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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML18040A2851993-12-0808 December 1993 LER 93-010-00:on 931108,HPCS Was Inoperable Due to Equipment Deficiency,Inadequate Managerial Methods & Poor Work Practices.Replaced Deficient Contactors & Restored Tap Setting.Also Reportable Per Part 21.W/931208 Ltr ML18038A3191990-08-10010 August 1990 LER 90-006-00:on 891027,discovered Unverified Assumption in App R Safe Shutdown Analysis.Caused by Fire Protection Program Failure to Provide Detailed Procedural Instructions for Operator Actions.New Procedures developed.W/900810 Ltr ML18038A4701989-05-15015 May 1989 LER 89-014-00:on 890413,unit Reactor Experienced Reactor Scram Which Was Result of Turbine Trip Due to Actuation of Generator Protection Circuitry.Turbine Trip Caused by Disconnected Wire.Wire relanded.W/890515 Ltr ML18038A4131988-08-22022 August 1988 LER 88-051-01:on 870813,shutdown Cooling Sys Isolated & Tech Specs 3.4.9.2 Exceeded.Caused by Equipment Failure,Personnel Error & Procedural & Design Deficiencies.Shutdown Cooling Sys Manually restored.W/880822 Ltr ML18038A4051988-07-0101 July 1988 LER 88-024-00:on 880605,ESF Actuation Occurred Due to Resetting of Failed Radiation Monitor Microcomputer.Caused by Lack of Personnel Training.Defective Cards & Modules in RE14B Microcomputer & DRMS Panel replaced.W/880701 Ltr ML18038A3901988-04-12012 April 1988 LER 88-014-00:on 880313,reactor Scram & ESF Actuations Occurred.Caused by Equipment Failure Due to Design Deficiency.Transmitter Replaced W/Upgraded Model & Temporary Mod Performed to Bypass Logic for valves.W/880412 Ltr ML18038A3891988-02-17017 February 1988 LER 88-001-00:on 880120,reactor Scram Occurred Due to Actual Low Water Level Condition.Caused by Design & Personnel Errors.Operator Disciplined & Mod Addressed Inadvertent Feedwater Control Valve lockup.W/880217 Ltr ML18038A7591987-12-22022 December 1987 LER 87-023-00:on 870422,trip of Normal Reactor Bldg Ventilation & Initiation of Emergency Ventilation Occurred. Caused by Personnel Error.Fuse Replaced.On 871123,util Discovered LER Not Submitted for event.W/871222 Ltr ML18038A2581987-06-15015 June 1987 LER 87-025-00:on 870519,secondary Containment Isolation Signal Generated Due to Technician Relanding Lifted Lead Prematurely.Caused by Breakdown in Communications.Gaitronics Phone &/Or Headset Jack installed.W/870615 Ltr ML18004C0061987-04-13013 April 1987 LER 86-002-01:on 861104,procedure N2-OSP-RMC-W0002 Ran for Over 2 H Thereby Violating Tech Specs.Caused by Personnel Error & Procedure Deficiency.Temporary Change Notice Issued to procedure.W/870413 Ltr ML20024E8331983-08-16016 August 1983 LER 83-021/03L-0:on 830720,22,26 & 28,emergency Cooling Sys Loop 11 Taken Out of Svc for Periods Up to 5 H.Caused by Attempt to Reseat Isolation Valve 39-05.Valve Seat Lapped & Loop Returned to svc.W/830819 Ltr ML20024E6341983-08-0202 August 1983 LER 83-017/03L-0:on 830707,HPCI Feedwater Booster Pumps 11 & 13 Taken Out to Svc to Inspect Impellers Due to Similar Problem on nonsafety-related Pump.Parts of Strainer Found in Pumps But Pumps undamaged.W/830805 Ltr ML20024E0251983-07-22022 July 1983 LER 83-019/03L-0:on 830623,two Monthly Surveillance Tests on Inadequate Core cooling-accident Level Monitor Missed Following 811231 Installation.Surveillance Procedures Generated & Added to schedule.W/830725 Ltr ML20024B7711983-06-17017 June 1983 LER 83-010/03L-0:on 830524,core Topping Pump 121 Removed from Svc to Replace Packing.Caused by Air Leaking Due to Iltr Pressure Introduction in Pump.Packing Replaced & Pump Returned to Svc within 22 h.W/830621 Ltr ML19277C5881983-06-16016 June 1983 LER 83-013/03L-0:on 830610,during Routine Surveillance,Lock Found Missing from Outside Inlet Valve 40-12 for Core Spray Sys.Valve & Breaker in Open Position.Lock Missing for No More than 15 Days.Lock replaced.W/830708 Ltr ML20024B7101983-06-16016 June 1983 LER 83-011/03L-0:on 830604,electromatic Relief Valve 121 Failed to Open.Caused by Dirty Pilot Due to Oxide Buildup During Extended Outage.Pilot Cleaned & Retested & Normal Shutdown initiated.W/830628 Ltr ML20023D9571983-05-24024 May 1983 LER 83-009/03L-0:on 830426,control Room Ventilation Sys Removed from Svc for Mods to Control Room Wall,Per LER 83-06.Temporary Flexible Ducting in Place During Mods. Mods Completed.Ventilation Sys Returned to svc.W/830526 Ltr ML20023D2551983-05-11011 May 1983 LER 83-006/03L-0:on 830411,while Performing Design Review, Discovered That Poured Concrete North & West Walls of Control Room Would Not Meet Original Seismic Criteria. Mods Made to Improve Wall Structural Loading Capabilities ML20023B8321983-04-18018 April 1983 LER 81-053/03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed ML20028C8391983-01-0505 January 1983 LER 82-018/03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20028C8361983-01-0505 January 1983 LER 82-017/03L-0:on 821206,during Maint Outage,Leakage from Valves 68-06 & 68-09 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20027C9681982-10-19019 October 1982 LER 82-001 Has Been Canceled ML17341B6651982-08-0505 August 1982 LER 82-011/03L-0:on 820802,oil Leak on Fuel Oil Supply Manifold Discovered on Diesel Fire Pump.Caused by Defective Braze Joint.Leak Repaired by Manufacturer ML20050N6691982-04-0505 April 1982 LER 82-009/01T-0:on 820323,while Conducting Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on Recirculation Piping.Cause Being Investigated ML20050C3881982-03-29029 March 1982 LER 82-008/01T-0:on 820317,review of Surveillance Test N1-ST-R7 Revealed Potential for Reactor Steam to Leak to Atmosphere from Emergency Condenser Vents.Caused by Potential Sys Leaks.Sys Modified Per NUREG-0737 Item II.B.1 ML20052F8991982-03-24024 March 1982 LER 82-009:on 820323,during Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on 11 Recirculation Piping Suction from Reactor Vessel.Cause Under Investigation ML20042C5041982-03-23023 March 1982 LER 82-006/04L-0:on 820225,during Normal Operation,While Tempering Plant Inlet Canal,Plant Discharge Temp Exceeded 85 F.Caused by Increase in Lake Temp Due to Weather Conditions & Inability to Fully Lower Tempering Gate ML20052F8461982-03-18018 March 1982 LER 82-008:on 820317,discovered Potential Path for Reactor Steam from Emergency Condenser Steam Line Vents to Atmosphere If Emergency Condenser Tube Leaks Occur.Caused by Mods Made to Comply w/NUREG-0737,Item II.B.1 ML20042A6891982-03-12012 March 1982 LER 82-007/04L-0:on 820222,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity Was Determined Not Met for Nov 1981.Cause Not Stated.Tech Spec Proposal Being Submitted to Update Stds ML20049H6101982-02-19019 February 1982 LER 82-005/03L-0:on 820208,115 Kv Line Taken Out of Svc for Maint,Placing Plant in Limited Condition of Operation.Maint on Line Required Due to Open Loop.Line Repaired & Returned to Svc ML20041C1651982-02-19019 February 1982 LER 82-004/01T-0:on 820207,during Routine 115-KV Breaker Exercising,Ground Directional Relay Caused Opening of Breaker Alternate 115-KV.Caused by Momentary Loss Offsite Power.Power Restored After Closing Oswego-NMP1 Breaker ML20041C1171982-02-17017 February 1982 LER 82-003/01T-0:on 820204,at 100% Power,Reactor Bldg Ventilation Sys Isolated & Emergency Ventilation Sys Initiated Due to Radioactive Release.Caused by Overflow of Reactor Water Cleanup Sys Filter Sludge Tank ML20041A7511982-02-10010 February 1982 LER 82-002/01T-0:on 820129,NRC Inspector Discovered That Primary Containment Following DBA LOCA May Not Be Vented Using Operating Procedure Due to Inaccessibility of Reactor Bldg.Combustible Gas Control Sys Will Be Installed ML20052F8961982-02-0808 February 1982 LER 82-004:on 820207,during Steady State Operation,Momentary Loss of 115 Kv Offsite Power Caused Emergency Diesel Generators to auto-start on Low Voltage to Power Boards 102 & 103 ML20052F8981982-02-0505 February 1982 LER 82-003:on 820204,during Steady State Operation,Cleanup Sludge Tank Vent Overflowed Into Reactor Bldg Exhaust Ventilation Sys Causing Emergency Ventilation Sys to Initiate.Cause Not Stated.Decontamination in Progress ML20052F8931982-02-0101 February 1982 LER 82-002:on 820129,during Steady State Power,Upon Review by Resident Inspector,Discovered That Operating Procedure Describing Steps to Vent Primary Containment Following DBA LOCA Required Personnel to Enter Reactor Bldg ML20040B8621982-01-18018 January 1982 LER 81-054/03L-0:on 811221,insertion of Shallow Control Rods Resulted in Average Planar Linear Heat Generation Rate in Excess of Tech Spec Limits.Caused by Flux Coupling Between Control Rods.Extra Rods Inserted & Tech Specs Modified ML20039E2951982-01-0202 January 1982 LER 81-025,is Cancelled ML20039C0951981-12-14014 December 1981 LER 81-053/03L-0:on 811120,emergency Condensers 11 & 12 Were Isolated When Emergency Condenser Vent Radiation Monitor de-energized Due to Loss of Dc Motor Speed Control.Caused by Defective Silicon Controlled Rectifier.Rectifier Replaced ML20038B4971981-11-25025 November 1981 LER 81-008/01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable ML20038B4561981-11-25025 November 1981 LER 81-050/03L-0:on 810715,reactor Bldg Ventilation Duct Radiation Monitor Showed Abnormal Spiking Which Initiated Emergency Ventilation Sys.Caused by Malfunctioning sensor-convertor Unit.Unit Replaced & Calibr ML20038B8801981-11-24024 November 1981 LER 81-052/03L-0:on 810812,failure of One Reactor Vessel Electromatic Relief Valve Thermocouple & Two Reactor Vessel Head Safety Valve Thermocouples Noted in Testing.Cause to Be Investigated Given Drywell Access in Next Cold Shutdown ML20038B7701981-11-24024 November 1981 LER 81-049/03L-0:on 811112,during Normal Operation,Feedwater Hydraulic Snubber 29-HS-6 Taken Out of Svc for Preventative Maint Because of Small Oil Leak.Cause Not Stated.Snubber Rebuilt & Returned to Svc ML20038B4581981-11-20020 November 1981 LER 81-051/04L-0:on 811109,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity (LLD) Not Met.Caused by Higher LLD Values When Test Data Converted from Wet to Dry Weight Units ML20011A4851981-09-30030 September 1981 LER 81-046/04T-0:on 810922,review of 810813 & 14 ETS Semiannual Samples of Cladophora Showed Co-60 & Nb-95 at Level of 10 Times Control Value.Probably Caused by Liquid Effluent Discharge & Oct 1980 Chinese Weapons Test ML20010G6931981-09-10010 September 1981 LER 81-042/04T-0:on 810831,during Weekly Environ Radiation Monitor Insp,Only Six Monitors Found Functioning Due to Defective Power Supply Units.Cause Unknown.Portable Monitor Installed ML20010G4341981-09-0404 September 1981 LER 81-040/03L-0:on 810818,chromated Water Found in Diesel Generator 102 Raw Water Due to Water Leaking Through Heat Exchangers.Cause Unknown.Raw Water Lines Drained & All Chromate Recovered 1998-07-02
[Table view] Category:RO)
MONTHYEARML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML18040A2851993-12-0808 December 1993 LER 93-010-00:on 931108,HPCS Was Inoperable Due to Equipment Deficiency,Inadequate Managerial Methods & Poor Work Practices.Replaced Deficient Contactors & Restored Tap Setting.Also Reportable Per Part 21.W/931208 Ltr ML18038A3191990-08-10010 August 1990 LER 90-006-00:on 891027,discovered Unverified Assumption in App R Safe Shutdown Analysis.Caused by Fire Protection Program Failure to Provide Detailed Procedural Instructions for Operator Actions.New Procedures developed.W/900810 Ltr ML18038A4701989-05-15015 May 1989 LER 89-014-00:on 890413,unit Reactor Experienced Reactor Scram Which Was Result of Turbine Trip Due to Actuation of Generator Protection Circuitry.Turbine Trip Caused by Disconnected Wire.Wire relanded.W/890515 Ltr ML18038A4131988-08-22022 August 1988 LER 88-051-01:on 870813,shutdown Cooling Sys Isolated & Tech Specs 3.4.9.2 Exceeded.Caused by Equipment Failure,Personnel Error & Procedural & Design Deficiencies.Shutdown Cooling Sys Manually restored.W/880822 Ltr ML18038A4051988-07-0101 July 1988 LER 88-024-00:on 880605,ESF Actuation Occurred Due to Resetting of Failed Radiation Monitor Microcomputer.Caused by Lack of Personnel Training.Defective Cards & Modules in RE14B Microcomputer & DRMS Panel replaced.W/880701 Ltr ML18038A3901988-04-12012 April 1988 LER 88-014-00:on 880313,reactor Scram & ESF Actuations Occurred.Caused by Equipment Failure Due to Design Deficiency.Transmitter Replaced W/Upgraded Model & Temporary Mod Performed to Bypass Logic for valves.W/880412 Ltr ML18038A3891988-02-17017 February 1988 LER 88-001-00:on 880120,reactor Scram Occurred Due to Actual Low Water Level Condition.Caused by Design & Personnel Errors.Operator Disciplined & Mod Addressed Inadvertent Feedwater Control Valve lockup.W/880217 Ltr ML18038A7591987-12-22022 December 1987 LER 87-023-00:on 870422,trip of Normal Reactor Bldg Ventilation & Initiation of Emergency Ventilation Occurred. Caused by Personnel Error.Fuse Replaced.On 871123,util Discovered LER Not Submitted for event.W/871222 Ltr ML18038A2581987-06-15015 June 1987 LER 87-025-00:on 870519,secondary Containment Isolation Signal Generated Due to Technician Relanding Lifted Lead Prematurely.Caused by Breakdown in Communications.Gaitronics Phone &/Or Headset Jack installed.W/870615 Ltr ML18004C0061987-04-13013 April 1987 LER 86-002-01:on 861104,procedure N2-OSP-RMC-W0002 Ran for Over 2 H Thereby Violating Tech Specs.Caused by Personnel Error & Procedure Deficiency.Temporary Change Notice Issued to procedure.W/870413 Ltr ML20024E8331983-08-16016 August 1983 LER 83-021/03L-0:on 830720,22,26 & 28,emergency Cooling Sys Loop 11 Taken Out of Svc for Periods Up to 5 H.Caused by Attempt to Reseat Isolation Valve 39-05.Valve Seat Lapped & Loop Returned to svc.W/830819 Ltr ML20024E6341983-08-0202 August 1983 LER 83-017/03L-0:on 830707,HPCI Feedwater Booster Pumps 11 & 13 Taken Out to Svc to Inspect Impellers Due to Similar Problem on nonsafety-related Pump.Parts of Strainer Found in Pumps But Pumps undamaged.W/830805 Ltr ML20024E0251983-07-22022 July 1983 LER 83-019/03L-0:on 830623,two Monthly Surveillance Tests on Inadequate Core cooling-accident Level Monitor Missed Following 811231 Installation.Surveillance Procedures Generated & Added to schedule.W/830725 Ltr ML20024B7711983-06-17017 June 1983 LER 83-010/03L-0:on 830524,core Topping Pump 121 Removed from Svc to Replace Packing.Caused by Air Leaking Due to Iltr Pressure Introduction in Pump.Packing Replaced & Pump Returned to Svc within 22 h.W/830621 Ltr ML19277C5881983-06-16016 June 1983 LER 83-013/03L-0:on 830610,during Routine Surveillance,Lock Found Missing from Outside Inlet Valve 40-12 for Core Spray Sys.Valve & Breaker in Open Position.Lock Missing for No More than 15 Days.Lock replaced.W/830708 Ltr ML20024B7101983-06-16016 June 1983 LER 83-011/03L-0:on 830604,electromatic Relief Valve 121 Failed to Open.Caused by Dirty Pilot Due to Oxide Buildup During Extended Outage.Pilot Cleaned & Retested & Normal Shutdown initiated.W/830628 Ltr ML20023D9571983-05-24024 May 1983 LER 83-009/03L-0:on 830426,control Room Ventilation Sys Removed from Svc for Mods to Control Room Wall,Per LER 83-06.Temporary Flexible Ducting in Place During Mods. Mods Completed.Ventilation Sys Returned to svc.W/830526 Ltr ML20023D2551983-05-11011 May 1983 LER 83-006/03L-0:on 830411,while Performing Design Review, Discovered That Poured Concrete North & West Walls of Control Room Would Not Meet Original Seismic Criteria. Mods Made to Improve Wall Structural Loading Capabilities ML20023B8321983-04-18018 April 1983 LER 81-053/03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed ML20028C8391983-01-0505 January 1983 LER 82-018/03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20028C8361983-01-0505 January 1983 LER 82-017/03L-0:on 821206,during Maint Outage,Leakage from Valves 68-06 & 68-09 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20027C9681982-10-19019 October 1982 LER 82-001 Has Been Canceled ML17341B6651982-08-0505 August 1982 LER 82-011/03L-0:on 820802,oil Leak on Fuel Oil Supply Manifold Discovered on Diesel Fire Pump.Caused by Defective Braze Joint.Leak Repaired by Manufacturer ML20050N6691982-04-0505 April 1982 LER 82-009/01T-0:on 820323,while Conducting Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on Recirculation Piping.Cause Being Investigated ML20050C3881982-03-29029 March 1982 LER 82-008/01T-0:on 820317,review of Surveillance Test N1-ST-R7 Revealed Potential for Reactor Steam to Leak to Atmosphere from Emergency Condenser Vents.Caused by Potential Sys Leaks.Sys Modified Per NUREG-0737 Item II.B.1 ML20052F8991982-03-24024 March 1982 LER 82-009:on 820323,during Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on 11 Recirculation Piping Suction from Reactor Vessel.Cause Under Investigation ML20042C5041982-03-23023 March 1982 LER 82-006/04L-0:on 820225,during Normal Operation,While Tempering Plant Inlet Canal,Plant Discharge Temp Exceeded 85 F.Caused by Increase in Lake Temp Due to Weather Conditions & Inability to Fully Lower Tempering Gate ML20052F8461982-03-18018 March 1982 LER 82-008:on 820317,discovered Potential Path for Reactor Steam from Emergency Condenser Steam Line Vents to Atmosphere If Emergency Condenser Tube Leaks Occur.Caused by Mods Made to Comply w/NUREG-0737,Item II.B.1 ML20042A6891982-03-12012 March 1982 LER 82-007/04L-0:on 820222,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity Was Determined Not Met for Nov 1981.Cause Not Stated.Tech Spec Proposal Being Submitted to Update Stds ML20049H6101982-02-19019 February 1982 LER 82-005/03L-0:on 820208,115 Kv Line Taken Out of Svc for Maint,Placing Plant in Limited Condition of Operation.Maint on Line Required Due to Open Loop.Line Repaired & Returned to Svc ML20041C1651982-02-19019 February 1982 LER 82-004/01T-0:on 820207,during Routine 115-KV Breaker Exercising,Ground Directional Relay Caused Opening of Breaker Alternate 115-KV.Caused by Momentary Loss Offsite Power.Power Restored After Closing Oswego-NMP1 Breaker ML20041C1171982-02-17017 February 1982 LER 82-003/01T-0:on 820204,at 100% Power,Reactor Bldg Ventilation Sys Isolated & Emergency Ventilation Sys Initiated Due to Radioactive Release.Caused by Overflow of Reactor Water Cleanup Sys Filter Sludge Tank ML20041A7511982-02-10010 February 1982 LER 82-002/01T-0:on 820129,NRC Inspector Discovered That Primary Containment Following DBA LOCA May Not Be Vented Using Operating Procedure Due to Inaccessibility of Reactor Bldg.Combustible Gas Control Sys Will Be Installed ML20052F8961982-02-0808 February 1982 LER 82-004:on 820207,during Steady State Operation,Momentary Loss of 115 Kv Offsite Power Caused Emergency Diesel Generators to auto-start on Low Voltage to Power Boards 102 & 103 ML20052F8981982-02-0505 February 1982 LER 82-003:on 820204,during Steady State Operation,Cleanup Sludge Tank Vent Overflowed Into Reactor Bldg Exhaust Ventilation Sys Causing Emergency Ventilation Sys to Initiate.Cause Not Stated.Decontamination in Progress ML20052F8931982-02-0101 February 1982 LER 82-002:on 820129,during Steady State Power,Upon Review by Resident Inspector,Discovered That Operating Procedure Describing Steps to Vent Primary Containment Following DBA LOCA Required Personnel to Enter Reactor Bldg ML20040B8621982-01-18018 January 1982 LER 81-054/03L-0:on 811221,insertion of Shallow Control Rods Resulted in Average Planar Linear Heat Generation Rate in Excess of Tech Spec Limits.Caused by Flux Coupling Between Control Rods.Extra Rods Inserted & Tech Specs Modified ML20039E2951982-01-0202 January 1982 LER 81-025,is Cancelled ML20039C0951981-12-14014 December 1981 LER 81-053/03L-0:on 811120,emergency Condensers 11 & 12 Were Isolated When Emergency Condenser Vent Radiation Monitor de-energized Due to Loss of Dc Motor Speed Control.Caused by Defective Silicon Controlled Rectifier.Rectifier Replaced ML20038B4971981-11-25025 November 1981 LER 81-008/01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable ML20038B4561981-11-25025 November 1981 LER 81-050/03L-0:on 810715,reactor Bldg Ventilation Duct Radiation Monitor Showed Abnormal Spiking Which Initiated Emergency Ventilation Sys.Caused by Malfunctioning sensor-convertor Unit.Unit Replaced & Calibr ML20038B8801981-11-24024 November 1981 LER 81-052/03L-0:on 810812,failure of One Reactor Vessel Electromatic Relief Valve Thermocouple & Two Reactor Vessel Head Safety Valve Thermocouples Noted in Testing.Cause to Be Investigated Given Drywell Access in Next Cold Shutdown ML20038B7701981-11-24024 November 1981 LER 81-049/03L-0:on 811112,during Normal Operation,Feedwater Hydraulic Snubber 29-HS-6 Taken Out of Svc for Preventative Maint Because of Small Oil Leak.Cause Not Stated.Snubber Rebuilt & Returned to Svc ML20038B4581981-11-20020 November 1981 LER 81-051/04L-0:on 811109,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity (LLD) Not Met.Caused by Higher LLD Values When Test Data Converted from Wet to Dry Weight Units ML20011A4851981-09-30030 September 1981 LER 81-046/04T-0:on 810922,review of 810813 & 14 ETS Semiannual Samples of Cladophora Showed Co-60 & Nb-95 at Level of 10 Times Control Value.Probably Caused by Liquid Effluent Discharge & Oct 1980 Chinese Weapons Test ML20010G6931981-09-10010 September 1981 LER 81-042/04T-0:on 810831,during Weekly Environ Radiation Monitor Insp,Only Six Monitors Found Functioning Due to Defective Power Supply Units.Cause Unknown.Portable Monitor Installed ML20010G4341981-09-0404 September 1981 LER 81-040/03L-0:on 810818,chromated Water Found in Diesel Generator 102 Raw Water Due to Water Leaking Through Heat Exchangers.Cause Unknown.Raw Water Lines Drained & All Chromate Recovered 1998-07-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20154P1821998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20153B2001998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Nmpns,Unit 1.With ML20237C6351998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20236T5911998-07-20020 July 1998 LER 98-S01-00:on 980618,security Force Member Left Nine Mile Point,Unit 2 Vehicle Gate Unattended Without Ensuring,Gate Alarm Had Been Reactivated.Caused by Inadequate Work Practice.Vehicle Gate Alarm Was Activated ML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML20236Q1701998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML20151P1751998-06-16016 June 1998 Rev 0 to SIR-98-067, Evaluation of NMP Unit 2 Feedwater Nozzle-to-Safe End Weld Butter Indication (Weld 2RPV-KB20, N4D) ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML20249B4971998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20198B4991998-05-15015 May 1998 Non-proprietary Replacement Pages for Attachment F to Which Proposed to Change TS 5.5, Storage of Unirradiated & Sf ML20247R1141998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217B0621998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1681998-03-19019 March 1998 Revised Niagara Mohawk Powerchoice Settlement Document for NMPC PSC Case Numbers 94-E-0098 & 94-E-0099, Vols 1 & 2 ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML17059B9051998-02-28028 February 1998 NMP Unit 1 Boat Samples Analyses Part Iii:Tension Tests, RDD:98:55863-004-000:01 1999-09-30
[Table view] |
Text
ACCELERATED DISIBUTION DEMONSTRATION SYSTEM I
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9008240177 DOC.DATE: 90/08/10 NOTARIZED: NO FACIL:50-220 Nine Mile Point Nuclear Station, Unit 1, Niagara Powe 05000220 AUTH. NAME AUTHOR AFFILIATION BELLER,R.
FIRLIT,J.F.
RECIP.NAME AFFILIATION'OCKET Niagara Mohawk Power Corp.
Niagara Mohawk Power Corp.
RECIPIENT
SUBJECT:
LER 90-006-00:on 891027,unverified assumption in App R safe shutdown analysis.
W/9 ltr. D DISTRIBUTION CODE IE22T COPIES RECEIVED'LTR 50.73/50.9 Licensee Event Report (LER),
ENCL L ncident Rpt, etc.SIZE'ITLE:
NOTES:
RECIPIENT COPIES }RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PDl-1 LA 1 1 PD1-1 PD 1 1 MARTIN,R. 1 1 D INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA AEOD/ROAB/DS P 1 .12 AEOD/DSP/TPAB 1 1 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 I4RR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 N SPLB8D1 1 1 NRR/DST/SRXB 8E 1 1 - GAL 1 1 RES/DSIR/EIB 1 1 FILE'2'GN1 01 1. 1 EXTERNAL EGGG BRYCE g J H 3 3 L ST LOBBY WARD 1 1
~ LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 R I
D A
D D
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 34 ENCL 34
'II'IASARA.
U SKNAWK NINE MILE POINT NUCLEAR STATION/P.O. BOX 32, LYCOMING.N.Y. 13093/TELEPHONE (315) 343-2110 NMP70166 August ]p , 1990 United States Nuclear Regulatory Commission Document. Control Desk Washington, DC 20555 RE: Docket No. 50-220 LER 90-06 Gentlemen:
In accordance with 10 CFR 50.73, we hereby submit the following voluntary Licensee Event Report: LER 90-06.
This report was completed in the format designated in NUREG-1022, Supplement 2, dated September 1985.
Very truly yours, oseph F. Firlit Vice President Nuclear Generation JFF/DS/lmc ATTACHMENT ZC Regional Administrator, Region I Sr. Resident Inspector, W. A. Cook g (775'46 9008200177 900'"10 PDR ADOCK 05000220 S PDC
il
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (64) 9) APPROVED 0MB NO. 3'I 500104 EXP IR ES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS, FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL "<<OP REVISION NUM ER '<<PB NUMSER Nine Mile Point Unit 1 o 5 o'o o 220 90 0 6 0 0 0 2OF 07 TEXT /// more 4/rece /4 rer)rr/rerL Iree tChdonel HRC Form 366A'4) (IT)
I. DESCRIPTION OF CONDITION On October 27, 1989, with Nine Mile Point; Uni.'t 1 (NMP1) in cold shutdown and the core off-loaded, assumption made on the Appendix R Safe Shutdown Analysis (SSA) it was discovered that an could not be verified. Specifically, operator actions to complete specific load shedding; to ensure battery capacity to start -a Diesel Generator (DG) at the conclusion of the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> Appendix R scenario; was not identified in applicable 'procedures. This condition was identified during corrective actions, being carried out as part of the NMPl Restart Action Plan (RAP), Specific Issue 18 (125 VDC system concerns).
The NMP1 Appendix R SSA, Rev. 0 and Rev. 1, dated October 1982 and September 1985, respectively, describes NMP1's ability to satisfy the specific requirements of 10CFR50 Appendix R Section III.G. The event in question's any postulated fire that has the potential to cause a loss of both emergency diesel generators (concurrent with a simultaneous Loss Of Off-Site Power;.(LOOP) for-up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />)..
The analysis credits the redundant ec((ergency condenser -system as providing hot shutdown capability automatically (via the shutdown supervisory control system) for up to eight hours without make-up and the Reactor Protection System (RPS) Motor Generator (MG) Sets powered from the Station's 125 VDC battery system for monitoring the shutdown process.
There are two long term safe shutdown functions which are dependent upon the availability of the 125 VDC system as a pait of Niagara Mohawk Power Corporation's (NMPC's) defense-in-depth approach for addressing potential Appendix R fire events. These two functions are:
- 1. Minimum required process monitoring instrumentation, and
- 2. The ability to start a diesel generator following'repairs.
In order for the 1500 amp-hour batteries to survive the full eight hours, it was necessary to perform load shedding, actions within the early stages of an Appendix R event. The load shedding requirements were contained in the 115 KV Power Failure Special Operating Procedure (N1-SOP-1 and Nl-SOP-5). These procedures did not provide specific guidance on which loads to shed. Instead, a "target" of 100 amps for Battery 11 and 460 amps for Battery 12 was considered adequate to meet the design basis load shedding objectives. Nl-SOP-1 and Nl-SOP-5 did not provide a specific time frame for the required load shedding objectives. Battery load profile calculations were not performed to verify that, the load shedding targets and the times required to achieve these load sheds assumed by the Appendix R SSA would have ensured sufficient battery NRC Form 366A (64)9)
NRC FORM 366A (64)9)
U.S. NUCLEAR REGULATORY COMMISSION e APPROVED 0MB NO. 31500104 EXPIRES. 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY FORWARD WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS.
COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31S041104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
DOCKET NUMBER (2) LER NUMBER (6) PAGE (3I FACILITY NAME (I)
YEAR SEOVENTIAL I43: REVISION NUMBER '?Yr? NVMSER Nine Nile Point Unit l o s o o o 2 2090 0 06 00 03 OF 0 7 TEXT /IImore 4/reoe b squired. oee alien@ HRC %%drrn 36SA'4/ (IT) capacity existed to start a diesel generator following the postulated 8-hour Appendix R scenario. The 1500 amp-hour battery load profile calculations performed in August 1988 (NMPC Calc.
125DC-Batt-11-ES) demonstrated that a 30-minute time frame to complete the target load shed would have satisfied the battery capacity requirements imposed by the postulated 8-hour Appendix R scenario for station battery 11 only. Current battery calculations indicate that the 1500 amp-hour Battery 12 would have only survived for three minutes under assumed normal loads. Therefore, the electrical maintenance supervisor would have directed all Damage Repair Procedure (DRP} actions for restoring a diesel generator.and providing 125 VDC safe shutdown loads to be performed at battery board 11. Consequently this analysis focuses on the capability to restore,and restart a diesel generator from station battery 11.
To reach the 100 amp discharge rate for Battery 11, the operators would have to shed battery charger MG Set 161, computer MG Set'167, and individual non-essential instrumentation and control loads.
Credit. was taken for the operators plant systems knowledge and operator training to..provide the necessary guidance to remove the.
non-essential battery loads.
Current industry', standards regarding the level of procedural guidance required to achieve the procedural objectives have .
increased since the issuance of Nl-SOP-1 Rev. 5, 6, and Nl-SOP-5 Rev. 0, 1, and 2. In the past many procedures were less specific and certain procedural objectives were satisfied by crediting operator training. I Since these procedures did not specify which loads were required to be shed in order to re'ach the 100 amp discharge current within the required time frame, the assumed eight-hour. battery capacity cannot be demonstrated. Also, NMPC is unable to provide documentation to support the operator training assumption.
II. CAUSE OF CONDITION The cause of 'this condition was the Fire Protection Program's failure to provide detailed .procedural instructions for implementing operator actions credited. by the Appendix R Safe Shutdown Analysis.
Since the detailed procedural instructions were not provided, procedures Nl-SOP-1 and Nl-SOP-5 were potentially insufficient to mitigate the postulated Appendix R fire scenario(s).
technical content of the existing loss of 115 KV power Special If the Operating Procedures (SOP) was questioned, the need to identify NRC Form 366A (669)
NRC FOAM 366A US. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31504)104 (64) 9)
EXPIRES: 4/30/92 ESTIMATED BUADEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION AEQUEST: SOJ) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND AEPORTS MANAGEMENT BRANCH IP4)30), U.S. NUCLEAR REGULATOAY COMMISSIONWASHINGTON, DC 20555, AND TO 1'HE PAPERWOAK REDUCTION PROJECT (31S04)104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR 5E DUE NTIAL i:P:. REVISION NVM ER <<??II NUMBER Nine Mile Point Unit 1 0 5 0 0 0 2 P P 9 0 0 0 6 90 04 OFp 7 TEXT ///IINuE 4/>>44 /4 mqu/md, u44 EddR4u>>/ HRC %%dmI 3///AS / (12) specific load shedding actions and required time frames would have resulted. This would have mandated the development of duty cycles (load profiles) and capacity calculations required 'to ensure an eight hour battery capacity.
III. ANALYSIS OF CONDITION Due to changes to the Special Operating Procedures that now specify the required load shedding steps (and equipment location),
time frame, and the operator training on these procedures, the'equired NMPC is unable to provide conclusive documentation that the actions assumed in the Appendix R SSA would have occurred. Since the operator bias (revised procedures and training) would support the postulated load shedding actions, this issue as a voluntary LER.
NMPC feels it prudent to report As described above, the event in question is an Appendix R fire which causes the loss of both diesel generators, or prevents their initial operation, coincident with LOOP. The 'LOOP, combined with the lack of diesel generators results in a station blackout, and requires the operators to enter and implement the 115 KV Power Failure Procedure.
The NMP1 Safe Shutdown Analysis credits operator load shedding actions under the guidance criteria of the 115 KV Power Failure Special Operating Procedure. In order to achieve the desired battery discharge rate (100 amp), the operator is credited with removing all nonessential instrumentation loads (which are not required to monitor the Safe Shutdown Process). The first operator action in this direction would be to trip the major non-essential loads, e.g., battery charger MG Set 161 and computer MG Set 167.
This would have reduced +he load on Battery 11 to approximately 190 amps.
It is NMPC's contenti'on that the operators would have continued reducing loads by removing all non-essential instrumentation (by the removal of fuses and tripping of breakers from instrument and control loops) until the 100 amp goal was reached. 'It is not conclusive whether these actions would have been taken within a sufficient time frame to ensure eight-hour battery capacity.
Battery calculation 125 VDC-Battery-App-R shows that after shedding MG Sets 161 and 167, without shedding any loads off the RPS MG Set instrumentation busses, Battery approximately 5.18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br />. Time lines used to evaluate the tasks ll capacity is sufficient for described in the DRP's and field walkdowns indicated that the steps required to restore and restart a diesel generator can be completed N AC Form 366A (64)9)
A f
NRC FORM366A U.S. NUCLEAR REGULATORY COMMISSION (649)
O APPROVED OMB NO. 3)504)04 EXPIRES: E/30/92 ESTIMATED 8UADEN PER AESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FOAWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE AECORDS TEXT CONTINUATION AND AEPOATS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504104). OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON, OC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL :~P/o REVISION NUMSER 4% NUMSER Nine IIi1e Point Unit 1 p g p p p 2 2 0 9 0 006 0 0 05 oF 0 7 TEXT //f more <<eoe/e r//I/red. Iree atdhkwol HRC Form 36843/ (12) within 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Additional actions would still be required to initiate cold shutdown within the prescribed eight hours in accordance with the DRPs.
The abo've analysis of an incomplete load shedding which provides 5.18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> of capacity for Battery 11, still assumes MG Sets 161 and 167 are shed within 15 minutes. NMPC cannot'ocument this assumption in an unbiased fashion. Although NMPC feels that this would have occurred, and furthermore feels that load shedding to reach 100 amps at 30 minutes would also have been performed, the operators would have been made aware of a battery capacity problem from the remote battery voltage indication at the Control Room.
Even if no load shedding occurred, the operator would eventually lose all RPS instrumentation. This is because the AC output from RPS MG Set 162 has an under frequency protective breaker which trips the AC output. Although Engineering calculations to show when this point would have been reached have not been performed; the larger the load on a battery, the more quickly the voltage would drop, and decreasing voltage would eventually cause the AC output frequency to drop to the set 'oint of the protective breaker. At this point the .operators . would lose all RPS instrumentation (Reactor Coolant System pressure level can be monitored locally). NMPC considers it credible that the operators would note the loss of instrumentation and quickly identify the
~
under-voltage problem (battery voltage is monitored in the Control Room) and shed all remaining loads on Battery 11. This would have preserved adequate capacity to restart a diesel indefinitely (with all loads shed) until the diesel generator DRPs were complete and the diesel could be restarted. 'MPC feels that adequate capacity would be preserved regardless of whether the under-frequency trip occurred at high load or at the "target" load of 100 amps since a diesel start requires a'aximum load of only 60.amps.
Therefore, NMPC concludes that there was no adverse safety-consequences to the lack of detailed load shedding procedures because:
Operator knowledge was sufficient to ensure load shedding to preserve a battery capacity of 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Thus, the battery would have the capacity required to start a Diesel Generator at the end of the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> Appendix R scenario.
- 2. Operators would have continued load shedding below the 190 amps necessary to achieve a 5.18 hour2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> capacity while the DRPs credit a diesel start at 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />; and NRC F onn 386A (889)
1' NRC FORM 366A (64)9)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION t U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 31500104 E XP I R ES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503, FACILITY NAME (1) DOCKET NUMBER 12) PAGE (3)
LER NUMBER (6)
YEAR SEQUENTIAL ?? SI REVISION NUMSER ?'A5 NUMSER Nine Mile Point Unit 1 0 5 0 0 0 9 0 0 6 0 0 '06 oF 0 7 TEXT /// more SPece b mr/er)erL See er/I/r)/one/H/I C %%dmr 3//SA'4/ ( 17) 3,. Even if no load shedding occurred, operators would have had unmistakable evidence of a battery capacity problem (via the MG Set 162 AC output trip) well before battery capacity decreased to the level which would impact the ability to start
'a diesel, and would have shed all remaining loads on Battery 11.
IV. CORRECTIVE ACTION NMPC has acknowledged certain programmatic and/or isolated deficiencies in some of NMP1 s Station Operating Procedures. NMPC has committed to upgrading the quality and detail of the station procedures. As a result, new Procedure Writers Guides (AP-2.0, AI-1.0) were developed, and many procedures have been revised and updated in accordance with the new guidelines.
The 115KV Power Failure Special Operating Procedure (Nl-SOP-5) was revised to incorporate the Appendix R load shedding. assumptions that were questioned during the RAP Specific Issue 18 effort. A new special operating procedure "Station Blackout" (Nl-SOP-18) was
~
developed to mitigate the effect of an Appendix R Station Blackout event as postulated in the Appendix R Safe Shutdown Analysis. This procedure specifies the non-essential loads, the location of these loads, and the time frame at which these loads are required to be shed to satisfy the Appendix R and Station Blackout submittals.
To ensure that the post repair safety margin (2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />) assumed to be provided for the DRPs will be maintained, to resolve. other 125VDC system deficiencies and to ensure the 125VDC System will satisfy all NMPl design basis commitments, NMPC replaced the two 1500 amp-hour batteries with two 2300 amp-hour batteries.
To ensure compliance to Appendix R as well as other NMPl analysis and commitments, NMPC performed detailed load profile calculations for the 1500 amp-hour and the new 2300 amp-hour station batteries.
NRC Form 366A (64)9)
NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION (6'4)9) APPROVED OMB NO. 31500104 5 XP I A ES: 4/30/92 LICENSEE EVENT REPORT (LER) ESTIMATED BURDEN PEA RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BUADEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATOAY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK AEDUCTION PROJECT (31500104)..OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LEA NUMBER (6) PAGE (3)
YEAR SEQUENTIAL >he<i REVISION
@ NVM SA NVMSSA Nine Mile Point Unit,l o s o o o 220 9 0 0 0 6 0 0 OF 0 7 TEXT /I/ more <<woe /4 I/or'reIL oee er/I//oooo/NRC Form 35543/ ()7)
V. ADDITIONAL INFORMATION A. Identification of components referred to in this LER:
IEEE 803 IEEE 805 COMPONENT FUNCTION SYSTEM ID Emergency Diesel Generator DG EK Battery BTRY EJ Emergency Condenser System NA BL Battery Board BYBD EJ Motor Generator Set MG EF Reactor Protection System (RPS) NA JC B. Failed components: none.
C. Previous similar events: none.
NRC Form 355A (669)
I 1