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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20151W3521998-09-0808 September 1998 Special Rept 98-01:on 980819,maint Could Not Be Performed on FPS Due to Isolation Boundary Leakage.Caused by Inadequate Info Provided in Fire Impairment Plan.Isolated Portion of FPS Was Returned to Svc ML20148K3721997-06-0909 June 1997 To Special Rept 96-04:on 961011,groundwater Level Was Above 731 Feet for 7 Days.Caused by Precipitation During Previous Week.Verified That No Other Groundwater Monitoring Instruments Were in Alarm ML20148A9881997-05-0101 May 1997 Special Rept 96-04-02:on 970429,groundwater Level at Well Mk GWA-2 Was in Alarm for 7 Days.Caused by Precipitation During Previous Week.Verified That No Other Groundwater Monitoring Instruments Were in Alarm ML20137P0711997-04-0707 April 1997 Special Rept 97-01:on 970226,Peak Accelerometer,1MIMT-5030, Removed Under WO 95092624 as Part of SG Replacement Project. Accelerometer Will Return to Svc Prior to Unit 1 Startup ML20133L6051997-01-0909 January 1997 Special Rept 96-04,Rev 1,groundwater Level at Well Mk GWA-2 Monitored by 2WZLS5060 Was in Alarm for 7 Days.Verified That No Other Groundwater Monitoring Instruments in Alarm ML20134N0261996-11-14014 November 1996 Special Rept:On 961006,groundwater Alarm Was Received & Entered in TS Action Item List for Tracking.Field Survey of Surrounding Areas Was Performed to Verify That No Water Was Percolating to Surface That Would Indicate Pipe Leak ML20116K0331996-08-0909 August 1996 Special Rept 96-03:on 960611,identified Broken Secondary Contact Blocks.Caused by Mishandling of Breakers or over- Torquing of Mounting Bolts.Breaker 2BYA Repaired,Tested & re-installed in Cabinet ML20086G9601995-07-12012 July 1995 Special Rept 95-002:on 950612,turbocharger Failed,As Detected by Excessive Noise & Vibration.Engine Subsequently Secured.Damaged Components Replaced & DG 2A Returned to Operable Status ML20080G4421995-02-0303 February 1995 Special Rept 95-01:on 950104,personnel on Unit 2 Operating in Solid Condition During Fill & Vent of Nc Sys ML20078R7651994-12-15015 December 1994 Special Rept 94-06:on 941012,fatigue Usage to SI Sys Piping by Manually Initiating Flow Through B Cold Leg from Fwst During Testing for Valve 1NI-71 Intentionally Increased. Startup of Facility Discontinued to Repair Valve ML20078L6571994-11-22022 November 1994 Special Rept SR-94-05:on 941024,Channel 3 of Vibration & Loose Parts Monitoring Sys Declared Inoperable Due to Noise.Channel 3 of V&Lpm Will Be Repaired Under WR 94043758 or Replaced by Nsm MG-12096 During Outage 1EOC10 ML20073C2451994-09-14014 September 1994 Special Rept 94-004:on 940821,valid Failure of DG 1A Occurred Due to Failure of Series Boost exciter-regulator (Voltage Regulator).Isolation Transformer T54 & Current Transformers CT1,CT2 & CT3 Will Be Inspected ML20065K2501994-04-15015 April 1994 Special Rept 94-03:on 940210,during Testing PORV Observed to Hang Open in Absence of air-assisted Closure.Caused by Incomplete Testing of Porvs.Compensatory Measures Reanalyzed & Reestablished Addressing Fire & Security Issues ML20064K0311994-03-15015 March 1994 Special Rept 94-01:on 940215,DG 2A Tripped W/Low Lube Oil Pressure Indication During Routine Surveillance Test.Caused by Pressure Too Low in Bldg Up in Sensing Lines.Test Satisfactorily Repeated ML20058M4281993-09-27027 September 1993 Special Rept 93-09:on 930920,notifies of Alarm Condition Showing Alert on Ground Water Level Outside 1A DG Room.Work Order 93063348 Initiated by Wc Personnel to Have Iae Personnel Check Operation & Calibr ML20056F8561993-08-23023 August 1993 Special Rept 93-06:on 930405,discovered Debris on Unit 1 Lower Core Plate.Four Other Unidentified Objects Noted During Video Insp of Lower Core Plate ML20126B5051992-12-15015 December 1992 Inplant Review Rept 92-20,special Rept Re Postulated Scenario That Could Introduce Air Into AFW Suction Piping. Caused by Functional Design Deficiency.Setpoints of Affected Pressure Switches Increased ML20106D7401992-10-0909 October 1992 RO 92-19:on 920804,discovered That Drive Shaft on Pump 1MNVPU0046 Was Rotating in Opposite Direction than Specified on Pump Casing.Caused by Mgt Deficiency.Motor Leads of Subj Pump Reconfigured to Provide Correct Pump Shaft Rotation ML20127E0191992-09-0909 September 1992 Special Rept:On 920421,unusual Event Declared Because Unit 1 Train B of Ssps Inoperable Due to Defective Circuit Card within Ssps.Failed Train B Ssps Circuit Board Replaced & Appropriate Procedures to Be Evaluated ML20101T9441992-07-13013 July 1992 Special Rept for Inplant Review 92-10:on 920610 No Mention Made on Work List of Vent Path Through SG 1B for Incoming SG Crews.Caused by Deficient Communication.Turnover Sheet Established to Document Existing Vent Path Status ML20101P5581992-07-0303 July 1992 In-Plant Review Rept 92-09:on 920619,setpoint Problems Noted W/Ts & Selected Licensee Commitment Values for Listed Field Data.Caused by Discrepancies W/Groundwater Level Monitoring Portion of Wz Sys.Ts Monitor Logged in Unit 2 Logbook ML20086Q1101991-12-20020 December 1991 Voluntary Special Rept 91-23:on 911008,reactor Vessel Lower Internals Contacted Reactor Vessel During Removal.Caused by Inappropriate Operator Action & Mgt Deficiency.Recovery Plan Developed Re Insp of Lower Internals & Refueling Canal ML20086H9431991-12-0404 December 1991 Special Rept 91-24:on 911104-29,concerns Noted Re Possible Leakage of Containment Spray Sys Check Valves Into Annulus, Causing Offsite Radioactive Dose.Caused by Design Deficiency.Check Valve Installed Downstream of Piping ML20091C0851991-08-0101 August 1991 Special Rept PIR 1-M91-0113:on 910616,diesel Engine Cooling Water Leak Discovered on Diesel Generator 1A at Discharge Flange on Intercooler End Bell Cover.Caused by Poor Casting Quality.New Covers Will Be Installed ML20081F7371991-06-0404 June 1991 Rev 1 to Special Rept 91-11 Dtd 910411:on 910215,turbine Driven Auxiliary Feedwater Pumps Automatically Started. Caused by Deficient Communication & Lack of Attention to Detail.Pump Speed Reduced & Discharge Valves Closed ML20062E7991990-11-14014 November 1990 Special Rept:On 901011,turbine Driven Auxiliary Feedwater Pump Declared Inoperable W/O Having Made Security Notification.Caused by Inappropriate Action ML20055G2161990-07-12012 July 1990 Ro:On 900602,discovered That Channel 7 of Vibration & Loose Parts Monitor Sys Had Low Noise Level.Probably Caused by Bad or Damaged Sensor Cable.Definite Cause of Failure Undetermined.Sys Scheduled to Be Replaced ML20034B9961990-04-19019 April 1990 Corrected Special Rept Re 900303 & 04 Failure of Diesel Generator 1A to Start.Caused by Loose Sliding Links at Terminations C33 & E33.Nuts Replaced ML20034B3111990-04-17017 April 1990 Revised Special Rept:On 900303 & 04,diesel Generator 1A Failed to Start During Start Attempts Due to Failure of Cooling Water High Temp Switch & Loose Sliding Links at Terminations C33 & E33,respectively.Nuts Replaced ML20246F7081989-07-0303 July 1989 Special Rept:On 890601,diesel Generator 1A Shut Down Due to Lack of Oil Flow.Due to Test Being Performed,Normal Stop Would Not Shutdown Engine.New Oil Added & Pumps Primed. Turbocharger Mods Under Investigation ML20247N8841989-05-30030 May 1989 Special Rept:On 890418,vibration & Loose Parts Monitor Failed.Caused by Damaged Cables to Sensors on Each Affected Channel.Vibration & Loose Parts Monitor Will Be Repaired During Next Refueling Outage After New Replacement Received ML20244C6731989-04-0606 April 1989 Special Rept:On 890225,operations Personnel Discovered That Channel 8 of Vibration & Loose Parts Monitoring Sys Had Low Noise Level.Investigation Scheduled to Be Completed During Unit 1 Tube Leak Outage ML20196E8241988-12-0505 December 1988 Special Rept:On 881205,diesel Generator 1B Experienced Invalid Test Failure.Caused by Improper Adjustment of Voltage Regulator Due to Personnel Error.Operations Mgt Will Cover Incident W/Representative from Each Shift ML20196B5211988-11-29029 November 1988 Special Rept:On 881030,Diesel Generator 1B Experienced Invalid Test Failure During Start Attempt 602.Applicable Procedures for Diesel Generator Testing Reviewed & Revised If Necessary ML20195H4901988-11-16016 November 1988 Special Rept:On 881017,diesel Generator 1A Started for Operability Test & Subsequently Tripped.Caused by Loose Wire on Jacket Pump Discharge Pressure Switch.Wire Reterminated & Pressure Switch Calibr ML20205G3401988-10-24024 October 1988 Special Rept:On 880916,Tech Spec 3.7.14.a Violated.Caused by Standby Shutdown Facility Being Inoperable for More than 7 Days Due to Transfer Canal Isolating & Draining Utilizing Weir Gate.Special Order 88-13 Issued ML20151R0971988-07-27027 July 1988 Special Rept:On 880627,diesel Generator 1A Failed to Start within 11 S.Caused by Missing Drain Valve on Starting Air Filter Housing on Right Bank Side of Diesel Engine.Work Request Written to Replace Filter Housing ML20151F4911988-07-22022 July 1988 Special Rept:On 880519,diesel Generator 1A Started for Operability Test & After Operating for 10 Minutes, Automatically Stopped & Declared Inoperable.Caused by Failure to Maintain Lubricating Level in Valve 1LD-7 ML20195J3601988-06-22022 June 1988 Special Rept:On 880323,Train a Safety Injection & Main Steam Sys Isolation Signals Received from Unknown Fault Inside Train a Solid State Protection Sys Logic Cabinet.Cause of Fault Could Not Be Isolated.Cabinet Returned to Svc ML20195J6161988-06-20020 June 1988 Advises That Special Rept Re Diesel Generator 1A Incident on 880519 Will Be Submitted by 880708 Instead of 880620 Due to Unresolved Concerns ML20195G2171988-06-17017 June 1988 Special Rept:On 880518,diesel Generator 1B Experienced Valid Failure.Caused by Fuel & Vol of Trapped Air Shook Debris Loose from Engine Mounted Duplex Fuel Filter.Filter Cartridges Replaced.Preventative Maint Procedure Revised ML20151C7691988-04-0404 April 1988 Ro:Change of Commitment Submitted Re Diesel Generator Turbocharger Rotor Assembly Replacement.Turbocharger Inlet Casings Replaced on All Four Engines W/New Design.Dye Penetrant Testing Will Continue to Be Performed ML20147F4311988-03-0303 March 1988 Special Rept:On 880123,Channels 3,4 & 8 of Vibration & Loose Parts Monitor Had Unusual Noise Level.Cause Not Determined Due to Number of Possible Failures & Location of Components within Plants.Monitor Will Be Repaired During 1988 Outage ML20237D1341987-12-14014 December 1987 Special Rept:On 871108,safe Shutdown Facility RCS Wide Range Transmitter Out of Calibr.Instrument Could Not Be Calibrated.Requisition Initiated for Replacement Transmitter ML20236Q1621987-11-13013 November 1987 Special Rept:On 870816,malfunction of Main Turbine Generator Controls Caused Rapidly Decreasing Main Steam Line Pressure Triggering Safety Injection/Reactor Trip.Safety Injection & Unusual Event Terminated & Repairs Completed on 870821 ML20214S5421987-06-0808 June 1987 Special Rept:On 870503,pressurizer PORV 2NC-34A Automatically Opened Due to Pressure Transient in Rcs.Cause Not Determined.Charging & Letdown Flow Adjusted & Procedures Re Allowable Setpoint Range Revised ML20214G7301987-05-13013 May 1987 Special Rept:On 870407 & 08,complete 18-month Insp Required for Standby Shutdown Diesel Generator Determined Not to Have Been Performed on Time.Caused by Personnel Error.Work Request Will Be Issued Prior to 18-month Due Dates 1999-03-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J1891999-10-0101 October 1999 Safety Evaluation Supporting Exemption from 10CFR54.17(c)re Schedule to Apply for Renewed Operating Licenses ML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20212G1211999-09-22022 September 1999 Safety Evaluation Supporting Amends 188 & 169 to Licenses NPF-9 & NPF-17,respectively ML20212G2671999-09-22022 September 1999 Safety Evaluation Supporting Amends 187 & 168 to Licenses NPF-9 & NPF-17,respectively ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20211P1371999-09-0808 September 1999 Safety Evaluation Supporting Amend 186 to License NPF-9 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis 05000369/LER-1999-001-04, :on 990306,TS SR for Ice Condenser Lower Inlet Doors Was Not Met.Caused by Failure to Recognize That Recorded Valve Was Outside Acceptance Criteria.Mgt Reinforced Expectations for Procedure Performance & Review1999-03-31031 March 1999
- on 990306,TS SR for Ice Condenser Lower Inlet Doors Was Not Met.Caused by Failure to Recognize That Recorded Valve Was Outside Acceptance Criteria.Mgt Reinforced Expectations for Procedure Performance & Review
ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B7991998-09-28028 September 1998 Safety Evaluation Supporting Amends 183 & 165 to Licenses NPF-09 & NPF-17,respectively ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage 05000369/LER-1998-006-02, :on 980812,noncompliance with Ice Condenser TS SR 4.6.5.1b.3 Noted.Caused by Lack of Clear Documentation Re Interpretation of TS SR 4.6.5.1b.3.Submitted TS Amend to Clearly Establish SR & Will Review Ice Condenser TSs1998-09-11011 September 1998
- on 980812,noncompliance with Ice Condenser TS SR 4.6.5.1b.3 Noted.Caused by Lack of Clear Documentation Re Interpretation of TS SR 4.6.5.1b.3.Submitted TS Amend to Clearly Establish SR & Will Review Ice Condenser TSs
1999-09-08
[Table view] |
Text
g a
I Duk 1%nt Company IIO4)8IMUOO AlcGuire Nuclear Station 12700 Hagm Terry R,ad Huntmeille, NC280iS 89M i
i DUKEPOWER November 14, 1990 U.S. Nuclear Regulatory Commission i
Document Control Desk Washington, D.C.
20555
Subject:
McGuire Nuclear Station Unit 1 j
Docket No. 50-369 Voluntary Special Report Gentlement Attached is Voluntary Special Report concerning an incident involving the Standby
-Shutdown' System in which compensatory measures were not established as required by
-l nthe McGuire Physical Security Plan. This' report is being submitted as a Voluntary Special Report. This event is considered to be of no significance with respect to the health and safety of the public, i
Very truly yours, 6
i
/np.tq %
l J
T.L. McConnell i
DVE/ADJ/chl
')
1
]9 Attachment xc:
Mr. S.D. Ebneter Mr, Darl Hood Administrator, Region II' U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation 101 Marietta St., NW, Suite 2900 Washington, D.C. 20555 Atlanta, GA 30323 Mr. P.K. Van Doorn l
INPO Records Center NRC Resident Inspector Suite 1500 McGuire Nuclear Station 1100 circle 75 Parkway Atlanta, GA 30339 M&M Nuclear Consultants 1221 Avenue of the Americas New York, NY 10020 9011260014 9011g4 i
{DR ADOCK 05000369 I
I pdc
(\\
- (.
ji McGUIRE SAFETY REVIEW GROUP INPLANT REVIFW REPORT 1.0 REPORT NUMBER:
90-28 2.0 DATE OF REVIEW: November. 1990 3.0 SUBJECT DESCRIPTION: A review was conducted of the circumstances relating to the incident described on Problem Investigation Report (PIR) 1-M90-0268. The c
specific purpose of the review was to determine the cause of the incident and possible solutions to prevent further problems of the type described by the PIR.
4.0 EVALUATION AND COMMENT:
PIR 1-M90-0268 documented an incident in which
-compensatory measures were not established as required by the McGuire Physical Security Plan (PSP).
4.1 Background
The Standby Shutdown System (SSS) provides an alternate and independent means to_ achieve and_ maintain a Hot Standby condition for one or both units. Through the SSS, capability is maintained for both units to remain in Hot Standby.for a conservative period of three days without damage control measures being implemented.
SSS instrumentation and controls are located in the Standby Shutdown Facility-(SSF). The SSF also contains a Diesel Generator.to provide assured power for SSS operation should external power be lost.
The SSF controls the secondary side volume by utilizing the Auxiliary Feedwater System (CA) Turbine Driven Pump. This supplies feedwater to the-Steam Generators, thereby providing a heat sink for the Reactor. Coolant System-(NC).
The McGuire PSP states that compensatory measures shall be provided during periods when the SSF is considered degraded. The SSS is required to be operable in Modes 1-(Power Operation), 2 (Startup), and 3 (Hot Standby),
{
per Selected Licensee Commitment 16.9.7.
A note is attached to 16.9.7
4..
I
' ' DPC/MNS r
Inplant Riview No. 90-28 Page 2 describing required actions whenever one or more SSS components become j
inoperable, which states:
Note -
THE SRO SHOULD ENSURE THAT SECURITY IS NOTIFIED 10 MINUTES PRIOR TO DECLARIN0 SSS COMPONENTS INOPERABLE (EXAMPLE: TDCA PUMP) OR ASAP IF SSS COMPONENTS ARE DISCOVERED OR RENDERED INOPERABLE SO THAT COMPENSATORY MEASURES CAN BE IN EFFECT WITHIN 10 MINUTES OF THE TIME OF INOPERABILITY. OTHEP. WISE, A 1 HOUR NOTIFICATION TO NRC IS REQUIRED BY SECURITY.
4.2 Description of Event At the start of night shift on October 10,'1990, Instrumentation And
!y Electrical (IAE) personnel arrived ~in the Control R: ~ with three work requests. These work requests involved working on the non-safety related valve operators for valves ICA-36 (Aux Feedwater No. 1 Discharge To Steam L
Generator ID Control) and ICA (Aux Feedwater Pump To Steam tienerator IB i
h Control)'. After talking with the IAE personnel, the Operations (OPS)
Shift Supervisor determined that it would be better to wait until after-2400 (midnight) to start this work. The Shift Manager was contacted and l
all parties agreed to wait until that time.
E 1At approximately 0130 on October 11, 1990, the IAE personnel returned to the Control Room for permission to begin work. The Control Room Senior; Reactor Operator (SRO) determined that the, nature of this work would make the Turbine Driven Auxiliary Feedwater (TDCA) Pump inoperable.
E l}
l At.this time, the Control Room SRO referenced Technical Specification (TS)
L 3.7.1'.2, Auxiliary Feedwater System, to determine the proper action statement requirements. He selected action 'a' as the-appropriate one, Action 'a' states as follows:
p With'one auxiliary feedwater pump inoperable, restore the reanired auxiliary feedwater pumps to-Operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least Hot Standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Hot Shutdown within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
q, DEC/MNS
)
.Inplant Review No. 90 -Page 3 He then referenced page'1,Section IV of tre TS Reference Manual to determine if other systems or components would be affected when the;TDCA pump was declared inoperable. No reference was made to other systems or components. Neither reference used addressed the fact that if the TDCA pump was declared inoperable, the Selected Licensee Commitments Manual should also be consulted.
Subsequently, at 0145, on October 11, 1990, the TDCA pump was declared inoperable.
Approximately twenty minutes later, the OPS Shif t Supervisor returned to the Control Room.- The Control Room SR0' informed him that he had declared-
.,.a-the TDCA pump inoperable. The Shift Supervisor then asked the Control U
Room SRO if he had also consulted the Selected Licensee Commitments Manual. The response was no.
i At that. time, the Shift Supervisor knew that an error had been made and
{
T directed the SRO to reference the Selected Licensee Commitments Manual, item 16.9.7, entitled Standby Shutdown System.
Based on the note attached to the page of 16.9.7, the Control Room SRO Lc
. realized that when he had declared the TDCA pump inoperable, a subsequent i
security notification should have been made.
o L.
At'0222, the Control Room SRO declared the SSF inoperable and notified the-Security Lieutenant of the error. He also informed him that the required-one-hour notification to the NRC had to be made by no later than 0245.
J Security personnel implemented appropriate compensatory actions at 0231.
This involved opening Fire Door 801J and placing constant Security Surveillance at the door. The Security Lieutenant then made the required-one hour notification to the NRC at 0240.
The Shift Manager:was informed of the event, and made appropriate 4
1 notifications.
The NRC Resident Inspector was also notified by Security personnel.
'S 4
DPC/MNS Inplant' Review No. 90-28
- Page 4 It was later determined that this event was not reportable under 10CFR73.71 Appendix G-1.
Therefore, the 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> notification to the NRC was not required.
4.3 Safety Evaluation During the time the SSF was degraded, the area accessed through Fire Door 801J was not provided security compensatory measures as required for approximately 46 minutes. During normal operating conditions when the SSF is not degraded, the equipment in this area is non-vital. When the SSF is degraded, the equipment in this area becomes vital because the equipment is necessary to safely shutdown the pl"at.
Pursuant to the McGuire PSP two levels of security protection are required for areas containing vital' equipment: One level of physical protection and access control for the protected area; and, a second level,of physical protection and access control for areas containing vital equipment within the protected area. This second level of security protection is provided to prevent. personnel inside the protected area from accessing areas containing vital equipment for which they have not been authorized access.
Personnel are allowed access to areas containing' vital equipment on an as needed basis. By limiting the. number of personnel accessing vital equipment, the-probability of insider sabotage is reduced. -During.the 46 minutes.when security protection was not'provided at Fire-Door 801J, the physical protection and access control to the protected area was maintained. Additionally, there were no challenges made to gain access to the protected' area. During the event, there were no ESF actuations or challenges to safety systems that required the use of the SSF to shut down the plant. The plant operated without incident during the: time the required. security compensatory measure was not fulfilled. Therefore, the health and safety of the public and on-site personnel were not affected by this incident.-
-5.0' CONCLUSION This incident is assigned a cause of Inappropriate Action because the required action as specified by the note attached to Selected Licensee Commitment 16.9.7 was omitted. The Control Room SRO failed to recognize the need to consult the
DPC/MNS Inplant Re cew No.-90-28 Page 5 f
Selected. Licensee Commitments Manual when he declared the TDCA Pump inoperable, l
Consequently, the required notification of Security personnel was omitted because the Control Room SRO did not reference the Selected Licensee Commitments Manual.
When questioned, the Control Room SRO involved stated that he had never performed this particular task as an SRO and was, therefore,- unaware of the requirements as specified by the Selected Licensee Commitment.
It should be noted that the Control Room SRO involved had only been promoted to that position four weeks prior to this event.
He also stated that the task was not one that he remembered as being emphasized during training. However, Production' Support Training personnel stated that their lesson plan covers using the Selected Licensee Commitments Manual whenever the TDCA pump is declared inoperable.- Subsequently, the incident has been covered with all appropriate OPS personnel to help preclude recurrence of.similar incidents.
Additionally, a copy of Selected Licensee Commitment 16.9.7, and tite attached note detailing' required actions, has been placed in the TS Reference Manual in '
the Control-Room. This should serve as a reference whenever the TDCA pump is declared inoperable in the' future.
Compliance personnel will evaluate and submit appropriate changes to the Selected Licensee Commitments Manual to clarify appropriate actions required whenever any component of the SSS is declared inoperable.
J6.0 RECOMMENDATIONS: None
7.0 REFERENCES
1.
.McGuire Technical Specification, Section 3.7.1.2, Auxiliary Feedwater
~
-System 2.
lMcGuire Technical Specification Reference Manual, Page 1,Section IV 3.
McGuire Selected Licensee Cossnitments Manual, Item 16.9.7, Standby Shutdown System
'4.
McGuire Senior Reactor Operator's Logbook, Unit 1 5.
McGuire Shift Manager's Logbook, Unit 1 6.
McGuire Technical Specification Action Item Logbook, Unit 1 7.
McGuire Safeguards ENS Event Report, For 10/11/90 at 0222 8.
McGuire Physical Security Plan 9.
- % ire Security Procedure EXAC-15 l
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