Safety Evaluation Conditionally Supporting BWR Owners Group Evaluation of Radiological Consequences for Accidental Releases Through BWR 2-inch Vent & Purge LinesML20211B815 |
Person / Time |
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Site: |
Limerick |
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Issue date: |
05/20/1986 |
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From: |
NRC |
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To: |
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Shared Package |
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ML20211B791 |
List: |
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References |
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RTR-NUREG-0578, RTR-NUREG-0737, RTR-NUREG-578, RTR-NUREG-737, TASK-2.E.4.2, TASK-TM NUDOCS 8606120048 |
Download: ML20211B815 (6) |
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
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Ltr Acceptable ML20246J8351989-05-0909 May 1989 Safety Evaluation Re Low Pressure Turbine Maint Program. Program Acceptable ML20245K7621989-05-0202 May 1989 Safety Evaluation Accepting Ultrasonic Test Indications in N2H nozzle-to-safe End Weld During Cycle 3 ML20151T5191988-08-0303 August 1988 Safeguards Evaluation Rept Supporting Amend 9 to License NPF-39 ML20154A8931988-05-0303 May 1988 Safety Evaluation Supporting Request for Extension of Const Dates for CP CPPR-107 ML20196H9341988-03-0404 March 1988 Safety Evaluation Supporting First 10-yr Interval Insp Program ML20236J2621987-11-0303 November 1987 Safety Evaluation Accepting Util Compliance W/Atws Rule 10CFR50.62 Re Alternate Rod Injection Sys,Recirculation Pump Trip & Standby Liquid Control Sys ML20236J2121987-11-0303 November 1987 Safety Evaluation Accepting Util Turbine Sys Maint Program ML20236P8201987-08-0707 August 1987 Safety Evaluation Approving Request to Retain RHR Svc Water Process Radiation Monitors ML20214F5871987-05-18018 May 1987 SER Granting Util 870422 Request for Approval of Plans Allowing Removal of Reactor Pressure Vessel Head Spray & Vent Piping & Detensioning Reactor Pressure Vessel Head Studs Prior to Connecting Standby Gas Treatment Sys ML20213G8351987-05-12012 May 1987 SER Supporting Util 870319 Request for Approval to Remove Primary Containment Head Prior to Connection of Standby Gas Treatment Sys to Refueling Floor Area ML20215J2201987-05-0404 May 1987 Safety Evaluation Approving post-irradiation Fuel Surveillance Program ML20205L7241987-03-27027 March 1987 Safety Evaluation Supporting Util 860327,1224,870113 & 27 Proposals to Use ASME Code Case N-411, Alternative Damping Values for Seismic Analysis of Classes 1,2 & 3 Piping Sections,Section Iii,Div 1 ML20205L8741987-03-26026 March 1987 Safety Evaluation Accepting Util 831110,840508 & 0607 Responses to Generic Ltr 83-28,Items 3.1.1,3.1.2,3.2.1,3.2.2 & 4.5.1 ML20207T1721987-03-18018 March 1987 Safety Evaluation Supporting Util Proposal to Delete Cooldown Air Flow Path to Each Charcoal Adsorber in Reactor Enclosure Recirculation Sys Filter Trains ML20209J5691987-02-0404 February 1987 Safety Evaluation Supporting Util 861117 Proposed Tech Spec Changes Re Operation W/Partial Feedwater Heating & Increased Core Flow Limits NUREG-0578, Safety Evaluation Conditionally Supporting BWR Owners Group Evaluation of Radiological Consequences for Accidental Releases Through BWR 2-inch Vent & Purge Lines1986-05-20020 May 1986 Safety Evaluation Conditionally Supporting BWR Owners Group Evaluation of Radiological Consequences for Accidental Releases Through BWR 2-inch Vent & Purge Lines ML20155H0941986-04-23023 April 1986 Safety Evaluation Supporting Util Responses to Generic Ltr 83-28,Item 1.2 Re post-trip Review Data & Info Capability ML20137L2021986-01-0606 January 1986 SER Supporting Util Responses to Generic Ltr 83-28,Items 3.1.3 & 3.2.3 Re post-maint Testing (Reactor Trip Sys Components) ML20214E4211984-09-18018 September 1984 Safety Evaluation Supporting Util Responses Re Containment Pressure Boundary Matls Cited by GDC 51 ML20235C0101971-11-29029 November 1971 Safety Evaluation of Util Application for CP & OL for Dual Unit Nuclear Power Plant Facility 1999-09-13
[Table view] Category:TEXT-SAFETY REPORT
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Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 B110078, Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 11998-12-31031 December 1998 Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 1 ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154H5691998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Limerick Generating Station,Units 1 & 2.With ML20151X3511998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Limerick Generating Station Units 1 & 2.With ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20237D1041998-08-17017 August 1998 Books 1 & 2 of LGS Unit 1 Summary Rept for 960301-980521 Periodic ISI Rept 7 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20236X7641998-07-31031 July 1998 Rev 0 to SIR-98-079, Response to NRC RAI Re RPV Structural Integrity at Lgs,Units 1 & 2 ML20237B4711998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Limerick Generating Station,Units 1 & 2 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20151Z4881998-06-30030 June 1998 GE-NE-B1100786-02, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 2 ML20236P9781998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Limerick Generating Station,Units 1 & 2 ML20196K1801998-06-30030 June 1998 Annual 10CFR50.59 & Commitment Rev Rept for 970701-980630 for Lgs,Units 1 & 2. with ML20249B3501998-06-11011 June 1998 Rev 1 to PECO-COLR-L2R4, COLR for LGS Unit 2 Reload 4,Cycle 5 ML20249A5331998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Limerick Units 1 & 2 ML20247M7071998-05-14014 May 1998 Safety Evaluation Supporting Amend 128 to License NPF-39 ML20217Q5101998-05-0404 May 1998 Safety Evaluation Supporting Amend 127 to License NPF-39 ML20247H5071998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Limerick Generating Station ML20216F3601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Limerick Generating Station,Units 1 & 2 ML20217M0791998-03-31031 March 1998 Safety Evaluation Supporting Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216F9471998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Limerick Generating Station,Units 1 & 2 ML20216F3471998-02-28028 February 1998 Revised Monthly Operating Rept for Feb 1998 for Limerick Genrating Station,Unit 1 1999-09-30
[Table view] |
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ENCLOSURE I EVALUATION OF THE RADIOLOGICAL CONSEQUENCES FOR ACCIDENTAL RELEASES THROUGH BWR 2-INCH VENT AND PURGE LINES INTRODUCTION NUREG-0737, Item II.E.4.2(7) required that the containment purge and vent isolation valves must close on a high radiation signal. This position was added to the original NUREG-0578 requirements of Recommendation 2.1.4 as a result of further staff evaluation of features needed to improve containment isolation dependability.
One basis for the implementation of II.E.4.2(7) was the additional protection it would provide against low rates of reactor coolant leakage and releases to the environment which would not initiate the other automatic isolation signals of reactor low water level and high drywell pressure. The BWR Owners Group (BWROG) previously transmitted an evaluation of offsite radiological
, consequences for accidental releases through BWR vent and purge lines which do not meet the requirement of NUREG-0737. Item II.E.4.2(7) in a letter from T. J. Dente of the BWROG to D. G. Eisenhut of the NRC, dated June 14, 1982.
In a June 20, 1985 meeting, the BWROG requested that the staff review its evaluation for small (2-inch diameter) vent and purge linas.
DISCUSSION The staff has reviewed the BWROG evaluation which provides calculations of the radiological consequences of the limiting reactor coolant system break which would not initiate automatic isolation with the current design. The limiting event was conservatively modeled as a reactor coolant system break such that the drywell atmosphere would contain saturated steam at a pressure just below the containment isolation setpoint. Steam release through one vent or purge line was assumed to pass directly to the environment with no credit given for holdup or dilution, or for filtering by the standby gas treatment system. The fraction of the iodine postulated to become airborne and available for release to the atmosphere, without credit for plateout, was assumed to equal the fraction of the coolant flashing to steam. The BWROG evaluation provided calculations for a typical plant as well as a generic analytical procedure.
Independent calculations of the radiological consequences of the limiting reactor coolant system break were performed by the staff. The staff conservatively estimated a mass release value of 492 cubic feet per ribute of saturated steam at 2 psig over a 30 minute duration until the one purg and
. vent line would be isolated by other actions.
The assumptions used in this staff analysis were as follows:
- 1. Dryweilatmosphereissaturatedsteamandatapressureequaltothe containment isolation setpoint (psig).
- 2. Operator action time to close the purge or vent valve is assumed to be 30 minutes.
4 8606120048 860520 PDR ADOCK 05000352 P PDR g - -
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- 3. Vent pipe length is conservatively assumed to be 10 ft. for purposes of flow calculations.
- 4. Elevation changes have been neglected.
The BWR Owners Group analysis used formusas described in NEDM-10363-13,
" Hydraulic Analyses Procedure for BWR Piping Systems." The staff used similar formulas, which are described in the Crane Flow of Fluid Manual and the above assumptions, and obtained similar results to those provided by the BWR Owners Group.
The staff, using the above release rate, performed plant specific calculations of the radiological consequences for Pilgrim Unit 1, Hatch Units 1 and 2, Peach Bottom Units 2 and 3, and Limerick Unit 1. The staff's calculation of offsite doses differed from the procedure outlined in the BWR0G's evaluation in two respects. First, the staff used short term diffusion estimates typical of other conservative regulatory evaluations of accidents; the BWROG used annual average relative concentrations typical of a realistic evaluation of doses from routine releases. Second, the staff used conservative reactor coolant iodine concentrations assuming a pre-accident iodine spike for those plants with a technical specification iodine spiking limit. For Pilgrim Unit 1, which has no technical specification iodine spiking limit, 'the staff used the maximum technical specification equilibrium concentration with an accident-initiated spike, modeled by increasing the equilibrium fission product activity release rate from the fuel by a factor of 500. The staff's iodine spiking model is typical of regulatory analyses involving accidental releases of primary coolant, as outlined in Section 15.6.2 of the Standard Review Plan (NUREG-0800). The BWROG's evaluation assumed equilibrium iodine concentrations with an accident-initiated spike using a 95% cumulative '
probability iodine spiking model.
RESULTS The staff estimates of the thyroid and whole body doses at the exclusion area and low population zone outer boundaries for the 6 units are presented in Table I (attached). Although specific acceptance criteria do not exist for this postulated accident, the radiological consequences and frequency of occurrence for this accident would tend to be similar to that of the failure of small lines carrying primary coolant outside containment. The staff concluded that the use of the acceptance criteria for the failure of small lines, which appear in Section 15.6.2 of the Standard Review Plan, would be appropriate for use in this evaluation. Thus, the radiological consequences of this postulated accident would be acceptable if the calculated whole-body and thyroid doses at the exclusion area and low population zone outer boundaries do not exceed a small fraction (10%) of the dose guideline values of 10 CFR Part 100, viz., 2.5 rem and 30 rem respectively, for whole body and thyroid doses. As summarized in Table I, the estimated doses are a small fraction of these dose guideline values of 10 CFR Part 100.
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TABLE 1 i
RADIOLOGICAL CONSEQUENCES FOR ACCIDENTAL RELEASES THROUGH BWR -
2-INCH VENT AND PURGE LINES '
Exclusion Area Boundary Low Population Zone (0-2 hr), rems Boundary (0-8 hr) . rems Thyroid Whole Body Thyroid Whole Body -
Limerick Unit 1 0.4 0.007 0.08 0.002 Peach Bottum Units 2 & 3 0.4 0.004 0.007 0.00006 Hatch Unit l' O.08 0.0008 0.04 0.0004 l Hatch Unit 2* 0.08 0.002 0.04 0.0008 -l Pilgrim Unit 1 3.3 0.03 0.2 0.002
- The difference in whole body doses between Hatch Unit I and Unit 2 was a result of dif ferent Technical Specification. primary coolant activity limits.
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The magnitudes of these doses calculated by the staff are higher than would realistically be expected because of the many conservative assumptions in the staff's methodology, particularly with respect to iodine spiking behavior and to meteorology. For example, coolant iodine concentration levels generally, are small fractions of equilibrium technical specification levels, iodine spiking does not always occur coincident with the transients, the iodine spiking concentrations assumed to occur are well in excess of any level recorded at an operating boiling water reactor, and the probability of better meteorological conditions is quite high. A more realistic analysis would yield dose estimates about 1/100th or less of the values noted above.
Since this evaluation assumes that operator action to close the purge or vent valve is taken within 30 minutes, for the BWROG evaluation to be acceptable the licensee must verify that the 30 minute operating time is valid based upon location and accessibility of the valve operators, and insturmentation necessary to determine the need for manual closure, and that plant procedure and operator training are sufficient to support the approach.
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- ENCLOSURE 2 BWR VENT & PURGE RADIATION HONITOR SET POINTS BACKGROUND - In a meeting on June 20, 1985 the BWR Owners Group requested that the staff establish set point criteria for isolation signals for vent and purge line radiation monitors required under TMI Action Item II.E.4.2(7) of NUREG-0737. The monitors are not considered safety related, but are to be provided solely to assure diverse isolation signals in the event of an accident.
EVALUATION - Radiation monitors with vent and purge line isolation capability are required as a post TMI item to ensure containment isolation. Other diverse isolation signals, such as drywell pressure and reactor water level, are also provided. A review of the regulations indicates t.here are no
, . explicit dose guidelines that apply to such monitors in the event of accidents, other than the siting values in 10 CFR 100. The Standard Review Plan contains design basis accident dose acceptance criteria which have previously been evaluated with respect to purge and vent valve closure time criteria. As discussed in Enclosure 1, the staff concluded that the use of acceptance criteria of calculated whole-body and thyroid doses at the exclusion area and low population zone outer boundaries which do not exceed a small fraction (10%) of the guideline values of 10 CFR Part 100 would be appropriate for use in the evaluation of the radiological consequences of accidental releases through open vent and purge lines. As a minimum i requirement, vent and purge radiation monitor set points should be l established such that this acceptance criteria is met.
The staff notes, however, that a guiding principle in establishing set point values for radiation monitors used to limit doses is to establish them as low as possible to avoid unnecessary exposures. If set too low, however, spurious signals resulting from minor changes in instrument detectability or background activity levels not representative of accident conditions can occur. As a practical matter, for radiation detectors which are located on the vent or purge line set points which do not exceed the highest radiation level expected in normal operation should provide suitable warning of accidents and avoid most spurious signals.
POSITION - Radiation monitors provided for assuring diverse isolation signals for BWR vent and purge valves should be set low enough to effectively limit accidental releases of radfoactivity from being released offsite when such valves are open during operation. While such set points should be established as low as possible to limit offsite accident releases, the set points should not cause unnecessary isolation signals resulting from instrument uncertainties or non-accident variations in radiation levels. As a minimum requirement, vent and purge radiation monitor set points should be established such that the raciological consequences of accidental releases through open vent and purge lines do
. t f
. e not exceed a small fraction (10%) of the dose guideline values of 10 CFR Part 100. As a practical matter, for well shielded monitors which directly measure activity levels in the flow past such valves, set points at a level which does not exceed the highest radiation level expected in nonnal operation should provide adequate assurance of accident isolation.
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