|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML18040A2851993-12-0808 December 1993 LER 93-010-00:on 931108,HPCS Was Inoperable Due to Equipment Deficiency,Inadequate Managerial Methods & Poor Work Practices.Replaced Deficient Contactors & Restored Tap Setting.Also Reportable Per Part 21.W/931208 Ltr ML18038A3191990-08-10010 August 1990 LER 90-006-00:on 891027,discovered Unverified Assumption in App R Safe Shutdown Analysis.Caused by Fire Protection Program Failure to Provide Detailed Procedural Instructions for Operator Actions.New Procedures developed.W/900810 Ltr ML18038A4701989-05-15015 May 1989 LER 89-014-00:on 890413,unit Reactor Experienced Reactor Scram Which Was Result of Turbine Trip Due to Actuation of Generator Protection Circuitry.Turbine Trip Caused by Disconnected Wire.Wire relanded.W/890515 Ltr ML18038A4131988-08-22022 August 1988 LER 88-051-01:on 870813,shutdown Cooling Sys Isolated & Tech Specs 3.4.9.2 Exceeded.Caused by Equipment Failure,Personnel Error & Procedural & Design Deficiencies.Shutdown Cooling Sys Manually restored.W/880822 Ltr ML18038A4051988-07-0101 July 1988 LER 88-024-00:on 880605,ESF Actuation Occurred Due to Resetting of Failed Radiation Monitor Microcomputer.Caused by Lack of Personnel Training.Defective Cards & Modules in RE14B Microcomputer & DRMS Panel replaced.W/880701 Ltr ML18038A3901988-04-12012 April 1988 LER 88-014-00:on 880313,reactor Scram & ESF Actuations Occurred.Caused by Equipment Failure Due to Design Deficiency.Transmitter Replaced W/Upgraded Model & Temporary Mod Performed to Bypass Logic for valves.W/880412 Ltr ML18038A3891988-02-17017 February 1988 LER 88-001-00:on 880120,reactor Scram Occurred Due to Actual Low Water Level Condition.Caused by Design & Personnel Errors.Operator Disciplined & Mod Addressed Inadvertent Feedwater Control Valve lockup.W/880217 Ltr ML18038A7591987-12-22022 December 1987 LER 87-023-00:on 870422,trip of Normal Reactor Bldg Ventilation & Initiation of Emergency Ventilation Occurred. Caused by Personnel Error.Fuse Replaced.On 871123,util Discovered LER Not Submitted for event.W/871222 Ltr ML18038A2581987-06-15015 June 1987 LER 87-025-00:on 870519,secondary Containment Isolation Signal Generated Due to Technician Relanding Lifted Lead Prematurely.Caused by Breakdown in Communications.Gaitronics Phone &/Or Headset Jack installed.W/870615 Ltr ML18004C0061987-04-13013 April 1987 LER 86-002-01:on 861104,procedure N2-OSP-RMC-W0002 Ran for Over 2 H Thereby Violating Tech Specs.Caused by Personnel Error & Procedure Deficiency.Temporary Change Notice Issued to procedure.W/870413 Ltr ML20024E8331983-08-16016 August 1983 LER 83-021/03L-0:on 830720,22,26 & 28,emergency Cooling Sys Loop 11 Taken Out of Svc for Periods Up to 5 H.Caused by Attempt to Reseat Isolation Valve 39-05.Valve Seat Lapped & Loop Returned to svc.W/830819 Ltr ML20024E6341983-08-0202 August 1983 LER 83-017/03L-0:on 830707,HPCI Feedwater Booster Pumps 11 & 13 Taken Out to Svc to Inspect Impellers Due to Similar Problem on nonsafety-related Pump.Parts of Strainer Found in Pumps But Pumps undamaged.W/830805 Ltr ML20024E0251983-07-22022 July 1983 LER 83-019/03L-0:on 830623,two Monthly Surveillance Tests on Inadequate Core cooling-accident Level Monitor Missed Following 811231 Installation.Surveillance Procedures Generated & Added to schedule.W/830725 Ltr ML20024B7711983-06-17017 June 1983 LER 83-010/03L-0:on 830524,core Topping Pump 121 Removed from Svc to Replace Packing.Caused by Air Leaking Due to Iltr Pressure Introduction in Pump.Packing Replaced & Pump Returned to Svc within 22 h.W/830621 Ltr ML19277C5881983-06-16016 June 1983 LER 83-013/03L-0:on 830610,during Routine Surveillance,Lock Found Missing from Outside Inlet Valve 40-12 for Core Spray Sys.Valve & Breaker in Open Position.Lock Missing for No More than 15 Days.Lock replaced.W/830708 Ltr ML20024B7101983-06-16016 June 1983 LER 83-011/03L-0:on 830604,electromatic Relief Valve 121 Failed to Open.Caused by Dirty Pilot Due to Oxide Buildup During Extended Outage.Pilot Cleaned & Retested & Normal Shutdown initiated.W/830628 Ltr ML20023D9571983-05-24024 May 1983 LER 83-009/03L-0:on 830426,control Room Ventilation Sys Removed from Svc for Mods to Control Room Wall,Per LER 83-06.Temporary Flexible Ducting in Place During Mods. Mods Completed.Ventilation Sys Returned to svc.W/830526 Ltr ML20023D2551983-05-11011 May 1983 LER 83-006/03L-0:on 830411,while Performing Design Review, Discovered That Poured Concrete North & West Walls of Control Room Would Not Meet Original Seismic Criteria. Mods Made to Improve Wall Structural Loading Capabilities ML20023B8321983-04-18018 April 1983 LER 81-053/03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed ML20028C8391983-01-0505 January 1983 LER 82-018/03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20028C8361983-01-0505 January 1983 LER 82-017/03L-0:on 821206,during Maint Outage,Leakage from Valves 68-06 & 68-09 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20027C9681982-10-19019 October 1982 LER 82-001 Has Been Canceled ML17341B6651982-08-0505 August 1982 LER 82-011/03L-0:on 820802,oil Leak on Fuel Oil Supply Manifold Discovered on Diesel Fire Pump.Caused by Defective Braze Joint.Leak Repaired by Manufacturer ML20050N6691982-04-0505 April 1982 LER 82-009/01T-0:on 820323,while Conducting Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on Recirculation Piping.Cause Being Investigated ML20050C3881982-03-29029 March 1982 LER 82-008/01T-0:on 820317,review of Surveillance Test N1-ST-R7 Revealed Potential for Reactor Steam to Leak to Atmosphere from Emergency Condenser Vents.Caused by Potential Sys Leaks.Sys Modified Per NUREG-0737 Item II.B.1 ML20052F8991982-03-24024 March 1982 LER 82-009:on 820323,during Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on 11 Recirculation Piping Suction from Reactor Vessel.Cause Under Investigation ML20042C5041982-03-23023 March 1982 LER 82-006/04L-0:on 820225,during Normal Operation,While Tempering Plant Inlet Canal,Plant Discharge Temp Exceeded 85 F.Caused by Increase in Lake Temp Due to Weather Conditions & Inability to Fully Lower Tempering Gate ML20052F8461982-03-18018 March 1982 LER 82-008:on 820317,discovered Potential Path for Reactor Steam from Emergency Condenser Steam Line Vents to Atmosphere If Emergency Condenser Tube Leaks Occur.Caused by Mods Made to Comply w/NUREG-0737,Item II.B.1 ML20042A6891982-03-12012 March 1982 LER 82-007/04L-0:on 820222,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity Was Determined Not Met for Nov 1981.Cause Not Stated.Tech Spec Proposal Being Submitted to Update Stds ML20049H6101982-02-19019 February 1982 LER 82-005/03L-0:on 820208,115 Kv Line Taken Out of Svc for Maint,Placing Plant in Limited Condition of Operation.Maint on Line Required Due to Open Loop.Line Repaired & Returned to Svc ML20041C1651982-02-19019 February 1982 LER 82-004/01T-0:on 820207,during Routine 115-KV Breaker Exercising,Ground Directional Relay Caused Opening of Breaker Alternate 115-KV.Caused by Momentary Loss Offsite Power.Power Restored After Closing Oswego-NMP1 Breaker ML20041C1171982-02-17017 February 1982 LER 82-003/01T-0:on 820204,at 100% Power,Reactor Bldg Ventilation Sys Isolated & Emergency Ventilation Sys Initiated Due to Radioactive Release.Caused by Overflow of Reactor Water Cleanup Sys Filter Sludge Tank ML20041A7511982-02-10010 February 1982 LER 82-002/01T-0:on 820129,NRC Inspector Discovered That Primary Containment Following DBA LOCA May Not Be Vented Using Operating Procedure Due to Inaccessibility of Reactor Bldg.Combustible Gas Control Sys Will Be Installed ML20052F8961982-02-0808 February 1982 LER 82-004:on 820207,during Steady State Operation,Momentary Loss of 115 Kv Offsite Power Caused Emergency Diesel Generators to auto-start on Low Voltage to Power Boards 102 & 103 ML20052F8981982-02-0505 February 1982 LER 82-003:on 820204,during Steady State Operation,Cleanup Sludge Tank Vent Overflowed Into Reactor Bldg Exhaust Ventilation Sys Causing Emergency Ventilation Sys to Initiate.Cause Not Stated.Decontamination in Progress ML20052F8931982-02-0101 February 1982 LER 82-002:on 820129,during Steady State Power,Upon Review by Resident Inspector,Discovered That Operating Procedure Describing Steps to Vent Primary Containment Following DBA LOCA Required Personnel to Enter Reactor Bldg ML20040B8621982-01-18018 January 1982 LER 81-054/03L-0:on 811221,insertion of Shallow Control Rods Resulted in Average Planar Linear Heat Generation Rate in Excess of Tech Spec Limits.Caused by Flux Coupling Between Control Rods.Extra Rods Inserted & Tech Specs Modified ML20039E2951982-01-0202 January 1982 LER 81-025,is Cancelled ML20039C0951981-12-14014 December 1981 LER 81-053/03L-0:on 811120,emergency Condensers 11 & 12 Were Isolated When Emergency Condenser Vent Radiation Monitor de-energized Due to Loss of Dc Motor Speed Control.Caused by Defective Silicon Controlled Rectifier.Rectifier Replaced ML20038B4971981-11-25025 November 1981 LER 81-008/01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable ML20038B4561981-11-25025 November 1981 LER 81-050/03L-0:on 810715,reactor Bldg Ventilation Duct Radiation Monitor Showed Abnormal Spiking Which Initiated Emergency Ventilation Sys.Caused by Malfunctioning sensor-convertor Unit.Unit Replaced & Calibr ML20038B8801981-11-24024 November 1981 LER 81-052/03L-0:on 810812,failure of One Reactor Vessel Electromatic Relief Valve Thermocouple & Two Reactor Vessel Head Safety Valve Thermocouples Noted in Testing.Cause to Be Investigated Given Drywell Access in Next Cold Shutdown ML20038B7701981-11-24024 November 1981 LER 81-049/03L-0:on 811112,during Normal Operation,Feedwater Hydraulic Snubber 29-HS-6 Taken Out of Svc for Preventative Maint Because of Small Oil Leak.Cause Not Stated.Snubber Rebuilt & Returned to Svc ML20038B4581981-11-20020 November 1981 LER 81-051/04L-0:on 811109,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity (LLD) Not Met.Caused by Higher LLD Values When Test Data Converted from Wet to Dry Weight Units ML20011A4851981-09-30030 September 1981 LER 81-046/04T-0:on 810922,review of 810813 & 14 ETS Semiannual Samples of Cladophora Showed Co-60 & Nb-95 at Level of 10 Times Control Value.Probably Caused by Liquid Effluent Discharge & Oct 1980 Chinese Weapons Test ML20010G6931981-09-10010 September 1981 LER 81-042/04T-0:on 810831,during Weekly Environ Radiation Monitor Insp,Only Six Monitors Found Functioning Due to Defective Power Supply Units.Cause Unknown.Portable Monitor Installed ML20010G4341981-09-0404 September 1981 LER 81-040/03L-0:on 810818,chromated Water Found in Diesel Generator 102 Raw Water Due to Water Leaking Through Heat Exchangers.Cause Unknown.Raw Water Lines Drained & All Chromate Recovered 1998-07-02
[Table view] Category:RO)
MONTHYEARML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML18040A2851993-12-0808 December 1993 LER 93-010-00:on 931108,HPCS Was Inoperable Due to Equipment Deficiency,Inadequate Managerial Methods & Poor Work Practices.Replaced Deficient Contactors & Restored Tap Setting.Also Reportable Per Part 21.W/931208 Ltr ML18038A3191990-08-10010 August 1990 LER 90-006-00:on 891027,discovered Unverified Assumption in App R Safe Shutdown Analysis.Caused by Fire Protection Program Failure to Provide Detailed Procedural Instructions for Operator Actions.New Procedures developed.W/900810 Ltr ML18038A4701989-05-15015 May 1989 LER 89-014-00:on 890413,unit Reactor Experienced Reactor Scram Which Was Result of Turbine Trip Due to Actuation of Generator Protection Circuitry.Turbine Trip Caused by Disconnected Wire.Wire relanded.W/890515 Ltr ML18038A4131988-08-22022 August 1988 LER 88-051-01:on 870813,shutdown Cooling Sys Isolated & Tech Specs 3.4.9.2 Exceeded.Caused by Equipment Failure,Personnel Error & Procedural & Design Deficiencies.Shutdown Cooling Sys Manually restored.W/880822 Ltr ML18038A4051988-07-0101 July 1988 LER 88-024-00:on 880605,ESF Actuation Occurred Due to Resetting of Failed Radiation Monitor Microcomputer.Caused by Lack of Personnel Training.Defective Cards & Modules in RE14B Microcomputer & DRMS Panel replaced.W/880701 Ltr ML18038A3901988-04-12012 April 1988 LER 88-014-00:on 880313,reactor Scram & ESF Actuations Occurred.Caused by Equipment Failure Due to Design Deficiency.Transmitter Replaced W/Upgraded Model & Temporary Mod Performed to Bypass Logic for valves.W/880412 Ltr ML18038A3891988-02-17017 February 1988 LER 88-001-00:on 880120,reactor Scram Occurred Due to Actual Low Water Level Condition.Caused by Design & Personnel Errors.Operator Disciplined & Mod Addressed Inadvertent Feedwater Control Valve lockup.W/880217 Ltr ML18038A7591987-12-22022 December 1987 LER 87-023-00:on 870422,trip of Normal Reactor Bldg Ventilation & Initiation of Emergency Ventilation Occurred. Caused by Personnel Error.Fuse Replaced.On 871123,util Discovered LER Not Submitted for event.W/871222 Ltr ML18038A2581987-06-15015 June 1987 LER 87-025-00:on 870519,secondary Containment Isolation Signal Generated Due to Technician Relanding Lifted Lead Prematurely.Caused by Breakdown in Communications.Gaitronics Phone &/Or Headset Jack installed.W/870615 Ltr ML18004C0061987-04-13013 April 1987 LER 86-002-01:on 861104,procedure N2-OSP-RMC-W0002 Ran for Over 2 H Thereby Violating Tech Specs.Caused by Personnel Error & Procedure Deficiency.Temporary Change Notice Issued to procedure.W/870413 Ltr ML20024E8331983-08-16016 August 1983 LER 83-021/03L-0:on 830720,22,26 & 28,emergency Cooling Sys Loop 11 Taken Out of Svc for Periods Up to 5 H.Caused by Attempt to Reseat Isolation Valve 39-05.Valve Seat Lapped & Loop Returned to svc.W/830819 Ltr ML20024E6341983-08-0202 August 1983 LER 83-017/03L-0:on 830707,HPCI Feedwater Booster Pumps 11 & 13 Taken Out to Svc to Inspect Impellers Due to Similar Problem on nonsafety-related Pump.Parts of Strainer Found in Pumps But Pumps undamaged.W/830805 Ltr ML20024E0251983-07-22022 July 1983 LER 83-019/03L-0:on 830623,two Monthly Surveillance Tests on Inadequate Core cooling-accident Level Monitor Missed Following 811231 Installation.Surveillance Procedures Generated & Added to schedule.W/830725 Ltr ML20024B7711983-06-17017 June 1983 LER 83-010/03L-0:on 830524,core Topping Pump 121 Removed from Svc to Replace Packing.Caused by Air Leaking Due to Iltr Pressure Introduction in Pump.Packing Replaced & Pump Returned to Svc within 22 h.W/830621 Ltr ML19277C5881983-06-16016 June 1983 LER 83-013/03L-0:on 830610,during Routine Surveillance,Lock Found Missing from Outside Inlet Valve 40-12 for Core Spray Sys.Valve & Breaker in Open Position.Lock Missing for No More than 15 Days.Lock replaced.W/830708 Ltr ML20024B7101983-06-16016 June 1983 LER 83-011/03L-0:on 830604,electromatic Relief Valve 121 Failed to Open.Caused by Dirty Pilot Due to Oxide Buildup During Extended Outage.Pilot Cleaned & Retested & Normal Shutdown initiated.W/830628 Ltr ML20023D9571983-05-24024 May 1983 LER 83-009/03L-0:on 830426,control Room Ventilation Sys Removed from Svc for Mods to Control Room Wall,Per LER 83-06.Temporary Flexible Ducting in Place During Mods. Mods Completed.Ventilation Sys Returned to svc.W/830526 Ltr ML20023D2551983-05-11011 May 1983 LER 83-006/03L-0:on 830411,while Performing Design Review, Discovered That Poured Concrete North & West Walls of Control Room Would Not Meet Original Seismic Criteria. Mods Made to Improve Wall Structural Loading Capabilities ML20023B8321983-04-18018 April 1983 LER 81-053/03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed ML20028C8391983-01-0505 January 1983 LER 82-018/03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20028C8361983-01-0505 January 1983 LER 82-017/03L-0:on 821206,during Maint Outage,Leakage from Valves 68-06 & 68-09 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20027C9681982-10-19019 October 1982 LER 82-001 Has Been Canceled ML17341B6651982-08-0505 August 1982 LER 82-011/03L-0:on 820802,oil Leak on Fuel Oil Supply Manifold Discovered on Diesel Fire Pump.Caused by Defective Braze Joint.Leak Repaired by Manufacturer ML20050N6691982-04-0505 April 1982 LER 82-009/01T-0:on 820323,while Conducting Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on Recirculation Piping.Cause Being Investigated ML20050C3881982-03-29029 March 1982 LER 82-008/01T-0:on 820317,review of Surveillance Test N1-ST-R7 Revealed Potential for Reactor Steam to Leak to Atmosphere from Emergency Condenser Vents.Caused by Potential Sys Leaks.Sys Modified Per NUREG-0737 Item II.B.1 ML20052F8991982-03-24024 March 1982 LER 82-009:on 820323,during Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on 11 Recirculation Piping Suction from Reactor Vessel.Cause Under Investigation ML20042C5041982-03-23023 March 1982 LER 82-006/04L-0:on 820225,during Normal Operation,While Tempering Plant Inlet Canal,Plant Discharge Temp Exceeded 85 F.Caused by Increase in Lake Temp Due to Weather Conditions & Inability to Fully Lower Tempering Gate ML20052F8461982-03-18018 March 1982 LER 82-008:on 820317,discovered Potential Path for Reactor Steam from Emergency Condenser Steam Line Vents to Atmosphere If Emergency Condenser Tube Leaks Occur.Caused by Mods Made to Comply w/NUREG-0737,Item II.B.1 ML20042A6891982-03-12012 March 1982 LER 82-007/04L-0:on 820222,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity Was Determined Not Met for Nov 1981.Cause Not Stated.Tech Spec Proposal Being Submitted to Update Stds ML20049H6101982-02-19019 February 1982 LER 82-005/03L-0:on 820208,115 Kv Line Taken Out of Svc for Maint,Placing Plant in Limited Condition of Operation.Maint on Line Required Due to Open Loop.Line Repaired & Returned to Svc ML20041C1651982-02-19019 February 1982 LER 82-004/01T-0:on 820207,during Routine 115-KV Breaker Exercising,Ground Directional Relay Caused Opening of Breaker Alternate 115-KV.Caused by Momentary Loss Offsite Power.Power Restored After Closing Oswego-NMP1 Breaker ML20041C1171982-02-17017 February 1982 LER 82-003/01T-0:on 820204,at 100% Power,Reactor Bldg Ventilation Sys Isolated & Emergency Ventilation Sys Initiated Due to Radioactive Release.Caused by Overflow of Reactor Water Cleanup Sys Filter Sludge Tank ML20041A7511982-02-10010 February 1982 LER 82-002/01T-0:on 820129,NRC Inspector Discovered That Primary Containment Following DBA LOCA May Not Be Vented Using Operating Procedure Due to Inaccessibility of Reactor Bldg.Combustible Gas Control Sys Will Be Installed ML20052F8961982-02-0808 February 1982 LER 82-004:on 820207,during Steady State Operation,Momentary Loss of 115 Kv Offsite Power Caused Emergency Diesel Generators to auto-start on Low Voltage to Power Boards 102 & 103 ML20052F8981982-02-0505 February 1982 LER 82-003:on 820204,during Steady State Operation,Cleanup Sludge Tank Vent Overflowed Into Reactor Bldg Exhaust Ventilation Sys Causing Emergency Ventilation Sys to Initiate.Cause Not Stated.Decontamination in Progress ML20052F8931982-02-0101 February 1982 LER 82-002:on 820129,during Steady State Power,Upon Review by Resident Inspector,Discovered That Operating Procedure Describing Steps to Vent Primary Containment Following DBA LOCA Required Personnel to Enter Reactor Bldg ML20040B8621982-01-18018 January 1982 LER 81-054/03L-0:on 811221,insertion of Shallow Control Rods Resulted in Average Planar Linear Heat Generation Rate in Excess of Tech Spec Limits.Caused by Flux Coupling Between Control Rods.Extra Rods Inserted & Tech Specs Modified ML20039E2951982-01-0202 January 1982 LER 81-025,is Cancelled ML20039C0951981-12-14014 December 1981 LER 81-053/03L-0:on 811120,emergency Condensers 11 & 12 Were Isolated When Emergency Condenser Vent Radiation Monitor de-energized Due to Loss of Dc Motor Speed Control.Caused by Defective Silicon Controlled Rectifier.Rectifier Replaced ML20038B4971981-11-25025 November 1981 LER 81-008/01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable ML20038B4561981-11-25025 November 1981 LER 81-050/03L-0:on 810715,reactor Bldg Ventilation Duct Radiation Monitor Showed Abnormal Spiking Which Initiated Emergency Ventilation Sys.Caused by Malfunctioning sensor-convertor Unit.Unit Replaced & Calibr ML20038B8801981-11-24024 November 1981 LER 81-052/03L-0:on 810812,failure of One Reactor Vessel Electromatic Relief Valve Thermocouple & Two Reactor Vessel Head Safety Valve Thermocouples Noted in Testing.Cause to Be Investigated Given Drywell Access in Next Cold Shutdown ML20038B7701981-11-24024 November 1981 LER 81-049/03L-0:on 811112,during Normal Operation,Feedwater Hydraulic Snubber 29-HS-6 Taken Out of Svc for Preventative Maint Because of Small Oil Leak.Cause Not Stated.Snubber Rebuilt & Returned to Svc ML20038B4581981-11-20020 November 1981 LER 81-051/04L-0:on 811109,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity (LLD) Not Met.Caused by Higher LLD Values When Test Data Converted from Wet to Dry Weight Units ML20011A4851981-09-30030 September 1981 LER 81-046/04T-0:on 810922,review of 810813 & 14 ETS Semiannual Samples of Cladophora Showed Co-60 & Nb-95 at Level of 10 Times Control Value.Probably Caused by Liquid Effluent Discharge & Oct 1980 Chinese Weapons Test ML20010G6931981-09-10010 September 1981 LER 81-042/04T-0:on 810831,during Weekly Environ Radiation Monitor Insp,Only Six Monitors Found Functioning Due to Defective Power Supply Units.Cause Unknown.Portable Monitor Installed ML20010G4341981-09-0404 September 1981 LER 81-040/03L-0:on 810818,chromated Water Found in Diesel Generator 102 Raw Water Due to Water Leaking Through Heat Exchangers.Cause Unknown.Raw Water Lines Drained & All Chromate Recovered 1998-07-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20154P1821998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20153B2001998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Nmpns,Unit 1.With ML20237C6351998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20236T5911998-07-20020 July 1998 LER 98-S01-00:on 980618,security Force Member Left Nine Mile Point,Unit 2 Vehicle Gate Unattended Without Ensuring,Gate Alarm Had Been Reactivated.Caused by Inadequate Work Practice.Vehicle Gate Alarm Was Activated ML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML20236Q1701998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML20151P1751998-06-16016 June 1998 Rev 0 to SIR-98-067, Evaluation of NMP Unit 2 Feedwater Nozzle-to-Safe End Weld Butter Indication (Weld 2RPV-KB20, N4D) ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML20249B4971998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20198B4991998-05-15015 May 1998 Non-proprietary Replacement Pages for Attachment F to Which Proposed to Change TS 5.5, Storage of Unirradiated & Sf ML20247R1141998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217B0621998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1681998-03-19019 March 1998 Revised Niagara Mohawk Powerchoice Settlement Document for NMPC PSC Case Numbers 94-E-0098 & 94-E-0099, Vols 1 & 2 ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML17059B9051998-02-28028 February 1998 NMP Unit 1 Boat Samples Analyses Part Iii:Tension Tests, RDD:98:55863-004-000:01 1999-09-30
[Table view] |
Text
NRC Form 366 UJ. NUCLEAR REGULATORY COMMISSION (94)3)
APPROVED OMB NO. 3150410l LICENSEE EVENT REPORT (LER) EXPIRES: SI31/65 FACILITY NAME (1) DOCKET NUMBER (2l PA 6 3I o s o o o 410 1 OF 08 Reactor Scram and Emergency Core Cooling System Actuation due to a
,EVENT DATE (5) r Flow Caused b a Desi n Deficienc LER NUMBER (6) REPORT DATE IT) OTHER FACILI1'IES INVOLVED ISI
. SEOVENTIAL MONTH DAY YEAR YEAR +i?2 NIIMSEII T6gp IIIIMSER MONTH DAY YEAR FACILITYNAMES DOCKET NVMBERIS)
N/A 0 5 0 0 0 00 0 12 88 N/A 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUANT T0 THE REGUIREMENTs oF 10 cF R 5: Icnech one or more ot the Ioiiowrnpi (11)
OPERATING MODE (6) 20A02(bl 20A05(c) 60.73(e l(2)osl 73.71III)
POWER 20A06(el)1)D) 50.36(cl(1) 50.73(e I l2 l(v) 73.71(cl LEVEL (10) 20A05 (e I (I) I i) I 60.36(cl(2) 50.73(e I (2((vii) OTHER ISpecify In Abstract below end In Test. HIIC Form 20A06 ( ~ I (1)(E ii) 50.73(el(2) li) 60.73(e l(2)(viEI)(Al 366AI 20A06 ( ~ ) ( I ) (iv) 50,73( ~ l(2)(iil 60.73( ~ I (2)(v i)i I (6 I 20A06(e)(1)(vl 50.73 (e I (2 I (iiil 50.73( ~ l(2) lel I.ICENSEE CONTACT FOR THIS LER (12I NAME TELEPHONE NUMBER AREA CODE Robert E. Jenkins, Assistant Supervisor Technical Support 315 349-.4220
~
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBEO IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANVFAC EPORTABLE MANUFAC. PER TAEEE TVRER TO NPRDS CAUSE SYSTEM COMPONENT E TVRER AD PT R369 Y
~!Nlk kCNRPr)::
SUPPLEMENTAL REPORT EXPECTED (Iel MONTH DAY YEAR EXPECTED SUBMISSION DATE (16)
YES (if yes, compsere EXPECTED SVBMISSIDH DATEI NO ABSTRACT ILImlt to Ie00 speces, I e., epprossmerery Hrreen sinpieepece rypewritren Iiness (16)
On March 13, 1988 at 17:39 with the reactor mode switch in Run (Operational Condition 1) and at a power level of approximately 43K (see note) rated thermal capacity, Nine Mile Point Unit 2 experienced an automatic reactor scram, an automatic initiation of the Division 3 Emergency Core Cooling System (ECCS) with a subsequent coolant injection, and the automatic actuation of several Engineered Safety Features. These events were the result of low water levels in the reactor vessel caused by a total loss of feedwater flow. An Unusual Event declared at 17:45 was terminated by 18:00 that day. The ECCS injection was manually terminated and a normal reactor shutdown was commenced by the NMP2 operators. (NOTE: Reactor power was at 9% two minutes prior to this event.
However, an instrument failure caused the reactor recirculation pumps to downshift to low speed operation, decreasing reactor power to 43K.)
The ir(mediate cause for this event is an equipment failure. However, the root cause for this event is a design deficiency.
The corrective actions for this event are; (1) a temporary modification has been performed to bypass the "seal inH logic for the low pressure heater string outlet isolation valves, (2) a permanent modification will be implemented to reroute the piping for the Second Point Feedwater Heaters level switches, and (3) the failed pressure transmitter, which was replaced with an upgraded model, will be sent to the vendor for a failure mode analysis..
88041c)003S 880012 po~"(~ go 89. IE NRC Form 366 (96>>
NRC form 388A U.S. NUCLEAR REOUI.ATORY COMMISSION (983)
LICENSE VENT REPORT (LER) TEXT CONTINUATION APPROVE 0 OMS NO 3150&(04 EXPIRES: 8/31/88 FACILITYNAME I'l OOCKET NUMBER (2)
LER NUMBER (8) PACE (3)
YEAR SEOVENZ/AL CPu REY SION NVM ER NVMSER Nine Mile Point Unit 2 o 5 o o o 410 88 014 00 02 oF 08 TIKT/8/AINe RMOP N nyule4 Cer aRRFabne/NRC form 3(I/)AS / OT)
I. DESCRIPTION OF EVENT On March 13, 1988 at 17:39 with the reactor mode switch in Run (Operational Condition 1) and at a power level of approximately 434 rated thermal capacity, Nine Mile Point Unit 2 (NMP2) experienced an automatic reactor scram, an automatic initiation of an Emergency Core Cooling System (ECCS), and the automatic actuation of several Engineered Safety Features (ESF). These events were the result of low water levels in the reactor vessel which were caused by a total loss of feedwater flow.
The sequence of events for this incident is as follows:
At 17:37:03, pressure transmitter 2ISC*PT122 failed, causing an erroneous low differential temperature signal for the steam dome/recirculation pump suction interlock. As a result, the Reactor Recirculation Pumps (RCP) automatically downshifted from high speed to low speed operation. Reactor power which was approximately 98K prior to this event decreased to approximately 43K within 15 seconds after the RCP downshift.
Between 17:37:38 and 17:39:00, the sharp reduction in reactor power caused a low pressure condition in the Extraction Steam System (ESS). Reduction in the extraction steam pressure caused steam flashing in the Second Point Feedwater Heaters (SPFH) affecting the level instrumentation for that equipment. This resulted in intermittent false high level signals for several of the low pressure feedwater heaters, which initiated an isolation for two of the low pressure feedwater heater strings. [These spurious signals were of an extremely short duration, typically alarming and cle'aring within one s'econd. However, the outlet isolation valves (2CNM-MOV32A(B,C)) for the low pressure feedwater heater strings have a "seal in" feature requiring only a single instantaneous high level signal to close these valves.]
At 17:39:00, the "A" and "C" low pressure feedwater heater strings were completely i sol ated.
At 17:39:33, the Reactor Feed Pumps (RFP) tripped on a low suction pressure condition. This condition resulted from a reduction of flow'o the RFP's after the "A" and "C" low pressure feedwater heater strings isolated. Tripping of the RFP's resulted in a loss of feedwater flow to the reactor.
At 17:39:38, the reactor water level began to decrease as a result of the loss of feedwater flow. At this time the reactor low water level'Level 4) alarm was annunciated in the NMP2 control room.
NRC FORM 385A
+U.S.OPO:19854.624 538/155 (945)
NRC Form 38SA (083) U.S. NUCLEAR REQULATORY COMMISSION LICENS VENT REPORT (LER) TEXT CONTIN TION APPROVED OMS NO. 3150MI OC EXPIRES: 8/31/88 FACILITY NAME (ll OOCKET NUMBER (2)
LER NUMBER (6) PACE (3)
YEAR 5EQV ENTIAL REVISION NUM S R 'I'N'i NVMSER Nine Mile Point Unit 2 p 6 p p p 410 88 014 00 03 08 TEXT EN'awe <<mco Ir /PSMIoc( oco AEI/ooo/NRC For/I/ 3(/543/ (ITl At 17:39:50, the reactor scramed on a reactor low water level (Level 3) trip.
At 17:39:57, the NMP2 licensed operators placed the reactor mode switch to s hut down.
Due to the continued loss of reactor water inventory (due to boiling by decay heat), reactor water level reached the low-low level trip setpoi nt at 17:40:02.
A reactor low-low water level (Level 2) trip signal was generated (as expected) which initiated the automatic actuation of the following systems:
- 1. The High Pressure Core Spray (HPCS) system (Note: HPCS is a Division 3 ECCS system.)
- 2. The Division 3 Emergency Diesel Generator (EDG2)
- 3. The Reactor Core Isolation Cooling (RCIC) system
- 4. The Division 1 and Division 2 Standby Gas Treatment Systems (GTS)
- 5. The Division l,and Division 2 Reactor Building Ventilation (HVR) Unit Coolers
- 6. Recirculation pump trip
- 7. Alternate Rod Insertion
- 8. The Division 1 Control Building Special Filter Ventilation (HVC) system
- 9. Isolation of the Normal Reactor Building Ventilation system
- 10. The Division 2 HVR Emergency Recirculation Unit Cooler (2HVR*UC413B) ll. Isolation of the primary containment except for the Main Steam Isolation Valves (MSIV's)
(Note: Primary Containment Isolation Valve Groups 4 and 5 isolate on a Level 3 signal.)
At 17:40:04, the HPCS system started to inject water from Condensate Storage Tank (CST) "B" to the reactor vessel. As a result, reactor water level began to increase.
At 17:40:05, EDG2 attained its normal operating parameters. Additionally, the ventilation system for EDG2 automatically started up. (The diesel generator ventilation systems are considered ESF systems.)
At 17:40:15, the RCIC system injected to the reactor from CST "A". As a result of the RCIC injection, a simultaneous Main Turbine-Generator trip was initiated.
NRC PORLI SSSA IS 83) oU.S.OPO.I SSSO 62C 538/455
NRC Form 388A (94)3) US. NUCLEAR REOULATORY COMMISSION LICENSE VENT REPORT (LER) TEXT CONTINUATION APPROVED OMB NO. 3150-0104 EXPIRES: 8/31/88 FACILITY NAME (1) DOCKET NUMBER 12)
LER NUMBER IB) PACE (3)
YEAR C~g BEDVBNTIAL REVISION whV,: NVMBBII NVMBBR Nine Mile Point Unit 2 p p p p p 410 88 014 00 04 oF 08 Tm(T O'AKBB <<>>CB EI /BBVBBB( VBB BIIt/BOn4////IC%%dnn 3()84'4/ (17)
At 17:42:27, the NMP2 operators restored partial feedwater flow to the reactor.
At 17:42:49, the reactor water level was restored to its normal level by the feedwater system and the HPCS and RCIC injections. All low water level annunciation had cleared by this time.
At 17:42:57, the HPCS injection was manually terminated by the NMP2 operators.
At 17:45, in accordance with Eme'rgency Action Procedure EAP-2, an Unusual Event was declared for NMP2. Additionally, the NMP2 operators placed the Scram Discharge Volume (SDV) bypass switches to bypass. (This is done to prevent another scram signal on high SDV water level.)
At 17:48:03, the alternate rod insertion initiation was reset by the NMP2 operators.
At 17:51, the reactor scram was reset by NMP2 operators in accordance with Operating Procedure N2-0P-101C.
At 17:55, NMP2 operators secured the HPCS system.
At 18:00, the Unusual Event was terminated.
At 18:12, the primary containment valve group 6 and 7 isolations were bypassed by Operations in order to place the Reactor Water Cleanup (RWCU) system back into service.
At 18:42, the RCIC injection was secured by the NMP2 Operations Department.
Between 18:43 to 18:50 the Division 1 and Division 2 GTS systems were secured and normal HVR was restored by the NMP2 Operators.
At 19:56, the Main Turbine-Generator trip was reset by the NMP2 Operations Department.
At 23:35, the NMP2 operators secured the Control Building Special Filter Ventilation System.
The duration for this event, from the initial event transient (failure of pressure transmitter 2ISC*PT122) to the termination of the Unusual Event was approximately 23 minutes; It is estimated that approximately 11,500 gallons of water were injected into the reactor vessel by the HPCS system from CST "B".
Add'itionally, it is estimated that the RCIC system supplied approximately 38,000 gallons of water from CST "A" to the reactor vessel. A small increase in reactor water conductivity (well within Technical Specification limits) was noted after this event.
The individual systems and components functioned as designed. There were no other inoperable systems which contributed to this event. No other plant system or component failure resulted from this event.
NRC FORM 344A *U.S.OPO:1985&824 538/455 (94)3)
NRC form SSSA U.S. NUCLEAR RECULATORY COMMISSION 1043)
LICENSE cVENT REPORT (LER) TEXT CONTINUATION APPROVED OMB NO. 3150&104 EXPIRES: B/31/BB PACILITY NAME 11) OOCKET NUMBER )2)
LER NUMBER )S) PACE 13)
YEAR V$) SEOVENTIAL NVM EII
>Mr REVISION I:<5 NOMBEII Nine Mile Point Unit 2 0 5 0 0 0 410 88 014 00 05 OF 08 TEXT %ewe <<>>oo /r /SENSe4 INo EEESOo>>/NRC fonrr SSSES/ )Ill To satisfy the reportability requirement of TS Section 3.5.1(f) the following information is being provided for the ECCS high pressure coolant injection event:
Total accumulated initiation cycles for the HPCS system (from receipt of the NMP2 operating license up to and including the March 13, 1988 event) = 3 The usage factor value for the HPCS injection nozzle (as of March 13, 1988) remains significantly below 0.70.
II. CAUSE OF EVENT The immediate cause for this event was the failure of pressure transmitter 2ISC*PT122. This instrument failure (which i s considered to have been a random incident) generated a spurious signal which caused the RCP's to switch to low speed operation; this in turn caused the sharp reduction in reactor power.
These initial events subsequently led to the reactor scram and the Division 3 ECCS actuation. However, this instrument failure is not considered to be the root cause for this event since the loss of feedwater flow (as it occurred in this event) is not an anticipated result for a transient involving a decrease in the reactor coolant system flow rate. (See the NMP2 Final Safety Analysis .
Report (FSAR) Section 15.3.)
Therefore, the most probable root cause for this event (and for the loss of feedwater flow) is a design deficiency. Spurious high water level signals, generated by the level switches for the SPFH's, initiated the "A" and "C" feedwater heater string isolations. These signals were the result of perturbations (caused by 'steam flashing) in the level switch instrument lines.
LIt is thought that the steam flashing (caused by. the reduction in the ESS system pressure) may have forced water slugs through the sensing lines for the SPFH's level instrumentation.]
Niagara Mohawk Engineering has determined that the physical installation of the sensing lines for the SPFH level instrumentation made these instruments particularly susceptible to the transients caused by steam flashing.
Engineering has concluded that a different installation configuration would make these level switches less susceptible to similar disturbances.
III. ANALYSIS OF EVENT ICOSI This event is considered reportable via 10CFR50.73(a)(2)(iv) because the reactor scram and th'e various safety system actuations (such as the automatic startup of the Division 3 ECCS and of the Division 1 and 2 GTS systems, the automatic alignment of HVR and HVC to their emergency modes, and the primary containment isolation (except for the MSIV's)) were automatic ESF actuations.
NRC FORM OSSA o U.S.CPO:10554-52E 535/455
Perm 388A (883) US. NUCLEAR REOULATORY COMMISSION LICENSEE ENT REPORT (LER) TEXT CONTINUATION APPROVED OMS NO. 3(50-0(04 EXPIRES: 8/31/88 I'ACILITYNAME (1) OOCKET NUMSER 121 LER NUMBER (8) PACE (31 YEAR SEOUENTIA(, >XP REVISION NUMB E R i??3 NUMSER Nine Mile Point Unit 2 p 6 p p p 410 88 014 00 06 OF 08 TE)(T 8'mw Nmoc 4 /CSUN< Imc Redone/NRC Fc/IR 388A'c/ (IT)
A reactor scram occurred on a Level 3 reactor low water level trip as a direct result of the loss of feedwater flow. A reactor scram is a conservative plant response which does not pose any safety consequences. The spectrum of events (which include the Division 3 ECCS and all the ESF actuations discussed above) that occurred as a result of the loss of feedwater flow are bounded within the analysis of the "Loss of Feedwater Flow" event discussed in the FSAR Section 15.2. 7.
Reactor water level decreased slightly below the Level 2 trip setpoint.
(Actually, the lowest water level attained was 100 inches above instrument zero.) HPCS and RCIC initiated as designed at the Level 2 setpoint and injected coolant from the CST's "B" and "A" respectively. Reactor water level was restored to its normal level approximately 3 minutes after the injection comenced. After the reactor water level was restored to normal, operators manually secured the HPCS and RCIC injections.
The temperature difference between the coolant injected i nto the reactor vessel and the reactor coolant was approximately 460 degrees. However, Niagara Mohawk Engineering has determined that the injection did not cause a damaging transient to the reactor components.
The automatic actuation of the HPCS system with a subsequent coolant injection was a conservative plant response with minimal plant impact and no resultant impact on public safety. The HPCS actuation is considered conservative because the ECCS systems are designed to provide timely protection against onset and consequences of conditions that threaten the integrity of the fuel barrier and the Reactor Coolant Pressure Boundary.
The other ESF actuations (i.e., Division 1 and 2 GTS startup, lineup of the HVR and the HVC systems to their emergency modes, and the primary containment isolation) were also conservative plant responses, with minimal plant impact and
. no resultant impact on public safety.
The primary containment valve isolation is considered conservative since the primary objective of the isolation function is to provide protection to the plant'and public by preventing releases of radioactive materials to the envi ronment.
The GTS system is designed; (1) to limit the release of radioactive gases from the RB to the environment within the guidelines of 10CFR100 in the event of a loss of coolant accident and, (2) to maintain a negative pressure in the RB under accident conditions. (The emergency recirculation mode of HVR helps achieve these objectives.) Therefore, an automatic initiation of GTS and the emergency recirculation mode of HVR are considered conservative since their proper function serves to limit and contain radioactive releases from the primary and secondary containments.
NRC CORM SSSA (883) *U.S.OPO:1988&82l 538/455
NRC POIIII 388A (083) U.S. NUCLEAR REOULATORY COMMISSION LICENSEE VENT REPORT (LER) TEXT CONTINUATION APPROVED OMS NO. 3(50W104 EXPIRES: 8/31/88 fACILITYNAME (1) DOCKET NUMBER (2)
LER NUMBER (8) PAGE (3) yEAR gM SEOUENTIAL HUMEER
~riN II1 V IS IO II IIUM E R Nine Mile Point Unit 2 o s o o o 41o 88 014 00 07 OF 08 TSXT (8'aWe Red 8 IFSU)FIS car aESS(Fne/A//IC %%dnII 3///AS / (17)
Finally, the automatic alignment of the HVC system to the special filter, ventilation mode provides monitored and filtered air to the control room under accident conditions. This mode of HVC minimizes the influx of radioactive contaminants into the control room. Therefore, an automatic alignment of HVC to thi s mode of operati on i s a conservati've response.
The elapsed time for the event, from the initial event transient to the termination of the Unusual Event was approximately 23 minutes.
I V. CORRECTIVE ACTIONS (1) To minimize future losses of feedwater flow due to spurious feedwater heater string isolations, a temporary modification (¹88-104) has been implemented to bypass the "seal in" feature for the low pressure feedwater heater string outlet i sol ati on val ves (2CNM-MOV32A(B,C)) . (The decision to remove or to permanently implement this modification will be based upon the operating experience of NMP2.)
(2) As an effort to desensitize the SPFH level transmitters to short term perturbations such as those caused by steam flashing, Modification (PN2Y88MX055) wi 11 be performed rerouting the piping for these instruments. It is anticipated that this modification will be installed no later than the mid-cycle outage (scheduled for September, 1988).
'(3) The failed pressure transmitter (2ISC*PT122), a Rosemount Model ¹1152GP, was replaced with a Rosemount Model ¹1153GB via Work Request (WR
¹138201). This defective transmitter will be sent to the manufacturer for an analysis of its failure mode.
V. ADDITIONAL INFORMATION LER's 88-01 and 88-12 also discuss events where the reactor scrammed on a low water level (Level 3) trip and the Division 3 ECCS system actuated. However, the causes for those events are not similar to the event discussed in this report. Therefore, there are no previous events similar to that discussed in this LER.
Failed Component Identification: . Pressure Transmitter Model ¹1152GP8 Manufacturer - Rosemount Vendor - General Electric (GE)
GE Part Number - 169C8393P882203 NRC FORM 305A (883) e U,S.GPO:10850.824 538/455
NFC Form 388A 083 l U.S. NUCLEAR REOULATORY COMMISSION LICENSE ENT REPORT (LER) TEXT CONTINU ION APPROVEO OM8 NO. 3150-0164 EXPIRES: IU31/88 FACILITYNAME 111 OOCKET NUMSER 12l LER NUMSER (81 PACE 13) yEAR @'C' 8 CUE NTIAL NUM ER ?j9? REVOIQN NUMSER Nine Mile Point Unit 2 o s o 4lO 88 014 00 08 08 o o oF TEXT EEr more <<coo k roEIem5 Ieo aAt5onel NRC Form%54'Fl lITI V. ADDITIONAL INFORMATION (Cont')
Identification of Components Referred to in this LER IEEE 803 IEEE 805 Component EIIS Funct System ID Pressure Transmitter PT AD Level Transmitter LT SJ Reactor Recirculation Pump P AD Feedwater Pump P SJ Low Pressure Feedwater Heater (SPFH) HX SJ .
Piping (Tubing) TBG SJ Diesel Generator DG EK Scram Bypass Switches HS JC Scram Discharge Volume COL AA Isolation Valves (Primary Containment 5 Feedwater Heaters) ISV JM,S J Main Steam Isolation Valves (MSIV's) ISV JM HVR Unit Coolers Cl R VA Condensate Storage Tank TK KA Reactor Mode Switch HS JC Extraction Steam System N/A SE Feedwater System N/A SJ High Pressure Core Spray System N/A BG Reactor Core Isolation Cooling System N/A BN Standby Gas Treatment System N/A BH Reactor Building Ventilation System N/A VA Reactor Water Cleanup System N/A CE Emergency Diesel Generator Ventilation System N/A VJ Control Building Ventil ation System N/A VI Primary Containment N/A NH Reactor Recirculation System N/A, AD NRC FORM 306A *U.S,OPO'.1986&62A 538/455 1843 I
7 NlAGARA NMP 32818 U MOHAWK NIAGARAMOHAWKPOWER CORPORATION/301 PLAINFIELDROAD, SYRACUSE, N.Y. 13212/TELEPHONE (315) 474-1511 April 12, 1988 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Re: Docket No. 50-410 LER 88-14 Gentlemen:
In accordance with 10 CFR 50.73, we hereby submit the following Licensee Event Report:
LER 88-14 Is being submitted in accordance with 10 CFR 50.73
('a)(2)(iv), "Any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)."
A 10CFR50.72 (b)(2)(ii) report was made at 1810 hours0.0209 days <br />0.503 hours <br />0.00299 weeks <br />6.88705e-4 months <br /> on March 13, 1988.
This report was completed in the format designated in NUREG-1022, Supplement 2, dated September 1985.
Very truly yours,
, 6n4 'i Thomas J. P / kins Vice President - Nuclear TJP/POB/meed Attachments cc: Regional Administrator, Region I Sr. Resident Inspector, W. A. Cook
IS