Letter Sequence Approval |
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EPID:L-2022-LRO-0065, (CPNPP) Unit 2 Refueling Outage 19 (2RF19) Steam Generator 180 Day Report (Approved, Closed) |
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Category:Inspection Report
MONTHYEARIR 05000445/20230042024-01-29029 January 2024 Integrated Inspection Report 05000445/2023004 and 05000446/2023004 ML24018A1072024-01-18018 January 2024 Notification of Commercial Grade Dedication Inspection (05000445/2024012 and 05000446/2024012) and Request for Information IR 05000445/20234022023-11-30030 November 2023 NRC Security Inspection Report 05000445/2023402 and 05000446/2023402 IR 05000445/20230052023-08-23023 August 2023 Updated Inspection Plan for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2023005 and 05000446/2023005)- Mid Cycle Letter 2023 IR 05000445/20233012023-08-21021 August 2023 NRC Examination Report 05000445/2023301 and 05000446/2023301 IR 05000445/20230112023-07-20020 July 2023 Fire Protection Team Inspection Report 05000445/2023011 and 05000446/2023011 IR 05000445/20230022023-07-14014 July 2023 Integrated Inspection Report 05000445/2023002 and 05000446/2023002 IR 05000445/20230012023-04-13013 April 2023 Integrated Inspection Report 05000445/2023001 and 05000446/2023001 IR 05000445/20234012023-03-29029 March 2023 NRC Security Inspection Report 050004452023401 and 050004462023401 (Cover Letter Only) IR 05000445/20230102023-03-24024 March 2023 Biennial Problem Identification and Resolution Inspection Report 05000445/2023010 and 05000446/2023010 IR 05000445/20220062023-03-0101 March 2023 Annual Assessment Letter for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2022006 and 05000446/2022006) IR 05000445/20220042023-01-26026 January 2023 Integrated Inspection Report 05000445/2022004 and 05000446/2022004 IR 05000445/20220102023-01-23023 January 2023 TI-194 Report 05000445/2022010 and 05000446/2022010 IR 05000445/20224012022-12-19019 December 2022 Cyber Security Inspection Report 05000445/2022401 and 05000446/2022401 (Cover Letter Only) IR 05000445/20224202022-12-0707 December 2022 Security Baseline Inspection Report Cover Letter 05000445/2022420 and 05000446/2022420 ML22319A0732022-11-15015 November 2022 Review of the Fall 2021 Steam Generator Tube Inspection Report IR 05000445/20220032022-11-0101 November 2022 Integrated Inspection Report 05000445/2022003 and 05000446/2022003 and Notice of Violation ML22299A0562022-11-0101 November 2022 Integrated Inspection Report 05000445/2022003 and 05000446/2022003 and Notice of Violation IR 05000445/20220052022-08-22022 August 2022 Updated Inspection Plan for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2022005 and 05000446/2022005) IR 05000445/20224032022-08-0909 August 2022 NRC Security Inspection Report 05000445/2022403 and 05000446/2022403 (Full Report) IR 05000445/20220022022-08-0505 August 2022 2nd Quarter 2022 Integrated Inspection Report 05000445/2022002 and 05000446/2022002 ML22174A2792022-06-22022 June 2022 Notification of NRC Evaluations of Changes, Tests and Experiments Inspection (05000445/2022003 and 05000446/2022003) and Request for Information IR 05000445/20220012022-04-26026 April 2022 Integrated Inspection Report 05000445/2022001 and 05000446/2022001 IR 05000445/20224022022-04-25025 April 2022 Security Baseline Inspection Report 05000445/2022402 and 05000446/2022402 IR 05000445/20210062022-03-0202 March 2022 Annual Assessment Letter for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2021006 and 05000446/2021006) IR 05000445/20200112022-02-0707 February 2022 Amended - Comanche Peak Nuclear Power Plant - Triennial Fire Protection Inspection Report 05000445/2020011 and 05000446/2020011 and Notice of Violation IR 05000445/20210042022-01-25025 January 2022 Integrated Inspection Report 05000445/2021004 and 05000446/2021004 IR 05000445/20210122022-01-13013 January 2022 TI-194 Report 05000445/2021012 and 05000446/2021012 IR 05000445/20214052021-12-15015 December 2021 Security Baseline Inspection Report 05000445/2021405 and 05000446/2021405 IR 05000445/20214032021-12-0909 December 2021 Powerplant, Units 1 and 2 - Security Baseline Inspection Report 05000445/2021403 and 05000446/2021403 IR 05000445/20210032021-11-0303 November 2021 Integrated Inspection Report 05000445/2021003 and 05000446/2021003 IR 05000445/20213012021-10-19019 October 2021 NRC Examination Report 05000445/2021301 and 05000446/2021301 IR 05000445/20210102021-10-0707 October 2021 Biennial Problem Identification and Resolution Inspection Report 05000445/2021010 and 05000446/2021010 IR 05000445/20214012021-09-0909 September 2021 Security Baseline Inspection Report 05000445/2021401 and 05000446/2021401 IR 05000445/20210052021-09-0101 September 2021 Mid-Cycle Inspection Plan Transmittal Letter for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2021005 and 05000446/2021005) IR 05000445/20214022021-08-19019 August 2021 Security Baseline Inspection Report 05000445/2021402 and 05000446/2021402 IR 05000445/20210022021-08-10010 August 2021 Integrated Inspection Report 05000445/2021002 and 05000446/2021002 IR 05000445/20210012021-06-23023 June 2021 Revised Report - Comanche Peak Nuclear Plant, Units 1 and 2 - Integrated Inspection Report 05000445/2021001; 05000446/2021001 and Independent Spent Fuel Storage Inspection 07200074/2021001 IR 05000445/20214042021-06-17017 June 2021 Material Control and Accounting Program (Public) Inspection Report 05000445/2021404 05000446/2021404 ML21131A0952021-05-11011 May 2021 CP2021001-RP-JE, Comanche Peak Nuclear Power Plant, Units 1 and 2 - Integrated Inspection Report 05000445/2021001 and 05000446/2021001 IR 05000445/20210112021-05-0606 May 2021 Design Basis Assurance Inspection (Teams) Inspection Report 05000445/2021011 and 05000446/2021011 and Notice of Violation IR 07200074/20214012021-03-17017 March 2021 (CPNPP) Independent Spent Fuel Storage Installation (ISFSI) IR 07200074/2021401 3-3 IR 05000445/20200062021-03-0303 March 2021 Annual Assessment Letter for Comanche Peak, Units 1 and 2, (Inspection Report 05000445/2020006 and 05000446/2020006) IR 05000445/20200042021-02-0909 February 2021 Integrated Inspection Report 05000445/2020004 and 05000446/2020004 IR 05000445/20200012020-12-22022 December 2020 Revised Report - Comanche Peak Nuclear Power Plant, Units 1 and 2 -Integrated Inspection Report 05000445/2020001 and 05000446/2020001 IR 05000445/20200032020-11-10010 November 2020 Integrated Inspection Report 05000445/2020003 and 05000446/2020003 IR 05000445/20200102020-10-0606 October 2020 Design Basis Assurance Inspection (Programs) Inspection Report 05000445/2020010 and 05000446/2020010 ML20265A0422020-09-21021 September 2020 Commanche Peak Nuclear Power Plant - Triennial Fire Protection Inspection Report 05000445/2020011 and 05000446/2020011 and Notice of Violation IR 05000445/20204102020-09-10010 September 2020 Security Baseline Inspection Report 05000445/2020410 and 05000446/2020410 IR 05000445/20200052020-09-0101 September 2020 Updated Inspection Plan for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2020005 and 05000446/2020005) 2024-01-29
[Table view] Category:Letter
MONTHYEARCP-202400030, License Renewal Application Revision 0 - Supplement 3, Revision 12024-01-31031 January 2024 License Renewal Application Revision 0 - Supplement 3, Revision 1 IR 05000445/20230042024-01-29029 January 2024 Integrated Inspection Report 05000445/2023004 and 05000446/2023004 CP-202400034, (CPNPP) - Core Operating Limits Report (Colr), Unit 2 Cycle 21, (ERX-23-001, Revision 1)2024-01-29029 January 2024 (CPNPP) - Core Operating Limits Report (Colr), Unit 2 Cycle 21, (ERX-23-001, Revision 1) ML24024A2102024-01-29029 January 2024 Summary of Regulatory Audit Regarding a License Amendment Request to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components for Nuclear Power Reactors ML24025A0052024-01-25025 January 2024 Review of the Spring 2023 Steam Generator Tube Inspection Report ML24023A0242024-01-24024 January 2024 Correction to Amendment Nos. 185 and 185 Regarding Implementation of Full Spectrum Loss-of-Coolant Accident Methodology ML24018A1072024-01-18018 January 2024 Notification of Commercial Grade Dedication Inspection (05000445/2024012 and 05000446/2024012) and Request for Information ML23159A2082023-12-20020 December 2023 Request for Withholding Information from Public Disclosure ML23319A3872023-12-20020 December 2023 Issuance of Amendment Nos. 185 and 185 Regarding Implementation of Full Spectrum Loss-of-Coolant Accident (Fsloca) Methodology ML23348A2392023-12-19019 December 2023 Nonacceptance of License Amendment Request to Relocate Technical Specification 3.9.3, Nuclear Instrumentation, to the Technical Requirements Manual CP-202300575, (Cpnpp), License Amendment Request to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors Supplement 22023-12-13013 December 2023 (Cpnpp), License Amendment Request to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors Supplement 2 ML23333A0872023-12-13013 December 2023 Transmittal of Dam Safety Inspection Report - Public CP-202300566, (Cpnpp), Special Report 1-SR-23-001-00, Inoperable Post Accident Monitoring Instrumentation2023-12-12012 December 2023 (Cpnpp), Special Report 1-SR-23-001-00, Inoperable Post Accident Monitoring Instrumentation CP-202300494, License Renewal Application Revision 0, Supplement 32023-12-0606 December 2023 License Renewal Application Revision 0, Supplement 3 ML23313A0732023-12-0606 December 2023 Issuance of Amendment Nos. 184 and 184 Regarding Revision to Technical Specifications to Implement WCAP-17661-P-A, Rev. 1, Improved Roac and CAOC Fq Surveillance Technical Specifications ML23291A4382023-11-30030 November 2023 Notice of Availability of the Draft Plant-Specific Supplement 60, to the Generic Environmental Impact Statement for License Renewal of Nuclear Plants Regarding Comanche Peak Nuclear Power Plant, Unit Numbers 1 and 2, License Renewal Applica ML23325A0182023-11-30030 November 2023 Schedule Revision for the License Renewal Application Review IR 05000445/20234022023-11-30030 November 2023 NRC Security Inspection Report 05000445/2023402 and 05000446/2023402 CP-202300349, License Amendment Request (Lar) 23-004 Technical Specifications (TS) 3.9.3, Nuclear Instrumentation2023-11-20020 November 2023 License Amendment Request (Lar) 23-004 Technical Specifications (TS) 3.9.3, Nuclear Instrumentation ML23308A0032023-11-17017 November 2023 Letter to R. Nelson, Executive Director; Achp; Re., Comanche Peak Draft Environmental Impact Statement ML23308A0022023-11-17017 November 2023 Letter to M. Wolfe, Executive Director; Shpo; Re., Comanche Peak Draft Environmental Impact Statement ML23317A3002023-11-13013 November 2023 Letter to R. Sylestine, Chairman, Alabama-Coushatta Tribe of Texas Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2972023-11-13013 November 2023 Letter to R. Martin, President, Tonkawa Tribe of Oklahoma Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2872023-11-13013 November 2023 Letter to J. Garza, Chairman, Kickapoo Traditional Tribe of Texas Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2832023-11-13013 November 2023 Letter to D. Dotson, President, Delaware Nation Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2852023-11-13013 November 2023 Letter to E. Martinez, President, Mescalero Apache Tribe Regarding Comanche Peak Draft Environmental Impact Statement ML23306A0302023-11-13013 November 2023 Letter to J. Cernek, Chairman; Coushatta Tribe of Louisiana Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2902023-11-13013 November 2023 Letter to M. Pierite, Chairman, Tunica Biloxi Tribe of Louisiana Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2982023-11-13013 November 2023 Letter to R. Morrow, Town King, Thlopthlocco Tribal Town Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2842023-11-13013 November 2023 Letter to D. Kaskaske, Chairman, Kickapoo Tribe of Oklahoma Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2822023-11-13013 November 2023 Letter to D. Cooper, Chairman, Apache Tribe of Oklahoma Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2962023-11-13013 November 2023 Letter to M. Woommavovah, Chairman, Comanche Nation Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2812023-11-13013 November 2023 Letter to C. Hoskin, Principal Chief, Cherokee Nation; Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2862023-11-13013 November 2023 Letter to J. Bunch, Chief, United Keetoowah Band of Cherokee Indians Regarding Comanche Peak Draft Environmental Impact Statement ML23317A3032023-11-13013 November 2023 Letter to W. Yargee, Chief, Alabama-Quassarte Tribal Town Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2882023-11-13013 November 2023 Letter to L. Johnson, Chief, Seminole Nation of Oklahoma Regarding Comanche Peak Draft Environmental Impact Statement ML23317A3012023-11-13013 November 2023 Letter to S. Yahola, Mekko, Kialegee Tribal Town Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2792023-11-13013 November 2023 Letter to B. Gonzalez, Chairman, Caddo Nation Regarding Comanche Peak Draft Environmental Impact Statement ML23317A3022023-11-13013 November 2023 Letter to T. Parton, President, Wichita and Affiliated Tribes Regarding Comanche Peak Draft Environmental Impact Statement ML23317A2892023-11-13013 November 2023 Letter to L. Spottedbird, Chairman, Kiowa Indian Tribe Regarding Comanche Peak Draft Environmental Impact Statement ML23311A2082023-11-0909 November 2023 Reassignment of U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch IV ML23360A6312023-10-26026 October 2023 FEMA, Submittal of Radiological Emergency Preparedness Final Report for the Comanche Peak Nuclear Power Plant Medical Services Drill Evaluated on August 23, 2023 CP-202300416, Supplemental Information to Facilitate Acceptance of Licensee Amendment Request 23-002, Application Regarding GDC-5 Shared System Requirements2023-10-12012 October 2023 Supplemental Information to Facilitate Acceptance of Licensee Amendment Request 23-002, Application Regarding GDC-5 Shared System Requirements CP-202300432, Response to Request for Additional Information Regarding the Safety Review of the License Renewal Application - Set 42023-10-0404 October 2023 Response to Request for Additional Information Regarding the Safety Review of the License Renewal Application - Set 4 ML23237B4222023-09-28028 September 2023 Energy Harbor Nuclear Corp. - Vistra Operations Company LLC - Letter Regarding Order Approving Transfer of Licenses and Draft Conforming License Amendments ML23263A0242023-09-21021 September 2023 Revision of Schedule for the Environmental Review of the Comanche Peak Nuclear Power Plant Units 1 and 2 License Renewal Application 2024-01-31
[Table view] |
Text
November 15, 2022 Mr. Ken J. Peters Senior Vice President and Chief Nuclear Officer Attention: Regulatory Affairs Vistra Operations Company LLC Comanche Peak Nuclear Power Plant 6322 N FM 56 P.O. Box 1002 Glen Rose, TX 76043
SUBJECT:
COMANCHE PEAK NUCLEAR POWER PLANT, UNIT NO. 2 - REVIEW OF THE FALL 2021 STEAM GENERATOR TUBE INSPECTION REPORT (EPID L-2022-LRO-0065)
Dear Mr. Peters:
By letter dated May 5, 2022 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML22125A267), as supplemented by letter dated September 14, 2022 (ML22258A234), Vistra Operations Company LLC (Vistra OpCo, the licensee) submitted information summarizing the results of the fall 2021 steam generator inspections performed at Comanche Peak Nuclear Power Plant, Unit No. 2 (Comanche Peak, Unit 2). The inspections were performed during refueling outage 19. The information was submitted in accordance with Comanche Peak Technical Specification (TS) 5.6.9, Steam Generator Tube Inspection Report.
The U.S. Nuclear Regulatory Commission (NRC) staff has completed its review of the information provided by Vistra OpCo and concludes that the licensee provided the information required by Comanche Peak TS 5.6.9 and that no follow-up is required at this time. A summary of the NRC staffs review is enclosed.
K. Peters If you have any questions, please contact me at 301-415-6256 or via e-mail at Dennis.Galvin@nrc.gov.
Sincerely,
/RA/
Dennis J. Galvin, Project Manager Plant Licensing Branch IV Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-446
Enclosure:
Review of the Fall 2021 Steam Generator Tube Inspection Report cc: Listserv
REVIEW OF THE FALL 2021 STEAM GENERATOR TUBE INSPECTION REPORT COMANCHE PEAK POWER COMPANY LLC AND VISTRA OPERATIONS COMPANY LLC COMANCHE PEAK NUCLEAR POWER PLANT, UNIT NO. 2 DOCKET NO. 50-446 By letter dated May 5, 2022 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML22125A267), as supplemented by letter dated September 14, 2022 (ML22258A234), Vistra Operations Company LLC (the licensee) submitted information summarizing the results of the fall 2021 steam generator (SG) inspections performed at Comanche Peak Nuclear Power Plant, Unit No. 2 (Comanche Peak, Unit 2). The inspections were performed during refueling outage (RFO) 19. In addition, the U.S. Nuclear Regulatory Commission (NRC) staff held a conference call with the licensee on November 4, 2021, regarding the ongoing SG inspection activities at Comanche Peak, Unit 2 (ML22020A178). The information was submitted in accordance with Comanche Peak Technical Specification 5.6.9, Steam Generator Tube Inspection Report.
Comanche Peak Unit 2 has four Westinghouse Model D5 SGs, each containing 4,570 thermally treated Alloy 600 tubes. Each tube has a nominal outside diameter of 0.750 inch and a nominal wall thickness of 0.043 inch. During SG fabrication, the tube ends were hydraulically expanded over the full depth of the tubesheet. The vertical sections of the tubes are supported on the hot-leg (HL) and cold-leg (CL) sides by horizonal stainless steel tube support plates (TSPs) with quatrefoil holes. The CL side also has a stainless steel flow distribution baffle and stainless steel preheater baffle plates, all with drilled holes. Some of the tubes in each SG were hydraulically expanded at selected preheater baffle plates to reduce tube vibration. Two sets of chrome-plated Alloy 600 anti-vibration bars support the U-bend section of the tubes. Following RFO 19 there were 62 remaining tubes identified as having potentially high manufacturing residual stress in the U-bend region, all in row 10 or higher.
The licensee provided the scope, extent, methods, and results of the SG tube inspections in the letter dated May 5, 2022, as supplemented. In addition, the licensee described corrective actions (e.g., tube plugging), if any were taken in response to the inspection findings.
Based on the review of the information provided, the NRC staff has the following observations:
A new degradation mechanism for Comanche Peak, Unit 2, axial outside diameter stress corrosion cracking (SCC) at a free span ding, was detected in one tube, in SG 1, row 1, column 69 (R1C69). The indication was located on the HL, approximately 18 inches above the third HL TSP in the tubing free span. The maximum depth and length of the indication were sized at 62 percent through-wall (TW) and 0.19 inches long, respectively.
Based on the screening criteria in industry guidelines, in situ pressure testing was not required. This was the only indication of SCC in this inspection.
Two tubes were stabilized and plugged in SG 3 due to a foreign object that caused wear on both tubes at the second CL TSP and could not be removed (R40C48 and R40C49).
Another tube in SG 3 (R6C79) was plugged due a wear indication in the U-bend region Enclosure
with a depth of 43 percent TW. The wear on tube R6C79 was attributed to a foreign object based on examination with a rotating probe, but the presence of an object could not be visually confirmed due to the inaccessible location. In the case of R6C79, the licensee explained in a clarification call on September 27, 2022, that no additional tubes were plugged because the other potentially affected tube (R6C80), which is adjacent to the wear on R6C79, was already plugged. The NRC staff confirmed that R6C80 was plugged during the spring 2002 outage, as documented in the SG tube inspection report dated June 5, 2002 (ML021640618), due to a single volumetric indication in the U-bend region.
Two tubes in SG 2 were plugged because they were previously identified as having potentially high manufacturing residual stress in the U-bend region (R1C55 and R1C95).
These were the last potentially high-stress tubes identified in rows 1-9 that were still in service.
Based on a review of the information provided, the NRC staff concludes that the licensee provided the information required by the Comanche Peak technical specifications. In addition, the NRC staff concludes that there are no technical issues that warrant additional follow-up action at this time since the inspections appear to be consistent with the objective of detecting potential tube degradation, and the inspection results appear to be consistent with industry operating experience at similarly designed and operated units.
ML22319A073 *by email OFFICE NRR/DORL/LPL4/PM NRR/DORL/LPL4/LA* NRR/DNRL/NCSG/BC*
NAME DGalvin PBlechman SBloom DATE 11/10/2022 11/15/2022 10/20/2022 OFFICE NRR/DORL/LPL4/BC* NRR/DORL/LPL4/PM NAME JDixon-Herrity DGalvin DATE 11/15/2022 11/15/2022