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{{#Wiki_filter:May 8, 2006 Joseph E. Venable Vice Presi dent Operations Waterford Stea m Elec tric S tation Unit 3 Entergy Operation s, Inc.17265 Riv er Road Killona, Louisiana 70066-0751 SUBJE CT: W ATERFORD STEAM ELECTRIC STATI ON, UNIT 3 - NRC PROBLEM IDENTIFICATI ON AND RESOLUTION INSPECTI ON REPORT 05000382/2006 008 Dear Mr. V enable: On March 24 , 2006, the U.
{{#Wiki_filter:==SUBJECT:==
WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000382/2006008


S. Nuclear R egulatory Co mmission (NRC) completed a team inspe ction at yo ur Waterford St eam El ectric Stati on, Un it 3. The enc losed report docume nts the inspecti on findings, w hich we re discussed with y ou and other members of your staff during an exit mee ting on Ma rch 24, 2006.
==Dear Mr. Venable:==
On March 24, 2006, the U. S. Nuclear Regulatory Commission (NRC) completed a team inspection at your Waterford Steam Electric Station, Unit 3. The enclosed report documents the inspection findings, which were discussed with you and other members of your staff during an exit meeting on [[Exit meeting date::March 24, 2006]].
This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, compliance with the Commissions rules and regulations and the conditions of your operating license. The team reviewed 237 condition reports, apparent cause and root cause analyses, as well as supporting documents. In addition, the team reviewed crosscutting aspects of NRC- and licensee-identified findings and interviewed personnel regarding the safety conscious work environment.


This i nspect ion w as an exami natio n of acti viti es con ducted under your lice nse as they relat e to the identifica tion and reso lution of probl ems, compliance with the Commission'
On the basis of the sample selected for review, there were no findings of significance identified during this inspection. The team concluded that, in general, problems were properly identified, evaluated, and corrected. The team concluded that a positive safety-conscious work environment existed at your Waterford Steam Electric Station, Unit 3. Several examples of minor problems were identified, including conditions adverse to quality that were not identified and entered into your corrective action program.
s rules and regulations an d the conditi ons of your op erating licen se. The team rev iewed 237 conditi on reports , appa rent ca use an d root cause analy ses, as wel l as s upport ing do cuments. In addition, the team review ed crosscutting as pects of NRC- an d licensee-identified findi ngs and interv iew ed per sonne l regar ding th e safety consc ious work e nvir onment.On the basis o f the sample sel ected for revie w, there w ere no findings o f significance ide ntified during this i nspection. The team concluded that, in general , problems w ere properly identified, eval uated, and c orrecte d. The team co nclud ed tha t a pos itiv e safety-consc ious work environment existed a t your Waterford Steam Electric S tation, Unit 3. Several examples of minor problems were ide ntified, incl uding conditi ons adverse to quality that were no t identified and en tered i nto y our co rrecti ve ac tion p rogram.


Entergy Operation s, Inc.-2-In acco rdance wit h 10 C FR 2.3 90 of th e NRC's "Rul es of Pr actice ," a co py of t his l etter a nd its enclosure, an d your resp onse (if any)
Entergy Operations, Inc. -2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
will be avail able elec tronically for public i nspection i n the NRC Publ ic Document R oom or from the Publ icly Av ailable Records (PAR S) component of NRC's doc ument system (AD AMS). AD AMS is accessibl e from the NRC Web site at http://w ww.nrc.gov/readi ng-rm/ada ms.html (the P ubli c Ele ctroni c Read ing Ro om).Since rely , /RA/Linda Joy Smith, Chie f Plant Engine ering Branch Divi sion of Reac tor Safe ty Docket: 50-382 License: N PF-38 Enclo sure: NRC Inspecti on Report 050 00382/2006008 ATTACHME NT A: Suppl emental Information ATTAC HME NT B: Waterford 3 Pres suriz er Surge Line Tempera ture Ch ange Ra te ATTAC HME NT C: White P aper o n Effect o f Diese l Sump Pump I nopera bili ty on Ulti mate Heat S ink Ope rabil ity cc w/encl osure: Senior Vi ce President and Chief Operatin g Officer Entergy Operation s, Inc.P.O. Box 319 95 Jackson, MS 39286-1995 Vice Presi dent, Op eratio ns Sup port Entergy Operation s, Inc.P.O. Box 319 95 Jackson, MS 39286-1995 Wise, Carter, Child & Ca raway P.O. Box 651 Jackson, MS 39205 General Ma nager, Plant Operati ons W aterford 3 SES Entergy Operation s, Inc.17265 Riv er Road Killona, LA 70066-07


Entergy Operation s, Inc.-3-Manager - Li censing Ma nager W aterford 3 SES Entergy Operation s, Inc.17265 Riv er Road Killona, LA 70066-07 51 Chairman Louisiana Public Se rvice Commi ssion P.O. Box 911 54 Baton Rouge, LA 70821-9154 Director, Nuclear Safet y & Regul atory Affairs W aterford 3 SES Entergy Operation s, Inc.17265 Riv er Road Killona, LA 70066-07 51 Michael E. Henry, State Liais on Officer Depart ment of E nvir onmenta l Qual ity Permits Div ision P.O. Box 431 3 Baton Rouge, LA 70821-4313 Paris h Pres ident St. Charles P arish P.O. Box 302 Hahnvil le, LA 700 57 Winston & Strawn LLP 1 7 0 0 K S t r e e t , N.W.Washington, DC 20006-3817 Entergy Operation s, Inc.-4-Electronic distribution by RIV:
Sincerely,
Region al Ad minis trator (BSM1)DRP Directo r (ATH)DRS D irecto r (DDC)DRS D eputy Direc tor (RJC1)Senio r Resi dent In specto r (MCH)Branch Chief, DRP/E (DNG)Senior Project Engineer, DRP/E (VGG)Team Leader, DRP/T SS (RLN1)RITS Co ordin ator (KEG)DRS STA (DAP)S. O'Co nnor, OE DO RIV Coord inato r (SCO)ROPrep orts W AT Site Se cretar y (AHY)ADAM S: / Yes G No Initi als: __ljs____ / Publi cly Av ailable G Non-Publicly Available G Sensitive
/RA/
/ Non-Sensit ive DOCUMEN T: R\_WAT\2006\W T2006-08RP-ELC.w pd RI:DRP/E PE:DR P/B PE:DR P/A SOE:DR S/OE RI:DRP/E ELCro we/l mb DHOverland MABro wn MEMu rphy GFLarkin/RA/ T/RA//RA//RA//RA/ T 5/5/06 5/5/06 5/5/06 5/5/06 5/5/06 BC:DR P/E SRI:DRS/EB2 BC:DRS/EB2 DNGraves D. Proulx LJSmi th/RA//RA//RA/5/8/06 5/5/06 5/8/06 OFFICIAL RECORD COPY T=Telephone E=E-mai l F=Fax Enclo sure-1-ENCLOSURE U.S. NUCLEAR REGULATORY COMMISSION
Linda Joy Smith, Chief Plant Engineering Branch Division of Reactor Safety Docket: 50-382 License: NPF-38


==REGION IV==
===Enclosure:===
Docket: 50-382 License: NPF-38 Report: 05000382/2006 008 Licensee: Entergy Operation s, Inc.Facility: Waterford Stea m Elec tric S tation , Unit 3 Location: Hwy. 18 Killona, Louisiana Dates: March 6-24 , 2006 Inspectors:
NRC Inspection Report 05000382/2006008 ATTACHMENT A: Supplemental Information ATTACHMENT B: Waterford 3 Pressurizer Surge Line Temperature Change Rate ATTACHMENT C: White Paper on Effect of Diesel Sump Pump Inoperability on Ultimate Heat Sink Operability
M. Brow n, Project Engine er, Projects Branch A E. Crowe, R esident Inspe ctor, Projects Branc h E G. Larkin, Reside nt Inspector, Projec ts Branch E M. Mu rphy, Seni or Operations E ngineer, Operation s Branch D. Overland, Project Engineer, Projects Branch B Approved by: L. J. Smith, Chi ef Engineering Bran ch 2 Divi sion of Reac tor Safe ty Enclo sure-2-SUMMA RY OF F INDING S IR 05000382/2006008; Enterg y Operations, Inc., 03/06-24/2006; W aterford Steam Electric Statio n, Uni t 3; bi ennia l bas elin e ins pecti on of th e ide ntifica tion a nd res oluti on of pr oblems. The inspection was cond ucted by tw o resident i nspectors, one s enior operati ons engineer, a nd two project e ngineers. The NR C's program for ove rseeing the safe op eration of commercia l nuclear pow er reactors is described i n NUREG-1649 , "Reactor Oversi ght Process," Rev ision 3, dated July 2000.Identi ficatio n and Resol ution of Prob lems*The team revie wed 237 corrective action program docu ments, apparent an d root cause analyses, as well as supportin g documents to asse ss problem i dentification and resol ution activ ities. Base d on th is rev iew , the te am found the l icens ee's proces s to identify, pri oritize, e valuate, a nd correct probl ems was genera lly effectiv e; thresholds for identifying i ssues remained appropriatel y low and, in most cases, correctiv e actions were adequate to address co nditions ad verse to qual ity. Ho wever, a number of issues were ide ntified associ ated with the proper i dentification of degraded conditi ons in the plant. The team re viewe d corrective actions asso ciated wi th these degraded conditions and design i ssues at Waterford Steam Electric S tation, Unit 3, which had crosscuttin g aspects in th e area of proble m identificatio n and resolu tion.The team conclud ed that a posi tive safety-co nscious w ork environment exists at Waterf ord Steam Ele ctric Station, Unit 3, base d upon inte rviews conducted w ith plant personnel. The team determined that employe es and contracto rs feel free to raise safety concerns to their superv ision or b ring concerns to the employe e concerns program.Insp ecto r-Id enti fied and Sel f-Rev eal ing F ind ings None Enclo sure-3-REPORT D ETA ILS 4.OT HE R AC TI VI TI ES (O A)4OA2 Identi ficatio n and Resol ution of Prob lems a.Effectiveness of Probl em Identification (1)Inspection Sc ope The in specto rs rev iew ed ite ms sel ected across four of th e sev en cor nersto nes to determine if probl ems were be ing properly identified, c haracterized , and entered i nto the corrective a ction program for eva luation an d resolution. Specifical ly, the tea m's review included a selection of 237 condi tion reports, equi pment walkdow ns, review of operator logs, maintenance records, and s tation quarterly trend reports. The majority of the condition re ports were o pened and cl osed since the last NRC problem ide ntification an d resolution i nspection co mpleted on M ay 21, 200 4. The team also performed a histori cal revi ew o f condi tion r eports wri tten ov er the last 5 year s for the high p ressur e safety injection sy stem, main feedwa ter isolatio n valv es, main steam i solation v alves, ess ential chillers, a nd the emergency diesel gene rators. The team rev iewed a sample of lic ensee audits and s elf assessments, trend ing reports, sys tem health repo rts, and vari ous other reports and d ocumen ts rel ated to the pr oblem ident ificati on and resol ution program. The audit and self-assessment resul ts were compa red with the self-reveal ing and NRC-identified issues to determ ine the effectiveness of the audits and self assessments.


The team intervi ewed stati on personnel and eval uated correctiv e action doc umentation to determine the licensee'
REGION IV==
s threshold for i dentifying probl ems and enteri ng them into the corrective a ction program. In a ddition, i n order to asse ss the lice nsee's hand ling of operat or ex perie nce, th e team r evie wed the li censee's ev aluat ion o f selec ted in dustry operating exp erience reports , includi ng licensee event reports, NRC generic l etters, NRC bull etins, and N RC information n otices, and gene ric vendo r notifications to assess if issues applicable to W aterford Steam Electric Station, Unit 3, were appropriately addressed.
Docket: 50-382 License: NPF-38 Report: 05000382/2006008 Licensee: Entergy Operations, Inc.


A listing of spe cific documents re viewe d during the i nspection i s included in the attach ment to this r eport. (2)Assessment The team determined that, in general , problems w ere adequately identified a nd entered into the correc tive acti on program, as ev idenced by the relativ ely few findings identi fied during the asses sment period.
Facility: Waterford Steam Electric Station, Unit 3 Location: Hwy. 18 Killona, Louisiana Dates: March 6-24, 2006 Inspectors: M. Brown, Project Engineer, Projects Branch A E. Crowe, Resident Inspector, Projects Branch E G. Larkin, Resident Inspector, Projects Branch E M. Murphy, Senior Operations Engineer, Operations Branch D. Overland, Project Engineer, Projects Branch B Approved by: L. J. Smith, Chief Engineering Branch 2 Division of Reactor Safety-1-  Enclosure


The licensee
=SUMMARY OF FINDINGS=
's threshold for entering issue s into the corr ecti ve act ion pr ogr am was appr opri atel y low. Ho wever, the t eam f ound two examples o f ineffective proble m identificatio n during this inspection.
IR 05000382/2006008; Entergy Operations, Inc., 03/06-24/2006; Waterford Steam Electric


The license e also failed in some instances to identif y or document deficiencies, which resulted in NRC nonci ted v iola tions.
Station, Unit 3; biennial baseline inspection of the identification and resolution of problems.


Enclo sure-4-Current Issues Example 1: The licens ee failed to i dentify multip le temperature ch anges of the pressurizer surge line, which exceeded the heatup and cooldown rate described in Section 5.4.3.1 of the station'
The inspection was conducted by two resident inspectors, one senior operations engineer, and two project engineers. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
s Final S afety Analy sis Report. S pecifically , the inspecti on team discove red during a pl ant shutdow n in August 20 05 that the pres surizer surge line had experienced 19 changes in temperatur e, which exceeded this limit. This example is further d escrib ed in Secti on 4OA 2.e of th is rep ort.Example 2: The te am found the l icens ee's i denti ficatio n of adv erse tr ends t o be w eak. The inspection team review ed 17 condi tions reports, i n which the licen see documented inadequacies in the procure ment of replacement p arts for the station.


The license e had ident ified a trend of impro per pa rts pas sing th rough th e rece ipt i nspect ion, b ut fail ed to identify adv erse trends rel ated to lack of engin eering invo lvement, as required by th e procur ement p rocess; failu re to p erform pro fession al en gineer ing ev aluat ions for parts transferred into the system; and rec eipt inspec tion documents missing required attributes. These pr ocurement process weakne sses resulted in a nonseismically qualified sy nchronizati on switch being instal led in an otherwise operable e mergency diesel genera tor and a non conforming fuel oil nipple pa ssing receipt i nspection.
Identification and Resolution of Problems
* The team reviewed 237 corrective action program documents, apparent and root cause analyses, as well as supporting documents to assess problem identification and resolution activities. Based on this review, the team found the licensees process to identify, prioritize, evaluate, and correct problems was generally effective; thresholds for identifying issues remained appropriately low and, in most cases, corrective actions were adequate to address conditions adverse to quality. However, a number of issues were identified associated with the proper identification of degraded conditions in the plant. The team reviewed corrective actions associated with these degraded conditions and design issues at Waterford Steam Electric Station, Unit 3, which had crosscutting aspects in the area of problem identification and resolution.


Example 3: Th e N RC id ent ifi ed tha t th e l ice nse e mi sse d se ve ral op por tun iti es t o i den tif y the c onta inme nt fan coo ler cond ensa te fl ow swi tche s tha t di d no t mee t the des ign requirements f or detecting a one gallon per minut e reactor coolant system leak (NRC Inspec tion R eport 0 50003 82/200 5005-0 1).Example 4: Control roo m operators missed several opportunities over a 32
The team concluded that a positive safety-conscious work environment exists at Waterford Steam Electric Station, Unit 3, based upon interviews conducted with plant personnel. The team determined that employees and contractors feel free to raise safety concerns to their supervision or bring concerns to the employee concerns program.
.5 hour period to i dentify that a vacuum had been draw n on the reacto r coolant sy stem during refueling outage drai ndown con ditions (sel f-revealing, NRC Inspection Report 05000 382/20 05010-03).Historical Issue Example: The NRC id entified the l icensee fail ed to identi fy an inappro priate val ue of the unfiltered in-l eakage parameter used to calculate the control ro om operator dose for design basis accident con ditions i nvolvi ng radiological releases (N RC Inspectio n Report 05000 382/20 04006-01). b.Prioritiz ation and E valuatio n of Issues (1)Inspection Sc ope The team revie wed condi tion reports, en gineering operabi lity ev aluations, a nd operations op erability determination s to assess the licensee'
s ability to evalu ate the importance of the co nditions ad verse to qual ity. The team review ed a sample of condi tion r eports , failu re mode anal yses, appar ent ca use an d root cause analy ses, to ascertain w hether the li censee iden tified and con sidered the ful l extent o f conditions, Enclo sure-5-generic impli cations, common c auses, and pre vious occ urrences. The team also observed manag ement oversigh t of th e signif icant co nditions adverse t o qualit y, inc lud ing o ne C orre ctiv e Ac tion Rev iew Boa rd me etin g.In addition , the inspecto rs review ed license e evalua tions of selecte d industry operating experience reports, incl uding licen see event reports, NRC gene ric letters, NR C bulleti ns, NRC information notices, and generic ven dor notices to assess w hether issues appli cable to Waterford S team El ectric Stati on, Un it 3, w ere ap propri ately addre ssed. The tea m performe d a hi storic al rev iew of cond ition report s cov ering t he la st 5 y ears regarding the high p ressure safety i njection sy stem, the emergency diesel genera tors, main fee dwat er iso latio n val ves, essent ial c hill ers, an d the d ry co olin g towe r to determine if the l icensee had appropriatel y addressed long-standing i ssues and tho se that mi ght be a ge depe ndent.A listing of spe cific documents re viewe d during the i nspection i s included in the attach ment to this r eport. (2)Assessment The team concluded that pr oblems were generally prioritized and evaluated in accordance with the licensee's corrective action progr am guidance and NRC requirements. The team foun d that for the sampl e of root cause an alyses rev iewed, th at the license e was genera lly sel f critical and exhaustiv e in its re search into th e history of significant condi tions adv erse to quality. Howev er, the team found on e example of ineffecti ve pr oblem eval uatio n duri ng this insp ectio n. Current Issues Example 1: The inspectors discovere d the lice nsee had cate gorized the fai lure of a fuel oil p ipe n ippl e in t he Eme rgency Dies el Gen erator B in 2 002, a s a con ditio n adv erse to quali ty. Th e lic ensee follo wed Proced ure EN-LI-102 , "Corr ectiv e Acti on Pro cess,"Revisio n 4, in making the determination of significance. The inspectors foll owed the steps o f Proced ure EN-LI-102 and a rrive d at th e same leve l of si gnifica nce, h owev er, the procedure p rovides a provisi on for the Condi tion Revi ew Group to change the lev el of significance, as warranted by the conditi ons. The insp ectors determined that this w as a significant co ndition ad verse to qual ity becau se the failure rendered one emergency diese l ino perabl e. The Emergen cy Di esel Generat or A ex perie nced a failu re of it s corresponding fuel oil nip ple in 20 05. The lice nsee determined this failure was a significant condi tion adve rse to quality solely because of the re petitive nature of the failure. c.Effectiveness of Correc tive Acti ons (1)Inspection Sc ope The team revie wed 237 condition reports to veri fy that correctiv e actions rel ated to the issues wer e identif ied and imp lement ed in a time ly manner commen surate with safe ty, includin g corrective a ctions to add ress common cause or generic conce rns. The team Enclo sure-6-review ed correctiv e actions pl anned and i mplemented by the licen see and sampl ed specific techni cal issues to determine w hether adequate d ecisions re lated to structure
, syste m, and c ompone nt ope rabil ity w ere mad e. In addition , the team revi ewed a s ample of those co ndition rep orts written to address NRC inspe ction findings to ensure that the corrective actions adequate ly addres sed the issues as described in the inspection report writeups. T he team also reviewed a sample of corrective ac tions close d to other cond ition reports and programs, such a s work and engineering work req uests to ensure that the condit ion described was adequately addressed and corrected.


A listing of spe cific documents re viewe d during the i nspection i s included in the attach ment to this r eport. (2)Assessment The effectiveness of id entified correcti ve action s to address a dverse cond itions w as generally adequate. The tea m evaluated several occurrences where the licensee did not effect ivel y add ress co nditi ons ad verse to qual ity a nd cor rectiv e acti ons ta ken we re untimely a nd inapprop riate. These i ncluded fiv e examples , one identi fied by the te am and fou r by other NRC inspect ions, wher e the licen see fa iled to tak e promp t corre ctive acti ons to re sol ve l ong-s tand ing i ssue s. Th e tea m al so e val uate d ni ne o ther find ings identified by the NRC ba seline i nspection pro gram and other NRC inspection s at Waterf ord Steam Ele ctric Station, Unit 3, sin ce the last p roblem identi fication and resolut ion inspec tion tha t had cro sscutt ing aspe cts rela ted to pr ompt an d eff ective correc tive actio ns to r esolv e cond ition s adv erse to quali ty. Current Issues Example 1: The re actor c oolan t drai ndow n proc edure failed to id entify that te mporary vent rigs, required by procedur e to properly establish vent paths, included in-line ball valves in series with the vent path a nd also fail ed to direct th ose ball valves be opened to esta blis h the v ent pa th. The lice nsee w as aw are of a nd di d not fi x the proce dure to addres s the b all v alve s in 2 002 (N RC Ins pecti on Rep ort 050 00382/20050 10-02).Example 2: The NRC i dentified the l icensee fail ed to correct the condition which resulted in multiple cy cle timer failu res in the es sential chi ller (NRC Inspection Report 05000 382/20 05002-01).Example 3: The NRC identified the licensee failed to prevent recu rrence of throug h wall pipe leakage on the main stea m line Pi pe 2MS2-123. This defici ency resul ted in an unisolabl e steam leak requiri ng NRC approv al to dev iate from the America n Society of Mech anica l Engi neers Boil er and Press ure Co de Cas e N523-2 to p erform tem porary repai rs prev entin g a pla nt shu tdow n (NRC Inspe ction Repor t 0500 0382/2 00500 4-03).
Inspector-Identified and Self-Revealing Findings None


Enclo sure-7-Historical Issues Example 1: The NRC i dentified the l icensee fail ed to correct a known deficie nt condition involv ing the failure to account for ins trument uncertainty to satisfy Techn ical Specification Surveil lance Require ment 4.7.6.5.a. This failure potenti ally affects the abil ity o f the con trol ro om env elope to per form its design functio n wi th resp ect to protecting operators from postulated de sign basis ac cidents resul ting in radio logical relea ses (N RC Ins pecti on Rep ort 050 00382/20040 06-03).Example 2: The NRC i dentified the l icensee fail ed to correct a known deficie nt condition involv ing multiple occasions of accumulator ov erpressure condi tions resulti ng from degraded hydraulic fluid adversely aff ecting the main feedwater isolation valve hydraulic actuator pressure re lief system. These over pressur e conditions potentially result in valve closure stroke ti mes outside de sign basis v alues (NRC Inspection Report 05000 382/20 04005-03).Example 3: The N RC id entifi ed the lice nsee fai led to prompt ly c orrect insta nces w here the main feedwater isolation valve actuator therm al relief valves failed to properly function. In one case, the li censee failed to properly address sy stem operabil ity and, for a 2-week peri od, actual v alve ope rability was unknow n (NRC Inspe ction Report 05000 382/20 04006-02).Example 4: The NRC i dentified the l icensee fail ed to correct de ficiencies i n the emergency dies el generator lo ading and fuel oil consumpti on analy sis. The li censee inappropriately closed a corrective action requiring the revisions, which subsequently resulted in the failure to mai ntain design control of the emergenc y diesel generator fuel oil s torage i nven tory r equire ments to ensur e a 7-d ay po stacci dent fue l oil inv entory (NRC I nspect ion R eport 0 50003 82/200 4002-0 5).Example 5: The NRC i dentified the l icensee fail ed to determine the cause an d precl uded r ecurre nce of ma in ste am iso latio n sol enoid-opera ted du mp val ve fai lures. The inspectors n oted that the l icensee's apparent cause did not pro vide an extent of condition a nalysis for the solenoi d-operated v alve fail ure (NRC Insp ection Report 05000 382/20 04004-03).Example 6: The N RC id entifi ed the lice nsee fai led to take ad equate correc tive actio n to ensure the torque a pplied to the flow con trol valv e for Accumulator B of main feedwate r isolation Valve 1 was sufficient to prevent an o-ring from extrudi ng, resulting in a loss-of-system hy draulic flui d and renderi ng the valv e inoperabl e (NRC Inspe ction Report 05000 382/20 04008-02).Example 7: The N RC id entifi ed the lice nsee fai led o n multi ple o ccasi ons to correc t a known defici ent co nditi on in volv ing the failu re to a ccount for ins trument uncer tainty to satisfy Techni cal S pecifi catio n Surv eill ance R equire ment 4.7.6.5.a. This fa ilure potentiall y affects the abil ity of the con trol room env elope to pe rform its design function with respect to protecting oper ators from pos tulated design basis accidents result ing in radio logica l rel eases (NRC I nspect ion R eport 0 50003 82/200 4006-0 3).
=REPORT DETAILS=


Enclo sure-8-Example 8: The licens ee failed to re place know n age-degraded o-rin gs affecting the main feedwater isolation valves in the Yea r 2000 resulti ng in o-ring failu re and inoperabil ity of the Train A feedwater i solation v alve on December 27, 20 03 (NRC I nspect ion R eport 0 50003 82/200 4002-0 1).Example 9: The NRC i dentified the l icensee fail ed to establi sh appropriate torque specification to ensure adequate o-ring compressio n that ultimate ly led to an o-ring failure and the inoperabi lity of the Trai n A main feedw ater isolati on valv e. The licen see had previ ously i dentified conce rns related to inadequate w ork instructions for performing maintenance ac tivities on the main feedwater isol ation val ves (NRC Inspection Report 05000 382/20 04002-02). d.Assessment of Safety-C onscious Work Environment (1)Inspection Sc ope The team intervi ewed 24 indivi duals from the li censee's staff, represen ting a cross sectio n of funct ional organi zati ons an d supe rvis ory a nd non superv isory perso nnel. These intervi ews assess ed whethe r conditions existed that woul d challen ge the establ ishmen t of a sa fety-co nscio us wo rk envi ronmen t. The t eam in tervi ewed the si te employ ee con cerns p rogram co ordin ator. (2)Assessment The team conclud ed that a posi tive safety-co nscious w ork environment exists at W aterford Steam Electric Station, Unit 3. Based on interviews, station personnel felt free to enter issues into th e corrective action program , raise safety concerns with their supervisi on, to the empl oyee conce rns program, and to th e NRC. The te am determined that the majority of safety concerns were addre ssed through the s ite's normal chain of command by the relative ly few sa fety concerns en tered into the employee c oncerns program and the sm all number of allegations made t o the NRC.
==OTHER ACTIVITIES (OA)==
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==


e.Specific Issues Identified Duri ng this Inspecti on (1)Inspection Sc ope During this assessment, the team perform ed the inspections scoped in Secti ons 4OA 2 a.(1), 4OA2 b.(1), 4 OA2 c.(1), and 4OA2 d.(1) ab ove. (2)Finding Details (i)Unresolve d Item: 05000382/2 006008-01 , "Failure to Maintai n Design Con trol of the Pressurizer Surge Line" Introduction. The team iden tified an unres olved i tem related to co mpliance w ith 10 CFR Part 50 , Appe ndix B, Cri terion III, "De sign C ontrol ," for the failu re to tr ansla te design-basi s heat up and cool down rates for the p ressur izer surge l ine i nto ap propri ate specifications , procedures, an d instruction s. As a resul t, Entergy Operatio ns, Inc., failed Enclo sure-9-to effectively control and e valuate p ressurizer s urge line tempera ture changes on numero us occ asion s. Description. Final Safety Analysi s Report (FSAR) Section 5.4
a. Effectiveness of Problem Identification
.3.1, "Reactor Co olant Pipi ng Desi gn Basi s," and Secti on 5.4.10.1, "Press uriz er Des ign Ba sis," s tates, in pa rt, that duri ng he atup and coo ldo wn of the pla nt, t he a llo wab le r ate o f temp erat ure c hang e for the s urge li ne is limi ted to 200°F/hr. Tec hnica l Requ iremen ts Ma nual (TRM), Section 3.4.8.2 , "Pressurize r Heatup/Cool down," spec ifies the li miting conditi on for operation, in part, as a max imum heatup rate of 200°F per hour and a maxi mum coold own rate of 1 35°F p er hou r.On Apri l 18, 2005, Entergy Condi tion R eport C R-WF3-2005-1 392 st ated th at a pressu rize r surge line temper ature t ransi ent oc curred wit h the s urge li ne temp erature dropping from 425°F to 140°F, a change of appr oximately 285°F with approximately 200°F occurr ing w ithin 8 minu tes. Tec hnica l Requ iremen ts Ma nual, Secti on 3.4.8.2 Actio n spec ifies, "With any o f the pre ssuriz er li mits i n exc ess of th e abov e, the operat ors must restore the affected pa rameter to wi thin the li mits withi n 30 minutes; perform an engineering ev aluation to determine the effects of the out-of-limit cond ition on th e structu ral i ntegrit y of th e pres suriz er; and enter TRM L CO 3.0.3." The team noted that Entergy Operation s, Inc., failed to restore pressuriz er/surge line limit s wi thin 3 0 minu tes an d perfor m an en gineer ing ev aluat ion to determ ine th e effects of the out-of-limit con dition on the structural i ntegrity of the pres surizer/surge l ine. The team review ed Entergy Opera tions, Inc.'s o perating procedure s for plant heatup and coold own activ ities , OP-01 0-005, "Plan t Shutd own," and OP-010-0 03, "Pl ant Sta rtup,"and did no t find procedure steps to limi t surge line te mperature changes to less than 200°F/hr, nor w ere there any procedure step s to assess w hether surge li ne stress or fatigue limits had been exc eeded. This a ppeared to be a viola tion of 10 CFR Part 50, Appendix B, Criterion III, "Design Contr ol," for the f ailure to translate design-bas is heatup and co oldown rates for the pressuri zer surge li ne into app ropriate speci fications, proced ures, a nd in structi ons. The des ign li mit in Repor t CEN-387-P was b ased, in pa rt, by temper ature gr adien ts greater than 200°F occurring less than 3.6 occurre nces per heatu p/cooldow n cycle for 500 heatup/coo ldown c ycles ov er the 40-ye ar life of the pl ant. Calcul ation CN-OA-04-53 documented 19 i nstances w here pressuriz er insurges, in excess of the v olume of the surge line, occ urred with a temperature gradi ent greater than 20 0°F. These pressu rizer insurges occurred during five refuel ing outage heatup/c ooldown cycles (R efueling Outages 8-12)for an av erage of 3.8 temperature gradi ents greater than 20 0°F per heatup/cooldo wn cycl e.Entergy Operation s, Inc. disagreed and provi ded a paper (Attachment B), w hich documented thei r position.
: (1) Inspection Scope The inspectors reviewed items selected across four of the seven cornerstones to determine if problems were being properly identified, characterized, and entered into the corrective action program for evaluation and resolution. Specifically, the teams review included a selection of 237 condition reports, equipment walkdowns, review of operator logs, maintenance records, and station quarterly trend reports. The majority of the condition reports were opened and closed since the last NRC problem identification and resolution inspection completed on May 21, 2004. The team also performed a historical review of condition reports written over the last 5 years for the high pressure safety injection system, main feedwater isolation valves, main steam isolation valves, essential chillers, and the emergency diesel generators. The team reviewed a sample of licensee audits and self assessments, trending reports, system health reports, and various other reports and documents related to the problem identification and resolution program.


While they acknowle dged that the FSA R was no t up to date, they stated th at the pressuri zer surge li ne temperature trans ient on Apri l 18, 2005, was bounded by Combustion E ngineering Own ers Group Report CEN-387-P, "Pre ssurizer Surge Line Flow Stratification Evaluation," subm itted to the NRC in response to NRC Bull etin 8 8-11, "Pressu rize r Surge Line Thermal Strati ficatio n." Report CEN-3 87-P concluded th at the pressuri zer surge li ne met all a pplicabl e design code s, FSAR, and Enclo sure-10-other regulatory commitments for the li censed life o f the plant consi dering the phenomenon of thermal stratification i n fatigue and stress evaluati ons. The team note d that this conclusion was based on operating the plant consist ent with the assumptions in the evalu ation (Report CEN-387-P). A dditional inspection is required to complete the review of Entergy Operatio ns, Inc.'s, positi on and determi ne whethe r the licens ee was operating their facility w ithin the a ssumptions of the a nalysis.Analysis. The significance of this issue depends on w hether or not the analysi s bounds past plant op eration. Enforcement. The p otenti al fai lure t o trans late t he des ign ba sis i nto ap propri ate specifications , procedures, an d instruction s to effectively control and evaluate surge line tempera ture ch anges, d uring p lant h eatup and co oldow n, that exce eded t hose l imits descri bed i n the F SAR a nd the TRM i s unre solv ed: (U RI 050 00382/20060 08-01);"Fail ure to Mai ntain Desi gn Cont rol of t he Pre ssuriz er Surge Line." (ii)Unresolve d Item 05000382
The audit and self-assessment results were compared with the self-revealing and NRC-identified issues to determine the effectiveness of the audits and self assessments.
/2006008-02 , "Failure to Ensure that Written Procedures Adequately Incorporate Regul atory Require ments and Desi gn Basis"Introduction. The te am ide ntifie d an u nresol ved i tem rel ated to compl iance wit h Technical Sp ecification, S ection 6.8.1, for the failure to ens ure that wri tten procedures adequately i ncorporate regulato ry requirements a nd the design basis for the dry cooling tower die sel-drive n sump pumps.


Description. Waterford Safety Evaluation Report, Suppl ement 4, Sectio n 2.4.2.3, discusses the design basi s rainfall ev ent and combi nation of eve nts. This suppl ement commits the li censee to the probable max imum precipita tion even t. Because of the fact that the motor-driv en sumps are no t seismicall y qualified, the NRC requeste d the licensee a nalyze the effects of a standard p roject storm, whi ch consists o f 50 percent of the probable maximum precipation event concur rent with an operating basis earthquake. The results of the licensee's analysis showed the licensee was susceptible to ponding in the dry co oling towe r sumps, assuming the loss of all motor-driven pumps, which w ould endan ger the safety-relate d transformers and motor c ontrol centers located in the cool ing tow er area s. The li censee submi tted Am endmen t 34, d ated J anuary 1984, subse quent to Safety Evaluati on Report, Sup plement 4. Se ction 2.4.2.3.4 of this amendment su bmittal contains an analysi s showin g the probabil ity of standard project storm and operating basis earthquake i s 3.6E-08, w hich is co nsidered negl igible. Ho wever, th e licensee prop osed to pr ovide a 100 g pm po rta ble pu mp th at wou ld be s uff icien t to p ump d own the dry cooling tower sumps in the event of the standar d project storm.
The team interviewed station personnel and evaluated corrective action documentation to determine the licensees threshold for identifying problems and entering them into the corrective action program. In addition, in order to assess the licensees handling of operator experience, the team reviewed the licensees evaluation of selected industry operating experience reports, including licensee event reports, NRC generic letters, NRC bulletins, and NRC information notices, and generic vendor notifications to assess if issues applicable to Waterford Steam Electric Station, Unit 3, were appropriately addressed.


The NRC determined that the portable p ump was sufficie nt (as evi denced in Safety Eval uation Report , Supp lement 4) pro vide d the p ump w as pl aced i n oper ation wit hin 6 hours. In 2000, after determini ng that more sump pumpi ng capacity was neede d, the licen see installed a diesel-dri ven sump pu mp, with 30 0 gpm capacity , in each d ry cooli ng tower sump. The Design Basis Cal culation E C-M99-010 analyz ed for a probabl e maximum precipation event, concu rrent with a loss-of-offsite powe r, and determine d that a higher capacity portable pump was needed. The calculation also analyzed for a rainfall equivalent to 60 percent o f the probable max imum precipati on event, co ncurrent wi th a loss o f all mo tor-dri ven s ump pum ps, an d dete rmined that a 300 gp m porta ble p ump Enclo sure-11-would b e sufficient. The li censee's Pro cedure OP-100-01 4, "Technical Specification s and Requirements Compliance,"
A listing of specific documents reviewed during the inspection is included in the attachment to this report.
Revisio n 14, states tha t two motor-dri ven sump pu mps or one motor-driv en pump and o ne diesel-driven pu mp are required for ul timate heat sink operabil ity. This p rocedure impl ies that the d iesel dri ven sump pu mp can be out of ser vi ce i nde fin ite ly wi tho ut a ffec tin g op era bi li ty of t he ul tim ate he at s in k. Th e N RC sta ff believes this procedure does not adequately address the requirement of the portable sump pu mp in t he des ign ba sis of t he ul timate heat s ink, no r does the pr ocedu re requi re any compensa tory actions be taken in th e event the diesel-dri ven sump pu mp becomes inope rable. Als o, the staff bel ieve s the c ontrol s and locat ion o f the di esel-driv en sump pump ar e not a dequate ly a ddress ed by the l icens ee. Analysis. The significance of this issue h as not been d etermined.
: (2) Assessment The team determined that, in general, problems were adequately identified and entered into the corrective action program, as evidenced by the relatively few findings identified during the assessment period. The licensees threshold for entering issues into the corrective action program was appropriately low. However, the team found two examples of ineffective problem identification during this inspection. The licensee also failed in some instances to identify or document deficiencies, which resulted in NRC noncited violations.


Enforcement. The licens ee has prov ided a pos ition pape r (Attachment C) rel ated to the design basis requirements for the dry cooling tow er diesel-dri ven sump pu mps, which has no t been fully revi ewed by th e NRC. The p otenti al fai lure t o ensu re regul atory require ments for these pumps is un resol ved: (URI 0 50003 82/200 6008-0 2) "Fai lure t o Translate Desi gn Control in to Station Do cuments Regarding D iesel-driv en Dry Co oling Tower Sump P umps" 4OA6 Exit M eeting The team discusse d the findings of the Problem Identi fication and R esolution i nspection with Mr. J. Venable, Vice President Operations, and other me mbers of the licensee's staff on March 24, 2006. Licen see management did not identi fy any materi als exami ned during the inspe ction as proprie tary.The licensee acknowledged the f indings presented. The inspect ors noted that while propri etary informa tion w as rev iew ed, no ne w ould be in clude d in t his re port.ATTACHMENT A
Current Issues Example 1: The licensee failed to identify multiple temperature changes of the pressurizer surge line, which exceeded the heatup and cooldown rate described in Section 5.4.3.1 of the stations Final Safety Analysis Report. Specifically, the inspection team discovered during a plant shutdown in August 2005 that the pressurizer surge line had experienced 19 changes in temperature, which exceeded this limit. This example is further described in Section 4OA2.e of this report.
: Supplementa l Information ATTACHM ENT B: Waterford 3 Pr essuri zer S urge Li ne Tempe rature Change Rate ATTACHM ENT C: White Pape r on Effec t of Die sel S ump Pu mp Inop erabi lity on Ul timate Heat Sink Op erabi lity Attach ment A A-1 KEY POINTS OF CONTACT Licensee Pe rsonnel B. Baxter, C ontrol Room S upervisor C. DeDeaux Sr., Senior P roject Manager, L icensing R. Dodds, M anager, Operations R. Fletcher, Trai ning Mana ger C. Fugate, Assis tant Operations M anager J. Hall, Opera tions Trainin g Supervisor - Operator Requali fication J. Holman, M anager, Nuclear Engineering J. Laque, Man ager, Mainten ance R. Muril lo, Senior Staff Engineer R. Osbo rne, M anager, Engin eerin g Programs and C ompone nts A. Pilutti, Manager, Rad iation Prote ction O. Pipkins, Seni or Licensin g Engineer R. Porter, Superi ntendent, M echanical Maintena nce B. Proctor, Sy stems Engineerin g Manager J. Rachal, D esign Engineeri ng Superviso r J. Ridgel, M anager, Correctiv e Action Pro gram T. Tankersley, Actin g Director, Nucl ear Safety Assu rance K. Walsh, General Mana ger, Plant Operatio ns B. Williams, Engineering D irector J. Venable, Site Vice President, Waterford 3 NRC M. Hay , Senior Re sident Inspecto r Waterford 3 LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened 05000382/2006 008-01 URI Fai lure to M ain tain Des ign C ontr ol o f the Pres suri zer Sur ge Line (Secti on 4OA 2 e.)05000382/2006 008-02 URI Fail ure to Transl ate De sign C ontrol into Statio n Docu ments Regarding Diese l-driven Dry Cool ing Tower Sump Pumps (Secti on 4OA 2 e.)


Attach ment A A-2 LIST OF DOCUMENTS REVIEWED Plant Proced ures NAME TITLE REVIS ION CEP-IS T-1 IST Bases Docume nt 3 EN-OP-115 Conduct of Operatio ns 0 LI-102 Corrective Action Proce ss 4 LI-19645 Quali ty Re lated Admin istrat ive Proced ure 2 MM-006-119 Yard Oil Se parator to CW Temporary Pumping S ystem 0 OI-042-000 Watch Station Procedures 1 OP-001-003 Reac tor Coola nt Sys tem Drain down 23 OP-005-004 Main S team 12 OP-009-008 Safety Injection System 18 OP-100-001 Operations Stan dards and M anagement Expe ctations 22 OP-100-009 Contro l of Va lves and B reakers 17 OP-100-0014 Techni cal S pecifi catio n and Techni cal R equire ments Compliance 13 UNT-005-004 Temporary Altera tion Control 16 Engine ering R eports ER-W3-2002-0055 ER-W3-2004-0537 ER-W3-2005-0426 ER-W3-00-0337 ER-W3-2003-0010 ER-W3-2005-0305 ER-W3-2002-0278 Calculati ons CN-OA-04-53 EC-M99-01 0 MN(Q)-6-27 Root Cause A nalysis Reports for CR-WF3-2001-0317 2002-0339 2003-0062 2003-3891 2004-759 2004-1011 Attach ment A A-3 Condition Reports, CR-WF3-1997-1227 2000-0441 2000-1347 2000-1455 2001-0596 2001-0673 2001-0782 2001-1284 2001-1367 2002-0468 2002-0470 2002-0588 2002-0678 2002-1410 2002-1842 2002-2799 2003-0147 2003-0577 2003-1192 2003-1202 2003-2758 2003-2759 2003-2991 2003-3088 2003-3649 2003-3891 2004-0251 2004-0304 2004-0309 2004-0326 2004-0420 2004-0464 2004-0483 2004-0494 2004-0508 2004-0634 2004-0651 2004-0701 2004-0703 2004-0721 2004-0759 2004-0821 2004-0835 2004-0865 2004-0903 2004-1011 2004-1047 2004-1190 2004-1208 2004-1312 2004-1340 2004-1446 2004-1480 2004-1518 2004-1553 2004-1572 2004-1593 2004-1621 2004-1645 2004-1646 2004-1668 2004-1679 2004-1684 2004-1716 2004-1751 2004-1753 2004-1763 2004-1810 2004-1850 2004-1854 2004-1855 2004-1863 2004-1880 2004-1942 2004-2002 2004-2228 2004-2290 2004-2320 2004-2326 2004-2382 2004-2404 2004-2487 2004-2496 2004-2517 2004-2520 2004-2522 2004-2545 2004-2547 2004-2549 2004-2638 2004-2690 2004-2722 2004-2734 2004-2766 2004-2884 2004-2890 2004-2928 2004-2973 2004-2995 2004-3066 2004-3130 2004-3200 2004-3219 2004-3244 2004-3413 2004-3460 2004-3464 2004-3695 2004-3720 2004-3725 2004-3753 2004-3853 2004-3881 2004-3924 2004-3944 2004-3949 2004-4000 2005-0033 2005-0081 2005-0098 2005-0109 2005-0132 2005-0134 2005-0197 2005-0217 2005-0346 2005-0413 2005-0415 2005-0471 2005-0489 2005-0530 2005-0587 2005-0590 2005-0591 2005-0592 2005-0608 2005-0717 2005-0763 2005-0804 2005-0805 2005-0806 2005-0839 2005-0852 2005-0921 2005-0966 2005-0967 2005-1132 2005-1143 2005-1173 2005-1247 2005-1260 2005-1279 2005-1315 2005-1332 2005-1346 2005-1362 2005-1363 2005-1392 2005-1463 2005-1626 2005-1646 2005-1694 2005-1821 2005-1836 2005-2070 2005-2139 2005-2267 2005-2272 2005-2350 2005-2402 2005-2469 2005-2489 2005-2536 2005-2546 2005-2548 2005-2600 2005-2679 2005-2685 2005-2695 2005-2780 2005-2799 2005-2819 2005-2837 2005-2844 2005-2869 2005-2874 2005-2990 2005-3006 2005-3091 2005-3293 2005-3308 2005-3455 2005-3474 2005-3659 2005-3698 2005-3812 2005-3822 2005-3830 2005-3831 2005-3840 2005-3872 2005-3872 2005-3902 2005-3914 2005-3924 2005-3928 2005-3960 2005-3961 2005-3985 2005-4038 2005-4065 2005-4066 2005-4067 2005-4147 2005-4149 2005-4151 2005-4173 2005-4251 2005-4444 2005-4480 2005-4597 2005-4647 2005-4694 2005-4915 2005-4917 2005-4929 2005-5024 2006-0006 2006-0058 2006-0164 2006-0200 2006-0380 2006-0492 2006-0759 2006-0767 2006-0839 2006-0895 Attach ment A A-4 Learni ng Organi zati on Con ditio ns Rep orts LO-OPX-2004-0247 LO-OPX-2005-0100 LO-OPX-2005-0217 LO-OPX-2006-0011 LO-OPX-2005-0036 LO-OPX-2005-0103 LO-OPX-2005-0243 LO-OPX-2006-0034 LO-OPX-2005-0085 LO-OPX-2005-0132 LO-OPX-2005-0252 Work Orders 51697 51699 52824 52825 57759 62641 72604 72606 412565 4281801 4599901 5100331101 Mai ntenan ce Act ion It ems 420105 438981 Mis cell aneou s Docu ments Commercial Grade Evaluati on 01214 C-PAC-002 L-19645 L-23993 MMR Project 53465 PO WPY20583 2004 S econd Quarter Waterford Quart erly Trend R eport 2004 Th ird Qua rter Waterford Qu arterl y Tren d Repo rt 2004 F ourth Qu arter Waterford Quarter ly Tre nd Rep ort Quali ty As suranc e Audi t Repo rt QA-12-20050-WF3-1 Quality A ssurance Audi t Report QA-12-200 50-WF3-009 Quali ty As suranc e Audi t Repo rt QA-12-20050-WF3-1 PO 10083675 INITIAL MATERIAL REQUEST INITIAL INFORMA TION REQUEST FROM WATERFORD 3 FOR PI&R INSP ECTION (Report Numbe r 05000382/200 4006)The inspection will cover the period of October 2 002 to Ma rch 2004. The i nformation may be provided in either electronic or paper media or a combination ther eof. Infor mation provided in electronic med ia may be in the form of CDs, or 3-1/2 inch floppy disks. The agency
Example 2: The team found the licensee's identification of adverse trends to be weak.
's text ed iting software is C orel WordPerfect 8, Presentations, and Quattro Pro; h owever, we hav e document viewi ng capabili ty for MS Word, Excel , Power Po int, and Ado be Acrobat (.pdf) tex t files.Please prov ide the follo wing informatio n to Peter Al ter by M arch 29, 2004 at the Resid ent Inspec tor Office at Waterford-3 Attach ment A A-5 All proced ures governin g or applyi ng to the correctiv e action program, i ncluding the processing of informatio n regarding generic communications and industry operating experience s Procedures and description s of any informal systems, used by engine ering, operation s, maintenance, security, tr aining, and emergency planning f or issues below the threshold of the formal correctiv e action program A sear chabl e tabl e of al l corr ectiv e acti on doc uments (condi tion r eports) that w ere initiated or closed du ring the period , include condition re port number, descri ption of issue and s ignificance cl assification Either annota te on the abo ve list or a separate l ist of all co ndition rep orts associated with: (1)Human performance i ssues (2)Emergency prepare dness issues (3)Respo nse to 10 CF R Part 21 rep orts A separate l ist of all co ndition rep orts closed to other programs, such a s maintenance action items/w ork orders, engineeri ng requests, etc.


A copy of eac h significant ev ent review team report and root cause ana lysis rep ort for the pe riod (not ne cessar ily the w hole condi tion r eport)Copies of cond ition reports (for the period) ass ociated w ith nonescal ated (no respon se required) or nonc ited vio lations for the period Copies of cond ition reports for the period as sociated w ith repetitiv e problems or issues Copies of condition reports f or the period associated with ineffec tive or untimely corrective a ctions List of all s elf assessments or quality ass urance assessmen ts/audits for the pe riod All correcti ve action program reports or metri cs used for tracking effective ness of the corrective a ction program for the pe riod All quali ty assurance audits and surveill ances, and functi onal self asse ssments of corrective a ction activ ities comple ted for the period Control room l ogs for the Year 2003 Security e vent logs for the year 2003 Radiation protection ev ent logs for the y ear 2003 List o f risk si gnifica nt sy stems fro m W3 PRA/PSA , base d on ri sk achi eveme nt wo rth (RAW) and "0% availabi lity CD F" Attach ment A A-6 Searchable list of all maintenance ac tion items/w ork orders for the perio d List of all S SC's plac ed in or remov ed from the maintenan ce rule a(1) c ategory for the period All correcti ve action documents rela ted to the follo wing indu stry operatin g experience generic communica tions: NRC Bull etins NRC Bull etin 2002-001 , "Reactor Pressu re Vessel H ead Degradation and Reactor Coolant Pressur e Boundar y Integ rity"NRC Information N otices NRC Information N otice 2004-00 1, "Auxil iary Feed water Pump R ecirculatio n Line Orifice Fouling - Po tential Common Cause Fai lure"NRC In formatio n Noti ce 200 3-019, "Unan alyz ed Con ditio n of Rea ctor Co olant Pump Seal Leakoff Li ne Dur ing Po stula ted Fi re Sce nario s or St ation Blac kout"NRC Information Notice 2003-013, "Steam Generat or Tube Degradation at Diablo Canyon"NRC Information N otice 2003-01 1, "Leakage Found o n Bottom-Moun ted Instrumentation No zzles"NRC In formatio n Noti ce 200 3-008, "Poten tial Flood ing Thro ugh Uns ealed Concr ete Floor Cracks" NRC Information N otice 2003-00 5, "Failure to Detect Freesp an Cracks in P WR Steam Generator Tubes" NRC Information N otice 2003-00 2, "Recent Ex perience With Reactor Coo lant Syste m Leakage And Bori c Acid Corro sion"NRC Information N otice 2002-03 4, "Failure of Safety-Related Circuit Brea ker External Auxili ary Swi tches at Colu mbia Generating S tation" Attach ment A A-7 Information Reque st 1 - January 2006 Waterford PIR Ins pection (IP 711 52; Inspection Report 50-382/0 6-08)The inspection will cover the period of M arch 1, 2004 to March 1, 2006. All requested information shoul d be limite d to this peri od unless o therwise s pecified. The in formation may be provided in either e lectronic or paper media o f a combination of this media. Informatio n provided in electroni c media may be in the form of e-mai l attachment(s), CD s, or 3 1/2 inch floppy disks. The agency's tex t editing softwa re is Corel WordPerfect 10, Presentations, and Quattro Pro; ho wev er, w e hav e docu ment v iew ing cap abil ity fo r MS Word, Excel , Pow erPoi nt, and Adobe A crobat (pdf.) text fil es.Please prov ide the follo wing by February 8 , 2006, to:
The inspection team reviewed 17 conditions reports, in which the licensee documented inadequacies in the procurement of replacement parts for the station. The licensee had identified a trend of improper parts passing through the receipt inspection, but failed to identify adverse trends related to lack of engineering involvement, as required by the procurement process; failure to perform professional engineering evaluations for parts transferred into the system; and receipt inspection documents missing required attributes. These procurement process weaknesses resulted in a nonseismically qualified synchronization switch being installed in an otherwise operable emergency diesel generator and a nonconforming fuel oil nipple passing receipt inspection.
U.S. Nuclear Regulatory C ommission Resident Inspector's Of fice - Attn. Gran t Larkin Waterford Stea m Elec tric S tation Unit 3 Entergy Operation s, Inc.17265 Riv er Road Killona, Louisiana 70066 Note: On summary li sts please i nclude a d escription o f problem, status, in itiating date, and owner organi zation 1.Summary lis t of all condi tion reports op ened during the period 2.Summary list of all open condi tion r eports wit h signi ficance of "B" o r greate r whi ch we re generated during the period 3.Summary lis t of all condi tion reports w ith significanc e of "B" or greater clo sed during the specified peri od 4.Summary list of all condition reports which were down-graded or up-g raded in significance du ring the period 5.A list of all corrective action documen ts that subsume o r "roll-up" on e or more small er issues for the pe riod 6.List of all ro ot cause anal yses comple ted during the p eriod 7.List of all a pparent cause analyses completed duri ng the period 8.List of root cause analyse s planned, b ut not complete at end of the peri od 9.List of plant sa fety issues rai sed or address ed by the employee c oncerns program during the peri od 10.List of action i tems generated or ad dressed by the plant safety review committees during the peri od Attach ment A A-8 11.Summary list of oper ator w ork-arou nds, e nginee ring re view request s and/or ope rabil ity evaluati ons, temporary mo difications, sa fety system defici encies, and control room deficiencies 12.All quali ty assurance audits and surveill ances of correctiv e action acti vities co mpleted during the peri od 13.A list of all quality a ssurance audi ts and surve illances scheduled for co mpletion duri ng the period, bu t which were not co mpleted 14.All corrective action activity reports, funct ional area self-assessmen ts, and non-NRC third party assessments compl eted during the period 15.Corrective action performance tre nding/tracking information generated during the period and broken dow n by function al organiza tion 16.Curren t proce dures/poli cies/gu idel ines for: 1.Condition Reporting 2.Corrective Action Program 3.Root Cause E valuatio n/Determination 4.Deficiency Reporting and R esolution 17.A listing of al l external events ev aluated for appl icabili ty at Waterford during the period 18.Cond ition Repor ts or othe r act ions gene rat ed f or ea ch of the it ems b elow [A DAMS access ion n umbers or othe r cross referen ce li sted for some]: 1.Part 21 Reports (2005-41-00; 20 05-38-00 [ml053 180299]; 2005-3 7-00;2005-33-01 [ml0 52860229]; 200 5-30-01 [ml0526 40220]; 2005-26-01[ml052 91038 9]; 200 5-22-0 0; 200 5-20-0 0; 200 5-17-0 0 [ml05 11100 87];2005-16-00 [ml0 51100285]; 200 5-13-00 [ml0509 50428]; 2005-12-01[ml052 08036 8]; 200 5-12-0 0 [ml05 06302 75]; 20 05-10-00 [ml0 50560 142];2005-0 7-00; 2 005-05-01 [ml 05110 0355]; 2005-01-00 [ml043 52007 7];2004-27-01 [ml0 43280541]; 200 4-24-00 [ml0424 70299]; 2004-22-00[ml042 66017 5]; 200 4-21-0 0 [ml04 25200 48]; 20 04-17-00 [ml0 41900 058];2004-15-00; 200 4-14-00; 2004-10-00 [ml0411403 35]; 2004-08-00
[ml041110893]; 2 004-02-01 [ml04 0420567]2.NRC Information N otices 05-32; 05-31; 05-30; 05-29; 05-26; 05-25
; 05-24; 05-23; 05-21; 05-19
; 05-16; 05-11; 0 5-09; 05-08; 05-0 6; 05-02; 04-021
; 04-019; 04-016; 04-012; 04-011; 04-010; 04-009; 04-008; 04-007; 04-001 3.All LERs issued by Waterford during the period 4.NCVs and V iolations issued to Waterford during the peri od 19.Safeguards event l ogs for the period 20.Rad iati on p rote ctio n ev ent l ogs Attach ment A A-9 21.Current system health reports or similar i nformation 22.Current predicti ve performance su mmary reports or s imilar informati on 23.Corrective action effectiven ess review reports generated d uring the perio d
ATTAC HM ENT B Waterford 3 Pres surizer Surge Lin e Temperature Change R ate Waterford 3 Pressurizer Surge Line Temperature Change RatePage 1 of 4PurposeThis Paper is to document the Entergy position on the potential NCV of 10CFR50Appendix B, Criterion III, "Design Control" for not translating design basis criteriainto plant operating procedures. The design basis criteria in question is astatement in the FSAR (Section 5.4.3.1) which states:During heatup and cooldown of the plant, the allowable rate oftemperature change for the surge line is increased to 200°F/hr as a designrequirement specified in Subsection 3.9.1.1.BackgroundThe following is a time line of the Entergy response to NRC Bulletin No. 88-11.This concludes that the fatigue life of the Waterford 3 surge line is 40 years whichthe NRC concurred with.* The NRC issued NRC Bulletin No. 88-11, Pressurizer Surge Line ThermalStratification, on December 20, 1988. The purpose of the Bulletin was torequest that addressees establish and implement a program to confirmpressurizer surge line integrity in view of the occurrence of thermalstratification and to inform the staff of the actions taken to resolve thisissue.* CEN-387-P was transmitted to the NRC on July 27, 1989. Thisdocumented that the Waterford 3 surge line fatigue life is longer than 40years.* On August 28, 1989, Entergy sent a letter to the NRC stating that Bulletin88-11 item 1b, 1c and 1d were addressed in CEN-387-P and that item 1a(visual inspection of the pressurizer surge line) would be addressed duringthe next refueling outage.* On March 7, 1990, Entergy sent a letter to the NRC which addressed theresults of the visual inspections of the pressurizer surge line. The letterconcluded that the Waterford 3 surge line was structurally sound.* On August 15, 1990, the NRC issued a letter stating there was not enoughinformation in the CEN document to conclude that the pressurizer surgeline meets all appropriate Code limits for a 40 year plant life.* On December 20, 1991, CEN-387-P, Revision 1-P was sent to the NRC toaddress the concerns of the August 15, 1990 NRC evaluation of the CENdocument.* On May 5, 1992, Entergy sent a letter to the NRC documenting thesubmittal of the revised CEN document and stated the only remainingaction to complete the response to the Bulletin is for the Waterford 3 toupdate the pressurizer surge line design documentation. This wascommitted to be completed within 180 days of issuance of a favorableSER by the NRC.


Waterford 3 Pressurizer Surge Line Temperature Change RatePage 2 of 4* On June 22, 1993, the NRC issued an SER for CEN-387-P, Revision 1. Itwas concluded that the analysis in the CEN adequately demonstrates thatthe bounding surge line and nozzles meet ASME Code stress and fatiguerequirements for the 40 year design life of the facility considering thephenomenon of thermal stratification and thermal stripping. The staffrequested Entergy to provide a final status of the Waterford 3 activitiesrequired by NRC Bulletin 88-11.* On December 23, 1993, Entergy sent a letter to the NRC stating that alldesign documents had been updated and that all actions required by NRCBulletin 88-11 had been completed.CEN-387-P, Revision 1, is the Combustion Engineering response to NRCBulletin 88-11. This document addresses pressurizer surge line flowstratification. The document provides a detailed fatigue analysis of stress due tostratified temperature profiles of the fluid in the pressurizer surge line. Note thatthis document indicates that thermal stratification is assumed for all surge flow asthe velocities will always be low. This document also specifically indicates thatthe stratified temperature analysis envelopes high velocity flow and thermalshock.The following paragraphs are excerpted from the Thermal Striping Analysis forthe pressurizer surge line in CEN-387-P, Revision 1. The conclusion is the"effect of thermal striping is negligible and will not affect the fatigue life of thepressurizer surge line".The term "striping" refers to the thermal oscillations that occur at the hot-cold interface.The period of oscillations was chosen to be 1 second and 4 seconds forthe surge line analysis. Test data was measured or was empiricallydetermined to be in the range of 1 second to 10 seconds. For the largetemperature differences and high heat transfer coefficient used in thisanalysis, the period is closer to 1 second than 4 seconds. A longer periodwould yield a lower heat transfer coefficient, and therefore smallerchanges in metal temperatures. However, to be conservative, the sameheat transfer coefficient was used for all cases.The stresses due to each gradient as a function of time were calculatedusing formulas in ASME Code Section III, NB-3653.2. Table 3.5.3-2 liststhe alternating stress calculated for each of the four transients used forevaluating fatigue. As can be seen from this table only one of the fourtransients contributes anything to fatigue. That transient is number four(4) with an alternating stress of 15,780 psi and a number of allowablecycles of 1.42E7.
Example 3: The NRC identified that the licensee missed several opportunities to identify the containment fan cooler condensate flow switches that did not meet the design requirements for detecting a one gallon per minute reactor coolant system leak (NRC Inspection Report 05000382/2005005-01).


Waterford 3 Pressurizer Surge Line Temperature Change RatePage 3 of 4Waterford 3 Design Specification 9270-PE-140 is the project specification forreactor coolant pipe and fittings. This document provides a summary of thedesign analysis for surge line temperature transients. It includes text sectionsand 2 tables as they apply to the surge line and surge line nozzle. The tablesaddress temperature differences anticipated as a result of thermal stratification.Table 4.5.15.3.1 lists expected occurrences of temperature differences betweenthe pressurizer and the RCS hot leg and provides the number of expectedoccurrences. Table 4.5.15.3.2 lists expected occurrences of temperaturedifferences between the top and bottom of the surge line piping. Thesetemperatures differences are for the pressurizer surge line piping and not thefluid temperature in the piping. The number of occurrences is the expectednumber for the life of the plant.Entergy PositionThe Entergy position is that pressurizer surge line temperature is not required tobe specifically monitored per procedure to ensure the design limits aremaintained, and that FSAR Section 5.4.3.1 should have been revised in 1993when the Waterford 3 stress and fatigue analyses and design specifications wererevised per NRC Bulletin 88-11 to reflect the results of CEN-387-P, Revision 1.This section of the FSAR has not been revised since the initial FSAR. CR-WF3-2006-0839 was initiated to revise the FSAR. The reasoning for Entergy'sposition is documented in the paragraphs below.The pressurizer surge line temperatures during heatup and cooldown aremaintained by ensuring the heatup and cooldown limits in the RCS andpressurizer are maintained. The RCS limits are located in the TS and thepressurizer limits are located in the TRM. Temperature changes in the surge linecan be greater than 200°F due to thermal stratification and thermal stripping.CEN-387-P, Revision 1 documented that the pressurizer surge line meets Codestress and fatigue requirements for the 40 year design life of the facilityconsidering the phenomenon of thermal stratification and thermal stripping.Analysis in the CEN has indicated that temperature differences of up to 340°Fhave been evaluated for.The data recorded by the temperature element in the surge line has shownperiods of temperature changes greater than 200°F/hr. Thermal stratification isapplicable to all of these recorded temperature changes. These temperaturechanges do not necessarily reflect the average temperature change of the surgeline but reflects a change in local fluid temperature at the temperature element.This recorded temperature changes over time are not the same deltatemperatures listed in the tables in 9270-PE-140.Therefore, the temperature difference in the pressurizer surge line is bounded bythe analysis performed in CEN-387-P, Revision 1 and monitoring pressurizer Waterford 3 Pressurizer Surge Line Temperature Change RatePage 4 of 4surge line temperature per procedure during heatup and cooldown is notnecessary.Additional InformationThe additional information specifically addresses the difference between thesurge line temperature increase seen during Refuel 13 and during the shutdownfor Hurricane Katrina, and the delta temperature values in 9720-PE-140. It alsoaddresses the reason Waterford 3 does not currently monitor surge linetemperature during heatups and cooldowns.There following information is clarification regarding cycles listed in DesignSpecification 9270-PE-140 and the temperatures recorded in PI with thetemperature element located in the surge line. The graphical data recording thesingle surge line temperature element over time for our Refuel 13 outage and theHurricane Katrina outage indicates periods of temperature changes greater than200 degrees within one hour. Thermal stratification is applicable to all of theserecorded temperature changes. Thermal stratification temperature changes wereaddressed by CEN-327-P (NRC accepted response to NRC Bulletin 88-11). Thissingle temperature element does not necessarily reflect the average temperaturechange of the surge line but reflects a change in local fluid temperature at thetemperature element. The recorded temperature changes of a single point overtime is not the same delta temperatures listed in the tables of the W3 Designspecification of RCS Piping and Fitting document (document #9270-PE-140).The table 4.5.15.3.1 lists expected occurrences of temperature differencesbetween two different locations; the pressurizer and the RCS hot leg andprovides the number of expected occurrences. Table 4.5.15.3.2 lists expectedoccurrences of temperature differences between the top and bottom of the surgeline piping. These tables clearly state this information at the end of theirrespective sections. Thus comparing a graph of temperature changes withrespect to time to these tables is not appropriate.The effects on the Pressurizer Surge Line due to thermal stratification andthermal stripping were evaluated in CEN-327-P, Revision 1. This was reviewedby the NRC and in the SER the Staff concluded that the surge line meets ASMECode stress and fatigue requirements for the 40-year design life. Waterford 3currently monitors heatups and cooldowns of the RCS and Pressurizer. Theeffects of these heatups and cooldowns on the pressurizer surge line have beenevaluated in CEN-327-P.
Example 4: Control room operators missed several opportunities over a 32.5 hour period to identify that a vacuum had been drawn on the reactor coolant system during refueling outage draindown conditions (self-revealing, NRC Inspection Report 05000382/2005010-03).


ATTAC HM ENT C White Paper on Effect of Diesel Sump Pump Inoperability on Ultimate H eat Sink Operab ility 11.0 PurposeThis paper provides an answer to the question, what is the original licensingbasis for flood protection of essential equipment in the Dry Cooling Tower Areas?The paper also provides the chronology of regulatory requirements and licensingbases that support the conclusion.2.0 Conclusion Regarding Licensing BasisThe original licensing basis for essential equipment in the Dry Cooling Towerareas is that essential equipment be protected from Standard Project Storm(SPS).The elements of the licensing basis are the following:§The SPS, with all installed sump pumps inoperative, was analyzed as anevent less severe than the probable maximum precipitation.§Provisions are required to be in place for emplacing the portable sump pumpwithin 6 hours of an SPS event to ensure that the ponding level from SPSdoes not adversely affect essential equipment if installed pumps areinoperative.§The electric pumps are seismically designed but not seismically qualified;therefore they were assumed not to be available following an OBE.§The probability of the occurrence of an SPS and OBE is 3.6E-8 andnegligible.In essence, the original licensing basis required that the portable sump pump beemplaced and started within 6 hours of the start of an SPS (sump high levelalarm) to ensure that essential equipment in the DCT areas is not flooded.On July 26, 1999, Condition Report CR-WF3-1999-0789 was initiated to identifythat the Dry Cooling Tower sump pump capacities were not sufficient to meet theoriginal licensing basis.A new discharge path for the DCT sump pumps was installed via DCP-3251.The DCP also replaced the 1 portable sump pump that had a capacity of 100gpm with 2 portable sump pumps having a capacity of 300 gpm each. Theinstalled sump pump's capacities were reduced from 325 gpm to 270 gpm due tothe new piping configuration. The revised time frame for starting the portablesump pump to ensure essential equipment is not flooded was re-established as 3hours from the start of an SPS (sump high level alarm). Procedure OP-901-521instructs Operations to operate the DCT Portable Sump Pumps in accordancewith OP-003-024, Sump Pump Operation within 3 hours of the sump level alarm.
Historical Issue Example: The NRC identified the licensee failed to identify an inappropriate value of the unfiltered in-leakage parameter used to calculate the control room operator dose for design basis accident conditions involving radiological releases (NRC Inspection Report 05000382/2004006-01).


23.0 ChronologyRegulatory Guide 1.70, Revision 2, September 1975Waterford 3 is committed to Regulatory Guide 1.70, Revision 2, as noted insection 1.8 of FSAR. Neither Regulatory Guide Section 2.4.2.3, "Effects of LocalIntense Precipitation," or Section 2.4.3.1, "Probable Maximum Precipitation(PMP)," have any requirement to consider OBE or SPS concurrently.Regulatory Guide Section 2.4.2.3 states:"Describe the effects of local probable maximum precipitation (see Section2.4.3.1) on adjacent drainage areas and site drainage systems, includingdrainage from the roofs of structures. Summarize the design criteria for sitedrainage facilities and provide analyses that demonstrate the capability of sitedrainage facilities to prevent flooding of safety related facilities resulting fromlocal probable maximum precipitation."The fundamental requirement in the Regulatory Guide is that the applicantensures that safety related equipment is not adversely impacted from maximumprecipitation.Regulatory Guide 1.59, Revision 2, August 1977Waterford 3 is committed to Regulatory Guide 1.59, Revision 2, as noted insection 1.8 of FSAR. Regulatory Guide 1.59, Revision 2, does not have aspecific requirement to consider OBE and SPS concurrently.Two important requirements are discussed in the Regulatory Guide.First, seismically induced floods are associated with land features specific toeach site such as streams, estuaries, dam failures, and landslides. Thisrequirement does not apply to flooding in the DCT sump areas.Second, the Regulatory Guide states that the most severe flood conditions maynot indicate potential threats to safety related systems that might result fromcombination of flood conditions thought to be less severe. The Regulatory Guidestates that reasonable combinations of less severe flood conditions should beconsidered to the extent needed. The Regulatory Guide states that suchcombinations should be evaluated in cases where theprobability of theirexisting at the same time and having significant consequences is at leasecomparable to that associated with the most severe hydro-meteorological orseismically induced flood. We judge that the requirement to consider the SPSoriginates from this requirement. Also, since the probability of a SPS and OBEconcurrent was later established to be negligible, we judge that not consideringthe SPS concurrent with the OBE is in conformance with the Regulatory Guide.
b. Prioritization and Evaluation of Issues
: (1) Inspection Scope The team reviewed condition reports, engineering operability evaluations, and operations operability determinations to assess the licensees ability to evaluate the importance of the conditions adverse to quality. The team reviewed a sample of condition reports, failure mode analyses, apparent cause and root cause analyses, to ascertain whether the licensee identified and considered the full extent of conditions,


3Standard Review Plan 2.4.3, Revision 2 July 1981Standard Review Plan 2.4.3 does not have a specific requirement to considerOBE and SPS concurrently.Standard Review Plan 2.4.3, Section I, states:Included is a review of the details of site drainage-, including the roofs of safetyrelated structures, resulting from potential PMP probable maximumprecipitation-"Standard Review Plan 2.4.3, Section IV, states:"The local PMF resulting from the estimated local PMP was found not to causeflooding of safety related facilities, since the site drainage system will be capableof functioning adequately during such a storm."The fundamental requirement in the Standard Review Plan is that the applicantensures that safety related equipment is not adversely impacted form maximumprecipitation.NRC Safety Evaluation Report, July 1981The NRC evaluates the effects of a 6-hr duration PMP on the open cooling towerareas and adjacent roofs. The NRC concludes that, assuming one sump pumpin each area is inoperable and that the roof drainage system is clogged withdebris during the PMP, that the ponding could inundate the transformers andMCC's in the cooling tower areas.The Safety Evaluation Report makes no reference to SPS or OBE.FSAR Amendment 25, January 1982FSAR Section 2.4.2.3.4 was initially added to the FSAR; previously it did notexist. This FSAR Section is titled, "Effects of Standard Project Storm (SPS) onCooling Tower Areas".Two important aspects of the licensing basis are established in this FSARSection.First, a probability evaluation is documented establishing that the occurrence ofan SPS and OBE is 3.6 E-8 and negligible.Second, FSAR Section states that the SPS was still analyzed, assuminginoperability of all pumps, in order to determine the time available before levelsare reached that could affect essential equipment in the Cooling Tower Areas.
generic implications, common causes, and previous occurrences. The team also observed management oversight of the significant conditions adverse to quality, including one Corrective Action Review Board meeting.


4Safety Evaluation Report, Supplement 4, October 1982The SER states the following:"An alternative combination which should be considered is an operating basisearthquake (OBE), which fails the sump pumps, coincident with a rainfall eventless than the PMP. This combination is considered appropriate since the pumpsare not seismically qualified1, and thus cannot be shown to be operable followinga seismic event. The staff therefore, requested that the applicant provide ananalysis of the effects of a standard project storm (SPS)2 assuming all fourpumps in the cooling tower areas are inoperable."The SER further states:"-the staff considered a SPS of 96 hours duration. This event would produce atotal rainfall of about 23 inches and would result in a ponding depth of about 1.9ft in the cooling tower areas assuming that all four pumps are inoperable. Sincethis is higher than the maximum allowable ponding depth of 1.71 feet, theapplicant has proposed to provide a portable pump with a pumping capacity of100 gpm and sufficient head to pump over the cooling tower wall. -a provisionwill be included for emplacing the portable pump within 6 hours of a seismicevent if the installed pumps fail."FSAR Amendment 33, September 1983FSAR Amendment 33 revises Section 2.4.2.3.4 to state the following:"The maximum height to which rainwater can rise in this area before essentialequipment is reached is 1.71 ft (see subsection 2.4.2.3.3d). As shown in Table2.4-6c, this level would not be reached for over seven hours into the SPS.""Furthermore, a portable pump is provided, with a pumping capacity of 100 gpmand sufficient head to pump over the cooling tower wall. Provisions are includedfor emplacing the portable pump within six hours of a seismic event if theinstalled pumps fail and heavy rains are expected."Thus, the FSAR Amendment 33 is in agreement with NRC SER Supplement 4 inthat the fundamental requirement is to protect essential equipment in the coolingtower areas in the event of a SPS. The specific requirement in FSARAmendment 33 is that provisions be made for emplacing the portable sumppump within 6 hours of a SPS event and that essential equipment be protected,by ensuring that the ponding level does not reach 1.71 ft. The seismic event is avehicle to postulate the installed pumps are not available; however, important tothe licensing basis is the condition that the electric sump pumps will not beavailable and that essential equipment needs to be protected prior to the pondinglevel reaching 1.71 ft.
In addition, the inspectors reviewed licensee evaluations of selected industry operating experience reports, including licensee event reports, NRC generic letters, NRC bulletins, NRC information notices, and generic vendor notices to assess whether issues applicable to Waterford Steam Electric Station, Unit 3, were appropriately addressed.


5NRC Letter dated December 18 1984, Issuance of Five Percent Power License,The NRC issues five percent power license, and Section 2.B.2 of the licenseapproves operation as described in FSAR as supplemented and amendedthrough Amendment 36.NRC Letter dated March 16, 1985, Issuance of 100% Power LicenseThe NRC issues 100 percent power license, and Section 2.B.2 of the licenseapproves operation as described in FSAR as supplemented and amendedthrough Amendment 36.Design Change, July 26, 1999On July 26, 1999, Condition Report CR-WF3-1999-0789 was initiated to identifythat the Dry Cooling Tower sump pump capacities were not sufficient to meet theoriginal licensing basis.A new discharge path for the DCT sump pumps was installed via DCP-3251.The DCP also replaced the 1 portable sump pump that had a capacity of 100gpm with 2 portable pumps having a capacity of 300 gpm each. The installedsump pump's capacities were reduced from 325 gpm to 270 gpm due to the newpiping configuration. The revised time frame for ensuring essential equipment isnot flooded was re-established as 3 hours from the start of SPS (sump high levelalarm). Procedure OP-901-521 instructs Operations to operate the DCT PortableSump Pumps in accordance with OP-003-024, Sump Pump Operation within 3hours of the sump level alarm.
The team performed a historical review of condition reports covering the last 5 years regarding the high pressure safety injection system, the emergency diesel generators, main feedwater isolation valves, essential chillers, and the dry cooling tower to determine if the licensee had appropriately addressed long-standing issues and those that might be age dependent.
 
A listing of specific documents reviewed during the inspection is included in the attachment to this report.
: (2) Assessment The team concluded that problems were generally prioritized and evaluated in accordance with the licensees corrective action program guidance and NRC requirements. The team found that for the sample of root cause analyses reviewed, that the licensee was generally self critical and exhaustive in its research into the history of significant conditions adverse to quality. However, the team found one example of ineffective problem evaluation during this inspection.
 
Current Issues Example 1: The inspectors discovered the licensee had categorized the failure of a fuel oil pipe nipple in the Emergency Diesel Generator B in 2002, as a condition adverse to quality. The licensee followed Procedure EN-LI-102, Corrective Action Process, Revision 4, in making the determination of significance. The inspectors followed the steps of Procedure EN-LI-102 and arrived at the same level of significance, however, the procedure provides a provision for the Condition Review Group to change the level of significance, as warranted by the conditions. The inspectors determined that this was a significant condition adverse to quality because the failure rendered one emergency diesel inoperable. The Emergency Diesel Generator A experienced a failure of its corresponding fuel oil nipple in 2005. The licensee determined this failure was a significant condition adverse to quality solely because of the repetitive nature of the failure.
 
c. Effectiveness of Corrective Actions
: (1) Inspection Scope The team reviewed 237 condition reports to verify that corrective actions related to the issues were identified and implemented in a timely manner commensurate with safety, including corrective actions to address common cause or generic concerns. The team
 
reviewed corrective actions planned and implemented by the licensee and sampled specific technical issues to determine whether adequate decisions related to structure, system, and component operability were made.
 
In addition, the team reviewed a sample of those condition reports written to address NRC inspection findings to ensure that the corrective actions adequately addressed the issues as described in the inspection report writeups. The team also reviewed a sample of corrective actions closed to other condition reports and programs, such as work and engineering work requests to ensure that the condition described was adequately addressed and corrected.
 
A listing of specific documents reviewed during the inspection is included in the attachment to this report.
: (2) Assessment The effectiveness of identified corrective actions to address adverse conditions was generally adequate. The team evaluated several occurrences where the licensee did not effectively address conditions adverse to quality and corrective actions taken were untimely and inappropriate. These included five examples, one identified by the team and four by other NRC inspections, where the licensee failed to take prompt corrective actions to resolve long-standing issues. The team also evaluated nine other findings identified by the NRC baseline inspection program and other NRC inspections at Waterford Steam Electric Station, Unit 3, since the last problem identification and resolution inspection that had crosscutting aspects related to prompt and effective corrective actions to resolve conditions adverse to quality.
 
Current Issues Example 1: The reactor coolant draindown procedure failed to identify that temporary vent rigs, required by procedure to properly establish vent paths, included in-line ball valves in series with the vent path and also failed to direct those ball valves be opened to establish the vent path. The licensee was aware of and did not fix the procedure to address the ball valves in 2002 (NRC Inspection Report 05000382/2005010-02).
 
Example 2: The NRC identified the licensee failed to correct the condition which resulted in multiple cycle timer failures in the essential chiller (NRC Inspection Report 05000382/2005002-01).
 
Example 3: The NRC identified the licensee failed to prevent recurrence of through wall pipe leakage on the main steam line Pipe 2MS2-123. This deficiency resulted in an unisolable steam leak requiring NRC approval to deviate from the American Society of Mechanical Engineers Boiler and Pressure Code Case N523-2 to perform temporary repairs preventing a plant shutdown (NRC Inspection Report 05000382/2005004-03).
 
Historical Issues Example 1: The NRC identified the licensee failed to correct a known deficient condition involving the failure to account for instrument uncertainty to satisfy Technical Specification Surveillance Requirement 4.7.6.5.a. This failure potentially affects the ability of the control room envelope to perform its design function with respect to protecting operators from postulated design basis accidents resulting in radiological releases (NRC Inspection Report 05000382/2004006-03).
 
Example 2: The NRC identified the licensee failed to correct a known deficient condition involving multiple occasions of accumulator overpressure conditions resulting from degraded hydraulic fluid adversely affecting the main feedwater isolation valve hydraulic actuator pressure relief system. These over pressure conditions potentially result in valve closure stroke times outside design basis values (NRC Inspection Report 05000382/2004005-03).
 
Example 3: The NRC identified the licensee failed to promptly correct instances where the main feedwater isolation valve actuator thermal relief valves failed to properly function. In one case, the licensee failed to properly address system operability and, for a 2-week period, actual valve operability was unknown (NRC Inspection Report 05000382/2004006-02).
 
Example 4: The NRC identified the licensee failed to correct deficiencies in the emergency diesel generator loading and fuel oil consumption analysis. The licensee inappropriately closed a corrective action requiring the revisions, which subsequently resulted in the failure to maintain design control of the emergency diesel generator fuel oil storage inventory requirements to ensure a 7-day postaccident fuel oil inventory (NRC Inspection Report 05000382/2004002-05).
 
Example 5: The NRC identified the licensee failed to determine the cause and precluded recurrence of main steam isolation solenoid-operated dump valve failures.
 
The inspectors noted that the licensees apparent cause did not provide an extent of condition analysis for the solenoid-operated valve failure (NRC Inspection Report 05000382/2004004-03).
 
Example 6: The NRC identified the licensee failed to take adequate corrective action to ensure the torque applied to the flow control valve for Accumulator B of main feedwater isolation Valve 1 was sufficient to prevent an o-ring from extruding, resulting in a loss-of-system hydraulic fluid and rendering the valve inoperable (NRC Inspection Report 05000382/2004008-02).
 
Example 7: The NRC identified the licensee failed on multiple occasions to correct a known deficient condition involving the failure to account for instrument uncertainty to satisfy Technical Specification Surveillance Requirement 4.7.6.5.a. This failure potentially affects the ability of the control room envelope to perform its design function with respect to protecting operators from postulated design basis accidents resulting in radiological releases (NRC Inspection Report 05000382/2004006-03).
 
Example 8: The licensee failed to replace known age-degraded o-rings affecting the main feedwater isolation valves in the Year 2000 resulting in o-ring failure and inoperability of the Train A feedwater isolation valve on December 27, 2003 (NRC Inspection Report 05000382/2004002-01).
 
Example 9: The NRC identified the licensee failed to establish appropriate torque specification to ensure adequate o-ring compression that ultimately led to an o-ring failure and the inoperability of the Train A main feedwater isolation valve. The licensee had previously identified concerns related to inadequate work instructions for performing maintenance activities on the main feedwater isolation valves (NRC Inspection Report 05000382/2004002-02).
 
d.
 
Assessment of Safety-Conscious Work Environment
: (1) Inspection Scope The team interviewed 24 individuals from the licensees staff, representing a cross section of functional organizations and supervisory and nonsupervisory personnel.
 
These interviews assessed whether conditions existed that would challenge the establishment of a safety-conscious work environment. The team interviewed the site employee concerns program coordinator.
: (2) Assessment The team concluded that a positive safety-conscious work environment exists at Waterford Steam Electric Station, Unit 3. Based on interviews, station personnel felt free to enter issues into the corrective action program, raise safety concerns with their supervision, to the employee concerns program, and to the NRC. The team determined that the majority of safety concerns were addressed through the sites normal chain of command by the relatively few safety concerns entered into the employee concerns program and the small number of allegations made to the NRC.
 
e.
 
Specific Issues Identified During this Inspection
: (1) Inspection Scope During this assessment, the team performed the inspections scoped in Sections 4OA2 a.(1), 4OA2 b.(1), 4OA2 c.(1), and 4OA2 d.(1) above.
: (2) Finding Details
: (i) Unresolved Item: 05000382/2006008-01, Failure to Maintain Design Control of the Pressurizer Surge Line
 
=====Introduction.=====
The team identified an unresolved item related to compliance with 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to translate design-basis heatup and cooldown rates for the pressurizer surge line into appropriate specifications, procedures, and instructions. As a result, Entergy Operations, Inc., failed
 
to effectively control and evaluate pressurizer surge line temperature changes on numerous occasions.
 
=====Description.=====
Final Safety Analysis Report (FSAR) Section 5.4.3.1, Reactor Coolant Piping Design Basis, and Section 5.4.10.1, Pressurizer Design Basis, states, in part, that during heatup and cooldown of the plant, the allowable rate of temperature change for the surge line is limited to 200°F/hr. Technical Requirements Manual (TRM),
Section 3.4.8.2, Pressurizer Heatup/Cooldown, specifies the limiting condition for operation, in part, as a maximum heatup rate of 200°F per hour and a maximum cooldown rate of 135°F per hour.
 
On April 18, 2005, Entergy Condition Report CR-WF3-2005-1392 stated that a pressurizer surge line temperature transient occurred with the surge line temperature dropping from 425°F to 140°F, a change of approximately 285°F with approximately 200°F occurring within 8 minutes. Technical Requirements Manual, Section 3.4.8.2 Action specifies, "With any of the pressurizer limits in excess of the above, the operators must restore the affected parameter to within the limits within 30 minutes; perform an engineering evaluation to determine the effects of the out-of-limit condition on the structural integrity of the pressurizer; and enter TRM LCO 3.0.3."
 
The team noted that Entergy Operations, Inc., failed to restore pressurizer/surge line limits within 30 minutes and perform an engineering evaluation to determine the effects of the out-of-limit condition on the structural integrity of the pressurizer/surge line. The team reviewed Entergy Operations, Inc.s operating procedures for plant heatup and cooldown activities, OP-010-005, Plant Shutdown, and OP-010-003, Plant Startup, and did not find procedure steps to limit surge line temperature changes to less than 200°F/hr, nor were there any procedure steps to assess whether surge line stress or fatigue limits had been exceeded. This appeared to be a violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to translate design-basis heatup and cooldown rates for the pressurizer surge line into appropriate specifications, procedures, and instructions.
 
The design limit in Report CEN-387-P was based, in part, by temperature gradients greater than 200°F occurring less than 3.6 occurrences per heatup/cooldown cycle for 500 heatup/cooldown cycles over the 40-year life of the plant. Calculation CN-OA-04-53 documented 19 instances where pressurizer insurges, in excess of the volume of the surge line, occurred with a temperature gradient greater than 200°F. These pressurizer insurges occurred during five refueling outage heatup/cooldown cycles (Refueling Outages 8-12)for an average of 3.8 temperature gradients greater than 200°F per heatup/cooldown cycle.
 
Entergy Operations, Inc. disagreed and provided a paper (Attachment B), which documented their position. While they acknowledged that the FSAR was not up to date, they stated that the pressurizer surge line temperature transient on April 18, 2005, was bounded by Combustion Engineering Owners Group Report CEN-387-P, Pressurizer Surge Line Flow Stratification Evaluation, submitted to the NRC in response to NRC Bulletin 88-11, Pressurizer Surge Line Thermal Stratification. Report CEN-387-P concluded that the pressurizer surge line met all applicable design codes, FSAR, and
 
other regulatory commitments for the licensed life of the plant considering the phenomenon of thermal stratification in fatigue and stress evaluations. The team noted that this conclusion was based on operating the plant consistent with the assumptions in the evaluation (Report CEN-387-P). Additional inspection is required to complete the review of Entergy Operations, Inc.'s, position and determine whether the licensee was operating their facility within the assumptions of the analysis.
 
=====Analysis.=====
The significance of this issue depends on whether or not the analysis bounds      past plant operation.
 
=====Enforcement.=====
The potential failure to translate the design basis into appropriate specifications, procedures, and instructions to effectively control and evaluate surge line temperature changes, during plant heatup and cooldown, that exceeded those limits described in the FSAR and the TRM is unresolved: (URI 05000382/2006008-01);
    "Failure to Maintain Design Control of the Pressurizer Surge Line."
: (ii) Unresolved Item 05000382/2006008-02, Failure to Ensure that Written Procedures Adequately Incorporate Regulatory Requirements and Design Basis
 
=====Introduction.=====
The team identified an unresolved item related to compliance with Technical Specification, Section 6.8.1, for the failure to ensure that written procedures adequately incorporate regulatory requirements and the design basis for the dry cooling tower diesel-driven sump pumps.
 
=====Description.=====
Waterford Safety Evaluation Report, Supplement 4, Section 2.4.2.3, discusses the design basis rainfall event and combination of events. This supplement commits the licensee to the probable maximum precipitation event. Because of the fact that the motor-driven sumps are not seismically qualified, the NRC requested the licensee analyze the effects of a standard project storm, which consists of 50 percent of the probable maximum precipation event concurrent with an operating basis earthquake. The results of the licensees analysis showed the licensee was susceptible to ponding in the dry cooling tower sumps, assuming the loss of all motor-driven pumps, which would endanger the safety-related transformers and motor control centers located in the cooling tower areas.
 
The licensee submitted Amendment 34, dated January 1984, subsequent to Safety Evaluation Report, Supplement 4. Section 2.4.2.3.4 of this amendment submittal contains an analysis showing the probability of standard project storm and operating basis earthquake is 3.6E-08, which is considered negligible. However, the licensee proposed to provide a 100 gpm portable pump that would be sufficient to pump down the dry cooling tower sumps in the event of the standard project storm. The NRC determined that the portable pump was sufficient (as evidenced in Safety Evaluation Report, Supplement 4) provided the pump was placed in operation within 6 hours. In 2000, after determining that more sump pumping capacity was needed, the licensee installed a diesel-driven sump pump, with 300 gpm capacity, in each dry cooling tower sump. The Design Basis Calculation EC-M99-010 analyzed for a probable maximum precipation event, concurrent with a loss-of-offsite power, and determined that a higher capacity portable pump was needed. The calculation also analyzed for a rainfall equivalent to 60 percent of the probable maximum precipation event, concurrent with a loss of all motor-driven sump pumps, and determined that a 300 gpm portable pump
 
would be sufficient. The licensees Procedure OP-100-014, Technical Specifications and Requirements Compliance, Revision 14, states that two motor-driven sump pumps or one motor-driven pump and one diesel-driven pump are required for ultimate heat sink operability. This procedure implies that the diesel driven sump pump can be out of service indefinitely without affecting operability of the ultimate heat sink. The NRC staff believes this procedure does not adequately address the requirement of the portable sump pump in the design basis of the ultimate heat sink, nor does the procedure require any compensatory actions be taken in the event the diesel-driven sump pump becomes inoperable. Also, the staff believes the controls and location of the diesel-driven sump pump are not adequately addressed by the licensee.
 
=====Analysis.=====
The significance of this issue has not been determined.
 
=====Enforcement.=====
The licensee has provided a position paper (Attachment C) related to the design basis requirements for the dry cooling tower diesel-driven sump pumps, which has not been fully reviewed by the NRC. The potential failure to ensure regulatory requirements for these pumps is unresolved: (URI 05000382/2006008-02) "Failure to Translate Design Control into Station Documents Regarding Diesel-driven Dry Cooling Tower Sump Pumps"
{{a|4OA6}}
==4OA6 Exit Meeting==
 
The team discussed the findings of the Problem Identification and Resolution inspection with Mr. J. Venable, Vice President Operations, and other members of the licensees staff on March 24, 2006. Licensee management did not identify any materials examined during the inspection as proprietary.
 
The licensee acknowledged the findings presented. The inspectors noted that while proprietary information was reviewed, none would be included in this report.
 
ATTACHMENT A: Supplemental Information ATTACHMENT B: Waterford 3 Pressurizer Surge Line Temperature Change Rate ATTACHMENT C: White Paper on Effect of Diesel Sump Pump Inoperability on Ultimate Heat Sink Operability
 
KEY POINTS OF CONTACT Licensee Personnel B. Baxter, Control Room Supervisor C. DeDeaux Sr., Senior Project Manager, Licensing R. Dodds, Manager, Operations R. Fletcher, Training Manager C. Fugate, Assistant Operations Manager J. Hall, Operations Training Supervisor - Operator Requalification J. Holman, Manager, Nuclear Engineering J. Laque, Manager, Maintenance R. Murillo, Senior Staff Engineer R. Osborne, Manager, Engineering Programs and Components A. Pilutti, Manager, Radiation Protection O. Pipkins, Senior Licensing Engineer R. Porter, Superintendent, Mechanical Maintenance B. Proctor, Systems Engineering Manager J. Rachal, Design Engineering Supervisor J. Ridgel, Manager, Corrective Action Program T. Tankersley, Acting Director, Nuclear Safety Assurance K. Walsh, General Manager, Plant Operations B. Williams, Engineering Director J. Venable, Site Vice President, Waterford 3 NRC M. Hay, Senior Resident Inspector Waterford 3 LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened 05000382/2006008-01        URI    Failure to Maintain Design Control of the Pressurizer Surge Line (Section 4OA2 e.)
 
05000382/2006008-02        URI    Failure to Translate Design Control into Station Documents Regarding Diesel-driven Dry Cooling Tower Sump Pumps (Section 4OA2 e.)
 
A
 
LIST OF
 
=DOCUMENTS REVIEWED=
 
Plant Procedures
NAME                                  TITLE                          REVISION
CEP-IST-1          IST Bases Document                                            3
EN-OP-115          Conduct of Operations                                        0
LI-102              Corrective Action Process                                    4
LI-19645            Quality Related Administrative Procedure                      2
MM-006-119          Yard Oil Separator to CW Temporary Pumping System            0
OI-042-000          Watch Station Procedures                                      1
OP-001-003          Reactor Coolant System Draindown                            23
OP-005-004          Main Steam                                                  12
OP-009-008          Safety Injection System                                      18
OP-100-001          Operations Standards and Management Expectations            22
OP-100-009          Control of Valves and Breakers                              17
OP-100-0014        Technical Specification and Technical Requirements          13
Compliance
UNT-005-004        Temporary Alteration Control                                16
Engineering Reports
ER-W3-2002-0055      ER-W3-2004-0537      ER-W3-2005-0426        ER-W3-00-0337
ER-W3-2003-0010      ER-W3-2005-0305      ER-W3-2002-0278
Calculations
CN-OA-04-53      EC-M99-010          MN(Q)-6-27
Root Cause Analysis Reports for CR-WF3-
2001-0317    2002-0339    2003-0062      2003-3891    2004-759    2004-1011
Attachment A
Condition Reports, CR-WF3-
1997-1227      2004-0759  2004-2404    2005-0109 2005-1626  2005-3831
2000-0441      2004-0821  2004-2487    2005-0132 2005-1646  2005-3840
2000-1347      2004-0835  2004-2496    2005-0134 2005-1694  2005-3872
2000-1455      2004-0865  2004-2517    2005-0197 2005-1821  2005-3872
2001-0596      2004-0903  2004-2520    2005-0217 2005-1836  2005-3902
2001-0673      2004-1011  2004-2522    2005-0346 2005-2070  2005-3914
2001-0782      2004-1047  2004-2545    2005-0413 2005-2139  2005-3924
2001-1284      2004-1190  2004-2547    2005-0415 2005-2267  2005-3928
2001-1367      2004-1208  2004-2549    2005-0471 2005-2272  2005-3960
2002-0468      2004-1312  2004-2638    2005-0489 2005-2350  2005-3961
2002-0470      2004-1340  2004-2690    2005-0530 2005-2402  2005-3985
2002-0588      2004-1446  2004-2722    2005-0587 2005-2469  2005-4038
2002-0678      2004-1480  2004-2734    2005-0590 2005-2489  2005-4065
2002-1410      2004-1518  2004-2766    2005-0591 2005-2536  2005-4066
2002-1842      2004-1553  2004-2884    2005-0592 2005-2546  2005-4067
2002-2799      2004-1572  2004-2890    2005-0608 2005-2548  2005-4147
2003-0147      2004-1593  2004-2928    2005-0717 2005-2600  2005-4149
2003-0577      2004-1621  2004-2973    2005-0763 2005-2679  2005-4151
2003-1192      2004-1645  2004-2995    2005-0804 2005-2685  2005-4173
2003-1202      2004-1646  2004-3066    2005-0805 2005-2695  2005-4251
2003-2758      2004-1668  2004-3130    2005-0806 2005-2780  2005-4444
2003-2759      2004-1679  2004-3200    2005-0839 2005-2799  2005-4480
2003-2991      2004-1684  2004-3219    2005-0852 2005-2819  2005-4597
2003-3088      2004-1716  2004-3244    2005-0921 2005-2837  2005-4647
2003-3649      2004-1751  2004-3413    2005-0966 2005-2844  2005-4694
2003-3891      2004-1753  2004-3460    2005-0967 2005-2869  2005-4915
2004-0251      2004-1763  2004-3464    2005-1132 2005-2874  2005-4917
2004-0304      2004-1810  2004-3695    2005-1143 2005-2990  2005-4929
2004-0309      2004-1850  2004-3720    2005-1173 2005-3006  2005-5024
2004-0326      2004-1854  2004-3725    2005-1247 2005-3091  2006-0006
2004-0420      2004-1855  2004-3753    2005-1260 2005-3293  2006-0058
2004-0464      2004-1863  2004-3853    2005-1279 2005-3308  2006-0164
2004-0483      2004-1880  2004-3881    2005-1315 2005-3455  2006-0200
2004-0494      2004-1942  2004-3924    2005-1332 2005-3474  2006-0380
2004-0508      2004-2002  2004-3944    2005-1346 2005-3659  2006-0492
2004-0634      2004-2228  2004-3949    2005-1362 2005-3698  2006-0759
2004-0651      2004-2290  2004-4000    2005-1363 2005-3812  2006-0767
2004-0701      2004-2320  2005-0033    2005-1392 2005-3822  2006-0839
2004-0703      2004-2326  2005-0081    2005-1463 2005-3830  2006-0895
2004-0721      2004-2382  2005-0098
Attachment A
Learning Organization Conditions Reports
LO-OPX-2004-0247        LO-OPX-2005-0100        LO-OPX-2005-0217      LO-OPX-2006-0011
LO-OPX-2005-0036        LO-OPX-2005-0103        LO-OPX-2005-0243      LO-OPX-2006-0034
LO-OPX-2005-0085        LO-OPX-2005-0132        LO-OPX-2005-0252
Work Orders
51697                52825              72604                412565              4599901
51699                57759              72606                4281801            5100331101
2824                62641
Maintenance Action Items
20105          438981
Miscellaneous Documents
Commercial Grade Evaluation 01214
C-PAC-002
L-19645
L-23993
MMR Project 53465
PO WPY20583
2004 Second Quarter Waterford Quarterly Trend Report
2004 Third Quarter Waterford Quarterly Trend Report
2004 Fourth Quarter Waterford Quarterly Trend Report
Quality Assurance Audit Report QA-12-20050-WF3-1
Quality Assurance Audit Report QA-12-20050-WF3-009
Quality Assurance Audit Report QA-12-20050-WF3-1
PO 10083675
INITIAL MATERIAL REQUEST
INITIAL INFORMATION REQUEST FROM WATERFORD 3
FOR PI&R INSPECTION (Report Number 05000382/2004006)
The inspection will cover the period of October 2002 to March 2004. The information may be
provided in either electronic or paper media or a combination thereof. Information provided in
electronic media may be in the form of CDs, or 3-1/2 inch floppy disks. The agencys text editing
software is Corel WordPerfect 8, Presentations, and Quattro Pro; however, we have document
viewing capability for MS Word, Excel, Power Point, and Adobe Acrobat (.pdf) text files.
Please provide the following information to Peter Alter by March 29, 2004 at the Resident
Inspector Office at Waterford-3
Attachment A
All procedures governing or applying to the corrective action program, including the
processing of information regarding generic communications and industry operating
experiences
Procedures and descriptions of any informal systems, used by engineering, operations,
maintenance, security, training, and emergency planning for issues below the threshold
of the formal corrective action program
A searchable table of all corrective action documents (condition reports) that were
initiated or closed during the period, include condition report number, description of
issue and significance classification
Either annotate on the above list or a separate list of all condition reports associated
with:
        (1)      Human performance issues
        (2)      Emergency preparedness issues
        (3)      Response to 10 CFR Part 21 reports
A separate list of all condition reports closed to other programs, such as maintenance
action items/work orders, engineering requests, etc.
A copy of each significant event review team report and root cause analysis report for
the period (not necessarily the whole condition report)
Copies of condition reports (for the period) associated with nonescalated (no response
required) or noncited violations for the period
Copies of condition reports for the period associated with repetitive problems or issues
Copies of condition reports for the period associated with ineffective or untimely
corrective actions
List of all self assessments or quality assurance assessments/audits for the period
All corrective action program reports or metrics used for tracking effectiveness of the
corrective action program for the period
All quality assurance audits and surveillances, and functional self assessments of
corrective action activities completed for the period
Control room logs for the Year 2003
Security event logs for the year 2003
Radiation protection event logs for the year 2003
List of risk significant systems from W3 PRA/PSA, based on risk achievement worth
(RAW) and "0% availability CDF"
Attachment A
Searchable list of all maintenance action items/work orders for the period
List of all SSCs placed in or removed from the maintenance rule a(1) category for the
period
All corrective action documents related to the following industry operating experience
generic communications:
NRC Bulletins
NRC Bulletin 2002-001, Reactor Pressure Vessel Head Degradation and Reactor
Coolant Pressure Boundary Integrity
NRC Information Notices
NRC Information Notice 2004-001, Auxiliary Feedwater Pump Recirculation Line Orifice
Fouling - Potential Common Cause Failure
NRC Information Notice 2003-019, Unanalyzed Condition of Reactor Coolant Pump
Seal Leakoff Line During Postulated Fire Scenarios or Station Blackout
NRC Information Notice 2003-013, Steam Generator Tube Degradation at Diablo
Canyon
NRC Information Notice 2003-011, Leakage Found on Bottom-Mounted
Instrumentation Nozzles
NRC Information Notice 2003-008, Potential Flooding Through Unsealed Concrete
Floor Cracks
NRC Information Notice 2003-005, Failure to Detect Freespan Cracks in PWR Steam
Generator Tubes
NRC Information Notice 2003-002, Recent Experience With Reactor Coolant System
Leakage And Boric Acid Corrosion
NRC Information Notice 2002-034, Failure of Safety-Related Circuit Breaker External
Auxiliary Switches at Columbia Generating Station
Attachment A
Information Request 1 - January 2006
Waterford PIR Inspection (IP 71152; Inspection Report 50-382/06-08)
The inspection will cover the period of March 1, 2004 to March 1, 2006. All requested
information should be limited to this period unless otherwise specified. The information may be
provided in either electronic or paper media of a combination of this media. Information
provided in electronic media may be in the form of e-mail attachment(s), CDs, or 3 1/2 inch
floppy disks. The agencys text editing software is Corel WordPerfect 10, Presentations, and
Quattro Pro; however, we have document viewing capability for MS Word, Excel, PowerPoint,
and Adobe Acrobat (pdf.) text files.
Please provide the following by February 8, 2006, to:
U.S. Nuclear Regulatory Commission
Resident Inspectors Office - Attn. Grant Larkin
Waterford Steam Electric Station Unit 3
Entergy Operations, Inc.
265 River Road
Killona, Louisiana 70066
Note: On summary lists please include a description of problem, status, initiating date, and
owner organization
1.      Summary list of all condition reports opened during the period
2.      Summary list of all open condition reports with significance of B or greater which were
generated during the period
3.      Summary list of all condition reports with significance of B or greater closed during the
specified period
4.      Summary list of all condition reports which were down-graded or up-graded in
significance during the period
5.      A list of all corrective action documents that subsume or "roll-up" one or more smaller
issues for the period
6.      List of all root cause analyses completed during the period
7.      List of all apparent cause analyses completed during the period
8.      List of root cause analyses planned, but not complete at end of the period
9.      List of plant safety issues raised or addressed by the employee concerns program
during the period
10. List of action items generated or addressed by the plant safety review committees
during the period
Attachment A
11. Summary list of operator work-arounds, engineering review requests and/or operability
evaluations, temporary modifications, safety system deficiencies, and control room
deficiencies
2. All quality assurance audits and surveillances of corrective action activities completed
during the period
13. A list of all quality assurance audits and surveillances scheduled for completion during
the period, but which were not completed
14. All corrective action activity reports, functional area self-assessments, and non-NRC
third party assessments completed during the period
15. Corrective action performance trending/tracking information generated during the period
and broken down by functional organization
16. Current procedures/policies/guidelines for:
1.      Condition Reporting
2.      Corrective Action Program
3.      Root Cause Evaluation/Determination
4.      Deficiency Reporting and Resolution
17. A listing of all external events evaluated for applicability at Waterford during the period
18. Condition Reports or other actions generated for each of the items below [ADAMS
accession numbers or other cross reference listed for some]:
1.      Part 21 Reports (2005-41-00; 2005-38-00 [ml053180299]; 2005-37-00;
2005-33-01 [ml052860229]; 2005-30-01 [ml052640220]; 2005-26-01
            [ml052910389]; 2005-22-00; 2005-20-00; 2005-17-00 [ml051110087];
2005-16-00 [ml051100285]; 2005-13-00 [ml050950428]; 2005-12-01
            [ml052080368]; 2005-12-00 [ml050630275]; 2005-10-00 [ml050560142];
2005-07-00; 2005-05-01 [ml051100355]; 2005-01-00 [ml043520077];
2004-27-01 [ml043280541]; 2004-24-00 [ml042470299]; 2004-22-00
            [ml042660175]; 2004-21-00 [ml042520048]; 2004-17-00 [ml041900058];
2004-15-00; 2004-14-00; 2004-10-00 [ml041140335]; 2004-08-00
            [ml041110893]; 2004-02-01 [ml040420567]
2.      NRC Information Notices 05-32; 05-31; 05-30; 05-29; 05-26; 05-25; 05-24; 05-
23; 05-21; 05-19; 05-16; 05-11; 05-09; 05-08; 05-06; 05-02; 04-021; 04-019; 04-
016; 04-012; 04-011; 04-010; 04-009; 04-008; 04-007; 04-001
3.      All LERs issued by Waterford during the period
4.      NCVs and Violations issued to Waterford during the period
19. Safeguards event logs for the period
20. Radiation protection event logs
Attachment A
21. Current system health reports or similar information
2. Current predictive performance summary reports or similar information
23. Corrective action effectiveness review reports generated during the period
Attachment A
ATTACHMENT B
Waterford 3 Pressurizer Surge Line Temperature Change Rate
Waterford 3 Pressurizer Surge Line Temperature Change Rate
Purpose
This Paper is to document the Entergy position on the potential NCV of 10CFR50
Appendix B, Criterion III, Design Control for not translating design basis criteria
into plant operating procedures. The design basis criteria in question is a
statement in the FSAR (Section 5.4.3.1) which states:
During heatup and cooldown of the plant, the allowable rate of
temperature change for the surge line is increased to 200°F/hr as a design
requirement specified in Subsection 3.9.1.1.
Background
The following is a time line of the Entergy response to NRC Bulletin No. 88-11.
This concludes that the fatigue life of the Waterford 3 surge line is 40 years which
the NRC concurred with.
    *  The NRC issued NRC Bulletin No. 88-11, Pressurizer Surge Line Thermal
Stratification, on December 20, 1988. The purpose of the Bulletin was to
request that addressees establish and implement a program to confirm
pressurizer surge line integrity in view of the occurrence of thermal
stratification and to inform the staff of the actions taken to resolve this
issue.
    *  CEN-387-P was transmitted to the NRC on July 27, 1989. This
documented that the Waterford 3 surge line fatigue life is longer than 40
years.
    *  On August 28, 1989, Entergy sent a letter to the NRC stating that Bulletin
88-11 item 1b, 1c and 1d were addressed in CEN-387-P and that item 1a
        (visual inspection of the pressurizer surge line) would be addressed during
the next refueling outage.
    *  On March 7, 1990, Entergy sent a letter to the NRC which addressed the
results of the visual inspections of the pressurizer surge line. The letter
concluded that the Waterford 3 surge line was structurally sound.
    *  On August 15, 1990, the NRC issued a letter stating there was not enough
information in the CEN document to conclude that the pressurizer surge
line meets all appropriate Code limits for a 40 year plant life.
    *  On December 20, 1991, CEN-387-P, Revision 1-P was sent to the NRC to
address the concerns of the August 15, 1990 NRC evaluation of the CEN
document.
    *  On May 5, 1992, Entergy sent a letter to the NRC documenting the
submittal of the revised CEN document and stated the only remaining
action to complete the response to the Bulletin is for the Waterford 3 to
update the pressurizer surge line design documentation. This was
committed to be completed within 180 days of issuance of a favorable
SER by the NRC.
Page 1 of 4
Waterford 3 Pressurizer Surge Line Temperature Change Rate
    *    On June 22, 1993, the NRC issued an SER for CEN-387-P, Revision 1. It
was concluded that the analysis in the CEN adequately demonstrates that
the bounding surge line and nozzles meet ASME Code stress and fatigue
requirements for the 40 year design life of the facility considering the
phenomenon of thermal stratification and thermal stripping. The staff
requested Entergy to provide a final status of the Waterford 3 activities
required by NRC Bulletin 88-11.
    *    On December 23, 1993, Entergy sent a letter to the NRC stating that all
design documents had been updated and that all actions required by NRC
Bulletin 88-11 had been completed.
CEN-387-P, Revision 1, is the Combustion Engineering response to NRC
Bulletin 88-11. This document addresses pressurizer surge line flow
stratification. The document provides a detailed fatigue analysis of stress due to
stratified temperature profiles of the fluid in the pressurizer surge line. Note that
this document indicates that thermal stratification is assumed for all surge flow as
the velocities will always be low. This document also specifically indicates that
the stratified temperature analysis envelopes high velocity flow and thermal
shock.
The following paragraphs are excerpted from the Thermal Striping Analysis for
the pressurizer surge line in CEN-387-P, Revision 1. The conclusion is the
effect of thermal striping is negligible and will not affect the fatigue life of the
pressurizer surge line.
The term striping refers to the thermal oscillations that occur at the hot-
cold interface.
The period of oscillations was chosen to be 1 second and 4 seconds for
the surge line analysis. Test data was measured or was empirically
determined to be in the range of 1 second to 10 seconds. For the large
temperature differences and high heat transfer coefficient used in this
analysis, the period is closer to 1 second than 4 seconds. A longer period
would yield a lower heat transfer coefficient, and therefore smaller
changes in metal temperatures. However, to be conservative, the same
heat transfer coefficient was used for all cases.
The stresses due to each gradient as a function of time were calculated
using formulas in ASME Code Section III, NB-3653.2. Table 3.5.3-2 lists
the alternating stress calculated for each of the four transients used for
evaluating fatigue. As can be seen from this table only one of the four
transients contributes anything to fatigue. That transient is number four
        (4) with an alternating stress of 15,780 psi and a number of allowable
cycles of 1.42E7.
Page 2 of 4
Waterford 3 Pressurizer Surge Line Temperature Change Rate
Waterford 3 Design Specification 9270-PE-140 is the project specification for
reactor coolant pipe and fittings. This document provides a summary of the
design analysis for surge line temperature transients. It includes text sections
and 2 tables as they apply to the surge line and surge line nozzle. The tables
address temperature differences anticipated as a result of thermal stratification.
Table 4.5.15.3.1 lists expected occurrences of temperature differences between
the pressurizer and the RCS hot leg and provides the number of expected
occurrences. Table 4.5.15.3.2 lists expected occurrences of temperature
differences between the top and bottom of the surge line piping. These
temperatures differences are for the pressurizer surge line piping and not the
fluid temperature in the piping. The number of occurrences is the expected
number for the life of the plant.
Entergy Position
The Entergy position is that pressurizer surge line temperature is not required to
be specifically monitored per procedure to ensure the design limits are
maintained, and that FSAR Section 5.4.3.1 should have been revised in 1993
when the Waterford 3 stress and fatigue analyses and design specifications were
revised per NRC Bulletin 88-11 to reflect the results of CEN-387-P, Revision 1.
This section of the FSAR has not been revised since the initial FSAR. CR-WF3-
2006-0839 was initiated to revise the FSAR. The reasoning for Entergys
position is documented in the paragraphs below.
The pressurizer surge line temperatures during heatup and cooldown are
maintained by ensuring the heatup and cooldown limits in the RCS and
pressurizer are maintained. The RCS limits are located in the TS and the
pressurizer limits are located in the TRM. Temperature changes in the surge line
can be greater than 200°F due to thermal stratification and thermal stripping.
CEN-387-P, Revision 1 documented that the pressurizer surge line meets Code
stress and fatigue requirements for the 40 year design life of the facility
considering the phenomenon of thermal stratification and thermal stripping.
Analysis in the CEN has indicated that temperature differences of up to 340°F
have been evaluated for.
The data recorded by the temperature element in the surge line has shown
periods of temperature changes greater than 200°F/hr. Thermal stratification is
applicable to all of these recorded temperature changes. These temperature
changes do not necessarily reflect the average temperature change of the surge
line but reflects a change in local fluid temperature at the temperature element.
This recorded temperature changes over time are not the same delta
temperatures listed in the tables in 9270-PE-140.
Therefore, the temperature difference in the pressurizer surge line is bounded by
the analysis performed in CEN-387-P, Revision 1 and monitoring pressurizer
Page 3 of 4
Waterford 3 Pressurizer Surge Line Temperature Change Rate
surge line temperature per procedure during heatup and cooldown is not
necessary.
Additional Information
The additional information specifically addresses the difference between the
surge line temperature increase seen during Refuel 13 and during the shutdown
for Hurricane Katrina, and the delta temperature values in 9720-PE-140. It also
addresses the reason Waterford 3 does not currently monitor surge line
temperature during heatups and cooldowns.
There following information is clarification regarding cycles listed in Design
Specification 9270-PE-140 and the temperatures recorded in PI with the
temperature element located in the surge line. The graphical data recording the
single surge line temperature element over time for our Refuel 13 outage and the
Hurricane Katrina outage indicates periods of temperature changes greater than
200 degrees within one hour. Thermal stratification is applicable to all of these
recorded temperature changes. Thermal stratification temperature changes were
addressed by CEN-327-P (NRC accepted response to NRC Bulletin 88-11). This
single temperature element does not necessarily reflect the average temperature
change of the surge line but reflects a change in local fluid temperature at the
temperature element. The recorded temperature changes of a single point over
time is not the same delta temperatures listed in the tables of the W3 Design
specification of RCS Piping and Fitting document (document #9270-PE-140).
The table 4.5.15.3.1 lists expected occurrences of temperature differences
between two different locations; the pressurizer and the RCS hot leg and
provides the number of expected occurrences. Table 4.5.15.3.2 lists expected
occurrences of temperature differences between the top and bottom of the surge
line piping. These tables clearly state this information at the end of their
respective sections. Thus comparing a graph of temperature changes with
respect to time to these tables is not appropriate.
The effects on the Pressurizer Surge Line due to thermal stratification and
thermal stripping were evaluated in CEN-327-P, Revision 1. This was reviewed
by the NRC and in the SER the Staff concluded that the surge line meets ASME
Code stress and fatigue requirements for the 40-year design life. Waterford 3
currently monitors heatups and cooldowns of the RCS and Pressurizer. The
effects of these heatups and cooldowns on the pressurizer surge line have been
evaluated in CEN-327-P.
Page 4 of 4
ATTACHMENT C
White Paper on Effect of Diesel Sump Pump
Inoperability on Ultimate Heat Sink Operability
1.0    Purpose
This paper provides an answer to the question, what is the original licensing
basis for flood protection of essential equipment in the Dry Cooling Tower Areas?
The paper also provides the chronology of regulatory requirements and licensing
bases that support the conclusion.
2.0    Conclusion Regarding Licensing Basis
The original licensing basis for essential equipment in the Dry Cooling Tower
areas is that essential equipment be protected from Standard Project Storm
(SPS).
The elements of the licensing basis are the following:
§  The SPS, with all installed sump pumps inoperative, was analyzed as an
event less severe than the probable maximum precipitation.
§  Provisions are required to be in place for emplacing the portable sump pump
within 6 hours of an SPS event to ensure that the ponding level from SPS
does not adversely affect essential equipment if installed pumps are
inoperative.
§  The electric pumps are seismically designed but not seismically qualified;
therefore they were assumed not to be available following an OBE.
§  The probability of the occurrence of an SPS and OBE is 3.6E-8 and
negligible.
In essence, the original licensing basis required that the portable sump pump be
emplaced and started within 6 hours of the start of an SPS (sump high level
alarm) to ensure that essential equipment in the DCT areas is not flooded.
On July 26, 1999, Condition Report CR-WF3-1999-0789 was initiated to identify
that the Dry Cooling Tower sump pump capacities were not sufficient to meet the
original licensing basis.
A new discharge path for the DCT sump pumps was installed via DCP-3251.
The DCP also replaced the 1 portable sump pump that had a capacity of 100
gpm with 2 portable sump pumps having a capacity of 300 gpm each. The
installed sump pumps capacities were reduced from 325 gpm to 270 gpm due to
the new piping configuration. The revised time frame for starting the portable
sump pump to ensure essential equipment is not flooded was re-established as 3
hours from the start of an SPS (sump high level alarm). Procedure OP-901-521
instructs Operations to operate the DCT Portable Sump Pumps in accordance
with OP-003-024, Sump Pump Operation within 3 hours of the sump level alarm.
3.0    Chronology
Regulatory Guide 1.70, Revision 2, September 1975
Waterford 3 is committed to Regulatory Guide 1.70, Revision 2, as noted in
section 1.8 of FSA
: [[contact::R. Neither Regulatory Guide Section 2.4.2.3]], Effects of Local
Intense Precipitation, or Section 2.4.3.1, Probable Maximum Precipitation
(PMP), have any requirement to consider OBE or SPS concurrently.
Regulatory Guide Section 2.4.2.3 states:
Describe the effects of local probable maximum precipitation (see Section
2.4.3.1) on adjacent drainage areas and site drainage systems, including
drainage from the roofs of structures. Summarize the design criteria for site
drainage facilities and provide analyses that demonstrate the capability of site
drainage facilities to prevent flooding of safety related facilities resulting from
local probable maximum precipitation.
The fundamental requirement in the Regulatory Guide is that the applicant
ensures that safety related equipment is not adversely impacted from maximum
precipitation.
Regulatory Guide 1.59, Revision 2, August 1977
Waterford 3 is committed to Regulatory Guide 1.59, Revision 2, as noted in
section 1.8 of FSA
: [[contact::R. Regulatory Guide 1.59]], Revision 2, does not have a
specific requirement to consider OBE and SPS concurrently.
Two important requirements are discussed in the Regulatory Guide.
First, seismically induced floods are associated with land features specific to
each site such as streams, estuaries, dam failures, and landslides. This
requirement does not apply to flooding in the DCT sump areas.
Second, the Regulatory Guide states that the most severe flood conditions may
not indicate potential threats to safety related systems that might result from
combination of flood conditions thought to be less severe. The Regulatory Guide
states that reasonable combinations of less severe flood conditions should be
considered to the extent needed. The Regulatory Guide states that such
combinations should be evaluated in cases where the probability of their
existing at the same time and having significant consequences is at lease
comparable to that associated with the most severe hydro-meteorological or
seismically induced flood. We judge that the requirement to consider the SPS
originates from this requirement. Also, since the probability of a SPS and OBE
concurrent was later established to be negligible, we judge that not considering
the SPS concurrent with the OBE is in conformance with the Regulatory Guide.
Standard Review Plan 2.4.3, Revision 2 July 1981
Standard Review Plan 2.4.3 does not have a specific requirement to consider
OBE and SPS concurrently.
Standard Review Plan 2.4.3, Section I, states:
Included is a review of the details of site drainage, including the roofs of safety
related structures, resulting from potential PMP probable maximum
precipitation
Standard Review Plan 2.4.3, Section IV, states:
The local PMF resulting from the estimated local PMP was found not to cause
flooding of safety related facilities, since the site drainage system will be capable
of functioning adequately during such a storm.
The fundamental requirement in the Standard Review Plan is that the applicant
ensures that safety related equipment is not adversely impacted form maximum
precipitation.
NRC Safety Evaluation Report, July 1981
The NRC evaluates the effects of a 6-hr duration PMP on the open cooling tower
areas and adjacent roofs. The NRC concludes that, assuming one sump pump
in each area is inoperable and that the roof drainage system is clogged with
debris during the PMP, that the ponding could inundate the transformers and
MCCs in the cooling tower areas.
The Safety Evaluation Report makes no reference to SPS or OB
: [[contact::E.
FSAR Amendment 25]], January 1982
FSAR Section 2.4.2.3.4 was initially added to the FSAR; previously it did not
exist. This FSAR Section is titled, Effects of Standard Project Storm (SPS) on
Cooling Tower Areas.
Two important aspects of the licensing basis are established in this FSAR
Section.
First, a probability evaluation is documented establishing that the occurrence of
an SPS and OBE is 3.6 E-8 and negligible.
Second, FSAR Section states that the SPS was still analyzed, assuming
inoperability of all pumps, in order to determine the time available before levels
are reached that could affect essential equipment in the Cooling Tower Areas.
Safety Evaluation Report, Supplement 4, October 1982
The SER states the following:
An alternative combination which should be considered is an operating basis
earthquake (OBE), which fails the sump pumps, coincident with a rainfall event
less than the PMP. This combination is considered appropriate since the pumps
are not seismically qualified1, and thus cannot be shown to be operable following
a seismic event. The staff therefore, requested that the applicant provide an
analysis of the effects of a standard project storm (SPS)2 assuming all four
pumps in the cooling tower areas are inoperable.
The SER further states:
the staff considered a SPS of 96 hours duration. This event would produce a
total rainfall of about 23 inches and would result in a ponding depth of about 1.9
ft in the cooling tower areas assuming that all four pumps are inoperable. Since
this is higher than the maximum allowable ponding depth of 1.71 feet, the
applicant has proposed to provide a portable pump with a pumping capacity of
100 gpm and sufficient head to pump over the cooling tower wall. a provision
will be included for emplacing the portable pump within 6 hours of a seismic
event if the installed pumps fail.
FSAR Amendment 33, September 1983
FSAR Amendment 33 revises Section 2.4.2.3.4 to state the following:
The maximum height to which rainwater can rise in this area before essential
equipment is reached is 1.71 ft (see subsection 2.4.2.3.3d). As shown in Table
2.4-6c, this level would not be reached for over seven hours into the SP
: [[contact::S.
Furthermore]], a portable pump is provided, with a pumping capacity of 100 gpm
and sufficient head to pump over the cooling tower wall. Provisions are included
for emplacing the portable pump within six hours of a seismic event if the
installed pumps fail and heavy rains are expected.
Thus, the FSAR Amendment 33 is in agreement with NRC SER Supplement 4 in
that the fundamental requirement is to protect essential equipment in the cooling
tower areas in the event of a SPS. The specific requirement in FSAR
Amendment 33 is that provisions be made for emplacing the portable sump
pump within 6 hours of a SPS event and that essential equipment be protected,
by ensuring that the ponding level does not reach 1.71 ft. The seismic event is a
vehicle to postulate the installed pumps are not available; however, important to
the licensing basis is the condition that the electric sump pumps will not be
available and that essential equipment needs to be protected prior to the ponding
level reaching 1.71 ft.
NRC Letter dated December 18 1984, Issuance of Five Percent Power License,
The NRC issues five percent power license, and Section 2.B.2 of the license
approves operation as described in FSAR as supplemented and amended
through Amendment 36.
NRC Letter dated March 16, 1985, Issuance of 100% Power License
The NRC issues 100 percent power license, and Section 2.B.2 of the license
approves operation as described in FSAR as supplemented and amended
through Amendment 36.
Design Change, July 26, 1999
On July 26, 1999, Condition Report CR-WF3-1999-0789 was initiated to identify
that the Dry Cooling Tower sump pump capacities were not sufficient to meet the
original licensing basis.
A new discharge path for the DCT sump pumps was installed via DCP-3251.
The DCP also replaced the 1 portable sump pump that had a capacity of 100
gpm with 2 portable pumps having a capacity of 300 gpm each. The installed
sump pumps capacities were reduced from 325 gpm to 270 gpm due to the new
piping configuration. The revised time frame for ensuring essential equipment is
not flooded was re-established as 3 hours from the start of SPS (sump high level
alarm). Procedure OP-901-521 instructs Operations to operate the DCT Portable
Sump Pumps in accordance with OP-003-024, Sump Pump Operation within 3
hours of the sump level alarm.
5
}}
}}

Latest revision as of 15:18, 22 December 2019

IR 05000382-06-008; Entergy Operations, Inc., 03/06-24/2006; Waterford Steam Electric Station, Unit 3; Biennial Baseline Inspection of the Identification and Resolution of Problems
ML061290021
Person / Time
Site: Waterford Entergy icon.png
Issue date: 05/08/2006
From: Laura Smith
Division of Reactor Safety IV
To: Venable J
Entergy Operations
References
IR-06-008
Download: ML061290021 (35)


Text

SUBJECT:

WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000382/2006008

Dear Mr. Venable:

On March 24, 2006, the U. S. Nuclear Regulatory Commission (NRC) completed a team inspection at your Waterford Steam Electric Station, Unit 3. The enclosed report documents the inspection findings, which were discussed with you and other members of your staff during an exit meeting on March 24, 2006.

This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, compliance with the Commissions rules and regulations and the conditions of your operating license. The team reviewed 237 condition reports, apparent cause and root cause analyses, as well as supporting documents. In addition, the team reviewed crosscutting aspects of NRC- and licensee-identified findings and interviewed personnel regarding the safety conscious work environment.

On the basis of the sample selected for review, there were no findings of significance identified during this inspection. The team concluded that, in general, problems were properly identified, evaluated, and corrected. The team concluded that a positive safety-conscious work environment existed at your Waterford Steam Electric Station, Unit 3. Several examples of minor problems were identified, including conditions adverse to quality that were not identified and entered into your corrective action program.

Entergy Operations, Inc. -2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Linda Joy Smith, Chief Plant Engineering Branch Division of Reactor Safety Docket: 50-382 License: NPF-38

Enclosure:

NRC Inspection Report 05000382/2006008 ATTACHMENT A: Supplemental Information ATTACHMENT B: Waterford 3 Pressurizer Surge Line Temperature Change Rate ATTACHMENT C: White Paper on Effect of Diesel Sump Pump Inoperability on Ultimate Heat Sink Operability

REGION IV==

Docket: 50-382 License: NPF-38 Report: 05000382/2006008 Licensee: Entergy Operations, Inc.

Facility: Waterford Steam Electric Station, Unit 3 Location: Hwy. 18 Killona, Louisiana Dates: March 6-24, 2006 Inspectors: M. Brown, Project Engineer, Projects Branch A E. Crowe, Resident Inspector, Projects Branch E G. Larkin, Resident Inspector, Projects Branch E M. Murphy, Senior Operations Engineer, Operations Branch D. Overland, Project Engineer, Projects Branch B Approved by: L. J. Smith, Chief Engineering Branch 2 Division of Reactor Safety-1- Enclosure

SUMMARY OF FINDINGS

IR 05000382/2006008; Entergy Operations, Inc., 03/06-24/2006; Waterford Steam Electric

Station, Unit 3; biennial baseline inspection of the identification and resolution of problems.

The inspection was conducted by two resident inspectors, one senior operations engineer, and two project engineers. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

Identification and Resolution of Problems

  • The team reviewed 237 corrective action program documents, apparent and root cause analyses, as well as supporting documents to assess problem identification and resolution activities. Based on this review, the team found the licensees process to identify, prioritize, evaluate, and correct problems was generally effective; thresholds for identifying issues remained appropriately low and, in most cases, corrective actions were adequate to address conditions adverse to quality. However, a number of issues were identified associated with the proper identification of degraded conditions in the plant. The team reviewed corrective actions associated with these degraded conditions and design issues at Waterford Steam Electric Station, Unit 3, which had crosscutting aspects in the area of problem identification and resolution.

The team concluded that a positive safety-conscious work environment exists at Waterford Steam Electric Station, Unit 3, based upon interviews conducted with plant personnel. The team determined that employees and contractors feel free to raise safety concerns to their supervision or bring concerns to the employee concerns program.

Inspector-Identified and Self-Revealing Findings None

REPORT DETAILS

OTHER ACTIVITIES (OA)

4OA2 Identification and Resolution of Problems

a. Effectiveness of Problem Identification

(1) Inspection Scope The inspectors reviewed items selected across four of the seven cornerstones to determine if problems were being properly identified, characterized, and entered into the corrective action program for evaluation and resolution. Specifically, the teams review included a selection of 237 condition reports, equipment walkdowns, review of operator logs, maintenance records, and station quarterly trend reports. The majority of the condition reports were opened and closed since the last NRC problem identification and resolution inspection completed on May 21, 2004. The team also performed a historical review of condition reports written over the last 5 years for the high pressure safety injection system, main feedwater isolation valves, main steam isolation valves, essential chillers, and the emergency diesel generators. The team reviewed a sample of licensee audits and self assessments, trending reports, system health reports, and various other reports and documents related to the problem identification and resolution program.

The audit and self-assessment results were compared with the self-revealing and NRC-identified issues to determine the effectiveness of the audits and self assessments.

The team interviewed station personnel and evaluated corrective action documentation to determine the licensees threshold for identifying problems and entering them into the corrective action program. In addition, in order to assess the licensees handling of operator experience, the team reviewed the licensees evaluation of selected industry operating experience reports, including licensee event reports, NRC generic letters, NRC bulletins, and NRC information notices, and generic vendor notifications to assess if issues applicable to Waterford Steam Electric Station, Unit 3, were appropriately addressed.

A listing of specific documents reviewed during the inspection is included in the attachment to this report.

(2) Assessment The team determined that, in general, problems were adequately identified and entered into the corrective action program, as evidenced by the relatively few findings identified during the assessment period. The licensees threshold for entering issues into the corrective action program was appropriately low. However, the team found two examples of ineffective problem identification during this inspection. The licensee also failed in some instances to identify or document deficiencies, which resulted in NRC noncited violations.

Current Issues Example 1: The licensee failed to identify multiple temperature changes of the pressurizer surge line, which exceeded the heatup and cooldown rate described in Section 5.4.3.1 of the stations Final Safety Analysis Report. Specifically, the inspection team discovered during a plant shutdown in August 2005 that the pressurizer surge line had experienced 19 changes in temperature, which exceeded this limit. This example is further described in Section 4OA2.e of this report.

Example 2: The team found the licensee's identification of adverse trends to be weak.

The inspection team reviewed 17 conditions reports, in which the licensee documented inadequacies in the procurement of replacement parts for the station. The licensee had identified a trend of improper parts passing through the receipt inspection, but failed to identify adverse trends related to lack of engineering involvement, as required by the procurement process; failure to perform professional engineering evaluations for parts transferred into the system; and receipt inspection documents missing required attributes. These procurement process weaknesses resulted in a nonseismically qualified synchronization switch being installed in an otherwise operable emergency diesel generator and a nonconforming fuel oil nipple passing receipt inspection.

Example 3: The NRC identified that the licensee missed several opportunities to identify the containment fan cooler condensate flow switches that did not meet the design requirements for detecting a one gallon per minute reactor coolant system leak (NRC Inspection Report 05000382/2005005-01).

Example 4: Control room operators missed several opportunities over a 32.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period to identify that a vacuum had been drawn on the reactor coolant system during refueling outage draindown conditions (self-revealing, NRC Inspection Report 05000382/2005010-03).

Historical Issue Example: The NRC identified the licensee failed to identify an inappropriate value of the unfiltered in-leakage parameter used to calculate the control room operator dose for design basis accident conditions involving radiological releases (NRC Inspection Report 05000382/2004006-01).

b. Prioritization and Evaluation of Issues

(1) Inspection Scope The team reviewed condition reports, engineering operability evaluations, and operations operability determinations to assess the licensees ability to evaluate the importance of the conditions adverse to quality. The team reviewed a sample of condition reports, failure mode analyses, apparent cause and root cause analyses, to ascertain whether the licensee identified and considered the full extent of conditions,

generic implications, common causes, and previous occurrences. The team also observed management oversight of the significant conditions adverse to quality, including one Corrective Action Review Board meeting.

In addition, the inspectors reviewed licensee evaluations of selected industry operating experience reports, including licensee event reports, NRC generic letters, NRC bulletins, NRC information notices, and generic vendor notices to assess whether issues applicable to Waterford Steam Electric Station, Unit 3, were appropriately addressed.

The team performed a historical review of condition reports covering the last 5 years regarding the high pressure safety injection system, the emergency diesel generators, main feedwater isolation valves, essential chillers, and the dry cooling tower to determine if the licensee had appropriately addressed long-standing issues and those that might be age dependent.

A listing of specific documents reviewed during the inspection is included in the attachment to this report.

(2) Assessment The team concluded that problems were generally prioritized and evaluated in accordance with the licensees corrective action program guidance and NRC requirements. The team found that for the sample of root cause analyses reviewed, that the licensee was generally self critical and exhaustive in its research into the history of significant conditions adverse to quality. However, the team found one example of ineffective problem evaluation during this inspection.

Current Issues Example 1: The inspectors discovered the licensee had categorized the failure of a fuel oil pipe nipple in the Emergency Diesel Generator B in 2002, as a condition adverse to quality. The licensee followed Procedure EN-LI-102, Corrective Action Process, Revision 4, in making the determination of significance. The inspectors followed the steps of Procedure EN-LI-102 and arrived at the same level of significance, however, the procedure provides a provision for the Condition Review Group to change the level of significance, as warranted by the conditions. The inspectors determined that this was a significant condition adverse to quality because the failure rendered one emergency diesel inoperable. The Emergency Diesel Generator A experienced a failure of its corresponding fuel oil nipple in 2005. The licensee determined this failure was a significant condition adverse to quality solely because of the repetitive nature of the failure.

c. Effectiveness of Corrective Actions

(1) Inspection Scope The team reviewed 237 condition reports to verify that corrective actions related to the issues were identified and implemented in a timely manner commensurate with safety, including corrective actions to address common cause or generic concerns. The team

reviewed corrective actions planned and implemented by the licensee and sampled specific technical issues to determine whether adequate decisions related to structure, system, and component operability were made.

In addition, the team reviewed a sample of those condition reports written to address NRC inspection findings to ensure that the corrective actions adequately addressed the issues as described in the inspection report writeups. The team also reviewed a sample of corrective actions closed to other condition reports and programs, such as work and engineering work requests to ensure that the condition described was adequately addressed and corrected.

A listing of specific documents reviewed during the inspection is included in the attachment to this report.

(2) Assessment The effectiveness of identified corrective actions to address adverse conditions was generally adequate. The team evaluated several occurrences where the licensee did not effectively address conditions adverse to quality and corrective actions taken were untimely and inappropriate. These included five examples, one identified by the team and four by other NRC inspections, where the licensee failed to take prompt corrective actions to resolve long-standing issues. The team also evaluated nine other findings identified by the NRC baseline inspection program and other NRC inspections at Waterford Steam Electric Station, Unit 3, since the last problem identification and resolution inspection that had crosscutting aspects related to prompt and effective corrective actions to resolve conditions adverse to quality.

Current Issues Example 1: The reactor coolant draindown procedure failed to identify that temporary vent rigs, required by procedure to properly establish vent paths, included in-line ball valves in series with the vent path and also failed to direct those ball valves be opened to establish the vent path. The licensee was aware of and did not fix the procedure to address the ball valves in 2002 (NRC Inspection Report 05000382/2005010-02).

Example 2: The NRC identified the licensee failed to correct the condition which resulted in multiple cycle timer failures in the essential chiller (NRC Inspection Report 05000382/2005002-01).

Example 3: The NRC identified the licensee failed to prevent recurrence of through wall pipe leakage on the main steam line Pipe 2MS2-123. This deficiency resulted in an unisolable steam leak requiring NRC approval to deviate from the American Society of Mechanical Engineers Boiler and Pressure Code Case N523-2 to perform temporary repairs preventing a plant shutdown (NRC Inspection Report 05000382/2005004-03).

Historical Issues Example 1: The NRC identified the licensee failed to correct a known deficient condition involving the failure to account for instrument uncertainty to satisfy Technical Specification Surveillance Requirement 4.7.6.5.a. This failure potentially affects the ability of the control room envelope to perform its design function with respect to protecting operators from postulated design basis accidents resulting in radiological releases (NRC Inspection Report 05000382/2004006-03).

Example 2: The NRC identified the licensee failed to correct a known deficient condition involving multiple occasions of accumulator overpressure conditions resulting from degraded hydraulic fluid adversely affecting the main feedwater isolation valve hydraulic actuator pressure relief system. These over pressure conditions potentially result in valve closure stroke times outside design basis values (NRC Inspection Report 05000382/2004005-03).

Example 3: The NRC identified the licensee failed to promptly correct instances where the main feedwater isolation valve actuator thermal relief valves failed to properly function. In one case, the licensee failed to properly address system operability and, for a 2-week period, actual valve operability was unknown (NRC Inspection Report 05000382/2004006-02).

Example 4: The NRC identified the licensee failed to correct deficiencies in the emergency diesel generator loading and fuel oil consumption analysis. The licensee inappropriately closed a corrective action requiring the revisions, which subsequently resulted in the failure to maintain design control of the emergency diesel generator fuel oil storage inventory requirements to ensure a 7-day postaccident fuel oil inventory (NRC Inspection Report 05000382/2004002-05).

Example 5: The NRC identified the licensee failed to determine the cause and precluded recurrence of main steam isolation solenoid-operated dump valve failures.

The inspectors noted that the licensees apparent cause did not provide an extent of condition analysis for the solenoid-operated valve failure (NRC Inspection Report 05000382/2004004-03).

Example 6: The NRC identified the licensee failed to take adequate corrective action to ensure the torque applied to the flow control valve for Accumulator B of main feedwater isolation Valve 1 was sufficient to prevent an o-ring from extruding, resulting in a loss-of-system hydraulic fluid and rendering the valve inoperable (NRC Inspection Report 05000382/2004008-02).

Example 7: The NRC identified the licensee failed on multiple occasions to correct a known deficient condition involving the failure to account for instrument uncertainty to satisfy Technical Specification Surveillance Requirement 4.7.6.5.a. This failure potentially affects the ability of the control room envelope to perform its design function with respect to protecting operators from postulated design basis accidents resulting in radiological releases (NRC Inspection Report 05000382/2004006-03).

Example 8: The licensee failed to replace known age-degraded o-rings affecting the main feedwater isolation valves in the Year 2000 resulting in o-ring failure and inoperability of the Train A feedwater isolation valve on December 27, 2003 (NRC Inspection Report 05000382/2004002-01).

Example 9: The NRC identified the licensee failed to establish appropriate torque specification to ensure adequate o-ring compression that ultimately led to an o-ring failure and the inoperability of the Train A main feedwater isolation valve. The licensee had previously identified concerns related to inadequate work instructions for performing maintenance activities on the main feedwater isolation valves (NRC Inspection Report 05000382/2004002-02).

d.

Assessment of Safety-Conscious Work Environment

(1) Inspection Scope The team interviewed 24 individuals from the licensees staff, representing a cross section of functional organizations and supervisory and nonsupervisory personnel.

These interviews assessed whether conditions existed that would challenge the establishment of a safety-conscious work environment. The team interviewed the site employee concerns program coordinator.

(2) Assessment The team concluded that a positive safety-conscious work environment exists at Waterford Steam Electric Station, Unit 3. Based on interviews, station personnel felt free to enter issues into the corrective action program, raise safety concerns with their supervision, to the employee concerns program, and to the NRC. The team determined that the majority of safety concerns were addressed through the sites normal chain of command by the relatively few safety concerns entered into the employee concerns program and the small number of allegations made to the NRC.

e.

Specific Issues Identified During this Inspection

(1) Inspection Scope During this assessment, the team performed the inspections scoped in Sections 4OA2 a.(1), 4OA2 b.(1), 4OA2 c.(1), and 4OA2 d.(1) above.
(2) Finding Details
(i) Unresolved Item: 05000382/2006008-01, Failure to Maintain Design Control of the Pressurizer Surge Line
Introduction.

The team identified an unresolved item related to compliance with 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to translate design-basis heatup and cooldown rates for the pressurizer surge line into appropriate specifications, procedures, and instructions. As a result, Entergy Operations, Inc., failed

to effectively control and evaluate pressurizer surge line temperature changes on numerous occasions.

Description.

Final Safety Analysis Report (FSAR) Section 5.4.3.1, Reactor Coolant Piping Design Basis, and Section 5.4.10.1, Pressurizer Design Basis, states, in part, that during heatup and cooldown of the plant, the allowable rate of temperature change for the surge line is limited to 200°F/hr. Technical Requirements Manual (TRM),

Section 3.4.8.2, Pressurizer Heatup/Cooldown, specifies the limiting condition for operation, in part, as a maximum heatup rate of 200°F per hour and a maximum cooldown rate of 135°F per hour.

On April 18, 2005, Entergy Condition Report CR-WF3-2005-1392 stated that a pressurizer surge line temperature transient occurred with the surge line temperature dropping from 425°F to 140°F, a change of approximately 285°F with approximately 200°F occurring within 8 minutes. Technical Requirements Manual, Section 3.4.8.2 Action specifies, "With any of the pressurizer limits in excess of the above, the operators must restore the affected parameter to within the limits within 30 minutes; perform an engineering evaluation to determine the effects of the out-of-limit condition on the structural integrity of the pressurizer; and enter TRM LCO 3.0.3."

The team noted that Entergy Operations, Inc., failed to restore pressurizer/surge line limits within 30 minutes and perform an engineering evaluation to determine the effects of the out-of-limit condition on the structural integrity of the pressurizer/surge line. The team reviewed Entergy Operations, Inc.s operating procedures for plant heatup and cooldown activities, OP-010-005, Plant Shutdown, and OP-010-003, Plant Startup, and did not find procedure steps to limit surge line temperature changes to less than 200°F/hr, nor were there any procedure steps to assess whether surge line stress or fatigue limits had been exceeded. This appeared to be a violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to translate design-basis heatup and cooldown rates for the pressurizer surge line into appropriate specifications, procedures, and instructions.

The design limit in Report CEN-387-P was based, in part, by temperature gradients greater than 200°F occurring less than 3.6 occurrences per heatup/cooldown cycle for 500 heatup/cooldown cycles over the 40-year life of the plant. Calculation CN-OA-04-53 documented 19 instances where pressurizer insurges, in excess of the volume of the surge line, occurred with a temperature gradient greater than 200°F. These pressurizer insurges occurred during five refueling outage heatup/cooldown cycles (Refueling Outages 8-12)for an average of 3.8 temperature gradients greater than 200°F per heatup/cooldown cycle.

Entergy Operations, Inc. disagreed and provided a paper (Attachment B), which documented their position. While they acknowledged that the FSAR was not up to date, they stated that the pressurizer surge line temperature transient on April 18, 2005, was bounded by Combustion Engineering Owners Group Report CEN-387-P, Pressurizer Surge Line Flow Stratification Evaluation, submitted to the NRC in response to NRC Bulletin 88-11, Pressurizer Surge Line Thermal Stratification. Report CEN-387-P concluded that the pressurizer surge line met all applicable design codes, FSAR, and

other regulatory commitments for the licensed life of the plant considering the phenomenon of thermal stratification in fatigue and stress evaluations. The team noted that this conclusion was based on operating the plant consistent with the assumptions in the evaluation (Report CEN-387-P). Additional inspection is required to complete the review of Entergy Operations, Inc.'s, position and determine whether the licensee was operating their facility within the assumptions of the analysis.

Analysis.

The significance of this issue depends on whether or not the analysis bounds past plant operation.

Enforcement.

The potential failure to translate the design basis into appropriate specifications, procedures, and instructions to effectively control and evaluate surge line temperature changes, during plant heatup and cooldown, that exceeded those limits described in the FSAR and the TRM is unresolved: (URI 05000382/2006008-01);

"Failure to Maintain Design Control of the Pressurizer Surge Line."

(ii) Unresolved Item 05000382/2006008-02, Failure to Ensure that Written Procedures Adequately Incorporate Regulatory Requirements and Design Basis
Introduction.

The team identified an unresolved item related to compliance with Technical Specification, Section 6.8.1, for the failure to ensure that written procedures adequately incorporate regulatory requirements and the design basis for the dry cooling tower diesel-driven sump pumps.

Description.

Waterford Safety Evaluation Report, Supplement 4, Section 2.4.2.3, discusses the design basis rainfall event and combination of events. This supplement commits the licensee to the probable maximum precipitation event. Because of the fact that the motor-driven sumps are not seismically qualified, the NRC requested the licensee analyze the effects of a standard project storm, which consists of 50 percent of the probable maximum precipation event concurrent with an operating basis earthquake. The results of the licensees analysis showed the licensee was susceptible to ponding in the dry cooling tower sumps, assuming the loss of all motor-driven pumps, which would endanger the safety-related transformers and motor control centers located in the cooling tower areas.

The licensee submitted Amendment 34, dated January 1984, subsequent to Safety Evaluation Report, Supplement 4. Section 2.4.2.3.4 of this amendment submittal contains an analysis showing the probability of standard project storm and operating basis earthquake is 3.6E-08, which is considered negligible. However, the licensee proposed to provide a 100 gpm portable pump that would be sufficient to pump down the dry cooling tower sumps in the event of the standard project storm. The NRC determined that the portable pump was sufficient (as evidenced in Safety Evaluation Report, Supplement 4) provided the pump was placed in operation within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. In 2000, after determining that more sump pumping capacity was needed, the licensee installed a diesel-driven sump pump, with 300 gpm capacity, in each dry cooling tower sump. The Design Basis Calculation EC-M99-010 analyzed for a probable maximum precipation event, concurrent with a loss-of-offsite power, and determined that a higher capacity portable pump was needed. The calculation also analyzed for a rainfall equivalent to 60 percent of the probable maximum precipation event, concurrent with a loss of all motor-driven sump pumps, and determined that a 300 gpm portable pump

would be sufficient. The licensees Procedure OP-100-014, Technical Specifications and Requirements Compliance, Revision 14, states that two motor-driven sump pumps or one motor-driven pump and one diesel-driven pump are required for ultimate heat sink operability. This procedure implies that the diesel driven sump pump can be out of service indefinitely without affecting operability of the ultimate heat sink. The NRC staff believes this procedure does not adequately address the requirement of the portable sump pump in the design basis of the ultimate heat sink, nor does the procedure require any compensatory actions be taken in the event the diesel-driven sump pump becomes inoperable. Also, the staff believes the controls and location of the diesel-driven sump pump are not adequately addressed by the licensee.

Analysis.

The significance of this issue has not been determined.

Enforcement.

The licensee has provided a position paper (Attachment C) related to the design basis requirements for the dry cooling tower diesel-driven sump pumps, which has not been fully reviewed by the NRC. The potential failure to ensure regulatory requirements for these pumps is unresolved: (URI 05000382/2006008-02) "Failure to Translate Design Control into Station Documents Regarding Diesel-driven Dry Cooling Tower Sump Pumps"

4OA6 Exit Meeting

The team discussed the findings of the Problem Identification and Resolution inspection with Mr. J. Venable, Vice President Operations, and other members of the licensees staff on March 24, 2006. Licensee management did not identify any materials examined during the inspection as proprietary.

The licensee acknowledged the findings presented. The inspectors noted that while proprietary information was reviewed, none would be included in this report.

ATTACHMENT A: Supplemental Information ATTACHMENT B: Waterford 3 Pressurizer Surge Line Temperature Change Rate ATTACHMENT C: White Paper on Effect of Diesel Sump Pump Inoperability on Ultimate Heat Sink Operability

KEY POINTS OF CONTACT Licensee Personnel B. Baxter, Control Room Supervisor C. DeDeaux Sr., Senior Project Manager, Licensing R. Dodds, Manager, Operations R. Fletcher, Training Manager C. Fugate, Assistant Operations Manager J. Hall, Operations Training Supervisor - Operator Requalification J. Holman, Manager, Nuclear Engineering J. Laque, Manager, Maintenance R. Murillo, Senior Staff Engineer R. Osborne, Manager, Engineering Programs and Components A. Pilutti, Manager, Radiation Protection O. Pipkins, Senior Licensing Engineer R. Porter, Superintendent, Mechanical Maintenance B. Proctor, Systems Engineering Manager J. Rachal, Design Engineering Supervisor J. Ridgel, Manager, Corrective Action Program T. Tankersley, Acting Director, Nuclear Safety Assurance K. Walsh, General Manager, Plant Operations B. Williams, Engineering Director J. Venable, Site Vice President, Waterford 3 NRC M. Hay, Senior Resident Inspector Waterford 3 LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened 05000382/2006008-01 URI Failure to Maintain Design Control of the Pressurizer Surge Line (Section 4OA2 e.)05000382/2006008-02 URI Failure to Translate Design Control into Station Documents Regarding Diesel-driven Dry Cooling Tower Sump Pumps (Section 4OA2 e.)

A

LIST OF

DOCUMENTS REVIEWED

Plant Procedures

NAME TITLE REVISION

CEP-IST-1 IST Bases Document 3

EN-OP-115 Conduct of Operations 0

LI-102 Corrective Action Process 4

LI-19645 Quality Related Administrative Procedure 2

MM-006-119 Yard Oil Separator to CW Temporary Pumping System 0

OI-042-000 Watch Station Procedures 1

OP-001-003 Reactor Coolant System Draindown 23

OP-005-004 Main Steam 12

OP-009-008 Safety Injection System 18

OP-100-001 Operations Standards and Management Expectations 22

OP-100-009 Control of Valves and Breakers 17

OP-100-0014 Technical Specification and Technical Requirements 13

Compliance

UNT-005-004 Temporary Alteration Control 16

Engineering Reports

ER-W3-2002-0055 ER-W3-2004-0537 ER-W3-2005-0426 ER-W3-00-0337

ER-W3-2003-0010 ER-W3-2005-0305 ER-W3-2002-0278

Calculations

CN-OA-04-53 EC-M99-010 MN(Q)-6-27

Root Cause Analysis Reports for CR-WF3-

2001-0317 2002-0339 2003-0062 2003-3891 2004-759 2004-1011

Attachment A

Condition Reports, CR-WF3-

1997-1227 2004-0759 2004-2404 2005-0109 2005-1626 2005-3831

2000-0441 2004-0821 2004-2487 2005-0132 2005-1646 2005-3840

2000-1347 2004-0835 2004-2496 2005-0134 2005-1694 2005-3872

2000-1455 2004-0865 2004-2517 2005-0197 2005-1821 2005-3872

2001-0596 2004-0903 2004-2520 2005-0217 2005-1836 2005-3902

2001-0673 2004-1011 2004-2522 2005-0346 2005-2070 2005-3914

2001-0782 2004-1047 2004-2545 2005-0413 2005-2139 2005-3924

2001-1284 2004-1190 2004-2547 2005-0415 2005-2267 2005-3928

2001-1367 2004-1208 2004-2549 2005-0471 2005-2272 2005-3960

2002-0468 2004-1312 2004-2638 2005-0489 2005-2350 2005-3961

2002-0470 2004-1340 2004-2690 2005-0530 2005-2402 2005-3985

2002-0588 2004-1446 2004-2722 2005-0587 2005-2469 2005-4038

2002-0678 2004-1480 2004-2734 2005-0590 2005-2489 2005-4065

2002-1410 2004-1518 2004-2766 2005-0591 2005-2536 2005-4066

2002-1842 2004-1553 2004-2884 2005-0592 2005-2546 2005-4067

2002-2799 2004-1572 2004-2890 2005-0608 2005-2548 2005-4147

2003-0147 2004-1593 2004-2928 2005-0717 2005-2600 2005-4149

2003-0577 2004-1621 2004-2973 2005-0763 2005-2679 2005-4151

2003-1192 2004-1645 2004-2995 2005-0804 2005-2685 2005-4173

2003-1202 2004-1646 2004-3066 2005-0805 2005-2695 2005-4251

2003-2758 2004-1668 2004-3130 2005-0806 2005-2780 2005-4444

2003-2759 2004-1679 2004-3200 2005-0839 2005-2799 2005-4480

2003-2991 2004-1684 2004-3219 2005-0852 2005-2819 2005-4597

2003-3088 2004-1716 2004-3244 2005-0921 2005-2837 2005-4647

2003-3649 2004-1751 2004-3413 2005-0966 2005-2844 2005-4694

2003-3891 2004-1753 2004-3460 2005-0967 2005-2869 2005-4915

2004-0251 2004-1763 2004-3464 2005-1132 2005-2874 2005-4917

2004-0304 2004-1810 2004-3695 2005-1143 2005-2990 2005-4929

2004-0309 2004-1850 2004-3720 2005-1173 2005-3006 2005-5024

2004-0326 2004-1854 2004-3725 2005-1247 2005-3091 2006-0006

2004-0420 2004-1855 2004-3753 2005-1260 2005-3293 2006-0058

2004-0464 2004-1863 2004-3853 2005-1279 2005-3308 2006-0164

2004-0483 2004-1880 2004-3881 2005-1315 2005-3455 2006-0200

2004-0494 2004-1942 2004-3924 2005-1332 2005-3474 2006-0380

2004-0508 2004-2002 2004-3944 2005-1346 2005-3659 2006-0492

2004-0634 2004-2228 2004-3949 2005-1362 2005-3698 2006-0759

2004-0651 2004-2290 2004-4000 2005-1363 2005-3812 2006-0767

2004-0701 2004-2320 2005-0033 2005-1392 2005-3822 2006-0839

2004-0703 2004-2326 2005-0081 2005-1463 2005-3830 2006-0895

2004-0721 2004-2382 2005-0098

Attachment A

Learning Organization Conditions Reports

LO-OPX-2004-0247 LO-OPX-2005-0100 LO-OPX-2005-0217 LO-OPX-2006-0011

LO-OPX-2005-0036 LO-OPX-2005-0103 LO-OPX-2005-0243 LO-OPX-2006-0034

LO-OPX-2005-0085 LO-OPX-2005-0132 LO-OPX-2005-0252

Work Orders

51697 52825 72604 412565 4599901

51699 57759 72606 4281801 5100331101

2824 62641

Maintenance Action Items

20105 438981

Miscellaneous Documents

Commercial Grade Evaluation 01214

C-PAC-002

L-19645

L-23993

MMR Project 53465

PO WPY20583

2004 Second Quarter Waterford Quarterly Trend Report

2004 Third Quarter Waterford Quarterly Trend Report

2004 Fourth Quarter Waterford Quarterly Trend Report

Quality Assurance Audit Report QA-12-20050-WF3-1

Quality Assurance Audit Report QA-12-20050-WF3-009

Quality Assurance Audit Report QA-12-20050-WF3-1

PO 10083675

INITIAL MATERIAL REQUEST

INITIAL INFORMATION REQUEST FROM WATERFORD 3

FOR PI&R INSPECTION (Report Number 05000382/2004006)

The inspection will cover the period of October 2002 to March 2004. The information may be

provided in either electronic or paper media or a combination thereof. Information provided in

electronic media may be in the form of CDs, or 3-1/2 inch floppy disks. The agencys text editing

software is Corel WordPerfect 8, Presentations, and Quattro Pro; however, we have document

viewing capability for MS Word, Excel, Power Point, and Adobe Acrobat (.pdf) text files.

Please provide the following information to Peter Alter by March 29, 2004 at the Resident

Inspector Office at Waterford-3

Attachment A

All procedures governing or applying to the corrective action program, including the

processing of information regarding generic communications and industry operating

experiences

Procedures and descriptions of any informal systems, used by engineering, operations,

maintenance, security, training, and emergency planning for issues below the threshold

of the formal corrective action program

A searchable table of all corrective action documents (condition reports) that were

initiated or closed during the period, include condition report number, description of

issue and significance classification

Either annotate on the above list or a separate list of all condition reports associated

with:

(1) Human performance issues

(2) Emergency preparedness issues

(3) Response to 10 CFR Part 21 reports

A separate list of all condition reports closed to other programs, such as maintenance

action items/work orders, engineering requests, etc.

A copy of each significant event review team report and root cause analysis report for

the period (not necessarily the whole condition report)

Copies of condition reports (for the period) associated with nonescalated (no response

required) or noncited violations for the period

Copies of condition reports for the period associated with repetitive problems or issues

Copies of condition reports for the period associated with ineffective or untimely

corrective actions

List of all self assessments or quality assurance assessments/audits for the period

All corrective action program reports or metrics used for tracking effectiveness of the

corrective action program for the period

All quality assurance audits and surveillances, and functional self assessments of

corrective action activities completed for the period

Control room logs for the Year 2003

Security event logs for the year 2003

Radiation protection event logs for the year 2003

List of risk significant systems from W3 PRA/PSA, based on risk achievement worth

(RAW) and "0% availability CDF"

Attachment A

Searchable list of all maintenance action items/work orders for the period

List of all SSCs placed in or removed from the maintenance rule a(1) category for the

period

All corrective action documents related to the following industry operating experience

generic communications:

NRC Bulletins

NRC Bulletin 2002-001, Reactor Pressure Vessel Head Degradation and Reactor

Coolant Pressure Boundary Integrity

NRC Information Notices

NRC Information Notice 2004-001, Auxiliary Feedwater Pump Recirculation Line Orifice

Fouling - Potential Common Cause Failure

NRC Information Notice 2003-019, Unanalyzed Condition of Reactor Coolant Pump

Seal Leakoff Line During Postulated Fire Scenarios or Station Blackout

NRC Information Notice 2003-013, Steam Generator Tube Degradation at Diablo

Canyon

NRC Information Notice 2003-011, Leakage Found on Bottom-Mounted

Instrumentation Nozzles

NRC Information Notice 2003-008, Potential Flooding Through Unsealed Concrete

Floor Cracks

NRC Information Notice 2003-005, Failure to Detect Freespan Cracks in PWR Steam

Generator Tubes

NRC Information Notice 2003-002, Recent Experience With Reactor Coolant System

Leakage And Boric Acid Corrosion

NRC Information Notice 2002-034, Failure of Safety-Related Circuit Breaker External

Auxiliary Switches at Columbia Generating Station

Attachment A

Information Request 1 - January 2006

Waterford PIR Inspection (IP 71152; Inspection Report 50-382/06-08)

The inspection will cover the period of March 1, 2004 to March 1, 2006. All requested

information should be limited to this period unless otherwise specified. The information may be

provided in either electronic or paper media of a combination of this media. Information

provided in electronic media may be in the form of e-mail attachment(s), CDs, or 3 1/2 inch

floppy disks. The agencys text editing software is Corel WordPerfect 10, Presentations, and

Quattro Pro; however, we have document viewing capability for MS Word, Excel, PowerPoint,

and Adobe Acrobat (pdf.) text files.

Please provide the following by February 8, 2006, to:

U.S. Nuclear Regulatory Commission

Resident Inspectors Office - Attn. Grant Larkin

Waterford Steam Electric Station Unit 3

Entergy Operations, Inc.

265 River Road

Killona, Louisiana 70066

Note: On summary lists please include a description of problem, status, initiating date, and

owner organization

1. Summary list of all condition reports opened during the period

2. Summary list of all open condition reports with significance of B or greater which were

generated during the period

3. Summary list of all condition reports with significance of B or greater closed during the

specified period

4. Summary list of all condition reports which were down-graded or up-graded in

significance during the period

5. A list of all corrective action documents that subsume or "roll-up" one or more smaller

issues for the period

6. List of all root cause analyses completed during the period

7. List of all apparent cause analyses completed during the period

8. List of root cause analyses planned, but not complete at end of the period

9. List of plant safety issues raised or addressed by the employee concerns program

during the period

10. List of action items generated or addressed by the plant safety review committees

during the period

Attachment A

11. Summary list of operator work-arounds, engineering review requests and/or operability

evaluations, temporary modifications, safety system deficiencies, and control room

deficiencies

2. All quality assurance audits and surveillances of corrective action activities completed

during the period

13. A list of all quality assurance audits and surveillances scheduled for completion during

the period, but which were not completed

14. All corrective action activity reports, functional area self-assessments, and non-NRC

third party assessments completed during the period

15. Corrective action performance trending/tracking information generated during the period

and broken down by functional organization

16. Current procedures/policies/guidelines for:

1. Condition Reporting

2. Corrective Action Program

3. Root Cause Evaluation/Determination

4. Deficiency Reporting and Resolution

17. A listing of all external events evaluated for applicability at Waterford during the period

18. Condition Reports or other actions generated for each of the items below [ADAMS

accession numbers or other cross reference listed for some]:

1. Part 21 Reports (2005-41-00; 2005-38-00 [ml053180299]; 2005-37-00;

2005-33-01 [ml052860229]; 2005-30-01 [ml052640220]; 2005-26-01

[ml052910389]; 2005-22-00; 2005-20-00; 2005-17-00 [ml051110087];

2005-16-00 [ml051100285]; 2005-13-00 [ml050950428]; 2005-12-01

[ml052080368]; 2005-12-00 [ml050630275]; 2005-10-00 [ml050560142];

2005-07-00; 2005-05-01 [ml051100355]; 2005-01-00 [ml043520077];

2004-27-01 [ml043280541]; 2004-24-00 [ml042470299]; 2004-22-00

[ml042660175]; 2004-21-00 [ml042520048]; 2004-17-00 [ml041900058];

2004-15-00; 2004-14-00; 2004-10-00 [ml041140335]; 2004-08-00

[ml041110893]; 2004-02-01 [ml040420567]

2. NRC Information Notices 05-32; 05-31; 05-30; 05-29; 05-26; 05-25; 05-24; 05-

23; 05-21; 05-19; 05-16; 05-11; 05-09; 05-08; 05-06; 05-02;04-021; 04-019; 04-

016;04-012; 04-011;04-010; 04-009;04-008; 04-007;04-001

3. All LERs issued by Waterford during the period

4. NCVs and Violations issued to Waterford during the period

19. Safeguards event logs for the period

20. Radiation protection event logs

Attachment A

21. Current system health reports or similar information

2. Current predictive performance summary reports or similar information

23. Corrective action effectiveness review reports generated during the period

Attachment A

ATTACHMENT B

Waterford 3 Pressurizer Surge Line Temperature Change Rate

Waterford 3 Pressurizer Surge Line Temperature Change Rate

Purpose

This Paper is to document the Entergy position on the potential NCV of 10CFR50

Appendix B, Criterion III, Design Control for not translating design basis criteria

into plant operating procedures. The design basis criteria in question is a

statement in the FSAR (Section 5.4.3.1) which states:

During heatup and cooldown of the plant, the allowable rate of

temperature change for the surge line is increased to 200°F/hr as a design

requirement specified in Subsection 3.9.1.1.

Background

The following is a time line of the Entergy response to NRC Bulletin No. 88-11.

This concludes that the fatigue life of the Waterford 3 surge line is 40 years which

the NRC concurred with.

  • The NRC issued NRC Bulletin No. 88-11, Pressurizer Surge Line Thermal

Stratification, on December 20, 1988. The purpose of the Bulletin was to

request that addressees establish and implement a program to confirm

pressurizer surge line integrity in view of the occurrence of thermal

stratification and to inform the staff of the actions taken to resolve this

issue.

  • CEN-387-P was transmitted to the NRC on July 27, 1989. This

documented that the Waterford 3 surge line fatigue life is longer than 40

years.

  • On August 28, 1989, Entergy sent a letter to the NRC stating that Bulletin 88-11 item 1b, 1c and 1d were addressed in CEN-387-P and that item 1a

(visual inspection of the pressurizer surge line) would be addressed during

the next refueling outage.

  • On March 7, 1990, Entergy sent a letter to the NRC which addressed the

results of the visual inspections of the pressurizer surge line. The letter

concluded that the Waterford 3 surge line was structurally sound.

  • On August 15, 1990, the NRC issued a letter stating there was not enough

information in the CEN document to conclude that the pressurizer surge

line meets all appropriate Code limits for a 40 year plant life.

  • On December 20, 1991, CEN-387-P, Revision 1-P was sent to the NRC to

address the concerns of the August 15, 1990 NRC evaluation of the CEN

document.

  • On May 5, 1992, Entergy sent a letter to the NRC documenting the

submittal of the revised CEN document and stated the only remaining

action to complete the response to the Bulletin is for the Waterford 3 to

update the pressurizer surge line design documentation. This was

committed to be completed within 180 days of issuance of a favorable

SER by the NRC.

Page 1 of 4

Waterford 3 Pressurizer Surge Line Temperature Change Rate

  • On June 22, 1993, the NRC issued an SER for CEN-387-P, Revision 1. It

was concluded that the analysis in the CEN adequately demonstrates that

the bounding surge line and nozzles meet ASME Code stress and fatigue

requirements for the 40 year design life of the facility considering the

phenomenon of thermal stratification and thermal stripping. The staff

requested Entergy to provide a final status of the Waterford 3 activities

required by NRC Bulletin 88-11.

  • On December 23, 1993, Entergy sent a letter to the NRC stating that all

design documents had been updated and that all actions required by NRC

Bulletin 88-11 had been completed.

CEN-387-P, Revision 1, is the Combustion Engineering response to NRC

Bulletin 88-11. This document addresses pressurizer surge line flow

stratification. The document provides a detailed fatigue analysis of stress due to

stratified temperature profiles of the fluid in the pressurizer surge line. Note that

this document indicates that thermal stratification is assumed for all surge flow as

the velocities will always be low. This document also specifically indicates that

the stratified temperature analysis envelopes high velocity flow and thermal

shock.

The following paragraphs are excerpted from the Thermal Striping Analysis for

the pressurizer surge line in CEN-387-P, Revision 1. The conclusion is the

effect of thermal striping is negligible and will not affect the fatigue life of the

pressurizer surge line.

The term striping refers to the thermal oscillations that occur at the hot-

cold interface.

The period of oscillations was chosen to be 1 second and 4 seconds for

the surge line analysis. Test data was measured or was empirically

determined to be in the range of 1 second to 10 seconds. For the large

temperature differences and high heat transfer coefficient used in this

analysis, the period is closer to 1 second than 4 seconds. A longer period

would yield a lower heat transfer coefficient, and therefore smaller

changes in metal temperatures. However, to be conservative, the same

heat transfer coefficient was used for all cases.

The stresses due to each gradient as a function of time were calculated

using formulas in ASME Code Section III, NB-3653.2. Table 3.5.3-2 lists

the alternating stress calculated for each of the four transients used for

evaluating fatigue. As can be seen from this table only one of the four

transients contributes anything to fatigue. That transient is number four

(4) with an alternating stress of 15,780 psi and a number of allowable

cycles of 1.42E7.

Page 2 of 4

Waterford 3 Pressurizer Surge Line Temperature Change Rate

Waterford 3 Design Specification 9270-PE-140 is the project specification for

reactor coolant pipe and fittings. This document provides a summary of the

design analysis for surge line temperature transients. It includes text sections

and 2 tables as they apply to the surge line and surge line nozzle. The tables

address temperature differences anticipated as a result of thermal stratification.

Table 4.5.15.3.1 lists expected occurrences of temperature differences between

the pressurizer and the RCS hot leg and provides the number of expected

occurrences. Table 4.5.15.3.2 lists expected occurrences of temperature

differences between the top and bottom of the surge line piping. These

temperatures differences are for the pressurizer surge line piping and not the

fluid temperature in the piping. The number of occurrences is the expected

number for the life of the plant.

Entergy Position

The Entergy position is that pressurizer surge line temperature is not required to

be specifically monitored per procedure to ensure the design limits are

maintained, and that FSAR Section 5.4.3.1 should have been revised in 1993

when the Waterford 3 stress and fatigue analyses and design specifications were

revised per NRC Bulletin 88-11 to reflect the results of CEN-387-P, Revision 1.

This section of the FSAR has not been revised since the initial FSAR. CR-WF3-

2006-0839 was initiated to revise the FSAR. The reasoning for Entergys

position is documented in the paragraphs below.

The pressurizer surge line temperatures during heatup and cooldown are

maintained by ensuring the heatup and cooldown limits in the RCS and

pressurizer are maintained. The RCS limits are located in the TS and the

pressurizer limits are located in the TRM. Temperature changes in the surge line

can be greater than 200°F due to thermal stratification and thermal stripping.

CEN-387-P, Revision 1 documented that the pressurizer surge line meets Code

stress and fatigue requirements for the 40 year design life of the facility

considering the phenomenon of thermal stratification and thermal stripping.

Analysis in the CEN has indicated that temperature differences of up to 340°F

have been evaluated for.

The data recorded by the temperature element in the surge line has shown

periods of temperature changes greater than 200°F/hr. Thermal stratification is

applicable to all of these recorded temperature changes. These temperature

changes do not necessarily reflect the average temperature change of the surge

line but reflects a change in local fluid temperature at the temperature element.

This recorded temperature changes over time are not the same delta

temperatures listed in the tables in 9270-PE-140.

Therefore, the temperature difference in the pressurizer surge line is bounded by

the analysis performed in CEN-387-P, Revision 1 and monitoring pressurizer

Page 3 of 4

Waterford 3 Pressurizer Surge Line Temperature Change Rate

surge line temperature per procedure during heatup and cooldown is not

necessary.

Additional Information

The additional information specifically addresses the difference between the

surge line temperature increase seen during Refuel 13 and during the shutdown

for Hurricane Katrina, and the delta temperature values in 9720-PE-140. It also

addresses the reason Waterford 3 does not currently monitor surge line

temperature during heatups and cooldowns.

There following information is clarification regarding cycles listed in Design

Specification 9270-PE-140 and the temperatures recorded in PI with the

temperature element located in the surge line. The graphical data recording the

single surge line temperature element over time for our Refuel 13 outage and the

Hurricane Katrina outage indicates periods of temperature changes greater than

200 degrees within one hour. Thermal stratification is applicable to all of these

recorded temperature changes. Thermal stratification temperature changes were

addressed by CEN-327-P (NRC accepted response to NRC Bulletin 88-11). This

single temperature element does not necessarily reflect the average temperature

change of the surge line but reflects a change in local fluid temperature at the

temperature element. The recorded temperature changes of a single point over

time is not the same delta temperatures listed in the tables of the W3 Design

specification of RCS Piping and Fitting document (document #9270-PE-140).

The table 4.5.15.3.1 lists expected occurrences of temperature differences

between two different locations; the pressurizer and the RCS hot leg and

provides the number of expected occurrences. Table 4.5.15.3.2 lists expected

occurrences of temperature differences between the top and bottom of the surge

line piping. These tables clearly state this information at the end of their

respective sections. Thus comparing a graph of temperature changes with

respect to time to these tables is not appropriate.

The effects on the Pressurizer Surge Line due to thermal stratification and

thermal stripping were evaluated in CEN-327-P, Revision 1. This was reviewed

by the NRC and in the SER the Staff concluded that the surge line meets ASME

Code stress and fatigue requirements for the 40-year design life. Waterford 3

currently monitors heatups and cooldowns of the RCS and Pressurizer. The

effects of these heatups and cooldowns on the pressurizer surge line have been

evaluated in CEN-327-P.

Page 4 of 4

ATTACHMENT C

White Paper on Effect of Diesel Sump Pump

Inoperability on Ultimate Heat Sink Operability

1.0 Purpose

This paper provides an answer to the question, what is the original licensing

basis for flood protection of essential equipment in the Dry Cooling Tower Areas?

The paper also provides the chronology of regulatory requirements and licensing

bases that support the conclusion.

2.0 Conclusion Regarding Licensing Basis

The original licensing basis for essential equipment in the Dry Cooling Tower

areas is that essential equipment be protected from Standard Project Storm

(SPS).

The elements of the licensing basis are the following:

§ The SPS, with all installed sump pumps inoperative, was analyzed as an

event less severe than the probable maximum precipitation.

§ Provisions are required to be in place for emplacing the portable sump pump

within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of an SPS event to ensure that the ponding level from SPS

does not adversely affect essential equipment if installed pumps are

inoperative.

§ The electric pumps are seismically designed but not seismically qualified;

therefore they were assumed not to be available following an OBE.

§ The probability of the occurrence of an SPS and OBE is 3.6E-8 and

negligible.

In essence, the original licensing basis required that the portable sump pump be

emplaced and started within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of the start of an SPS (sump high level

alarm) to ensure that essential equipment in the DCT areas is not flooded.

On July 26, 1999, Condition Report CR-WF3-1999-0789 was initiated to identify

that the Dry Cooling Tower sump pump capacities were not sufficient to meet the

original licensing basis.

A new discharge path for the DCT sump pumps was installed via DCP-3251.

The DCP also replaced the 1 portable sump pump that had a capacity of 100

gpm with 2 portable sump pumps having a capacity of 300 gpm each. The

installed sump pumps capacities were reduced from 325 gpm to 270 gpm due to

the new piping configuration. The revised time frame for starting the portable

sump pump to ensure essential equipment is not flooded was re-established as 3

hours from the start of an SPS (sump high level alarm). Procedure OP-901-521

instructs Operations to operate the DCT Portable Sump Pumps in accordance

with OP-003-024, Sump Pump Operation within 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> of the sump level alarm.

3.0 Chronology

Regulatory Guide 1.70, Revision 2, September 1975

Waterford 3 is committed to Regulatory Guide 1.70, Revision 2, as noted in

section 1.8 of FSA

R. Neither Regulatory Guide Section 2.4.2.3, Effects of Local

Intense Precipitation, or Section 2.4.3.1, Probable Maximum Precipitation

(PMP), have any requirement to consider OBE or SPS concurrently.

Regulatory Guide Section 2.4.2.3 states:

Describe the effects of local probable maximum precipitation (see Section

2.4.3.1) on adjacent drainage areas and site drainage systems, including

drainage from the roofs of structures. Summarize the design criteria for site

drainage facilities and provide analyses that demonstrate the capability of site

drainage facilities to prevent flooding of safety related facilities resulting from

local probable maximum precipitation.

The fundamental requirement in the Regulatory Guide is that the applicant

ensures that safety related equipment is not adversely impacted from maximum

precipitation.

Regulatory Guide 1.59, Revision 2, August 1977

Waterford 3 is committed to Regulatory Guide 1.59, Revision 2, as noted in

section 1.8 of FSA

R. Regulatory Guide 1.59, Revision 2, does not have a

specific requirement to consider OBE and SPS concurrently.

Two important requirements are discussed in the Regulatory Guide.

First, seismically induced floods are associated with land features specific to

each site such as streams, estuaries, dam failures, and landslides. This

requirement does not apply to flooding in the DCT sump areas.

Second, the Regulatory Guide states that the most severe flood conditions may

not indicate potential threats to safety related systems that might result from

combination of flood conditions thought to be less severe. The Regulatory Guide

states that reasonable combinations of less severe flood conditions should be

considered to the extent needed. The Regulatory Guide states that such

combinations should be evaluated in cases where the probability of their

existing at the same time and having significant consequences is at lease

comparable to that associated with the most severe hydro-meteorological or

seismically induced flood. We judge that the requirement to consider the SPS

originates from this requirement. Also, since the probability of a SPS and OBE

concurrent was later established to be negligible, we judge that not considering

the SPS concurrent with the OBE is in conformance with the Regulatory Guide.

Standard Review Plan 2.4.3, Revision 2 July 1981

Standard Review Plan 2.4.3 does not have a specific requirement to consider

OBE and SPS concurrently.

Standard Review Plan 2.4.3,Section I, states:

Included is a review of the details of site drainage, including the roofs of safety

related structures, resulting from potential PMP probable maximum

precipitation

Standard Review Plan 2.4.3,Section IV, states:

The local PMF resulting from the estimated local PMP was found not to cause

flooding of safety related facilities, since the site drainage system will be capable

of functioning adequately during such a storm.

The fundamental requirement in the Standard Review Plan is that the applicant

ensures that safety related equipment is not adversely impacted form maximum

precipitation.

NRC Safety Evaluation Report, July 1981

The NRC evaluates the effects of a 6-hr duration PMP on the open cooling tower

areas and adjacent roofs. The NRC concludes that, assuming one sump pump

in each area is inoperable and that the roof drainage system is clogged with

debris during the PMP, that the ponding could inundate the transformers and

MCCs in the cooling tower areas.

The Safety Evaluation Report makes no reference to SPS or OB

E.

FSAR Amendment 25, January 1982

FSAR Section 2.4.2.3.4 was initially added to the FSAR; previously it did not

exist. This FSAR Section is titled, Effects of Standard Project Storm (SPS) on

Cooling Tower Areas.

Two important aspects of the licensing basis are established in this FSAR

Section.

First, a probability evaluation is documented establishing that the occurrence of

an SPS and OBE is 3.6 E-8 and negligible.

Second, FSAR Section states that the SPS was still analyzed, assuming

inoperability of all pumps, in order to determine the time available before levels

are reached that could affect essential equipment in the Cooling Tower Areas.

Safety Evaluation Report, Supplement 4, October 1982

The SER states the following:

An alternative combination which should be considered is an operating basis

earthquake (OBE), which fails the sump pumps, coincident with a rainfall event

less than the PMP. This combination is considered appropriate since the pumps

are not seismically qualified1, and thus cannot be shown to be operable following

a seismic event. The staff therefore, requested that the applicant provide an

analysis of the effects of a standard project storm (SPS)2 assuming all four

pumps in the cooling tower areas are inoperable.

The SER further states:

the staff considered a SPS of 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> duration. This event would produce a

total rainfall of about 23 inches and would result in a ponding depth of about 1.9

ft in the cooling tower areas assuming that all four pumps are inoperable. Since

this is higher than the maximum allowable ponding depth of 1.71 feet, the

applicant has proposed to provide a portable pump with a pumping capacity of

100 gpm and sufficient head to pump over the cooling tower wall. a provision

will be included for emplacing the portable pump within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of a seismic

event if the installed pumps fail.

FSAR Amendment 33, September 1983

FSAR Amendment 33 revises Section 2.4.2.3.4 to state the following:

The maximum height to which rainwater can rise in this area before essential

equipment is reached is 1.71 ft (see subsection 2.4.2.3.3d). As shown in Table

2.4-6c, this level would not be reached for over seven hours into the SP

S.

Furthermore, a portable pump is provided, with a pumping capacity of 100 gpm

and sufficient head to pump over the cooling tower wall. Provisions are included

for emplacing the portable pump within six hours of a seismic event if the

installed pumps fail and heavy rains are expected.

Thus, the FSAR Amendment 33 is in agreement with NRC SER Supplement 4 in

that the fundamental requirement is to protect essential equipment in the cooling

tower areas in the event of a SPS. The specific requirement in FSAR

Amendment 33 is that provisions be made for emplacing the portable sump

pump within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of a SPS event and that essential equipment be protected,

by ensuring that the ponding level does not reach 1.71 ft. The seismic event is a

vehicle to postulate the installed pumps are not available; however, important to

the licensing basis is the condition that the electric sump pumps will not be

available and that essential equipment needs to be protected prior to the ponding

level reaching 1.71 ft.

NRC Letter dated December 18 1984, Issuance of Five Percent Power License,

The NRC issues five percent power license, and Section 2.B.2 of the license

approves operation as described in FSAR as supplemented and amended

through Amendment 36.

NRC Letter dated March 16, 1985, Issuance of 100% Power License

The NRC issues 100 percent power license, and Section 2.B.2 of the license

approves operation as described in FSAR as supplemented and amended

through Amendment 36.

Design Change, July 26, 1999

On July 26, 1999, Condition Report CR-WF3-1999-0789 was initiated to identify

that the Dry Cooling Tower sump pump capacities were not sufficient to meet the

original licensing basis.

A new discharge path for the DCT sump pumps was installed via DCP-3251.

The DCP also replaced the 1 portable sump pump that had a capacity of 100

gpm with 2 portable pumps having a capacity of 300 gpm each. The installed

sump pumps capacities were reduced from 325 gpm to 270 gpm due to the new

piping configuration. The revised time frame for ensuring essential equipment is

not flooded was re-established as 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> from the start of SPS (sump high level

alarm). Procedure OP-901-521 instructs Operations to operate the DCT Portable

Sump Pumps in accordance with OP-003-024, Sump Pump Operation within 3

hours of the sump level alarm.

5