IR 05000461/2007002

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IR 05000461-07-002; Amergen Energy Company LLC; 01/01/52007 - 03/31/2007; Clinton Power Station; Event Followup
ML071100080
Person / Time
Site: Clinton Constellation icon.png
Issue date: 04/19/2007
From: Ring M
NRC/RGN-III/DRP/RPB1
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-07-002
Download: ML071100080 (28)


Text

ril 19, 2007

SUBJECT:

CLINTON POWER STATION NRC INTEGRATED INSPECTION REPORT 05000461/2007002

Dear Mr. Crane:

On March 31, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Clinton Power Station. The enclosed report documents the inspection results, which were discussed on April 5, 2007, with Mr. Bryan Hanson and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, two self-revealing findings of very low safety significance (Green), one of which was determined to involve a violation of NRC requirements, were identified. However, because of the very low safety significance and because it is entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with Section VI.A of the NRC Enforcement Policy.

If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the US Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, US Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, US Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at Clinton Power Station facility. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket No. 50-461 License No. NPF-62 Enclosure: Inspection Report No. 05000461/2007002 w/Attachment: Supplemental Information cc w/encl: Site Vice President - Clinton Power Station Plant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois Chairman, Illinois Commerce Commission

SUMMARY OF FINDINGS

IR 05000461/2007002; AmerGen Energy Company LLC; 01/01/52007 - 03/31/2007; Clinton

Power Station; Event Followup.

This report covers a 3-month period of baseline resident inspection and announced baseline inspections on radiation protection and security. The inspection was conducted by Region III inspectors and the resident inspectors. Two Green findings were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the sate operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector-Identified and Self Revealing Findings

Cornerstone: Mitigating Systems

Green: A finding of very low safety significance (Green) involving a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V, was self revealed when a low main condenser vacuum alarm was received in the main control room. The alarm was caused by the failure of an electronic circuit card. This circuit card failure also resulted in the main turbine bypass valves being interlocked closed (loss of safety function). The inspectors determined that the cause of this issue was inadequate instructions contained in the licensees Performance Centered Maintenance (PCM) process.

The finding was greater than minor because failure to have adequate instructions to implement an effective preventive maintenance program could be reasonably viewed as a precursor to a more significant event. Additionally, this finding could affect the mitigating systems cornerstone in that it is associated with a degraded condition that could concurrently influence mitigation equipment and the operators response to an initiating event. This finding was of very low safety significance because the exposure time was of short duration, less than 3 days. (Section 4OA3.1)

Green: A finding of very low safety significance (Green) was self-revealed following the loss of the division 3 shutdown service water (SX) system on August 17, 2006.

The loss of division 3 of SX occurred when a security guard bumped an SX circuit breaker hand switch for the cross tie valve, 1SX014C, with a piece of protective equipment. This finding resulted from the licensees failure to do an adequate inadvertent contact configuration control risk assessment during the implementation of a 2005 requirement for security personnel to carry new equipment on their person.

The finding was more than minor because it impacted the mitigating systems cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. With the circuit breaker in the OFF position, 1SX014C would remain open during a loss of offsite power event. In this configuration, the

SX system could not perform its safety function of supplying cooling water to both the division 3 diesel generator and the high pressure core spray pump room cooling system. This finding was of very low safety significance due to the short duration exposure time, less than three days, and credit for operator actions to restore the system back to service. This finding affected the work practices component of the cross-cutting area of human performance. Licensee management failed to ensure the proper management and oversight of security personnel rounds activities.

(Section 4OA3.2)

Licensee-Identified Violations

No findings of significance were identified.

REPORT DETAILS

Summary of Plant Status

The plant was operated at approximately 96 to 97 percent rated thermal power (maintaining 100 percent electrical output) throughout the inspection period with one exception. On March 2, 2007, operators lowered reactor power to approximately 50 percent to make repairs to an extraction steam line leak. Operators returned reactor power to 96 percent following the completion of repairs on March 4, 2007, and remained there through the close of the inspection period.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignments

a. Inspection Scope

The inspectors performed partial walkdowns of accessible portions of divisions of risk-significant mitigating systems equipment during times when the divisions were of increased importance due to the redundant divisions or other related equipment being unavailable. The inspectors utilized the valve and electric breaker checklists listed at the end of this report to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and issue reports (IRs) associated with the divisions to verify that those documents did not reveal issues that could affect division function. The inspectors used the information in the appropriate sections of the Updated Safety Analysis Report (USAR) to determine the functional requirements of the systems. The documents listed at the end of this report were also used by the inspectors to evaluate this area.

The inspectors performed four samples by verifying the alignment of the following divisions:

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the individual plant examination of external events with later additional insights, and their potential to impact equipment which could cause a plant transient, to verify that fire hoses and extinguishers were in their designated locations and available for immediate use, that fire detectors and sprinklers were not obstructed, that transient material loading was within the analyzed limits, and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program.

The inspectors reviewed portions of the licensees fire protection evaluation report and the USAR to verify consistency in the documented analysis with installed fire protection equipment at the station.

The inspectors completed nine samples by inspection of the following areas:

  • Fire Zones CB-2 Division 2 and CB-4 Division 1 cable spreading room;
  • Fire Zone T-1m, Turbine deck;
  • Fire Area C-2, 737'-0" Containment;
  • Fire Zone R-1c, RW 702 General access area;
  • Fire Zones A-1a and A-1b Auxiliary building general access area;
  • Fire Zone D-5a Division 1 diesel generator room;
  • Fire Zone T-1a, Turbine building 712' general access area and
  • Fire Area C-2, 803'-3," 789'-1," 778', and 755' Containment.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Quarterly Resident Inspector Review

a. Inspection Scope

The inspectors reviewed licensed-operator requalification training to evaluate operator performance in mitigating the consequences of a simulated event, particularly in the areas of human performance. The inspectors evaluated operator performance attributes which included communication clarity and formality, timely performance of appropriate operator actions, appropriate alarm response, proper procedure use and adherence, and senior reactor operator oversight and command and control.

Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the following documents:

  • SE-LOR-31, Loss of coolant accident, blowdown, and reflood, Revision 1;
  • OP-AA-101-111, Roles and responsibilities of on-shift personnel, Revision 1;

The inspectors also assessed the performance of the training staff evaluations involved in the requalification process. For any weaknesses identified, the inspectors observed that the licensee evaluators also noted the issues and discussed them in the critique at the end of the session. The inspectors verified all issues were captured in the training program and licensee corrective action process.

These activities completed one inspection sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 Routine Evaluation

a. Inspection Scope

The inspectors reviewed the effectiveness of the licensees maintenance efforts in implementing 10 CFR 50.65 (the maintenance rule (MR)) requirements, including a review of scoping, goal-setting, performance monitoring, short and long-term corrective actions, and current equipment performance problems. These systems were selected based on their designation as risk-significant under the maintenance rule, or being in the increased monitoring (MR category (a)(1)) group. In addition, the inspectors interviewed the system engineers and maintenance rule coordinator. The inspectors also reviewed IRs and associated documents for appropriate identification of problems, entry into the corrective action system, and appropriateness of planned or completed actions. The documents reviewed are listed at the end of the report. The inspectors completed one sample by reviewing the following:

  • Condensate booster pump and associated high risk air operated valves.

b. Findings

No findings of significance were identified.

.2 Periodic Evaluation

a. Inspection Scope

The inspectors examined the maintenance rule periodic evaluation report completed for the period of March 1, 2004, through March 1, 2006. The inspectors reviewed a sample of (a)(1) Action Plans, Performance Criteria, Functional Failures, and Condition Reports to evaluate the effectiveness of (a)(1) and (a)(2) activities. These same documents were reviewed to verify that the threshold for identification of problems was at an appropriate level and the associated corrective actions were appropriate. Also, the inspectors reviewed the maintenance rule procedures and processes. The inspectors focused the inspection on the following systems:

  • Control Room Ventilation (VC);
  • Diesel Generator (DG);
  • Neutron Monitoring (NR); and
  • Leak Detection (LD).

The inspectors verified that the periodic evaluation was completed within the time restraints defined in 10 CFR 50.65 (once per refueling cycle, not to exceed 24 months).

The inspectors also ensured that the licensee reviewed its goals, monitored Structures, Systems, and Components (SSCs) performance, reviewed industry operating experience, and made appropriate adjustments to the maintenance rule program as a result of the above activities.

The inspectors verified that:

  • the licensee balanced reliability and unavailability during the previous cycle, including a review of high safety significant SSCs;
  • (a)(1) goals were met, that corrective action was appropriate to correct the defective condition, including the use of industry operating experience, and that (a)(1) activities and related goals were adjusted as needed; and
  • the licensee has established (a)(2) performance criteria, examined any SSCs that failed to meet their performance criteria, and reviewed any SSCs that have suffered repeated maintenance preventable functional failures including a verification that failed SSCs were considered for (a)(1).

In addition, the inspectors reviewed maintenance rule self-assessments and audit reports that addressed the maintenance rule program implementation.

This review represented five triennial inspection samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment and Emergent Work Control

a. Inspection Scope

The inspectors observed the licensees risk assessment processes and considerations used to plan and schedule maintenance activities on safety-related structures, systems, and components particularly to ensure that maintenance risk and emergent work contingencies had been identified and resolved. The inspectors completed seven samples by assessing the effectiveness of risk management activities for the following work activities or work weeks:

  • Low pressure core spray pump and water leg pump maintenance and operability surveillance activities;
  • Risk assessment and planned work activities for division 1 main control room ventilation and standby gas treatment system maintenance windows;
  • Plans and risk assessment for CPS 9071.09, CO2 Puff test, following 0CO602 maintenance, and

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following operability determinations and evaluations affecting mitigating systems to determine whether operability was properly justified and the component or system remained available such that no unrecognized risk increase had occurred. The inspectors completed two samples of operability determinations and evaluations by reviewing the following:

  • Operability basis for IR 582162 and IR 582173, division 2 and 3 diesel generator air intake filter housing and

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of important mitigating, barrier integrity, and support systems that were identified as risk significant in the licensees risk analysis. The inspectors reviewed these activities to verify that the post maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. During this inspection activity, the inspectors interviewed maintenance and engineering department personnel and reviewed the completed post maintenance testing documentation. The inspectors used the appropriate sections of the Technical Specifications (TS) and USAR, as well as the documents listed at the end of this report, to evaluate this area.

Testing subsequent to the following activities was observed and evaluated to complete four inspection samples:

  • Work orders 995047 and 995048, addressing loose bolts on division 3 diesel generator;
  • Division 1 main control room ventilation addressing hydramotor 0FZC024 and calibration of control room chiller inlet temperature;
  • Standby gas treatment monthly operability surveillance to assess operability following planned maintenance activities, and

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed selected surveillance testing and/or reviewed test data to verify that the equipment tested using the surveillance procedures met the TS, the Technical Requirements Manual (TRM), the USAR, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in verifying mitigating systems capability and barrier integrity. The inspectors used the documents listed at the end of this report to verify that the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. In addition, the inspectors interviewed operations, maintenance and engineering department personnel regarding the tests and test results.

The inspectors evaluated the following surveillance tests to complete seven inspection samples:

  • Low pressure core spray pump and water leg pump operability surveillance;
  • Division 2 diesel generator surveillance test;
  • Division 3 diesel generator monthly surveillance test;
  • Anticipated transient without scram, reactor level channel check, calibration and functional test;
  • Division 1 diesel generator operability surveillance test.

These inspections represented the completion of six in-service tests and one routine test.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed and evaluated the following temporary plant modification on risk significant equipment to verify that the instructions were consistent with applicable design modification documents and that the modifications did not adversely impact system operability or availability. The inspectors interviewed operations, engineering and maintenance personnel as appropriate and reviewed the design modification documents and the 10 CFR 50.59 evaluations against the applicable portions of the USAR. The documents listed at the end of this report were also used by the inspectors to evaluate this area. The inspectors reviewed the issues that the licensee entered into its corrective action program to verify that identified temporary modification problems were being entered into the program with the appropriate characterization and significance. The inspectors also reviewed the licensees corrective actions for temporary modification related issues documented in selected condition reports.

The condition reports are specified in the List of Documents Reviewed.

The inspectors completed one inspection sample by reviewing the following temporary modification:

  • EC 365082, Rev 0, Disconnect leads for circuit breaker 252-AT1AA1 relay 74-AT1AA1 to bypass alarm to window 1D on main control room panel 1H13-P877-14A.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES (OA)

4OA1 Performance Indicator Verification

Cornerstones: Initiating Events

a. Inspection Scope

The inspectors sampled the licensees submittals for performance indicators for the period of first quarter 2005 through fourth quarter 2006. The inspectors used performance indicator definitions and guidance contained in Revision 4 of Nuclear Energy Institute (NEI) document 99-02, Regulatory Assessment Performance Indicator Guideline to verify the accuracy of the performance indicator data. The inspectors performed three samples by reviewing the following:

  • Scrams with Loss of Normal Heat Removal;
  • Unplanned Scrams per 7,000 Critical Hours; and

b. Issues and Findings No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review and Identification of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action system at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action system as a result of inspectors observations are generally denoted in the report.

b. Findings

No findings of significance were identified.

.2 Reactor water clean-up system leakage (Annual sample)

a. Inspection Scope

The inspectors reviewed licensee actions associated with recurring alarms for reactor water clean up A heat exchanger room delta temperature and an increasing reactor water clean up differential flow, to determine if corrective actions were timely, accurate and complete. The inspectors interviewed licensee personnel from operations and work management and reviewed issue reports and work documents to complete one inspection sample. A list of documents reviewed is included in the attachment to this report.

b. Observations On January 23, 2007, main control room operators responded to annunciators 5004-3F, SPDS CSF Alarm due to secondary containment delta temperature and 5000-3F, Reactor water cleanup equipment room differential temperature high.

Operators also noticed an increase in reactor water cleanup differential flow associated with these alarms, and entered the reactor coolant leakage off-normal procedure, CPS 4001.01. Plant personnel then made an entry into the reactor water cleanup A heat exchanger room, but observed no indications of system breach or gross leakage.

An issue report was generated and operators continued to monitor the conditions of the reactor water cleanup A heat exchanger room. Between January 23 and February 5, 2007, operators responded to these same alarms several times, and conducted a historical search on this issue. Between September 24, 2004, and December 7, 2006, nine issue reports had been generated to address this issue. On February 2, 2007, the maintenance organization identified high tailpipe temperatures downstream of reactor water cleanup regenerative heat exchanger AA shell side drain valves 1G33-F018A and 1G33-F019A. In addition, using thermography, maintenance technicians confirmed high tailpipe temperatures and ongoing seat leakage past regenerative heat exchanger AA tube side drain valves 1G33-F014A and 1G33-F015A, which had been identified in 2004. On February 5, 2007, operations swapped reactor water cleanup heat exchanger trains to place the B train in service. All of the issue reports related to this drain valve leak by and alarm responses were closed to work order 992459. The inspectors looked at work order 992459 to ensure all of the issues were captured for repair, but the work order was still in the plan stage, and no job steps had been written. The inspectors questioned the corrective action program manager and a work week manager about the process of converting corrective action program documents into work documents. These individuals informed the inspectors that in the process, all of the items closed to the work order were linked through references in Passport, and the maintenance planner had access to all of the issue reports. It was the maintenance planners responsibility to ensure the work order included job steps to address all of the deficiencies identified through the corrective action process.

c. Conclusions

The inspectors did not identify any performance deficiencies in the licensees response to the reactor water cleanup heat exchanger valve leakage and resultant alarms. The licensee did identify the source of leakage and cause for the alarms and addressed each of these appropriately in its corrective action program. The inspectors concluded that the licensees process for converting corrective action program items to work documents had some vulnerability however. Once issue reports are closed to a work order, a single maintenance planner has responsibility to correctly identify, classify, and develop actions to correct all of the conditions addressed in multiple issue reports. The feedback process incorporated in the corrective action program notifies the originator of the issue that work will be done to address the issue. The inspectors were concerned that some issues, addressed through the licensees corrective action program and closed to the work process, could get missed or dropped, and the organization would not be aware that the anticipated actions were not taken. The inspectors discussed their concern with the licensee.

.3 Adverse effects of scaffolding on safety related equipment (Annual sample)

a. Inspection Scope

The inspectors reviewed licensee corrective action program documents and work documents related to scaffolding between March 1, 2005, and February 28, 2007, to identify the possible effects of scaffolding on the availability or operability of safety related systems. A list of documents reviewed is included in the attachment to this report. This activity represented one inspection sample.

b. Observations A word search of the licensees corrective action program for scaffolding between March 2005 and February 2007 resulted in a thirty eight page list of documents. Many of these hits were related to work requiring scaffolding or requesting scaffolding be built or wrecked. Only seven of these issues were related to improperly built or evaluated scaffolding. The inspectors reviewed these issues and had no concerns that scaffolding could have caused a safety function or safety related system to be inoperable or unavailable as described in the industry operating experience reviewed.

4OA3 Event Followup

.1 (Closed) LER 05000461/2006002-00 and 01. Main Turbine Bypass System Safety

Function Lost Due to Circuit Card Failure

Introduction:

A finding of very low safety significance (Green) involving a non-cited violation of 10 CFR 50, Appendix B, Criterion V was self-revealed when a low main condenser vacuum alarm was received in the main control room. The alarm was caused by the failure of an electronic circuit card. This card failure also resulted in the main turbine bypass valves being interlocked closed (loss of safety function). The inspectors determined that the cause of this issue was inadequate instructions contained in the licensees Performance Centered Maintenance (PCM) process.

Description:

On August 17, 2006, operators in the control room received a main condenser low vacuum alarm. The plant was at full power operations. After verifying all pertinent indications were normal, the licensee identified that with this alarm in place, the main turbine bypass valves were interlocked closed. Clinton Improved TS require the main turbine bypass valves to be operable when the reactor thermal power is greater than or equal to 21.6 percent. The operators correctly entered TS 3.7.6, Main Turbine Bypass System, which has a limiting condition for operation (LCO) 2-hour action statement.

Shortly after entry into this LCO action statement, a troubleshooting team determined that the failure of a single main condenser pressure trip unit was the cause of the event. The alarm/trip units (electronic circuit cards) are arranged in a 1 out of 2 logic to inhibit the main turbine bypass valve opening function when main condenser vacuum is too low for steam to be admitted. The licensee performed a system modification that involved lifting the leads to the electronic circuit card to remove the low vacuum inhibit logic input. This action restored the main turbine bypass valve safety function. The low vacuum light extinguished as expected.

As part of the investigation into this event, the licensee completed an equipment apparent cause evaluation (EACE), to find the apparent cause of the low vacuum alarm and subsequent loss of safety function. A failure analysis completed by the vendor showed that the circuit card had degraded due a leaky electrolytic capacitor. The licensees EACE identified that the electronic circuit card was approximately 27 years old and had approximately 22 years of actual service time.

The licensees PCM process, as described in licensee procedure MA-AA-716-210, is a process for selecting effective preventive maintenance (PM) activities for components to minimize consequential failures. The PCM provides standardized generic PM tasks and frequencies based on the importance of the component. The results of the PCM process are PCM Templates which contain recommended PM frequencies for critical components. According to the licensee, Electric Power Research Institutes Plant Material Condition Excellence Initiative (PMCEI) was the basis document for the PCM process. A licensee review of the PCM template applicable to this electronic circuit card was performed. The PCM Template, Circuit Cards - Moore Industries contains a specific section for the model direct current alarm (DCA) card that has a requirement to replace it every 30 years.

The licensee investigation concluded that the cause of this event was the failure of the electrolytic capacitor on the main condenser pressure trip unit due to the PCM template not specifying the appropriate replacement interval for Moore Industries model DCA cards. The circuit card replacement frequency in the PCM template for Moore model DCA cards is 30 years, and is in direct contrast to a PCM template created for power supplies, which addresses electrolytic capacitor aging, and has a replacement frequency of 7.5 years. The PMCEI basis document states A lifetime for a particular card was calculated by identifying all the sub-components on that card and then determining the individual failure rates for the sub-components. The sub-component failure rates were taken from published databases. An overall circuit card failure rate was then determined based on the sub-component failure rates. Since the Moore Industries DCA cards had electrolytic capacitors as sub-components, the cards should have been replaced on a 7.5 year frequency, not the 30 year frequency in the PCM Template.

The inspectors reviewed procedures MA-AA-716-210, Performance Centered Maintenance Process, and MA-AA-716-210-1001, Performance Centered Maintenance Templates to ensure that the guidance contained in the basis document was incorporated into the process procedures. Specifically, the inspectors reviewed step 4.13 of MA-AA-716-210 which describes the process of making changes to existing PCM templates or creating new PCM templates. During this review the inspectors concluded that the procedure lacks specific guidance that would ensure that individuals reviewing, changing, or creating a new PCM template would be aware of the PMCEI document statement referenced above. The inspectors concluded that this lack of guidance was the cause of the PCM template for the Moore model DCA card being incorrect.

Analysis:

Failure of the electrical circuit card resulted in a loss of safety function for the main turbine bypass valves. The PCM template contained an incorrect PM frequency, which resulted in an unexpected failure of the electrical circuit card. This issue was caused by inadequate instructions in the licensee PCM program process procedure.

This was a performance deficiency warranting a significance evaluation. The inspectors concluded that the finding was greater than minor in accordance with Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, issued on November 16, 2006. Failure to have instructions to implement an effective preventive maintenance program could be reasonably viewed as a precursor to a more significant event. Additionally, this finding could affect the mitigating systems cornerstone in that it is associated with a degraded condition that could concurrently influence mitigation equipment and the operators response to an initiating event (Attribute: External Factor - Loss of Heat Sink).

The inspectors completed a phase 1 significance determination of this issue using IMC 0609, Significance Determination Process, Appendix A, Attachment 1, dated March 23, 2007. The inspectors concluded that the finding affected the mitigating systems cornerstone. The inspectors answered Yes to question 2, which asked whether this issue resulted in a loss of system safety function. The inspectors completed a phase 2 analysis and determined that this issue was of very low safety significance (Green) because the exposure time was of short duration, less than three days.

Enforcement:

10 CFR 50 Appendix B, Criterion V, states that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Contrary to the above, the licensee failed to develop an adequate PCM template because of lack of sufficient details in procedure MA-AA-716-210, Performance Centered Maintenance Program. This failure resulted in loss of the safety function of the main turbine bypass valves on August 17, 2006. This was a violation. This issue was considered to be of very low safety significance and was entered into the licensees corrective action program as IR 555579. The licensee performed an apparent cause evaluation that developed actions to correct this issue. Therefore, this issue is being treated as non-cited violation (NCV 05000461/2007-002-01). Licensee Event Reports05000461/2006002-00 and 01, Main Turbine Bypass System Safety Function Lost Due to Circuit Card Failure are closed.

.2 (Closed) LER 05000461/2006004-00: Inadequate Configuration Control Risk

Assessment Causes Loss of Safety Function

Introduction:

A finding of very low safety significance (Green) was self-revealed following the loss of the division 3 shutdown service water (SX) on August 17, 2006.

This finding resulted from the licensees failure to do an adequate inadvertent contact configuration control risk assessment during the implementation of a 2005 requirement for security personnel to carry new equipment on their person.

Description:

During the performance of shiftly rounds, a security officer bumped a circuit breaker hand switch for the SX to normal service water crosstie isolation valve (1SX014C) to the OFF position. After the breaker hand switch was bumped, a high pressure core spray system alarm was received in the main control room coincident with the loss of position indication for 1SX014C. With the breaker in the OFF position, the division 3 emergency diesel generator and the high pressure core spray system were rendered inoperable. The operators also declared the division 3 SX system inoperable and unavailable. Before returning the breaker to the ON position, the licensee conducted troubleshooting and determined that the breaker had not tripped due to an actual adverse condition. The operators returned the breaker to its normal position after approximately one hour and declared the systems operable.

The licensee completed a root cause report and determined that the root cause of this event was that security management failed to adequately assess the inadvertent contact configuration control risk when the requirement for security officers to carry a protective mask in a bag attached to the thigh was implemented in 2005. The root cause also concluded that the licensees Operations organization failed to provide adequate information and expectations to the plant organization regarding configuration control inadvertent contact events, at the level of detail needed to identify and mitigate these hazards.

Analysis:

The inspectors determined that the failure to perform an adequate configuration control risk evaluation was a performance deficiency warranting a significance evaluation. The inspectors concluded that the finding was more than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, issued on November 17, 2006, because it impacted the equipment performance attribute of the mitigating systems cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. With the circuit breaker in the OFF position, 1SX014C would remain open during a loss of offsite power event. In this configuration, the SX system could not perform its safety function of supplying cooling water to both the division 3 diesel generator and the high pressure core spray (HPCS) pump room cooling system.

The inspectors completed a phase 1 significance determination using IMC 0609, Significance Determination Process, Appendix A, Attachment 1, dated March 23, 2007. The inspectors concluded that the finding affected the mitigating systems cornerstone. The inspectors answered Yes to question 2, which asked whether this issue resulted in a loss of system safety function. The inspectors proceeded to do a phase 2 analysis and the results showed that this issue had very low safety significance (Green) due to the short duration exposure time, less than three days, and credit for operator actions to restore the system back to service. This finding involved the cross-cutting area of human performance (work practices).

Licensee management failed to ensure the proper management and oversight of security personnel rounds activities.

Enforcement:

No violation of regulatory requirements occurred. This issue was considered a finding of very low safety significance (FIN 05000461/2007-002-02).

This issue was entered into the licensees corrective action program as IRs 520922 and 613643. Licensee Event Report 05000461/2006004-00, Inadequate Configuration Control Risk Assessment Causes Loss of Safety Function is closed.

.3 (Closed) LER 05000461/2006003-00: High Reactor Water Level Scram Result of Bad

Inverter Circuit Board Solder Joint.

On August 27, 2006, Clinton Power Station experienced an automatic reactor scram on high water level condition (>52 inches). This high water level condition was created by the automatic start and injection of HPCS and a subsequent trip of the 1A reactor recirculation pump. The HPCS injection and recirculation pump trip occurred because of a failure of the Division 4 Nuclear Safety Protection System Inverter.

The licensees investigation into this event determined that the inverter failure occurred because of an inadequate/faulty solder joint on a back plane connector.

This conclusion was verified by the vendor and PowerLabs during post-event testing of the back plane connector. Both the vendor and PowerLabs concluded that poor quality soldering (lack of solder flow through etched circuit board eyelet) resulted in pooling (no penetration through eyelet) of solder at common connection between the R103 resistor, the J2 board, and the DC to DC converter.

In NRC Inspection Report 50-461/2006007, the inspectors documented a self-revealed Green finding and a Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion XVI, (NCV 05000461/2006007-01). The NCV was identified due to the licensees failure to identify and correct a condition adverse to quality.

Specifically, the licensee failed to identify and correct the cause of a failure of the Division 4 Nuclear Safety Protection System (NSPS) Inverter in March of 2006.

Licensee Event Report 05000461/2006003-00, High Reactor Water Level Scram Result of Bad Inverter Circuit Board Solder Joint. is closed.

4OA4 Cross-Cutting Aspects of Findings

.1 A finding described in Section 4OA3.2 of this report had, as its primary cause, a human

performance deficiency, in that the licensee management failed to ensure proper management and oversight of security personnel rounds activities. This inadequate oversight resulted in the Division 3 SX system being rendered inoperable.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. B. Hanson and other members of licensee management at the conclusion of the inspection on April 5, 2007. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meeting

An interim exit meeting was conducted for:

Maintenance Effectiveness Periodic Evaluation with Mr. B. Hanson, Site Vice President on January 26, 2007.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

B. Hanson, Site Vice President
R. Kearney, Plant Manager
R. Schenck, Work Management Director
G. Vickers, Radiation Protection Director
R. Frantz, Regulatory Assurance Representative
J. Icard, Maintenance Rule Coordinator
K. Scott, Regulatory Assurance Director
C. Vanderburgh, Nuclear Oversight Manager
J. Domitrovich, Maintenance Director
D. Schavey, Operations Director
W. Scott, Chemistry Manager
J. Lindsay, Training Director
C. Williamson, Security Manager
R. Peak, Site Engineering Director
T. Chalmers, Shift Operations Superintendent

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000461/2007-002-01 NCV Failure of the electrical circuit card resulted in a loss of safety function for the main turbine bypass valves.
05000461/2007-002-02 FIN Failure to perform an adequate configuration control risk evaluation was a performance deficiency warranting a significance evaluation.
05000461/2006002-00 and 01 LER Main Turbine Bypass System Safety Function Lost Due to Circuit Card Failure
05000461/2006004-00 LER Inadequate Configuration Control Risk Assessment Causes Loss of Safety Function.
05000461/2006003-00 LER High Reactor Water Level Scram Result of Bad Inverter Circuit Board Solder Joint.

Discussed

None Attachment

LIST OF DOCUMENTS REVIEWED