ML22299A056

From kanterella
Jump to navigation Jump to search
Integrated Inspection Report 05000445/2022003 and 05000446/2022003 and Notice of Violation
ML22299A056
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 11/01/2022
From: Greg Werner
NRC/RGN-IV/DORS/PBB
To: Peters K
Vistra Operations Company
Werner G
References
IR 2022003
Download: ML22299A056 (30)


See also: IR 05000445/2022003

Text

November 1, 2022

Mr. Ken Peters

Senior Vice President

and Chief Nuclear Officer

Vistra Operations Company, LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 INTEGRATED

INSPECTION REPORT 05000445/2022003 AND 05000446/2022003 AND NOTICE

OF VIOLATION

Dear Mr. Peters:

On September 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at Comanche Peak Nuclear Power Plant, Units 1 and 2. On October 6, 2022, the

NRC inspectors discussed the results of this inspection with Mr. A. Marzloff, Plant Manager, and

other members of your staff. The results of this inspection are documented in the enclosed

report.

The enclosed report discusses a Severity Level IV violation. The NRC evaluated this violation in

accordance with section 2.3.2 of the NRC Enforcement Policy, which can be found at

http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html. The violation is cited in

Enclosure 1, Notice of Violation (Notice), and the circumstances surrounding it are described in

detail in the subject inspection report (Enclosure 2). We determined that this violation did not

meet the criteria to be treated as a non-cited violation (NCV) because your staff failed to restore

compliance within a reasonable period after the violation was identified consistent with

section 2.3.2 of the NRC Enforcement Policy. You are required to respond to this letter and

should follow the instructions specified in the enclosed Notice when preparing your response.

The NRCs review of your response will also determine whether further enforcement action is

necessary to ensure your compliance with regulatory requirements.

Additionally, one finding of very low safety significance (Green) is documented in this report.

This finding involved a violation of NRC requirements. We are treating this violation as an NCV

consistent with section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

K. Peters 2

Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector

at Comanche Peak Nuclear Power Plant, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the

NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice and Procedure, a copy of

this letter, its enclosures, and your response will be made available electronically for public

inspection in the NRC Public Document Room or in the NRCs Agencywide Documents

Access and Management System (ADAMS), accessible from the NRC website at

http://www.nrc.gov/reading-rm/adams.html. To the extent possible, any response should not

include any personal privacy or proprietary information so that it can be made available to the

public without redaction.

Sincerely,

Signed by Werner, Gregory

on 11/01/22

Gregory E. Werner, Chief

Projects Branch B

Division of Operating Reactor Safety

Docket Nos. 05000445, 05000446

License Nos. NPF-87, NPF-89

Enclosures:

1. Notice of Violation

2. Inspection Report 05000445/2022003

and 05000446/2022003

cc w/ encl: Distribution via LISTSERV

ML22299A056

X Non-Sensitive x Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE SRI:DORS/B RI:DORS/B SEC:ACES TL/ACES

SIGNATURE JEllegood /RA/ NDay /RA/ JKramer /RA/ JGroom /RA/

DATE 10/19/2022 10/19/2022 10/27/2022 10/28/2022

OFFICE SPE:DORS/B BC:DORS/B D: DORS BC:DORS/B

SIGNATURE DProulx /RA/ GWerner GEW RLantz GWerner GEW

DATE 10/26/2022 10/26/2022 10/31/2022 11/01/2022

NOTICE OF VIOLATION

Vistra Operations Company, LLC Docket No. 50-445

Comanche Peak Nuclear Power Plant, Unit 1 License No. NPF-87

During an NRC inspection conducted from June 1 to September 30, 2022, a violation of NRC

requirements was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

Title 10 of the Code of Federal Regulations (10 CFR) 50.59(c)(2) requires, in part, that a

licensee shall obtain a license amendment pursuant to 10 CFR 50.90 prior to implementing

a proposed change if the change would: result in more than a minimal increase in the

likelihood of occurrence of a malfunction of a structure, system, or component (SSC)

important-to-safety previously evaluated in the final safety analysis report (as updated); or,

create a possibility for a malfunction of an SSC important to safety with a different result

than any previously evaluated in the final safety analysis report (as updated).

Contrary to the above, from February 13, 2019, to September 30, 2022, the licensee failed

obtain a license amendment pursuant to 10 CFR 50.90 prior to implementing a proposed

change if the change that would: result in more than a minimal increase in the likelihood of

occurrence of a malfunction of a SSC important-to-safety previously evaluated in the final

safety analysis report (as updated); or, create a possibility for a malfunction of an SSC

important to safety with a different result than any previously evaluated in the final safety

analysis report (as updated). Specifically, the licensee revised the Final Safety Analysis

Report associated with the Unit 1 DC power system to change the facility's commitments to

NRC Regulatory Guide (RG) 1.81, which demonstrated compliance with General Design

Criterion 5, without obtaining a license amendment.

This is a Severity Level IV violation (Enforcement Policy Section 6.1.d.4).

Pursuant to the provisions of 10 CFR 2.201, Vistra Operations Company, LLC., is hereby

required to submit a written statement or explanation to U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 1600 E. Lamar Blvd., Arlington,

TX 76011-4511, and a copy to the NRC resident inspector at Comanche Peak Nuclear Power

Plant, Units 1 and 2, within 30 days of the date of the letter transmitting this Notice of Violation

(Notice). This reply should be clearly marked as a Reply to a Notice of Violation and should

include for the violation: (1) the reason for the violation or, if contested, the basis for disputing

the violation or severity level, (2) the corrective steps that have been taken and the results

achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will

be achieved.

Your response may reference or include previous docketed correspondence if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

2

If you contest this enforcement action, you should also provide a copy of your response, with the

basis for your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs Agencywide Documents Access and Management

System (ADAMS), accessible from the NRC website at http://www.nrc.gov/reading-

rm/adams.html, to the extent possible, it should not include any personal privacy or proprietary

information so that it can be made available to the public without redaction.

If personal privacy or proprietary information is necessary to provide an acceptable response,

then please provide a bracketed copy of your response that identifies the information that

should be protected and a redacted copy of your response that deletes such information. If you

request that such material is withheld from public disclosure, you must specifically identify the

portions of your response that you seek to have withheld and provide in detail the bases for your

claim (e.g., explain why the disclosure of information will create an unwarranted invasion of

personal privacy or provide the information required by 10 CFR 2.390(b) to support a request for

withholding confidential commercial or financial information).

Dated this 1st day of November, 2022

3

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers: 05000445 and 05000446

License Numbers: NPF-87 and NPF-89

Report Numbers: 05000445/2022003 and 05000446/2022003

Enterprise Identifier: I-2022-003-0003

Licensee: Vistra Operations Company, LLC

Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2

Location: Glen Rose, TX 76043

Inspection Dates: June 1 to September 30, 2022

Inspectors: R. Alexander, Regional State Liaison Officer

J. Braisted, Senior Reactor Inspector

D. Bryen, Reactor Inspector

N. Day, Resident Inspector

J. Ellegood, Senior Resident Inspector

G. George, Senior Reactor Inspector

R. Kopriva, Senior Reactor Inspector

D. Reinert, Reactor Inspector

H. Strittmatter, Emergency Preparedness Inspector

Approved By: Gregory E. Werner, Chief

Projects Branch B

Division of Operating Reactor Safety

Enclosure 2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Comanche Peak Nuclear Power Plant,

Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight

Process is the NRCs program for overseeing the safe operation of commercial nuclear power

reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Restore Compliance for Non-Cited Violation 05000445/2019001-02 "Failure to

Evaluate a Change to the Facility DC Power System"

Cornerstone Severity Cross-Cutting Report

Aspect Section

Not Applicable Severity Level IV Not Applicable 71111.17T

NOV 05000445/2022003-01

Open

The inspectors identified a Severity Level IV, notice of violation of 10 CFR 50.59, "Changes,

tests, and experiments," for the failure to restore compliance of previously identified non-cited

violation 05000445/2019001-02. The previous violation identified the licensee's failure to

obtain a license amendment or perform a written evaluation demonstrating the basis for not

obtaining a license amendment prior to making a change to the facility as described in the

Final Safety Analysis Report. Specifically, the licensee revised the Final Safety Analysis

Report to change the facility's commitments to NRC Regulatory Guide 1.81, which

demonstrated compliance with General Design Criterion 5, without obtaining a license

amendment.

Degraded Emergency Response Facility Communications Capabilities

Cornerstone Significance Cross-Cutting Report

Aspect Section

Emergency Green [P.3] - 71152A

Preparedness NCV 05000445,05000446/2022003-02 Resolution

Open/Closed

The inspectors identified a Green finding and associated non-cited violation of 10 CFR

50.47(b)(6) when the licensee failed to ensure prompt communications among principal

response organizations were available from the main control room. Specifically, on March 21,

2022, due to a loss of internet and degraded backup communication methods, there were no

communication methods available from within the main control room to contact offsite

response organizations.

Additional Tracking Items

None.

2

PLANT STATUS

On September 5, Unit 1 tripped due to a trip of the main turbine from 100 percent power. The

licensee corrected the issue causing the trip and restarted Unit 1 on September 12, 2022. Unit 1

returned to 100 percent on September 15, 2022.

Unit 2 remained at or near rated thermal power for the entire assessment period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) High winds and drought conditions contributed to wildfires that came within three

miles of the plant on July 19, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 1, diesel generators diesel and exhaust systems on July 20, 2022

(2) fire pumps on July 22, 2022

(3) independent spent fuel storage installation on July 30, 2022

(4) Unit 2, train A diesel generator starting air system on September 1, 2022

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the

Unit 2 containment spray A system on August 4, 2022.

3

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1) Unit 2, trains A and B component cooling water pumps on August 8, 2022

(2) Units 1 and 2, component cooling water heat exchanger room on August 8, 2022

(3) Unit 1, emergency diesel generator 1-01 room and fuel oil day tank 1-01 room on

September 26, 2022

(4) Unit 1, emergency diesel generator 1-02 room and fuel oil day tank 1-02 room on

September 26, 2022

(5) Unit 1, charging pump rooms on September 29, 2022

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an

unannounced fire drill on September 2, 2022.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Unit 2, feedwater enclosures

(2) 25KV power cable vaults supplying independent spent fuel storage installation power

71111.07T - Heat Exchanger/Sink Performance

Heat Exchanger (Service Water Cooled) (IP Section 03.02) (1 Sample)

The inspectors evaluated heat exchanger performance on the following:

(1) component cooling water pump lube oil cooler 1-02

Heat Exchanger (Closed Loop) (IP Section 03.03) (2 Samples)

The inspectors evaluated heat exchanger performance on the following:

(1) motor driven auxiliary feedwater pump room fan cooler 1-07

(2) residual heat removal pump room fan cooler 2-01

Ultimate Heat Sink (IP Section 03.04) (1 Sample)

The inspectors evaluated the ultimate heat sink performance on the following:

(1) ultimate heat sink and service water system

4

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control

room during plant cooldown to 205 degrees Fahrenheit on September 7, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated a simulated control room fire and plant

shutdown on August 9, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1) Units 1 and 2, 6.9 kilovolt distribution system.

(2) Unit 2, turbine control system.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1) Unit 1, risk controls associated with feedwater heater outlet pressure transmitter 0508

card replacement on July 17, 2022

(2) Unit 1, operator actions to maintain availability of the turbine driven auxiliary

feedwater pump 1-01 on August 4, 2022

(3) Unit 1, flooding, and operator response due to circulating water lube water

pumps 1-01 and 1-02 flooding on August 9, 2022

(4) Unit 1, forced outage risk for the week of September 5, 2022

(5) Unit 1, startup risk on September 11 and 12, 2022

(6) Unit 1, risk during emergent motor driven feedwater pump 1-01 recirculation line leak

on September 15, 2022.

5

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1) Unit 2, pressurizer heaters per condition report 2022-5808

(2) Unit 1, pressurizer master controller 1-PK-455A per condition report 2022-005681

(3) Unit 1, turbine driven and motor driven feedwater pump 1-02 per condition

report 22-006748

(4) Unit 1, emergency diesel generator 1-02 starting air receiver 1-03 leaking by

valve 1DO-0041 per condition reports 21-008182 and 22-006804

(5) Unit 2, tornado door per tracking report 2022-006923.

71111.17T - Evaluations of Changes, Tests, and Experiments

Sample Selection (IP Section 02.01) (27 Samples)

The inspectors reviewed the following evaluations, screenings, and/or applicability

determinations for 10 CFR 50.59 from [enter dates].

(1) EV-CR-2019-000901-2, Replace Units 1 and 2 Diesel Generator Starting Air

Compressors

(2) EV-CR-2022-005805-8, Comp Action to Intermittently Isolate 1-HV-4393, Diesel

Generator, Service Water Outlet Flow Valve

(3) EV-IR-2021-003710-1, Shift Manager Clearance SMP21-0016 STA-707 Review

(4) EV-TR-2019-001133-5, FDA-2019-000036-01 / TM 5735389

(5) EV-TR-2019-009096-1, Maintenance Clearance TR-2019-009096 Spent Fuel

Pool X-02 Ventilation Exhaust Fan X-35 Motor

(6) EV-TR-2020-005137-11, Containment Building Polar Crane Use During Modes 3

Through 4

(7) EV-TR-2020-007888-3, Lubrication Recommendation Change to the Station Service

Water Pump Motor 1-02 Lower Bearing Grease

(8) EV-TR-2021-002308-9, Plugging up to 65 Tubes in the Unit 1 & Unit 2 CCW HXs

(CP1/2-CCAHHX-01/-02)

(9) EV-TR-2021-003204-1, Maintenance Clearance Greater Than 90 Days on

CPX-WTPMWP-01 Water Treatment Waste Sump X-01

(10) EV-IR-2021-003254-1, Comp Action Evaluation for Monitoring RCP 1-03 Vibration

(11) EV-TR-2019-000777-6, VDRT 5775695, Westinghouse Calculation CN-PCSA-14-5,

Revision 2

(12) EV-CR-2019-003377-8, Change Control Room A/C Units (CRAC) Compressor

Suction Pressure Pumpdown Setpoint to greater than or equal to 45 psig

(13) EV-TR-2020-003698-5, Shift Manager Clearance Placed to Isolate 2-HV-4166

Leaking By

(14) EV-TR-2021-000607-1, Maintenance Clearance CP20-1066 Unit 2 Train A UPS

Room Fan Coil Unit CP2-VAAUPR-01

(15) EV-TR-2019-06006-15, Application of WCAP-17627, Revision 1, to Unit 2 Reload

Analyses, beginning with Unit 2 Cycle 19 and Subsequent Unit 1 and Unit 2 Reload

Analyses (50.59 Safety Evaluation)

6

(16) EV-TR-2019-007450-4, Procedure Revision - Response to a Fire in the Control

Room or Cable Spreading Room

(17) EV-CR-2020-009014-1, Unit 1 Turbine Shaft Displacement Channel 1 Defective

Components

(18) EV-CR-2019-004542-5, Perform STA-707

(19) EV-CR-2020-005070-11, Compensatory Action: Manually Purging of Safety Chiller

(20) EV-CR-2021-002241-3, XEB4-2/1SS Motor Control Center Transfer Switch

Maintained in Off Position

(21) EV-CR-2020-002810-9, Unit 2 Train B Core Exit Thermocouple Alternate

Temperature Monitoring

(22) EV-TR-2020-002067-7, Manual Control Rod Drop Timing

(23) EV-TR-2019-008867-1, Degraded RCP Seal Standpipe Level Control Valve on

Reactor Coolant Pumps 2-01 and 2-03

(24) EV-CR-2018-004605-4, Component Cooling Water Pump Shaft Bearing Diameter

and Tolerance Changes

(25) 59SC-2017-000182-01, Increase Time Delay for Reactor Coolant Pump Vibration

Alarm

(26) 59SC-2019-000025-01, Replace Alternate Power Diesel Generators

(27) 59SC-2019-000051-01, Motor Operated Valve Limit Switch Setting Modifications

71111.18 - Plant Modifications

Severe Accident Management Guidelines (SAMG) Update (IP Section 03.03) (1 Sample)

(1) The inspectors verified the site Severe Accident Management Guidelines were

updated in accordance with the pressurized water reactor generic severe accident

technical guidelines and validated in accordance with NEI 14-01, Emergency

Response Procedures and Guidelines for Beyond Design Basis Events and Severe

Accidents, revision 1.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1) Unit 1, pressure transmitter 0508 feedwater heater outlet header pressure transmitter

following card replacement per work order 22-345906

(2) Unit 1, repairs to turbine shaft displacement probes between per work

order 22-448268

(3) Unit 1, pressurizer heater control 1-PK-455A per work order 22-381599

(4) Unit 2, pressurizer heater control 2-PK-455A per work order 22-394264

(5) Unit 1, motor driven auxiliary feedwater pump 1-01 recirculation line leak repair per

work order 22-457619

(6) Unit 1, main feedwater pump 1B following servo replacement per work

orders 22-456325 and 22-456467

7

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated a forced outage between September 6 and 12, 2022

caused by a unit trip. The unit trip resulted from a turbine trip caused by a spurious

shaft displacement indication.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (4 Samples)

(1) Unit 2, pressurizer heater per procedure IPO-001B on December 1, 2021

(2) Unit 1, pressurizer heaters per procedure IPO-001A on May 8, 2022

(3) Unit 2, condensate storage tank inspection on August 23, 2022

(4) Unit 1, scram breaker testing on September 12, 2022.

71114.01 - Exercise Evaluation

Inspection Review (IP Section 02.01-02.11) (1 Sample)

(1) The inspectors evaluated the biennial emergency plan exercise conducted on July 26

and 27, 2022. The exercise scenario simulated a greater than Operating Basis

Earthquake seismic event resulting in several simulated in-plant failures requiring the

rapid escalation to a Site Area Emergency declaration due the loss of all cooling

water flow to the secondary heat sink. Though the scenario did not include a

radiological release requiring issuance of protective action recommendations to the

offsite authorities, it did include opportunities for the licensee emergency response

organization to mitigate and repair additional simulated failures in electrical

switchgear and respond to a simulated medical emergency. The licensee's exercise

activities during the week also included a separate emergency scenario which

required the licensee demonstrate of one of the station's extensive damage mitigation

guideline strategies, per the requirements of 10 CFR 50.155(b)(2), in mitigating the

loss of the spent fuel pool water inventory.

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated the following submitted Emergency Action Level and

Emergency Plan changes.

  • ANS (Alert and Notification System) Design Report, revision 2, change

1 -effective March 11, 2021

  • On-Shift Staffing Analysis, revision 1 - effective June 24, 2021

This evaluation does not constitute NRC approval.

8

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)

(1) Unit 1 (July 1, 2021, through June 30, 2022)

(2) Unit 2 (July 1, 2021, through June 30, 2022)

MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)

(1) Unit 1 (July 1, 2021, through June 30, 2022)

(2) Unit 2 (July 1, 2021, through June 30, 2022)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (July 1, 2021, through June 30, 2022)

(2) Unit 2 (July 1, 2021, through June 30, 2022)

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (2 Samples)

(1) Unit 1 (July 1, 2021, through June 30, 2022)

(2) Unit 2 (July 1, 2021, through June 30, 2022)

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1) Unit 1 (July 1, 2021, through June 30, 2022)

(2) Unit 2 (July 1, 2021, through June 30, 2022)

EP01: Drill/Exercise Performance (DEP) Sample (IP Section 02.12) (1 Sample)

(1) April 1, 2021, through June 30, 2022

EP02: Emergency Response Organization (ERO) Drill Participation (IP Section 02.13)

(1 Sample)

(1) April 1, 2021, through June 30, 2022

EP03: Alert and Notification System (ANS) Reliability Sample (IP Section 02.14) (1 Sample)

(1) April 1, 2021, through June 30, 2022

9

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1) loss of internet in the main control room and the impact on Emergency Plan

communication equipment

71153 - Follow Up of Events and Notices of Enforcement Discretion

Event Followup (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated a Unit 1 trip and licensees response on September 5 and

6, 2022.

INSPECTION RESULTS

Failure to Restore Compliance for Non-Cited Violation 05000445/2019001-02 "Failure to

Evaluate a Change to the Facility DC Power System"

Cornerstone Severity Cross-Cutting Report

Aspect Section

Not Severity Level IV Not 71111.17T

Applicable NOV 05000445/2022003-01 Applicable

Open

The inspectors identified a Severity Level IV, notice of violation (NOV) of 10 CFR 50.59,

"Changes, tests, and experiments," for the failure to restore compliance of previously

identified non-cited violation (NCV)05000445/2019001-02. The previous violation identified

the licensee's failure to obtain a license amendment or perform a written evaluation

demonstrating the basis for not obtaining a license amendment prior to making a change to

the facility as described in the final safety analysis report. Specifically, the licensee revised

the Comanche Peak Final Safety Analysis Report (FSAR) to change the facility's

commitments to NRC Regulatory Guide (RG) 1.81, which demonstrated compliance with

General Design Criterion 5, without obtaining a license amendment.

Description: The inspectors reviewed corrective actions associated with

NCV 05000445/2019001-02. Through review of the associated condition

reports (CR) 2019-001711 and CR-2019-004542, the inspectors identified that the licensee

did not restore compliance with the requirements of 10 CFR 50.59, Change, tests, and

experiments. Specifically, the licensee failed to correct the NCV when they closed corrective

actions for the violation without obtaining a license amendment.

In January 2000, the licensee discovered electrical power panels that shared safety-related

alternating current and direct current electrical power between Units 1 and 2, contrary to what

was described in the Comanche Peak FSAR and NUREG-0797, Safety Evaluation Report

related to the Operation of Comanche Peak Steam Electric Station, Units 1 and 2, Docket

Nos. 50-445 and 50-446, Supplement 22. The licensee took corrective action to modify the

plant and revise the FSAR description of their original commitments to NRC RG 1.81,

Shared Emergency and Shutdown Electric Systems for Multi-Unit Nuclear Power Plants.

9

RG 1.81 was used by the licensee to comply with General Design criterion 5, Sharing of

structures, systems, and components.

In April 2002, the licensee issued 10 CFR 50.59 screening document 59SC-2000-000142-02-

02 which changed the description of RG 1.81 commitments in the FSAR. The licensee was

originally committed to positions C.1 and C.3 of RG 1.81, which describes that there was no

sharing of emergency power sources between units. The 10 CFR 50.59 screening document

changed the description of the licensees commitment to position C.2 of RG 1.81, which

allowed sharing of emergency power sources given specific conditions. Specifically,

position C.2 applied only to plants under construction permits issued before June 1, 1973,

and the position was NRC reviewed on an individual case basis. The change was

screened-out of the 10 CFR 10.59 process and no license amendment was submitted.

The inspectors determined that the licensee inappropriately applied position C.2 of RG 1.81

because the Comanche Peak construction permit was issued after June 1, 1973, and

Comanche Peak was originally evaluated against position C.3 of RG 1.81. The inspectors

determined these were changes to commitments that were used to meet General Design

Criteria 5. Additionally, the unit specific loads on the common unit panels could result in new

failure modes for previously evaluated accidents.

The inspectors reviewed 10 CFR 50.59 guidance as documented in NEI 96-07, revision 1,

Guidelines for 10 CFR 50.59 Implementation, as endorsed by NRC RG 1.187, revision 3,

"Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments." Based

on this determination, the inspectors determined that the 10 CFR 50.59 screening document

should have screened to a 10 CFR 50.59 evaluation. Further, the 10 CFR 50.59 safety

evaluation would have determined that the licensee was required to submit a license

amendment for the change because the change resulted in more than a minimal increase in

the likelihood of occurrence of a malfunction of a structure, system, or component important

to safety previously evaluated in the final safety analysis report. Additionally, the change

created a possibility for a malfunction of a structure, system, or component important to

safety with a different result than any previously evaluated in the final safety analysis report.

Corrective Actions: The licensee entered the issue into the corrective action program. There

are no operability concerns because the licensee corrected the technical aspects of the issue

in previous corrective actions.

Corrective Action References: CR 2019-001711, CR-2019-003684, CR-2019-004542,

CR-2019-006767, CR-2022-006915, CR-2022-006916

Performance Assessment: The inspectors determined this violation was associated with a

minor performance deficiency.

Enforcement: The reactor oversight processes significance determination process does not

specifically consider the regulatory process impact in its assessment of licensee

performance. Therefore, it is necessary to address this violation which impedes the NRCs

ability to regulate using traditional enforcement to adequately deter non-compliance.

Severity: The violation was determined to be Severity Level IV using Section 6.1.d.4 of the

NRC Enforcement Policy, dated January 14, 2022. Specifically, it was a violation of

10 CFR 50.59 because the change required prior Commission review and approval, and the

violation was determined to be associated with a minor performance deficiency.

11

Violation: Title 10 CFR 50.59(c)(2) requires, in part, that a licensee shall obtain a license

amendment pursuant to 10 CFR 50.90 prior to implementing a proposed change if the

change would: result in more than a minimal increase in the likelihood of occurrence of a

malfunction of a structure, system, or component (SSC) important-to-safety previously

evaluated in the final safety analysis report (as updated); or, create a possibility for a

malfunction of an SSC important to safety with a different result than any previously

evaluated in the final safety analysis report (as updated).

Contrary to the above, from February 13, 2019, to September 30, 2022, the licensee failed

obtain a license amendment pursuant to 10 CFR 50.90 prior to implementing a proposed

change if the change that would: result in more than a minimal increase in the likelihood of

occurrence of a malfunction of a SSC important-to-safety previously evaluated in the final

safety analysis report (as updated); or, create a possibility for a malfunction of an SSC

important to safety with a different result than any previously evaluated in the final safety

analysis report (as updated). Specifically, the licensee revised the Final Safety Analysis

Report associated with the Unit 1 DC power system to change the facility's commitments to

NRC Regulatory Guide (RG) 1.81, which demonstrated compliance with General Design

Criterion 5, without obtaining a license amendment.

Enforcement Action: This violation is being cited because the licensee failed to restore

compliance within a reasonable period after the violation was identified consistent with

section 2.3.2 of the Enforcement Policy.

Degraded Emergency Response Facility Communications Capabilities

Cornerstone Significance Cross-Cutting Report

Aspect Section

Emergency Green [P.3] - 71152A

Preparedness NCV 05000445,05000446/2022003-02 Resolution

Open/Closed

The inspectors identified a Green finding and associated non-cited violation of 10 CFR 50.47(b)(6) when the licensee failed to ensure prompt communications among principal

response organizations were available from the main control room. Specifically, on March 21,

2022, due to a loss of internet and degraded backup communication methods, there were no

communication methods available from within the main control room to contact offsite

response organizations.

Description: On March 21, 2022, Comanche Peak experienced a loss of internet at the site.

This loss created degradation of communications in multiple emergency response facilities,

especially the main control room. The main control room has multiple methods of

communication available to communicate to various onsite, offsite, stakeholders, and the

NRC as described in section 4.0 of the Emergency Plan. Since many of the methods rely on

internet (e.g., voice over internet protocol (VOIP)) technology, the dependent communication

methods that relied upon internet were rendered non-functional. Table 4.1 in the Emergency

Plan illustrates the communication interfaces from Comanche Peak's facilities to the other

onsite/offsite facilities and response organizations with the different communication methods

available. The inspectors discussed available communications methods with licensee staff

and were informed that no communications methods were available in the control room

without breaching the control room envelope.

12

The unplanned loss of internet on March 21, 2022, lasted approximately one hour. The

inspectors noted that from March 10 through April 18, 2022, there were a total of five

instances of the loss of all internets at the site ranging from one hour to seventeen hours;

however, aside from the March 21, 2022, instance, some form of emergency communications

was available from within the control room. Furthermore, the inspectors noted there were

multiple loss of internet occurrences in 2021. However, the loss of internet occurrence on

March 21, 2022, was the most significant due to the contributing factors affecting the other

methods of communication concurrent with that loss. Specifically, the following methods were

affected; all commercial telephones due to their reliance on VOIP, the emergency notification

number due to its reliance on VOIP, the black start satellite phone (which is antenna wired

capable for control room use) due to inadequate instructions, VESTA online notification

program (notifies state/local authorities) due to its reliance on internet, and the land line

telephone system (copper based redundant telephone lines) due to degraded connection and

static. The individuals in the control room were left with no methods to make phone calls from

the control room envelope; however, the black start satellite phone could receive calls.

On March 21, 2022, Comanche Peak did have handheld satellite phones available; however,

for those phones to function, the antenna needed to be deployed outside of the control room

envelope. Although there is a door to the turbine building roof from the main control room, the

door forms part of the control room envelope and routing through the door violates the control

room envelope. While cell phones can normally be used via Wi-Fi, the internet loss precluded

main control room use of cell phones on March 21, 2022. The inspectors assessed this

situation to see if a viable compensatory method of communications among principal

response organizations was provided for in the event of a radiological emergency. To ensure

assumptions about the maximum radiological dose to control room emergency workers were

provided for their protection, the ventilation envelope could not be breached to set up the

antenna. Therefore, there was no viable compensatory measure in place. .

Comanche Peak updated the dedicated copper lines federal telephone system to VOIP

emergency notification system using RIS 2000-11 in the spring 2021 due to reliability

concerns of the copper circuitry. The inspectors noted that the licensee's modification to

VOIP protocols failed to account for the introduction of single point vulnerabilities.

Specifically, the connection to the sites internal network by the internet service provider

included only one line. Internet outages created by damage or degradation of a single line

occur on occasion; therefore, they are reasonably within the licensee's ability to foresee. In

addition, numerous losses occurred in 2021 providing the licensee with sufficient information

to recognize the vulnerability and take interim actions to ensure communications capability

until redundancy in the internet connection could be implemented. The inspectors note that

there was overall improvement in line clarity with the upgrade to emergency notification

system, but the station remained vulnerable to communications degradation due to the known

single point vulnerability.

The inspectors previously reviewed emergency preparedness communication issues in 2021.

No more than minor performance deficiencies were identified during that review. This

inspection was documented in the 71152 Inspection in the 2021004 (ADAMS Accession No.

ML22019A304 https://www.nrc.gov/docs/ML2201/ML22019A304.pdf).

Corrective Actions: For completed corrective actions, Comanche Peak has updated the black

start satellite telephone dialing protocol procedure and added a second internet line with a

diverse method (microwave vs. local area network). Planned corrective action included

adding a third internet line with a diverse switch which eliminates an existing single point

14

vulnerability in the currently installed internet lines. Additional actions are I documented in

CR-2022-1892.

Corrective Action References: Comanche Peak entered the loss of internet events into the

corrective action program under CR-2021-7895, tracking report (TR) 2022-1822,

TR-2022-1892, TR-2022-1886, CR-2021-3239, TR-2021-7938, CR-2021-6637,

TR-2021-5058, CR-2021-5014, TR 2021-1209, TR-2022-1688, TR-2021-5017,

CR-2022-1894, TR-2022-1823, TR-2022-1848, CR-2021-2796, TR-2021-7588.

Performance Assessment:

Performance Deficiency: The failure to ensure reliable emergency communication methods

were available from the control room was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Facilities and Equipment attribute of the Emergency

Preparedness cornerstone and adversely affected the cornerstone objective to ensure that

the licensee can implement adequate measures to protect the health and safety of the public

in the event of a radiological emergency. Specifically, on March 21, 2022, the unplanned loss

of internet impacted emergency communication methods to offsite response organizations,

which effects public health and safety in the event of a radiological emergency.

Significance: The inspectors assessed the significance of the finding using Manual

Chapter 0609, Significance Determination Process, attachment 4 (effective date December

13, 2019), and the corresponding Appendix B, Emergency Preparedness Significance

Determination Process, table 5.6-1. The performance deficiency was determined have very

low safety significance (Green) because it was a failure to comply with NRC requirements,

was a degraded planning standard function, and the deficiency lasted less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> from

the time of discovery and there were no compensatory measures implemented.

Cross-Cutting Aspect: P.3 - Resolution: The organization takes effective corrective actions to

address issues in a timely manner commensurate with their safety significance. Comanche

Peak modified the site's telecommunication infrastructure with the intent to improve the

reliability of control room communication by transitioning from degraded copper circuitry to

VOIP technology. However, the site experienced multiple outages the year following the

modification but failed to implement timely corrective actions prior to more significant

communications equipment outages.

Enforcement:

Violation: Title 10 CFR 50.54(q)(2), requires, in part, that a power reactor licensee follow and

maintain the effectiveness of an emergency plan which meets the requirements of

appendix E to 10 CFR Part 50 and the standards of 10 CFR 50.47(b). Title 10 CFR 50.47(b)(6) requires, in part, that provisions exist for prompt communications among principal

response organizations to emergency personnel and to the public.

Contrary to the above, on March 21, 2022, the licensee failed follow and maintain the

effectiveness of an emergency plan which meets the requirements of appendix E to

10 CFR Part 50 and the standards of 10 CFR 50.47(b). Specifically, the license failed to meet

the planning standard in 10 CFR 50.47(b)(6) due to a loss of internet event and degraded

backups resulting in no communication methods available from within the main control room

to offsite response organizations.

14

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 28, 2022, the inspectors presented the triennial heat exchanger and heat sink

performance inspection results to Mr. T. McCool, Site Vice President, and other

members of the licensee staff.

On August 25, 2022, the inspectors presented the emergency plan exercise inspection

results to Mr. T. McCool, Site Vice President, and other members of the licensee staff.

On September 22, 2022, the inspectors presented the evaluations of changes, tests, and

experiments inspection results to Mr. T. McCool, Site Vice President, and other

members of the licensee staff.

On October 6, 2022, the inspectors presented the integrated inspection results to

Mr. A. Marzloff, Plant Manager, and other members of the licensee staff.

15

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.04 Procedures SOP-204B Containment Spray System 6

71111.04 Procedures SOP-809A Diesel Generator Ventilation System 13

71111.04 Procedures SOP-904 Fire Protection Main Water Supply and Fire Pumps System 17

71111.04 Procedures SOP-908B Diesel Generator System 18

71111.05 Fire Plans FPI-104A Unit 1 Train A Diesel Generator and Equipment Elevation 4

810 and Fuel Oil Day Tank Room Elevation 844

71111.05 Fire Plans FPI-105A Unit 1 Train B Diesel Generator and Equipment Elevation 4

810 and Fuel Oil Day Tank Room Elevation 844

71111.05 Fire Plans FPI-401 Auxiliary Building Elevation 790'-6" 3

71111.05 Fire Plans FPI-403 Auxiliary Building Elevation 810'-6" 5

71111.05 Miscellaneous Drill No 22-12-03 Fire Drill Scenario: Train A Centrifugal Charging Pump 09/02/2022

71111.06 Calculations 2-NU-0059 Unit 2 Safeguards Building Flooding Analysis 3

71111.06 Corrective Action TR-YYYY-NNNN TR-2022-000683

Documents

71111.06 Corrective Action CR-YYYY-NNNN 2015-000079

Documents

71111.07T Calculations 1-EB-302-04 Auxiliary Feedwater Pump Rooms - Unit 1 6

71111.07T Calculations 1-EB-302-05 RHR Pump Rooms Unit 1 5

71111.07T Calculations 1-EB-303-01 Centrifugal Charging Pump Rooms -Unit 1 7

71111.07T Calculations 1-EB-311-01 ESF Local Cooler Areas Summary Spare Heat Gains and 9

Maximum Temperatures (LOCA with LOOP)

71111.07T Calculations 1-EB-311-08 Safety Chilled Water Pump Evaluation 5

71111.07T Calculations 1-EB-311-12 Evaluation of Safety Chiller Capacities at Reduced CCW 0

Flow Rates - Unit 1

71111.07T Calculations 1-EB-311-3 ESF Local Cooler Areas Summary - Space Heat Gains and 4

Maximum Temperatures (LOCA w/OPA) - Unit 1

71111.07T Calculations 16345-ME(B)-088 Station Service Water System Steady State Hydraulic 8

Calculations

71111.07T Calculations 16345-ME(B)-183 SSI Heat Loads 5

71111.07T Calculations X-SC-04-04 SSW Travelling Screen 02 Differential Pressure X-L-4289A 8

16

71111.07T Corrective Action CR-YYYY-NNNN 2019-007485, 2020-004666, 2020-004864, 2020-006675,

Documents 2020-009296, 2021-002257, 2021-002716, 2021-005490,

2022-002640, 2022-003351, 2022-004955

71111.07T Corrective Action TR-YYYY-NNNN 2021-005163

Documents

71111.07T Corrective Action Issue Report (IR) 2022-005606, 2022-005664

Documents

Resulting from

Inspection

71111.07T Drawings M1-0229 Flow Diagram Component Cooling Water System CP-22

71111.07T Drawings M1-0311 Flow Diagram Ventilation Safety Chilled Water System CP-30

71111.07T Miscellaneous Open Cooling Water Plant Specific Guidelines 4

71111.07T Miscellaneous CCP 1-02 Lube Unit 1 Service Water Visual Inspection Form 03/03/2021

Oil Cooler

71111.07T Miscellaneous CCP 1-02 Lube Unit 1 Service Water Visual Inspection Form 03/26/2019

Oil Cooler

71111.07T Miscellaneous CP-0001-024 Centrifugal Charging Pumps and Motors 73

71111.07T Miscellaneous CP-0081-001 Air Handling Units 3

71111.07T Miscellaneous CPNPP System Safety Chilled Water 2nd Quarter,

Status 2022

71111.07T Miscellaneous DBD-CS-096 Safe Shutdown Impoundment/Dam 14

71111.07T Miscellaneous DBD-ME-229 Comanche Peak Nuclear Power Plant Units 1 and 2, Design 50

Basis Document, Component Cooling Water System

71111.07T Miscellaneous DBD-ME-233 Comanche Peak Nuclear Power Plant Units 1 and 2 Design 39

Basis Document, Station Service Water System

71111.07T Miscellaneous DBD-ME-311 Comanche Peak Nuclear Power Plant Units 1 and 2, Design 21

Basis Document, Safety Chilled Water System

71111.07T Miscellaneous NALCO Water Quarterly Closed Loop Analysis - 2022 Q1 06/15/2022

Letter

71111.07T Procedures ABN-501 Station Service Water Malfunction 10

71111.07T Procedures ABN-907 Acts of Nature 17

71111.07T Procedures COP-501 Chemistry Operating Procedures, Station Service Water 12

71111.07T Procedures COP-502A Unit 1 Chemistry Operating Procedures Manual, Component 7

Cooling Water

71111.07T Procedures COP-814 Unit 1 Chemistry Operating Procedure Manual, Ventilation 5

17

Chilled Water

71111.07T Procedures COP-815A Unit 1 Chemistry Operating Procedures Manual, Safety 5

Chilled Water

71111.07T Procedures MSE-G0-4003 Motor Insulation Resistance Testing 5

71111.07T Procedures OPT-201A Charging System 15

71111.07T Procedures OPT-207A Service Water System 20

71111.07T Procedures OPT-209A Surveillance Test, Safety Chilled Water System 16

71111.07T Procedures OPT-209B Surveillance Test, Safety Chilled Water System 12

71111.07T Procedures PPT-SX-7517 Safe Shutdown Impoundment Inspection 2

71111.07T Procedures STA-734 Service Water System Fouling Monitoring Program 5

71111.07T Procedures TDM-901A Systems Data, Throttled Valves/Flow Rates 14

71111.07T Procedures TSP-509 Predictive Maintenance Thermographic Analysis Program 6

71111.07T Work Orders Work Orders 3667839, 3868301, 3953450, 3975749, 4260995, 4434930,

(WO) 4765986, 4813602, 4941796, 5135252, 5282413, 5326811,

5370719, 5436260, 5532319, 5535113, 5671623, 5685144,

5695618, 5779054, 5794744, 5813178, 5814385, 5823278,

5924058, 5926668, 5927760, 5928617, 5951210, 5955001,

5958222, 5968810, 5972626, 5974285, 5980342, 6006826,

6020235, 6024697, 21-776632, 21-940915, 21-941868, 22-

103231, 22-14288, 22-183905, 22-70886, 22-79326

71111.12 Corrective Action CR-YYYY-NNNN 2019-7903, 2022-1492

Documents

71111.12 Miscellaneous System Health Report AC Distribution 6.9KV Switchgear 4th quarter

2021

71111.12 Miscellaneous Maintenance Rule Program Reports

Database for Unit

2 Main Turbine

71111.12 Miscellaneous System Health

Report for Unit 2

Main Turbine

71111.13 Corrective Action TR-YYYY-NNNN 2022-004908

Documents

71111.13 Miscellaneous SORC 22-010 Unit 1 Forced Outage Start up Meeting Package 09/11/2022

71111.17T Calculations ME-CA-0229- CCW Parameters for Fouling Monitoring 1

18

5129

71111.17T Corrective Action CR-YYYY-NNNN 2019-001271, 2019-001317, 2019-001428, 2019-001430,

Documents 2019-001711, 2019-004542, 2019-003684, 2019-006767,

2022-005805

71111.17T Corrective Action TR-YYYY-NNNN 2019-001133, 2019-009096, 2020-005137, 2020-007888,

Documents 2021-002308, 2021-003710, 2022-000031, 2022-004593

71111.17T Corrective Action Issue Report (IR-) 2022-006839, 2022-006874, 2022-006886, 2022-006890,

Documents 2022-006915, 2022-006916

Resulting from

Inspection

71111.17T Drawings 554 Starting Air Receivers Delaval Part No. 76001-125 7

71111.17T Drawings M1-0215 Flow Diagram Starting Air Piping CP1-MEDGEE-01 CP-27

71111.17T Engineering FDA-2017- Replace the Unit 1 and Unit 2 Emergency Diesel Generator 12

Changes 000092-01 Starting Air Compressors

71111.17T Miscellaneous DBD-ME-006 Control of Heavy Loads at Nuclear Plants 40

71111.17T Miscellaneous DBD-ME-011 Diesel Generator Sets 41

71111.17T Miscellaneous DBD-ME-303-01 Fuel Building Ventilation System 11

71111.17T Procedures CPNPP 50.59 Resource Manual 6

71111.17T Procedures ABN-712 Rod Control System Malfunction 14

71111.17T Procedures INC-3027 Control Rod Drop Timing 0

71111.17T Procedures IPO-010B Reactor Coolant System Reduced Inventory Operations 18

71111.17T Procedures MDA-304 Control of Heavy Loads and Critical Lifts 7

71111.17T Procedures MSG-2013 Polar Crane/Telescoping Jib Crane Operating Instructions 4

and Restrictions

71111.17T Procedures NUC-114 Core Performance Engineering Periodic Duties 20

71111.17T Procedures NUC-206 Control Rod Drop Timing 22

71111.17T Procedures SOP-608A 120, 208, 208/120, and 120/240 VAC Distribution System 14

71111.17T Procedures SOP-608B 120, 208, 208/210, and 120/240 VAC Distribution System 5

71111.17T Procedures STA-707 10CFR50.59 and 10CFR72.48 Reviews 23

71111.17T Procedures STI-707.01 10CFR50.59 Screens 0

71111.17T Procedures STI-707.04 10CFR50.59 and 10CFR72.48 Reviews Applicability 1

Determinations

71111.18 Corrective Action TR-YYYY-NNNN 2018-3643, 2022-1952, 2022-1407

Documents

20

71111.18 Procedures SAG-1.0 Control Room Severe Accident Initial Response 0

71111.18 Procedures SAG-9.0 Technical Severe Accident Response Mitigate Fission 0

Product Release

71111.18 Procedures STI-203.02 Preparation of Sever Accident Management Guidance 0

71111.18 Procedures STI-203.02 Preparation of Severe Accident Management Guidance 0

71111.19 Corrective Action TR-YYYY-NNNN 2022-4908

Documents

71111.22 Procedures IPO-002A Plant Startup from Hot Standby 23

71114.01 Corrective Action CR-YYYY-NNNN CR-2017-009505, CR-2019-008751, CR-2019-008766,

Documents TR-YYYY-NNNN CR-2019-008787, CR-2019-008798, CR-2019-008800,

CR-2020-001364, CR-2020-001368, CR-2020-002313,

CR-2020-004960, CR-2020-006058, CR-2020-006768,

CR-2020-007289, CR-2021-008503, CR-2021-008514,

CR-2022-000174, CR-2022-001649, CR-2022-004837,

CR-2022-005181, CR-2022-005234, CR-2022-006005,

CR-2022-006006, CR-2022-006007, CR-2022-006008,

CR-2022-006052, CR-2022-006061, CR-2022-006063,

CR-2022-006064, TR-2017-009355, TR-2017-009418,

TR-2017-009419, TR-2017-009430, TR-2017-009436,

TR-2017-009487, TR-2017-009491, TR-2017-009492,

TR-2017-009506, TR-2017-009508, TR-2017-009509,

TR-2017-009511, TR-2019-008671, TR-2019-008770,

TR-2019-008799, TR-2021-008177, TR-2022-005307,

TR-2022-0060062

71114.01 Corrective Action Issue Reports IR-2022-006242

Documents

Resulting from

Inspection

71114.01 Miscellaneous Management Challenge Presentation: 07/27/2022 Green 08/15/2022

Team Exercise Summary

71114.01 Miscellaneous Control Room Simulator Exercise Participant Logs 07/27/2022

71114.01 Miscellaneous Exercise Report, Red Team November 06, 2019 07/12/2022

71114.01 Miscellaneous Exercise Report, Gold Team, August 16,2017 10/15/2017

71114.01 Miscellaneous Green Team, Exercise Report, June 24, 2020 07/12/2022

71114.01 Miscellaneous Technical Support Center Exercise Participant Logs 07/27/2022

21

71114.01 Miscellaneous Technical Support Center Focused Drill Participant Logs 07/26/2022

71114.01 Miscellaneous Operations Support Center Exercise Participant Logs 07/27/2022

71114.01 Miscellaneous Operations Support Center Focused Drill Participant Logs 07/26/2022

71114.01 Miscellaneous Emergency Operations Facility Exercise Participant Logs 07/27/2022

71114.01 Miscellaneous Joint Information Center Exercise Participant Logs 07/27/2022

71114.01 Miscellaneous CPNPP Emergency Plan 45

71114.01 Miscellaneous Management Challenge Presentation: 7/26/2022 Green 08/15/2022

Team Exercise Summary (Focused Area Drill TSC and OSC

Only)

71114.01 Procedures ABN-907 Acts of Nature 17

71114.01 Procedures ABN-909 Spent Fuel Pool/Refueling Cavity Malfunction 9

71114.01 Procedures BSI-3.0 Spent Fuel Cooling Safety Function Restoration 0

71114.01 Procedures EPP-116 Emergency Repair & Damage Control and Immediate Entries 9

71114.01 Procedures EPP-201 Assessment of Emergency Action Levels Emergency 13

Classification and Plan Activation

71114.01 Procedures EPP-201 Emergency Action Level Technical Bases Document 1

Technical Bases

71114.01 Procedures EPP-203 Notifications 16

71114.01 Procedures EPP-205 Activation and Operation of the Operations Support 12

Center (OSC)

71114.01 Procedures EPP-206 Activation and Operation of the Emergency Operations 18

Facility (EOF)

71114.01 Procedures EPP-303 Operation of Computer Based, Emergency Dose 13

Assessment System

71114.01 Procedures EPP-304 Protective Action Recommendations 22

71114.01 Procedures EPP-309 Onsite/In-Plant Radiological Surveys and Offsite Radiological 15

Monitoring

71114.01 Procedures FRH-0.1A Response to Loss of Secondary Heat Sink 9

71114.01 Procedures SAG-1.0 Control Room Severe Accident Initial Response 0

71114.01 Procedures SAG-10.0 TSC Severe Accident response Control SFP Level 0

71114.01 Procedures SOP-506 Spent Fuel Pool Cooling and Cleanup System 22

71114.04 Miscellaneous CPNPP 10 CFR 50.54(q)(3) Screening Evaluation Form for 03/11/2021

ANS Design Report Change

22

71114.04 Miscellaneous CPNPP 10 CFR 50.54(q)(3) Screening and Effectiveness 06/23/2021

Evaluation Forms for OSSA Change

71114.04 Procedures CPNPP 10 CFR 50.54(q)(3) Screening and Effectiveness 05/24/2021

Evaluation Form for Emergency Plan Revision 45

71114.04 Procedures CPNPP Emergency Plan 45

71114.04 Procedures CPNPP Emergency Plan 44

71114.04 Procedures EPP-123 10 CFR 50.54(q) Screening and Evaluation of Changes to 3

Emergency Plan Documentation

71151 Miscellaneous NucIQ data on reactor coolant system for Units 1 and 2 for

June, 2022

71151 Miscellaneous Control room log leak rate readings July 1, 2021, through

June 30, 2022.

71151 Miscellaneous MSPI Margin Reports

PRA Living Model Report

71151 Miscellaneous ANS Test Report Data 2021Q2-2022Q2

71151 Miscellaneous Quarterly Key ERO Member Drill Participation

Trackers 2021Q2-2022Q2

71151 Miscellaneous DEP PI Data 2021Q2-2022Q2

71151 Procedures SG-012 Alert and Notification System Surveillance 31

71151 Procedures SG-020 NRC Performance Indicators 23

71151 Procedures STA-662 Administrative Control of the Siren System 1

71152A Procedures STI-433.02 Emergency Response Facility Functionality Evaluation 2

24