ML20028C836

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LER 82-017/03L-0:on 821206,during Maint Outage,Leakage from Valves 68-06 & 68-09 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest
ML20028C836
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 01/05/1983
From: Burgmeier M
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20028C833 List:
References
LER-82-017-03L, LER-82-17-3L, NUDOCS 8301140199
Download: ML20028C836 (1)


Text

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I o 2 l Durino a maior maintenance outage while performing leakage testing, leakage from l o 3 l valves 68-0'6 and 68-09 were found to exceed Technical Specifications. These two l  ;

n 4 l' valves are tested simultaneously. LERs 79-05, 79-10, 81-09, 81-22, 81-23 and 82-18 l

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47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i O l Failure is attributed to poor seal design. A modification from the vendors (Attwood l )

i i land hforril for valve 68-06, Allis Chalmers for valve 68-09) is availabic. Modificationi i 2 l of these valves will be completed during the current outage and followed by a retest. I i 3 l l t 4 l l 7 s 9

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NAME OF PREPARER bl. Burgmeier (315) 349-2616 PHONE:

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