|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML17355A4601999-10-26026 October 1999 Forwards Revised Epips,Including Revs to 0-EPIP-1102, 0-EPIP-1212,0-EPIP-20110,0-EPIP-20111,0-EPIP-20132, 0-EPIP-20133 & 0-EPIP-20201,per 10CFR50.54(q) & 10CFR50, App E.Epip 0-EPIP-20107,has Been Deleted ML17355A4301999-10-0808 October 1999 Forwards Rev 16 of Updated Fsar.Info Accurately Reflects Plant Changes Made Since Previous Submittal.Rev Incorporates Changes Completed Between 971015 & 990408.Summary of Accuracy Review Changes & Instructions,Included L-99-208, Forwards Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408. Summary of PORV Actuations & Results of Plants SG Tube Insp,Which Occurred During That Time Included1999-10-0404 October 1999 Forwards Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408. Summary of PORV Actuations & Results of Plants SG Tube Insp,Which Occurred During That Time Included ML17355A4291999-10-0404 October 1999 Forwards Response to NRC Telcon Questions Re License Amend Request Dtd 990727,proposing Amend on one-time Basis to Modify TS 3.8.1.1 & TS 3.4.3 & 3.5.2 to Extend Allowed Outage Time for EDG from 72 H to 7 Days ML17355A4461999-10-0404 October 1999 Notifies NRC of Change in Commitment to Perform Periodic Testing of Critical Welds & Parts on Special Lifting Devices IAW NUREG-0612.Use of Ae Technology Will Provide Same Level of Testing Quality as Did NDE Methods Noted in ANSI Std ML20212M1601999-09-28028 September 1999 Refers to 990908 Engineering Meeting Conducted at NRC Region II to Discuss Engineering Issues at Lucie & Turkey Point Facilities.List of Attendees & Copy of Presentation Handout Encl ML17355A4251999-09-22022 September 1999 Forwards NRC Form 536 in Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams, Issued 990820 ML17355A4111999-09-0909 September 1999 Informs That Thermo-Lag Upgrades for Fire Zones 47,54,113, 114,115,116,118,119,120 & 143 Completed on 990726,per GL 92-08 ML17355A4131999-09-0707 September 1999 Forwards Revised Relief Request 20 Re Requirement to Perform Exams as Required by IWL-2524 & IWL-2525,Table IWL-2500-1 for Exempt Tendon Insp,Per Recent Discussions with NRC ML17355A4141999-09-0202 September 1999 Documents That Util Has No Concerns or Challenges Related to site-specific Written Exam Administered at Plant on 990830 ML17355A4041999-08-23023 August 1999 Forwards Info to Support Assessment of Potential Risks Associated with Proposed Civil Aircraft Operations at Former Homestead Air Force Base to FP&L Turkey Point Nuclear Facility Units 3 & 4 ML17355A4061999-08-23023 August 1999 Forwards Semiannual FFD Performance Rept for Period of Jan- June 1999,for Turkey Point Units 3 & 4.List of Events Reported & Summary of Mgt Actions Taken,Included ML17355A4071999-08-23023 August 1999 Informs That FPL Has Completed Review of Info Listed in Reactor Vessel Integrity Database,Version 2 & Found Listed Discrepancies,Re Closure of GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity. ML17355A4001999-08-20020 August 1999 Informs That on 990722,util Determined Blind Specimen Submitted to Smithkline Beecham Clinical Labs on 990721,was Reported Back with Unsatisfactory Results.Attachment 1 Is Summary of Investigation of Unsatisfactory Performance ML17355A3941999-07-27027 July 1999 Submits Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for FY00 & FY01 ML17355A3871999-07-16016 July 1999 Provides Supplement to FP&L Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants ML17355A3851999-07-14014 July 1999 Informs That Pages Missing from 1998 Annual Radiological Environ Operating Rept, Contain Info Unrelated to ODCM- Specified Sampling & Were Not Included as Part of Rept ML17355A3711999-07-0606 July 1999 Forwards Revised EPIPs 0-EPIP-20201, Maintaining Emergency Preparedness - Radiological Emergency Plan Training & 0-EPIP-20126, Off-Site Dose Calculations. with Summary of Changes ML17355A3591999-06-30030 June 1999 Forwards Turkey Point,Unit 4 ISI Rept. Listed Repts Are Encl.No Eddy Current Exams Scheduled for Unit 4 Steam Generators ML17355A3661999-06-30030 June 1999 Forwards Florida Power & Light Topical QA Rept, Dtd June 1999.Encl I Includes Summary of Changes Made to Topical QA Rept Since 1998 ML17355A3571999-06-28028 June 1999 Informs That Util Voluntarily Reporting Facility Readiness as Outlined in Suppl 1 to GL 98-01.Encl Is Y2K Readiness Disclosure for Units 3 & 4,reporting Status of Facility Y2K Readiness ML17355A3521999-06-18018 June 1999 Forwards Response to NRC 990415 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves. ML17355A3491999-06-0404 June 1999 Forwards Summary of Corrective Actions Implemented by FPL Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions. ML17355A3441999-05-27027 May 1999 Modifies FPLs Consent to Confirmatory Order to Reflect Resolution of Four Issues Identified as Pending in L-99-031 ML17355A3451999-05-24024 May 1999 Requests Waiver of 520 Hours (13 Wks) Required Parallel Watchstanding in Control Room Prior to License Application Submittal for W Conley ML17355A2921999-04-22022 April 1999 Forwards Rev 35 to Turkey Point EP & Revised EPIP 0-EPIP-20101, Duties of EC, Per Requirements of 10CFR50, App E & 10CFR50.54(q).Summary of Changes,Encl.Implementation Date for Both Documents Was 990330 ML20205M0431999-04-13013 April 1999 Eighth Partial Response to FOIA Request for Records.App Q & R Records Encl & Being Made Available in PDR ML17355A2891999-04-0909 April 1999 Forwards Relief Request 20, Exempt Tendon Insp, Requesting Relief from ASME Section XI Code,1992 Edition,Paragraph IWL-2521.1(c) Which Requires That Each Exempted Tendon Be Examined IAW IWL-2524 & IWL-2525.Approval Needed by 991001 ML17355A2861999-04-0505 April 1999 Forwards COLR for Turkey Point Unit 4,Cycle 18,IAW TS 6.9.1.7 ML17336A0681999-04-0101 April 1999 Expresses Support for FP&L Request for Waiver of Applicable Review Fees Upon FP&L Submittal of an Application for License Renewal for Turkey Point Units 3 & 4 ML17355A2751999-03-25025 March 1999 Informs NRC & Staff of Fp&Ls Plans to Submit License Renewal Application for Turkey Point Units 3 & 4 by End of Dec 2000 ML17355A2641999-03-19019 March 1999 Requests Changes to FPL Official Service List for Turkey Point,Units 3 & 4.Add s Franzone & Remove G Hollinger from All Correspondence ML17355A2651999-03-19019 March 1999 Forwards Annual Radioactive Effluent Release Rept for Jan-Dec 1998 & Rev 7 to ODCM for Gaseous & Liquid Effluents from Turkey Point,Units 3 & 4. ML17355A2621999-03-16016 March 1999 Forwards Special Rept as Result of Turkey Point Unit 3 End-of-Cycle 16 ISI of SG Tubes.Rept Summarizes Results of SG Tube ISI ML17355A2631999-03-12012 March 1999 Forwards FPL Decommissioning Fund Status Repts for St Lucie, Units 1 & 2 & Turkey Point,Units 3 & 4.Rept for St Lucie, Unit 2 Provides Status of Decommissioning Funds for All Three Owners of That Unit ML20204C6991999-03-10010 March 1999 Requests Amend to Turkey Point PSP to Modify Requirement to Post Security Officers to Provide Continuous Observation of Entire PA Perimeter in Event of Security Computer Failure. Change to Security Force Staffing Level Also Requested ML17355A2451999-03-0909 March 1999 Submits Info on FPL Current Levels of Nuclear Property Insurance,Per 10CFR50.54(w)(3) ML17355A2501999-03-0808 March 1999 Informs That Licensee Reviewed NRC 990228 Ltr Issuing Exemption Requested Re Fire Rating of Raceway Fire Barriers in Open Turbine Bldg.Tabulated Summary of Util Comments & Marked Copy of NRC Ltr & SER Encl ML17355A2441999-03-0101 March 1999 Provides Update to Util Written Notices,Dtd 961120 & 970627 of Claim Involving Alleged Bodily Injury Arising Out of or in Connection with Use of Radioactive Matl at Units 3 & 4 ML17355A2431999-02-25025 February 1999 Informs That FPL Does Not Have Any Candidates from Turkey Point Scheduled to Participate in 990407,Generic Fundamentals Examination (GFE) ML17355A2361999-02-18018 February 1999 Forwards Tabulation of 1998 Occupational Exposure Data for Turkey Point,Units 3 & 4,per TS 6.9.1.2.a.Reactor Coolant Specific Activity Limits of 100/E-bar Mci Per Gram of Gross Radioactivity Were Not Exceeded During 1998 ML17355A2341999-02-18018 February 1999 Provides Response to RAI Re GL 97-01, Degradation of Crdm/ CEDM Nozzle & Other Vessel Closure Head Penetrations. ML17355A2301999-02-18018 February 1999 Forwards Semiannual Fitness for Duty Performance Data for Period of 980701-981231 for Turkey Point Units 3 & 4 L-99-042, Forwards Rev 13 to Turkey Point Physical Security Plan,Per 10CFR50.54(p).Util Determined That Rev Does Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR2.790(a)(3)1999-02-18018 February 1999 Forwards Rev 13 to Turkey Point Physical Security Plan,Per 10CFR50.54(p).Util Determined That Rev Does Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR2.790(a)(3) ML17355A2231999-02-0808 February 1999 Informs That Util Will Comply with Commitment with Respect to Units 3 & 4,in Response to Ja Zwolinski 990129 Ltr.Util Also Agrees to Incorporate Commitment Into Confirmatory Order Modifying License Effective Immediately Upon Issuance ML17355A2031999-01-29029 January 1999 Forwards Rev 3 to Turkey Point Nuclear Plant Recovery Plan. Rev Does Not Decrease Effectiveness of Plan ML17355A2171999-01-20020 January 1999 Forwards Listed ISI Repts for Turkey Point Unit 3,in Accordance with Provisions of ASME Code,Section XI ML17354B2241999-01-0606 January 1999 Forwards Annual 10CFR50.46 Rept Re Changes To,Or Errors Discovered in ECCS Evaluation Models,Or in Application of Such Models That Effect Peak Clad Temp Calculation ML17354B2081998-12-15015 December 1998 Informs That Fpl,In Cooperation with State of Fl & County Emergency Response Agencies,Will Conduct Exercise of Turkey Point Radiological Emergency Plan on 990210.Scenario Package Forwarded to Emergency Preparedness Section Chief,Region II ML17354B2091998-12-15015 December 1998 Forwards Price Anderson Guarantees Annual Financial Rept,Per 10CFR140.21.Exhibit 1 Submitted to Satisfy Annual Financial Reporting Requirement of 10CFR50.71(b) 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17355A4601999-10-26026 October 1999 Forwards Revised Epips,Including Revs to 0-EPIP-1102, 0-EPIP-1212,0-EPIP-20110,0-EPIP-20111,0-EPIP-20132, 0-EPIP-20133 & 0-EPIP-20201,per 10CFR50.54(q) & 10CFR50, App E.Epip 0-EPIP-20107,has Been Deleted ML17355A4301999-10-0808 October 1999 Forwards Rev 16 of Updated Fsar.Info Accurately Reflects Plant Changes Made Since Previous Submittal.Rev Incorporates Changes Completed Between 971015 & 990408.Summary of Accuracy Review Changes & Instructions,Included L-99-208, Forwards Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408. Summary of PORV Actuations & Results of Plants SG Tube Insp,Which Occurred During That Time Included1999-10-0404 October 1999 Forwards Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408. Summary of PORV Actuations & Results of Plants SG Tube Insp,Which Occurred During That Time Included ML17355A4291999-10-0404 October 1999 Forwards Response to NRC Telcon Questions Re License Amend Request Dtd 990727,proposing Amend on one-time Basis to Modify TS 3.8.1.1 & TS 3.4.3 & 3.5.2 to Extend Allowed Outage Time for EDG from 72 H to 7 Days ML17355A4461999-10-0404 October 1999 Notifies NRC of Change in Commitment to Perform Periodic Testing of Critical Welds & Parts on Special Lifting Devices IAW NUREG-0612.Use of Ae Technology Will Provide Same Level of Testing Quality as Did NDE Methods Noted in ANSI Std ML17355A4251999-09-22022 September 1999 Forwards NRC Form 536 in Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams, Issued 990820 ML17355A4111999-09-0909 September 1999 Informs That Thermo-Lag Upgrades for Fire Zones 47,54,113, 114,115,116,118,119,120 & 143 Completed on 990726,per GL 92-08 ML17355A4131999-09-0707 September 1999 Forwards Revised Relief Request 20 Re Requirement to Perform Exams as Required by IWL-2524 & IWL-2525,Table IWL-2500-1 for Exempt Tendon Insp,Per Recent Discussions with NRC ML17355A4141999-09-0202 September 1999 Documents That Util Has No Concerns or Challenges Related to site-specific Written Exam Administered at Plant on 990830 ML17355A4041999-08-23023 August 1999 Forwards Info to Support Assessment of Potential Risks Associated with Proposed Civil Aircraft Operations at Former Homestead Air Force Base to FP&L Turkey Point Nuclear Facility Units 3 & 4 ML17355A4061999-08-23023 August 1999 Forwards Semiannual FFD Performance Rept for Period of Jan- June 1999,for Turkey Point Units 3 & 4.List of Events Reported & Summary of Mgt Actions Taken,Included ML17355A4071999-08-23023 August 1999 Informs That FPL Has Completed Review of Info Listed in Reactor Vessel Integrity Database,Version 2 & Found Listed Discrepancies,Re Closure of GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity. ML17355A4001999-08-20020 August 1999 Informs That on 990722,util Determined Blind Specimen Submitted to Smithkline Beecham Clinical Labs on 990721,was Reported Back with Unsatisfactory Results.Attachment 1 Is Summary of Investigation of Unsatisfactory Performance ML17355A3941999-07-27027 July 1999 Submits Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for FY00 & FY01 ML17355A3871999-07-16016 July 1999 Provides Supplement to FP&L Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants ML17355A3851999-07-14014 July 1999 Informs That Pages Missing from 1998 Annual Radiological Environ Operating Rept, Contain Info Unrelated to ODCM- Specified Sampling & Were Not Included as Part of Rept ML17355A3711999-07-0606 July 1999 Forwards Revised EPIPs 0-EPIP-20201, Maintaining Emergency Preparedness - Radiological Emergency Plan Training & 0-EPIP-20126, Off-Site Dose Calculations. with Summary of Changes ML17355A3591999-06-30030 June 1999 Forwards Turkey Point,Unit 4 ISI Rept. Listed Repts Are Encl.No Eddy Current Exams Scheduled for Unit 4 Steam Generators ML17355A3661999-06-30030 June 1999 Forwards Florida Power & Light Topical QA Rept, Dtd June 1999.Encl I Includes Summary of Changes Made to Topical QA Rept Since 1998 ML17355A3571999-06-28028 June 1999 Informs That Util Voluntarily Reporting Facility Readiness as Outlined in Suppl 1 to GL 98-01.Encl Is Y2K Readiness Disclosure for Units 3 & 4,reporting Status of Facility Y2K Readiness ML17355A3521999-06-18018 June 1999 Forwards Response to NRC 990415 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves. ML17355A3491999-06-0404 June 1999 Forwards Summary of Corrective Actions Implemented by FPL Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions. ML17355A3441999-05-27027 May 1999 Modifies FPLs Consent to Confirmatory Order to Reflect Resolution of Four Issues Identified as Pending in L-99-031 ML17355A3451999-05-24024 May 1999 Requests Waiver of 520 Hours (13 Wks) Required Parallel Watchstanding in Control Room Prior to License Application Submittal for W Conley ML17355A2921999-04-22022 April 1999 Forwards Rev 35 to Turkey Point EP & Revised EPIP 0-EPIP-20101, Duties of EC, Per Requirements of 10CFR50, App E & 10CFR50.54(q).Summary of Changes,Encl.Implementation Date for Both Documents Was 990330 ML17355A2891999-04-0909 April 1999 Forwards Relief Request 20, Exempt Tendon Insp, Requesting Relief from ASME Section XI Code,1992 Edition,Paragraph IWL-2521.1(c) Which Requires That Each Exempted Tendon Be Examined IAW IWL-2524 & IWL-2525.Approval Needed by 991001 ML17355A2861999-04-0505 April 1999 Forwards COLR for Turkey Point Unit 4,Cycle 18,IAW TS 6.9.1.7 ML17336A0681999-04-0101 April 1999 Expresses Support for FP&L Request for Waiver of Applicable Review Fees Upon FP&L Submittal of an Application for License Renewal for Turkey Point Units 3 & 4 ML17355A2751999-03-25025 March 1999 Informs NRC & Staff of Fp&Ls Plans to Submit License Renewal Application for Turkey Point Units 3 & 4 by End of Dec 2000 ML17355A2641999-03-19019 March 1999 Requests Changes to FPL Official Service List for Turkey Point,Units 3 & 4.Add s Franzone & Remove G Hollinger from All Correspondence ML17355A2651999-03-19019 March 1999 Forwards Annual Radioactive Effluent Release Rept for Jan-Dec 1998 & Rev 7 to ODCM for Gaseous & Liquid Effluents from Turkey Point,Units 3 & 4. ML17355A2621999-03-16016 March 1999 Forwards Special Rept as Result of Turkey Point Unit 3 End-of-Cycle 16 ISI of SG Tubes.Rept Summarizes Results of SG Tube ISI ML17355A2631999-03-12012 March 1999 Forwards FPL Decommissioning Fund Status Repts for St Lucie, Units 1 & 2 & Turkey Point,Units 3 & 4.Rept for St Lucie, Unit 2 Provides Status of Decommissioning Funds for All Three Owners of That Unit ML20204C6991999-03-10010 March 1999 Requests Amend to Turkey Point PSP to Modify Requirement to Post Security Officers to Provide Continuous Observation of Entire PA Perimeter in Event of Security Computer Failure. Change to Security Force Staffing Level Also Requested ML17355A2451999-03-0909 March 1999 Submits Info on FPL Current Levels of Nuclear Property Insurance,Per 10CFR50.54(w)(3) ML17355A2501999-03-0808 March 1999 Informs That Licensee Reviewed NRC 990228 Ltr Issuing Exemption Requested Re Fire Rating of Raceway Fire Barriers in Open Turbine Bldg.Tabulated Summary of Util Comments & Marked Copy of NRC Ltr & SER Encl ML17355A2441999-03-0101 March 1999 Provides Update to Util Written Notices,Dtd 961120 & 970627 of Claim Involving Alleged Bodily Injury Arising Out of or in Connection with Use of Radioactive Matl at Units 3 & 4 ML17355A2431999-02-25025 February 1999 Informs That FPL Does Not Have Any Candidates from Turkey Point Scheduled to Participate in 990407,Generic Fundamentals Examination (GFE) ML17355A2301999-02-18018 February 1999 Forwards Semiannual Fitness for Duty Performance Data for Period of 980701-981231 for Turkey Point Units 3 & 4 ML17355A2341999-02-18018 February 1999 Provides Response to RAI Re GL 97-01, Degradation of Crdm/ CEDM Nozzle & Other Vessel Closure Head Penetrations. ML17355A2361999-02-18018 February 1999 Forwards Tabulation of 1998 Occupational Exposure Data for Turkey Point,Units 3 & 4,per TS 6.9.1.2.a.Reactor Coolant Specific Activity Limits of 100/E-bar Mci Per Gram of Gross Radioactivity Were Not Exceeded During 1998 L-99-042, Forwards Rev 13 to Turkey Point Physical Security Plan,Per 10CFR50.54(p).Util Determined That Rev Does Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR2.790(a)(3)1999-02-18018 February 1999 Forwards Rev 13 to Turkey Point Physical Security Plan,Per 10CFR50.54(p).Util Determined That Rev Does Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR2.790(a)(3) ML17355A2231999-02-0808 February 1999 Informs That Util Will Comply with Commitment with Respect to Units 3 & 4,in Response to Ja Zwolinski 990129 Ltr.Util Also Agrees to Incorporate Commitment Into Confirmatory Order Modifying License Effective Immediately Upon Issuance ML17355A2031999-01-29029 January 1999 Forwards Rev 3 to Turkey Point Nuclear Plant Recovery Plan. Rev Does Not Decrease Effectiveness of Plan ML17355A2171999-01-20020 January 1999 Forwards Listed ISI Repts for Turkey Point Unit 3,in Accordance with Provisions of ASME Code,Section XI ML17354B2241999-01-0606 January 1999 Forwards Annual 10CFR50.46 Rept Re Changes To,Or Errors Discovered in ECCS Evaluation Models,Or in Application of Such Models That Effect Peak Clad Temp Calculation ML17354B2091998-12-15015 December 1998 Forwards Price Anderson Guarantees Annual Financial Rept,Per 10CFR140.21.Exhibit 1 Submitted to Satisfy Annual Financial Reporting Requirement of 10CFR50.71(b) ML17354B2081998-12-15015 December 1998 Informs That Fpl,In Cooperation with State of Fl & County Emergency Response Agencies,Will Conduct Exercise of Turkey Point Radiological Emergency Plan on 990210.Scenario Package Forwarded to Emergency Preparedness Section Chief,Region II ML17354B2061998-12-0909 December 1998 Informs That Request for Exemption Specified in Section II.B.3 Will Not Be Needed Re Fire Rating of Raceway Fire Barriers in Open Turbine Bldg ML17354B1981998-11-25025 November 1998 Forwards Scope & Objective for 1999 Plant Annual Emergency Preparedness Exercise.Objectives Developed in Conjunction with State & Local Govts.Exercise Scheduled for 990210 1999-09-09
[Table view] Category:PUBLIC ENTITY/CITIZEN/ORGANIZATION/MEDIA TO NRC
MONTHYEARML20055G8151990-07-10010 July 1990 Forwards Response of Nuclear Energy Accountability Project & Tj Saporito to Florida Power & Light Motion for Reconsideration & Dismissal of Petition to Intervene ML20055G7661990-07-0707 July 1990 Requests Full & Complete 900524 ACRS Meeting Transcript Re Reactor Vessel Embrittlement,For Review.Nuclear Energy Accountability Project Considers Comments Re ACRS Meeting Transcript in Washington,Dc Unfair.W/Certificate of Svc ML20058K6871990-06-26026 June 1990 Advises That Nuclear Energy Accountability Project Lacks Sufficient Funds to Send Representative to Oral Argument Scheduled for 900710 in Bethesda,Md.Urges Appeal Board to Grant Motion to Relocate Hearing.W/Certificate of Svc ML20055D8631990-06-20020 June 1990 Advises That Firm Retained to Represent Tj Saporito & Nuclear Energy Accountability Project for Sole Purpose of Advising Organization & Saporito on Responding to Board 900615 Memorandum & Order.Certificate of Svc Encl ML20012E6711990-03-26026 March 1990 Requests That Concerns to Adopt New Set of Tech Specs for Facility Be Fully Investigated to Ensure That Public Health & Safety Not in Jeopardy.Certificate of Svc Encl.Related Correspondence ML20006C5151990-01-12012 January 1990 Statement for Permission to Represent.* Forwards JW Edleson Statement ML20006C5051990-01-0606 January 1990 Statement for Permission to Represent.* Forwards Statement from a Weinkle ML17347B5381989-12-29029 December 1989 Requests NRC Actions,Including Immediate Investigation of Recent Trips at Plant to Determine Root Cause of Events & Imposition of Escalated Civil Penalty in Trips Due to Poor Maint Practices or Incorrect Operations,Per 10CFR2.206 & 2 ML19332D9821989-11-23023 November 1989 Discusses Licensee 891121 Ltr to Board Re Author Supposedly Unjustified Further Allegations & Innuendoes of Wrongdoing, Illegality & Violations by Licensee.Licensee Proffers No Probative Evidence to Contrary.W/Certificate of Svc ML19325E9801989-11-0101 November 1989 Requests That Author Name Be Placed on Distribution List Re Schedule of Hearing in Alchemie Case.W/Certificate of Svc. Served on 891101 ML19325E0091989-10-20020 October 1989 Fax Transmission of Affidavit of J Lorion for Presssure/Temp Proceeding (Turkey Point).* Forwards Author Affidavit to Be Incorporated W/Intervenors Response to Licensee Motion for Summary Disposition of Intervenors Contentions ML20248J1381989-09-29029 September 1989 Advises That Intervenors Motion for Extension of Time & Motion for Rev to Hearing Schedule Should No Longer Be Considered by Board Due to Author Not Nominated to PSC of Florida ML20247B6531989-09-0808 September 1989 Advises That Intervenors,Ctr for Nuclear Responsibility & J Lorion Have Advised Franz,Counsel for Licensee & P Jehle,Counsel for Nrc,That Contention 3 Withdrawn.Concerns Re Critical Welds Remain Unresolved ML20247F8061989-07-0505 July 1989 FOIA Request for Documentation Re Incidents of Drug &/Or Alcohol Abuse During Past Five Yrs Amoung Employees or Contractors ML20246J3551989-07-0303 July 1989 FOIA Request for Records of NRC Regional Staff Meeting on 890329,NRC Bulletin 88-011,util Ltr L-89-79,INPO SER 25-87, NRC 890411 Meeting Re Westinghouse Owners Group Rept & Topical Repts WCAP-12277 & WCAP-12278 ML20247E6951989-06-27027 June 1989 Advises That Newly Formed Environ Conservation Organization Intends to Oppose Any Util Actions That Might Impact Negatively on Future Operability of Facility ML20247H3631989-06-26026 June 1989 Advises of Formation of Resources Conservation Organization. New Group Intends to Oppose Any Util Actions That Might Impact Negatively on Future Facility Operability.Ad Rossin Will Serve as Organization Coordinator ML20247Q7761989-05-24024 May 1989 Fowards Resolution Being Sponsored by Dade County Commissioner B Carey Which Urges Board to Hold Formal Public Hearings Requested by Ctr for Nuclear Responsibility,For Consideration.W/Certificate of Svc.Served on 890731 ML20245B3981989-05-0808 May 1989 Discusses Technical & Safety Concerns Re Flow & Pressure Drop Calculations for RWCU & Feedwater & Condensate Sample Panels at Plant ML20247H0911989-04-26026 April 1989 Requests NRC to Take Immediate Actions to Cause Imposition of Escalated Civil Penalty,Suspension of Licenses DPR-31 & DPR-41 & Order to Correct Numerous Plant Deficiencies ML17345A6511989-04-25025 April 1989 Requests Suspension of Licenses DPR-31 & DPR-41 & Imposition of Civil Penalty,Based on NRC Finding Security Guard Asleep at Post & Visitor in Vital Area W/O Access ML20245L5851989-03-22022 March 1989 Requests Enforcement Actions Resulting in Issuance of Notice of Violation W/Imposed & Escalated Civil Penalty & Immediate Suspension & Revocation of Licenses DPR-31 & DPR-41 ML20245B4081989-03-10010 March 1989 Requests Response to 881014 & 890119 & 23 Ltrs Re Technical & Safety Concerns at Plant ML20244B0011989-03-0808 March 1989 Lists Facts to Consider for Action to Fix or Close GE Reactors Once & for All ML20245L5991989-03-0606 March 1989 Ack Receipt of & Petition for Director'S Decision Under 10CFR2.206 Re Licenses DPR-31 & DPR-41.Advises of Plans,In Interest of Public Safety,To Request Resolution by Ofc of Internal Auditing of Concerns Re NRC Conduct ML20245L5481989-03-0202 March 1989 Advises of Error Contained in 2.206 Document Faxed to Ofc on 890301.L Jennings,South Dade News Leader Reporter,Spoke W/K Clark of NRC & Not O Demiranda,As Reported ML20245L5941989-03-0101 March 1989 Requests Immediate Suspension & Revocation of Licenses DPR-31 & DPR-41 ML20247H1721989-02-0707 February 1989 Requests Revocation of Licenses DPR-31 & DPR-41 & Issuance of Notice of Violation W/Imposed & Escalated Civil Penalty for Util Unlawful Actions,Per 10CFR2.206 ML20247H1291989-01-30030 January 1989 Requests Suspension & Revocation of Licenses DPR-31 & DPR-41 on Basis of Failure of Personnel to Follow Procedures,Very Poorly Written Procedures,Poor Personnel Training & Overwhelming Maint Problems,Per 10CFR2.206 ML20245B4091989-01-23023 January 1989 Refers to Re Corrosion Inhibitors in Closed Water Sys at Plant.Last Sentence on First Page of Ltr Should Be Changed to Read One Example Is Loss of Air Cooling to Shutdown Board Rooms at Sequoyah ML20245B4101989-01-19019 January 1989 Requests That Jg Partlow Pursue Completion of Engineering Assignment of ED Buggs at Plant Concerning Corrosion Inhibitors for Closed Water Sys.Draft Engineering Rept Recommending Corrosion Inhibitors for Closed Water Sys Encl ML17345A5271988-10-31031 October 1988 Notifies of Alleged Activities at Plant Violating Info Notice 81-22,Section 235 ML20206D8951988-10-15015 October 1988 Expresses Opinion That Plants Should Remain Closed Until Converted to Alternative Fuel Source ML20245B4121988-10-14014 October 1988 Informs of Several Technical Concerns Expressed While at Util & Requests That Jg Partlow Pursue Resolution of Listed Concerns ML20206D9711988-09-0808 September 1988 Forwards Ltrs Exchanged Between NRC & Author in 1984 Re Problems in Commercial Nuclear Power Field & Change in Federal Regulations to Allow Senior Reactor Operator to Deviate from Tech Specs in Emergency ML20206D9451988-08-12012 August 1988 Annotated Ltr Expressing Appreciation for Reply to & Assurance in Response to Concerns Pertaining to Operation of Ref Plants ML20245D6611988-08-0808 August 1988 Submits Listed Comments in Response to Re Safety Practice to Schedule Nuclear Plant Operating & Maint Personnel for 16 H Shifts &/Or Excessive Overtime ML20206E0281988-07-0707 July 1988 Advises That Nuclear Industry Overlooked Most Important Lesson Resulting from TMI Accident,To Wit,That Station Operator/Mgt Official Stationed in Control Room Would Have Prevented Accident ML20150A7961988-06-30030 June 1988 Comments on Util 880616 Request to Suspend Antitrust License Condition.Economic Advantages for Util Owning Nuclear Power Plants Have Failed to Materialize ML20155B6651988-06-16016 June 1988 FOIA Request for plant-specific Documents Re Fire Protection Requirements,Insp repts,hardware-specific Deficiencies & NRC Communications W/Util ML20206E0361988-04-29029 April 1988 Opines That 10CFR50.54(x) & (Y) Superfluous & Dangerous.Nrc Should Instruct Operators Not to Depart from Tech Specs in Emergency.Author Resume Detailing Experience in Commercial Nuclear Power Field Encl ML20155A7431988-02-24024 February 1988 Discusses Safety Problems at Comm Ed Nuclear Power Plants Re Risking Fuel Meltdown by Turning Off Safety Sys as Directed by Util Policy in Emergency If Core Cooling Is Adequate. Vice President Instruction Encl ML20148G9001988-02-0101 February 1988 FOIA Request for Documents Re 10CFR50,App R Insps & Enforcements ML20206E0431988-01-29029 January 1988 Expresses Concern Re Two Hazardous Practices at Ref Plants, Including Risking Meltdown by Authorizing Operators to Turn Off Nuclear Plant Safety Sys During Emergency ML20149G1051987-12-18018 December 1987 Opposes NRC Reduction at TMI-2.Reducing Staff Prior to Completion of Core Removal Inappropriate & Misguided Move. Recent Shutdown of Oyster Creek for Incident Re Destruction of Data Decreases Util Standing W/Local Residents ML17303A6161987-09-30030 September 1987 Forwards Scenario Review for Rancho Seco Emergency Preparedness Exercise,871104. Incomplete Scenario Provided for Review.Plant data,in-plant Chemistry & Radiological Data & Controller Info to Support Fire Drill Missing Elements ML20235T7341987-09-0101 September 1987 Requests That EIS Documents Re Meltdown Prepared by Impartial Sources Be Made Available to Public.Observation of Plant Life Indicates Level of Contamination of General Environ Causing Widespread Severe Damage ML20238B7731987-08-0707 August 1987 FOIA Request for Records Explaining Status of Listed LERs Omitted from List,Previously Received from Nrc,Of LERs Filed by Commercial Nuclear Power Plant Licensees for Operating Year 1986 ML20238E0261987-07-15015 July 1987 Responds to Recipient 870528 Response to Bg Strout Re Maine Yankee & Pilgrim.Author Distressed by NRC Answers & Requests Addl Response to Listed Questions ML20235L7061987-07-0808 July 1987 Opposes Util Application for Amends to Licenses,Allowing New Ownership & Financing Arrangement.Nshc Should Not Be Made W/O Public Hearings on Serious Financial Qualifications Questions 1990-07-07
[Table view] |
Text
'
V -
., ye
()
,,=1 a . ~
s 's - i j
.- J. C. HOBBS 2507 COUNTRY CLUB PRADO, CORAL GABLES. FLORIDA 60 WOOD STREET, PAINESVILLE, OHIO Ilay 2 3, 1973 Mr. F.E. Kruesi Director of Regulatory Operations United States Atomic Energy Comrnission Washington, D.C. 20545
Dear Sir:
Thanks for your letter of 21ay 9, 1973 and copy of ROE-72-15 The drawings will be very helpful. Some additional facts are needed. They are the detailed dimensions of the --
L. "2G" main steam piping O.D. and I.D.
B. The Reducers from 26" to 12" and 12" Cap. The original reduction was reported to be 20" to 16" saddle and 16" to 12".
. C. Piping Specs D. Safety Valve -- Original was 4" #Std. # Bolted Flange.
E. The Safety Valves described seem to be unsatisfactory.
Mountings created objectionable stresses.
Great weight about 3006 for Original and 4000 for each of replacements. Drawings of the Original and Replacenent Valves could be helpful.
F. Welding design proceedures and heat treatment could have been factors. Better practice vould have reduced the Stresses to absolute Safety.
G. None of the " repairs" take care of the thornal stresces which causedthe violent explosion.
The replacement was said to be 5" eStd..
Lack of time has not alloued me to go to the Homested Library.
If you could lend me a copy of Hearing I would not need to have copies made for careful study.
My impressions from incomplete data are:
- 1. Original Safety Valve lieaders were dangerous.
2 Replacements are also hazards.
- 3. Headers were not necessary. No explosion could have occurred in non existant headers.
Yours truly, h- [/ /[g['
/
8306020614 730604 /
PDR ADOCK 05000250 S PDR - '.'
J.C. Hobbs t,-
, N._/ /
9 9
The report ROE 72-17 Copy of ROE 71-12 please ROE 72-15 concludes Explosion was caused by dynamic loading 1 J.C.H.-- The piping included undesirable features which multiplied the destructive forces. Those features were unnecensary The shear diagrams confirn.
The report indicates that all fractures started near welds.
No explosion could have occurred in the safety valve piping if none existed!
The destructive force was the result of piping design vhich resulted in shear and tensil and Tortion Stresses multiplied by reaction of Safety Valve discharge forces and vibration.
- k. -)
r l.
d O 1" o
ROE 71'12 '
RUPTURE OF MAIN STEAM SAFETY VALVE PIPE N0ZZLE
. NOTE The incident described in this Reactor Operating Experience was also reported in the newly established AEC series of " Reactor Construction Ex-perience" reports (RCE 71-1). The RCE reports are directed primarily to individuals directly responsible for plant construction and quality as-surance and control. Thus, the emphasis of the RCE reports is often on different aspects of an event than those of special interest to operating personnel. Since this particular incident is also of special interest to reactor operating personnel, the operational aspects of the incident are
- discussed in this report.
Summary During hot functional testing of a new pressurized water reactor plant, a SIX-INCH DIAMETER PIPE N0ZZLE between a pressurized main steam line and a. safety valve FAILED COMPLETELY. Seven men, involved in test-ing the valve, were injured by the escaping steam. At the time of the incident, the nuclear core had not been placed in the reactor vessel. The incident provided an unusual opportunity to observe the non-nuclear plant transient aspects associated with a rupture in the main steam system.
DESCRIPTION OF MAIN STEAM SYSTEM, SAFETY VALVE ASSEMBLY AND PIPE N0ZZLE BREAK The secondary system is comprised of three steam generators each with one separate main steam line passing from each generator through the con-l- tainment wall to a common main steam header. Four safety valves and two
! relief valves are installed on each of the three separate main steam lines (see Figure 1).
All safety valves were welded to a 6-inch schedule 80 pipe nozzle, with the nozzle weld preparation formed by counterboring and tapering the nozzle to schedule 40. The schedule 80/40 pipe nozzle was in turn welded to a 26-inch OD main steam pipe spool piece (see Figure 2).
These welds and the pipe nozzle were subjected to a " cold hydro" test at 1356 psig and had subsequently been exposed to elevated tempera-l tures and pressures for approximately nine days prior to the incident.
l During this 9 day period, system temperatures varied from 520* -- 540*F and pressures varied from 800-1000 psig.
The. failure occurred in the reduced section ef the six-inch pipe nozzle which connected the safety . valve to a 26-inch steam line. The internal fracture path coincided exactly with the end of the machined internal diameter taper.
w -' w-rw+w 4-v-
o o
145 .
r ORNL-0WG 76-440e0 g
g g f] f] [f FAILURE PolNT FROM STEAM . T T T T 17 GENERATOR
FROM STEAM GENERATOR RV iSV-t -2 -3 -4 RELIEF SAFETY VALVES g E LOOPi Y
DRAIN A B C PRV-1325 h PRESSURE RELIEF VALVES 0
Figure 1. Main Steam Piping System l
7___
146 O O 4-O RNL- Owe 74-44082
_ 29Y2in.
=
I \/ EXHAUST CHUTE SAFETY VALVE SV 10in.
d 5.375 in.
ID 9.0 in. 00 6.065 In.
ID VALVE l
26-in-OD STEAM PIPE .
SACKUP RING :
[
-- ;- - -- FAILURE AT END OF TAPER 17' % / _
6.625 in. 00 5.761 in. ID h 6-in. SCHED 80 PIPE w
WELD JOINT j Figure 2. Safety Valve Connection
.m
' O.4 bM4. M'4S.Q 6 @M b .&WL& m_m ,e _ . . _ _ ,e ~-
O o 147 ERDE 71 12 Circumstances t
l A. Description of Incident. ,For several days prior to the nozzle failure, the final stages of the hot functional testing program had been
- in progress using the reactor coolant pumps to heat the primary system.
i At the time of the incident, the lift set pressure was being checked for the steam generator secondary system safety valve. Verification of safety valve set points and adjustments as necessary were being performed using a pneumatic test device attached to the safety valve which allows the set points to be verified without raising the system pressure up to lift pres-sure.. Eight'of a total of twelve safety valves had been tested on two of three steam lines and all settings were found to be very close to the certified settings. The primary system was at 533*F and 2225 psi and the secondary system was at 900 psig. Constant level was being maintained in the steam generator associated with the safety relief valve nozzle which
! failed. Steam lines had been blown down briefly for one to three minutes the day of the incident by drain valves prior to testing.
It was determined that the failure occurred about the time that a
. member of the test group was opening the valved air pressure regulator
- of the pneumatic test device installed on the safety valve. The opening
< of this valved air pressure regulator balances the safety valve spring force to make a detennination of the, safety valve set pressure. No warn-ing of the impending failure was evident to the men in the vicinity of the safety valve. A loud noise was heard, followed by a shower of steam, insulation, scaffolding, metal parts and construction debris. The men
! in the vicinity of the valve were either knocked to the flooring by the force of the steam release or were forced. to lie down due to . lack of air to breathe. The rapid release of steam displaced the air from the area above the severed pipe nozzle requiring the men to stay in a position
- near the floor. The men immediately made their way out of the area and l
down a stairway, away from the immediate scene of the accident, without assistance. The men were transported to a local hospital by ambulance and treated for burns and injuries. One man was released after immediate j treatment at the hospital, but the other six were admitted for treatment of their injuries.
Crafts workmen, construction supervisory personnel and operations and test personnel witnessed the incident from several vantage points.
The following description of the incident is based on interviews of the l eye-witnesses:
i~
The initial noise was immediately followed by a second louder noise.
The initial steam accumulation in the area of the break spread in an almost horizontal plane, followed by the formation of a vertical column of steam which rose an estimated 150 feet into the air.
Upon inspection following the incident, it was observed that there 1
l was an area of localized cutting of insulation on a nearby pipe line i-
l
. , .. % 148 j l
ROE 71 12 located in about the same horizontal plane as the break. This damage suggested an initial crack in one quadrant of the pipe. Steam was ap-parently directed in a fan shape, horimntally toward the nearby pipe line for a brief period of time prior to a complete severance of the pipe nozzle and prior to the expulsion of the total valve assembly from the area by the force of the steam jet. Such a sequence of events is also suggested by the reported two stages of sound, the post-accident appearance of the fracture surface, and the direction of travel of the separated valve. The valve was propelled in a direction approximately 180* opposite to the quadrant in which the initial crack is thought to have occurred. In its rebounding flight, it struck supporting structures, carried away an angle brace and dented and moved the stack from the auxi-liary boilers causing its supports to bend and break away. The valve came to rest on the turbine building mezzanine floor eighteen feet below its original position. I B. Initial Plant Conditions and Action of Control Operators During Incident. Two personnel were on duty in the control room prior to the incident, a control operator and a shift foreman. The plant was being operated in accordance with a hot functional test program with three re-actor coolant pumps in service to provide system heat (533*F) with sys- i tem pressure being automatically comtrolled by the pressurizer at 2225 psig. One charging pump was operating in automatic control with letdown l through a 45 GPM letdown orifice and feeding one train of the mixed bed demineralizer. Makeup to the system was being controlled automatically.
Secondary system pressure was approximately 900 psig with the main steam isolation and main steam bypass valves closed. All three steam generator blowdown lines were valved to the blowdown tank and throttled to achieve system temperature and pressure control. Steam generator levcis were be-ing maintained at approximately 70 percent level. The motor-driven auxi-liary feed pumps were lined up to take suction from the condensate tank and feed the steam generators as required to maintain proper level. The main feedwater and feedwater bypass valves were closed and the main feed-water pumps were secured. The steam-driven auxiliary feed pump was also secured and its discharge valves closed. No feedvater was being added to any steam generator at the time of the incident.
At the instant of the pipe rupture, a loud noise was heard by the shift foreman and the control operator. The noise was followed by a rapid decrease in indicated pressurizer level and pressure. In addition, level decreased rapidly in the steam generator associated with the failed safety valve pipe nozzle. Reactor coolant temperature decreased rapidly.
The control room personnel secured the reactor coolant pumps. Two addi-tional charging pumps were placed in service and letdown was stopped to minimize the effects of pressurizer level and pressure decrease. Pres-surizer heaters were manually de-energized prior to reaching the auto-matic heater cutoff set point on pressurizer low level. Even though the pressurizer level decreased off scale, it seemed reasonably certain (and was later verified by analysis) th~at the pressurizer steam bubble did not I
g o
- 7
=
149 ROE 71 12 '
expar.d out of the surge line. Pressurizer pressure did not decrease be- -
low the safety injection set point of 1715 psi owing to the timely actions of the operators, which increased the system mass and minimized system shrinkage.
Two boric acid transfer pumps were started to provide makeup _
to the charging pumps in addition to the automatic makeup which was in service at the time of the accident. The extremely loud noise produced by the escaping steam rendered communications by the plant intercom sys- _
tem ineffective and plant operators reported in person to the control room for instuctions. -
The bottom blowdown valve on the affected steam generator was opened fully to aid in depressurization of the steam gen-erator and it was blown dry.
The overall transient caused the reactor coolant system hour period. temperature to decrease approximately 213*F within a one-A detailed survey of the reactor coolant and secondary systems was conducted to assure that there was no damaged equipment, pipe or other abnormalities.
No other abnormalities were found. Pressurizer level was restored to normal, no-load, operating level which resulted in regaining !?
- a coolant pressure of approximately 2050 psig. Normal charging and let-down was established.
A In preparation for starting the reactor coolant pump associated with the affected steam generator, the temperature and pressure of the two -.
unaffected steam generators was reduced to minimize the thermal and pres-sure transients.
! Steam generator temperature and pressure were reduced *"
- by intermittent use of bottom blowdown and feedwater addition and by steaming through the main steam isolation bypass valves. Reactor coolant 3
pressure spray was reduced to approximately 1250 psig by use of the auxiliary system.
made. A review of all available plant temperature instrument readings was .
and coolant loops to assure that there were no large temperature differ-
=
ences between components and the primary / secondary interface. The reac-tor coolant pump associated with the affected steam generator was started --
with no abnormalities noted. After the plant temperatures were stabilized, the remaining reactor coolant pumps were started and the plant was cooled down utilizing normal operating procedures.
C. Transient Aspects of the Pipe Nozzle Failure. Since the safety -
valve cident.
was blown clear, it can be assumed that from the moment of the ac- r 0.176 ft unimpeded d.
steam discharge took place through a break area of This was slightly smaller than the design basis steam line break evaluated in the Final Safety Analysis Report (FSAR) for the plant. i If this type of failure were to occur during reactor operation, protec- -
i tion against overheating of the reactor core would normally be provided by the safety injection system initiated by coincident signals of pres-surizer low pressure and low level. In this incident, the automatic initiation of the safety injection system was precluded by the corrective <
w,---n-m -w-*--- W O
2'o O
ROE 71 12 actions of the operators. The available instrumentation in the plant recorded a sufficient number of plant parameters during the accident to enable a comparison to be made between the calculations of plant behavior for a steam line rupture and the actual experience. Although the timely actions of the plant operators resulted in a transient behavior of the reactor coolant system which differed considerably from the accident cal-culations presented in the FSAR, an analytical investigation revealed that the calculational technique used to evaluate steam line rupture ac-cidents could yield realistic predictions of the transient behavior during the incident, given input data concerning operator action. A delay of a few minutes in implementing the actions which were taken to increase pri-mary system mass and minimize shrinkage would have resulted in emptying the pressurizer and surge line, in which case the pressurizer pressure would have decreased rapidly through the safety injection pressure set .
point of 1715 psig.
Although there was no fuel in the reactor at the time of the accident, the operators did follow the emergency boration procedure by starting both boric acid transfer pumps and delivering fluid from boric acid tanks to the suction of the charging pumps. Under normal reactor operating condi-tions, these actions would have resulted in the additional boration of the reactor coclant to prevent the reactor from returning to criticality.
The effects of the transient on plant equipment were reviewed by the applicable equipment designers. The affected steam generator and' reactor internals were subjected to analysis 'and examination to determine if pos-sible detrimental effects occurred and were found to be in satisfactory condition.
Causes and Results At the time of this writing the cause of the failure has not been determined by the post-incident investigation. The stress analysis per- '
formed for the failed valve nozzle indicated that the sum of known stresses
~
was significantly less than the yield strength and ultimate strengths of the failed nozzle material. It was postulated during the course of the investigation that a full capacity steam discharge (at existing steam con-ditions) at the time of the incident may have caused the failure. To achieve the full discharge, one of the following conditions must have been satisfied: (a) the set point of the safety valve lif t device was exerting an equivalent of an additional 100 psi steam line pressure via 50 psig set into its air pressure regulator. If this were the case, the 900 psig reported in the steam line would have caused the valve to open.
However, this would require that either the safety valve set pressure as certified by the manufacturer was incorrect, or the set pressure decreased during shipment, handling or after installation. (b) The air pressure regu-lator of the valve device was set above 120 psi. At this setting, the equivalent steam line pressure would have been greater than 1140 psig en-abling the valve to discharge at full capacity. However, the air pressure
~~ ~ -
d 151 ROE 71 12 .
regulator is a sensitive device requiring manual adjustmant. Therefore, a deliberate action would be required to change the 50 psig as reported to allow 120 psi to enter the valve lift device.
Because the valve manufacturer's representative performing the valve check had paused during the test to check steam line pressure just prior
,4 to the incident, the equivalent steam line pressure could have been no greater than that necessary to bring about a balance valve condition.
This condition would have caased a " simmering" of the valve which would have been noticeable, but was not detected.
Although full capacity steam discharge is improbable, it cannot be ruled out entirely. The stresses computed for a full capacity steam dis-charge condition were nearly equal to the ultimate strength determined for the nozzle material. Further, should the total stress, under these conditions, be coincident with a stress intensification factor due to pipe wall imperfection, stresses may have resulted which exceeded the ultimate strength of the nozzle material. Thus, it appears that the in-let nozzle may have been marginally designed for a full discharge load condition.
The results of the investigation (available at this writing) indi-cate that the fracture initiated at*one location on the pipe nozzle and proceeded circumferentially around it in both the clockwise and counter-clockwise directions terminating about 180' opposite the fracture start-ing point. All areas of the fracture showed evidence of extensive plastic deformation and the internal diameter fracture path coincided exactly with the end of the machined inner diameter taper (see Figure 2) . The fracture path was not associated with the heat-affected zone of the weld although it did penetrate the heat affected zone in several locations. No signifi-cant material deficiencies were found with respect to chemical analysis, microstructure, pre-existing defects, or mechanical properties. No evi-dence of fatigue damage was observed in any area of the fract'ure.
Corrective Action The twelve main steam line safety valve inlet nozzles were redesigned to provide for a conservative design and to negate the effects of possible stress intensification factors. The extent of the revision included in-creasing inlet pipe nozzle size to 8-inch schedule 160 thereby enlarging the nozzle diameter and decreasing the thickness differences between the nozzle wall and the valve body wall. The seven relief valve pipe nozzles have also been modified using the same approach taken for the modification of the safety valve pipe nozzles.
Conclusion The lack of any material deficiency and the extreme plastic strain viewed on the fracture surface, indicate that failure was caused by over-loading. The peak stress must reach the ultimate stress to initiate a
.. _ ~_ _ - ._
a o m o ROE 71 12 failure and although the preliminary stress analysis of the static condi-tion did not account for the overload, there are mechanisms which may be postulated for generating the required increase in stress. These mecha-nisms become significant especially since the stresses computed for a full capacity steam discharge were nearly equal to the ultimate strength determined for the pipe nozzle material.
Although this report is based upon interim findings, sufficient in-formation is available to identify the probable mode of failure and to indicate that the inlet pipe nozzle apparently was marginally designed for a full discharge load condition or other increased stress condition.
P. S. Colby, Carolina Power and Light Co., to Dr. P. A. Morris, AEC Division of Reactor Licensing, Docket 50-261, July 3, 1970, available at AEC Public Document Room.
6 o
I a
e
_q
'g mA