05000220/LER-1982-018-03, /03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest

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/03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest
ML20028C839
Person / Time
Site: Nine Mile Point 
Issue date: 01/05/1983
From: Burgmeier M
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20028C833 List:
References
LER-82-018-03L, LER-82-18-3L, NUDOCS 8301140207
Download: ML20028C839 (1)


LER-1982-018, /03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest
Event date:
Report date:
2201982018R03 - NRC Website

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