ML20205S570

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Monthly Operating Rept for Mar 1999 for NMP Unit 1.With
ML20205S570
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 03/31/1999
From: Close R, Rich Smith
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NMP91487, NUDOCS 9904260264
Download: ML20205S570 (4)


Text

,

Niagara $ Mohawk' April 14, 1999 NMP91487 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 RE:

Nine Mile Point Unit 1 Docket No. 50-220 DPR-63

Subject:

Monthly Operating Report for March 1999 Gentlemen:

Submitted herewith is the Operating Data Report, Unit Shutdeve ed Power Reductions, and a Narrative of Operating Experience for March -

Nr the Nine Mile Point Nuclear Station Unit #1. Submittal of this information.

ies with Section 6.9.1.c of the Unit #1 Technical Specifications.

Very truly yours,

/

Robert G. Smith l[

l Plant Manager - Unit 1 Ilh Attachments pc:

H.J. Miller, Regional Administrator, Region 1 3.K. Hunegs, Senior Resident inspector Records Management 6 M.1 0 9904260264 990331 DR ADOCK O go

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ATTACHMENT A OPERATING DATA REPORT DOCKET NO.: 50-210 DATE: 04/08/99 PREPARED BY: R.S. Cf OSE TELEPHONE:(315) 349-12.72 OPERATING STATUS Unit Name: Nine Mile Point Unit #1 Reporting Period: MARCH 1999 1..

Design Electrical Rating:(Net Mwe) 613 2.

Maximum Dependable Capacity (Net Mwe) 565 This Month Yr-to-Date Cumulative

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Critical Hours.

744 2160 177,271.6 4.

Hours Generator On-Line 744 2160 173,224.1 5.

~ Unit Resen>e Shutdown Hours 0

0 20.4 6.

Net Electrical Energy Generated (MWH) 455,052 1,325,129 95,731,236 l

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SUMMARY

OF OPERATING EXPERIENCES The unit operated during the month of March 1999 with a Net Design Electrical Capacity Factor of 99.8%. Power was reduced on March 23,1999 for a 3 day period to address an unexpected entry into a thermal limit LCO; the condition was fully corrected following a control rod pattern adjustment. Additional derates occurred when #11 reactor recirculation pump was removed from service for planned maintenance and later returned to service. Also, the control rod pattern was adjusted 4 other times during the month and turbine stop valve testing was performed. There were no challenges to the Electromatic Relief Valves or Safety Valves.