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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217H6341999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for Kh Curran,Lm Gerlach,Rc Weber & Bt Rhodes Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC Form 396 Encl.Proprietary Info Withheld ML20217H6251999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for MR Kahn,Aj Mclaughlin,De Montgomery & Kr Murphy Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC from 396 Encl.Proprietary Info Withheld ML20217F4301999-10-14014 October 1999 Responds to 991012 Rai,Based on 991001 Telcon Re Suppl to Request for TS Change to Revise MCPR Safety Limit & Add Approved Siemens Topical Rept for LaSalle County Station, Unit 1 ML20217D3191999-10-12012 October 1999 Submits Request for Addl Info Re Licensee 990707 Proposed License Amend to Revise Min Critical Power Ratio.Listed Questions Were Discussed with Util in 991001 Telcon ML20217C1671999-10-0808 October 1999 Provides Suppl to RAI for Approval of Unreviewed Safety Question Re Assessment of Certain safety-related Concrete Block Walls at LaSalle County Station,Units 1 & 2 ML20217A7601999-10-0606 October 1999 Forwards Insp Repts 50-373/99-15 & 50-374/99-15 on 990729-0916.One Violation of NRC Requirements Occurred & Being Treated as Ncv,Consistent with App C of Enforcement Policy ML20212M0931999-10-0404 October 1999 Refers to 990922-23 Meeting Conducted by Region II at LaSalle Nuclear Power Station.Purpose of Visit,To Meet with Licensee Risk Mgt Staff to Discuss Util Initiatives in Risk Area & to Establish Dialog Between SRAs & Risk Mgt Staff 05000373/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl1999-10-0404 October 1999 Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20217A6201999-09-30030 September 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC Feedback on Any Planned Insps Which May Conflict with Plant Activities.Plant Issue Matrix & Insp Plan Encl ML20212E7171999-09-22022 September 1999 Forwards RAI Re Requesting Approval of License Amend to Use Different Methodology & Acceptance Criteria for Reassessment of Certain Masonry Walls Subjected to Transient HELB Pressurization Loads 05000374/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl1999-09-20020 September 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl ML20212C0591999-09-17017 September 1999 Informs That NRC Reviewed Licensee Justifications for Deviations from NEDO-31558 & Determined That Justifications acceptable.Post-accident Neutron Flux Monitoring Instrumentation Acceptable Alternative to Reg Guide 1.97 ML20212A3581999-09-13013 September 1999 Confirms That Fuel MCPR Data for LaSalle County Station,Unit 1,Cyle 9,sent by Ltr Meets Condition 2,as Stated in 970509 NRC Ltr ML20211Q9911999-09-10010 September 1999 Informs That License SOP-4048-4,for Wp Sly May Be Terminated Due to Individual Retiring ML20212A1141999-09-10010 September 1999 Forwards RAI Re Licensee 990519 Amend Request,Which Proposed to Relocate Chemistry TSs from TS to licensee-controlled Documents.Response Requested by 990930,so That Amend May Be Issued to Support Upcoming Unit 1 Refueling Outage ML20211P2211999-09-0808 September 1999 Forwards Insp Repts 50-373/99-14 & 50-374/99-14 on 990809- 13.No Violations Noted.Insp Concluded That Emergency Preparedness Program Maintained in Good State of Operational Readiness ML20212A8571999-09-0707 September 1999 Informs That Proprietary Document, Power Uprate SAR for LaSalle County Station,Units 1 & 2, Rev 2,Class III, NEDC-32701P,submitted in ,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20211Q6861999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Plant License Applicants During Wks of 001113 & 20. Validation of Exam Will Occur at Station During Wk of 001023 05000374/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl1999-09-0303 September 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl ML20211M1151999-08-31031 August 1999 Requests That Following Eleven Individuals Take BWR Gfes of Written Operator Licensing Exam to Be Administered on 991006 ML20211G1831999-08-27027 August 1999 Provides Addl Clarification of Proposed Refueling Practices Under Proposed Core Alterations Definition Re 990813 Application for Amend to TS ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211F8731999-08-25025 August 1999 Forwards Insp Repts 50-373/99-13 & 50-374/99-13 on 990804-06 & 09-11.No Violations Noted.Fire Protection Program Strengths Includes Low Number of Fire Protection Impairments & Excellent Control of Transient Combustibles ML20210U3201999-08-17017 August 1999 Forwards Insp Repts 50-373/99-12 & 50-374/99-12 on 990623-0728.No Violations Noted ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed 05000373/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed1999-07-23023 July 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed ML20210E0501999-07-22022 July 1999 Submits Summary of 990630 Management Meeting Re Licensee Performance Activities Since Start Up of Unit 2.List of Attendees & Matl Used in Presentation Enclosed ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20209H5171999-07-15015 July 1999 Discusses 990701 Telcon Re Arrangements for NRC to Inspect Licensed Operator Requalification Program at LaSalle County Nuclear Generating Station for Weeks of 990913,1018 & 1129 ML20209G4031999-07-14014 July 1999 Forwards Insp Repts 50-373/99-11 & 50-374/99-11 on 990614-18.No Violations Noted ML20209E1211999-07-14014 July 1999 Submits mid-cycle Rev of COLR IAW LaSalle County Tech Spec 6.6.A.6.d.Rev to COLR Was Necessary Due to Implementation of TS Change Approved by Ltr Dtd 990212,which Changed Turbine Stop Valve & Turbine Control Valve Scram ML20209F6931999-07-13013 July 1999 Forwards Insp Repts 50-373/99-04 & 50-374/99-04 on 990513-0622.No Violations Noted.Determined That Multiple Challenges to Main Control Room Operators Occurred During Insp Period Due to Human Performance Weaknesses ML20210C1521999-07-0909 July 1999 Forwards Post-Outage (90 Day) Summary Rept for ISI Examinations & Repair/Replacement Activities Conducted from Beginning of First Insp Period of Second ten-yr Insp Interval Through L2R07 Refueling Outage ML20209G3901999-07-0909 July 1999 Informs NRC of Status of Commitments & Requests NRC Concurrence for Use of ASME Section III App F Acceptance Criteria to Permanently Qualify Units 1 & 2 Penetrations M-49 & M-50 ML20209E0341999-07-0909 July 1999 Provides NRC with Siemens Power Corp (SPC) Fuel & GE Fuel MCPR Data for LaSalle Unit 1 Cycle 9.LaSalle Unit 1 Is Currently Scheduled to Start Cycle 9 in 991101 ML20209E0361999-07-0808 July 1999 Forwards LaSalle County Station Unit 2 Cycle 8 Startup Test Rept Summary,Iaw TS NPF-18,Section 6.6.A.1.Startup Test Program Was Satisfactorily Completed on 990501 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196J4711999-06-30030 June 1999 Discusses Closure of GL 92-01,Rev 1,Suppl 1, Rv Structural Integrity, Issued on 950519 to Plant,Units 1 & 2 ML20212J0311999-06-21021 June 1999 Informs of Actions Taken to Close Remaining Open Items in .Attachment Provides Detailed Justification for Closure of Open Items in Sections 5.2.2 & 5.2.8 ML20196B1951999-06-18018 June 1999 Informs NRC That Do Werts,License OP-30373-2,no Longer Requires Use of NRC License for LaSalle County Station. License May Be Terminated ML20195J7761999-06-15015 June 1999 Submits Request Relief CR-23,requesting Relief from Code Required Selection & Examinations of Noted Integral Attachments & Proposes to Utilize Alternative Selection & Examination Requirements Similar to Code Case N-509 ML20196G8021999-06-15015 June 1999 Requests Renewal of SRO License for Vv Masterson.Current License for Vv Masterson Will Expire Jul 1999.NRC Forms 398 & 396,encl.Without Encls ML20195G7101999-06-11011 June 1999 Informs That Effective 990514,GH Mccallum,License SOP-31412, No Longer Requires Use of NRC License for LaSalle Station. License Should Be Terminated ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20207D2821999-05-27027 May 1999 Requests That Implementation Date for Unit 1 Be Changed Prior to Startup for L1C10 to Allow Best Allocation of Resources to Implement Unit 1 Amend Prior to Startup for Either L1C9 or L1C10.Unit 2 Will Implement Mod IAW Request 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217H6251999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for MR Kahn,Aj Mclaughlin,De Montgomery & Kr Murphy Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC from 396 Encl.Proprietary Info Withheld ML20217H6341999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for Kh Curran,Lm Gerlach,Rc Weber & Bt Rhodes Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC Form 396 Encl.Proprietary Info Withheld ML20217F4301999-10-14014 October 1999 Responds to 991012 Rai,Based on 991001 Telcon Re Suppl to Request for TS Change to Revise MCPR Safety Limit & Add Approved Siemens Topical Rept for LaSalle County Station, Unit 1 ML20217C1671999-10-0808 October 1999 Provides Suppl to RAI for Approval of Unreviewed Safety Question Re Assessment of Certain safety-related Concrete Block Walls at LaSalle County Station,Units 1 & 2 05000373/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl1999-10-0404 October 1999 Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr 05000374/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl1999-09-20020 September 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl ML20211Q9911999-09-10010 September 1999 Informs That License SOP-4048-4,for Wp Sly May Be Terminated Due to Individual Retiring 05000374/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl1999-09-0303 September 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl ML20211M1151999-08-31031 August 1999 Requests That Following Eleven Individuals Take BWR Gfes of Written Operator Licensing Exam to Be Administered on 991006 ML20211G1831999-08-27027 August 1999 Provides Addl Clarification of Proposed Refueling Practices Under Proposed Core Alterations Definition Re 990813 Application for Amend to TS ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed 05000373/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed1999-07-23023 July 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed ML20209E1211999-07-14014 July 1999 Submits mid-cycle Rev of COLR IAW LaSalle County Tech Spec 6.6.A.6.d.Rev to COLR Was Necessary Due to Implementation of TS Change Approved by Ltr Dtd 990212,which Changed Turbine Stop Valve & Turbine Control Valve Scram ML20210C1521999-07-0909 July 1999 Forwards Post-Outage (90 Day) Summary Rept for ISI Examinations & Repair/Replacement Activities Conducted from Beginning of First Insp Period of Second ten-yr Insp Interval Through L2R07 Refueling Outage ML20209E0341999-07-0909 July 1999 Provides NRC with Siemens Power Corp (SPC) Fuel & GE Fuel MCPR Data for LaSalle Unit 1 Cycle 9.LaSalle Unit 1 Is Currently Scheduled to Start Cycle 9 in 991101 ML20209G3901999-07-0909 July 1999 Informs NRC of Status of Commitments & Requests NRC Concurrence for Use of ASME Section III App F Acceptance Criteria to Permanently Qualify Units 1 & 2 Penetrations M-49 & M-50 ML20209E0361999-07-0808 July 1999 Forwards LaSalle County Station Unit 2 Cycle 8 Startup Test Rept Summary,Iaw TS NPF-18,Section 6.6.A.1.Startup Test Program Was Satisfactorily Completed on 990501 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20212J0311999-06-21021 June 1999 Informs of Actions Taken to Close Remaining Open Items in .Attachment Provides Detailed Justification for Closure of Open Items in Sections 5.2.2 & 5.2.8 ML20196B1951999-06-18018 June 1999 Informs NRC That Do Werts,License OP-30373-2,no Longer Requires Use of NRC License for LaSalle County Station. License May Be Terminated ML20196G8021999-06-15015 June 1999 Requests Renewal of SRO License for Vv Masterson.Current License for Vv Masterson Will Expire Jul 1999.NRC Forms 398 & 396,encl.Without Encls ML20195J7761999-06-15015 June 1999 Submits Request Relief CR-23,requesting Relief from Code Required Selection & Examinations of Noted Integral Attachments & Proposes to Utilize Alternative Selection & Examination Requirements Similar to Code Case N-509 ML20195G7101999-06-11011 June 1999 Informs That Effective 990514,GH Mccallum,License SOP-31412, No Longer Requires Use of NRC License for LaSalle Station. License Should Be Terminated ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20207D2821999-05-27027 May 1999 Requests That Implementation Date for Unit 1 Be Changed Prior to Startup for L1C10 to Allow Best Allocation of Resources to Implement Unit 1 Amend Prior to Startup for Either L1C9 or L1C10.Unit 2 Will Implement Mod IAW Request ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206R4561999-05-12012 May 1999 Provides Notification That Ws Jakielski,License SOP-30168-3, Is Being Reassigned & No Longer Requires Use of NRC License, IAW 10CFR50.74 05000373/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(ii).Attachment a Provides Commitments for Submittal1999-05-0707 May 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(ii).Attachment a Provides Commitments for Submittal ML20206K7081999-05-0707 May 1999 Forwards 10CFR50.46(a)(3) Rept Re Significant Change in Calculated Pct.Loca Analyses for Both GE Fuel & Siemens Power Corp Fuel Demonstrates Results within All of Acceptance Criteria Set Forth in 10CFR50.46 ML20206K1861999-04-30030 April 1999 Informs That in Comed Submitted Annual Exposure Rept for Personnel Receiving Greater than 0 Mrem/Yr Rather than 100 Mrem/Yr.Updated Rept Limiting Data to Personnel Receiving Greater than 100 Mrem/Yr,Attached ML20206R0751999-04-30030 April 1999 Forwards License Renewal Applications & Certification of Medical Examinations for LaSalle County Station Personnel Whose Licenses Expire in Nov.Personnel Listed.Without Encls ML20206F0931999-04-30030 April 1999 Forwards LaSalle County Nuclear Power Station,Units 1 & 2 Effluent & Waste Disposal Semi-Annual Rept for 1998. LaSalle County Station Tech Specs Recently Revised to Reduce Periodicity of 10CFR50.36a ML20206D5921999-04-28028 April 1999 Forwards Annual Environ Operating Rept for 1998 for Environ Protection Plan, for LaSalle County Station,Units 1 & 2. Rept Includes Info Required by Listed Subsections of App B to Licenses NPF-11 & NPF-18 ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20205L8161999-04-0808 April 1999 Advises NRC of Util Review & Approval of Cycle 8 Reload Under Provisions of 10CFR50.59 & Transmit COLR for Upcoming Cycle Consistent with GL 88-16.Reload Licensing Analyses Performed for Cycle 8 Utilize NRC-approved Methodologies ML20205J9451999-04-0505 April 1999 Submits Petition Per 10CFR2.206 Requesting That LaSalle County Nuclear Plant Be Immediately Shut Down & OL Suspended or Modified Until Such Time That Facility Design & Licensing Bases Are Properly Updated ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util ML20207J9841999-03-0505 March 1999 Informs That Effective 990212,KC Dorwick Has Resigned & No Longer Requires Use of NRC License for LaSalle County Station ML20207F9581999-03-0101 March 1999 Requests That Initial License Examination Currently Scheduled for Weeks of May 15 & 22,2000 Be Changed to Weeks of Nov 13 & 20,2000.Class Size Is Projected to Be Twelve RO & SRO Candidates ML20207C7251999-03-0101 March 1999 Forwards Annual Rept for LaSalle County Station, for Period of 980101-981231.App E to Rept Provides Info on All Personnel Receiving Exposures of More than 0 Mrem/Yr Rather than 100 Mrem/Yr Requirement of TS 6.6.A.2 ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) ML20207C8401999-02-25025 February 1999 Forwards Rev 60 of Comed LSCS Security Plan,Iaw 10CFR50.4(b) (4).Rev Eliminates Requirement for Annual change-out of Vital & PA Keys & Locks & re-configuration of PA Fence Around North Access Facility.Rev Withheld ML20207A9361999-02-24024 February 1999 Forwards Rev 4 to Restart Plan,To Reflect Review,Oversight & Approval Process Necessary to Restart Unit 2.Review & Affirmation Process Will Focus on Station Capability to Support Safe Dual Unit Operations 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059H5321990-09-11011 September 1990 Requests Withdrawal of Application for Amend to Licenses NPF-11 & NPF-18,per 891215 & s.Amend Would Have Removed Applicability of Tech Spec (TS) 3.0.4 to TS 3.6.5.2, Secondary Containment Automatic Isolation Dampers ML20059H4271990-09-0707 September 1990 Provides Supplemental Response to NRC Bulletin 90-001.Plant Initial Review of Calibr Records Completed on 900831 ML20059G0941990-09-0505 September 1990 Forwards LaSalle County Station Unit 2 Third Refueling Outage,Asme Section XI Summary Rept for Spring 1990 Insp ML20059C6891990-08-30030 August 1990 Forwards LaSalle County Nuclear Power Station Unit 2,Cycle 4 Startup Test Rept & Test Rept Summary ML20056B4061990-08-21021 August 1990 Submits Supplemental Response to Generic Ltr 88-14 Re Design & Verification of Instrument Air Sys.Mfg Purchase Specs & Vendor Manuals Reviewed for Air Quality Requirements ML20059B8961990-08-14014 August 1990 Documents Approval of Schedular Extension & Accepts Human Engineering Discrepancies Discussed ML20059D1731990-08-10010 August 1990 Responds to NRC Re Exercise Weaknesses Noted in Insp Repts 50-373/90-05 & 50-374/90-06.Corrective Actions: LOA-FP-01, Fire Alarm Response Will Be Revised to Alert Control Room Operators to Refer to Emergency Action Levels ML20058N2971990-08-0606 August 1990 Forwards Rev 34 to Security Plan.Rev Details Addl Gate Position for Security Testing & Maint.Rev Withheld (Ref 10CFR73.21) ML20064A5491990-07-27027 July 1990 Responds to NRC Re Violations Noted in Insp Repts 50-373/90-12 & 50-374/90-13.Corrective Actions:Program Implemented Identifying & Correcting Repetitive Local Leak Rate Failures Through Testing & LER Investigation ML20056A7031990-07-27027 July 1990 Responds to NRC Re Violations Noted in Insp Repts 50-373/90-13 & 50-374/90-14.Corrective actions:LRP-1250-3 Revised to Include Addl Requirement for Extremity Monitoring ML20055H7631990-07-25025 July 1990 Forwards Financial Info Re Decommissioning of Plants ML20055H7661990-07-24024 July 1990 Forwards Supplemental Response to Generic Ltr 90-04, Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions ML20055G2011990-07-13013 July 1990 Forwards Corrected Monthly Operating Rept for June 1990 for LaSalle County Unit 1.Outage/Reduction 16 Corrected ML20055F1831990-07-0909 July 1990 Provides Status Rept on Breaker Replacements in Response to NRC Bulletin 88-010.Breaker Replacements for Plants Scheduled to Be Completed by 901031 ML20044B1751990-07-0909 July 1990 Responds to NRC Request for Addl Info Re Util 890726 Proposed Amend to Tech Specs to Allow Continued Operation for Period of 12 H W/Main Steam Tunnel High Ambient Temp & High Ventilation Sys Differential Trips Bypassed ML17202L2861990-07-0202 July 1990 Forwards Dresden II Upper Vessel Contract Variation Review, La Salle II Upper Vessel Fabrication Summary & Quad-Cities II Upper Vessel Fabrication Summary. ML20055D1921990-06-29029 June 1990 Responds to Generic Ltr 90-04 Re Status of Licensee Implementation of Generic Safety Issues ML20055J2021990-06-26026 June 1990 Responds to NRC Re Violations Noted in Insp Repts 50-373/90-06 & 50-374/90-06.Corrective Actions:Perimeter Zone Repairs Commenced on Schedule & Completely Functional & Out of Compensatory Measures on 900614 ML20044A5071990-06-22022 June 1990 Forwards Revised Response to Station Blackout Rule for Plant.During Blackout Event,Plant Can Utilize RCIC Sys or HPCS to Provide Required Reactor Vessel Inventory Makeup ML20043E8651990-06-0707 June 1990 Forwards Relief Request RV-57 for Emergency Fuel Pool Makeup Crosstive Vent Valve 1(2)E12-F097.Expedious Review of Request Requested Because Valve 1(2)E12-F097 Inoperable & Will Remain So Until NRC Approval Received ML20043D3221990-06-0101 June 1990 Forwards Rev 33 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043C8241990-06-0101 June 1990 Advises of Intentions to Review & Approve Cycle 4 Reload,Per 10CFR50.59 & Forwards Rev 1 to LAP-1200-16, Core Operating Limits Repts for LaSalle County Station Unit 2,Reload 3, Cycle 4, Per Generic Ltr 88-16 ML20043B6581990-05-25025 May 1990 Requests Schedular Extension of Two Human Engineering Deficiencies Re CRT Displays W/Current Ramtek Sys & Approval to Leave Seven Human Engineering Discrepancies Accepted as Is. ML20043B7921990-05-23023 May 1990 Forwards Endorsements 14 to Nelia Policy N-71 & Maelu Policy M-71 & Endorsements 12 to Nelia & Maelu Policies N-83 & M-83,respectively ML20042E8841990-04-30030 April 1990 Responds to Generic Ltr 89-04 Re Weaknesses of Inservice Testing Programs.Plant Has Implemented Rev 2 of Inservice Testing Program Submitted by Util 891002 & 24 Ltrs.No Equipment Mods Required as Result of Generic Ltr ML20042F3591990-04-29029 April 1990 Provides Suppl Response to NRC Bulletin 88-004, Potential Safety-Related Pump Loss. Precaution Added to Operating Procedures Which Allows ECCS Pump to Be Secured & Restarted as Necessary to Preclude Running Pumps at Min Flow ML20042F0341990-04-23023 April 1990 Forwards Part 3 to 1989 Operating Rept,Containing Results of Radiological Environ & Meteorological Monitoring Programs. W/O Encl ML20064A6281990-03-30030 March 1990 Submits Supplemental Response to Insp Repts 50-373/86-04 & 50-374/86-04 Re Fire Detection Concerns,Per NRC 900214 Request.Proposed Administrative Controls & Training Will Eliminate Concerns That Assure Protection of Personnel ML20055E1461990-03-29029 March 1990 Provides Supplemental Response to Re Violations Noted in Insp Repts 50-373/89-18 & 50-374/89-18 on 890724- 0825.Corrective Actions:Plant Performs Safety Evaluation for Mods Not Designed by Corporate Nuclear Engineering Dept ML20012C6991990-03-15015 March 1990 Forwards Corrected Tech Spec Page to 881129 Application for Amend to Licenses NPF-11 & NPF-18,removing Specific Load Profiles for Each Dc Battery ML20012B6541990-02-26026 February 1990 Forwards LaSalle County Station Unit 1 Third Refueling Outage ASME Section XI Summary Rept, for Fall 1989 Inservice Insps Performed.Conditions Observed & Corrective Measures Taken Also Contained in Rept ML20006E7421990-02-0909 February 1990 Responds to NRC 900110 Ltr Re Violations Noted in Insp Repts 50-373/89-23 & 50-374/89-22.Corrective Actions:Ltr from Station Manager to All Dept Heads Was Issued on 891218, Discussing Personnel Performance Issues ML20005F5771990-01-0808 January 1990 Documents Guidance Given by P Shemanski Re Typos in Earlier Approved Amend to License NPF-11.Guidance Should Adhere to Wording of Unit 2 Tech Specs.Guidance Given on 900105 & Will Be Followed Until Correction Made at NRR Ofcs ML20011D9661989-12-22022 December 1989 Forwards Core Operating Limits Rept for LaSalle County Station Unit 1,Reload 3 (Cycle 4). Intention to Review & Approve Cycle 4 Reload Under Provisions of 10CFR50.59 Stated ML20005E1661989-12-22022 December 1989 Forwards Rev 32 to Security Plan,Reflecting Administrative Changes in Mgt Structure at Facilities.Rev Withheld (Ref 10CFR73.21) ML19332E4531989-11-29029 November 1989 Responds to Generic Ltr 89-21, Status of Implementation of USI Requirements. Response to USI A-48 Expected by 900319 ML19332C2461989-11-0808 November 1989 Provides Supplemental Response to Insp Repts 50-373/88-05 & 50-374/88-05 on 890302-10.Scheduled Completion Dates for Sample Panel Mods Changed from Third to Fourth Refueling Outages of Each Unit ML19325E5191989-10-31031 October 1989 Forwards Qualification Test Rept QTR87-018, Max Credible Fault Tests CM249-Q2 Carrier Modulator for Fermi 2 SPDS, in Response to NRC 890304 Request for Addl Info Re Facility Validyne Isolator CM-249 ML19325E3601989-10-26026 October 1989 Forwards Addl Info Re Application for Amend to Licenses NPF-11 & NPF-18,revising Tech Specs to Conform W/Diesel Generator Test Schedule Recommendations,Per Generic Ltr 84-15 ML19325E7921989-10-24024 October 1989 Submits Response to SALP 8 Board Repts 50-373/89-01 & 50-374/89-01.Expresses Appreciation for NRC Recognition of High Level of Performance in Area of Plant Operations, Emergency Preparedness & Security ML19325E0941989-10-24024 October 1989 Forwards Clarification to Summary of Changes Made in Rev 2 to Plant Inservice Testing Program ML19353A9051989-10-23023 October 1989 Responds to NRC 890921 Ltr Re Violations Noted in Insp Repts 50-373/89-19 & 50-374/89-19.Corrective Actions:Hose Connection That cross-connected Svc Air Sys W/Clean Condensate Sys Uncoupled & Secured ML17285A8081989-10-18018 October 1989 Responds to Request for Info on Environ Qualification of Taped Electrical Splices.Scotch Tapes Allowed by Electrical Test Guide Included Scotch 33,23 & 70 ML19325D1931989-10-13013 October 1989 Forwards Quarterly Rept on Static-O-Ring Failures Third Quarter 1989,per IE Bulletin 86-002.Stated Switches Replaced ML19327B0431989-10-0505 October 1989 Responds to NRC 890821 Ltr Re Violations Noted in Insp Repts 50-373/89-15 & 50-374/89-15.Corrective actions:post-order for Assembly Revised to Provide Specific Guidance on Use of Siren & Loudspeaker on Mobile Vehicles During Assemblies ML19327A7491989-10-0202 October 1989 Forwards Rev 2 to Combined Units 1 & 2 Inservice Testing Program for Pumps & Valves. Implementation of Program Will Require Procedure Revs Expected to Be Completed by 900228 ML19325D3271989-10-0202 October 1989 Forwards Rept Re Findings & Conclusions of Investigation Re 890826 Scram ML20248D0881989-09-21021 September 1989 Forwards Rev 56 to QA Program Topical Rept CE-1-A ML20247Q6431989-09-21021 September 1989 Documents Relaxation of Commitment Re Disassembling & Insp of Sor Switches ML19327A7681989-09-18018 September 1989 Forwards Response to Allegations Re Potential Employment Discrimination.Encl Withheld (Ref 10CFR2.790(a)(7)) 1990-09-07
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.,, . Commonwealth Edison C One First N:tionti Plaza, Chicrgo, lihnos G
- Address RIply to: Post Office Box 767 Chicago, Illinois 60690 January 7, 1986 Mr. James G. Keppler Regional Administrator U.S. Nuclear Regulatory Cotanission Region III 799 Roosevelt Road Glen Ellyn, IL 60137
Subject:
LaSalle Cetnty Station Units 1 and 2 Response in Inspection Report Nos.
50-373/85-026 and 50-374/85-027 NRC Docket Mos. 50-373 and 50-374 Reference (a): C. J. Paperiello letter to Cordell Reed dated December 6, 1985.
Dear Mr. Keppler:
This letter is in response to the inspection conducted by Mr. Z.
Falevits on August 12-14, 26-28, and September 3, 1985, of activities at LaSalle County Station. Reference (a) indicated that certain activities appeared to be in noncompliance with NRC requirements. The Cotunonwealth Edison Company's response to the Notice of Violation is provided in Attachment A. Certain other activities appeared to be deviations from previous commitments made to the Nuclear Regulatory Conunission. The Commonwealth Edison Company's response to the Notice of Deviation is provided in Attachment B.
Commonwealth Edison disagrees with the basis for the Notice of Violation on items numbered IR 373/85-027-02 and IR 373/85-026-04; 374/85-027-04. We request you review your conclusions in light of the information provided in this report.
If you have any further questions regarding this matter, please direct them to this office.
Very t y yours, i .
I D. L. Farrar Director of Nuclear Licensing la i Attachment cc: NRC Resident Inspector - LSCS 1087K 8701120231 860107 PDR ll G
ADOCK 05000373 PDR ..
JAN 8W lf S 4 2'0l
y ATTACHMENT A ITEM OF NONCOMPLIANCE (373/85-026-01)
Technical Specification 3.7.7 (Area Temperature Monitoring) states that "The temperature of each area of Unit 1 and Unit 2 shown in Table 3.7.7-1 shall be maintained within the limits indicated in Table 3.7.7-1".
Action item for 3.7.7.a requires that with one or more areas exceeding the temperature limit (s) shown in Table 3.7.7-1 for more than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, the licensee shall prepare and submit a Special Report to the Commission within the next 30 days and including an analysis to demonstrate the continued operability of the affected equipment.
Contrary to the above, the temperature limits of Table 3.7.7-1 were exceeded in the Unit 1 drywell during numerous and extended periods during 1984 and 1985 and a Special Report for these events were not submitted in a timely manner to the Commission to demonstrate the continued operability of the affected equipment.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED This violation occurred due to a misunderstanding of the reporting requirements committed to in the December 22, 1983 letter for the first fuel cycle. As soon as the misunderstanding became apparent, a special report was forwarded (DVR 1-1-85-166) to document all temperature excursions which occurred during the period January 1984 to August 1985.
The significance of this occurrence was discussed with those personnel involved with gathering and transmitting drywell temperature data to ensure that they were aware that all temperatures above 150*F in the vicinity of safety related electrical equipment were reportable occurrences.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER NONCOMPLIANCE To prevent any further misunderstanding of reporting requirements, a formal, permanent station procedure (LTP-300-17) has been written to clearly define data gathering, handling, and reporting requirements. This procedure is approved for use and will be used for routine monitoring of drywell temperatures.
DATE OF FULL COMPLIANCE Full compliance has been achieved.
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ITEM OF WONCOMPLIANCE (374/85-027-02) 10 CFR 50, Appendix B, Criterion XIV, as implemented by
, Conunonwealth Edison company Quality Assurance Manual, Nuclear Generating I
Stations, Section 14, requires that measures be established for indicating the operating status of structures, systems, and components, such as by tagging.
4 Contrary to the above, on August 12 and 28, 1985, operator yellow i caution tags attached in September 1984 to the control room containment j monitoring recorders 2TR-CM037 and 2TR-CM038 indicated that the recorder
- alarms were set at 150*F whereas calibration records indicated that these
- alarms had been set at 140*F and 141*F respectively since January 26, 1984.
t l CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED
, A thorough review of calibration records on the above equipment j does not substantiate this violation. The initial calibration of the drywell high temperature alarms (LIS-CM-204) was completed on 31 January 1982 with the alarms set at 140*F and 141*F.
On March 13, 1984, Onsite Review 84-22 was initiated to approve raising the alarm set points to 150*F if necessary (Unit 2 had not yet i entered the heat up phase of start up testing). The basis for.this Onsite l Review was Unit 1 experience which nad demonstrated that the temperature i
sensors are located in a locally hot area of the drywell and would exceed o ~their alarm points well before any high temperature limits were exceeded.
l The Onsite Review was approved on March 22, 1984.
l In September of 1984 Unit 2 had proceeded through startup testing to full power. When the unit reached full power, temperature in the vicinity of these sensors was found to be 135'F to 145'F, causing the alarms to be annunciated at least'50% of the time. In order to allow the alans to
! annunciate only when temperatures higher than normal were encountered, the
- alarms were raised to 150*F, in accordance with Onsite Review 84-22, under l Nuclear Work Requests as L35938 and L35939.
r During the inspection period of August 12 and 28, 1985, instrument calibration records indicate that the recorder alarm set points were 149'F
- and 148.8'F. The Commonwealth Edison individual assisting the inspector was apparently in error when he stated that the current setpoints were 140*F and 141*F.
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The calibration procedure indicates that the alarms were calibrated on October 15, 1985 (18 month calibration frequency). The calibration proce-dure indicates that the alarm set points were "found" at 149'F and 148.8*F and "left" at 138.9'F and 140.5*F. When (in August) the caution cards were found by the inspector, they were properly placed to indicate that the alarms were set higher than their calibration procedure specified in accordance with LaSalle Onsite Review 84-22.
Commonwealth Edison requests that this violation be reevaluated in light of the above information.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER NONCOMPLIANCE None required.
DATE OF FULL COMPLIANCE Not required.
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ITEN OF NONCOMPLIANC5 (373/85-026-03) 10 CFR 50, Appendix B, Criterion V, as implemented by Commonwealth Edison Company (CBCo) Quality Assurance Manual, Nuclear Generating Station, Section 5, requires that activities affecting quality be performed in accordance with documented instructions and procedures of a type appropriate to the circumstances.
Contrary to the above, the following examples of failure to follow
. procedures or lack of documented procedures were identified:
- a. Ceco procedure LLp 84-21: (1) Did not contain a specific time table for monitoring drywell temperatures, (2) The " checking" and
" reviewer" signatures were missing from the available drywell temperature monitoring data, (3) The drywell temperature monitoring data was submitted to S&L in a noncontrolled manner contrary to Ceco Quality procedure Q.p. No. 6-1 titled " Distribution of Design Documents," (4) Acceptance criteria for Equipment Qualification (EQ) threshold temperatures used to assure component qualified life was erroneous in that ambient rather than housing temperatures were used, and (5) Attachments A and D lacked documented evidence of site engineering review as required by the QA program, Section 6.
- b. Documented procedures were not available to address corrective actions to be taken by power plant operational personnel when temperatures exceed the TS 3.7.7 limits.
- c. A documented survelliance procedure requiring inspections and surveillance of piping or equipment insulation and other potential sources of increased sensible heat load, prior to closure of the drywell and return to power was not available.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED The immediate corrective action, as listed below were initiated and performed until both units were shutdown. A review of temperature data taken at the station was performed with off-site engineering to verify that all required data had been transmitted.
During an exit meeting on September 3, 1985, the licensee presented a temporary temperature monitoring program. The program included (1) Weekly monitoring of all Unit 1 drywell permanent and temporary thermocouples.
(2) Daily monitoring on Unit 2 of permanent and temporary thermocouples.
(3) All data collected to be transmitted to S&L through SNED for review and evaluation of qualified life of components.
c (4) Formalization of the surveillance program to include procedures addressing: frequency of data collection; action required upon loss of a thermocouple; requirements of site review of data; method of transmittal of data to SNED and S&L; time limit for data evaluation; interface with EQ program; calibration requirements; inspection of drywell thermocouples; and other applicable requirements.
The licensee agreed to contact Region III prior to the next Unit 1 and Unit 2 shutdown and drywell entry to allow for a visual inspection of electrical components and cables by the inspector.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER NONCOMPLIANCE
- a. A permanent station procedure LTP 300-17 has beer written and approved to govern data taking, handling, and temp 0rature limits.
- 1) Routine performance of the procedure is scheduled as part of the station general surveillance program. The procedure includes guidelines for accelerated data gathering after startup and when higher than normal temperatures are encountered.
- 2) Acceptance criteria for temperature data in LTP 300-12 are based upon Technical Specification 3.7.7 and 3.6.1.7 and Environmental Qualification (E.Q.) limits as specified by off-site engineering (SNED). The acceptance criteria were reviewed and approved as part of the permanent procedure. The procedure incudos a mechanism for review and approval of changes to the acceptance criteria.
- 3) The procedure includes a mechanism for formal transmittal of temperature data to off-site engineering (SNgD).
- 4) Procedure LLP 84-21 has been allowed to expire. All data gathering is covered under procedure LIP 300-17.
- 5) Data taken using LTP 300-17 will be reviewed and approved as part of the general station survelliance program.
- b. LTP 300-17 specifically states the actions required by Technical Specification 3.7.7 in the event a temperature in excess of 150*F or 180*F is encountered. In addition the procedure specifies required notifications and engineering evaluations to be performed if E.Q.
limits are exceeded.
- c. The drywell close out procedure (LOP-DW-01) has been changed to require the Technical Staff Supervisor to sign-off that an insulation inspection either has been performed or is not required as appropriate.
DATE OF FULL COMPLTANCE Full Compliance has been achieved.
r ITEM OF WONCOMPLIANCE (373/85-026-04; 374/85-027-04) 10 CFR 50, Appendix B, Celterion IVI, as implemented by Commonwealth Edison Company Quality Assurance Manual, Nuclear Generating Stations, Section 16, requires that measures be established to assure that conditions adverse to quality such as deviations, nonconformances . . . are promptly identified and corrected.
Contrary to the above, the licensee's Station Nuclear Engineering Department (SNED) failed to respond in a prompt and responsible manner regarding their evaluation and recommendations for containment monitoring (temperature) alarm set points as recalculated and supplied by S&L. S&L submitted this data through the LaSalle plant management for SNED review and evaluation in December 1984 for Unit 1 and January 1985 for Unit 2.
Requested response dates were designated as January and February 1985; however, as of August 14, 1985, no effective action had been taken by SNED engineers to disposition this issue.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED In order to clarify the above Item of Noncompliance, we believe the second sentence of the second paragraph should read, "LaSalle plant personnel submitted modifications via Action Item Records (AIRS) for SNED review and evaluation in December 1984 for Unit 1 and January 1985 for Unit 2".
Action Item Record (AIR) dated December 3, 1984 requested SNED assistance for a modification revising the setpoints of 2 points on recorders 1TR-CM037 and ITR-CM038. This Unit 1 AIR had a requested completion date of January 2, 1985. Another AIR dated January 28, 1985 requested SNED assistance for modification revising the setpoints of 2 points of recorders 2TR-CM037 and 2TR-CN038. This Unit 2 AIR had a requested completion date of February 18, 1985.
The Unit i drywell temperature data evaluated by S&L was dated 1/2/84, 1/9/84, 1/13/84, 2/1/84, 3/22/84 and 3/27/84. The S&L analysis and recommendation was contained in a September 28, 1984 letter to the LaSalle project engineer. The S&L recommendation to SNED was to establish new alarm setpoints for recorder ITR-CN037 at 155'F and for recorder 1TR-CM038 at 145*F. SNED evaluated the recommended changes and determined that the present 140*F alarm setpoints were conservative, as compared to raising them to 145*F and 155'F and did not approve raising the Unit 1 CM alarm setpoints.
Temperature dets was being recorded for the Unit 2 drywell temperature profile with the first data taken December 26, 1984. Additional temperature data was collected for Unit 2 on January 10, 1985 and January 24, 1985.
r S&L evaluated the Unit 2 temperature data and based on their letter dated March 25, 1985, recommended the Unit 2 CM alarm setpoints be revised to 1460F and 1340F, At this time, Unit 2 had already begun an outage Which started February 27, 1985. Since the unit was in cold shutdown, SNED did not consider processing of the setpoint changes to be urgent. In addition, it was SNED's opinion that no CM alarm setpoint changes should be implemented during this time period, because of the drywell work and its effect on the resulting drywell temperature profile. The readings on which these setpoints are based would likely be affected by changes in air distribution, condition of pipe insulation and the addition of equipment.
In addition, any future changes made in the drywell would require new sets of temperature data for comparison and validation of the recommended setpoints. I Following the conclusion of the Unit 2 outage on July 21, 1985, new temperature readings were taken on 8/5/85, 8/6/85, 8/14/85, 8/23/85 and 8/28/85. Additional temperature readings were taken in the Unit 1 drywell, approximately at the same time, 8/8/85, 8/23/85 and 8/28/85, updating each unit's equipment qualification calculations for an SRV equipment area ambient temperature of 1700F, S&L's recommendation was not to revise the Unit 1 or Unit 2 CM setpoints, but to leave them unchanged at 1400F. This recommendation was addressed in S&L's October 11, 1985 letter to SNED. SNED addressed this S&L evaluation in a November 6, 1985 letter to LaSalle Station, recommending the CM alarm setpoints for both Units 1 & 2 remain unchanged at 1400F. Additionally, SNED requested that AIR's and modifications on this topic be closed.
The Unit 1 modification was cancelled November 11, 1985 and AIR was cancelled December 5,1985. The Unit 2 modification was cancelled November 11, 1985 and AIR was cancelled December 5, 1985.
CORRECTIVE ACTION TO AVOID FURTHER NONCOMPLIANCE Based on the above findings we do not feel that this item is a I
violation. It is our conclusion that SNED utilized conservative engineering judgment and the extended unit outage time to address fully the CM alarm setpoint issue, concluding and recommending to LaSalle Station that no changes were necessary, and that the associated modifications and AIR's should be cancelled.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED l
1 Full compliance has been achieved.
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. o ATTACHMENT B DgVIATION (373/85-026-05)
(a) As a result of the inspection conducted August 12-14, 26-28, and September 3, 1985, the following deviation in four parts to NRC commitments contained in your LaSalle Unit 1 letter dated December 22, 1983, were identified:
- 1. Commitment - Page 11. Paragraph 5. " Augmented temperature monitoring will be performed...to monitor actual temperatures to assure safety-related equipment does not degrade beyond pre-defined thresholds..."
Attachment A of LAP-820-7 for procedure LLP 84-25 dated July 9, 1984, states that the reason for the special Unit 1 drywell temperature monitoring program procedure is to " provide a time table for collecting data regarding temperatures in the Unit 1 drywell thru first refuel."
Contrary to the above, monitoring of drywell temperatures using the temporary thermocouples stopped in December 1984.
- 2. Commitment - Page 10, Paragraph 3, "A temperature monitoring program has been defined to evaluate the results from the short term fixes."
Contrary to the above, adequate documented evaluation of the results was not available for review.
- 3. Commitment - Page 14. Paragraph 1.c., "Should the temperature in an area where safety related equipment is located exceed the limiting temperature on which the 18-month life is based for that equipment, for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, an analysis for continued operation will be completed within seven days or the unit will be temporarily shut down for a visual inspection and correction of the anomalous condition (s)".
Contrary to the above, such an analysis was not available for review for various periods of time when the limiting terperature was exceeded for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
- 4. Commitment - Annex A, Technical Specification, "The temperature monitoring program will verify that these temperature limits are correlated to Control Room CM Monitors (4).
Contrary to the above, the analysis that was provided to correlate local temperatures in the drywell to alarm setpoints on control room containment monitoring (CM) recorders was found erroneous.
n' CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED
- 1. Weekly monitoring of Unit 1 Drywell temperatures was initiated inunediately. The purpose of the augmented drywell temperature monitoring program stated in the 22 December 1983 letter, was four fold. When the augmented temperature monitoring program (LLP-84-25) was stopped on December 1984, Commonwealth Edison believed that all four purposes had been accomplished and that daily monitoring of six temperatures on routine surveillances was adequate to assure continued equipment operability.
In retrospect, continued performance of this program would have provided better assurance that the drywell temperature was adequately monitored.
The inspection made in August 1985 revealed that a local " hot-spot" had developed in the Unit 1 drywell which was not discovered by routine monitoring. Had the augmented program been performed, this local high temperature would have been discovered earlier.
Environmental Qualification (EQ) calculations performed based upon the temperatures (December 1984 to September 1985) encountered in the Unit 1 drywell have demonstrated that no abnormal degradation of safety related components has occurred. These calculations have been substantiated by physical inspections performed during the current refueling outage. The affects of the temperature problem have been considered in calculating the remaining qualified-life of these components.
- 2. A formal written evaluation of the results of "short term fixes" as described in the December 22, 1983 war not performed. The intent of this statement in the letter was to use the temperature data itself as an evaluation.
The temperatures that were recorded were compared against previous data and regulatory limits to determine if changes in air flow were required. At each available unit shutdown, adjustments were made to air flows in an attempt to shift cooling from areas with larger cooling margin to those areas needing more margin. Upon subsequent return to power, the temperature data colected would clearly show the success or failure of the changes.
4 While not all changes made were successful, this iterative approach was as a whole extremely successful. A review of the temperature data clearly shows the affect of these changes and a general leveling of the margin to tempersture limits.
- 3. This alleged deviation resulted from two factors:
(1) The inadequate specification of temperature limits in the December 22, 1983 letter in that the limiting temperature for the SRV solenoids was not specified as a metal temperature.
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(2) The uncertain status of the SRV solenoids as to their NUREG-0588 category. The limit specified in the December 22 letter was based upon Category I criteria.
Immediate corrective action for (1) was to contact off site engineering to insure that no confusion existed as to the source of data used to calculate current Environmental Qualification lifetimes. No confusion existed and calculated lifetimes were based upon proper data. No component was at any time exposed to conditions which would have caused the component to exceed its qualified life prior to the first refueling outage. As documented in Inspection Report 50-373/85026, 50-374/85027 the SRV solenoids have in excess of 13 years qualified life remaining at a housing
' temperature of 187'F. During 1984, clarification was received from off-site engineering (SNED) which classified the SRV solenoids as NUREG 0588 Category II.
- 4. The intent of this commitment was to generate on overall drywell temperature profile. This profile would then serve as a basis for selecting alarm set points for the four. safety-related drywell temperature sensors such that no safety related component could exceed a temperature limit without an alarm being received.
From the experience gained from multiple data taking and evaluation of the drywell temperatures it is apparent that the generation of an overall temperature profile is not feasible. The temperature profile changes after every outage due to changes in air distribution condition of pipe insulation and the addition of equipment. These changes are done every outage to " fine tune" the air flow distribution to achieve the maximum usage of available capacity. The station will continue to perform the temperature monitoring program as defined in LTP 300-17.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER NONCOMPLIANCE A new procedure (LTP-300-17) is currently in use. This procedure removes all judgement and interpretation concerning when and how to monitor drywell temperature. This procedure monitors and records data from all
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permanent and temporary sensors. The procedure is scheduled to be performed i weekly by the station general surveillance program. In addition, multipoint recorders have been rented and installed to facillitate monitoring of all temporary sensors. The utilization of this procedure addresses all four parts of the deviation.
j DATE OF FULL COMPLTANCE l Full compliance of all four parts has been achieved.
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