubbers left 1

in place.

.

4 --. we, s , , ,+ .. . . . . , , , . , , . , . , . _ _ _ r. , ,%, ,,_,....-,.g . . . - . , - , --,.M .m -,--,-.,mu .

- - .- . . - _ - _ - - - - - - . -. -

t

34

NRC 1R 50 325(324)/96 05 documented the observation that tem)eratures on i

the upper elevations of the Unit 2 drywell had exceeded the JFSAR peak  !

drywell tem)erature of 200 degrees Fahrenheit. This observation was  ;

identified )y the NRC as an URI 50 325(324)/96-05-02. FSAR

Discrepancies, and recorded by the licensee in CR 96-1388. Exceeding 200

degrees Fahrenheit temperature. Subsequently the licensee evaluated the

effect of the high temperatures on the qualified life of components

located in the u)per elevations in order to justify exceeding the limit

in the UFSAR. T11s evaluation was recorded in ESR 96-397. Evaluate

Change to the FSAR. ESR 96-397 redefined the maximum peak temperature '

and qualified life for snubbers located in both units. ESR 96 397

evaluated the ISI/ Snubber program using a predicted temperature profile

for the balance of the Unit 1 and 2 fuel cycles. The profiles predicted

a maximum temperature for Unit 1 of 221.7 degrees Fahrenheit and 240

degrees Fahrenheit for Unit 2. This action concluded that the increased

drywell temperature for Unit 2 had decreased the six year snubber seal

life by approximately two and a half years and determined that since the

Unit 1 calculated average temperature was below the previously evaluated

temperature, no seal 11fe adjustment was necessary.

Following the drywell cooler failure in June 1997. the inspector

discussed the drywell temperature problem with the Unit 1 operators and

pulled a plot of temperature from the plant computer to review the  ;

temperature increase. Operations personnel indicated that engineering

was aware of the problem and that an existing analysis for Unit 2

allowed temperatures up to 240 degrees Fahrenheit. No further

information was received regarding this problem until the snubber

operability evaluation was referenced in the control logs on ,

September 19, 1997. The snubbers were declared inoperable on

September 21. 1997. An analysis determined the head vent line was still

operable without the snubbers.

c. f_inii.ngs

On September 19. 1997 CR 97-3214. Drywell Tem)erature Limitation, was

. written during an engineering evaluation of t1e qualified life for those

components on the upper elevations of Unit 1 for the next Unit 1 fuel

cycle. This evaluation revealed that the June 1997 failure of the 101

drywell cooler motor resulted in temperatures above those predicted in

ESR 96-397 and requested an operability assessment on those components

be conducted. The evaluation. ESR 97-532. Evaluate Snubber Removal for

Head Vent Piping, determined that the seal life for seven of 10 snubbers

located above tne 52 foot elevation could not be qualified until the

A)ril 1998 refueling outage. The evah.ation provided justification for

t1e removal of-these snubbers based on the completion of pipe support

and stress calculations SA-821-508-9700529,- revision 1A and PS-B21-508-

9700529. revision 3A.

The inspector reviewed this issue and found that u)on the failure of the

101 drywell cooler in June 1997 no actions were tacen to evaluate the-

effect of the subsequent t?mperature rise on the seal life of those

snubbers in the upper elevations. It was determined that several

e

v+ - , .w + - . - - e- - , - , e w.<c-e.-,-syen.m,c, . . , ,e .>-m-riw ,w e , w v v ,*v -

m 1

. _ _ _ _ _ _ _ _ _

35

factors contributed to the licensee *s failure to promptly identify this

abnormal condition. The inspector reviewed temperature trending data

which indicated that the temperature in some areas for Unit I had

exceeded the UFSAR limit of 200 degrees Fahrenheit somewhere around

June 6. 1996. DuringJune1997,thetemperaturejum

-degrees Fahrenheit after the failure of the cooler. ped Thetoinspectors

around 230

noted that Operations had informed the system engineer of the condition,

but no follow up actions were identified to assure correction. There

was no action taken once the drywell temperatures were above the upper

limit bounded by ESR 96-397. Accordingly, this-is the first example of

an apparent violetion of 10 CFR 50 Appendix B. Criterion XVI. Corrective

Action. This will be tracked as eel 50-325(324)/97 12 07. Failure to

Take Corrective Action for High Drywell Temperatures and Torus Bypass,

d. Conclusions

The inspector-concluded that an a> parent corrective action violation

occurred because no action was tacen once the drywell temperatures

exceeded their limit bounded by an engineering analysis. This problem

occurred due to a known deficiency that was allowed to exist. The

deficiency was routinely red circled in operations daily logs 6s an

out-of-specification condition and above the UFSAR limit.

E2.3 Drywell to Torus Bvoass

a. Insnection Scone (37551)

The inspector reviewed the potential for the pressure suppression design

function of the primary containment to be bypassed in the event of a

Loss of Coolant Accident (LOCA) during the simultaneous

purging /inerting/deinerting of the torus and drywell. Operating

procedures for o)eration of the Containment Atmosqheric Control (CAC)

system and Stand)y Gas Treatment (SBGT) system. O. 24 and OP-10

respectively, as well as the piping drawings associated with the CAC and

SBGT systems were reviewed. The inspector reviewed LER 97-011-00 and

CR-97-02937 level 2 Root Cause Investigation.

b. .0bservations and Findinas

In April 1997 the licensee first responded to the )ressure suppression

containment bypass issue following an Operational Experience report

issued by Lasalle. The licensee concluded at that time that the valves

associated with purging /inerting/deinerting activities closed upon

receipt of a Group 6 isolation in the event of a LOCA, thus they

concluded that the bypass issue was not a concern. Again. in May 1997.

Operations provided Regulatory Affairs a similar response to a Dresden

.10 CFR 50.72 report. The licensee revisited this-issue in August 1997

after the NRC Resident Inspector questioned them about the issue and

-raised concerns about primary containment isolation valve timing

speci fications.

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' Based on industry related experience on this issue, the inspector

reviewed CAC and SBGT procedures and drawings to verify whether tre

necessary conditions existed during purging /inerting/deinerting

activities to establish a sup)ression pool bypass. Followino this

review it was determined by tle ins)ector that the procedures and plant

piping configuration allowed for a )ypass condition to exist. This

concern was discussed with Regulatory Affairs, including a concern ,

regarding primary containment isolation valve timing specifications. The '

concern with valve timing discussed that the UFSAR report describes the

pressure event. during a LOCA, as only taking a couple of seconds so

-that with a bypass condition established the containment isolation

valves would not close in time to allow for adequate pressure

suppression. However, primary containment isolation valves are allowed

by TS to close in 15 seconds. On September 4. 1997, the licensee issued ,

a Standing Instruction to prevent opening valves necessary to establish

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a by) ass path. CR 97 02937 recommended that administrative controls be

esta)11shed since an additional review had been conducted which

indicated that a suppression pool bypass path could be established. The '

CR described concerns with primary containment isolation valve timing

and that two of the CAC system valves had t6. same isolation division

logic signal (Division 1); so that a single failure of relay contacts

could result in.the bypass path remaining open since they would not

automatically close.

LER 50-325(324)/97 011 00. dated October 13.1997. with an event report .

date of September 12, 1997, determined that operating practices  !

established a flow path where the primary containment pressure

suppression design function was being bypassed. The CAC system valve

lineup associated with purging /inerting/deinerting activities

established a direct path between the drywell and torus air spaces. The

procedures have allowed the simultaneous aerfcrmance of drywell and

torus purging /inerting/deinerting since t1e procedures were approved in

1974.

The LER additionally repnrted that the operation with the existence of a

bypass path was of concern for two reasons described previously: that

was the containment isolation valve timing issue and the single failure

of relay contacts in the isolation signal to the valves. Engineering  !

reviewed both of these scenarios and concluded that during a small break

LOCA the bypass path was of sufficient size to result in exceeding the

drywell design pressure.

l

NRC 1R 50 325(324)/97-11 docume~ 'd that the PNSC held on Septembe u.

1997 recognized that they had m ied to properly evaluate indust:y

experience information and identify that the same issue existed at

Brunswick.

10 CFR 50 Criterie, XVI of Appendix' B. Corrective Actions, requires that l

measures shall be established to assure that conditions adverse to

cuality, such as failures, malfunctions, deficiencies, deviations,

cefective materials and equipment, and nonconformances are promptly

identified and corrected.  !

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Measures were not taken promptly to identify and correct a condition

that was adverse to quality. The licensee missed two opportunities to

identify the condition. The third time this issue was considered by the

licensee was when the NRC Resident I; .ctor questioned them on the ,

matter. This issue was identified as the second example of an apparent

violation EEI 50 325(324)/97-12-07, failure to Take Corrective Action ,

for High Orywell Temperatures and Torus Bypass.

c. Conclusions I

Brunswick conducted activities, since original procedural ap3rovals in

1974, which could have potentially established a condition tlat could

have exceeded the containment design in the event of a LOCA. They had

two missed opportunities to recognize the problem and take prompt

action. The third opportunity was initiated by the Resident Inspector,

and only after questions from the inspector did the licensee recognize

that the problem existed. Once the licensee recognized the problem,

corrective action was taken to correct the problem via a procedural

,

change. This issue was identified as the second example of an apparent '

violation for failure to take corrective action.

E3 Engineering Procedures and Documentation

!

E3.1 B1C11 POWERPLEX Minimum Critical Power Ratios (MCPR) Limit Errors

a. Inspection Scone (37551)

The inspector reviewed the activities surrounding the discovery by the

licensee that errors existed in the Unit 1 Cycle 11 POWERPLEX HCPR

database. This event was described in CR 97 3331. BlC11 PPX MCPR Limits

Error.

b. Observations and Findin g

The minimum critical power ratios (MCPR) is a TS safety limit

'

established to avoid fuel damage due to severe overheating c' the

cladding. TS 3/4.2,2.2, Minimum Critical Power Ratio (Option B).

verifies that the control rod scram distribution assumed in the Option B

' analysis was consistent with actual control rod scram times. If

different. the TS allows adjustment of the limit. The erroneous data

section identified in CR 97-3331 was never used to determine the MCPR

due to the scram times never matching the erroneous data set. CR 97-

3331 indicated that this was the second time an error had been

identified in the POWERPLEX data. The licensee determined that the

database error was in the conservative direction, therefore no safety

limit would have been exceeded.

The inspector reviewed the root cause and failure mode determination for

CR 97-3331 and CR 97-1502. In the CRs. both events attributed the

errors to inattention to detail by both the data initiator and the

reviewer." CR 97-1502. BlC11 POWERPLEX Database Error, documented the

April 24, 1997 discovery of a typographical error in one of the 16 data

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sets used to determine the MCPR limit. After correction of the error.

the licensee performed a s)ot-check for consistency with the Core

0)erating Limits Report Every value was not specifically reviewed.

1le f ailure to assure that adecuate corrective actions taken to preclude

repetition of errors identifiec in the MCPR database is a violation.

This violation is identified as V10 50 325(324)/97 12 08. MCPR Database

Errors. The root cause also identified schedule pressure as a

contributing factor for the inadequate design review performed on the

data. The inspector determined, through review of associated procedures

and discussion with the licensee, that c minimum of four procedures

governed the review of the data. The licensee indicated that specific

guidance for the POWERPLEX data cycle creation update and verification

was contained in Nuclear fuels Management & Safety Analysis Section

Guideline NFG 14-23. POWERPLEX Data Bank Creation Standard Verification

Scope and NFG 14 29, POWERPLEX New Cycle update. Further discussion

revealed that these guidelines used, in addition to the rther design

verification procedures for verification of the data for deter 711ning TS

safety limits, were not controlled in accordance with the quality

assurance requirements as described in 10 CFR 50. Appendix B.

c. Conclusions

inadm uate design review during initial com)osition allowed errors to be

introcuced into the database which establisled the Option B minimum

critical power ratio limits. A violation was issued for the failure to

assure that corrective actions taken upon discovery of an error in the

MCPR database precluded repetition.

E3.2 Special UFSAR Revirm

A recent discovery of a licensee o)erating the facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures, and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this re) ort, the inspectors reviewed the applicable

portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures, and/or parameters.

Review of UFSAR drywell temperature limits were reviewed. The licensee

was determined to be above the UFSAR limit and outside an existing

analysis as discussed in Section E2.2.

E7 Quality Assurance in Engineering Activities (37550)

E7.1 Licensee Assessments

a Insoection Stone

The inspectors reviewed assessments which were performed by the

Brunswick Nuclear Assessment Section of activities in the

Brunswick Env ineering Support Section (BESS).

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b. Observation and Findinas

lhe inspectors reviewed Assessment Report numbers B ES 97-01 and

B-ES 97-02 which document the results of assessments performed by

the Nuclear Assessment Section (NAS) to determine the

effectiveness of engineering activities performed at Brunswick,

Assessment number B-ES-97 01. which was performed between May 27

and June 6,1997. resulted in identification of two strengths,

four issues and three weaknesses, The strengths involved

improvements shown in the engineering continuing training program

and the fact that weekly program / system review meeting are

conducted. The four issues were as follows: 1) Failure to

document ESR reviews and design verifications: 2) Some engineering

supervisors were not knowledgeable or involved in the engineering

training program: 3) Engineering workload is not being etfectively

managed; and 4) Corrective actions for many NAS assessment

m es/ weaknesses identified in BESS have not been fully

effective, The three weaknesses were as follows: 1) Engineering

management has not effectively established performance standards

and expectations with regard to processes and personnel: 2) Three

of the approved engineering training guides contain outdated

information: and 3) There was an inability to use ERFIS

downloaded information for performance monitoring.

One strength, three issues, and one weakness were identified

during Assessment number B-ES 97 02 which was performed on

September 8 through September 19, 1997. The strength recognized

that BESS initiatives related to inservice inspection testing have

resulted in significant dose and manpower savings. The issues

were as follows: 1) Some EQ ESRs were prepared by individuals who

'had not completed training: 2) An A/E firm providing engineering

services to BESS were unable to provide records which documented

training of their engineering personnel: and 3) A continuing

problem with lack of atter ion to detail in preparation of ESRs

which resulted in administrative errors / omissions in the ESRs,

The weakness identified that modification ESRs were not

consistently screened in accordance with CP&L procedures.

The licensee issued CRs to document the issues and weaknesses

identified in the assessments. The ins)ectors reviewed CR 97-

03305 which was initiated to document tle ESRs 97-00238 and 97-

00343 were prepared by individuals who had not completed the

required training, The inspectors noted that the licensee

previously identified the similar occurrences of unqualified

individuals-completing ERS or ESR reviews in CR 96 03693.

Initiated on November 12, 1996, and CR 97-01436 which was

initiated on April 20, 1997. CR 97 01905 identified a similar

issue where an unqualified engineer in the EQ group was signing

field verification data sheets, The inspectors concluded that the

licensee's corrective actions have been ineffective in resolving

the issue of engineering managers assigning work activities to

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individuals who were not qualified under the licensee's training

program. This was identified to the licensee as example four

violation VIO 50 325(324)/97-12 05, for failure to implement the

corrective action program.

c. Conclusions

The NAS assessments were adequate in evaluating the licensee's

onsite engineering program. However the results of the

assessments showed that the licensee's corrective actions in

response to previously identified assessment findings have been

ineffective. An additional violation was identified regarding

failure to implement the corrective action pr" ram.

E8 Hiscellaneous Engineering Issues (92903)

E8.1 (Closed) Unresolved item 50-325(324)/97 08 08: Control of

Moisture in Installation of E0 Components.

During the review of the E0 equipment deta sheets during the inspection

documented in NRC Inspection Report number 50-225(324)/97 38. the

inspectors determined that deficiencies in installation of E0 equipment

documented in the data sheets had not been addressed by licensee E0

engineers when the data sheets were reviewed. CP&L Procedure PLP 04

Corrective Action Management, requ. es managers and personnel to

initiate CRs when they become aware of adverse conditions or conditions

which do not meet expectations. The failure of managers and personnel

to initiate CRs to document the E0 equipment installation deficiencies

when they became aware of these conditions not meeting expectations was

identified to the licensee as another example of Violation item 50-325

(324)/97-12-05. Failure to implement Corrective Actions in Accordance

with Corrective Action Program.

The licensee had initiated three CRs to address the effects of moisture

and moisture intrusion issues on E0 components. These were CR rambers

97-01841. 97-02025. and 97 02408. The licensee had also identified

other CR to address specific moisture issues, for example 9/-02017. or

issued WR/JO to address repairs to specific equipment. However, these

were not issued for several weeks af ter the field walkdown inspections

were completed and the data sheets had been reviewed and signed by the

E0 engineers. As discussed above, the inspectors performed a detailed

review of the licensee's corrective ar' ions required to resolve these

issues. An additional violation example was identified for failure to

document operability reviews and is identified as example three of

VIO 50-325(324)/97-12 04, for failure to implement corrective actions.

E8.2 10nen) Licensee Event R oort (LER) 50-325(324)/97-04: Spent Fuel

Shipping Cask Handling Activities

On April 11. 1996, the NRC issued NRC Bulletin 96-02 Movement of Heavy

toads Over Spent Fuel. Over fuel in the Reactor Core, or Over Safety-

Related Equipment. This bulletin described another utility's inadequate

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evaluation of the movement of a spent fuel shipping cask over safety-

related equi) ment. The utility was )lanning to perform this activity

under a 10 CrR 50.59 evaluation. wit 1 the determination that no

unreviewed safety questions (US0) existed. However this bulletin

described a subsecuent NRC review which determined that a US0 was

involved because cropping of a spent fuel cask would have created an

accident of a different type than any evaluated previously and could

have also resulted in the increase in the potential consequences

evaluated in the UFSAR. The bulletin requested the submission of

information concerning the movement of heavy loads. The licensee

responded to the bulletin on May 10. 1996. This LER recorded that a

plant specific review of an identified deficiency at another facility

revealed that the Brunswick heavy load analysis as described in the

UFSAR did not completely bound movement of the shipping cask from the

primary non single failure proof lif t to the secondary lift with the

valve box covers removed. This condition was not previously analyzed

and therefore constituted a US0. In accordance with 10 CFR 50.59 a US0

requires prior NRC approval before implementation. The failure to

identify a condition outside of the design basis during the 10 CFR 50.59

screening for the cask transfer is a violation. This ap)arent violation

is identified as EEI 50 325(324)/97 12 09. US0 on Spent ruel Cask

Movement.

In a letter dated. August 6. 1997, the licensee submitted a license

amendment request for a US0. The letter contends that further

evaluation determined that a drop of the fuel cask during transfer from

the tilting cradle to the secondary yoke is not a credible event.

However, the licensee contended that the use of a single lifting device

during the transfer still re) resented an event not previously reviewed

by the NRC. Pending review )y the NRC of the licensee amendment request

this item will remain open.

E8.3 (Closed) Violation V10 50-325(324)/97-02-06: ESR Design Verification

Requirements

This item is closed based on the review documented in IR 50-325(324)/

97-09. Section E8.3.

IV. Plant Suo. pact

R1 Radiological Protection and Chemistry Controls

Rl.1 Radiation Control Practices Durina Unit 2 Outace

a. Insnection Scone (71750)

The inspector observed drywell, torus, and refuel activities during

routine plant tours,

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b. Observations and Findinos  !

During the Unit 2 refueling outage. the inspector observed improved

supervisory oversight of radiation control practices. Supervisory  !

oversight presence was visible and noticeable each time an inspector was I

ct one of the work locations.

!

Drywell and torus work activities were well planned and coordinated.

The licensee used briefing rooms with detailed ma)s to review dose rates 1

and contamination levels prior to entrance into t1ese areas. Remote ,

reading dosimetry was used for areas as the drywell dose rates were

high. This allowed remote tracking of exposure from someone not

involved in the work activities.

4

c. Conclusions

improved suaer visory oversight of radiation cc :rol practices was noted

during the Jnit 2 refueling outage.

R8 Hiscellaneous RP&C Issues

R8.1 (Closed) Violation VIO 50-325(324)/96-15 09: Improper Implementation of

-ARM Response Procedure

During inspection activities documented in IR 50-325(324)/96 15. a 1

violation was issued for the improper 1mplementation of the area

radiation monitor (ARM) radiation res)onse test. Inspector review of

Environmental & Radiation Control OE&RC-0358. Area Radiation Monitors

Radiation Response Monthly Test determined that the ARM setpoints were

inaccurate and abnormal readings were not being appropriately

dispositioned.

The inspector reviewed the August 13 and September 10,19'.J.

performances of the revised E&RC procedure. With the exception of an

abnormal reading in the Radiochemistry Lab during the August 13

performance, abnormal readings were dispositioned by notifying

Operations of the readings and initiation of work tickets or performance

of surveys to log the change in the ARM vicinity. Based on the

completion of the procedure revision and verification of proper

,

implementation, this item is closed.

S4 Security and Safeguards Staff Knowledge and Performance

S4.1 Protected Area Access Control

a. Insnection Scnne (71750) 1

The inspector observed protected area (PA) access measures including

equipment or pat-down searches for illegal contraband and reviewed

actions taken to address an operating experience report concerning an

observed weakness at another utility in granting authorized PA access.

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.b. Observations and Findinas

On October 3 and again on October 7. 1997, the inspector observed two-

individuals between the waist high turnstiles and the PA turnstiles. The

Access Control Person (ACP) as well as nearby Members of the Security

Force appeared to be monitoring other activities and did not lock down

the turnstile or remove the second individual from the area.

The inspector reviewed the Security Olan as well as various security

procedures including Security Instruction 051-09. Personnel A" cess

Authorization, Control, and identification. The procedure out' ted the

responsibilities of the ACP, The ACP was tasked with preventing entry

of unauthorized personnel into the PA by locking the turnstiles, As a

result of similar PA access issues at-another facility the NRC issued

information in a letter dated February 20, 1997, about potential

weaknesses in PA access control. As a result of this information the

licensee implemented long term corrective actions for potential software

problems and the licensee stated that another concern was corrected by

the conduct of training. The inspector reviewed training records

conducted in November 1996 and noted that the actions tak.en regarding

the ACP ensuring proper identification, assessment and response were not

covered in any training activities or a w .nistrative instruction

reviewed. The inspector noted that no additional training was conducted

to address security response to this issue, despite a different physical

layout, when the new access facility was placed in service in

July 1997. In addition no procedural guidance was identified that

outlinad the means to determine whether a threat existed; if present,

the extent of the threat: and those actions to be taken to neutralize

the threat. This lack of procedural guidance has allowed for diverse

methods of implerentation, in the events observed above the inspector

determined that the response for one instance, gesturing or using an

inaudible intercom, was ineffective in notifying those individuals

involved that their activities were in conflict with plant security

requirements, in addition, the inspector determined that the ACPs on

both occasions failed to lock down the PA access or remove the second

individual from the area to ensure the correct individual was being

granted access when faced with a situation that may have allowed an

unauthorized person access to the PA.

The failure to provide adequate procedural guidance for those actions

required for the ACP to control the final access function into the

protected area to prevent unauthorized access is a violation.

Specifically. no guidar ce existed for controlling a condition observed

by the inspector on October 3 and again on October 7, 1997 wherein the

ACP failed to lock down the Protected Area turnstiles or remove the-

second individual from the area during a condition which could have

allowed an unauthorized individual to gain access into the PA. This-

violation is identified as VIO 50-325(324)/97-12-10. Protected Area

Personnel Access Control Deficiency.

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c. Conclusions

Corrective actions for a generic event identified at another facility

were found to be incomplete. Due to an inadequate procedure, security

personnel failed to secure PA access on two occasions which could have

resulted in the entrance of an unauthorized individual into the

Protecte, trea. These failures were identified as a violation.

V. Manaaement Meetinoi

X1 Exit Meetino Summary

The inspector presented the inspection results to members of liceisee

management at the conclusion of the insDection on November 13, 1997.

Post inspection briefings were conducted on October 2 and 31, 1997. The j

. licensee acknowledged the findings presented.  !

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

A. Brittain. Manager Security

M. Christinziano, Manager Environmental and Radiation Control

W. Dorman. Supervisor Licensing and Raulatory Programs

N. Gannon. Manager Maintenance

J. Gawron. Manager Nuclear Assessment Section

S. Hinnant. Vice President. Brunswick Steam Electric Plant

K. Jury Manager Regulatory Affairs

B. Lindgren. Manager Site Support Services

J. Lyash. Plant General Manager

G. Hiller Manager Brunswick Engineering Support Section

R. Mullis. Manager Operations

Other licensee employees or contractors included office, operation,

maintenance, chemistry, radiation, and corporate personnel.

E

E. Brown

J. Coley

G. Guthrie

F. Jape

J. Lenahan

C. Patterson

M. Shymlock

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INSPECTION PROCEDURES USED

IP 37550: Engineering- l

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations i

IP 71750: Plant Support Activities

IP 73753: Inservice Inspection  !

IP 92901: Followup Plant Operations i

IP 92902: Followup - Maintenance

IP 92903: Followup Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED ,

1

Doened l

50 324/97-12 01 VIO Clearcnce Errors (paragraphs 02.3 and M2.1 )

50 325/97 12-02 NCV Control Rod Movement Error (paragraph 04.2)

50 325/97-12-03 URI Recirculation Pump Runbacks (paragraph 04.3)

50 325(324)/97-12-04 URI Diesel Generator low Voltage Auto Start Defeated

(paragraph 04.4)

50-325(324)/97-12-05 V10 Failure to implement Corrective Actions in

Accordance with Corrective Action Program

(paragraph El.l.b.2) )

50 325(3241/97-12-06 V10 Failure to Prepare ESR/JC0 to Document Equipment

Operability Problems (paragraph El.l.b.3)

50-325(324)/97-12-07 eel Failure to Take Corrective Action (High Drywell

Temperature and Torus Bypass) (paragraphs E2.2

and E2.3)

50 325(324)/97-12 08 VIO MCPR Dat base Error (paragraph E3.1)

4

50-325(324)/97-12 09 eel US0 on Spent Fuel Cask Movement (paragraph E8.1)

50-325(324)/97-12-10 V10 Protected Area Personnel Access Control

Deficiency (paragraph S4,1)

C1053d

50-325(324)/97-02 06 VIO ESR Design Verification Requirements (paragraph

E8.3)  ;

50-325/97-12 02 NCV Control Rod Movement Error (paragraph 04.2)

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50 325(324)/97 08 08 URI Control of Moisture in Installation of E0

Components (paragraph E8.1)  ;

50-325(324)/96-15-09 VIO Imp,oper Implementation of ARM Response  :

Procedure (paragraph R8.1) l

Discussed

[

50 325(324)/97-02-07 V10 Failure to initiate CR-for HPCI Valve Time i

Discrepancy (paragraph 08.1) l

50 325(324)/97 08 LER ' Main Stack Radiation Monitor-Tests not Performed

as Required. (paragraph M8.1) l

50-325(324)/97 04 LER Spent Fuel Shipping Cask Handling Activities l

(paragraph E8,1) i

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