|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20209H6921999-07-15015 July 1999 Forwards Comments on Preliminary Accident Sequence Precursor Analysis Provided in NRC Re Operational Condition Reported in LER 269/1998-04 ML20195H1681999-06-10010 June 1999 Forwards Copy of Preliminary ASP Analysis of Operational Condition Discovered at Ons,Units 1,2 & 3 on 980212 & Reported in LER 269/98-004,for Review & Comment ML20207C0321999-05-18018 May 1999 Forwards Fifth Rept Which Covers Month of Apr 1999. Commission Approved Transfer of TMI-1 Operating License from Gpu to Amergen & Transfer of Operating License for Pilgrim Station from Beco to Entergy Nuclear Generating Co ML20206E4101999-04-26026 April 1999 Forwards Four Copies of Rev 9 Todpc Nuclear Security & Contingency Plan,Per 10CFR50.54(p)(2).Changes Do Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR73.21 ML20205T1301999-04-0909 April 1999 Informs That on 990317,C Efin & Ho Christensen Confirmed Initial Operator Licensing Exam Schedule for Y2K.Initial Exam Dates Scheduled for Wks of 000710 & 17 for Approx 13 Candidates ML20205B0571999-03-24024 March 1999 Informs That Author Determined That Partial Exemption from 10CFR170 Fee Requirements Appropriate for Footnote 4 of Review of License Renewal Application for Ons,Units 1,2 & 3, That Staff Determines Has Generic Value to Industry ML20207C0501999-02-25025 February 1999 Submits Annual Rept Specifying Quantity of Each of Principal Radionuclides Released to Environment in Liquid & Gaseous Effluents,Per 10CFR72.44(d)(3).Effluent Release from ISFSI for CY98 Was Zero ML20202H7621999-01-28028 January 1999 Discusses Guidance Re License Renewal for Operating Power Reactors Developed in Response to FY99 Energy & Water Development Appropriations Act Rept 105-581 ML20202J1901999-01-28028 January 1999 Discusses License Renewal for Operating Power Reactors.Two Applications Received for Renewing Operating Licenses. Commission Established Adjudicatory Schedule Aimed at Completing License Renewal Process in 30-36 Months ML20198Q8871999-01-0707 January 1999 Responds to to Chairman SA Jackson Re Issues for Consideration for Commission During Oconee License Renewal Process.Commissioners Must Remain Impartial During Pendency of Case.Copy of Order LBP-98-33 Encl.Served on 990107 ML20198S8721999-01-0707 January 1999 Responds to Message to Marks Re Info Request on Appeal Deadline & Desire to Serve Appeal Either by e-mail or by Alternative Regular Mail ML20198Q8971998-12-17017 December 1998 Expresses Concerns Re License Renewal of Duke Energy,Oconee Nuclear Station,Units 1,2 & 3.Commends NRC on Steps Agency Has Undertaken to Conclude Renewal Process.With Certificate of Svc.Served on 990107 05000269/LER-1998-012, Forwards LER 98-012-01,re RB Spray Pumps Being Declared Inoperable Due to Npsh.Rept Has Been Revised to Indicate Results of Testing & Corrective Actions Taken to Date1998-12-0303 December 1998 Forwards LER 98-012-01,re RB Spray Pumps Being Declared Inoperable Due to Npsh.Rept Has Been Revised to Indicate Results of Testing & Corrective Actions Taken to Date 05000269/LER-1998-013, Forwards LER 98-013-00 Re Condition Prohibited by Ts,Per 10CFR50.73(a)(1)(d).Circumstances & Causes for Event Have Not Been Fully Determined & Will Be Provided in Supplemental LER on or Before 9812021998-11-0202 November 1998 Forwards LER 98-013-00 Re Condition Prohibited by Ts,Per 10CFR50.73(a)(1)(d).Circumstances & Causes for Event Have Not Been Fully Determined & Will Be Provided in Supplemental LER on or Before 981202 ML20155D2651998-10-23023 October 1998 Expresses Appreciation for Supporting Commission Initiative in Issuing Recent Statement of Policy on Conduct of Adjudicatory Proceedings.Case-specific Orders Were Issued in Calvert Cliffs & Oconee License Renewal Proceedings ML20155B1481998-10-21021 October 1998 Informs That as Result of Discussion of Issues Re Recent Events in Ice Condenser Industry,Ice Condenser Mini-Group (Icmg),Decided to Focus Efforts on Review & Potential Rev of Ice condenser-related TS in Order to Clarify Issues ML20154B9421998-09-30030 September 1998 Amends Chattooga River Watershed Coalition Petition to Intervene in Proceedings Re Application of Duke Energy Corp to Renew OLs for Oconee Nuclear Station,Units 1,2 & 3 ML20154A8971998-09-30030 September 1998 Requests That Submitted Info Be Attached to Amends to Petition to Intervene in Proceedings Re Application of Duke Energy Corp to Renew Operating Licenses for Units 1,2 & 3 ML20153H6881998-09-27027 September 1998 Requests Consideration of Motion to Enlarge Time Required to Submit Amended Petition to Intervene in Proceeding Re Application of Duke Energy Corp to Renew OLs for Facilities ML20153E4721998-09-24024 September 1998 Forwards Notices of Appearances for Attorneys Representing Duke Energy Corp,Applicant in Proceeding for License Renewal of Oconee Units 1,2 & 3.With Certificate of Svc ML20153D1831998-09-17017 September 1998 Ack Receipt of of Duke Energy Co Inviting Reconsideration of Denial by NRC CFO of Duke Exemption Request from Annual Fee Requirements for General License Under 10CFR171.11(d) ML20151S7501998-08-31031 August 1998 Provides Update on Commitment Made by Licensee in Response to NOV & Imposition of Civil Penalty Re Valves in Ldst Instrument Lines That Were Incorrectly Translated Into Station Procedures ML20237B0871998-08-11011 August 1998 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 981007.Sample Registration Ltr Encl ML20236V9581998-07-27027 July 1998 Forwards Corrected Pages 3.5-30b of 961211 & 3.16-2 of 970205 TS Bases.Old Amend Numbers Were Left on Pages.Rev Changes Footer on Both Pages to Reflect Bases Changes ML20236P9451998-07-15015 July 1998 Forwards Emergency Response Data Sys Implementation Documents Including Data Point Library Updates for Oconee (Number 255),Dresden (Number 257) & Susquehanna (Number 258) ML20153D1961998-07-0909 July 1998 Requests NRC Reconsider & Grant Util Request for Exemption from Duplicative License Fee Under 10CFR171.11(d) for Storage of Spent Nuclear Fuel at Oconee Nuclear Station ML20236J9871998-06-24024 June 1998 First Final Response to FOIA Request for Documents.Documents Listed in App a Already Available in Pdr.Documents Listed in App B Being Released in Entirety ML20247G0881998-05-14014 May 1998 Provides Rev 2 to Section 3.3, Instrumentation, in Support of TS-362 Amend Request.Position on Testing of Analog Trip Type Instruments W/Regard to Transition from CTS to ITS, Restated.Summary Description of Its/Bases Changes,Encl 05000269/LER-1998-002, Forwards LER 98-002-01 Re non-isolable Weld Leak on Pressurizer Surge Line Drain Pipe Which Resulted in Unit Shutdown1998-04-30030 April 1998 Forwards LER 98-002-01 Re non-isolable Weld Leak on Pressurizer Surge Line Drain Pipe Which Resulted in Unit Shutdown ML20217G0351998-03-26026 March 1998 Submits Ltr to Update Commitment Made by Oconee in Response to Subject Violation.Update Assures That Details of Particular CA Are Appropriately Contained in Docketed Correspondence ML20203J9301998-02-26026 February 1998 Submits Response to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs. Suppl 1 to Bulletin Attached & Contains Listed Commitments ML20199J7441998-02-0202 February 1998 Responds to NRC Bulletin 96-004 for NUHOMS-24P Sf Storage Sys Used at Plant Site.Nrc Reviewed Response & Found Response to Be Acceptable ML20198K9321998-01-13013 January 1998 Ack Receipt of Requesting Exemption from 10CFR171 for ISFSI License SNM-2503 & General License Provisions of 72.214 ML20198M9361998-01-12012 January 1998 Responds to Request That rept,BAW-2303P,rev 3 Be Considered Exempt from Mandatory Public Disclosure.Determined That Info Sought to Be Withheld Contains Proprietary Commercial Info & Will Be Withheld from Public Disclosure ML20203C8481997-12-10010 December 1997 Forwards Emergency Response Data Sys Implementation Documents for Plants.W/O Encl 05000269/LER-1997-003, Forwards LER 97-003-01 Re post-LOCA Boron Dilution Design Basis Not Being Met.Rept Includes Updated Info & Revised Corrective Action1997-11-12012 November 1997 Forwards LER 97-003-01 Re post-LOCA Boron Dilution Design Basis Not Being Met.Rept Includes Updated Info & Revised Corrective Action ML20198Q5741997-11-0303 November 1997 Provides Suppl to Initial 971020 Application for Amend to TS Re SG Tubing Surveillance Requirements,In Response to NRC 971030 Request for Addl Info.Proprietary Rev 3 to BAW-2303P, OTSG Repair Roll Qualification Rept Encl.Rept Withheld ML20211P1591997-10-17017 October 1997 Ack Receipt of & Check for $330,000 in Payment for Civil Penalty.Corrective Actions Will Be Examined During Future Insp ML20217D7261997-10-0101 October 1997 Informs That Staff Intends to Use Working Draft SRP-LR as Aid in Reviewing License Renewal Submittals Received from Dpc,Other Licensees & Owners Groups.Policy Issues Will Be Referred to Commission for Resolution ML20211F7981997-09-25025 September 1997 Submits Response to Violations Noted in Insp Repts 50-269/97-10,50-270/97-10 & 50-287/97-10 & Proposed Imposition of Civil Penalty in Amount of $330,000.Corrective Actions:Ldst Instrument Mods on All Three Units Completed ML20217D9341997-09-22022 September 1997 Informs That NRC Staff Has Accepted Deferral of Completion of Certain Actions Requested by Bulletin 96-03, Potential of Plugging of ECCS Strainers by Debris in Boiling Water Reactor ML20211C8021997-09-18018 September 1997 Forwards Revised TS Amend Re Reactor Bldg Structural Integrity.Previously Submitted TSs Contained Editorial Error ML20216G5821997-09-0404 September 1997 Informs That 970730 Submittal Re Oconee Nuclear Station, Units 1,2 & 3 Will Be Marked Proprietary & Being Withheld Per 10CFR2.790(b)(5) & Section 103(b) of AEC Act of 1954 ML20210T7121997-09-0404 September 1997 Informs That Representatives from Oconee Who Compose LERs Would Like to Meet W/Staff & AEOD at Convenient Place & Time to Facilitate Process.Concerns Addressed in Encl IR 05000269/19970071997-08-27027 August 1997 Discusses Insp Repts 50-269/97-07,50-270/97-07,50-287/97-07, 50-269/97-08,50-270/97-08 & 50-287/97-08 on 970606 & Forwards Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $330,000 ML20210M8381997-08-13013 August 1997 Confirms Conversation Between J Burchfield & R Carroll on 970807 Re Mgt Meeting to Be Conducted in Region II Ofc on 971113.Meeting to Discuss Status of Plant Performance Improvement Initiatives ML20210N1531997-08-13013 August 1997 Confirms 970807 Telcon Between J Burchfield & R Carroll Re Management Meeting to Be Conducted at Oconee Nuclear Station on 970922.Purpose of Meeting to Discuss Oconee Emergency Power Project Initiatives ML20210N1121997-08-12012 August 1997 Informs That NRC Plans to Administer Generic Fundamentals Exam Section of Written Operator Licensing Exam on 971008. Facililty Must Submit Either Ltr Indicating No Candidates Scheduled to Participate or Listing Names of Candidates ML20149J4841997-07-21021 July 1997 Forwards Addl Pages to Rev 5 to Duke Power Co Nuclear Security & Contingency Plan. Encl Withheld 1999-08-10
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20209H6921999-07-15015 July 1999 Forwards Comments on Preliminary Accident Sequence Precursor Analysis Provided in NRC Re Operational Condition Reported in LER 269/1998-04 ML20206E4101999-04-26026 April 1999 Forwards Four Copies of Rev 9 Todpc Nuclear Security & Contingency Plan,Per 10CFR50.54(p)(2).Changes Do Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR73.21 ML20207C0501999-02-25025 February 1999 Submits Annual Rept Specifying Quantity of Each of Principal Radionuclides Released to Environment in Liquid & Gaseous Effluents,Per 10CFR72.44(d)(3).Effluent Release from ISFSI for CY98 Was Zero ML20198Q8971998-12-17017 December 1998 Expresses Concerns Re License Renewal of Duke Energy,Oconee Nuclear Station,Units 1,2 & 3.Commends NRC on Steps Agency Has Undertaken to Conclude Renewal Process.With Certificate of Svc.Served on 990107 05000269/LER-1998-012, Forwards LER 98-012-01,re RB Spray Pumps Being Declared Inoperable Due to Npsh.Rept Has Been Revised to Indicate Results of Testing & Corrective Actions Taken to Date1998-12-0303 December 1998 Forwards LER 98-012-01,re RB Spray Pumps Being Declared Inoperable Due to Npsh.Rept Has Been Revised to Indicate Results of Testing & Corrective Actions Taken to Date 05000269/LER-1998-013, Forwards LER 98-013-00 Re Condition Prohibited by Ts,Per 10CFR50.73(a)(1)(d).Circumstances & Causes for Event Have Not Been Fully Determined & Will Be Provided in Supplemental LER on or Before 9812021998-11-0202 November 1998 Forwards LER 98-013-00 Re Condition Prohibited by Ts,Per 10CFR50.73(a)(1)(d).Circumstances & Causes for Event Have Not Been Fully Determined & Will Be Provided in Supplemental LER on or Before 981202 ML20155B1481998-10-21021 October 1998 Informs That as Result of Discussion of Issues Re Recent Events in Ice Condenser Industry,Ice Condenser Mini-Group (Icmg),Decided to Focus Efforts on Review & Potential Rev of Ice condenser-related TS in Order to Clarify Issues ML20154B9421998-09-30030 September 1998 Amends Chattooga River Watershed Coalition Petition to Intervene in Proceedings Re Application of Duke Energy Corp to Renew OLs for Oconee Nuclear Station,Units 1,2 & 3 ML20154A8971998-09-30030 September 1998 Requests That Submitted Info Be Attached to Amends to Petition to Intervene in Proceedings Re Application of Duke Energy Corp to Renew Operating Licenses for Units 1,2 & 3 ML20153H6881998-09-27027 September 1998 Requests Consideration of Motion to Enlarge Time Required to Submit Amended Petition to Intervene in Proceeding Re Application of Duke Energy Corp to Renew OLs for Facilities ML20153E4721998-09-24024 September 1998 Forwards Notices of Appearances for Attorneys Representing Duke Energy Corp,Applicant in Proceeding for License Renewal of Oconee Units 1,2 & 3.With Certificate of Svc ML20151S7501998-08-31031 August 1998 Provides Update on Commitment Made by Licensee in Response to NOV & Imposition of Civil Penalty Re Valves in Ldst Instrument Lines That Were Incorrectly Translated Into Station Procedures ML20236V9581998-07-27027 July 1998 Forwards Corrected Pages 3.5-30b of 961211 & 3.16-2 of 970205 TS Bases.Old Amend Numbers Were Left on Pages.Rev Changes Footer on Both Pages to Reflect Bases Changes ML20153D1961998-07-0909 July 1998 Requests NRC Reconsider & Grant Util Request for Exemption from Duplicative License Fee Under 10CFR171.11(d) for Storage of Spent Nuclear Fuel at Oconee Nuclear Station ML20247G0881998-05-14014 May 1998 Provides Rev 2 to Section 3.3, Instrumentation, in Support of TS-362 Amend Request.Position on Testing of Analog Trip Type Instruments W/Regard to Transition from CTS to ITS, Restated.Summary Description of Its/Bases Changes,Encl 05000269/LER-1998-002, Forwards LER 98-002-01 Re non-isolable Weld Leak on Pressurizer Surge Line Drain Pipe Which Resulted in Unit Shutdown1998-04-30030 April 1998 Forwards LER 98-002-01 Re non-isolable Weld Leak on Pressurizer Surge Line Drain Pipe Which Resulted in Unit Shutdown ML20217G0351998-03-26026 March 1998 Submits Ltr to Update Commitment Made by Oconee in Response to Subject Violation.Update Assures That Details of Particular CA Are Appropriately Contained in Docketed Correspondence ML20203J9301998-02-26026 February 1998 Submits Response to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs. Suppl 1 to Bulletin Attached & Contains Listed Commitments 05000269/LER-1997-003, Forwards LER 97-003-01 Re post-LOCA Boron Dilution Design Basis Not Being Met.Rept Includes Updated Info & Revised Corrective Action1997-11-12012 November 1997 Forwards LER 97-003-01 Re post-LOCA Boron Dilution Design Basis Not Being Met.Rept Includes Updated Info & Revised Corrective Action ML20198Q5741997-11-0303 November 1997 Provides Suppl to Initial 971020 Application for Amend to TS Re SG Tubing Surveillance Requirements,In Response to NRC 971030 Request for Addl Info.Proprietary Rev 3 to BAW-2303P, OTSG Repair Roll Qualification Rept Encl.Rept Withheld ML20211F7981997-09-25025 September 1997 Submits Response to Violations Noted in Insp Repts 50-269/97-10,50-270/97-10 & 50-287/97-10 & Proposed Imposition of Civil Penalty in Amount of $330,000.Corrective Actions:Ldst Instrument Mods on All Three Units Completed ML20211C8021997-09-18018 September 1997 Forwards Revised TS Amend Re Reactor Bldg Structural Integrity.Previously Submitted TSs Contained Editorial Error ML20210T7121997-09-0404 September 1997 Informs That Representatives from Oconee Who Compose LERs Would Like to Meet W/Staff & AEOD at Convenient Place & Time to Facilitate Process.Concerns Addressed in Encl ML20149J4841997-07-21021 July 1997 Forwards Addl Pages to Rev 5 to Duke Power Co Nuclear Security & Contingency Plan. Encl Withheld ML20141F1381997-06-25025 June 1997 Forwards Rev 4 to Nuclear Security Training & Qualification Plan, Per 10CFR50.4 ML20140C9531997-06-0303 June 1997 Requests NRC Approval of Amend to Oconee ISFSI to Obtain Commission Approval of Proposed Rev 6 to Encl Physical Security Plan.W/O Encls ML20148C8621997-05-22022 May 1997 Informs That TR BAW-2241P Will Be Ref in Future Submittals of P/T Limit Curve Revs for B&W Plants as Result of 970519 Telcon Between L Lois & J Taylor ML20141K1981997-05-19019 May 1997 Forwards Rev 6 to Duke Power Co Nuclear Security & Contingency Plan.Encl Withheld,Per 10CFR73.21 ML20138G8981997-04-30030 April 1997 Forwards Rev 5 to DPC Security & Contingency Plan.Encl Withheld ML20138B3421997-04-22022 April 1997 Submits Response to Request for Addl Info Re Proposed Amend to Reactor Bldg Structural Integrity Tech Specs.Info Provided in Attachments 2 & 3 Supersedes Revised Pages & Markup Pages in Attachment 1 & 2,respectively ML20137N0231997-03-26026 March 1997 Forwards Revised TS 3.1.6 Bases Pages Deleting Detection Time of Reactor Bldg Air Particulate Monitor for RCS Leak of 1 Gpm ML20137B4731997-03-12012 March 1997 Forwards Rev 3 to Security Training & Qualification Plan.Rev Withheld,Per 10CFR73.21 ML20134P3831997-02-18018 February 1997 Submits Clarification of Design Basis Requirements at ONS for Permanently Installed Insulation in Response to NRC Bulletin 93-002, Debris Plugging of Emergency Core Cooling Suction Strainers ML20138L2101997-02-14014 February 1997 Forwards Monthly Operating Repts for Jan 1997 for Oconee Nuclear Station,Units 1,2 & 3 & Revised Monthly Operating Status Repts for Dec 1996 ML20134G5511997-02-0404 February 1997 Requests Exemption to Requirements of 10CFR70.24 Re Criticality Accident Monitoring,Per 10CFR70.14(a) & 70.24(d) ML20133M5971997-01-13013 January 1997 Forwards Revs to Oconee Selected Licensee Commitments Manual ML20138G8411996-12-26026 December 1996 Submits Supplementatl Info Re Emergency Power Engineered Safeguards Functional Test Amend Request ML20132F0911996-12-17017 December 1996 Forwards Response to 961212 & 13 Telcons Re Amend to Licenses for Proposed Changes to Updated Final Safety Analysis Rept Re one-time Emergency Power Engineered Safeguards Functional Test 05000269/LER-1996-008, Forwards Suppl to LER 96-008 Concerning Missed Valve Surveillance Which Resulted in Borated Water Storage Tank Technical Inoperability1996-10-31031 October 1996 Forwards Suppl to LER 96-008 Concerning Missed Valve Surveillance Which Resulted in Borated Water Storage Tank Technical Inoperability ML20134H2231996-10-30030 October 1996 Forwards Revised TS 3.7 Bases,Indicating Info Deleted ML20129B2571996-10-16016 October 1996 Submits Addl Info Re 960220 Application for Amends to Licenses DPR-38,DPR-47 & DPR-55 Concerning Proposed Rev to Chemistry TS Sections 3.1.5,3.1.10 & 4.1,in Response to NRC Telcon Request.Revised TS Pages Encl ML20128H2731996-09-19019 September 1996 Forwards Public Version of Rev 96-06 to Plant Emergency plan.W/961003 Release Memo ML20117D5691996-08-23023 August 1996 Requests Exemption for Ons,Units 1 & 2 & Cns,Units 1 & 2 Iaw/Provisions of 10CFR73.5, Requirements for Physical Protection of Licensed Activities in Nuclear Power Reactors Against Radiological Sabotage ML20116F0051996-08-0101 August 1996 Forwards Corrected Page for Proposed Amend to TS Re Removal of Es Signal from Valves LPSW-4 & LPSW-5 ML20117E6031996-06-26026 June 1996 Forwards Public Version of Change 2 to RP/0/B/1000/01, Emergency Classification & Change 4 to RP/0/B/1000/22, Procedures for Site Fire Damage Assessment & Repair ML20112A0581996-05-14014 May 1996 Responds to NRC Bulletin 96-002, Movement of Heavy Loads Over Spent Fuel,Over Fuel in Reactor Core or Over Safety-Related Equipment ML20115C4371996-05-13013 May 1996 Responds to NRC Bulletin 96-02, Movement of Heavy Loads Over Spent Fuel,Over Fuel in Reactor Core,Or Over Safety-Related Equipment, ML20117D4931996-04-24024 April 1996 Submits Clarification of Reporting Requirements Under 10CFR50.72(b)(2)(vi) ML20107K4991996-04-19019 April 1996 Forwards Rev 2 to Security Training & Qualification Plan. Changes Identified in Rev 2 Do Not Decrease Effectiveness of Plan & Thereby Submitted,Per 10CFR50.54(p),(2).Rev Withheld, Per 10CFR73.21 ML20108D6461996-04-18018 April 1996 Forwards Public Version of Rev 96-05 to Vol C of Epips, Including Emergency Telephone Directory Dtd March 1996 & Change to RP/0/B/1000/20, EOF Director Procedure 1999-07-15
[Table view] Category:UTILITY TO NRC
MONTHYEARML16259A2391990-08-22022 August 1990 Forwards Public Version of Rev 27 to Company Crisis Mgt Implementing Procedure CMIP-2, News Group Plan. W/ Dh Grimsley 900906 Release Memo ML20059C1201990-08-20020 August 1990 Forwards Rept Summarizing Util Findings Re Three False Negative Blind Performance Urine Drug Screens Which Occurred During Jan & Feb 1990.Recommends That NRC Consider Generic Communication to Clearly State Reporting Requirement ML20063Q2671990-08-14014 August 1990 Forwards Public Version of Revised Crisis Mgt Implementing Procedures,Including Rev 36 to CMIP-1,Rev 32 to CMIP-4,Rev 36 to CMIP-5,Rev 41 to CMIP-6,Rev 40 to CMIP-7,Rev 27 to CMIP-8 & Rev 35 to CMIP-9.W/DH Grimsley 900821 Release Memo ML20055C9851990-06-25025 June 1990 Forwards Rev 9 to Training & Qualification Plan.Rev Withheld ML16152A9841990-06-19019 June 1990 Forwards Revised Public Version of Rev 90-03 to Vol B of Epips,Including CP/2/A/2002/04C, Operating Procedure for Post-Accident Liquid Sampling, & Maint Directive 8.1 ML16152A9821990-06-14014 June 1990 Forwards Public Version of Rev 90-02 to Vol B to Oconee Nuclear Station Epips. W/Dh Grimsley 900627 Release Memo ML20044A4491990-06-14014 June 1990 Forwards Public Version of Rev 90-05 to Vol C to EPIP Manual. W/Dh Grimsley 900627 Release Memo ML20043E2571990-05-31031 May 1990 Forwards Request for Relief 90-01 from Requirements of Section XI of ASME Boiler & Pressure Vessel Code Re Inservice Insp During Second 10-yr Interval ML20043F4761990-05-30030 May 1990 Forwards Public Version of Revised Crisis Mgt Implementing Procedures,Consisting of Rev 20 to CMIP-13 & Deletion of CMIP-15 & CMIP-17.W/900612 Release Memo ML20043A5441990-05-16016 May 1990 Discusses Status of Safety & Performance Improvement Program Portion of B&W Owners Group EOP Review Project ML16152A9621990-05-0909 May 1990 Forwards Public Version of Revised Crisis Mgt Implementing Procedures,Including Rev 35 to CMIP-1,Rev 26 to CMIP-2,Rev 31 to CMIP-4,Rev 35 to CMIP-5,Rev 40 to CMIP-6,Rev 39 to CMIP-7 & Rev 26 to CMIP-8.W/DH Grimsley 900517 Release Memo ML16152A9531990-05-0202 May 1990 Forwards Proprietary DPC-NE-2000P-A & Nonproprietary DPC-NE-2000-A, DCHF-1 Correlation for Predicting Heat Flux in Mixing Vane Grid Fuel Assemblies. Proprietary Rept Withheld ML20042H0321990-04-30030 April 1990 Forwards Public Version of Rev 90-04 to Vol C to EPIP Manual ML15217A1051990-03-26026 March 1990 Forwards Revised 1989 Annual Radiological Environ Operating Rept,Consisting of Revised Pages Summarizing Annual Liquid Dose Calculations ML20012D6941990-03-21021 March 1990 Advises of No Human Engineering Discrepancy Mods of Safety Significance for Overall Operation of Plant,Per 880420 Commitment ML16152A9411990-03-14014 March 1990 Forwards Public Version of Rev 90-01 (Vol a) to Emergency Plan Manual & Revs 90-01 (Vol B) & 90-03 (Vol C) to EPIP Manual.W/Dh Grimsley 900329 Release Memo ML20012B3741990-03-0101 March 1990 Requests Extension to Respond to Generic Ltr 90-01 Re Participation in Regulatory Impact Survey Until 900402.Util in Process of Completing Questionnaires for All Units ML17347B5881990-03-0101 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey. Info Covers Time Spent by Key Power Plant Managers in Responding to Operational Insps & Audits ML15217A1031990-02-28028 February 1990 Forwards Semiannual Radioactive Effluent Release Rept for Jul-Dec 1989 for McGuire Nuclear Station Units 1 & 2 & Revised Process Control Programs & Offsite Dose Calculation Manuals ML18094B3221990-02-28028 February 1990 Forwards Executed Amend 14 to Indemnity Agreement B-74 ML20011F3821990-02-26026 February 1990 Confirms Amount Electronically Transferred to Us Dept of Treasury,Nrc on 900223 for Payment of NRC Review Fees of 10CFR50 Applications & 10CFR55 Svcs Per 10CFR170,for Period of 890101-0617 for Listed Invoices ML20006G0621990-02-22022 February 1990 Forwards Revised Proprietary Pages to DPC-NE-2004, Core Thermal Hydraulic Methodology Using VIPRE-01, Reflecting Minor Methodology Changes Made During Review & Approval Process.Pages Withheld ML20012B4541990-02-21021 February 1990 Forwards Public Version of Vol C to Rev 90-02 to EPIP Manuals ML20012B3661990-02-21021 February 1990 Forwards Rev 1 to Cycle 12 Reload Rept,Changing Assumed RCS Flow & Correcting Typo ML20012B1691990-02-19019 February 1990 Forwards Public Version of Crisis Mgt Implementing Procedures,Including Rev 34 to CMIP-1,Rev 25 to CMIP-2, Rev 30 to CMIP-4,Rev 34 to CMIP-5,Rev 39 to CMIP-5 & Rev 38 to CMIP-7 ML20006E1441990-02-16016 February 1990 Forwards Suppl to Rev 1 to Updated FSAR for Braidwood Station,Units 1 & 2 & Byron Station,Units 1 & 2,per 881214 & 891214 Submittals ML20006E9071990-02-16016 February 1990 Discusses Plants Design Control Program.Util Adopted Concept of Design Change Implementation Package (Dcip).Dcip Will Contain or Ref Design Change Notice Prepared Per Approved Procedures ML20006E4201990-02-14014 February 1990 Requests NRC Approval for Use of Alloy 690 Steam Generator Tube Plugs for Facility,Prior to 900301,pending Final ASME Approval of Code Case for Alloy 690 ML20011E6151990-02-12012 February 1990 Forwards Revs 1 to Security Plan & Security Training & Qualification Plan & Rev 2 to Security Contingency Plan. Salem Switchyard Project Delayed.Revs Withheld (Ref 10CFR73.21) ML20011E4991990-02-0606 February 1990 Discusses Liability & Funding Requirements Re NRC Decommissioning Funding Rules & Verifies Understanding of Rules.Ltr from NRC Explaining Liability & Requirements of Rule Requested ML20006D6911990-02-0202 February 1990 Provides Alternative Design Solution to Dcrdr Implementation at Facilities.Simpler Design Devised,Using Eyelet Screw Inserted in Switch Nameplate Which Is Identical to Providing Caution Cards in Close Proximity to Switch Handle ML20006C5661990-01-31031 January 1990 Provides Certification Re Implementation of Fitness for Duty Program Per 10CFR26 at Plants ML20011E2521990-01-29029 January 1990 Forwards Proprietary Safety Analysis Physics Parameters & Multidimensional Reactor Transients Methodology. Three Repts Describing EPRI Computer Code Also Encl.Proprietary Rept Withheld (Ref 10CFR2.790) ML20006D6611990-01-29029 January 1990 Advises That 900117 License Amend Request to Remove Certain cycle-specific Parameter Limits from Tech Specs Inadvertently Utilized Outdated Tech Specs Pages.Requests That Tech Specs Changes Made Via Amends 101/83 Be Deleted ML20006C6711990-01-29029 January 1990 Responds to Generic Ltr 89-13, Svc Water Sys Problems Affecting Safety-Related Equipment. Plants Have Established Preventive Maint Program for Intake Structure & Routine Treatment of Svc Water Sys W/Biocide to Control Biofouling ML20006B7961990-01-29029 January 1990 Forwards Summaries of Latest ECCS Evaluation Model Changes ML18153C0951990-01-29029 January 1990 Forwards Response to Generic Ltr 89-13, Svc Water Sys Problems Affecting Safety-Related Equipment. Belief in Appropriateness to Address Generic Ltr 89-13 Concerns within Context of Established Programmatic Improvements Noted ML20006D2431990-01-26026 January 1990 Provides Info Re Emergency Response Organization Exercises for Plants.Exercises & Callouts Would Necessitate Activation of Combined Emergency Operations Facility Approx Eight Times Per Yr,W/Some Being Performed off-hours & Unannounced ML18094B2861990-01-26026 January 1990 Forwards Response to Generic Ltr 89-13, Svc Water Problems Affecting Safety-Related Equipment. Aggressive Program of Monitoring,Insp & Matl Replacement Initiated in Advance of Generic Ltr 89-13 Issuance ML18153C0871990-01-26026 January 1990 Responds to NRC Bulletin 89-003, Potential Loss of Required Shutdown Margin During Refueling Operations. Refueling Procedures to Be Revised & Familiarization Sessions Will Be Conducted Prior to Each Refueling Outage ML17347B5451990-01-24024 January 1990 Informs of Plans to Apply ASME Code Case N-356 at Plants to Allow Certification Period to Be Extended to 5 Yrs.Rev to Inservice Insp Programs Will Include Use of Code Case ML19354E6711990-01-24024 January 1990 Requests Approval to Use Alloy 690 Plugs as Alternative to Requirements of 10CFR55(a),codes & Stds for Plants Prior to 900226 ML20006C7181990-01-22022 January 1990 Forwards Rev 30 to Security Plan.W/O Encl ML19354E4461990-01-22022 January 1990 Forwards Proprietary Rev 1 to DPC-NE-2001, Fuel Mechanical Reload Analysis Methodology for MARK-BW Fuel, Adding Section Re ECCS Analysis Interface Criteria & Making Associated Administrative Changes.Rev Withheld ML19354E4451990-01-22022 January 1990 Submits Update on Status of RHR Sys Iconic Display at Facilities,Per Generic Ltr 88-17 Re Loss of Dhr.Computer Graphics Display Data in Real Time & Reflect Status of Refueling Water Level & RHR Pump Parameters ML20005G7161990-01-20020 January 1990 Forwards Rev 1 to Updated FSAR for Braidwood & Byron Units 1 & 2.Changes in Rev 1 Include Facility & Procedures Which Were in Effect as of 890610.W/o Encl ML16152A9061990-01-19019 January 1990 Forwards Public Version of Rev 90-01 to Vol C to Oconee Nuclear Station Implementing Procedures Emergency Plan & Rev 89-03 to Vol a to Oconee Nuclear Station Emergency Plan. W/900131 Release Memo ML20006A8001990-01-19019 January 1990 Forwards Response to NRC 891220 Ltr Re Violations Noted in Plant Insps.Response Withheld (Ref 10CFR73.21) ML16152A9091990-01-18018 January 1990 Forwards Public Version of Rev 33 to Crisis Mgt Implementing Procedure CMIP-1, Recovery Manager & Immediate Staff & Rev 24 to CMIP-2, News Group Plan. W/900131 Release Memo ML18153C0771990-01-17017 January 1990 Forwards North Anna Power Station Emergency Plan Table 5.1, 'Min Staffing Requirements for Emergencies' & Surry... Table 5.1, 'Min Staffing Requirements...', for Approval,Per 10CFR50.54(q),NUREG-0654 & NUREG-0737,Suppl 1 1990-08-22
[Table view] |
Text
_
( '
b,
- DUKE Powen' COMPANY Powen Den.mwo 42c Sourn Cauwcu Srazzr, CnAutoriz. N. C. une4a wf LLI Ate O. PA R M r.R, J R.
%Cf PassiogwT Ttt t >=o=t; Amta 704
- sitaw PmOOUCTION 373-4083 i
September 22, 1980
'Mr. Robert Bernero, Director Probabilistic Analysis Staff Office of Nuclear Regulatory Research
. U. S. Nuclear. Regulatory Commission Washington, D. C. 20555-Subj ect: IfotseneTrIdig)-
Draft of RSSMAP Report
Dear Mr. Bernero:
<Your letter of September 3,.1980 enclosed the draft report on the Oconee RSSMAP study, performed by the Probabilistic Analysis Staf f and
~
its contractors, for our review and comment. We have been able to conduct only a limited review of this draft because of the short time made'available to us. Nevertheless, we have found a number of areas
- in the study and in the report itself where changes would be desirable and perhaps necessary. These areas of concern include the validity of-the system success criteria, correctness and appropriateness of the assumptions made in the systems analysis, and the applicability of the
~
. comparison of the results of the Oconee study to those of the RSS reference plant. Our comments are summarized below and elaborated in the Attachment to this letter.
In the area of the system's success criteria, we found that the criteria used for the emergency core cooling were incorrect and that. tlie success criterion used for the emergency feedwater system needs to he modified.
In the systems analysis area, there exist discrepancies between the
~
assumed and. actual c, afigurations .of the HPI and LPI systems. ~Also the assumed' values of~ failure probabilities-for manual actions in a number of instances we believe are overly conservative (HPI cooling, steam generator cooling by HRASWS, reestablishing AC power, etc.).
It-is apparent tint in-some instances an attempt was made to utilize
. Oconec specific component reliability (reliability of the turbine-driven N
h5 59 830331 SHDLLYe3-gg3 B0liO22 PDR ,
qv
.t; L w -
. - ( (,
Mr. Robert '2rnero.
Page 2 Sept ember , 1980 emergency feedwater pump and the reliability of the 'Keowee units) . Our review of the applicable failure data indicates that the failure and demand data were not properly interpreted, and as such the unavail-abilities for the affected systems were significantly overestimated.
We understand that in the RSSMAP study the RSS methodology was modified in several critical areas (common mode failure contribution, human reliability, etc.). Thus the indicated difference in the risk and severe core melt probabilities between the Oconee and the RSS reference
-plant does not provide a valid comparison.
The problem areas and discrepancies summarized above and elaborated in the Attachment would have a significant impact on the calculated frequencies of each of the dominant sequences, except perhaps the Event-V sequence, and as such warrant appropriate reanalysis. We suggest that, inasmuch as possible, the draft report be revised taking into account the reviewfcomments provided herein.
We recognize that the Oconee RSSMAP study had to rely primarily on FSAR-
.. type information, which is -outdated in several areas, and did not have the benefit of a more complete information base on the actual plant characteristics in several important aspects. A more thorough characterization of the Oconee accident sequer :es and plant risk is expected by way of the Duke /NSAC Oconee PRA program. The Oconee RSSMAP
' study would certainly serve as a valuable" reference and road map for the Oconee PRA program.
^
.It should be pointed out that the Oconee RSSMAP study and our carlier auxiliary feedwater system reliability study have uncovered two areas of the Oconec emergency feedwater system where further improvements p . .
are possible and desirable. Design modifications have been initiated to eliminate the AC dependencies in the turbine-driven EFWS train.
+ . As a result of these modifications, flow of cooling water-to the turbine oil. cooler and to the pump cooling jacket will be by ' gravity flow f rom ~
the high pressure service water. system. This modification should
- . nignificantly reduce the-unavailability of the EFWS for transients involving loss. of of f site power or loss of ' all AC power. With regard i to the Event-V sequence, Duke is evaluating measures to reduce the risk
- 'of this event and will implement appropriate procedure changes and/or. ,
modifications to . reduce the risk to an acceptable level.
In su= mary, we consider the report to be flawed to'such a degree that correction of certain portions of the report should be considered. prior to publication. To resolve these comments, we suggest that a meeting be held at'a mutually agreeable time.
e f
b
Y
- h; .i D
- '
k
. . 7 - . . . . ,
Mr. Robert Bernero Page 3 September 22, 1980 Any questions or comments regarding.the matters discussed in this letter and attachment may be directed to P. M. Abraham of our Project Coordination and Licensing Section phone: . (704)373-4520).
Ve truly yours, x
u s' lb . O. LN
. William O. Parker,'Jr.
.PMA:vr
-Attachment 4
.m e
4 9 m . . . -
t i.
. l' s
.i'.
e 1 - ' ?
r
..- g * ,
bri m in -l 1. i
. . .. .. . . ._ .......ah-
( (
DUKE POWER COMPANY COMMENTS
, ON DRAFT OCONEE 3 RSSMAP REPORT ,,
e fi September 22, 1980 e
b 4
e L
(- *
~
(
DUKE PO'JER COMPAhT COPJENTS ON OCONEE RSSMAP REPORT
. The following comments primarily address the assumptions and analyses in the Appendices, the source of basic information, but are also applicable to per-tinent sections of the main body of the report.
I. Appendix A1. LOCA Event Trees.
2.1.4 The success criteria for emergency core cooling identified on page 14-57 of the FSAR and used in RSSMAP have been revised as the result of a more recent analysis. The currently applicable criteria, based on Appendix K requirements and documented in BAW-10103, Rev. 3A, are listed below:
LOCA Equivalent Diameter Success Criteria Large Break (A) D > 10" 2/2 CFT '
and 1/3 LPI Pumps Sma'll Break (S1 ) 4" < D $ 10" 2/2 CFT and 1/3 HPI Pumps and 1/3 LPI Pumps Very Small Break (S 2) D-5 4" 1/3 HPI Pumps-Therefore, it is not necessary {.o consider a specific break spectrum in the range of 10" < D $ 13" In addition, the suc-cess criteria used are overly conservative and' the emergency core cooling unavailability will be reduced, thereby reducing the estimated frequencies of sequences involving the term D.
f 2.2.1 Per the preceeding discussion, only three break sizes need to be considered, eliminating the 10" < D $ 13" categoryE' -
2.2.2 The RPS is required to operate for S and t S 2 LOCA's, but not for A LOCA's as redefined above.
- 2.2.8 The success criteria for ECR are listed below:
LOCA , Functional Success J
A 1 of 3 LPRS S 1 of 3~LPRS 4 . S2 1 of 3 LPRS and' 1 of 3 llPRS e O v
( , '(
3.0 Per the preceeding discussion, a stuck-open RCS relief valve results in an S LOCA2 rather than S 3LOCA.
Table A-1 should be revised to reflect the revised success criteria discussed -
above.
II. Appendix A2. Transient Event Tree 2.1 Per the redefinition of LOCA categories, RCS integrity is re-quired to prevent a small small (S 2) LOCA.
2.1.2 The RCS heat removal requirements as stated are unduly con-servative, and the following evaluation demonstrates that flow from any one of the three EFW pumps to either steam generator is sufficient.
Using the August, 1979 ANS Decay Heat Standard and assuming an EFW enthalpy of 61 Btu /lb (corresponding to 90F and 1000 psi), the EFW flow requirements following shutdown are listed below:
Time (Sec) Power Function Flowrate (gpm) 60 0.0342 531 80 0.0322 500
. 100 0.0308 479 150 0.0283 440 200 0.0267 415 400 0.02329 361 600 0.0213 331-The demand for EFW flow occurs when the initial steam generator inventory boils off to the minimum Icvel. At this time the capacity of one motor-driven pump (500 gpm) is adequate for RCS heat removal. This will reduce the unavailability of the EFW system, and consequently the frequencies of sequei:es*
involving the term L.
Two-additional means of removing RCS heat were not discussed explicitly. If off-site power is available, one hotwell -
- pump and one condensate booster pump provide sufficient flow if steam generator pressure is reduced using the turbine bypass valves. The original auxiliary service ' water pump is also still available, requiring opening of the manual atmospheric dump valves to depressurize the steam generators'
'to approximately 60 psig.
As reported in BAW-1610, the maximum RCS pressure expected for an event involving failure of the RPS is 3600 psig,.
rather that 4000 psig.
'p n . , . . . . . . c., . . _g . . , . . _ . . .. . .. . . . . . . . . . . . . , . . _ _ _
_m _ _. . . ___,. . ., _., _ _ , , . _ . _ _ _ . . , , , , ,
,. . . is k_ '
av
' . x 2.2.3 The unavailability estimate of the PCS during T2 transients is unrealistically high for Oconee. To obtain the necessary main _feedwater flow prior to SG dryout, only one. train of the
-hot-well - condensate booster - main feedwater. pumps combination
- is_necessary. In the event the PCS recovery is unsuc'cessful prior to SG dryout, the hotwell-booster pump combination can be utilized since the:resulting SG pressure is low, and further the turbine bypass valves can be controlled to maintain SG pres-sure within the HWP-CBP flow capability. The Oconee turbine
, driven main feedwater pumps can be supplied with motive steam
- via the station auxiliary steam header.
7
. A survey of recent Oconee operating experience for 1979 and 1980 identified nine reactor trips involving feedwater tran-sients. In all nine occurences,-the main feedwater. system was either available throughout the transient or was recovered within 30 minutes of.the. reactor trip. This operating ex-perience suppo,rts the contention that a PCS non-recoverability probability of 1.0 grossly exagerates the unavailability lof j- the PCS during transients other than T3 transients.
Based on the above considerations, it is inappropriate.to !
assume a value of I for the PCS unavailability during T2 events. Rather, a value of 10 2, consistent'with the operat-ing experience, would be appropriate. .This change would
,, reduce the. presently calculated probability _of sequences involving the term M.
2.2.4 The discussion should_ identify hFW capabilities'as two 100%
motor-driven pumps and one 200% turbine driven pump.
2.2.7 reseat af ter being The frequency challenged of the PZR is assigned relief value the same valves(10 to_2) for the PORV and the safety values. We believe that the value_for the safety. valves is much smaller (of the order of 10 4).fWith respect to the PORV, operator action to close the PORY block
~
value should be considered in light"of the recent' changes
~
in operator training and procedures and thetimplemenation of direct PORV position indications. Considering the smaller frequency of safety value failure ~and the changestin PORV is ' -.
olation~capabilit'y, it-is suggested that_a much smaller value for. Q, perhaps . in .the range of -10 4 - 10 3 would:be appropriate.
.This change #'ould reduce the currently calculated frequencies
. of sequences involving Q by a factor of 10 to 100.
TheLunava11 ability of feed and bleed cooling _during transient.
? -sequences-involving failure of the PCS, EFS, and HASWS is overestimated. .HPI cooling in the: absence of SGLcooling is
[-- explicity' required by_ the emergency procedures. Because of-the RCS' saturation alarm and the obvious ~ indications of inadequate.SG~ cooling, and considering that?a~ time' inter-
, Lval :offgreatcr : than 20 ' minutes -is available to initiate thi,s -
A + p
-_: 3_
9 . . , - , w ,
A - .
.k ( ,.
function, we believe that the unavailability of this fun-ction is of the same order as that of the ECC recirculation I function. Furthermore, continued boil-off of the RCS in-ventory through the PZR relief values would eventually ac-tuate the ESF on high RB pressure.
3.0 The stuck' open relief safety valves r esult in S 2 1.0CA's rather than S3 LOCA's.
III. Appendix Bl. Emergency Power System 2.1.1 At least one of the two Lee combustion turbines is started and energizes the dedicated 100 KV line to Oconee whenever.
one of the Keowee units is unavailable. In the event-the
\
Keowee outage is an extended one, a load from Oconee (nor-mally a 4160 volt bus) is placed on the Lee turbine for operat-ing reliability.
5.2 The unavailability calculated for the Keowce units based on the number of tests and failures appears to be too high. It was apparently assumed that only a monthly test of each Keowee unit was made, yielding 168 tests. However, seven annual tests have been performed in addition to system demands upon the Keowee units to supply power to the grid. Properly accounting for Keowee startup demands from.all sources indicates that ireater than 2500' demands have occurred. . Twelve instances have been identified-wherein a unit failed to deliver power upon demand, regardless of the source of the demand. Of the twelve instances, seven involved -a unique failure of a 3 articular component over a five month period. The problem is belived to have been rec-'
tified. This type of failure has not reoccurred in the suc-ceeding two years and may justifiably be counted as a single failure. Thus, the Keowee failure per demand ratio can be conservatively calculated as 6/2000.
On a qualitative basis, the Oconee EPS reliability is" jqual to ar better than that of many other nuclear stations. Alternate power sources are available to an individual Oconee unit from the other nuclear units at the station, from the system grid, from the near site Keowee units, and from the' combustion tur- ~
bines at the Lee' Steam Station. The hyd,roelectric generators at the Keowee facility have inherently simpler design and operating characteristics relative to diesel generators and thus. represent a more reliable backup power source. Further-more,-the Keowee' units are frequently called upon toisupply power to'the system grid -and therefore problems are more likely to be detected and corrected prior to emergency.use. Based upon these considerations, the AC power non-recovery probability
-(within toi3 hours) of 0.1 - 0.5 used in the report 'is un-realistic.
~
c 4.-
? 6 l'_ ---
( ( >
IV. . Appendix B3. Reactor Protection System 5.2 Q(RPS) = 2.6 x 10~5 /RY, not 2.6 x 10 5 /RY Table B3-1 Two reactor trip setpoints are incorrectly listed.
The correct setpoints are identified below:
Over Power 105.5% of rated power RC Pressure 2300 psig - High V. Appendix B6. Low Pressure Injection System 2.1 During normal operation, motor-operated valves LP-21 and LP-22 in the LPIS suction lines from the BWST are left open. This will reduce somewhat the unavailability of the LPIS.
Although it is not important to the results, the notation for the LPIS pumps and coolers refer to Oconee-1 components. The correct notati'on for Oconee 3 is LP-P3A, LP-C3A, etc.
5.1 The correct success criterion for LPIS for both A and S LOCA's t
is one out of two pump trains.
5.2.1 Since the LPIS success criterion is the same for LOCA's A and S2 , only one Boolean equation _is required, i.e., Equation B6-1.
~
5.2.2 The LPIS unavailability for failure of 2 of 2 trains is re-calculated for the case when MOV's LP-21 and LP-22 are normally open. g for LP-21 plugging 1x10[4 LP-22 operator error 3 x 10 4 (Consistent with LP-28)
Q2 total 4 x 10 4 E. B: LP-22 + LP-30 4 x 10~4 + 10~4 = 5 x 104 C: LP-21 + LP-29 - 5 x 10~4 [ -.
. The unavailability of ~the LPIS is therefore reduced fr'om 2.6 x 10~3 to 2.1 x 10 3, so the change is not very significant.
Table B6-4 should be deJeted.
VI. Appendix .B7. - Low Pres,sure Recirculation System 5.1 Successful ECR requires one LPRS train for A and S LOCA's.
1 5.2.1 The Boolean equation for LPRS failure excludes some terms in-cluded in LPIS since success of LPRS is important only given success of LPIS. Therefore, the terms from the LPIS equation which are -included here do not have the same unavailabilites, and should be' lower.
Also, although the discussion in 2.1 includes the third LPIE
, pump, no credit is-taken forLits availability in ,the analysis.
~
.I' _ ..
r . . .
Y 3,
VII. Appendix B8. High Pressure Injection System 2.1 :
The~ electric power for each of the three HPIS pumps is sup-plied from a different 4160 volt bus. It appears that this discussion should refer to the digital ES channels which -
actuate the three pumps.
2.2 The injection valve in the B train (HP-27) is normally left open with power to its motor operator removed. This should reduce the unavailability of this train somewhat. A cross connection is available between all three injection lines, with isolation by normally closed motor-operated valves HP-409 and HP-410. The injection points are downstream from the normal isolation valves, HP-26 and HP-27, allowing operator action to assure two trains of HPIS flow in the event of failure of the injection' valves or an HPI pump. This also should reduce the unavailability of the HPIS.
5.2.1 - The HPIS unava'ilability due to' pump testing is incorrectly calculated. At Oconee, the A and B HPI pumps are used alter-nately to . supply normal makeup sea 1 ' injection. Test procedures for the C pump 'specify that it be used to supply normal- makeup by' closing.HP-27 (refer to Figure B8-1) and opening thel cross-tie valves from the B injection line, HP-116 and 117 (not labeled in the. figure). Thus, this pump is available should
,, an HPI actuation signal occur- during testing of that pump.
Therefore, HPI pump testing does not contribute to the HPIS unavailability.
D VIII. Appendix B9. High Pressure Recirculation System -
2.1 The discussion concerning electric power contains the same error identified above, i.e., three separate buses supply power-to the three respective pumps.
IX. Appendix B10. Engineered Safeguards Protection System I'~.
2.2 In response to NUREG-0578, reactor building isolation is act-uated by channels 1 and 2 to provide isolation on either low reactor coolant pressure or high containment pressure. -
X. Appendix B11. Containment Spray Injection' System -
I 2.2 -
Valves LP-21 and LP-22 are normally open and are therefore not required to change positions on ES 7 and 8 actuation. This should reduce the unavailability of the CSIS.
5.0 The dominant failure contributor of the CSIS during transients and small' break LOCA events was treated to be the failure of the operator.to start the system whenever the CSIS is manually.
bypassed. Resetting ~the applicable ESFAS channels'would'still-maintain,the system in the safety mode. Deliberate operator
- action is required to-bypass ~an automatic safety function and
- is not-permitted unless it'is confirmed that the plant mode does~not require that function. Even under bypass conditions, T-1 - I a g - . -- - - - ' ' ii - -' m
_ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ . - -----_-__---_____J
y . . _ .- . -
-.:1 *
- *-9. . . -
the high reactor building pressure alarm would alert the C - operator to activate the sprays. Therefore, the assignment of a higher probability for the CSIS failure during transients and small break LOCA events does not seem to be necessary.
XI. Appendix B13. Emergency Feedwater System and.High Head Auxiliary Service
~ Water System
- 1. Since 1973, 158 tests of the turbine driven emergency feedwater pumps have been performed. A review of the test results iden-tified four incidents wherein the pump failed to start. This data supports a pump unavailability probability of 2.5 x 10 2 which is more than three times lower than the value used in the report.
- 2. The auxiliary service water system cross-ties frons the other units are still available, in addition to the new high head system. Thus, two additional backup systems are available.
- 3. In addition, as discussed in the comments for Appendix A2, the
-correct success criterion for EFW is one of the three pumps, or a flowrate of 500 gpm.
- 4. The unavailability of the HMASWS is estfrated at 0.1 based on human error. This seems unrealistically high considering the
~ fact that it is a dedicated system and further that the operators will be dedicated to the SSF. It is expected to yield fairly high availability, on the order of that for the 'rps, D
XII. Appendix BIS. Reactor Building Cooling Systems 5.2.2 The failure of'the RBCS was estimated for cases with and with-out?AC power initially available, although these cases were not investigated for other systems.
- 77. .
e 9 **
e g
8 .
m 0
7 g
V
-. 3 -,
Dun e POWER COM PANY Pownu Dun.oixo 422 Sourn Cut ncis Si uner. CnAnt.oTrz, N. C. ::nm W 8 L LI A *4 Q. PAR et C R, J R. ,
Tg 6 t >=o = CAnta 704 V*Cr Pers.or-t sic.- e-coves o= November 3, 1981 Mr. Thomas M. Novak Assistant Director .for Operating React ors Division of Licensing U. S. Nuclear Regulatory Cor.. mission Washington, D. C. 20555 Subj ect: QPcuegdig .
hifE1NjWir
- - 3
Dear Mr. Novak:
s The following information is submitted in response to your 1ctter of September'8, 1981 concerning the Reactor Safety Study Methodology Application Program (RSSMAP) study of Oconee Unit 3. Duke Power Company previously (by our letter of September 22, 1980) provided comments on an earlier draft report of this study.
We note with appreciation that some of our comments were considered in the preparation of the final version of the report. Specific comments on the con-clusions of the study reported in Section 6.3.1 and some discussion on changes in plant systems and procedures implemented at Oconce subsequent to the RSSMAP study with potential positive impact on the RSSMAP estimated probabilitics and consequences of accidents are provided ,in the following paragraphs.
With regard to the frequency of an interf acing system LOCA event. we have instituted a program for periodic leakage testing of the check valves of inter-est and further have ceased the stroke testing of the normally closed MOV's-LP-17 6 -18 at operating conditions. (Stroke testing of these values is done
~
only at cold conditions.) Since the Icak-leak failures are essentially elimi-nated by the periodic Icak testing program and by climination of the MOV stroke _
testing at operating conditions and since the Icak-rupture and rupture-rupture
. f ailures are significantly small with the normally closed configuration of the MOV's, the event V is'now believed to'be a non-significant risk. contributor.
Plant codification has been completed to eliminate the AC dependency of the turbine driven emergency feedwater pump. With this modification, the avail-ability of the emergency feedwater system during accidents involving loss of offsite power or loss of all AC power has improved. Consequently, the frequency of core melt accidents initiated by.or involving these events would be less ,
than that estimated in.the RSSMAP~ study.. 1
' TVo. changes which are outside -the scope of 'the RSSMAP study and whidh came to
- our attention in conjunction with the : ongoing NSAC-Duke Oconce PRA program are being implemented'now. . One is a change in the emergency procedures to deal with a situation in which the LPI pumps could be running at shutoff head for ar. cxtended period of . tin . Such a ~ situation is postulated to occur during 8 -
k
~
- a. .
Mr. Thomas M. Novak November 3,1981 Page 2 certainsmallbreakLOCAandseveresteamlinebreakeventsiftheRbSdoes not depressurize sufficiently below the LPI actuation setpoint. Although the operators are aware of the need to secure the LP1 pumps within reasonable time under this situation, the existing emergency procedures do not include this requirement. A change in the applicable procedures is now being imple-mented to include the necessary guidance. The other change pertains to two ICS simulator relays. A postulated spurious energization of these relays could lead to a feedwater transient (resulting in a reactor trip) and the turbine bypass valves failing closed. A modification of the system to de-activate this circuitry is being impicmented. The interim results of the Ocor.e5 PRA are being monitored to assure early identification of any important risk outliers. At this point, no additional items have been identified which merit consideration in the near term.
A number of the post-TMI changes to plant 1 systems and procedures have con-tributed to improved safety both with. respect to probabilities and. consequences of accidents. Among the measures contributing to reduced probabilities of accidents are: ~ -
(a) Modification to the turbine EHC System to reduce the frequency ,
~
of turbine-reactor trips.
(b) Modifications to the main feedwater system to minimize tLa occurrence of feedwater transients. -
(c) Changes in the control system power supply to minimize the occurrence of power supply failure induced transients and to better cope with such events.
(d) Modification of the emergency feedwater system initiation, control, -
and indication functions for better reliability and performance.
The following other post-TMI efforts, which are in various stages of impicmenta-
- tion, are considered to effect further reduction in the probabilities and cons'equences of accidents.
'(a) Renewed vigilance and scarching reviews now being conducted on operational occurrences through the operating experience evaluation program. ,
(
(b) Control room design review and incorporation of safety pargpeter display system.
(c) Improved operator training, development and-impicmentation of improved 4
-procedures and the utilization of shift technical _ advisors.
~
Mr. Thomas M. Novak November 3, 1981 Page 3 *
(d) Implementation of RCS high point vents, post-accident samp5ing panel, and dedicated hydrogen penetrations.
(e) Implementation of PORV/PSV position indicator and RCS subcooling monitor.
(f) Impicmentation of accident monitors and expanded emergency planning programs and facilities.
We are not certain whether the conclusion reached.in the Oconee RSSMAP study rega-Jing hydrogen burning and the associated impact 1on containment is valid.
There is reason to ,believe that the Oconee containment failure pressure is much higher than.that assumed in the RSSMAP study (183 psia versus 133 psia).
Furthentore, the MARCH code treatment of hydrogen in regard to its generation in the core, accumulation in the containment, and degree of burn- in the con-tainment is generally recognized to be very conservative, particularly for small break and transient induced core melt events. A more realistic analysis of the containment accident; process is expected in the NSAC-Duke Oconee PRA analysis, It is our impression that the Oconce RSSMAP study has been a very worthwhile undertaking. Although there are some limitations in this-study, it still
.provides some useful insights into the dominant accident sequences and their contributing factors.
Ver 'truly yours,
/
. /
n., un -
William O. Parker, Jr. ,
PMA/php cc: Mr. Robert. F. Bernero, Director Division of Risk Analysis
- Office of Nuclear Regulatory Research U. S. Nuclear Regulatory Commission Washington, D. C. 20555 ,
(
. 1 9
N
!:._ . .