05000220/LER-1981-053-03, /03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed

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/03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed
ML20023B832
Person / Time
Site: Nine Mile Point 
Issue date: 04/18/1983
From: Randall R
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20023B831 List:
References
LER-81-053-03L, LER-81-53-3L, NUDOCS 8305060428
Download: ML20023B832 (1)


LER-1981-053, /03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed
Event date:
Report date:
2201981053R03 - NRC Website

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