ML20067B601

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Special Rept:On 900917,control Rod Inadvertently Removed from Fuel Assembly During Removal of Upper Internals. Possibly Caused by Procedural Deficiency.Procedures Enhanced & Lighting & Equipment Improved
ML20067B601
Person / Time
Site: Mcguire
Issue date: 01/31/1991
From: Mcconnell T
DUKE POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
2-M90-0245, 2-M90-245, NUDOCS 9102080300
Download: ML20067B601 (7)


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Duke Ibuer Company (7011875 M 00 AftGuire Nuclear Station 12700 Hagers ferry la>ad Hunterstille, NC:soi8s%S DUKE POWER January 31, 1991 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Subj ect : McGuire Nuclear Station Unit 2 Docket No. 50-370 Voluntary Special Report, Revision 1 Gentlemen:

Attached is a revision to the Voluntary Special Report submitted on November 9, 1990. This revision contains additional planned corrective actions. This event is considered to be of no significance with respect to the health and safety of the public.

Very truly yours, l#n

/ WW T.L. McConnell hYI ADJ/cb1 Attachment xc: Mr. S.D. Ebneter Mr. Tim Reed Administrator, Region II- U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation 101 Marietta St., NW, Suite 2900 Washington, D.C. 20555 Atlanta, GA 30323 Mr. P.K. Van Doorn INPO Records Center NRC Resident Inspector Suite 1500 McGuire Nuclear Station 1100 Circle 75 Parkway-Atlanta, GA 30339 M&M Nuclear Consultants 1221 Avenue of the Americas New York, NY 10020

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DUKE POWER COMPANY McGUIRE NUCLEAR STATION Special Report No. 2-M90-0245, Revision 1 A Control Rod Was Inadvertently Pulled From A Fuel Assembly '

During Removal _0f The Upper Internals Caused By Reasons Unknown,_Possible Procedure Deficiency ABSTRACT:

On-Septcmber 17,-1990, at 0645, Unit 2 was in Mode 6 (Refueling) in  !

- preparation for-unloading the fuel from the Core. The_ Operations Refueling l Senior Reactor Operator discove ed a Control Rod laying on top of the Core.

The Control Rod had-been inadvertently pulled from the Fuel Assembly when the

. Reactor Vessel Upper Internals vere removed by Maintenance personnel. The Upper Internals had been removed at 0200 on September 17, 1990. This  :

incident is assigned a root cause of Unknown, Possible Procedure Deficiency.

A_ contributing cause of Defective Procedure, Lack of Procedural-Precautions is also assigned. Corrective actions include procedure enhancements, lighting improvements, and equipment improvements.

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.- DPC/MNS 1 Special Report No.-2-M90-0245, Revision 1

.Page 2 EVALUATION:

Background-The Reactor Vessel Upper Internals section is comprised of the Top Support Plate, the Upper Core Plate, Support Columns, and Guide Tube Assemblies.

These Internals are designed to be removed as one unit during Refueltog

- operations. The Upper Internals, including the lifting device', weighs

-approximately 167,000 pounds when submerged in water.

Control Rods'are used to help in controlling the power level of the Reactor.

Each Control Rod has rodlets which enter the top of the Fuel Assembly. The  ;

ceight of a Control Rod is approximately 74 pounds. The tops of the rodlets ate connected to a Spider Assembly. The center of the Spider Assembly has a

- bub which latches to.a Control Rod Drive Rod. The Drive Rod passes up through Guide Tube Assemblies which protect and guide the Control Rod Drive Rods. The top of the Drive Rod is raised or lowered by the Control Rod Drive Mechanism.

Technical Specifications defines Shutdown Margin as "the instantaneous amount of reactivity by which the Reactor is, or would be suberitical from its present condition assuming all Control Rods are fully inserted except for.the single Control Rod of highest reactivity worth, which is assumed to be fully withdrawn."

Description of Event On September 14, 1990, refueling activities began in the Unit 2 refueling outage. At 1434, the Reactor Vessel Head was removed from the Reactor Vessel and placed on the Head Stand by Maintenance (MNT) personnel. Operations personnel began filling the Refueling-Cavity with borated water at 1753 in preparation for unloading the fuel from the Reactor to the Spent Fuel Pool.

On September 16, at 1236, after the Refueling Cavity had been' filled, MNT personnel began unlatching the Control Rods from the Drive Assemblies as directed.in procedure MP/2/A/7150/73, Rod Cluster Control Assembly Drive Rod Unlatching And Latching. The MNT personnel stated that three of the'four underwater lights were burning when they began the unlatching procedure. The day shift MNT crew had completed unlatching 37 of the 53 Control Rods at 1830 wneu _the night shift MNT crew reported for work. The day shift MNT supervisor stated that a second underwater light had burned out just prior to- '

the night shift crew coming in to work. This MNT supervisor stated that .

adequate lighting was available to proceed with unlatching the Control Rods with the remaininr two underwater lights in service. The day shift MNT supervisor noted ta the turnover log that the lights in the Reactor Cavity needed to be cheued. ,

The night shift MNT crew completed unlatching the remaining 16 Control Rods at approximately 2300 on September 16, 1990. The night shift MNT crew next began-removing the Reactor Vessel Upper Internals as directed by procedure

-MP/0/A/7150/43, Reactor Vessel Upper Internals Removal and Replacement. This ,

procedure, in part, directs MNT personnel to utilize the Polar Crane with a load cell and lifting device connected to the Reactor Vessel Upper Internals.

These Internals are lifted up high enough to clear the Reactor Vessel Flange and then placed on the Upper Internals Storage Stand. During the lift of the Upper Internals, and subsequent moving to the Storage Stand, the crane

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.- DPC/MNS i Special keport No. 2-M90-0245, Revision 1 Page 3 operator monitors the load cell indications to ensure the Internals are not binding. Also, an observer is positioned at the Refueling Canal deep end to ensure that components are not attached to the Upper Internals Core Plate.

The Upper Internals were placed on the Storage Stand at approximately 0200 on September 17, 1990.

At 0600, the Operaticas Refueling Senior Reactor Operator (SRO) entered the Reactor Building and began lowering lights around the Reactor Cavity in preparation for unloading fuel. During the process, the SRO discovered a Control Rod Assembly laying at an angle on top of the fuel assemblies. The Spider Hub end of the Control Rod wae leaning against the Core Barrel and the rodlets were laying on top of the Fuel Assemblies. The Refueling SRO notified the Operations Control Room SR0 of his discovery.

At 0630, Operations personnel verified adequate Shutdown Margin with one Control Rod withdrawn from the Reactor Core.

At 1145, on September 17, a camera was lowered down to inspect the Control Rod. Viewing of the tape from this inspection did not reveal any major damage to the Control Rod or to the tops of the Fuel Assemblies in the area of the Control Rod.

Procedure T0/2/A/9600/057, Retrieval of RCCA On Top Of Rx Core, was written and approved and the Control Rod was retrieved and placed on the floor of the Refueling Canal at 2030 on September 17, 1990. The Control Rod was moved to the Spent Fuel Pool for storage on October 16, 1990.

Conclusion This incident is assigned a cause of Unknown, Possible Procedure Deficiency.

The exact cause for the Control Rod coming out of the Core could not be determined. MNT personnel performing the procedure for removal of the Upper Internals stated they believed the Control Rod was properly unlatched. They also stated that had the Control Rod not been unlatched, it would not have dropped free when the Upper Internals were being moved. The Rodlets would probably have bent when they bumped into the Core Barrel, but the Drive Shaft should have remained latched to the Spider Assembly of the Control Rod.

A possible scenario for the Control Rod being lifted with the Upper Internals is associated with the Control Rod Unlatching procedure. This procedure requires the MNT personnel to position the Unlatching Tool over the Control I Rod. The Unlatching Tool is latched to the Drive Rod and the entire Control '

Rod Assembly is lifted approximately 6 inches while monitoring a load cell. j This ensures the Control Rod is properly attached to the Unlatching tool.

The Control Rod is then lowered back and the Drive Rod is Unlatched from the Control Rod. The Drive Rod is raised approximately 12 inches while monitoring the load cell to ensure the Control Rod is unlatched. The Drive l' Rod is.then set on top of the Hub of the Spider Assembly of the Control Rod and the Unlatching Tool is disconnected from the Drive Rod (see Enclosure 6).

When' all of the Control Rods br- been unlatched, a check pass is performed.

The check pass has the MNT r ,-

  • latch each Drive Rod and raise it l approximately 6 inches while w n .ing the load cell. This check pass again verifies the Control Rod is t. t 'ed. The Drive Rods are removed with the l Upper Internals.

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., DPC/MNS y Special Report No.~2-M90-0243,-Revisio'n 1

. Page 4 Elevation marks are establisted on the Unlatching Tool-lifting bail during the unlatching of-the first Drive Rod. The Manipulator Crane handrail is the reference point for these elevation marks. The handrail is located approximately 6 inches away from.the elevation-marks on the Unlatching Tool.

The lower elevation mark is the unlatched position and the upper elevation mark is the latched position. These-reference points are used to help ensure each Control Rod is properly unlatched.

The Control Rod possibly remained partially attached to the Drive Rod following the check pass. This could occur if the Drive Rod did not sit down exactly-on top of the Spider Assembly Hub._ During the check pass, the Unlatching ~ Tool is aligned over each Control Rod Drive Rod The Unlatching Tool can be latched.to the Drive Rod even if it is not exactly centered over

-the-Drive Rod. A deviation of a fraction of an inch will still allow the Drive Rod to be latched. The Drive Rod is raised approximately_6 inches and.-

then lowered back down on top of the Spider Assembly Hub. The small amount the Unlatching Tool was off enter could cause the Drive Rod to miss sitting flush on the Spider Assembly Hub. This could allow the Drive Rod latching fingers to straddle the Hub of the Spider Assembly,. partly in the-Hub and partly outside of-the Hub. If this occurred, the potential exists for the fingers-to. catch enough to raise the Centrol Rod when the Drive Rod was lifted with the Upper Internals. When the Upper Internals had been lifted sufficiently-to clear the-Reactor Vessel T1ange,-the Upper Internals were

-moved--toward the Internals-Stand. The Control Rod would have been hanging-

-below'the Upper Internals and would have contacted the Core Barrel. This would have jarred the Control Rod free.

,The Control Rod was discovered laying on the opposite side of the Core from the Core location that it came from. The procedure for unlatching the Control _ Rods did not. instruct the MNT. personnel to ensure the unlatching tool was aligned for plumbness over the Control Rod Drive Rod.  ;

MNT personnel use a load cell when lifting the Upper Internals. The weight 7 of'the Upper Internals and'the lifting device-is approximately 167,000 pounds.-- The-Control' Rod weight of 74 pounds would not be noticeable to the 1 MNT_ personnel performing this procedure.- i The elevation marks' used-to ensure that a Control Rod is unlatched could have given an indication of a Drive Rod not' sitting-properly .on top of the Spider.

Assembly Hub. If the: Drive Rod was straddling the Hub, the elevation mark would.be slightly higher-than normal. 'The MNT-personnel are required to l sight from the handrail to the elevation marks on the Unlatching Tool-lifting L

-bail,-'a. distance of approximately 6 inches. This small amount of difference i would be very difficult to notice.

A-contributing cause of.Defecti.ve Procedure, Lack.of Procedural Precautions, l! is;being assigned to-this event. -The procedure for_ removing the Upper.

Internals requires an observer to stand at the Refueling Canal deep end to ensure that Core components are not attached to the Upper Internals Core

' Plate. The MNT person performing this task is approximately 40 feet away and attempting to_look down-through the water. The procedure did not have any lighting requirments for the Reactor Cavity Area. The underwater lights ased for' unlatching the Contro1~ Rods.are not sufficient to enable this observer to see that a Control-Rod was being lifted with the Upper Internals. The positioning of the lights and~the amount of light were both inadequate.

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. .j o- DPC/MNS . _

._ Special Report No. 2-M90-0245, Revision-1

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'A review ofL he t Operating _ Experience Program data base for the past twenty  ;

-four months prior to this incident revealed no incidents involving Control o Rods _or Fuel assemblies being inadvertently removed from the Core.

Therefore, this incident is-not considered recurring. >

-This event is not Nuclear Plant Reliability Data System (NPRDS) reportable.

There vere no personnel injuries, radiation overexposures or-uncontrolled releases of radioactive material as a result'of this incident.

COP.RECTIVE ACTIONS:

Immediate: 1) Operations personnel verified adequate Shutdown Margin with one Control Rod out of the-Core, l ,

Subsequent: 1) Operations and MNT personnel inspected the dropped Control Rod with a submersible video camera.

, 2) The Operations Fuel Handling supervisor wrote procedure T0/2/A/9600/057, Retrieval Of RCCA On Top Of Rx Core.

3) Operations and MHT personnel retrieved the Control Rod-from the top of the Core and placed it on soie floor of i the Refueling Canal.

4). Operations and MNT personnel inspected the Fuel l Assemblies in the area where the Control Rod _ dropped-with

-a video. camera..

5) MNT-personnel designed and fabricated a pointer to be attached ~to the handrail, during Control Rod Unlatching, to improve the accuracy of the elevation marks on the Unlatching Tool.  !

6)- Lights were installed by MNT personnel on,the Unlatching:

Tool to better illuminate the area where the Unlatching Tool connects'to:the. Drive Rod.

'7) .A video. camera inspection was performed by MNT personnel- <

of the bottom of'the Upper Internals and of the Spider Assembly Hub on-the Control Rod that was dropped-searching for the cause of the Control ~ Rod being-lifted.

No conclusive evidence was found.

8) The Drive Rod for the affected Control Rod was inspected- l by MNT personnel. No damage was found. ]

Planned: 1) -MNT personnel will revise the Control Rod Unlatching procedure (MP/2/A/7150/73) to_ require verification of plumbness of-the 1Jnlatching Tool over the Drive Rods when latching or unlatching.

2) MNT personnel will revise the procedure for removing the Upper' Internals (MP/0/A/7150/43) to require a back light to help-in deterinining that Control Rods or Fuel Assemblies are not being inadvertently lifted.

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. DPC/MNS ,

Y *' -Special Report No. 2-M90-0245, Pavision 1 l

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3) MNT personnel will investigate the feasibility of using a submersible camera in conjunction with a back light.to ensure that no Control Rods or Fuel Assemblies are inadvertently being lifted with the Upper Internals.
4) MNT personnel will revise the Control Rod Unlatching procedure (MP/2/A/7150/73) to specify weight limits which must be verified prior to releasing the Unlatching Tool from the Drive Rod during the check pass portion of the procedure.
5) MNT personnel will revise the procedure for removing the .

Upper Internals (MP/0/A/7150/43) to verify there is no foreign material on the Canal floor inside the Upper Internals Starage Stand when placing the Upper Internals

-on the stand.

6) MNT personnel will revise the procedure for removing the Upper Internals (MP/0/A/7150/43) to provide an elevation mark to match the water level on the Internals Lifting Rig to ensure the Fuel Alignment Pins clear potential obstacles.

SAFETY ANALYSIS: ,

Technical Specifications requires that the boron concentration.of the Reactor Coolant System and the Refueling Canal be the more restrictive of either a Shutdown Margin of 5 percent or a minimum boror. aoncentration of 2000 parts per million (ppm) while in Mode 6. This requic+ent ensures that the Reactor will remain suberitical during Core Alterations.

During the time of this incident, the N actor Coolant System and Refueling.

Canal-Boron concentration was 2049 ppm. This concentration was more than adequate to ensure the Reactor remained suberitical. Calculations show that even with the most reactive Control Rod out of the Core, the ruuired Boron Concentration to ensure a Shutdown Margin of 5 percent is 1659 ppm.

The Fuel Assemblies were not damaged in this incident. In a worst case scenario, the-dropping of a Control Rod could have caused a breach in the fuel clad. The dose _ consequences.for such an event would be bounded by the analysis for Fuel Handling Accidents performed in Chapter 15.7.4 of the Final Safety Analysis Report which states that the doses from this accident are within 10CFR100 limits.

The health and-safety of:the public were not affected by this incident.

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