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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20151W3521998-09-0808 September 1998 Special Rept 98-01:on 980819,maint Could Not Be Performed on FPS Due to Isolation Boundary Leakage.Caused by Inadequate Info Provided in Fire Impairment Plan.Isolated Portion of FPS Was Returned to Svc ML20148K3721997-06-0909 June 1997 To Special Rept 96-04:on 961011,groundwater Level Was Above 731 Feet for 7 Days.Caused by Precipitation During Previous Week.Verified That No Other Groundwater Monitoring Instruments Were in Alarm ML20148A9881997-05-0101 May 1997 Special Rept 96-04-02:on 970429,groundwater Level at Well Mk GWA-2 Was in Alarm for 7 Days.Caused by Precipitation During Previous Week.Verified That No Other Groundwater Monitoring Instruments Were in Alarm ML20137P0711997-04-0707 April 1997 Special Rept 97-01:on 970226,Peak Accelerometer,1MIMT-5030, Removed Under WO 95092624 as Part of SG Replacement Project. Accelerometer Will Return to Svc Prior to Unit 1 Startup ML20133L6051997-01-0909 January 1997 Special Rept 96-04,Rev 1,groundwater Level at Well Mk GWA-2 Monitored by 2WZLS5060 Was in Alarm for 7 Days.Verified That No Other Groundwater Monitoring Instruments in Alarm ML20134N0261996-11-14014 November 1996 Special Rept:On 961006,groundwater Alarm Was Received & Entered in TS Action Item List for Tracking.Field Survey of Surrounding Areas Was Performed to Verify That No Water Was Percolating to Surface That Would Indicate Pipe Leak ML20116K0331996-08-0909 August 1996 Special Rept 96-03:on 960611,identified Broken Secondary Contact Blocks.Caused by Mishandling of Breakers or over- Torquing of Mounting Bolts.Breaker 2BYA Repaired,Tested & re-installed in Cabinet ML20086G9601995-07-12012 July 1995 Special Rept 95-002:on 950612,turbocharger Failed,As Detected by Excessive Noise & Vibration.Engine Subsequently Secured.Damaged Components Replaced & DG 2A Returned to Operable Status ML20080G4421995-02-0303 February 1995 Special Rept 95-01:on 950104,personnel on Unit 2 Operating in Solid Condition During Fill & Vent of Nc Sys ML20078R7651994-12-15015 December 1994 Special Rept 94-06:on 941012,fatigue Usage to SI Sys Piping by Manually Initiating Flow Through B Cold Leg from Fwst During Testing for Valve 1NI-71 Intentionally Increased. Startup of Facility Discontinued to Repair Valve ML20078L6571994-11-22022 November 1994 Special Rept SR-94-05:on 941024,Channel 3 of Vibration & Loose Parts Monitoring Sys Declared Inoperable Due to Noise.Channel 3 of V&Lpm Will Be Repaired Under WR 94043758 or Replaced by Nsm MG-12096 During Outage 1EOC10 ML20073C2451994-09-14014 September 1994 Special Rept 94-004:on 940821,valid Failure of DG 1A Occurred Due to Failure of Series Boost exciter-regulator (Voltage Regulator).Isolation Transformer T54 & Current Transformers CT1,CT2 & CT3 Will Be Inspected ML20065K2501994-04-15015 April 1994 Special Rept 94-03:on 940210,during Testing PORV Observed to Hang Open in Absence of air-assisted Closure.Caused by Incomplete Testing of Porvs.Compensatory Measures Reanalyzed & Reestablished Addressing Fire & Security Issues ML20064K0311994-03-15015 March 1994 Special Rept 94-01:on 940215,DG 2A Tripped W/Low Lube Oil Pressure Indication During Routine Surveillance Test.Caused by Pressure Too Low in Bldg Up in Sensing Lines.Test Satisfactorily Repeated ML20058M4281993-09-27027 September 1993 Special Rept 93-09:on 930920,notifies of Alarm Condition Showing Alert on Ground Water Level Outside 1A DG Room.Work Order 93063348 Initiated by Wc Personnel to Have Iae Personnel Check Operation & Calibr ML20056F8561993-08-23023 August 1993 Special Rept 93-06:on 930405,discovered Debris on Unit 1 Lower Core Plate.Four Other Unidentified Objects Noted During Video Insp of Lower Core Plate ML20126B5051992-12-15015 December 1992 Inplant Review Rept 92-20,special Rept Re Postulated Scenario That Could Introduce Air Into AFW Suction Piping. Caused by Functional Design Deficiency.Setpoints of Affected Pressure Switches Increased ML20106D7401992-10-0909 October 1992 RO 92-19:on 920804,discovered That Drive Shaft on Pump 1MNVPU0046 Was Rotating in Opposite Direction than Specified on Pump Casing.Caused by Mgt Deficiency.Motor Leads of Subj Pump Reconfigured to Provide Correct Pump Shaft Rotation ML20127E0191992-09-0909 September 1992 Special Rept:On 920421,unusual Event Declared Because Unit 1 Train B of Ssps Inoperable Due to Defective Circuit Card within Ssps.Failed Train B Ssps Circuit Board Replaced & Appropriate Procedures to Be Evaluated ML20101T9441992-07-13013 July 1992 Special Rept for Inplant Review 92-10:on 920610 No Mention Made on Work List of Vent Path Through SG 1B for Incoming SG Crews.Caused by Deficient Communication.Turnover Sheet Established to Document Existing Vent Path Status ML20101P5581992-07-0303 July 1992 In-Plant Review Rept 92-09:on 920619,setpoint Problems Noted W/Ts & Selected Licensee Commitment Values for Listed Field Data.Caused by Discrepancies W/Groundwater Level Monitoring Portion of Wz Sys.Ts Monitor Logged in Unit 2 Logbook ML20086Q1101991-12-20020 December 1991 Voluntary Special Rept 91-23:on 911008,reactor Vessel Lower Internals Contacted Reactor Vessel During Removal.Caused by Inappropriate Operator Action & Mgt Deficiency.Recovery Plan Developed Re Insp of Lower Internals & Refueling Canal ML20086H9431991-12-0404 December 1991 Special Rept 91-24:on 911104-29,concerns Noted Re Possible Leakage of Containment Spray Sys Check Valves Into Annulus, Causing Offsite Radioactive Dose.Caused by Design Deficiency.Check Valve Installed Downstream of Piping ML20091C0851991-08-0101 August 1991 Special Rept PIR 1-M91-0113:on 910616,diesel Engine Cooling Water Leak Discovered on Diesel Generator 1A at Discharge Flange on Intercooler End Bell Cover.Caused by Poor Casting Quality.New Covers Will Be Installed ML20081F7371991-06-0404 June 1991 Rev 1 to Special Rept 91-11 Dtd 910411:on 910215,turbine Driven Auxiliary Feedwater Pumps Automatically Started. Caused by Deficient Communication & Lack of Attention to Detail.Pump Speed Reduced & Discharge Valves Closed ML20062E7991990-11-14014 November 1990 Special Rept:On 901011,turbine Driven Auxiliary Feedwater Pump Declared Inoperable W/O Having Made Security Notification.Caused by Inappropriate Action ML20055G2161990-07-12012 July 1990 Ro:On 900602,discovered That Channel 7 of Vibration & Loose Parts Monitor Sys Had Low Noise Level.Probably Caused by Bad or Damaged Sensor Cable.Definite Cause of Failure Undetermined.Sys Scheduled to Be Replaced ML20043A9761990-05-18018 May 1990 Special Rept:On 900418,diesel Generator 1B Tripped on Overspeed During Start Attempts 688 & 689.Possibly Caused by Test Lead Hookup or Inductive Voltage Spike Preventing Field Flash.Diodes Installed Across Coils in All Five Relays ML20034B9961990-04-19019 April 1990 Corrected Special Rept Re 900303 & 04 Failure of Diesel Generator 1A to Start.Caused by Loose Sliding Links at Terminations C33 & E33.Nuts Replaced ML20034B3111990-04-17017 April 1990 Revised Special Rept:On 900303 & 04,diesel Generator 1A Failed to Start During Start Attempts Due to Failure of Cooling Water High Temp Switch & Loose Sliding Links at Terminations C33 & E33,respectively.Nuts Replaced ML20033H1791990-04-0202 April 1990 Special Rept:On 900303,Diesel Generator 1A Failed to Start During Start Attempt 781.Caused by Failure of Cooling Water High Temp Switch.Similar Event Occurred on 900304.Both Failures Due to Normal Equipment Wear.Temp Switch Replaced ML19332E8171989-11-29029 November 1989 Special Rept:On 891030,diesl Generator 1A Declared Inoperable.Caused by Discovery of Large Fuel Oil Leak from Valve 1FD-83 Vent Hole.New Valve Diaphragm Installed in Valve.On 891106,valve Found Leaking Again & Replaced ML19325F3421989-11-13013 November 1989 Revised Special Rept:On 890914,pressurizer Level Indication in Standby Shutdown Facility Failed Low.Caused by Faulty Pressure Sensing Element.Rept Written to Replace Pressure Transmitters ML19324C1641989-11-0202 November 1989 Revised Special Rept:On 890914,operations Determined That Pressurizer Level Indication in Standby Shutdown Facility Failed Low.Caused by Faulty Pressure Sensing Element.Faulty Transmitter Taken to Vendor for Repair.Transmitter Replaced ML19327B6271989-10-23023 October 1989 Special Rept:On 890909,determined That Pressurizer Level Indication in Standby Shutdown Facility Failed Low.Caused by Faulty Pressure Sensing Element.Faulty Transmitters Taken to Vendor for Repair.Barton Transmitter Installed ML19327A9861989-10-10010 October 1989 Ro:On 890922,loss of Power to Sirens Occurred Due to Power Lines Downed by Hurricane Hugo.Ler Will Be Submitted Re Event ML20246F7081989-07-0303 July 1989 Special Rept:On 890601,diesel Generator 1A Shut Down Due to Lack of Oil Flow.Due to Test Being Performed,Normal Stop Would Not Shutdown Engine.New Oil Added & Pumps Primed. Turbocharger Mods Under Investigation ML20247N8841989-05-30030 May 1989 Special Rept:On 890418,vibration & Loose Parts Monitor Failed.Caused by Damaged Cables to Sensors on Each Affected Channel.Vibration & Loose Parts Monitor Will Be Repaired During Next Refueling Outage After New Replacement Received ML20244C6731989-04-0606 April 1989 Special Rept:On 890225,operations Personnel Discovered That Channel 8 of Vibration & Loose Parts Monitoring Sys Had Low Noise Level.Investigation Scheduled to Be Completed During Unit 1 Tube Leak Outage ML20196E8241988-12-0505 December 1988 Special Rept:On 881205,diesel Generator 1B Experienced Invalid Test Failure.Caused by Improper Adjustment of Voltage Regulator Due to Personnel Error.Operations Mgt Will Cover Incident W/Representative from Each Shift ML20196B5211988-11-29029 November 1988 Special Rept:On 881030,Diesel Generator 1B Experienced Invalid Test Failure During Start Attempt 602.Applicable Procedures for Diesel Generator Testing Reviewed & Revised If Necessary ML20195H4901988-11-16016 November 1988 Special Rept:On 881017,diesel Generator 1A Started for Operability Test & Subsequently Tripped.Caused by Loose Wire on Jacket Pump Discharge Pressure Switch.Wire Reterminated & Pressure Switch Calibr ML20205G3401988-10-24024 October 1988 Special Rept:On 880916,Tech Spec 3.7.14.a Violated.Caused by Standby Shutdown Facility Being Inoperable for More than 7 Days Due to Transfer Canal Isolating & Draining Utilizing Weir Gate.Special Order 88-13 Issued ML20151R0971988-07-27027 July 1988 Special Rept:On 880627,diesel Generator 1A Failed to Start within 11 S.Caused by Missing Drain Valve on Starting Air Filter Housing on Right Bank Side of Diesel Engine.Work Request Written to Replace Filter Housing ML20151F4911988-07-22022 July 1988 Special Rept:On 880519,diesel Generator 1A Started for Operability Test & After Operating for 10 Minutes, Automatically Stopped & Declared Inoperable.Caused by Failure to Maintain Lubricating Level in Valve 1LD-7 ML20195J3601988-06-22022 June 1988 Special Rept:On 880323,Train a Safety Injection & Main Steam Sys Isolation Signals Received from Unknown Fault Inside Train a Solid State Protection Sys Logic Cabinet.Cause of Fault Could Not Be Isolated.Cabinet Returned to Svc ML20195J6161988-06-20020 June 1988 Advises That Special Rept Re Diesel Generator 1A Incident on 880519 Will Be Submitted by 880708 Instead of 880620 Due to Unresolved Concerns 1999-03-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J1891999-10-0101 October 1999 Safety Evaluation Supporting Exemption from 10CFR54.17(c)re Schedule to Apply for Renewed Operating Licenses ML20217G7951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for McGuire Nuclear Station,Units 1 & 2 ML20212G2671999-09-22022 September 1999 Safety Evaluation Supporting Amends 187 & 168 to Licenses NPF-9 & NPF-17,respectively ML20212G1211999-09-22022 September 1999 Safety Evaluation Supporting Amends 188 & 169 to Licenses NPF-9 & NPF-17,respectively ML20217F3661999-09-22022 September 1999 Rev 18 to McGuire Unit 1 Cycle 14 Colr ML20212D1911999-09-20020 September 1999 SER Accepting Exemption from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Closed System Isolation Valves for McGuire Nuclear Station,Units 1 & 2 ML20211P1371999-09-0808 September 1999 Safety Evaluation Supporting Amend 186 to License NPF-9 ML20216E8851999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Units 1 & 2 ML20217G8101999-08-31031 August 1999 Revised Monthly Operating Repts for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211G5261999-08-24024 August 1999 SER Accepting Approval of Second 10-year Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20210S2371999-07-31031 July 1999 Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216E8951999-07-31031 July 1999 Revised Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20209H1631999-06-30030 June 1999 Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20210S2491999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for McGuire Nuclear Station,Units 1 & 2 ML20209H1731999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20195K3691999-05-31031 May 1999 Monthly Operating Repts for May 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20206N3511999-05-11011 May 1999 Safety Evaluation Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Movs ML20206R0891999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20195K3761999-04-30030 April 1999 Revised MORs for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205L2341999-04-0505 April 1999 SFP Criticality Analysis 05000369/LER-1999-001-04, :on 990306,TS SR for Ice Condenser Lower Inlet Doors Was Not Met.Caused by Failure to Recognize That Recorded Valve Was Outside Acceptance Criteria.Mgt Reinforced Expectations for Procedure Performance & Review1999-03-31031 March 1999
- on 990306,TS SR for Ice Condenser Lower Inlet Doors Was Not Met.Caused by Failure to Recognize That Recorded Valve Was Outside Acceptance Criteria.Mgt Reinforced Expectations for Procedure Performance & Review
ML20205P8991999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20206R0931999-03-31031 March 1999 Revised Monthly Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205C4171999-03-25025 March 1999 Special Rept 99-02:on 801027,Commission Approved for publication,10CFR50.48 & 10CFR50 App R Delineating Certain Fire Protection Provisions for Nuclear Power Plants Licensed to Operate Prior to 790101.Team Draft Findings Reviewed ML20207K2051999-03-0505 March 1999 Special Rept 99-01:on 990128,DG Tripped After 2 H of Operation During Loaded Operation for Monthly Test.Caused by Several Components That Were Degraded or Had Intermittent Problems.Parts Were Replaced & Initial Run Was Performed ML20204C8911999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20205P9021999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2 ML20204C8961999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for McGuire Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20199E0301998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for McGuire Nuclear Station,Units 1 & 2 ML20198A4481998-12-11011 December 1998 Safety Evaluation Concluding That for Relief Request 97-004, Parts 1 & 2,ASME Code Exam Requirements Are Impractical. Request for Relief & Alternative Imposed,Granted ML20199E0491998-11-30030 November 1998 Revised Monthly Operating Rept for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198D7561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199E9651998-11-24024 November 1998 Rev 1 to ATI-98-012-T005, DPC Evaluation of McGuire Unit 1 Surveillance Weld Data Credibility ML20196D4171998-11-24024 November 1998 Special Rept 98-02:on 981112,failure to Implement Fire Watches in Rooms Containing Inoperable Fire Barrier Penetrations,Was Determined.Repair of Affected Fire Barriers in Progress ML20196G0581998-11-0606 November 1998 Rev 17 to COLR Cycle 13 for McGuire Unit 1 ML20196G0761998-11-0606 November 1998 Rev 15 to COLR Cycle 12 for McGuire Unit 2 ML20195E5961998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20198D7771998-10-31031 October 1998 Revised Monthly Operating Rept for Oct 1998 for McGuire Nuclear Station,Units 1 & 2 ML20195E6021998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154L6251998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for McGuire Nuclear Station,Units 1 & 2 ML20154B7991998-09-28028 September 1998 Safety Evaluation Supporting Amends 183 & 165 to Licenses NPF-09 & NPF-17,respectively ML20154B4131998-09-22022 September 1998 Rev 0 to ISI Rept for McGuire Nuclear Unit 1 Twelfth Refueling Outage ML20153F6401998-09-22022 September 1998 Safety Evaluation Supporting Amends 182 & 164 to Licenses NPF-9 & NPF-17,respectively 1999-09-08
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DukeIbwerCompany T C McMinn McGuare Nuclear Generatton Department Vice Presodent 12700Hagers ferryRoad(MG01VP)
(104)8754800 Huntenville.NC280782985 (704)8754809 Fax DUKEPOWER February 3,1995 U.S. Nuclear Regulatory Commission Document Control Desk Was.11ngton, D.C. 20555
Subject:
McGuire Nuclear Station Unit 2 Special Report No.: 95-01 Problem investigation Process No.: 2-M95-0034 Gentiemen:
Attached for your information is Special Report No. 95-01, pursuant to requirements of Technical Specification 3.4. 9.3, Reactor Coolant System Overpressure Trotection System, Action e. This report documents actuation of power-operated relief valve 2NC-34 to reduce NC system pressure while operating in a solid condition during the fill and vent of the NC system on Unit 2. This actuation was determined to be appropriate by design to mitigate an increase in NC system pressure at that time. The actuation is not significant from a fatigue standpaint and of no significance with respect to the health and safety of the public.
Very truly yours, NFLN T.C. McMeekin RJD/beb Attachment cc:
Mr. S.D. Ebneter INPO Records Center Administrator, Region 11 Suite 1500 i
U.S. Nuciear Regulatory Commission 1100 Circle 75 Parkway i
101 Marietta St., NW, Suite 2900 Atlanta,GA 30339 Atlanta, GA 30323 Mr. Victor Nerses Mr. George Maxwell j
U.S. Nuclear Regulatory Commission NRC Resident inspector Office of Nuclear Reactor Regulation McGuire Nuclear Station Washington, D.C. 20555 b[(.'[..'
9502070307 950203 PDR ADOCK 05000369 g[
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B.L. Walsh (EC11C)
Zack Taylor (CNS)
G.A. Copp (EC050)
J.l. Glenn (MG02ME)
~ P.R. Herran (MG01VP)
R.C. Norcutt (MG01WC)
S.G. Bonesole (ONS Reg Compliance)
G.H. Savage (EC06E)
G.B. Swindlehurst (EC11-0842)
M.S. Tuckman (EC07H)
R.F. Cole (EC05N)
D.B. Cook (EC13A)
Tim Becker (PB02L)
P.M. Abraham (EC081)
Bruce Caldwell(MG01VP)
L.V. Wilkie (ONO3SR)
D.P. Kimball (CN05SR)
NSRB Support Staff (EC05N)
Kay Crane (MG01RC)
Rich Casler (EC05N) i i
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i DUKE POWER COMPANY McGUIRE NUCLEAR STATION SAFETY REVIEW GROUP SPECIAL REPORT This Special Report is due to requirements of Technical Specification 3.4.9.3, Reactor Coolant System Overpressure Protection Systems, Action e.
This report concerns an actuation of Power-Operated Relief Valve (PORV) 2NC-34, to reduce Reactor Coolant (NC) system pressure while operating in a solid condition during the fill and vent of the NC system on Unit 2.
This occurrence is documented on problem investigation process (PIP) 2-M95-0034.
l Special Report No.: 25-D1 Date Of Report: January 31. 1995 t
i On January 4, 1995, Operations (OPS) personnel on Unit 2 were operatir.g i
in a solid condition during the fill and vent of the NC system.
The unit was in Mode 5 (Cold Shutdown).
System venting had virtually been completed and; therefore, pressure control was very sensitive to any change in NC system mass due to a minimal amount of entrained air in the j
system at that time.
The Reactor Operators (ROs) assigned to Unit 2 stated that they had discussed the need for additional caution with control of NC system pressure and temperature during turnover. With this evolution in mind, OPS Management personnel had assigned an additional RO to assist with the performance of procedures for operation of the Unit 2 Reactor Coolant pumps. This was done in an effort to allow the RO at the controls (ROATC) to devote greater attention to the control of NC system temperature and pressure and the RO assigned to the balance of the plant (BOP)to handle any other items concerning operat,'.on of the unit.
However, as the day progressed, the level of act:Wity concerning Unit 2 became greater and greater due to restart activities in progress. The ROs stated that they were extremely busy. The ROATC as well as the RO i
assigned to the BOP and the additional RO found themselves performing multiple tasks at the same time.
At 1155, the ROATC noted a decrease in NC system pressure to less than 250 psig.
He stated that he then adjusted letdown flow to increase system pressure to approximately 275 psig.
He also stated that he had made an adjustment to the Component Cooling (KC) system flow to increase the NC system temperature.
At that time he was called to assist Instrumentation and Electrical personnel performing testing on the 2A Feedwater (CF) system pump.
Both the RO assigned to the BOP and the additional RO assigned were occupied with support of various other activities in progress at that time and were not monitoring NC system pressure or temperature. At 1204, the annunciator alarm was received for actuation or PORV 2NC-34.
The ROATC stated that the NC system i
pressure had increased to 371 psig as indicated by the control room alarm typer and the PORV had actuated as it should to reduce pressure while in the Low Temperature Overpressure Protection (LTOP) mode.
OPS personnel then took action by adjusting letdown flow to further reduce NC system pressure to within the appropriate limits. The PORV reseated properly when pressure was reduced to a level below the actuation setpoint. OPS personnel were then able to stabilize the NC system pressure and no further problems were noted.
The cycling of 2NC-34 is not significant from a safety or fatigue standpoint.
The Design Stress Report for the PORVs allows for up to 340 1
a cycles.
This limit has not yet been approached.
Also, the Pressurizer Helief Tank (PRT) is designed to withstand a pressure increase of up to 140 psig, at which time the rupture dick would relieve to reduce system pressure.
The PRT pressure did not increase significantly during this time period and no safety systems were challenged as a result.
When interviewed, the OPS personnel involved stated that they attributed the increase in NC syitem pressure to transients introduced by valve manipulations during testing ongoing at that time on the Safety Injection (NI) system check valves and consequent leakage to the check valve test header.
However, investigation into the activities associated with NI check valve testing revealed that there were no valve i
manipulations associated with this testing ongoing at that time.
Personnel involved in the check valve testing stated that they were unable to establish any flow at the time of this occurrence, and could not have induced any transient to the NC system pressure.
j The root cause for the PORV actuation is established as the sensitivity of the NC system pressure to very small changes in system mass as previously described, and the diversion of OPS personnel at the controls from paying strict attention to system pressure and temperature at that i
time.
The level of activities in progress at that time had progressed to the point of pulling the ROs from their original focus as discussed 1
in the turnover. This contributed to the pressure being allowed to increase to the point at which the PORV actuated.
In an effort to prevent recurrence of similar actuations OPS personnel will evaluate the methedology used for assignment of duties in the Control Room during evolutions such as control of NC system pressure and temperature while operating in a solid condition.
Also, in conjunction with System Engineering personnel, OPS personnel will evaluate the uce of additional control or alarm methods to assist the Control Room OPS personnel in their duties during such evolutions.
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