ML20247R114

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Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1
ML20247R114
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 04/30/1998
From: Coleman D, Rich Smith
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NMP91470, NUDOCS 9805290077
Download: ML20247R114 (5)


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l NIAGARA MOHAWK GENERATlON BUSINESS GROUP kdP91'4 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 RE:

Nine Mile Point Nu:: lear Station Unit #1 Docket No. 50-220 I

DPR-63

Subject:

Operating Statistics and Shutdowns - April 1998 Gentlemen:

Submitted herewith is the Operating Data Report, Unit Shutdowns and Power Reductions, and a Narrative of Operating Experience for April 1998 for the Nine Mile Point Nuclear Station Unit #1.

l Very truly yours, Robert G. Smith Plant Manager - NMP1 l

/lh Enclosures pc:

H.J. Miller, Regional Administrator, Region 1 B.S. Norris, Senior Resident Inspector

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9 OPERATING DATA REPORT DOCKLT NO.: 50-220 DATE: 5/06/98 PREPARED BY: D. E. Coleman TEL.EPilONE: (315) 349-2558 OPERATING STATUS i

1. Unit Name: Nine Mile Point Unit #1
2. Reporting Period: April 1998 Notes
3. Licensed Thermal Power (MWt):

1850

4. Nameplate Rating (Gross Mwe):

642

5. Design Electrical Rating (Net Mwe):

613

6. Maximum Dependable Capacity (Gross Mwe):

584

7. Maximum Dependable Capacity (Net Mwe):

565 S. If Changes Occur in Capacity Ratings (Items Number 3 through 7) Since Last Report, Give Reasons:

9. Power f.evel To Which Restricted, if Any (Net MWe):
10. Reavms For Restrictions,If Any:

This Month Yr-to-Date Cumulative

11. Ilours in Reporting Period 719.0 2879.0 250,8 %.2
12. Number of Ilours Reactor Was Critical 688.3 2828.3 169,830.7
13. Reactor Reserve Shutdown llours 0

0 1,204.2

14. Ilours Geaerator On-Line 662.2 2822.2 165,801.0
15. Unit Reserve Shutdown llours 0

0 20.4

16. Gross Thermal Energy Generated (MWil) 1,212,877.0 5,168,487.0 282,643,233.0
17. Gross Electrical Energy Generated (MWil) 413,335.0 1,773,176.0 94,126,069.0
18. Net Electrical Enetgy Generated (MWil) 402,787.0 1,727,331.0 91,287.459.0
19. Unit Service Factor 92.1 98.0 66.1
20. Unit Availability Factor 92.1 98.0 66.1 21.' Unit Capacity Factor (Using MDC Net) 99.2 106.2 60.4
22. Unit Capacity Factor (Uning DER Net) 91.4 97.9 58.8
23. Unit Forced Outage Rate 7.9 2.0 22.5 L
24. Shutdowns Scheduled Over Next 6 Months (Type, Date and Duration of Each):
25. If shutdown At End of Report Period, Estimated Date of Startup: May 22,1998

_ _ _ _ _ ________________________ _ _ a

l OPERATING DATA REPORT DOCKET NO.: 50-220 DATE:5/06/98 :

PREPARED BY: D. E. Coleman TELEPilONE: (315) 349-2558 MONTli April 1998 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (Mwe-Net)

(Mwe-Net) 1 617 17 610 2

616 18 610 3

616 19 613 4

613 20 613 5

616 21 614 6

615 22 614 7

615 23 612 8

616 24 613 9

616 25 613 10 611 26 614 11 616 27 612 12 616 28 230 13 615 29 0

L 14 615 30 0

15 614 31 16 610 INSTRUCTIONS On this format, list the average daily unit power level in Mwe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

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NIAGARA MOHAWK POWER CORPORATION NINE MILE POINT NUCLEAR STATION UNIT #1 NARRATIVE OF OPERATING EXPERIENCE The station operated during the month of April 1998 with a Unit Availability Factor of 92.1%

and a Net Design Electrical Capacity Factor of 91.4%. There were no challenges to the Electromatic Relief Valves. Reductions in Capacity Factor were due to a forced outage which started on April 28,1998 @ 1509. The unit was removed frorn service due to inoperability of Control Room Emergency Ventilation System. On April 4,1998, #13 Reactor Recirculation Pump was returned to service following preventive maintenance that

- commenced in March. On April 6,1998, #11 Reactor Recirculation Pump was removed from service due to a failed Tach Generator and was returned to service on April 10,1998.

Other reductions in capacity factor were due to two aborted shutdowns. On April 16,1998, the unit commenced a controlled shutdown due to an identified breach in secondary containment. The shutdown was terminated when the Containment Spray Vent valves were shut. On Apiil 17,1998, the unit commenced a controlled shutdown due to a failed surveillance of Reactor Building Ventilation System Isolation valves. The shutdown was terminated when engineering provided analysis to restore operability. Both events resulted in minimalloss of generation.

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