ML060440603

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IR 05000445-05-005, 05000446-05-005; 09/24/2005-12/31/2005; Comanche Peak Steam Electric Station, Units 1 and 2; Inservice Inspection Activities, Event Follow-up, and Other Activities
ML060440603
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 02/13/2006
From: Clay Johnson
NRC/RGN-IV/DRP/RPB-A
To: Blevins M
TXU Power
References
IR-05-005
Download: ML060440603 (44)


See also: IR 05000445/2005005

Text

February 13, 2006

Mike Blevins, Senior Vice President

and Chief Nuclear Officer

TXU Power

ATTN: Regulatory Affairs

Comanche Peak Steam Electric Station

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT: COMANCHE PEAK STEAM ELECTRIC STATION - NRC INTEGRATED

INSPECTION REPORT 05000445/2005005 AND 05000446/2005005

Dear Mr. Blevins:

On December 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Comanche Peak Steam Electric Station, Units 1 and 2, facility. The enclosed

integrated inspection report documents the inspection findings which were discussed on

January 12, 2006, with Mr. R. Flores and other members of your staff.

This inspection examined activities conducted under your licenses as they related to safety and

compliance with the Commission's rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

The report documents four self-revealing findings of very low safety significance (Green). All

four of these findings were determined to involve violations of NRC requirements. However,

because of the very low safety significance and because they are entered into your corrective

action program, the NRC is treating these four findings as noncited violations (NCVs) consistent

with Section VI.A.1 of the Enforcement Policy. If you contest any NCV in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington

DC 200555-0001; with copies to the Regional Administrator Region VI; the Director, Office of

Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001;

and the NRC Resident Inspector at the Comanche Peak Steam Electric Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be made available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

TXU Power -2-

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Claude Johnson, Chief

Project Branch A

Division of Reactor Projects

Docket Nos.: 50-445, 50-446

License Nos.: NPF-87, NPF-89

Enclosure: NRC Inspection Report 05000445/2005005 and 05000446/2005005

w/Attachment: Supplemental Information

cc w/enclosure:

Fred W. Madden, Director

Regulatory Affairs

TXU Power

P.O. Box 1002

Glen Rose, TX 76043

George L. Edgar, Esq.

Morgan Lewis

1111 Pennsylvania Avenue, NW

Washington, DC 20004

Terry Parks, Chief Inspector

Texas Department of Licensing

and Regulation

Boiler Program

P.O. Box 12157

Austin, TX 78711

The Honorable Walter Maynard

Somervell County Judge

P.O. Box 851

Glen Rose, TX 76043

Richard A. Ratliff, Chief

Bureau of Radiation Control

Texas Department of Health

1100 West 49th Street

Austin, TX 78756-3189

TXU Power -3-

Environmental and Natural

Resources Policy Director

Office of the Governor

P.O. Box 12428

Austin, TX 78711-3189

Brian Almon

Public Utility Commission

William B. Travis Building

P.O. Box 13326

Austin, TX 78711-3326

Susan M. Jablonski

Office of Permitting, Remediation and Registration

Texas Commission on Environmental Quality

MC-122

P.O. Box 13087

Austin, TX 78711-3087

Technological Services Branch

Chief

FEMA Region VI

800 North Loop 288

Federal Regional Center

Denton, Texas 76201-3698

TXU Power -4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (DBA)

Branch Chief, DRP/A (CEJ1)

Senior Project Engineer, DRP/A (TRF)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

Regional State Liaison Officer (WAM)

NSIR/DIPM/EPHP (REK)

Only inspection reports to the following:

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

ROPreports

CP Site Secretary (ESS)

SUNSI Review Completed: __CEJ_ ADAMS: / Yes G No Initials: __CEJ_

/ Publicly Available G Non-Publicly Available G Sensitive / Non-Sensitive

R:\_REACTORS\_CPSES\2005\CP2005-05RP-DBA.wpd

RIV:RI:DRP/A PE:DRP/A SRI:DRP/A C:DRS/EB C:DRS/OB C:DRS/PEB

AASanchez MABrown DBAllen JAClark ATGody LJSmith

E-CEJ /RA/ E-CEJ /RA/ /RA/ DLProulx for

2/3/06 1/27/06 2/3/06 1/27/06 1/31/06 1/27/06

C:DRS/PSB C:DRP/A

MPShannon CEJohnson

/RA/ /RA/

1/31/06 2/13/06

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-445, 50-446

Licenses: NPF-87, NPF-89

Report: 05000445/2005005 and 05000446/2005005

Licensee: TXU Generation Company LP

Facility: Comanche Peak Steam Electric Station, Units 1 and 2

Location: FM-56

Glen Rose, Texas

Dates: September 24 through December 31, 2005

Inspectors: D. Allen, Senior Resident Inspector

A. Sanchez, Resident Inspector

T. Brown, Project Engineer

W. McNeill, Reactor Inspector, Engineering Branch 1

P. Elkmann, Emergency Preparedness Inspector

S. Garchow, Operations Engineer

D. Livermore, Reactor Inspector

J. Keeton, Consultant

Approved by: Claude Johnson, Chief, Project Branch A

Division of Reactor Projects

Attachment: Supplemental Information

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -3-

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -6-

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -6-

1R01 Adverse Weather Protection (71111.01) . . . . . . . . . . . . . . . . . . . . . . . . . . . . -6-

1R04 Equipment Alignment (71111.04) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -6-

1R05 Fire Protection (71111.05Q) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -8-

1R07 Heat Sink Performance (71111.07) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -9-

1R08 Inservice Inspection Activities (71111.08) . . . . . . . . . . . . . . . . . . . . . . . . . . . -9-

1R11 Licensed Operator Requalification (71111.11) . . . . . . . . . . . . . . . . . . . . . . -13-

1R12 Maintenance Rule Implementation (71111.12) . . . . . . . . . . . . . . . . . . . . . . -14-

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13) -14-

1R14 Personnel Performance During Nonroutine Plant Evolutions (71111.14) . . -15-

1R15 Operability Evaluations (71111.15) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -16-

1R16 Operator Workarounds (71111.16) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -17-

1R19 Postmaintenance Testing (71111.19) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -17-

1R20 Refueling and Outage Activities (71111.20) . . . . . . . . . . . . . . . . . . . . . . . . -18-

1R22 Surveillance Testing (71111.22) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -19-

1R23 Temporary Plant Modifications (71111.23) . . . . . . . . . . . . . . . . . . . . . . . . . -20-

1EP1 Exercise Evaluation (71114.01) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -21-

1EP6 Drill Evaluation (71114.06) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -22-

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -22-

4OA1 Performance Indicator Verification (71151) . . . . . . . . . . . . . . . . . . . . . . . . . -22-

4OA2 Problem Identification and Resolution (71152) . . . . . . . . . . . . . . . . . . . . . . -23-

4OA3 Event Followup (71153) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -27-

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -30-

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -34-

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-5

-2- Enclosure

SUMMARY OF FINDINGS

IR 05000445/2005005, 05000446/2005005; 09/24/2005-12/31/2005; Comanche Peak Steam

Electric Station, Units 1 and 2; Inservice Inspection Activities, Event Follow-up, and Other

Activities

This report covered a 3-month period of inspection by two resident inspectors, two reactor

inspectors, one operations engineer, one emergency preparedness inspector, one regional

project engineer, and one consultant. Four Green non-cited violations were identified. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, Significance Determination Process (SDP). Findings for

which the SDP does not apply may be Green or may be assigned a severity level after NRC

management review. The NRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, ?Reactor Oversight Process, Revision 3,

dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

C Green. A Green self-revealing noncited violation of Technical Specification 5.4.1.a was identified for failure to implement the maintenance procedure to

properly install a check valve in the Emergency Diesel Generator 1-01 lubrication

system. On October 20, 2005, the diesel generator shutdown for lack of lube oil

to the turbo-chargers after 60 seconds during a post maintenance test. The lube

oil strainer check valve had been installed backwards during the previous

refueling outage but the opposite strainer had been in service for the ensuing 18

months. The check valve was reinstalled properly, the flow direction of similar

check valves verified, and the damaged turbo-chargers replaced.

The violation was more than minor because one of two lube oil strainers for the

turbo-chargers was incapable of flow, thus affecting the reliability of the diesel

generator. The finding has a human performance crosscutting aspect because

the failure to follow the procedure caused the diesel generator failure. However,

the error was committed in April 2004. The violation is of very low safety

significance because CPSES operating experience indicated that the lube oil

strainers had never been swapped outside of an outage, and then only to

balance run time on the equipment. The significance determination process

screened this out as Green because it only affected the mitigating systems

cornerstone and it did not cause an actual loss of safety function of a single train

nor a loss of safety function that contributed to external event initiated core

damage sequences. This finding has a problem identification and resolution

crosscutting aspect because it was caused by lack of effective corrective actions.

This event was entered into the corrective action program as Smart Form 2005-

004233 (Section 4OA3.1).

-3- Enclosure

C Green. A Green self-revealing noncited violation of Appendix B, Criterion XVI

was identified for failure to implement effective corrective actions for a significant

condition adverse to quality. Specifically, station service water Pump 1-01 was

returned to service on October 20, 2005, and after two hours of operation tripped

on an electrical fault on Phase C of the motor leads. The degraded electrical

condition of the motor lead had been identified during restoration from the pump

maintenance, but the actions taken to ensure the pump was reliable failed.

Phase C of the motor leads was replaced prior to returning the pump to service.

The failure to take effective corrective actions was the performance deficiency.

The violation was more than minor because the pump was returned to service

with a degraded motor lead. At the time of the event, Unit 1 was defueled and

did not require an operable station service water pump. However, Unit 2 was

required by Technical Specifications 3.7.8 to have at least one operable station

service water pump from the opposite unit. With Unit 2 at 100 percent power, a

significance determination was performed using Appendix A of Manual

Chapter 0609. The finding was determined to be of very low safety significance

(Green) because it did not represent a loss of system safety function, was not an

actual loss of safety function for a single Unit 2 train, did not involve equipment

or function specifically designed to mitigate a seismic, flooding, or severe

weather initiating event, and did not involve the total loss of any safety function

that contributed to external event initiated sequences. The cause of this finding

is related to the crosscutting aspects of problem identification and resolution.

The event was entered into the corrective action program as Smart

Form 2005-004220 (Section 4OA3.2).

was identified, after both the alternate and emergency power supplies to a

6.9 kV safeguards bus failed to provide power to the bus within the time

assumed in the accident analysis. On October 19, 2004, an unplanned loss of

the preferred offsite power caused the Unit 2, Train B, 6.9 kV safeguards bus to

de-energize. A degraded Agastat relay delayed the normal power supply

breaker from opening for 30 seconds, which delayed powering the bus from the

alternate offsite AC power supply or the emergency diesel generator. This issue

had crosscutting aspects in the area of problem identification and resolution

because the licensee previously identified that aged Agastat relays were

unreliable and should be replaced if they were in service greater than 12 years.

The failed relay had been in service for 16 years.

The violation was more than minor because it impacted the Mitigating Systems

Cornerstone objective of availability, reliability, and capability of systems that

respond to initiating events. Using Inspection Manual Chapter 0609,

Appendix A, Determining the Significance of Reactor Inspection Findings for

At-Power Situations, the finding was determined to be of very low safety

significance because the likelihood of a medium or large break loss of coolant

accident coincident with a loss of offsite power, which are the only conditions

where the deficiency would cause a non-negligible change in the baseline risk

-4- Enclosure

profile, is less than or equal to 1E-6 per year. Therefore the change in core

damage frequency will be less than 1E-6 per year. The licensee captured the

issue in their corrective action program as Smart Form SMF-2004-003528

(Section 4OA5.2).

Cornerstone: Barrier Integrity

(Corrective Action) was identified, in that licensee personnel failed to identify the

cause for a body-to-bonnet leak, a significant condition adverse to quality and

take corrective action to prevent recurrence. Specifically, licensee welders

repaired a body-to-bonnet leak on Valve 1-8702B, Residual Heat Removal Pump

1-02 hot-leg recirculation isolation valve, in April 2004 by installing a seal weld.

The valve required additional repair in October 2005 for a body-to-bonnet leak.

The failure to identify the root cause and to take effective corrective action to

prevent recurrence was a performance deficiency. This finding is greater than

minor because it is similar to Example 3.g. of Appendix E of Manual

Chapter 0612 because the leakage reoccurred. The inspectors found this

finding screened out of the Phase 1 process as Green. The inspectors

considered this finding to be of very low safety significance because the event

was leakage and not a line break. The cause of this finding is related to the

crosscutting aspects of problem identification and resolution. (Section 1R08.1)

B. Licensee Identified Violations

None.

-5- Enclosure

REPORT DETAILS

Summary of Plant Status

Comanche Peak Steam Electric Station (CPSES) Unit 1 began the reporting period at

100 percent power. The unit began power coastdown on October 5, 2005 and commenced a

reactor shutdown on October 8, 2005 at 8:56 a.m. to begin refueling outage 1RF11. The

reactor was manually tripped and entered Mode 3 at 11:39 a.m. that same day. On

November 8, 2005 Unit 1 ended refueling outage 1RF11 when the main generator output

breakers were closed at 1:51 a.m. The reactor achieved 100 percent reactor power on

November 15, 2005 at 3:51 p.m., and operated at essentially 100 percent power for the

remainder of the period.

CPSES Unit 2 operated at essentially 100 percent power for the entire reporting period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

a. Inspection Scope

The inspectors reviewed Abnormal Conditions Procedure Manual (ABN) ABN-912, Cold

Weather Preparations / Heat Tracing and Freeze Protection System Malfunction,

Revision 7, Section 2, Cold Weather Preparations, in the Unit 1 control room at the

onset of colder weather conditions during the week of November 28, 2005. The

inspectors reviewed the ABN-912 attachments and control room log to verify that plant

cooling units and dampers had been aligned for cold weather and that temperatures

were being monitored in accordance with the attachments.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1 Partial System Walkdown (71111.04)

a. Inspection Scope

The inspectors: (1) walked down portions of the below listed risk important system and

reviewed plant procedures and documents to verify that critical portions of the selected

system were correctly aligned; and (2) compared deficiencies identified during the

walkdown to the licensee's corrective action program to ensure problems were being

identified and corrected.

-6- Enclosure

  • Unit 2 Train B safety injection system in accordance with System Operating

Procedure (SOP) SOP-201B, Safety Injection System, Revision 6, while the

Train A emergency diesel generator (EDG) system was inoperable for scheduled

surveillance, on December 14, 2005

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

.2 Detailed Semiannual System Walkdown (71111.04S)

a. Inspection Scope

The inspectors conducted a detailed semiannual inspection of the Unit 1 and Unit 2

atmospheric relief valves (ARVs), and supporting systems, to verify the functional

capability of the system. The inspectors referenced and used the following documents

to verify proper system alignment, electrical power supply and setpoints :

  • Integrated Plant Operating Procedure (IPO) IPO-002A, Plant Startup From Hot

Standby, Revision 18

  • Technical Data Manual TDM-501A, SG - Feedwater Controller Data, Revision 4

Steam Dump, multiple sheets and revisions

The inspectors also reviewed recent corrective action documents, system health reports,

outstanding work requests, and design issues to determine if any of these items

impacted the systems ability to operate as designed or indicated a degradation in

capability. In addition, the inspectors interviewed the system engineer and site valve

experts and discussed the systems maintenance history, and current and long range

plans to monitor, modify, or update the system and its components. A complete field

walkdown was completed by the inspectors during the week of December 26, 2005.

The inspector completed one sample.

b. Findings

No findings of significance were identified.

-7- Enclosure

1R05 Fire Protection (71111.05Q)

Fire Area Tours

a. Inspection Scope

The inspectors walked down the listed plant areas to assess the material condition of

active and passive fire protection features and their operational lineup and readiness.

The inspectors: (1) verified that transient combustibles and hot work activities were

controlled in accordance with plant procedures; (2) observed the condition of fire

detection devices to verify they remained functional; (3) observed fire suppression

systems to verify they remained functional; (4) verified that fire extinguishers and hose

stations were provided at their designated locations and that they were in a satisfactory

condition; (5) verified that passive fire protection features (electrical raceway barriers,

fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems)

were in a satisfactory material condition; (6) verified that adequate compensatory

measures were established for degraded or inoperable fire protection features; and

(7) reviewed the corrective action program to determine if the licensee identified and

corrected fire protection problems.

  • Fire Area CA - Unit 1 containment building, all elevations on November 4, 2005
  • Fire Zone SE016 - Unit 1 safeguards building 832 foot elevation electrical

equipment Room 96 on November 10, 2005

  • Fire Zone EA057 - Unit 1 inverter battery room corridor Room 125 on

November 26, 2005

  • Fire Zone EA054 - Unit 2 inverter battery room corridor Room 122 on

November 26, 2005

  • Fire Zone 1-SB008 - Unit 1 safeguards corridor 810 foot elevation Rooms 78, 79,

and 82 on December 13, 2005

  • Fire Zone 2-SB008 - Unit 2 safeguards corridor 810 foot elevation Rooms 78, 79,

and 82 on December 13, 2005

  • Fire Zone AA21F - Units 1 and 2 auxiliary building 852 foot elevation

Rooms 234-235, 238-242 on December 13, 2005

The inspectors completed seven samples.

b. Findings

No findings of significance were identified.

-8- Enclosure

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed the licensees program for maintenance, testing, and

surveillance of the Unit 1 Trains A and B Component Cooling Water (CCW) heat

exchangers to ensure that these risk-important heat exchangers are capable of

performing their required safety function during the design basis accident. Specifically,

the Unit 1 Train A CCW heat exchanger interior was physically inspected for foreign

material following the Unit 1 Train A station service water (SSW) pump ingestion of a

vacuum hose in August 2005. The inspectors also viewed the contents from a

containment spray seal oil cooler that was supplied from Train A CCW heat exchanger.

The inspectors also observed actual heat exchanger testing for the Train A CCW heat

exchanger, and reviewed the test data for the Train B CCW heat exchanger. The

inspectors verified that the frequency of monitoring and inspection was sufficient to

detect degradation prior to loss of heat removal capability. Corrective action documents

and system drawings were reviewed by the inspectors. The system engineer was also

interviewed by the inspectors.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities (71111.08)

This inspection procedure requires a minimum sample size of four samples consisting of

Sections 02.01, 02.02, 02.03, and 02.04. All sections were completed except for 02.02

because the associated TI 2515/150 is not completed.

.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurizer Water

Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control

(Section 02.01)

a. Inspection Scope

The inspection procedure requires review of two or three types of nondestructive

examination activities and one to three welds performed on the reactor coolant pressure

boundary.

The inspectors observed 20 nondestructive examination activities including volumetric,

surface and visual examinations as follows:

-9- Enclosure

System Component/Weld Identification Examination Method

Safety 17 components, 11 struts, 5 snubbers and VT-3 (visual)

Injection 1 spring can: Summary Numbers 672400-

800, 673200, 673400-600, 673800,

673900, 674200, 674400, 674500, and

674600.

Safety 2 welded lugs: Summary Numbers 784300 Liquid Penetrant

Injection and 784550.

Residual Pipe to valve TBX-1-4101-3: Augmented Ultrasonic

Heat Removal Examination.

During the observation of each examination, the inspectors verified that activities were

performed in accordance with the American Society of Mechanical Engineers (ASME)

Boiler and Pressure Vessel Code requirements and applicable procedures. The

inspectors verified that the licensee compared the indications revealed by the

examinations against the previous outage examination reports as applicable. No

defects or reportable flaws were detected during the inservice examinations. The

inspectors verified that the licensee used calibrated and qualified instruments and

personnel.

Of the five ASME Class 1 and 2 welding activities performed by licensee personnel, the

inspectors reviewed Work Order (WO) WO-04-05-163997-00, a canopy seal weld on

Valve 1-CS8411. The inspectors verified that the welding activities met ASME Code

requirements.

The inspector completed all required samples.

b. Findings

Introduction. The inspectors identified a Green self-revealing noncited violation (NCV)

of 10 CFR Part 50, Appendix B, Criterion XVI. The licensee took inadequate corrective

actions in that the licensee repaired a leaking valve with a seal weld which subsequently

leaked.

Description. The inspectors found that licensee personnel planned to reweld a seal

weld because of evidence of boron leakage on Valve 1-8702B found during this outage.

Licensee welders repaired this valve in April 2004 because of boric acid leakage at that

time. Valve 1-8702B is a Residual Heat Removal Pump 1-02 hot-leg recirculation

isolation valve.

A review of the history of this type of repair found three additional examples where

licensee welders had seal welded the valve body-to-bonnet flanged connections

-10- Enclosure

because of evidence of boron leakage since 1995. The valves were 2-8378B, Reactor

Coolant System Loop 2-04 charging upstream check valve; 2-8379A, and 2-8379B,

Reactor Coolant System Loop 2-01 charging system downstream check valves.

Licensee personnel found all of these welds to subsequently leak within a year in 1996.

In 2005, licensee welders also repaired two valve body-to-bonnet flanged connections

because of evidence of leakage. These valves were numbered 2-8818B and 2-8818C,

residual heat removal loop check valves. In summary, this repair has been done six

times and failed four times. Two of the six times this repair has been done are unknown

at this time in respect to leakage because a refueling outage has not occurred. The

inspectors considered the evidence of boron leakage in these body-to-bonnet flanged

connections to be a significant condition adverse to quality.

Analysis. The inspectors found this finding to be greater than minor because it is similar

to Example 3.g. of Appendix E of Manual Chapter 0612 because the leakage reccurred.

The inspectors considered this finding as of very low safety significance because the

event was leakage and not a line break. The inspectors found this finding screened out

of the Phase 1 process as Green. The licensee issued a Smart Form (SMF)

SMF-2005-004209 regarding this finding.

Enforcement. Criterion XVI, Corrective Actions, of Appendix B to 10 CFR Part 50

states, in part, that measures shall be established to assure that conditions adverse to

quality are promptly identified and corrected. In the case of significant conditions

adverse to quality, the measures shall assure that the cause of the condition is

determined and corrective action taken to preclude repetition. Contrary to the above,

the measures established to identity the root cause and take corrective actions to

prevent recurrence were inadequate in that leakage of the body-to-bonnet flanged

connections on Valve 1-8702B after previous repair in 2004, and on Valves 2-8378B,

2-8379A/B in 1995, were recurrent. The inspectors identified this finding as an NCV

because of its very low safety significance and because the licensee has entered this

finding in its corrective action program. This is consistent with Section VI.A. of the NRC

Enforcement Policy: NCV 05000445/2005005-01, Inadequate Corrective Actions for a

Leaking Valve with a Seal Weld which Subsequently Leaked.

.2 Pressurizer Water Reactor Vessel Upper Head Penetration Inspection Activities

(Section 02.02)

a. Inspection Scope

The inspection procedure requires observation or review of upper head inspections after

the completion of Temporary Instruction 2515/150. The procedure requires samples

similar in number to the preceding section.

The licensee plans to replace this head, and thus close the Temporary

Instruction 2515/150. The licensee did not perform upper head inspections other than

visual during this outage. The visual inspection activities are documented in

Section 1R20 of this report.

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b. Findings

No findings of significance were identified.

.3 Boric Acid Corrosion Control Inspection Activities (Section 02.03)

a. Inspection Scope

The procedure requires observation or review of boric acid corrosion control activities.

Specifically, the procedure requires review of one to three engineering evaluations

performed for boric acid residue found on reactor coolant system piping and

components. This procedure also required review of one to three corrective actions

taken because of evidence of boric acid leaks.

The inspectors reviewed records of a visual examination of the reactor coolant system

pressure boundary integrity walkdown. The inspectors reviewed the 58 areas with light

boric acid residue identified by the licensee as of the time of this review (the licensee

had not completed all the inspections) to assure identification and correction of leakage.

The inspectors reviewed the SMF written to evaluate and clean the areas identified

during the last inspection. The inspectors verified that licensee personnel adequately

evaluated 30 minor leaks including one active leak to assure correction of leakage

problems. The inspectors reviewed the corrective actions taken at that time.

The inspector completed all required samples.

b. Findings

No findings of significance were identified.

.4 Steam Generator Tube Inspection Activities (Section 02.04)

a. Inspection Scope

The inspectors reviewed the leakage history for the steam generators to verify that the

licensee had no leakage during operations before the shutdown. The inspectors verified

that licensee personnel and contractors used properly qualified eddy current probes and

equipment for the expected types of tube degradation to assure proper identification and

evaluation of indications. The inspectors observed the collection and analysis and

resolution of nine calibration groups of eddy current data performed by contractor

personnel to evaluate tubes and possible loose parts in the steam generators to assure

proper implementation of the procedures and program requirements. The inspectors

verified that the licensee analysts reviewed the areas of potential degradation, based on

site-specific and industry experience, to assure proper use of this information. The

inspectors verified that the licensee compared flaws detected during the current outage

against the previous outages data. The inspectors reviewed the repair criteria used to

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assure compliance with technical requirements. The inspectors also verified the

licensees eddy current examination scope and expansion criteria met the Technical

Specifications, industry guidelines, and commitments to the NRC.

Regarding plugging and in-situ pressure testing, at the time of this inspection the

licensee had not established the full scope of plugging and in-situ pressure testing to be

performed. The inspectors verified that the predictions of tube plugging appeared to be

the same as experienced in the past.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

The inspector observed two licensed operator requalification training scenarios in the

control room simulator on December 14, 2005. The first training session began with a

short lesson on immediate operator actions for a pressurizer channel failure response.

This was followed by a scenario that consisted of a feedwater heater tube leak, a main

feedwater trip followed by a reactor trip, and loss of heat sink. The second training

scenario consisted of a slow degradation of grid voltage and frequency, eventual loss of

the 345kV buses, reactor trip, loss of the 138 kV switchyard, loss of all AC power and

Train B DC power.

Simulator observations included formality and clarity of communications, group

dynamics, the conduct of operations, procedure usage, command and control, and

activities associated with the emergency plan. The inspectors also verified that

evaluators and the operators were identifying crew performance problems as applicable.

The inspectors also observed a requalification classroom training session regarding the

main feedwater system.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

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1R12 Maintenance Rule Implementation (71111.12)

a. Inspection Scope

The inspectors independently verified that CPSES personnel properly implemented

10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants, for the following equipment performance problems:

C During the week of November 28, the inspectors reviewed the corrective actions

and performance history of the Units 1 and 2 charging pump suction high point

vent problems identified in SMF-2002-002396 and SMF-2002-004242 that had

resulted in both systems being placed in Maintenance Rule (a)(1). Both Units

systems have been returned to (a)(2) status based on successfully meeting the

performance criteria.

C The common control room Heating Ventilation and Air Conditioning (HVAC)

System, Train B was placed into (a)(1) status due to exceeding the functional

performance criterion of two functional failures within two years. Both failures

were from misaligned motor control center electrical bucket stabs. New

performance criterion for the system has been established. This issue was

entered and is being tracked in the corrective action program as

SMF-2005-003830.

The inspectors reviewed whether the structures, systems, or components (SSCs) that

experienced problems were properly characterized in the scope of the Maintenance

Rule Program and whether the SSC failure or performance problem was properly

characterized. The inspectors assessed the appropriateness of the performance criteria

established for the SSCs where applicable. The inspectors also independently verified

that the corrective actions and responses were appropriate and adequate.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a. Inspection Scope

The inspectors reviewed selected activities regarding risk evaluations and overall plant

configuration control. The inspectors discussed emergent work issues with work control

personnel and reviewed the potential risk impact of these activities to verify that

the work was adequately planned, controlled, and executed. The activities reviewed

were associated with:

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C Delay of completion of maintenance on switchyard Breaker 7980 resulted in

increased risk for scheduled troubleshooting and maintenance of SSW

Pump 1-02 flow indication on September 30, 2005

C Reschedule of crane operations near Transformer XST1 during scheduled

surveillance testing of EDG 2-02 and ATWS Mitigation System Actuation Circuit

on October 5 - 6, 2005

C Outage Risk Assessment for Refueling Outage 1RF11 (scheduled for

October 8 - November 7, 2005) on October 6, 2005

C Delayed completion of maintenance on switchyard Breaker 8090 with concurrent

scheduled maintenance on EDG 2-02 and Unit 1 reactor coolant system reduced

inventory on October 27 - 28, 2005

C Switchyard Breaker 8050 restored but air switch left open, making the Venus line

inoperable, discovered October 30 after opening Breaker 7970 on

October 29-30, 2005

C Unit 1 reduced inventory evolution reschedule conflicted with the scheduled

EDG 2-02 surveillance on November 2, 2005

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Nonroutine Plant Evolutions (71111.14)

a. Inspection Scope

For the two nonroutine events described below, the inspectors observed the simulator

just-in-time training and reviewed the applicable procedures prior to the evolution. The

inspectors attended pre-job briefings and observed portions of the evolution from the

control room. Procedural use, communications, coordination between organizations and

safe operation of the plant during the evolution were evaluated to ensure risk was

minimized and safety was maintained.

  • On October 8, 2005, the control room operators commenced the Unit 1 reactor

shutdown to begin refueling outage 1RF11 via boration as per IPO-003A, Power

Operations, Revision 24. At 11:39 a.m., reactor operators manually tripped the

reactor and entered EOP-0.0A, Reactor Trip or Safety Injection, Revision 7.

Operators transitioned to EOS-0.1A, Reactor Trip Response, Revision 7 and

IPO-005A, Plant Cooldown From Hot Standby to Cold Shutdown, Revision 21.

The inspectors observed control room activities and operator actions during the

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evolution to ensure formal and clear communications, proper procedure usage,

command and control activities, proper use of emergency procedures, and the

controlled and safe shutdown of the Unit 1 reactor.

  • On October 11, 2005, the control room operators lowered Unit 1 reactor coolant

system water level to approximately 56 inches above the reactor core (Midloop)

in preparation to remove steam generator primary manways and install steam

generator nozzle dams. The inspectors reviewed Generic Letter Number 88-17,

Loss of Decay Heat Removal and TXUs responses. Integrated Plant

Operating Procedure IPO-010A, Reactor Coolant System Reduced Inventory

Operations, Revision 16, was reviewed to ensure adequate controls were in

place. The control room activities and operators actions were observed during

the evolution to ensure the procedure was followed, plant instruments were

responding correctly, conservative decisions were made, and that the evolution

was completed safely. Control room activities were periodically observed for

distractions to the operators while the reactor vessel water level remained in

reduced inventory.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors: (1) reviewed plant status documents such as operator shift logs,

emergent work documentation, deferred modifications, and standing orders to

determine if an operability evaluation was warranted for degraded components;

(2) referred to the Updated Safety Analysis Report and design basis documents to

review the technical adequacy of licensee operability evaluations; (3) evaluated

compensatory measures associated with operability evaluations; (4) determined

degraded component impact on any Technical Specifications; (5) used the SDP to

evaluate the risk significance of degraded or inoperable equipment; and (6) verified that

the licensee has identified and implemented appropriate corrective actions associated

with degraded components. The inspectors interviewed appropriate licensee personnel

to provide clarity to operability evaluations, as necessary. Specific operability

evaluations reviewed are listed below:

C Quick Technical Evaluation (QTE) QTE-2005-002098-01-00, distance between

Unit 1 Train C Cable NK130951 and Handswitch 1/1-8823 does not meet

separation criteria of ES-100 Appendix F, Attachment 1, Table 1, reviewed the

week of November 21, 2005

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EDG 1-01 with Check Valve 1DO-0152 installed backwards, reviewed on

November 22, 2005

  • QTE-2005-003945-01-00, determine operability of the common uninterruptible

power supply (UPS) and distribution room HVAC system Train B following an

observation of the compressor failing to start when the UPS air conditioning

system was manually requested to start, reviewed on December 29-30, 2005

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds (71111.16)

Cumulative Review of the Effects of Operator Workarounds

a. Inspection Scope

On November 29, 2005, the inspectors reviewed cumulative effects of identified

operator workarounds on reliability, availability, and potential for system misoperation on

both Units. The inspectors reviewed the cumulative effects of the operator workarounds

on multiple mitigating systems and the ability of operators to respond in a correct and

timely manner to plant transients and accidents.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors witnessed or reviewed the results of the postmaintenance tests for the

following maintenance activities:

  • Unit 1 SSW Pump 1-01 motor following failure of the Phase C cable to the motor

on October 20, 2005, in accordance with Maintenance Section - Electrical

procedure MSE-G0-4201, "Megger Testing of Power Cables, Motors and

Generators," Revision 6, and MSE-G0-4003, "DC High Potential Testing With

Baker Advanced Winding Analyzer," Revision 0, on October 24, 2005

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C Unit 1 EDG 1-02 following digital upgrade of the voltage regulation system, in

accordance with Maintenance Section-Mechanical Manual Procedure

MSM-P0-3375, "Emergency Diesel Engine Break-in Run and Post Maintenance

Run," Revision 7, on November 3, 2005

C Unit 1 Turbine Driven Auxiliary Feedwater (TDAFW) Pump following outage

related maintenance including replacement of the governor, in accordance with

Equipment Test Procedure ETP-304A, "Turbine Driven Auxiliary Feedwater

Pump Overspeed Test," Revision 3, System Operation Procedure SOP-304A,

"Auxiliary Feedwater System," Revision 16, Testing Procedure PPT-S1-9103A,

"TDAFW Pump Actuation and Response Time Test, Train A," Revision 2 and

OPT-206A, "AFW System," Revision 25, on November 6, 2005

In each case, the associated work orders and test procedures were reviewed in

accordance with the inspection procedure to determine the scope of the maintenance

activity and to determine if the testing was adequate to verify equipment operability.

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities (71111.20)

a. Inspection Scope

The inspectors evaluated licensees 1RF11 activities to ensure that risk was considered

when developing and when deviating from the outage schedule, the plant configuration

was controlled in consideration of facility risk, mitigation strategies were properly

implemented, and Technical Specification requirements were implemented to maintain

the appropriate defense-in-depth. Specific outage inspections performed and outage

activities reviewed and/or observed by the inspectors included:

  • Discussions and review of the outage schedule concerning risk with the Outage

Manager

C Unit shutdown and cooldown

C Containment walkdowns to identify indications of reactor coolant leakage,

evaluate material condition of equipment not normally available for inspection,

inspect fire protection equipment and fire hazards, observe radiation protection

postings and barriers, and evaluate coatings and debris for potential impact on

the recirculation containment sumps

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C Reduced inventory and midloop activities to perform steam generator manway

removal, nozzle dam installation and removal

C Reactor coolant system instrumentation including Mansell level instrumentation

C Defense in depth and mitigation strategy implementation

C Containment closure capability

C Verification of decay heat removal system capability

C Spent fuel pool cooling capability

C Reactor water inventory control including flow paths, configurations, alternate

means for inventory addition, and controls to prevent inventory loss

C Controls over activities that could affect reactivity

C Refueling activities that included fuel offloading, fuel transfer, and core reloading

C Electrical power source arrangement

C Containment cleanup and inspection

C Containment recirculation sump inspection

C Unit heatup and startup

C Reactor vessel upper head penetration review and inspection

C Reactor vessel lower head penetration review and inspection

C Licensee identification and resolution of problems related to refueling activities

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors evaluated the adequacy of periodic testing of important nuclear plant

equipment, including aspects such as preconditioning, the impact of testing during plant

operations, and the adequacy of acceptance criteria. Other aspects evaluated included

test frequency and test equipment accuracy, range, and calibration; procedure

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adherence; record keeping; the restoration of standby equipment; test failure

evaluations; system alarm and annunciator functionality; and the effectiveness of the

licensees problem identification and correction program. The following surveillance test

activities were observed and/or reviewed by the inspectors:

  • Unit 1 containment close out inspection in accordance with procedure OPT-305,

"Containment Close Out Inspection," Revision 10 and WO-5-04-504191-AA,

reviewed on November 4, 2005

  • Unit 1 low power physics testing following refueling, in accordance with Nuclear

Engineering Procedure NUC-301, "Low Power Physics Testing," Revision 12,

reviewed on November 10, 2005

OPT-303, "Reactor Coolant System Water Inventory," Revision 10, reviewed on

November 21, 2005

  • Unit 1 Train A slave relay and containment isolation valve actuation test, in

accordance with OPT-459A, Train A Safeguards Slave Relay K623 Actuation

Test, Revision 5, reviewed on December 13, 2005

The inspectors completed four samples.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, plant drawings,

procedure requirements, Technical Specification and Technical Requirements Manual to

ensure that the below listed temporary modification was properly implemented. The

inspectors: (1) verified that the modification did not have an affect on system

operability/availability; (2) verified that the installation was consistent with the

modification documents; (3) ensured that the post-installation test results were

satisfactory and that the impact of the temporary modification on permanently installed

SSC's were supported by the test; (4) verified that the modification was identified on

control room drawings and that appropriate identification tags were placed on the

affected equipment; and (5) verified that appropriate safety evaluations were

completed. The inspectors verified that licensee identified and implemented any needed

corrective actions associated with temporary modifications.

  • Unit 1 Construction Access Facility installed at tornado missile Door S1-27 at the

south end of the Unit 1 safeguards building, reviewed on December 4, 2005

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The inspectors completed one sample.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP1 Exercise Evaluation (71114.01)

a. Inspection Scope

The inspectors reviewed the objectives and scenario for the 2005 biennial emergency

plan exercise to determine if the exercise would acceptably test major elements of the

emergency plan. The scenario simulated a failure to automatically isolate a liquid

release, plant fire lasting greater than 15 minutes, a reactor coolant pump failure,

mechanical core damage, fission product barrier failures, and a radiological release to

the environment via a steam generator tube rupture and stuck-open steam generator

atmospheric safety valve, to demonstrate the licensee's capabilities to implement the

emergency plan.

The inspectors evaluated exercise performance by focusing on the risk-significant

activities of classification, notification, protective action recommendations, and offsite

dose consequences in the following emergency response facilities:

  • Simulator Control Room
  • Operations Support Center
  • Emergency Operations Facility

The inspectors also assessed personnel recognition of abnormal plant conditions, the

transfer of emergency responsibilities between facilities, communications, protection of

emergency workers, emergency repair capabilities, and the overall implementation of

the emergency plan.

The inspectors attended the post-exercise critiques in each of the above facilities to

evaluate the initial licensee self-assessment of exercise performance. The inspectors

also attended a subsequent formal presentation of critique items to plant management.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

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1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

On November 28, 2005, the inspectors evaluated the adequacy of emergency drills that

contributed to performance indicator statistics performed on that day. Observations of

two operations crews in the control room simulator included opportunities for emergency

classifications and offsite notifications. The inspectors reviewed the drill scenario, drill

objectives, activity log sheets, evaluations, and critique notes. The inspectors also

observed the shift manager critique for both crews and discussed observations with the

drill controllers and evaluators from the control room simulator. The inspectors verified

that the licensee adequately conducted the drills and critiqued the drill performance in

accordance with the facility guidelines.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

a. Inspection Scope

The inspector sampled licensee submittals for the performance indicators listed below

for the period July 2004 through September 2005. The definitions and guidance of

NEI 99-02, Regulatory Assessment Indicator Guideline, Revisions 2 and 3, were used

to verify the licensees basis for reporting each data element in order to verify the

accuracy of performance indicator data reported during the assessment period.

Licensee performance indicator data was reviewed against the requirements of Staff

Guideline 20, NRC Performance Indicators, Revisions 6 and 7.

Emergency Preparedness Cornerstone:

  • Drill and Exercise Performance
  • Emergency Response Organization Participation
  • Alert and Notification System Reliability

The inspector reviewed a 100 percent sample of drill and exercise scenarios and

licensed operator simulator training sessions, notification forms, and attendance and

critique records associated with training sessions, drills, and exercises conducted during

the verification period. The inspector reviewed selected emergency responder drill

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participation records. The inspector reviewed alert and notification system testing

procedures, maintenance records, and a 100 percent sample of siren test records. The

inspector also interviewed licensee personnel responsible for collecting and evaluating

performance indicator data.

The inspector completed three samples during this inspection.

b. Findings

The inspector identified 11 instances in which the licensee evaluated offsite notification

forms as accurate when a site-wide emergency condition was marked as applying only

to Unit 1. NEI 99-02, Regulatory Assessment Performance Indicators, Revisions 2

and 3, identifies the unit applicability of an emergency condition as a component of

offsite notification form accuracy. The inspector determined that the licensee had not

provided guidance regarding the correct marking of unit applicability when emergency

conditions impact more than one unit, resulting in inconsistent performance in marking

the offsite notification form. The reevaluation of these 11 opportunities has the potential

to cause the licensees Drill and Exercise Performance Indicator to drop below the

established 90% threshold.

This finding is similar to the Reactor Oversight Program (ROP) Frequently Asked

Question (FAQ) 338, dated March 2003, which addressed evaluation of Drill or Actual

Event as marked on offsite notification forms. FAQ 338 instructed licensees to submit

similar issues to the ROP working group for guidance regarding post-submittal

reevaluation. An Unresolved Item has been opened pending resolution of an FAQ

submitted to the ROP working group on this issue; URI 05000445;05000446/2005005-

02, Notification Form Accuracy Requires Additional Guidance.

4OA2 Problem Identification and Resolution (71152)

.1 Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a routine screening of all items entered

into the licensees corrective action program. This review was accomplished by

reviewing the licensees computerized corrective action program database (SMFs),

reviewing hard copies of selected SMFs and attending related meetings such as Plant

Event Review Committee (PERC) meetings.

b. Findings

No findings of significance were identified.

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.2 Semiannual Trend Review

a. Inspection Scope

On December 23, 2005, the inspectors completed a semiannual review of licensee

internal documents, reports, and performance indicators to identify trends that

might indicate the existence of more safety significant issues. The inspectors reviewed

the following types of documents:

C Corrective Action Documents (Smart Forms)

C System Health Reports

C Planned Maintenance Work Week Critiques

C CPSES Nuclear Overview Department Evaluation Reports (Audits)

C Human Performance Program Health Indicators Package

C Corrective Action Program Health report

C Station Reliability Issues

C Degraded conditions evaluated in accordance with Generic Letter 91-18

C CPSES Self-Assessment Reports

b. Findings and Observations

No findings of significance were identified. However, during the review, the inspectors

did note the following two items: (1) several issues related to foreign material exclusion,

including fuel clad failure due to debris; and (2) issues related to the reliability of the

main turbine generator digital control system and operator errors committed while

operating the controls. The inspectors did not identify any additional trends.

The inspectors determined that the licensee had adequately identified adverse trends

and entered them into the corrective action program using an appropriate threshold.

.3 Selected Issue for In-Depth Review: Review of Unit 2 TDAFW Pump

a. Inspection Scope

The inspectors performed a detail review of an issue involving the Unit 2 TDAFW pump

failure to reduce speed during an operational surveillance test run. This issue was

placed into the licensees corrective action program as SMF-2005-002054. The

inspectors reviewed the apparent cause evaluation, vendor written communication

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(VL-05-002561), and procedure MSM-C0-8721, Governor Valve for Terry Turbine,

Revision 1. The inspectors also performed a detailed system walkdown, and discussed

the issue with the system engineer.

b. Findings and Observations

No findings of significance were identified. On May 12, 2005 during an operational

surveillance run on the Unit 2 TDAFW pump, the turbine failed to reduce speed below

2440 revolutions per minute (rpm) when directed, by the procedure, for verification of

governor oil level. The licensee determined that there was proper oil level in the

governor, and determined that the ability of the governor valve to close completely did

not cause the TDAFW pump to become inoperable. The safety function of the TDAFW

pump is to operate at a speed of at least 4075 rpm, which it was capable of doing at that

time.

The apparent cause analysis was completed and approved on August 10, 2005 and was

determined using the Why Tree technique. The cause for the TDAFW pump not being

able to reduce speed below 2440 rpm was determined to be the improper setting of the

governor valve linkage. The governor valve linkage was not set correctly due to the

difficulty of measuring the gap between the governor valve stem and the cam plate,

which was specified as 0.075 inch, with a dial indicator in a physically cramped space.

Two corrective actions were generated from the apparent cause analysis. The

procedure controlling the TDAFW maintenance was modified to measure the gap

between the governor valve stem and the cam plate in terms of 1/16 inch. This allows

the mechanics to measure the gap with a ruler instead of a dial indicator. The licensee

plans to purchase a spare Terry Turbine to allow the just-in-time training of the

mechanics.

The licensee took the immediate action of readjusting the governor valve linkage and

completed the necessary corrective action in a reasonable amount of time

commensurate with the safety significance of the issue. SMF-2005-004986-00 was

initiated to complete an effectiveness review of the completed corrective actions.

The inspectors completed one sample.

.4 Selected Issue for In-Depth Review: Review of Unit 2, Steam Generator 2-04

Atmospheric Relief Valve Repeatedly Exceeding Operational Alert Limits

a. Inspection Scope

The inspectors performed a detail review of an issue involving the Unit 2 ARV,

2-PV-2328, repeatedly exceeding its operational alert limit stroke time (open direction)

test. The inspectors identified at least five occurrences since February 2004. The stroke

time surveillance is performed on a 92 day frequency. The inspectors reviewed

OPT-504B, MS Section XI Valves, Revision 10, recent system and component health

reports, and Smart Forms. The Smart Forms reviewed are: SMF-2004-000566,

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SMF-2004-003610, SMF-2005-000228, SMF-2005-002654, and SMF-2005-003804.

Interviews were conducted with the system engineer, in-service testing engineer, and

licensee valve experts. The inspectors also performed a system walkdown.

b. Findings and Observations

No findings of significance were identified; however the inspectors identified that the

licensee had not identified nor had any action in place for Unit 2 ARV, 2-PV-2328,

repeatedly exceeding the alert threshold for stroke time (open direction) during

operational surveillance testing.

Between February 15, 2004 and October 10, 2005, the Unit 2 ARV, 2-PV-2328, had

exceeded its operational alert limit stroke time test five times. In each instance the ARV

had exceeded its surveillance alert stroke time limit of 9.0 seconds (open direction), but

had not exceeded the acceptance criterion of 10 seconds. The design basis document

states that the ARVs are required to be capable of a full stroke within 20 seconds,

therefore, the valve was declared operable. Each of these instances of the valve

exceeding its stroke time alert limit, the issue was placed into the corrective action

program and evaluated. In each instance, the inservice testing engineer had evaluated

the results, recommended no action, and determined that there was no significant

degradation of valve performance.

In general, there has been a step increase in all Unit 2 ARV stroke times in the October

2003 time frame. The step change and the trend are especially obvious for the ARV

2-PV-2328. This trend was not identified and was not being addressed by the licensee.

ASME Section XI sets alert limits and acceptance criteria for valve stroke times based

on reference stroke time valves. This program is in place to detect degrading

components to protect from unexpect failures. The licensee was not trending any of the

surveillance testing results or the number of times this valve had exceeded the alert

setpoint. The result of this review is that the licensee was not trending or aware of the

change in ARV performance. This was a missed opportunity to identify a change in

component function. The licensee has entered the issue into the corrective action

program as SMF-2006-00125 and is currently reviewing the issue to determine a cause

and to determine what corrective actions should be taken.

The inspectors complete one sample.

.5 Emergency Preparedness Annual Sample Review

a. Inspection Scope

The inspectors reviewed summaries of corrective actions assigned to emergency

preparedness during calendar years 2004 and 2005, reviewed 6 drill reports, and

observed licensee performance during a full-scale exercise, to determine the

effectiveness of previous corrective actions.

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b. Findings and Observations

No findings of significance were identified.

.6 Inservice Inspection Review of Problem Identification and Resolution

a. Inspection Scope

The inspection procedure requires review of a sample of problems associated with

inservice inspections and steam generator inspections documented by licensee

personnel in the corrective action program for appropriateness of the corrective actions.

The inspectors reviewed 9 of the 56 SMFs written since the last outage which dealt with

inservice inspection and steam generator eddy current inspection activities and found

the corrective actions were appropriate. The inspectors performed this review to assure

that the licensee had an appropriate threshold for entering issues into the corrective

action program and had procedures that direct root cause evaluations when necessary.

b. Findings

No findings of significance were identified.

4OA3 Event Follow-up (71153)

.1 Unit 1 EDG 1-01 trip due to Check Valve 1DO-0152 installed backwards in lubrication oil

system

a. Inspection Scope

The inspectors reviewed the trip of the EDG 1-01 which occurred on October 20, 2005

during the initial post maintenance run. The inspectors interviewed personnel involved,

attended the PERC meeting, reviewed SMFs and procedures.

b. Findings

Introduction. A Green, self-revealing, NCV was identified for failure to properly perform

the installation procedure for Check Valve 1DO-0152 in the EDG 1-01 lube oil system,

as prescribed in Technical Specification 5.4.1.a.

Description. On October 20, 2005, EDG 1-01 was started for a post maintenance run

following the 1RF11 outage work on the EDG. The EDG tripped 60 seconds after

starting on low lube oil pressure to the turbo-chargers. Troubleshooting by the licensee

found that the right bank lube oil strainer outlet Check Valve 1DO-0152 was installed

backwards, preventing lube oil flow to the turbo-chargers and rocker arm assemblies.

The turbo-chargers were replaced and found to have been damaged by this event.

Check Valve 1DO-0152 had last been replaced the previous refueling outage on

-27- Enclosure

April 11, 2004. The installation had been performed in accordance with maintenance

procedure MSM-P0-332, "Emergency Diesel Generator Lube Oil Check Valve

Maintenance," Revision 2, Step 8.16.2, which required a verification of the check valve

to ensure it was installed with the flow (arrow) pointing away from the strainer. Check

Valve 1DO-0152 was found with the flow arrow pointing towards the strainer. The

EDG 1-01 lube oil system had been aligned through the left bank lube oil strainer during

the operating cycle, and the strainer alignment was shifted following the 1RF11 work

window to balance run time on the equipment. Similar check valves in the other three

EDGs were verified to be installed with the proper orientation, and Check

Valve 1DO-0152 was reinstalled correctly. A review of the CPSES operating experience

indicated the lube oil strainers had never been swapped outside of an outage for either

units.

Analysis. The inspectors determined that the licensees failure to install check valve

1DO-0152 in the EDG 1-01 lube oil system correctly was a performance deficiency.

This finding is more than minor because the improper installation of the check valve

prevented flow through the right bank lube oil strainer, which affected the mitigating

systems cornerstone objective to ensure the availability, reliability and capability of

systems that respond to initiating events to prevent undesirable consequences. This

finding has a human performance cross-cutting aspect because the failure to follow the

maintenance procedure was the cause of the degraded condition. Phase 1 of the

significance determination process screened this finding as very low safety significance

(Green) because it only affected the mitigating systems cornerstone, was not a design

or qualification deficiency, did not cause a loss of system safety function or an actual

loss of safety function of a single train, did not involve equipment or functions

specifically designed to mitigate a seismic, flooding, or severe weather initiating event,

and did not involve the total loss of a safety function that contributes to external event

initiated core damage sequences.

Enforcement. Technical Specification 5.4.1.a requires written procedures to be

established, implemented, and maintained covering activities recommended in

Regulatory Guide 1.33, Revision 2, Appendix A, which includes maintenance

procedures that could affect performance of safety-related equipment. Contrary to the

above, maintenance procedure MSM-P0-332, "Emergency Diesel Generator Lube Oil

Check Valve Maintenance," Revision 2 was not properly implemented on April 11, 2004.

Because this violation was of very low safety significance and was entered into the

corrective action program as SMF-2005-004233, it is being treated as an NCV,

consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000445/2005005-03, Trip of Emergency Diesel Generator Due to Lube Oil

Check Valve Installed Backwards.

-28- Enclosure

.2 Unit 1 Station Service Water Pump 1-01 Trip Due to Overcurrent Condition on Phase C

a. Inspection Scope

The inspectors reviewed the trip of the SSW Pump 1-01 which occurred on October 20,

2005. The inspectors interviewed personnel involved, attended the PERC meeting,

reviewed Smart Forms, and procedures.

b. Findings

Introduction. A Green, self-revealing, NCV was identified for failure to implement

effective corrective actions for a condition adverse to quality prior to returning a safety

related SSW pump to service.

Description. On October 19, 2005, a degraded condition had been noted on the Phase

C cable of the SSW Pump 1-01 during preparations to reland the motor leads following

pump overhaul. The licensee made repairs to correct the degraded conditions by

replacing part of the Phase C cable closest to the motor. Following surveillance testing,

the licensee declared the SSW Pump 1-01 operable. On October 20, 2005 at 5:00 a.m.,

SSW Pump 1-01 was placed in service and SSW Pump 1-02 was tagged out in

preparations for a scheduled Train B SSW outage. At 6:55 a.m., SSW Pump 1-01

tripped on an overcurrent condition sensed on the Phase C motor lead. At the time of

the trip, Unit 1 was in "no mode" (reactor fuel was in the spent fuel pool for 1RF11) and

Unit 2 was at 100 percent power with both SSW trains in service. In response to the trip

of SSW Pump 1-01, the licensee restored SSW Pump 1-02 to service at 10:35 a.m.

The degraded condition on Phase C motor lead was corrected by replacing the entire

cable.

Analysis. The failure to take effective corrective actions for the degraded motor lead

was the performance deficiency. The inspectors consider this finding to be more than

minor because there are several examples in Appendix E of Manual Chapter 0612

where an issue is more than minor because the system is returned to service with a

degraded condition. Although Unit 1 was in an outage, Appendix G of Manual

Chapter 0609 was not applicable, as there was no requirement for Unit 1 to have an

operable SSW system. However, Unit 2 was required to have an operable Unit 1

SSW pump for Mode 1 by Technical Specification 3.7.8. A Phase 1 significance

determination in accordance with Appendix A was performed. Since this finding did not

affect the initiating events cornerstone for Unit 2, it only affected one cornerstone, the

mitigating systems cornerstone. The finding was determined to have a very low safety

significance (Green) because it did not represent a loss of system safety function, was

not an actual loss of safety function for a single Unit 2 train, did not involve equipment or

function specifically designed to mitigate a seismic, flooding, or severe weather initiating

event, and did not involve the total loss of any safety function that contributed to external

event initiated sequences. This finding has a problem identification and resolution

crosscutting aspect because it was caused by lack of effective corrective actions.

-29- Enclosure

Enforcement. Criterion XVI of Appendix B to 10 CFR Part 50 requires that measures

shall be established to assure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment and

nonconformances are promptly identified and corrected. Contrary to the above, on

October 20, 2005, SSW Pump 1-01 was returned to service after identification of a

deficiency in the Phase C motor lead without implementing effective corrective actions.

Because this violation was of very low safety significance and was entered into the

corrective action program as SMF-2005-004220, it is being treated as an NCV,

consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000445/2005005-04, Trip of Station Service Water Pump Due to Degraded

Motor Lead.

4OA5 Other Activities

.1 Pressurizer Penetration Nozzles and Steam Space Piping Connections in U.S.

Pressurized Water Reactors (NRC Bulletin 2004-01) (Temporary Instruction 2515/160)

This Temporary Instruction provided the guidelines to verify compliance with licensee

commitments to NRC Bulletin 2004-01, Inspection of Alloy 82/182/600 Materials Used

in the Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at

Pressurized-Water Reactors. The inspector used the inspection requirements for the

bare metal visual examination to conduct this inspection on the CPSES Unit 1

pressurizer and steam space penetrations during the 1RF11 refueling outage, Fall 2005.

a. Inspection Scope

The inspector performed this performance-based evaluation and assessment to ensure

that the NRC had an independent review of the condition of the pressurizer and steam

space piping alloy 82/182 dissimilar metal welds. The inspector assessed the

effectiveness of the licensee examinations of the pressurizer vessel and penetrations.

Specifically, the inspector:

  • met with licensee representatives to review and discuss inspection plans and

contingencies

  • attended pre-job briefs
  • directly inspected and assessed the condition of the pressurizer and the

associated piping weld penetrations

  • assessed the physical difficulties in performing the inspection, which included

any debris, dirt, boron, and other viewing impediments

  • interviewed the licensee inspectors

-30- Enclosure

  • assessed the licensees ability to distinguish small boron deposits located at the

weld locations

  • verified that the licensee documented deficiencies in their corrective action

program

  • assessed the overall effectiveness of the process used to perform the bare metal

visual inspection

The inspector also reviewed the following documents during this inspection:

Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at

Pressurized-Water Reactors, dated May 28, 2004

Nozzles and in Surge Line Nozzle, dated May 6, 2004

  • Comanche Peak Steam Electric Station 60-Day Response to NRC

Bulletin 2004-01, Inspection of Alloy 82/182/600 Materials Used in the

Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at

Pressurized Water Reactors, TXX-04140, dated July 27, 2004

  • Comanche Peak Steam Electric Station Response to NRCs Request for

Additional Information Request regarding the response to NRC Bulletin 2004-01,

Inspection of Alloy 82/182/600 Materials Used in the Fabrication of Pressurizer

Penetrations and Steam Space Piping Connections at Pressurized Water

Reactors, TXX-05056 , dated March 7, 2005

Corrosion Detection and Evaluation, Revision 3

Examination, issued March 9, 1999

b. Findings

No findings of significance were identified. The inspector concluded that the licensee

met the applicable commitments in that they performed a 100 percent bare metal visual

inspection of the circumference over the axial length of the Alloy 82/182 identified welds

for the Unit 1 pressurizer. These inspections were performed by a VT-2 Level II certified

examiner. The inspector has provided the following details of the inspection as required

by Temporary Instruction 2515/160, Pressurizer Penetration Nozzles and Steam Space

Piping Connections in U.S. Pressurized Water Reactors (NRC Bulletin 2004-01), issued

October 6, 2004.

-31- Enclosure

1. Examination

The licensees examiner was certified in accordance with CPSES procedures to meet

the ASME Section XI for VT-2 Level II.

The examination was conducted in accordance with a CPSES examination plan, RCS

Pressure Boundary DM Weld Supplemental Visual Examination Plan, Revision 1,

approved on March 28, 2005. The examination plan provided: (1) responsibilities for the

examination process; (2) examiner qualification; (3) scope of welds to be examined, a

description of the basic bare metal inspection technique and the expectation of

100 percent inspection coverage; (4) acceptance criteria for the inspection; (5) types of

indications that shall be further investigated; (6) criteria for cleaning the examined area;

and (7) sufficient guidance to satisfy licensee commitments for the inspection. The

inspectors concluded that the inspection plan, combined with training, have provided

adequate guidance for the licensee examiner to identify, disposition, and resolve

deficiencies.

Due to the proximity of the bare metal visual examination, VT-2 Level II qualified

personnel, and the accessability of the specified Alloy 82/182 welds, the inspectors

determined that RCS leakage described in NRC Bulletin 2004-01 would be identified, if

present.

2. Physical condition penetration nozzles and steam space piping

In general, the condition of the weld areas examined were in excellent condition.

Access to the welds only required the removal of a relatively small amount of mirror

insulation, radiation levels were acceptable, and the welds themselves were very new

looking with no residue of previous spills or in-service inspections. Only on the downhill

side of the safety and pressurizer power operated relief valve welds was it necessary to

use a mirror (due to limited space below the piping). All other examinations were

performed with the naked eye.

3. Visual inspection protocol

Direct visual inspection and the use of a mirror were the inspection techniques used by

qualified examination personnel.

4. Inspection coverage

The inspectors observed that the licensee completed a 100 percent, 360 degree bare

metal inspection of the pressurizer penetration nozzles and steam space piping

connections.

5. Capability to identify and characterize small boric acid deposits

-32- Enclosure

The inspectors determined that the direct visual inspections, coupled with mirror

assisted visual inspections were capable of detecting, identifying and characterizing

small boric acid deposits, if present, as described in NRC Bulletin 2004-01. This fact

was determined via direct inspection during the licensee inspection of the pressurizer

and associated steam space piping connections.

6. Identified deficiencies that required repair

No deficiencies were identified.

7. Impediments to effective examinations

There were no impediments that adversely affected effective bare metal visual

examinations. In all examination cases, mirror insulation was required to be removed.

The examination of the pressurizer safety and power operated relief valve line welds

was supplemented by a mirror to allow examination of the downhill side of the welds.

The dose rates were acceptable, and the inspectors received approximately 50 mRem

to complete the in-plant portion of the temporary instruction.

8. Techniques used for augmented inspections

Augmented inspections were not required.

9. Appropriateness of follow-on examinations

Follow-on examinations were not required.

.2 (Closed) URI 05000446/2005009-01: Inoperability of Emergency Power to a Safety Bus

Introduction. A Green self-revealing noncited violation of Technical Specification 3.8.1

was identified because both the alternate offsite AC power source and the EDG did not

supply power to a 6.9 kV safeguards bus within the time assumed in the accident

analysis.

Description. Technical Specification 3.8.1 requires two operable qualified circuits

between the offsite transmission network and the onsite Class 1E AC electrical power

distribution system; and two operable diesel generators (DGs) capable of supplying the

onsite Class 1E power distribution subsystem. On October 19, 2004, an unplanned loss

of the preferred offsite power caused the Unit 2, Train B, 6.9 kV safeguards bus to

deenergize. A degraded Agastat relay delayed the normal power supply breaker from

opening for 30 seconds. Both the EDG and the alternate power supply were prevented

from powering the bus due to a breaker interlock with the normal supply. This delay

rendered both the EDG and alternate offsite AC power supplies inoperable. The

30 second delay in providing power to the safeguards bus would have resulted in the

station not meeting the 10 CFR Part 50, Appendix K, Emergency Core Cooling System

Evaluation Models Acceptance Criteria, for that equipment train.

-33- Enclosure

The licensee had a previous opportunity to correct the degraded Agastat relay issues.

On October 7, 2002, EDG 1-02 unexpectedly started due to a degraded Agastat relay.

The licensee concluded that the failure could have been caused by aging and formed a

corrective action plan to replace all safety-related Agastat relays that have been in

service for greater than the licensee established 12 year lifetime.

EVAL-2003-001440-01-01 stated that the main effect of aging on these relays was an

increase in setpoint drift. The licensee issued SMF-2004-003528 to track the root cause

and corrective actions associated with the faulty Agastat relays. Also, the NRC

previously identified that Agastat relays used in the 6.9 kV bus transfer circuitry were

exhibiting setpoint drift (SMF-2002-001504 and Inspection Report 05000445/2003006;

05000446/2003006). The relay that failed in October 2004 was 16 years old.

Analysis. The licensees failure to identify the cause and implement corrective actions to

prevent repetitive failures of safety-related Agastat relays was a performance deficiency.

The violation was more than minor because it impacted the Mitigating Systems

Cornerstone objective of availability, reliability, and capability of systems that respond to

initiating events. Using Inspection Manual Chapter 0609, Appendix A, Determining the

Significance of Reactor Inspection Findings for At-Power Situations, the finding was

determined to be of very low safety significance because the likelihood of a medium or

large break loss of coolant accident coincident with a loss of offsite power, which are the

only conditions wherein the deficiency would cause a non-negligible change in the

baseline risk profile, is less than or equal to 1E-6 per year. Therefore the change in

core damage frequency will be less than 1E-6 per year. The violation has a problem

identification and resolution crosscutting aspect because the licensee had previously

identified that aged Agastat relays can cause these types of problems but had failed to

take effective corrective actions in a timely manner. The licensee captured the issue in

their corrective action program as SMF-2004-003528.

Enforcement. Technical Specification 3.8.1 required the licensee to restore either the

alternate offsite transmission source or the EDG to the onsite Class 1E AC electrical

distribution system within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to the above, neither the alternate offsite

transmission source nor the EDG were capable of supplying the Class 1E AC electrical

distribution within the response time assumed in the accident analysis. This condition

existed for an extended duration, in excess of the 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> TS limiting condition for

operation. Because this issue is of very low safety significance and has been entered

into the corrective action program as SMF-2004-003528, this violation is being treated

as a NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000446/2005005-05, Inoperability of Emergency Power to a Safety Bus Due to

Degraded Relay.

4OA6 Meetings, Including Exit

Exit Meeting Summary

The inspectors presented the results of the inservice inspection to Mr. M. Lucas, Vice

President of Nuclear Engineering, and other members of licensee management on

-34- Enclosure

October 21, 2005. Licensee management acknowledged the inspection findings. The

licensee confirmed that any proprietary information reviewed by the inspectors was not

retained by the inspectors.

On December 15, 2005, the inspector debriefed the preliminary results of the

emergency preparedness inspection to Mr. M. Blevins, Senior Vice President and Chief

Nuclear Officer, and other members of his staff who acknowledged the findings. The

inspector confirmed that proprietary information was not provided or examined during

the inspection. After additional information was provided by the licensee on January 11,

2006, the inspector presented the inspection results to Mr.R. Flores, Vice President,

Nuclear Operations, and other members of his staff who acknowledged the findings.

On January 31, 2006, Mr. N. O'Keefe presented the inspection results of the URI in

regards to Agastat relays to Mr. T. Hope and D. Snow of your staff, who acknowledged

the finding, by teleconference.

The inspector presented the resident inspection results to Mr. R. Flores, Vice President,

Operations, and other members of licensee management on January 12, 2006. The

inspectors confirmed that proprietary information was not provided or examined during

the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

-35- Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

O. Bhatty, Inservice Test Engineer

M. Blevins, Senior Vice President and Chief Nuclear Officer

D. Bozeman, Manager, Emergency Planning

S. Bradley, Supervisor, Health Physics, Radiation Protection & Safety Services

R. Calder, Executive Assistant

T. Clouser, Manager, Shift Operations

J. Curtis, Radiation Protection Manager, Radiation and Industrial Safety

D. Ellis, Level III Qualified Data Analyst

S. Ellis, Director, Nuclear Oversight

R. Flores, Vice President, Nuclear Operations

T. Hope, Manager, Regulatory Performance

R. Kidwell, Licensing Engineer

M. Lucas, Vice President Nuclear Engineering

F. Madden, Director, Regulatory Affairs

J. Meyer, Technical Support Manager

P. Passalugo, Inservice Inspection Program Coordinator

P. Polefrone, Plant Manger

V. Polizzi, Steam Generator Programs Engineer

S. Sewell, Nuclear Training Manager

J. Skelton, System Engineer

R. Smith, Director, Operations

S. Smith, Director, System Engineering

C. Tran, Engineering Programs Manager

D. Wilder, Radiation and Industrial Safety Manager

I. Witt, Boric Acid Program Coordinator

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000445;05000446/2005005-02, URI Notification Form Accuracy Requires Additional

Guidance (Section 40A1)

Opened and Closed

05000445/2005005-01 NCV Inadequate Corrective Actions for a Leaking Valve

with a Seal Weld which Subsequently Leaked

(Section 1R08.1)

A-1 Attachment

05000445/2005005-03 NCV Trip of Emergency Diesel Generator Due to

Lube Oil Check Valve Installed Backwards

(Section 4OA3.1)05000445/2005005-04 NCV Trip of Station Service Water Pump Due to

Degraded Motor Lead (Section 4OA3.2)05000446/2005005-05 NCV Inoperability of Emergency Power to a

Safety Bus Due to Degraded Relay

(Section 4OA5.2)

Closed

05000446/2005009-01 URI Inoperability of Emergency Power to a

Safety Bus (Section 4OA5.2)

Discussed

None

LIST OF DOCUMENTS REVIEWED

Section 1R08 Inservice Inspection Activities (71111.08)

Boric Acid Evaluation

Unit 1 Containment Boron Leaks 1RF11, draft report

Procedures

Number Title Revision

STA-737 Boric Acid Corrosion Detection and Evaluation 3

TX-ISI-8 VT-1 and VT-3 Visual Examination 56

TX-ISI-11 Liquid Penetrant Examination for Comanche Peak Steam 11

Electric Station

TX-ISI-302 Ultrasonic Examination of Austenitic Piping Welds 2

WLD-106 ASME/ANSI General Welding Requirements 2 with

Procedure

Change

Notice 4

A-2 Attachment

Nondestructive Examination Reports

Penetrant Report, 11PT06, dated October 14, 2005

Ultrasonic, Calibration Data Sheet, Weld TBX-1-4101, dated October 14, 2005

Visual Examination Data, Report No. 11VT14, dated October 11, 2005

Smart Forms

SMF-2004-000502 SMF-2004-002974 SMF-2005-004021

SMF-2004-001292 SMF-2005-000934 SMF-2005-004095

SMF-2004-001971 SMF-2005-001089 SMF-2005-004195

SMF-2004-002758 SMF-2005-001635 SMF-2005-004209

SMF-2004-002074 SMF-2005-002813 SMF-2005-004243

Work Orders

3-04-344421-01

Miscellaneous

Site specific training and testing results of various contracted eddy current testing personnel

Technical Specifications Sections 5.5.9, Amendment 112

TXU Power Comanche Peak Steam Electric Station Steam Generator Assessment for Unit #1

Cycle 11, September 2, 2004

Unit 1 - Second Interval ASME Section XI Inservice Inspection Program Plan, Revision 4

Unit 1 Steam Generator Eddy Current Analysis Guidelines 1RF11, Revision 0

Welding Procedure Specification CP-301, Revision 11

Westinghouse Letter MSR-TRC-1669, Use of Appendix H Qualified Techniques at Comanche

Peak Unit 1 11th RFO, dated September 9, 2005

Various Certifications of education, training, experience and visual acuity of contracted ECT

personnel

Section 1EP1 Exercise Evaluation (71114.01)

EP1

Procedures

1. EPP-109, Duties and Responsibilities of the Emergency Coordinator/Recovery

Manager, Revision 12

A-3 Attachment

2. EPP-116, Emergency Repair and Damage Control and Immediate Entries," Revision 6

3. EPP-204, Activation and Operation of the Technical Support Center," Revision 14

4. EPP-205, Activation and Operation of the Operations Support Center, Revision 11

5. EPP-206, Activation and Operation of the Emergency Operations Facility, Revision 14

6. EPP-303, Operation of the Computer Based Emergency Dose Assessment System,

Revision 12

7. EPP-305, Emergency Exposure Guidelines and Personnel Dosimetry, Revision 11

8. EPP-306, Use of Thyroid Blocking Agents, Revision 10

4OA1

Procedures

1. EPP-201, Assessment of Emergency Action Levels, Emergency Classification, and

Plan Activation, Revision 11

2. EPP-203, Notifications, Revision 14

3. EPP-304, Protective Action Recommendations, Revisions 17 and 18

Section 4OA5.2 , Inoperability of Emergency Power to a Safety Bus

Smart Forms: SMF-2002-003391 , SMF-2004-003528

A-4 Attachment

LIST OF ACRONYMS

ABN abnormal conditions procedure

ARV atmospheric relief valve

ASME American Society of Mechanical Engineers

ATWS anticipated transient without scram

CCW component cooling water

CFR Code of Federal Regulations

CPSES Comanche Peak Steam Electric Station

EDG emergency diesel generator

EVAL evaluation

HVAC heating, ventilation and air conditioning

IPO integrated plant operating procedure

MSM maintenance section-mechanical manual

NCV noncited violation

NRC Nuclear Regulatory Commission

OPT operations testing

PERC plant event review committee

QTE quick technical evaluation

SMF smart form

SOP system operating procedure

SSC structures, systems, or components

SSW station service water

STA station administrative procedure

TDAFW turbine driven auxiliary feed water

UPS uninterruptible power supply

WO work order

A-5 Attachment