ML20265A042

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Commanche Peak Nuclear Power Plant - Triennial Fire Protection Inspection Report 05000445/2020011 and 05000446/2020011 and Notice of Violation
ML20265A042
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 09/21/2020
From: Nick Taylor
NRC/RGN-IV/DRS/EB-2
To: Peters K
Vistra Operations Company
References
IR 2020011
Download: ML20265A042 (17)


See also: IR 05000445/2020011

Text

September 21, 2020

Mr. Ken Peters

Senior Vice President and Chief Nuclear Officer

Vistra Operations Company LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT:

COMANCHE PEAK NUCLEAR POWER PLANT - TRIENNIAL FIRE

PROTECTION INSPECTION REPORT 05000445/2020011 AND

05000446/2020011 AND NOTICE OF VIOLATION

Dear Mr. Peters:

On August 27, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Comanche Peak Nuclear Power Plant and discussed the results of this inspection with

Mr. T. McCool, Site Vice President, and other members of your staff. The results of this

inspection are documented in the enclosed report.

Enclosure 2 discusses a violation associated with a finding of very low safety significance

(Green). The NRC evaluated this violation in accordance Section 2.3.2 of the NRC

Enforcement Policy, which can be found at http://www.nrc.gov/about-

nrc/regulatory/enforcement/enforce-pol.html. We determined that this violation did not meet the

criteria to be treated as a non-cited violation because your staff did not restore compliance

within a reasonable period of time after a violation was previously identified by the NRC as

NCV 05000445/2017008-01; 05000446/2017008-01.

The NRC has concluded that information regarding: (1) the reason for the violations; (2) the

corrective actions that have been taken and the results achieved; and (3) the date when full

compliance was achieved is already adequately addressed on the docket in the inspection

report (Enclosure 2). Therefore, you are not required to respond to this letter unless the record

does not accurately reflect your corrective actions or your position. In that case, or if you

choose to provide additional information, you should follow the instructions specified in the

Notice of Violation (Enclosure 1).

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector

at Comanche Peak Nuclear Power Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

K. Peters

2

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the

NRC Resident Inspector at Comanche Peak Nuclear Power Plant.

This letter, its enclosures, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Nicholas H. Taylor, Chief

Engineering Branch 2

Division of Reactor Safety

Docket Nos. 05000445 and 05000446

License Nos. NPF-87 and NPF-89

Enclosures:

1. Notice of Violation

2. Inspection Report

cc w/ encl: Distribution via LISTSERV

Nicholas

H. Taylor

Digitally signed by

Nicholas H. Taylor

Date: 2020.09.21

08:19:02 -05'00'

ML20265A042

X

SUNSI Review

X

Non-Sensitive

Sensitive

X

Publicly Available

Non-Publicly Available

OFFICE

SRI:EB2

SRI:EB2

RI:EB2

C:PBB

TL:ACES

D:DRA

C:EB2

NAME

JMateychick

JDrake

SAlferink

NOKeefe

JGroom

RLantz

NTaylor

SIGNATURE

/RA/

/RA/

/RA/

/RA/

/RA/

/RA/

/RA/

DATE

9/11/2020

9/13/2020

9/14/2020

9/8/2020

9/8/2020

9/17/2020

9/21/2020

Enclosure 1

NOTICE OF VIOLATION

Vistra Operations Company LLC

Comanche Peak Nuclear Power Plant,

Units 1 and 2

Docket Nos.: 05000445 and 05000446

License Nos.: NPF-87 and NPF-89

During an NRC inspection completed on August 27, 2020, a violation of NRC requirements was

identified. In accordance with the NRC Enforcement Policy, the violation is listed below:

License Condition 2.G for Unit 1 requires, in part, that the licensee implement and

maintain in effect all provisions of the approved fire protection program as described in

the Final Safety Analysis Report through Amendment 78 and as approved in the Safety

Evaluation Report and its supplements through Supplement 24.

License Condition 2.G for Unit 2 requires, in part, that the licensee implement and

maintain in effect all provisions of the approved fire protection program as described in

the Final Safety Analysis Report through Amendment 87 and as approved in the Safety

Evaluation Report and its supplements through Supplement 27.

The Fire Protection Report was included as part of the licensees approved fire

protection program for both units. Section I-2.4 states, in part, that administrative control

of the fire protection program is provided through station procedures to ensure that the

fire protection systems and equipment are operable and properly maintained and

operational at all times. Section IV-2.1.c.1 requires, in part, that the required fire rated

assemblies and penetration sealing devices are confirmed operable by visually

inspecting the exposed surfaces using a site approved sampling plan every 18 months.

Contrary to this requirement, from 2009 to June 25, 2020, the licensee failed to ensure

that fire protection program procedures used to establish inspection criteria for

penetration sealing devices appropriately captured all required penetration sealing

devices for visual inspection using a site approved sampling plan every 18 months.

Specifically, Procedure FIR-310, Penetration Seal Inspection, revised in response to

NCV 05000445/2017008-01; 05000446/2017008-01, Failure to Implement and Maintain

Adequate Inspection Procedures for Penetration Sealing Devices, did not ensure that all

required penetration sealing devices would be inspected within the licensees sampling

plan interval. Consequently, the licensee failed to restore compliance to the previous

NCV since the revised procedure did not ensure the fire rated penetration seals in the

auxiliary building were included in the maintenance list so they would be scheduled for

inspection.

This violation is associated with a Green SDP finding.

2

The NRC has concluded that information regarding the reason for the violation, the corrective

actions taken to correct the violation and prevent recurrence and the date when full compliance

was achieved is already adequately addressed in the enclosed inspection report (Enclosure 2).

However, you are required to submit a written statement or explanation pursuant to

10 CFR 2.201 if the description therein does not accurately reflect your corrective actions or

your position. In that case, or if you choose to respond, clearly mark your response as a "Reply

to a Notice of Violation," and send it to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 1600 East Lamar Blvd.,

Arlington, Texas 760114511, and a copy to the NRC Resident Inspector at the Comanche

Peak Nuclear Power Plant that is the subject of this Notice, within 30 days of the date of the

letter transmitting this Notice of Violation (Notice).

If you choose to respond, your response will be made available electronically for public

inspection in the NRC Public Document Room or from the NRCs document system (ADAMS),

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html. Therefore, to

the extent possible, the response should not include any personal privacy or proprietary

information so that it can be made available to the public without redaction.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days of receipt.

Dated this 21st day of September 2021

Enclosure 2

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000445 and 05000446

License Numbers:

NPF-87 and NPF-89

Report Numbers:

05000445/2020011 and 05000446/2020011

Enterprise Identifier: I-2020-011-0039

Licensee:

Vistra Operations Company LLC

Facility:

Comanche Peak Nuclear Power Plant

Location:

Glen Rose, Texas

Inspection Dates:

June 08, 2020 to August 27, 2020

Inspectors:

S. Alferink, Reactor Inspector

J. Drake, Senior Reactor Inspector

J. Mateychick, Senior Reactor Inspector

Approved By:

Nicholas H. Taylor, Chief

Engineering Branch 2

Division of Reactor Safety

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting a triennial fire protection inspection at Comanche Peak Nuclear

Power Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight

Process is the NRCs program for overseeing the safe operation of commercial nuclear power

reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Implement and Maintain Adequate Inspection Procedures for Penetration Sealing

Devices

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NOV 05000445;05000446/2020011-01

Opened/Closed

H.8 - Procedure

Adherence

71111.21N.

05

The team identified a Green violation of License Condition 2.G for the licensees failure to

maintain adequate procedures for the inspection of penetration sealing devices as required by

the licensees Fire Protection Report, Section IV-2.1.c.1. Specifically, the licensee

implemented a revision to Fire Protection Procedure FIR-310, Penetration Seal Inspection,

in 2020 to provide corrective actions for an NCV issued in 2017 due to the procedure not

ensuring that all penetrations seals would be inspected during the required 15-year cycle.

However, the revised procedure incorrectly excluded from the inspection schedule all

penetration seals in the auxiliary building.

Additional Tracking Items

None

3

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.21N.05 - Fire Protection Team Inspection (FPTI)

SSC Credited for Fire Prevention, Detection, Suppression, or Post-Fire SSD Review

(IP Section 03.01) (4 Completed Samples and 2 Partial Samples)

The inspectors verified that components and/or systems will function as required to support

the credited functions stated for each sample. Additional inspection considerations are

located in the fire hazards analysis (FHA) or safe shutdown analysis (SSA).

(1)

The auxiliary feedwater system and the steam generator power-operated relief

valves.

(2)

The fire water system including the fire water tanks, fire pumps, and yard loop

distribution piping system.

(3)

The fire detection systems and fire suppression systems installed in Fire Area EN,

Unit 1 Cable Spreading Room.

(4)

The fire detection systems and fire suppression systems installed in Fire Area EM,

Unit 2 Cable Spreading Room.

(5)

(Partial Sample)

Subsection b states, Verify that operator actions can be accomplished as assumed

in the licensees FHA, or as assumed in the licensees fire probabilistic risk

assessment (FPRA) analysis and SSA. Due to conditions related to COVID-19 in

the area of the plant, onsite inspector walkdowns of procedures with licensee

operations personnel could not be performed at this time. An inspector will visit the

licensees site to perform this activity later as conditions permit. The results of the

additional inspection will be documented in a resident inspectors quarterly report.

(6)

(Partial Sample)

Subsection e states, Perform a walkdown inspection to identify equipment alignment

discrepancies. Inspect for deficient conditions such as corrosion, missing fasteners,

cracks, and degraded insulation. Due to conditions related to COVID-19 in the area

of the plant, onsite inspector walkdowns of fire protection systems with licensee fire

protection personnel could not be performed at this time. An inspector will visit the

licensees site to perform this activity later as conditions permit. The results of the

additional inspection will be documented in a resident inspectors quarterly report.

4

Fire Protection Program Administrative Controls (IP Section 03.02) (2 Samples)

The inspectors verified that the selected control or process is implemented in accordance

with the licensees current licensing basis. If applicable, ensure that the licensees fire

protection program contains adequate procedures to implement the selected administrative

control. Verify that the selected administrative control meets the requirements of all

committed industry standards.

(1)

The inspectors reviewed the licensees administrative controls of hot work, transient

combustibles, and fire impairments.

(2)

The inspectors reviewed the licensees fire brigade training program.

Fire Protection Program Changes/Modifications (IP Section 03.03) (2 Samples)

(1)

The inspectors reviewed changes to the approved fire protection program concerning

the inspection of fire rated penetration sealing devices.

(2)

The inspectors reviewed the changes to the approved fire protection program

incorporated into the Comanche Peak Nuclear Power Plant Fire Protection Report

Units 1 and 2, Revision 33.

INSPECTION RESULTS

Failure to Implement and Maintain Adequate Inspection Procedures for Penetration Sealing

Devices

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NOV 05000445; 05000446/2020011-

01

Opened/Closed

H.8 - Procedure

Adherence

71111.21N.0

5

The team identified a Green violation of License Condition 2.G for the licensees failure to

maintain adequate procedures for the inspection of penetration sealing devices as required

by the licensees Fire Protection Report, Section IV-2.1.c.1. Specifically, the licensee

implemented a revision to Fire Protection Procedure FIR-310, Penetration Seal Inspection,

in 2020 to provide corrective actions for an NCV issued in 2017 due to the procedure not

ensuring that all penetrations seals would be inspected during the required 15-year cycle.

However, the revised procedure incorrectly excluded from the inspection schedule all

penetration seal devices in the auxiliary building.

Description: During the 2017 triennial fire protection inspection, the NRC identified a Green

non-cited violation for the failure to maintain adequate procedures for the inspection of fire

penetration seals. As part of this violation, the NRC noted that the licensee used an

automated random sampling process for selection of penetration seals for inspection and this

process failed to ensure that all required penetration seals were inspected within their 15-year

sampling plan interval.

The team documented this violation as NCV 05000445/2017008-01; 05000446/2017008-01,

Failure to Implement and Maintain Adequate Inspection Procedures for Penetration Sealing

Devices, on July 31, 2017. The licensee documented this issue in the corrective action

program in Condition Report CR-2017-007746.

5

In response to this violation, the licensee generated a list of over 16,000 fire penetration seals

that required inspection. The licensee divided this list into different groups based on the

penetration seal location. The licensee associated these groups with 15 repetitive preventive

maintenance tasks. The licensee then updated Procedure FIR-310, Penetration Seal

Inspection, to require the inspection of penetration seals using one of these 15 preventive

maintenance tasks each year over a 15-year period, thereby ensuring that each penetration

seal would be inspected once during the 15-year period. The licensee revised this procedure

on February 6, 2020.

During the current inspection, the team reviewed the revised inspection procedure and the

repetitive preventive maintenance tasks. The team identified that the fire penetration seal

group associated with the auxiliary building was not included in any of the 15 repetitive

preventive maintenance tasks. This group contained 1,956 penetration seals. Since this

group was not included in any of the 15 preventive maintenance tasks, the team determined

that these 1,956 penetration seals were not scheduled to be inspected during the current

15-year period.

In response to the teams questions, the licensee reviewed the previous fire penetration seal

inspections for the penetration seals associated with the auxiliary building. The licensee

identified that 1,192 of the penetration seals were inspected and 764 of the penetration seals

were not inspected during the previous 15-year period. Of the penetration seals that were

inspected, the licensee determined that only two of them failed the inspection.

Corrective Actions: There was no immediate safety concern since the licensee had observed

a very low failure rate of penetration seals during the previous 15-year cycle. The licensee

entered this issue into the corrective action program for resolution and incorporated the

auxiliary building penetration seals into eight of the preventive maintenance tasks required by

procedure FIR-310. The licensee restored compliance with the approved fire protection

program on June 25, 2020, and performed an Organizational Effectiveness Investigation to

determine the cause of the violation. The licensee identified a lack of attention to detail and

verbatim compliance with procedure STA-422, Corrective Action Program, as causes. The

verification of the lists of penetration seals to be inspected was not completed and was

transferred to future actions. This was not in compliance with procedure STA-442, Section

6.6, Condition Report Closure to Future Actions, which states that when the condition report

documents a Licensing Basis Deviation the condition report may not close to future actions.

The licensee provided coaching for the personnel involved.

Corrective Action References: Condition Report CR-2020-004473

Performance Assessment:

Performance Deficiency: The failure to ensure that fire protection program procedures used

to establish inspection criteria for penetration sealing devices appropriately captured all

required penetration sealing devices for visual inspection using a site approved sampling plan

was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Protection Against External Factors attribute of the

Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences.

6

Significance: The inspectors assessed the significance of the finding using Appendix F, Fire

Protection and Post - Fire Safe Shutdown SDP. The team assigned the fire confinement

category to the finding since it involved fire rated penetration seals. The team noted that the

licensee observed a very low failure rate of the auxiliary building penetration seals during the

past 15 years.

The team discussed the finding with a senior reactor analyst because the finding involved

multiple fire areas. In consultation with the senior reactor analyst, the team assigned a low

degradation rating to the finding because of the very low failure rate and the fact that a

majority of the auxiliary building penetration seals have been previously inspected.

The team determined the finding was of very low risk significance (Green) in Step 1.3 since

the finding was assigned a low degradation rating.

H.8 - Procedure Adherence: Individuals follow processes, procedures, and work instructions.

Specifically, the licensee failed to complete required verifications of corrective actions to

assure adequacy.

Enforcement:

Violation: License Condition 2.G for Unit 1 requires, in part, that the licensee implement and

maintain in effect all provisions of the approved fire protection program as described in the

Final Safety Analysis Report through Amendment 78 and as approved in the Safety

Evaluation Report and its supplements through Supplement 24.

License Condition 2.G for Unit 2 requires, in part, that the licensee implement and maintain in

effect all provisions of the approved fire protection program as described in the Final Safety

Analysis Report through Amendment 87 and as approved in the Safety Evaluation Report

and its supplements through Supplement 27.

The Fire Protection Report was included as part of the licensees approved fire protection

program for both units, and states, in part, that administrative control of the fire protection

program is provided through station procedures to assure that the fire protection equipment

and systems are operable and properly maintained. This includes periodic tests and

inspections, compensatory measures concerning items which may be inoperable, and quality

assurance audits. Section IV-2.1.c.1 of the Fire Protection Report required, in part, that the

required fire rated assemblies and penetration sealing devices are confirmed operable by

visually inspecting the exposed surfaces using a site approved sampling plan every 18

months.

Contrary to this requirement, from 2009 to June 25, 2020, the licensee failed to ensure that

fire protection program procedures used to establish inspection criteria for penetration sealing

devices appropriately captured all required penetration sealing devices for visual inspection

using a site approved sampling plan every 18 months. Specifically, Procedure FIR-310,

Penetration Seal Inspection, revised in response to NCV 05000445/2017008-01; 05000446/2017008-01, Failure to Implement and Maintain Adequate Inspection Procedures

for Penetration Sealing Devices, did not ensure that all required penetration sealing devices

would be inspected within the licensees sampling plan interval. Consequently, the licensee

failed to restore compliance to the previous NCV since the revised procedure did not ensure

the fire rated penetration seals in the auxiliary building were included in the maintenance list

so they would be scheduled for inspection.

7

Enforcement Action: This violation is being cited because the licensee failed to restore

compliance after the violation was previously identified consistent with Section 2.3.2 of the

Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On June 25, 2020, the inspectors presented the triennial fire protection inspection results

to Mr. T. McCool, Site Vice President, and other members of the licensee staff in a

debrief meeting.

On August 27, 2020, the inspectors presented the triennial fire protection inspection

results to Mr. T. McCool, Site Vice President, and other members of the licensee staff in

an exit meeting.

8

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.21N.05 Calculations

0210-063-0031

Unit 1 and Common Hydraulic Calculation Verification

1

71111.21N.05 Calculations

2-FP-0006

Determination of the Pressure and Flow at the Fire Pump

Discharge

1

71111.21N.05 Calculations

DBD-ME-003

Control Room Habitability

13

71111.21N.05 Calculations

DBD-ME-027

Radiological Accident Analysis

13

71111.21N.05 Corrective Action

Documents

CR-2010-004331 CR-2013-001933 CR-2015-004590

CR-2016-002210 CR-2017-001410 CR-2017-001552

CR-2017-002011 CR-2017-002035 CR-2017-003949

CR-2017-004235 CR-2017-004324 CR-2017-004560

CR-2017-004691 CR-2017-007536 CR-2017-007745

CR-2017-007746 CR-2017-008728 CR-2017-008890

CR-2017-008961 CR-2018-006426 CR-2018-007079

CR-2018-007442 CR-2018-008405 CR-2019-003625

CR-2019-005334 CR-2019-009310 CR-2020-000558

CR-2020-000864 CR-2020-001701 CR-2020-002817

CR-2020-003204 TR-2014-010354 TR-2014-010370

TR-2014-012160 TR-2016-003548 TR-2017-003590

TR-2017-008741 TR-2017-012520 TR-2018-006427

TR-2019-003269 TR-2020-000040 TR-2020-001999

TR-2020-004586 TR-2917-009888

71111.21N.05 Corrective Action

Documents

Resulting from

Inspection

CR-2020-004397 CR-2020-004473 IR-2020-004760

71111.21N.05 Fire Plans

FPI - 504

Electrical & Control Building Elevation 807'-0"

Unit 2 Cable Spreading Room

1

71111.21N.05 Fire Plans

FPI - 505

Electrical & Control Building

Unit 1 Cable Spreading Room Elevation 807'-0"

3

71111.21N.05 Miscellaneous

Comanche Peak Nuclear Power Plant Fire Protection

Report Unit 1 and Unit 2

32 & 33

71111.21N.05 Miscellaneous

Comanche Peak Fire PRA Summary

1

71111.21N.05 Miscellaneous

AO5407

Response to Fire in the Control Room or Cable Spreading

02/21/03

9

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Room, Perform AO #1 Actions

71111.21N.05 Miscellaneous

20023

Transient Combustible Permit

0

71111.21N.05 Miscellaneous

20060

Transient Combustible Permit

0

71111.21N.05 Miscellaneous

20079

Transient Combustible Permit

0

71111.21N.05 Miscellaneous

20085

Transient Combustible Permit

0

71111.21N.05 Miscellaneous

20088

Transient Combustible Permit

0

71111.21N.05 Miscellaneous

2323-AS-18

Specification Hollow Metal Doors and Frames

1

71111.21N.05 Miscellaneous

5527599

Fire Permit

0

71111.21N.05 Miscellaneous

5563972

Fire Permit

0

71111.21N.05 Miscellaneous

5595567

Fire Permit

0

71111.21N.05 Miscellaneous

5611222

Fire Permit

0

71111.21N.05 Miscellaneous

5832506

Fire Permit

0

71111.21N.05 Miscellaneous

AO6413

Response to fire in Control Room or Cable spreading

room

13

71111.21N.05 Miscellaneous

AO6414

Response to a fire in the Control Room or Cable

Spreading Room opening pressurizer PORV MOV 8000A

12/19/01

71111.21N.05 Miscellaneous

AO6415

Align Alternate Auxiliary Feedwater Supply from Station

Service Water

71111.21N.05 Miscellaneous

DBD-ME-001

CPSES Fire Protection Program Design Basis Document

12

71111.21N.05 Miscellaneous

DBD-ME-225

Fire Suppression System

27

71111.21N.05 Miscellaneous

FB44.FBR.193

FBR - 2019 Live Fire Requal Training

0

71111.21N.05 Miscellaneous

FB44FBR196

FBR - 2020 Live Fire Requal Training

0

71111.21N.05 Miscellaneous

FBD2FBI103

Portable Fire Extinguishers 1

0

71111.21N.05 Miscellaneous

FBD2FBI107

Fire Hose

0

71111.21N.05 Miscellaneous

FBD2FBI108

Fire Streams and Nozzles

0

71111.21N.05 Miscellaneous

FBD2FBI109

Hoselines and Master Streams

0

71111.21N.05 Miscellaneous

FBD2FBI201

Personal Protective Equipment (Fire Brigade)

0

71111.21N.05 Miscellaneous

FBD2FBI204

Search and Rescue

0

71111.21N.05 Miscellaneous

FBD2FBI207

Handling Hoselines

0

71111.21N.05 Miscellaneous

FBD2FBI208

Foam Operations (Fire Brigade)

0

71111.21N.05 Miscellaneous

FBDSFBI102

Combustion and Fire Behavior

0

71111.21N.05 Miscellaneous

Final Safety

Analysis Report

Emergency Planning

Amendment

No. 109

10

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Section 13.3

71111.21N.05 Miscellaneous

Final Safety

Analysis Report

Section 9.5.1

Fire Protection Program

Amendment

No. 109

71111.21N.05 Miscellaneous

OER-2017-

007276

IER L4-17-6 Fire Event Trend and Causes

06/13/17

71111.21N.05 Miscellaneous

OER-2017-

009751

NRC IN-2917-04 High Energy Arching Faults In Electrical

Equipment Containing Aluminum Components

08/29/17

71111.21N.05 Miscellaneous

OER-2018-

006316

NRC Information Notice 2018-09; Electrical Arc Flash

Caused by Foreign Material Damages Fire Door

09/20/18

71111.21N.05 Miscellaneous

RO4406

Respond To Fire In Control Room Or Cable Spread Room 08/31/08

71111.21N.05 Procedures

ABN-803A

Response To A Fire In The Control Room Or Cable

Spreading Room

13

71111.21N.05 Procedures

ABN-803B

Response To A Fire In The Control Room Or Cable

Spreading Room

10

71111.21N.05 Procedures

ABN-804A

Response To Fire In The Safeguards Building

6

71111.21N.05 Procedures

ABN-804B

Response To Fire In The Safeguards Building

4

71111.21N.05 Procedures

ABN-805A

Response To Fire In The Auxiliary Building Or The Fuel

Building

8

71111.21N.05 Procedures

ABN-805B

Response To Fire In The Auxiliary Building Or The Fuel

Building

8

71111.21N.05 Procedures

ABN-806A

Response To Fire In The Electrical And Control Building

8

71111.21N.05 Procedures

ABN-806B

Response To Fire In The Electrical And Control Building

6

71111.21N.05 Procedures

ABN-807A

Response To Fire In The Containment Building

8

71111.21N.05 Procedures

ABN-807B

Response To Fire In The Containment Building

6

71111.21N.05 Procedures

ABN-808A

Response To Fire In Service Water Intake Structure

6

71111.21N.05 Procedures

ABN-808B

Response To Fire In Service Water Intake Structure

4

71111.21N.05 Procedures

ABN-809A

Response To Oil Leak Or Fire In The Turbine Building

8

71111.21N.05 Procedures

ABN-809B

Response To Oil Leak Or Fire In The Turbine Building

5

71111.21N.05 Procedures

ABN-901

Fire Protection System Alarms or Malfunctions

9

71111.21N.05 Procedures

FBD2FBI104

Portable Fire Extinguishers 2

0

71111.21N.05 Procedures

FBD2ICS111

Incident Management

0

71111.21N.05 Procedures

FIR-201

Preparation, Control, Review and Use of Fire Preplan

9

11

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Instructions

71111.21N.05 Procedures

FIR-302

Fire Door Tests and Inspections

8

71111.21N.05 Procedures

FIR-308

Fire Brigade Equipment

4

71111.21N.05 Procedures

FIR-310

Penetration Seal Inspection

4

71111.21N.05 Procedures

FIR-PX-3200

Fire Suppression Loop Flow Test

3

71111.21N.05 Procedures

FIR-PX-3801

Electric Driven Fire Protection Pump CPX-FPAPFP-04

Operability Test

4

71111.21N.05 Procedures

FIR-PX-3802

Diesel Driven Fire Protection Pump CPX-FPAPFP-05

Operability Test

4

71111.21N.05 Procedures

FIR-PX-3803

Diesel Driven Fire Protection Pump CPX-FPAPFP-06

Operability Test

4

71111.21N.05 Procedures

INC-3020

Maintenance and Rework of Plant Doors

2

71111.21N.05 Procedures

OPT-220

Fire Suppression Water System Operability Test

13

71111.21N.05 Procedures

STA-202

Nuclear Generation Procedure Change Process

39

71111.21N.05 Procedures

STA-421

Control of Issue Reports

21

71111.21N.05 Procedures

STA-422

Corrective Action Program

34

71111.21N.05 Procedures

STA-602

Temporary Modifications and Transient Equipment

Placements

20

71111.21N.05 Procedures

STA-716

Modification Process

27

71111.21N.05 Procedures

STA-722

Fire Protection Program

7

71111.21N.05 Procedures

STA-723

Fire Protection Systems/Equipment Requirements

5

71111.21N.05 Procedures

STA-724

Fire Reporting and Response

4

71111.21N.05 Procedures

STA-727

Fire Brigade

6

71111.21N.05 Procedures

STA-729

Control of Transient Combustibles, Ignition Sources and

Fire Watches

12

71111.21N.05 Procedures

STA-738

Fire Protection Systems/Equipment Impairments

7

71111.21N.05 Procedures

STI-422.03

Performing Coaching and Investigations

2

71111.21N.05 Procedures

STI-422.04

Processing of Condition Reports

0

71111.21N.05 Procedures

STI-423.01

Processing Tracking Reports

0

71111.21N.05 Procedures

TRA-104

Fire Protection Training

16

71111.21N.05 Self-

Assessments

EVAL-2018-010

Fire Protection Program

12/15/18

71111.21N.05 Self-

IR-2019-005207

Fire Protection Self-Assessment Report

0

12

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Assessments

71111.21N.05 Work Orders

5209230, 5329355, 5511184, 5557316, 5558257,

5578521, 5655850, 5668385, 5747089, 5749736,

5757975, 5821733, 5840282, 5841173, 5856117,

5861142, 5920545