ML20207G267

From kanterella
Jump to navigation Jump to search
Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch
ML20207G267
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 03/01/1999
From: Rich Smith
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NMP1L-1413, NUDOCS 9903120037
Download: ML20207G267 (2)


Text

_ _ _

~

7 uiagaragmona.u-March 1, 1999 NMPIL 1413 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 RE:

Nine Mile Point Unit 1 Docket No. 50-220 DPR-63

Subject:

Special Report Gentlemen:

In accordance with Nine Mile Point Unit 1 (NMP1) Technical Specification Table 3.6.11-1,

" Accident. 'onitoring Instrumentation," and associated Action Statement 4.a, Niagara Mohawk Power Corporation (NMPC) is submitting rhe following Special Report concerning the inoperability of ',he #12 Containment Hydrogen Monitoring System (HMS).

Desniotion of Event On February 15,1999, at 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, with the reactor mode switch in the "RUN" position during normal operations, NMP1 Operators declared the #12 HMS inoperable because flow switch FS-201.2-1495 failed to initiate an alarm for an indicated sample low fic,w condition.

Operators adjusted the sample flow rate to the required range, and then removed the #12 HMS from service to troubleshoot the flow sv/ itch.

Cause of Erttd NMP1 Maintenance personnel determined that the cause of the failure was a degraded encapsulated reed switch within flow switch FS-201.2-1495.

O NMP1 Maintenance personnel performed a review of the Deviation / Event Report and work convol databases and concluded that there have been no similar failures of flow switch FS-201.2-1495 or the #11 HMS flow switch, FS-201.2-1493.

The cause of the sample low flow condition has not yet been determined.

e i

b" 9903120037 990301 7 PDR ADOCK 050CO2204 S

PDR Nir.e Mile Point Nuclear Station, P0. Box 63,lycoming, New York 130934063 + 315.343.2110

  • www.nimo.com

E l

~

,t Page 2, i

Cometive Actions NMP1 Instrument and Control Technicians replaced flow switch FS-201.2-1495 and satisfactorily tested the switch on February 22,1999.

HMP1 Operators returned the #12 HMS to service at 1420 hours0.0164 days <br />0.394 hours <br />0.00235 weeks <br />5.4031e-4 months <br /> on February 22,1999.

NMPC will investigate the low flow condition and submit a supplement to this report when the cause has been determined.

1 Very truly yours, Robert G. Smith Plant Manager - NMP1 RGS/KLIJkap xc:

Regional Administrator, Region I Mr. Gordon K. Hunegs, Senior Resident Inspector Records Management I

I l

i 1

4 4

g.