ML20042C504

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LER 82-006/04L-0:on 820225,during Normal Operation,While Tempering Plant Inlet Canal,Plant Discharge Temp Exceeded 85 F.Caused by Increase in Lake Temp Due to Weather Conditions & Inability to Fully Lower Tempering Gate
ML20042C504
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 03/23/1982
From: Mclaughlin K
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20042C499 List:
References
LER-82-006-04L, LER-82-6-4L, NUDOCS 8203310462
Download: ML20042C504 (2)


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LICENSEE EVENT REPORT

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h I O I 2 l l lharinn normal operation, while tempering the plant inlet canal, plant, discharge temperg-Io j al lture exceeded 85 F. This is in violation of Environmental Technical Specification l 1 o 14 l l 2.1.5, which concerns !! cat Treatment of the Circulating Water System. l IT Til l I 10 l E> I l l I C ! 71 l l l o !a l i I 7 8 , 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUSCODE CO*4PONENT CODE SU8 CODE SUSCODE 10191 7 8 lii IF lh Wh Wh l Zl Zl Zl Zl Zl Zlh W@ W@

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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h I i JM l The increase in plant discharge temperature was caused by an increase in lake tempera- 1 i i l ture due to weather conditions. The tempering gate could not be fully lowered to I i 7 l accomodate this condition. Shortly after the temperature increase was noticed, lake l i 3 l temperature decreased, bringing plant discharge temperature within acceptable limits. l gl A review of recording instrumentation revealed that the discharge temperature had l

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1.ER 82-06 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (Continued) been over 85 F for approximately 44 minutes, reaching a peak of 87.3 F. The plant tempering gate will be modified during the next refueling outage to correct this situation.

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