IR 05000456/2011002
ML111230224 | |
Person / Time | |
---|---|
Site: | Braidwood |
Issue date: | 05/02/2011 |
From: | Eric Duncan Region 3 Branch 3 |
To: | Pacilio M Exelon Nuclear, Exelon Generation Co |
References | |
IR-11-002 | |
Download: ML111230224 (58) | |
Text
May 2, 2011
SUBJECT:
BRAIDWOOD STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000456/2011002; 05000457/2011002
Dear Mr. Pacilio:
On March 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Braidwood Station, Units 1 and 2. The enclosed inspection report documents the results of this inspection, which were discussed on April 6, 2011, with Mr. D. Enright and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the results of this inspection, the NRC has determined that one Severity Level IV violation of NRC requirements occurred. The NRC has also identified three issues that were evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has determined that three violations of NRC requirements are associated with these issues. However, because of their very low safety significance, and because the issues were entered into your corrective action program, the NRC is treating the violations as Non-Cited Violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in Section 4OA7 of this report.
If you contest the subject or severity of any of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Senior Resident Inspector at the Braidwood Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Senior Resident Inspector at the Braidwood Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Eric R. Duncan, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77
Enclosure:
Inspection Report 05000456/2011002; 05000457/2011002 w/Attachment: Supplemental Information
REGION III==
Docket Nos: 50-456; 50-457 License Nos: NPF-72; NPF-77 Report No: 05000456/2011002; 05000457/2011002 Licensee: Exelon Generation Company, LLC Facility: Braidwood Station, Units 1 and 2 Location: Braceville, IL Dates: January 1 through March 31, 2011 Inspectors: J. Benjamin, Senior Resident Inspector D. Betancourt-Roldan, Acting Resident Inspector N. Feliz-Adorno, Reactor Engineer J. Gall, Reactor Engineer J. Gilliam, Reactor Engineer, Electrical M. Holmberg, Senior Reactor Engineer R. Jickling, Senior Emergency Preparedness Inspector M. Thorpe-Kavanaugh, Reactor Engineer M. Perry, Resident Inspector Illinois Emergency Management Agency Approved by: E. Duncan, Chief Branch 3 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000456/2011002, 05000457/2011002; 01/01/2011 - 03/31/2011; Braidwood Station,
Units 1 & 2; Followup of Events; Other Activities.
This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. This report contains three NRC-identified Green findings and one NRC-identified Severity Level IV violation. Three of these issues were considered Non-Cited Violations (NCVs) of NRC regulations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Assigned cross-cutting aspects were determined using IMC 0310, Components Within the Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
NRC-Identified
and Self-Revealed Findings Severity Level IV: A Severity Level IV NCV of 10 CFR 50.9, Completeness and Accuracy of Information, was identified by the inspectors when licensee personnel failed to provide information to the NRC that was complete and accurate in all material respects in Licensee Event Report (LER) 05000457/2010-004-00, Unplanned Limiting Condition for Operation Entry Due to Low Header Pressure on the 2B Essential Service Water Pump. Specifically, the LER stated that an analysis had determined that both units and trains of the Essential Service Water (SX) system were capable of mitigating the effects of design basis events. However, the referenced analysis had not been performed at the time the LER was submitted.
The inspectors determined that this issue was a Severity Level IV violation based on a similar example referenced in Section 6.9, Inaccurate and Incomplete Information or Failure to Make a Required Report, of the NRC Enforcement Policy. In particular, example d.1 identified that a licensee failing to make a required report which, had it been submitted, would have resulted in, for instance, increasing the scope of the next regularly scheduled inspection, was a Severity Level IV violation. The inaccurate information was considered to be material to the NRC because it potentially affected an NRC assessment of whether a loss of safety function occurred and whether it should have been reported to the NRC. This issue was entered into the licensees corrective action program and corrective actions included the station performing the analysis referenced in the LER. The inspectors had previously reviewed the Reactor Oversight Process (ROP) aspect of this finding and a self-revealed NCV of 10 CFR Part 50,
Appendix B, Criterion V, Instructions, Procedures, and Drawings, was documented in Section 1R22 of NRC Integrated Inspection Report 05000456/2010004; 05000457/2010004 for this issue. (Section 4OA3.1)
Cornerstone: Mitigating Systems
- Green.
A finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified by the inspectors when licensee personnel failed to establish instructions for measuring pipe voids detected during surveillances of the emergency core cooling systems for gas accumulation. Specifically, instructions to measure the size of gas voids detected during venting at each safety injection and residual heat removal system vent location were not provided so that the effect of the void on system operability could be evaluated. The licensee entered this issue into the corrective action program and initiated procedure revisions to provide additional guidance for recording data to size voids identified during venting operations.
The performance deficiency was determined to be more than minor because if left uncorrected it would have the potential to lead to a more significant safety concern.
The finding screened as having very low safety significance because it did not result in a loss of operability or functionality. Specifically, a qualitative assessment of the voids detected by venting since the implementation of the licensees resolution of Generic Letter 2008-01 established reasonable assurance that the voids did not result in a loss of operability. The inspectors did not identify a cross-cutting aspect that represented the underlying cause of this performance deficiency. Therefore, no cross-cutting aspect was assigned. (Section 4OA5.2)
Cornerstone: Barrier Integrity
- Green.
The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control, when licensee personnel failed to account for vortexing when determining the maximum available time to secure flow from the containment spray additive tank. Specifically, the applicable calculation failed to account for the impact of vortexing, but assumed that the nitrogen in the tank would not enter the system until the tank was completely drained.
The licensee entered this issue into the corrective action program and, at the time of the inspection, planned to revise the applicable calculation.
The performance deficiency was determined to be more than minor because it was associated with the Structures, Systems, Components, and Barrier Performance attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. The finding screened as having very low safety significance because it was a design deficiency of the physical integrity of the reactor containment that did not: (1) affect the barrier function of the control room against smoke or a toxic atmosphere; (2) represent an actual open pathway in the physical integrity of reactor containment; and (3) involve an actual reduction in function of hydrogen igniters in the reactor containment. The inspectors determined that this finding had a cross-cutting aspect in the area of Problem Identification and Resolution, Operating Experience, because the licensee did not thoroughly evaluate external operating experience. P.2(a) (Section 4OA5.2)
- Green.
The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control, when licensee personnel failed to evaluate the effects of dynamic loads at the containment spray discharge piping. The inspectors were concerned because portions of the containment spray discharge piping were normally voided by design and neither the structural design nor operation of the system addressed the dynamic loads that would result when the voided piping was rapidly filled following system initiation. The licensee entered this issue into the corrective action program and, at the time of the inspection, planned to review the design to ensure compliance.
The performance deficiency was determined to be more than minor because it was associated with the Structures, Systems, Components, and Barrier Performance attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. The finding screened as having very low safety significance because it did not affect either core damage frequency or large early release frequency. The inspectors determined that this finding had a cross-cutting aspect in the area of Problem Identification and Resolution,
Operating Experience, because the licensee did not thoroughly evaluate external operating experience. P.2(a) (Section 4OA5.2)
Licensee-Identified Violations
A violation of very low safety significance that was identified by the licensee has been reviewed by inspectors. Corrective actions planned or taken by the licensee have been entered into the licensees corrective action program. The violation and corrective action tracking number is listed in Section 4OA7 of this report.
REPORT DETAILS
Summary of Plant Status
Unit 1 operated at or near full power during the inspection period.
Unit 2 operated at or near full power during the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
.1 External Flooding
a. Inspection Scope
The inspectors evaluated the design, material condition, and procedures for coping with the design basis probable maximum flood. The evaluation included a review to check for deviations from the descriptions provided in the Updated Final Safety Analysis Report (UFSAR) for features intended to mitigate the potential for flooding from external factors.
As part of this evaluation, the inspectors checked for obstructions that could prevent draining, checked that the roofs did not contain obvious loose items that could clog drains in the event of heavy precipitation, and determined whether barriers required to mitigate the flood were in place and operable. Additionally, the inspectors performed a walkdown of the protected area to identify any modification to the site which would inhibit site drainage during a probable maximum precipitation event or allow water ingress past a barrier. The inspectors also walked down underground bunkers/manholes subject to flooding that contained multiple train or multiple function risk-significant cables. The inspectors also reviewed the abnormal operating procedure for mitigating the design basis probable maximum flood to ensure it could be implemented as written.
This inspection constituted one external flooding sample as defined in IP 71111.01-05.
b. Findings
No findings of significance were identified.
.2 Readiness for Impending Adverse Weather Condition - Blizzard Conditions
a. Inspection Scope
On February 1 and February 2, 2011, a blizzard advisory was issued for the surrounding area. The inspectors observed the licensees preparations and planning for the significant winter weather. The inspectors reviewed licensee procedures and discussed potential compensatory measures with control room personnel. The inspectors focused on plant managements actions for implementing the stations procedures for ensuring that adequate personnel for safe plant operation and emergency response would be available. The inspectors conducted a site walkdown that included plant structures and systems to check for maintenance or other apparent deficiencies that could affect system operations during the predicted significant weather. The inspectors also reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Documents reviewed are listed in the Attachment.
This inspection constituted one readiness for impending adverse weather condition sample as defined in IP 71111.01-05.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
.1 Quarterly Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant systems:
- 1B Residual Heat Removal System with the 1A Residual Heat Removal System Out-of-Service;
- 2A Emergency Diesel Generator with the 2B Emergency Diesel Generator Out-of-Service; and
- 2B Containment Spray System After Return to Service From Maintenance.
The inspectors selected these systems based on their risk significance relative to the Reactor Safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the
.
These activities constituted three partial system walkdown samples as defined in IP 71111.04-05.
b. Findings
No findings of significance were identified.
.2 Semiannual Complete System Walkdown
a. Inspection Scope
On March 28, 2011, the inspectors performed a complete system alignment inspection of the Unit 2 Auxiliary Feedwater System to verify the functional capability of the system.
This system was selected because it was considered both safety-significant and risk-significant in the licensees probabilistic risk assessment. The inspectors walked down the system to review mechanical and electrical equipment lineups, electrical power availability, system pressure and temperature indications, component labeling, component lubrication, component and equipment cooling, hangers and supports, and the operability of support systems, and to ensure that auxiliary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding WOs was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the CAP database to ensure that system equipment alignment problems were being identified and appropriately resolved.
Documents reviewed are listed in the Attachment.
These activities constituted one complete system walkdown sample as defined in IP 71111.04-05.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
.1 Routine Resident Inspector Tours
a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
- Auxiliary Building 346 Elevation, Fire Zone 11.2-0;
- 2A Emergency Diesel Generator Room, Fire Zone 9.2-0;
- 2A Diesel Oil Storage Tank Room, Fire Zone 10.2-2;
- 1A Safety Injection Pump Room, Fire Zone 11.3A-1; and
- Unit 1 Auxiliary Building Basement Area, Fire Zone 11.1A-0.
The inspectors reviewed these areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that issues identified during the inspection were entered into the licensees CAP.
These activities constituted five quarterly fire protection inspection samples as defined in IP 71111.05-05.
b. Findings
No findings of significance were identified.
1R06 Flooding
.1 Internal Flooding
a. Inspection Scope
The inspectors reviewed selected risk-important plant design features and licensee procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors reviewed flood analyses and design documents, including the UFSAR, engineering calculations, and abnormal operating procedures to identify licensee commitments. In addition, the inspectors reviewed licensee drawings to identify areas and equipment that may be affected by internal flooding caused by the failure or misalignment of nearby sources of water, such as the fire suppression or the circulating water systems. The inspectors also reviewed the licensees corrective action documents with respect to past flood-related items identified in the corrective action program to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following plant area to assess the adequacy of watertight doors and verify drains and sumps were clear of debris and were operable, and that the licensee complied with its commitments:
- 1A/2A Essential Service Water Room.
Documents reviewed are listed in the Attachment.
This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program
.1 Resident Inspector Quarterly Review
a. Inspection Scope
On March 8, 2011 the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
- licensed operator performance;
- crews clarity and formality of communications;
- ability to take timely actions in the conservative direction;
- prioritization, interpretation, and verification of annunciator alarms;
- correct use and implementation of abnormal and emergency procedures;
- control board manipulations;
- oversight and direction from supervisors; and
- ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.
The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment.
This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
.1 Routine Quarterly Evaluations
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk-significant systems:
- Unit 2 Essential Service Water System;
- Unit 1 Auxiliary Feedwater System; The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
- implementing appropriate work practices;
- identifying and addressing common cause failures;
- scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
- characterizing system reliability issues for performance;
- charging unavailability for performance;
- trending key parameters for condition monitoring;
- ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
- verifying appropriate performance criteria for structures, systems, and components/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified as (a)(1).
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.
This inspection constituted two quarterly maintenance effectiveness samples as defined in IP 71111.12-05.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
.1 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
- Unit 1 Rods in Manual - Rod Control Issue the Week of January 10 - Emergent Yellow;
- 1B Residual Heat Removal Work the Week of January 23 - Planned Yellow;
- 1A Diesel Generator Out-of-Service During a Blizzard the Week of January 31- Unplanned Orange;
- 2B Diesel Generator Out-of-Service for 6-Year Inspection the Week of February 13 - Planned Yellow;
- 2A Diesel Generator Ventilation Failure the Week of February 7 - Unplanned Yellow;
- 1A Safety Injection Pipe Replacement the Week of February 28- Unplanned Yellow; and
- 1A and 2A Motor Driven Auxiliary Feedwater Pump Declared Unavailable due to Voiding that Occurred the Week of March 30- Unplanned Orange.
These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
These maintenance risk assessments and emergent work control activities constituted seven samples as defined in IP 71111.13-05.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
.1 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following issues:
- Bus 141 Degraded Voltage Capacitor, IR 1124974;
- Auxiliary Feedwater Essential Service Water Suction Void, IR 1173517;
- Westinghouse Software Issue Impacts Containment Analysis, IR 117319;
- 2CV8409 Inoperable Weld, IR 1166795;
- Residual Heat Removal Instrument Time Response, IR 1147181;
- Impact of Voids in Safety Injection Accumulators Not Accounted For, IR 1174764; and
- Degraded Stab Assemblies at Pressurizer Heaters, IR 1181341.
The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sample of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the
.
These operability evaluation inspection activities constituted seven samples as defined in IP 71111.15-05.
b. Findings
No findings of significance were identified.
1R18 Plant Modifications
.1 Plant Modifications
a. Inspection Scope
The inspectors reviewed the following modifications:
- Temporary Modification - Unit 1 Phase Sensing Transformer Modification in Rod Control Circuitry;
- Permanent Modification - Unit 2 Main Steam Leak Encapsulation and Bracing Repair from a Tap Line Off the 30-inch Main Steam Line Feeding the High Pressure Turbine;
- Permanent Modification - Unit 1 and Unit 2 Auxiliary Feedwater Voided Section Fill.
The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to verify that the modification did not affect the operability or availability of the affected systems. The inspectors, as applicable, observed ongoing and completed work activities to ensure that the modifications were installed as directed and consistent with the design control documents; the modifications operated as expected; post-modification testing adequately demonstrated continued system operability, availability, and reliability; and that operation of the modifications did not impact the operability of any interfacing systems. As applicable, the inspectors verified that relevant procedure, design, and licensing documents were properly updated. Lastly, the inspectors discussed the plant modification with operations, engineering, and training personnel to ensure that the individuals were aware of how the operation with the plant modification in place could impact overall plant performance. Documents reviewed are listed in the Attachment.
This inspection constituted one temporary modification sample and two permanent plant modification samples as defined in IP 71111.18-05.
b. Findings
No findings of significance were identified.
1R19 Post-Maintenance Testing
.1 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
- Post-Maintenance Testing Associated with Engineering Change 382805 - Unit 1 Phase Sensing Rod Control Transformer Modification;
- 1A Residual Heat Removal Pump Post-Maintenance Testing - Pump Oil Change
- 2B Emergency Diesel Generator 6-year Inspection;
- 1A Safety Injection Inoperable Weld- Radiography Test Associated with the Weld Repair;
- 1A Safety Injection Inoperable Weld - System Fill and Vent Associated with Piping Replacement; and
- 1A Safety Injection Inoperable Weld - Bonnet Replacement Associated with Drain Valve.
These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable):
the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with the post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment.
This inspection constituted six post-maintenance testing samples as defined in IP 71111.19-05.
b. Findings
No findings of significance were identified.
1R20 Outage Activities
.1 New Fuel Receipt
a. Inspection Scope
During this quarter, the inspectors observed new fuel receipt inspections in anticipation of the Unit 2 refueling outage, 2AR15, which was scheduled to begin in the Spring of 2011. The inspectors verified that the licensee performed inspections in accordance with their procedures and that any issues were appropriately dispositioned.
The inspection did not constitute an outage sample as defined in IP 71111.20-05, but will be a part of the Unit 1 refueling outage sample planned for next quarter
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
.1 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:
- Unit 1 Reactor Coolant System Unidentified Leakage - (Reactor Coolant System (RCS) Leak Detection sample);
- 1B Emergency Diesel Generator Bypass of Auto Trips - (Routine sample);
- Unit 1 Rod Drive Exercising - (Routine sample);
- 1B Auxiliary Feedwater Pump Monthly - (Routine sample);
- 1A Safety Injection System Fill and Vent - (Routine sample); and
- 2B Containment Spray Valve 2CS 003B/11B American Society of Mechanical Engineers Testing (ASME) - (In-Service Testing (IST) sample).
The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:
- did preconditioning occur;
- were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
- were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
- plant equipment calibration was correct, accurate, and properly documented;
- as-left setpoints were within required ranges; and the calibration frequency was in accordance with TS, the UFSAR, procedures, and applicable commitments;
- measuring and test equipment calibration was current;
- test equipment was used within the required range and accuracy;
- applicable prerequisites described in the test procedures were satisfied;
- test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures;
- jumpers and leads lifted were controlled and restored where used;
- test data and results were accurate, complete, within limits, and valid;
- test equipment was removed after testing;
- where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, ASMEs code, and reference values were consistent with the system design basis;
- where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
- where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
- where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
- prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
- equipment was returned to a position or status required to support the performance of its safety functions; and
- all problems identified during the testing were appropriately documented and dispositioned in the CAP.
Documents reviewed are listed in the Attachment.
This inspection constituted four routine surveillance testing samples, one IST sample, and one RCS leak detection inspection sample as defined in IP 71111.22, Sections -02 and -05.
b. Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP2 Alert and Notification System Evaluation
.1 Alert and Notification System Evaluation
a. Inspection Scope
The inspectors reviewed documents and conducted discussions with Emergency Preparedness (EP) staff and management regarding the operation, maintenance, and periodic testing of the Alert and Notification System (ANS) in the Braidwood Station's plume pathway Emergency Planning Zone. The inspectors reviewed monthly trend reports and the daily and monthly operability records from October 2009 through December 2010. Information gathered during document reviews and interviews was used to determine whether the ANS equipment was maintained and tested in accordance with Emergency Plan commitments and procedures. Documents reviewed are listed in the Attachment.
This Alert and Notification System inspection constituted one sample as defined in IP 71114.02-05.
b. Findings
No findings of significance were identified.
1EP3 Emergency Response Organization Staffing and Augmentation System
.1 Emergency Response Organization Staffing and Augmentation System
a. Inspection Scope
The inspectors reviewed and discussed with plant EP management and staff the emergency plan commitments and procedures that addressed the primary and alternate methods of initiating an Emergency Response Organization (ERO) activation to augment the on shift staff as well as the provisions for maintaining the stations ERO qualification and team lists. The inspectors reviewed reports and a sample of corrective action program records of unannounced off-hour augmentation tests and pager test, which were conducted between December 2009 and December 2010, to determine the adequacy of the drill critiques and associated corrective actions. The inspectors also reviewed a sample of the EP training records of approximately 24 ERO personnel, who were assigned to key and support positions, to determine the status of their training as it related to their assigned ERO positions. Documents reviewed are listed in the
.
This Emergency Response Organization Augmentation Testing inspection constituted one sample as defined in IP 71114.03-05.
b. Findings
No findings of significance were identified.
1EP5 Correction of Emergency Preparedness Weaknesses
.1 Correction of Emergency Preparedness Weaknesses
a. Inspection Scope
The inspectors reviewed the Nuclear Oversight staffs 2010 audit of the Braidwood Station's emergency preparedness program to determine that the independent assessments met the requirements of 10 CFR 50.54(t). The inspectors also reviewed samples of corrective action program records associated with the 2010 biennial exercise, as well as various EP drills conducted in 2009 and 2010, in order to determine whether the licensee fulfilled drill commitments and to evaluate the licensees efforts to identify and resolve identified issues. The inspectors reviewed a sample of EP items and corrective actions related to the stations EP program and activities to determine whether corrective actions were completed in accordance with the sites corrective action program. Documents reviewed are listed in the Attachment.
This Correction of Emergency Preparedness Weaknesses and Deficiencies inspection constituted one sample as defined in IP 71114.05-05.
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation
.1 Training Observation
a. Inspection Scope
The inspector observed a simulator training evolution for licensed operators on March 10, 2011 which required emergency plan implementation by a licensee operations crew. This evolution was planned to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed emergency response operations in the Control Room and Technical Support Center to determine whether the event classification, notifications, and protective actions recommendations were performed in accordance with procedures. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that the licensee evaluators noted the same issues and entered them into the corrective action program. As part of the inspection, the inspectors reviewed the scenario package and other documents listed in the Attachment.
This inspection of the licensees training evolution with emergency preparedness drill aspects constituted one sample as defined in IP 71114.06-05.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
4OA1 Performance Indicator Verification
.1 Unplanned Scrams Per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Scrams Per 7000 Critical Hours Performance Indicator (PI) for Braidwood Unit 1 and Unit 2. To determine the accuracy of the performance indicator (PI) data reported during those periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated Inspection Reports from January 1 through December 2010, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator.
Documents reviewed are listed in the Attachment.
This inspection constituted two Unplanned Scrams Per 7000 Critical Hours samples as defined in IP 71151-05.
b. Findings
No findings of significance were identified.
.2 Unplanned Scrams with Complications
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Scrams with Complications PI for Braidwood Unit 1 and Unit 2. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated Inspection Reports from January 1 through December 2010, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment.
This inspection constituted two Unplanned Scrams with Complications samples as defined in IP 71151-05.
b. Findings
No findings of significance were identified.
.3 Unplanned Transients Per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Transients Per 7000 Critical Hours PI for Braidwood Unit 1 and Unit 2. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated Inspection Reports from January 1 through December 2010, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator.
Documents reviewed are listed in the Attachment to this report.
This inspection constituted two Unplanned Transients Per 7000 Critical Hours samples as defined in IP 71151-05.
b. Findings
No findings of significance were identified.
.4 Emergency Response Organization Drill and Exercise Performance
a. Inspection Scope
The inspectors sampled licensee submittals for the Drill and Exercise Performance (DEP)
PI for the period from the first quarter 2010 through fourth quarter 2010. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the DEP indicator in accordance with relevant procedures and the NEI guidance. Specifically, the inspectors reviewed licensee records and processes including procedural guidance on assessing opportunities for the PI, assessments of PI opportunities during pre-designated control room simulator training sessions, performance during the 2010 biennial exercise, and performance during other drills. Documents reviewed are listed in the Attachment.
This inspection constitutes one Drill and Exercise Performance sample as defined in Inspection Procedure 71151-05.
b. Findings
No findings of significance were identified.
.5 Emergency Response Organization Readiness
a. Inspection Scope
The inspectors sampled licensee submittals for the Emergency Response Organization (ERO) Drill Participation PI for the period from the first quarter 2010 through fourth quarter 2010. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures and the NEI guidance. Specifically, the inspectors reviewed licensee records and processes including procedural guidance on assessing opportunities for the PI, performance during the 2010 biennial exercise and other drills, and revisions of the roster of personnel assigned to key emergency response organization positions. Documents reviewed are described in the Attachment.
This inspection constitutes one ERO Drill Participation sample as defined in Inspection Procedure 71151-05.
b. Findings
No findings of significance were identified.
.6 Alert and Notification System Reliability
a. Inspection Scope
The inspectors sampled licensee submittals for the Alert and Notification System (ANS)
PI for the period from the first quarter 2010 through fourth quarter 2010. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, was used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures and the NEI guidance. Specifically, the inspectors reviewed licensee records and processes including procedural guidance on assessing opportunities for the PI and results of periodic ANS operability tests. Documents reviewed are listed in the Attachment.
This inspection constitutes one ANS sample as defined in Inspection Procedure 71151-05.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
.1 Routine Review of Items Entered into the Corrective Action Program
a. Inspection Scope
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: identification of the problem was complete and accurate; timeliness was commensurate with the safety significance; evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent-of-condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue.
Issues entered into the licensees CAP as a result of the inspectors observations are included in the Attachment to this report.
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
b. Findings
No findings of significance were identified.
.2 Daily Corrective Action Program Reviews
a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific human performance issues for followup, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily condition report packages.
These daily reviews were performed by procedure as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
b. Findings
No findings of significance were identified.
4OA3 Followup of Events and Notices of Enforcement Discretion
.1 (Closed) Licensee Event Report 05000457/2010-004-00, Unplanned Limiting Condition
for Operation Entry Due to Low Header Pressure on the 2B Essential Service Water Pump
a. Inspection Scope
On August 24, 2010, Operations personnel performed a Unit 2 B train Essential Service Water (SX) pump surveillance. To establish test flow conditions, the operators were instructed by the procedure to throttle open the Unit 2 component cooling (CC)heat exchanger outlet valve to establish a flow rate of 24,000 gallons per minute (gpm)at the pump discharge. Instead of observing the flow rate at the pump discharge as prescribed in Step 3B of the procedure, operators used a flow meter that measured the flow rate at the inlet of the 2B CC heat exchanger. As a result of this error, the total flow at the pump discharge approached 36,000 gpm and the header pressure rapidly lowered from approximately 90 pounds per square inch (psig) to 65 psig. A low discharge pressure alarm was received in the control room and operators took prompt action to restore the discharge pressure to 90 psig by re-throttling closed the Unit 2 CC heat exchanger outlet valve. This action took approximately 5 minutes. During this time, Operations personnel entered multiple TS Limiting Conditions for Operations (LCOs)due to one inoperable SX train and two inoperable CC trains.
The inspectors reviewed this LER to determine if it was completed in accordance with NRC regulations. In addition, the inspectors reviewed the response to the event and the root cause evaluation.
Documents reviewed are listed in the Attachment. This LER is closed.
b. Findings
Introduction:
A Severity Level IV NCV of 10 CFR 50.9, Completeness and Accuracy of Information, was identified by the inspectors when licensee personnel failed to provide information that was complete and accurate in all material respects in LER 05000457/2010-004-00, Unplanned Limiting Condition for Operation Entry Due to Low Header Pressure on the 2B Essential Service Water Pump.
Description:
The inspectors assessed LER 05000457/2010004-00, Unplanned Limiting Condition for Operation Entry Due to Low Header Pressure on the 2B Essential Service Water Pump, dated October 25, 2010. As part of this assessment, the inspectors reviewed operator logs, CAP documents, Root Cause Report 1105448, and 10 CFR 50.72 Event Notification System (ENS) Report 46203. The inspectors identified several inaccuracies in the 10 CFR 50.73 LER report.
For example, the LER was reported as a condition prohibited by TSs. This was not accurate, since although the station did enter the required LCO, the associated Allowed Outage Time (AOT) was not exceeded. The condition that required entry into the LCO only existed for 5 minutes.
In addition, the LER contained the following conflicting statements regarding the ability of the system to perform its safety function:
- It was determined that with the essential service water system operating at reduced pressure, if an emergency actuation signal had occurred, the pump flow and performance could not be predicted based on the available vendor data.
Therefore, this event is reportable under 10 CFR 50.73 (a)(2)(i)(B), any operation and condition prohibited by TSs.
- Evaluation of the low essential service water pressure effects indicates that both units and trains of essential service water were capable of mitigating the effects of design basis events.
The first statement described a potential unanalyzed condition and a potential loss of safety function, neither of which were discussed in the LER. The second statement referenced an analysis that was performed to evaluate a potential loss of safety function.
The inspectors requested the analysis as referenced in the LER and associated Root Cause Report 1105448. Over the next 3 weeks the licensee was not able to obtain the analysis and determined that the engineering change tracking the analysis had been cancelled. The information used to develop the LER was based on Root Cause Report 1105448, which referenced the performance of an analysis. Based on numerous interviews with licensee staff, the inspectors determined that a lack of communication within the licensees organization led to the inaccurate information in the LER.
Analysis:
Because violations of 10 CFR 50.9, Completeness and Accuracy of Information, are considered to potentially impede or impact the regulatory process, they are dispositioned using the traditional enforcement process. The inspectors concluded that the licensee had reasonable opportunity to foresee and correct the inaccurate information prior to the information being submitted to the NRC. As a result, the inaccurate information contained in LER 05000457/2010004-00, Unplanned Limiting Condition for Operation Entry Due to Low Header Pressure on the 2B Essential Service Water Pump, dated October 25, 2010, was a performance deficiency.
The inspectors determined that this issue was a Severity Level IV violation based on a similar example referenced in Section 6.9, Inaccurate and Incomplete Information or Failure to Make a Required Report, of the NRC Enforcement Policy. In particular, example d.1 identified that a licensee failing to make a required report which, had it been submitted, would have resulted in, for instance, increasing the scope of the next regularly scheduled inspection, as a Severity Level IV violation. The inaccurate information was considered to be material to the NRC because it potentially affected an NRC evaluation of whether a loss of safety function occurred and whether it should had been reported to the NRC.
The inspectors had previously reviewed the Reactor Oversight Process (ROP) aspect of this finding and a self-revealed violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was documented in Section 1R22 of NRC Integrated Inspection Report 05000456/2010004; 05000457/2010004.
Enforcement:
10 CFR 50.9, Completeness and Accuracy of Information, requires, in part, that information provided to the Commission by a licensee shall be complete and accurate in all material respects. Contrary to the above, on October 25, 2010, the licensee submitted LER 05000457/2010004-00, Unplanned Limiting Condition for Operation Entry Due to Low Header Pressure on the 2B Essential Service Water Pump, involving an unplanned Limiting Condition of Operation entry due to low header pressure on the Unit 2 Train B Essential Service Water system, which was not complete and accurate in all material respects. Specifically, the LER had several contradictory statements related to the ability of the system to perform its safety function. The LER stated that an analysis had been performed although at the time the inspectors requested the analysis after the LER was submitted, the analysis had not been performed. As part of the licensees corrective actions, this issue was entered into the licensees corrective action program with an action to perform the analysis referenced in the LER. However, because the violation was a Severity Level IV issue and it was entered into the licensees corrective action program as IR 1166336, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000457/2011002-01, Failure to Provide Complete and Accurate Information in LER 05000457/2010-004-00).
.2 March 24, 2011 Notice of Unusual Event Operator Response
a. Inspection Scope
On March 24, 2011, the inspectors reviewed the Unit 2 operators response following an unexpected loss of all Unit 2 Control Room annunciators. This issue resulted in the licensee declaring a Notice of Unusual Event to the NRC. At the time of the event, the licensee was performing planned maintenance on the Unit 2 annunciator system, however, the maintenance and associated clearance order was not expected to result in a loss of all the Unit 2 control room annunciators. The inspectors responded to the control room to observe the operators and plants response. Documents reviewed are listed in the Attachment.
This inspection constituted one inspection sample as defined in Inspection Procedure 71153.
b. Findings
No findings of significance were identified in this inspection. However, aspects related to the scope of this inspection was also reviewed by a NRC Special Inspection Team. Related findings and observations will be documented in NRC Inspection Report 05000456/2011012.
4OA5 Other Activities
.1 (Closed) Unresolved Item 05000456/2010004-04; 05000457/2010004-04, Potentially
Inadequate Emergency Preparedness Critique As discussed in NRC Inspection Report 05000456/2010004; 05000457/2010004, the inspectors evaluated the conduct of a routine licensee emergency preparedness drill on July 21, 2010, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation (PAR) development activities, and identified an Unresolved Item (URI) due to concerns regarding the licensees critique. This URI was opened to determine whether the licensees critique process adequately identified the appropriate weaknesses associated with a DEP PI failure on July 21, 2010.
Specifically, the inspectors questioned the adequacy of the critique process regarding the basis for this DEP PI failure. According to the licensees final critique, the scenario was designed such that the first indication for meeting the General Emergency declaration threshold was given at 9:15 a.m. In the next 15 minutes, Technical Support Center players did not declare a General Emergency under Emergency Action Level (EAL) MG1 as expected and required. At 9:32 a.m., the lead controller informed the Station Emergency Director that the time limit for classification of the General Emergency under EAL MG1 was exceeded and instructed the Station Emergency Director to declare a General Emergency. However, the licensees final critique concluded that the Station Emergency Director did not have sufficient evidence to support a realistic appraisal that plant conditions could not be recovered, and as a result, the threshold for declaring a General Emergency under EAL MG1 was not met. The licensee concluded that the reason for the DEP PI failure was due to an improper inject provided by the lead controller.
During this inspection period, the inspectors conducted a review of the licensees critique process to determine if the licensee adequately identified the appropriate weakness associated with the DEP PI failure. Specifically, the inspectors reviewed additional information including player logs, controller logs, condition reports, corrective actions, and additional information provided by the licensee. Additionally, the inspectors reviewed the licensees EAL basis document and NEI 99-01, Methodology for Development of Emergency Action Levels, Revisions 4 and 5.
As a result of this review, the inspectors identified an opportunity for improvement regarding the timely assessment and evaluation of changing plant conditions. The inspectors noted that Braidwoods EAL MG1 for the prolonged loss of all offsite power and prolonged loss of all onsite alternating current power to essential buses stated that the likelihood of restoring at least one Engineered Safety Feature (ESF) bus should be based on a realistic appraisal of the situation since a delay in an upgrade decision based on only a chance of mitigating the event could result in a loss of valuable time in preparing and implementing public protective actions. Specifically, the inspectors observed the licensees ability to make a realistic appraisal was affected by missed opportunities in the Technical Support Center to promptly respond to changing plant conditions when issues were communicated. The indications regarding the status of damage to Bus 141, one of the required onsite ESF buses that had a potential impact on an EAL entry, were provided at approximately 8:29 a.m. However, the action to assess simulated damage to Bus 141 was not upgraded to a high priority until 9:24 a.m., and an assessment team was not dispatched until approximately 9:29 a.m. This delay in dispatching the team presented a missed opportunity and subsequent delay in making this realistic appraisal that was necessary for classifying the event.
Additionally, the inspectors noted that communications between the control room and the Technical Support Center was poor and caused confusion regarding plant conditions. Moreover, it was observed that there was a lack of questioning attitude with regard to clarification and verification of provided information. This further affected the licensees ability to perform the required realistic appraisal.
As a result of this review, the inspectors determined the licensees critique process adequately identified the appropriate weakness associated with the DEP PI failure on July 21, 2010. No findings of significance were identified and this item is closed.
.2 (Open) NRC Temporary Instruction 2515/177, Managing Gas Accumulation in
Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems (NRC Generic Letter 2008-01)
a. Inspection Scope
The inspectors verified that the onsite documentation, system hardware, and licensee actions were consistent with the information provided in the licensees response to NRC Generic Letter (GL) 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems. Specifically, the inspectors verified that the licensee has implemented or was in the process of implementing the commitments, modifications, and programmatically controlled actions described in the licensees response to GL 2008-01. The inspection was conducted in accordance with Temporary Instruction (TI) 2515/177, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems (NRC GL 2008-01),and considered the site-specific supplemental information provided by the Office of Nuclear Reactor Regulations (NRR) to the inspectors. In addition, a member of the NRR staff participated in this inspection.
b. Inspection Documentation The selected TI areas of inspection were licensing basis, design, testing, and corrective actions. The documentation of the inspection effort and any resulting observations are below.
Licensing Basis: The inspectors reviewed selected portions of licensing basis documents to verify that they were consistent with the NRR assessment report and that they were processed by the licensee. The licensing basis verification included the verification of selected portions of TS, TS basis, and UFSAR.
The inspectors also verified that selected applicable documents that described the plant and plant operation, such as calculations, piping and instrumentation diagrams (P&IDs),procedures, and CAP documents, addressed the areas of concern and were changed if needed following plant changes. The inspectors noted one example where the onsite documentation was not consistent with the information provided in the licensees response to GL 2008-01. Specifically, in the 9-month response to GL 2008-01, the licensee stated the containment spray piping was designed for the dynamic loads created when it fills with water. However, the inspectors noted Section CL2-3.5.3.6, Flow transient analysis, of the design specification for containment spray, Document No. 01-10-52, Commonwealth Edison Company, Byron/Braidwood Stations, Unit 1 and Unit 2, Piping Design Specifications, stated that, No dynamic loads due to flow transient forces are considered in the analysis of the containment spray system. After discussion with NRR, the inspectors confirmed that the inaccurate information provided by the licensee was no material because it would likely not have caused NRR to reconsider a regulatory position or undertake a substantial further inquiry such as a formal request for additional information. The licensee captured this issue in their CAP as IR 1150198. The licensees recommended corrective action at the time of the inspection was to revise the applicable calculation.
The inspectors confirmed that the frequency of selected surveillance procedures was at least as frequent as required by TSs and that the licensee will:
- (1) evaluate resolution of TS issues with respect to the elements contained in the technical specification task force traveler; and
- (2) submit a license amendment request, if deemed necessary based on this evaluation, within 180 days following NRC approval of the technical specification task force. This commitment was captured in the CAP as IR 833259. In addition, the inspectors noted that, unlike the emergency core cooling system (ECCS), the containment spray did not have a TS surveillance to address gas accumulation/intrusion issues and that the licensee has elected to perform periodic monitoring of the containment spray suction piping only. The inspectors noted that the containment spray system discharge piping high point locations at the curved wall area in the auxiliary building were readily accessible for venting or ultrasonic testing (UT) to monitor for gas accumulation.
Design: The inspectors reviewed selected design documents, performed system walkdowns, and interviewed plant personnel to verify that the design and operating characteristics were addressed by the licensee. Specifically:
The inspectors assessed the licensees efforts for identifying the gas intrusion mechanisms that apply to the plant and identified the following two examples where the licensee failed to recognize gas intrusion mechanisms associated with the residual heat removal (RHR) and containment spray systems:
1. The licensee did not identify all mechanisms that would lead to steam void formation at the RHR system during a loss of cooling accident (LOCA) at Mode 4. Specifically, the licensee determined that both RHR trains would experience steam void formation following RHR realignment from its decay heat removal (DHR) mode to its ECCS mode of operation when evaluating NSAL 09-08, Presence of vapor in ECCS/RHR in Modes 3/4 LOCA, in 2010.
The licensee was concerned that transferring the RHR suction to the refueling water storage tank (RWST) would lead to flash evaporation of the RHR system because RCS conditions exceed the saturation conditions provided by the RWST. The RHR system is subjected to RCS temperatures and pressures when operated in the DHR mode, which exceeds saturation conditions of water at atmospheric pressure. As a result, the licensee established corrective actions to protect one train of RHR in its ECCS mode of operation in Mode 4. However, the inspectors noted that steam voids would form before the suction of the RHR trains are transferred to the RWST if a LOCA occurs of sufficient size to depressurize the RCS because a shutdown-large-LOCA could depressurize the reactor to atmospheric conditions. This would result in the flash evaporation of water inside the RHR system because its temperature would be above the saturation temperature of water at atmospheric pressure.
The licensees failure to identify all flashing mechanisms of RHR in Mode 4 was contrary to 10 CFR Part 50, Appendix B, Criterion III, Design Control, and was a performance deficiency. It was of minor significance because the corrective actions for the flashing mechanism that was identified by the licensee also addressed the performance deficiency identified by the inspectors. Thus, it was determined that the performance deficiency identified by the inspectors did not represent a safety concern. This issue was captured in the licensees CAP as IR 1141819. The performance deficiency identified by the licensee was determined to be of more than minor significance and it is discussed in Section 4OA7 of this report. The inspectors also identified that the licensee failed to report this condition within 60 days of discovery in accordance with 10 CFR 50.73. This issue is discussed in more detail under the Corrective Action subsection.
2. The licensee failed to identify that the calculation that determined the maximum available time to secure the containment spray additive tank did not account for vortexing. The details and enforcement of this issue are discussed in Section 4OA5.1.c of this report.
The inspectors also verified the licensee had identified the gas intrusion mechanisms associated with the operability evaluation associated with a void found at the suction of the A train of the safety injection system in an earlier inspection period. This additional activity counted towards the completion of this TI and was documented in Inspection Report 05000456/2010005; 05000457/2010002.
The inspectors verified that the licensees void acceptance criteria was consistent with NRRs void acceptance criteria. The inspectors also confirmed that:
- (1) the licensee addressed the effect of pressure changes during system startup and operation since such changes could significantly affect the void fraction from the initial value; and
- (2) the range of flow conditions evaluated by the licensee was consistent with the full range of design basis and expected flow rates for various break sizes and locations.
However, the inspectors noted that the licensee also relied on the use of the computer code GOTHIC to evaluate the acceptability of voids. This computer code factors in void transport behavior into the analysis by performing two-phase and two-component analysis of gas movement to predict such behavior as how a void volume in piping is translated into a transient void fraction at the entrance of a pump following pump start.
The inspectors noted instances where the basis of this void assessment analysis tool was questionable. Specifically, the licensee used WCAP-16631-NP, Testing and evaluation of gas transport to the suction of ECCS pumps, to show that GOTHIC can acceptably predict quantitative void transport behavior. WCAP-16631-NP documented tests that were conducted by Westinghouse to study the transport of a gas void through a piping system. The inspectors noted that test configuration and conditions differed from actual plant configuration and conditions, and questioned if the application of some of the test results was acceptable. For example:
1. The difference between test and plant pressures was not considered in assessing void decrease in the vertical test section. The pressure range used during the test was significantly lower than the typical range in nuclear power plants. This effect would be insignificant in a nuclear power plant due to the higher pressures. Therefore, the inspectors questioned if the void fraction change observed during testing would be analogous in a nuclear power plant.
2. Two phase fluid flow test data typically exhibited significant scatter. This was addressed by running many duplicate tests and carefully examining the test results. However, NRR stated in ML090150637, Forthcoming Meeting With The Nuclear Energy Institute To Discuss NRC Generic Letter 2008-01, that this effort was not fully successful and some of the conclusions were not adequately supported by the test data due to data scatter. For example, this effort did not address allowance for uncertainty and the effect of actual plant pressures in contrast to test pressures.
3. The inspectors questioned if the test report adequately considered a water fall
effect (also known as hydraulic jump) when the upper part of the vertical pipe was voided. Specifically, the inspectors questioned if the pipe length used for the test was representative of the limiting conditions of a plant. The inspectors were concerned if such an effect could propel air further down in the pipe than would be predicted using a single dimensional Froude number and would be of concern if the vertical pipe length was significantly less than the pipe used for the test.
4. The use of an average of pipe slopes to determine an equivalent pipe length associated with an elbow with a void reduction of 20 percent was debatable. For example, the average slope of -0.055 was obtained from slopes of -0.333, -0.15, and -0.0883. In addition, as discussed above, the 20% factor does not consider the pressures that will be encountered in nuclear power plants.
The inspectors discussed these observations with NRR. It was determined that these observations required further evaluation by NRR to
- (1) better understand the acceptability of the application of the test results contained in WCAP-16631-NP to void assessment analysis and
- (2) assess potential generic implications. Therefore, this Temporary Instruction will remain open until this issue is resolved.
The inspectors also reviewed the void acceptance criteria used by the licensee when evaluating the operability of the A train of the SI system in an earlier inspection period.
This additional activity counted towards the completion of this TI and was documented in Inspection Report 05000456/2010005; 05000457/2010002.
The inspectors selectively reviewed applicable documents, including calculations and engineering evaluations, with respect to gas accumulation in containment spray and SI systems. Specifically, the inspectors verified that these documents addressed venting requirements, keep-full systems, aspects where pipes are normally voided such as some containment spray piping inside containment, and void control during system realignments.
The inspectors identified one example where the licensee had not properly evaluated the effects of gas accumulation with respect to dynamic loads. Specifically, portions of the containment spray discharge piping are normally voided by design. However, neither the design nor operation of the system addressed the dynamic loads that would result when the voided piping is rapidly filled following system initiation. The details and enforcement of this issue are discussed in Section 4OA5.1.c of this report.
In addition, the inspectors noted that the licensee intended to change their UFSAR to include the piping location near the SI8811 and CS009A valves as acceptable unventable locations. The licensee accepted the potential void sizes at these piping locations of SI and containment spray using GOTHIC. Although the basis of this void assessment tool was questionable, the inspectors noted that the licensee used significant conservatisms when assessing the void sizes at these locations.
Consequently, it was determined, with assistance from NRR, that there is reasonable assurance that these unventable locations do not represent an adverse condition pending further assessment of GOTHIC. This TI will remain open pending the resolution of this issue.
The inspectors conducted a walkdown of selected regions of the B train on the Unit 2 safety injection and B train of the Unit 2 containment spray in sufficient detail to assess the licensees walkdowns.
In addition, the inspectors verified that the licensee had P&IDs and isometric drawings that describe the containment spray and safety injection system configurations and had confirmed the accuracy of the drawings resolution. The inspectors review of the selected portions of isometric drawings considered the following:
1. Selected high point vents were identified.
2. Selected high points that do not have vents were recognizable.
3. Other areas where gas can accumulate and potentially impact subject system operability, such as at orifices in horizontal pipes, isolated branch lines, heat exchangers, improperly sloped piping, and under closed valves, were described in the drawings or in referenced documentation.
4. Selected pipes and fittings were clearly shown.
The inspectors also conducted a similar walkdown of selected portions of safety injection in an earlier inspection period. This additional activity counted towards the completion of this TI and was documented in Inspection Report 05000456/2009005; 05000457/2009005.
The inspectors verified that licensees walkdowns have been completed. In addition, the inspectors selectively verified that information obtained during the licensees walkdowns were addressed in procedures, the CAP, and training documents.
Testing: The inspectors reviewed selected surveillance and post-maintenance procedures and results to verify that the licensee has approved and was using procedures that were adequate to address the issue of gas accumulation and/or intrusion in the safety injection and containment spray systems. In addition, the inspectors observed licensee staff conducting the monthly venting surveillance in the Unit 2 safety injection and RHR systems to evaluate procedure compliance. This review included the verification of procedures used for conducting surveillances and determination of void volumes to ensure that the void criteria was satisfied and will be reasonably ensured to be satisfied until the next scheduled void surveillance. The inspectors noted that the licensee had not established instructions for measuring pipe voids detected during surveillances of the ECCS performed using the venting method.
The details and enforcement of this issue are discussed in Section 4OA5.1.c of this report. Also, the inspectors reviewed procedures used for filling and venting following conditions which may have introduced voids into the subject systems to verify that the procedures addressed testing for such voids and provided processes for their reduction or elimination. In addition, the inspectors reviewed training material associated with GL 2008-01 and noted that additional training was being pursued by the licensee.
The inspectors also review selected portions of procedures used during the surveillance testing of the ECCS in an earlier inspection period. This additional activity counted towards the completion of this TI and was documented in Inspection Report 05000456/2010002; 05000457/2010002.
Corrective Actions: The inspectors reviewed selected licensees assessment reports, CAP documents, and trending data to assess the effectiveness of the licensees CAP when addressing the issues associated with GL 2008-01. In addition, the inspectors verified that selected corrective actions identified in the licensees 9-month and supplemental reports were documented. The inspectors also verified that commitments were included in the CAP.
The inspectors identified a Severity Level IV Non-Cited Violation of 10 CFR 50.73(a)(2)(v) in an earlier inspection period which counted towards the completion of this TI. Specifically, the licensee personnel failed to report known conditions that could have prevented the fulfillment of the RHR system to perform its ECCS function while operating in the DHR mode of operation within 60 days of discovery. This violation was documented in Inspection Report 05000456/2010005; 05000457/2010005 and is associated with the licensee-identified finding discussed in Section 4OA7 of this report.
This inspection concluded that this TI must remain open for Braidwood Station and additional inspection will be necessary using this TI. Specifically, at the conclusion of this inspection period, questions remained unresolved regarding the use of GOTHIC to justify the acceptability of design basis changes associated with the subject of gas accumulation.
c. Findings
- (1) Failure To Account For Vortexing When Calculating The Maximum Available Time To Secure The Containment Spray Additive Tank
Introduction:
A finding of very low safety significance and associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified by the inspectors for the failure to account for vortexing when determining the maximum available time to secure the containment spray additive tank. Specifically, the applicable calculation assumed that nitrogen would intrude the system only when the tank was completely drained.
Description:
On November 16, 2010, the inspectors identified that the calculation that determined the maximum available time to secure the containment spray additive tank did not account for vortexing. The inspectors were concerned because nitrogen would intrude into the suction of the containment spray pumps if the containment spray additive tank is not secured before its level reached the submergence level to prevent vortexing.
The nitrogen entrainment effects due to vortexing were not analyzed.
Section 6.5.2, Containment Spray Systems, of the UFSAR stated that the containment spray system is designed to remove fission products, primarily iodine, from the containment atmosphere for the purpose of minimizing the offsite radiological consequences following the design-basis LOCA. At the same time, the spray water serves to nominally reduce containment temperature and pressure during the injection phase. In addition, the containment spray additive tank provide a sufficient quantity of 30 percent to 36 percent NaOH solution to the containment to form an 8.0-10.5 pH solution when combined with the spilled RCS water, the SI accumulator inventory, and the RWST inventory. This range of pH values bounds the evaluation of pH effects on equipment qualification and hydrogen generation described in the UFSAR.
The containment spray additive tank injects the NaOH solution via an eductor to the suction line headers of both containment spray pumps. The containment spray pumps would initially take suction from the RWST and, when reaching a predetermined low level, their suction is transferred to the containment recirculation sump. The time to deplete the containment spray additive tank is greater than the time to deplete the RWST under the worst-case condition for maximum spray pH described in UFSAR 6.5.2. This will result in transferring the suction of the containment spray pump to the containment recirculation sump and continuing eduction of NaOH from the containment spray additive tank until its Lo-2 level is reached. The containment spray additive tank is then manually isolated from the containment spray eductor.
Calculation BRW-97-0274, Containment Spray Additive Tank Level Switch LO-2 Setpoint Analysis, determined, in part, the maximum time available to isolate the containment spray additive tank to prevent nitrogen from entering the process lines upon reaching the LO-2 level. It stated that the motivation of this part of the calculation was that the introduction of nitrogen into the process lines has not been evaluated. However, the inspectors noted that the calculation did not account for vortexing. That is, the calculation assumed that nitrogen would enter the process lines only when the tank was completely drained.
Vortexing is a gas intrusion mechanism identified in GL 2008-01. For instance, GL 2008-01 stated that additional work might be necessary to develop realistic criteria to determine the amount of gas that could impact operability resulting from the ingestion of gas from tanks (i.e., vortexing). In addition, GL 2008-01 requested, in part, the licensee to evaluate its containment spray system design to ensure that gas accumulation is maintained less than the amount that challenges operability of this system.
As a result of the inspectors concerns, the licensee calculated the required submergence and determined that 6.1 inches above the suction pipe inlet was necessary to prevent vortexing. The inspectors independently verified this value.
When the submergence level was considered, the maximum available time to isolate the containment spray additive tank was reduced from 5.25 minutes to 4 minutes. The action to close the containment spray additive tank valves is listed in 1/2 BwEP-1, Continuous Action Summary in Emergency Operating Procedures. The steps provided in this procedure are performed in a continuous basis and are a prompt to the operators for incomplete steps or conditions that may require further action. In addition, the LO-2 level is provided with an alarm at the control room which prompts the operators to respond using alarm response procedure BwAR 1-3-B3, Spray Additive Tank Level LO-2. The combination of this programmatic controls provided reasonable assurance that the operators would respond within the required timeframe to isolate the containment spray additive tank. The licensee captured the inspectors concerns in their CAP as IR1146838. The licensees recommended corrective action at the time of the inspection was to revise the applicable calculation.
Analysis:
The inspectors determined that the failure to account for vortexing when determining the maximum available time to secure the containment spray additive tank was contrary to 10 CFR Part 50, Appendix B, Criterion III, Design Control, and was a performance deficiency.
The performance deficiency was determined to be more than minor because it was associated with the containment barrier cornerstone attribute of structure, systems, components, and barrier performance and affected the cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, the inspectors had reasonable doubt on the operability of the containment spray system because the effects of vortexing in the tank and potential nitrogen entrainment to the system pumps suction were not analyzed.
The inspectors determined the finding could be evaluated using the SDP in accordance with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of findings, Table 4a for the containment barrier cornerstone. The finding screened as of very low safety significance (Green) because it was a design deficiency of the physical integrity of the reactor containment that:
- (1) did not affect the barrier function of the control room against smoke or a toxic atmosphere;
- (2) did not represent an actual open pathway in the physical integrity of reactor containment; and
- (3) did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Specifically, the licensee performed an additional evaluation that concluded that sufficient time would exist for the operators to take actions to preclude vortexing.
The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because the licensee did not thoroughly evaluate external operating experience. Specifically, the licensee did not address potential vortexing at the containment spray additive tank when evaluating the subject of gas accumulation/intrusion as requested by GL 2008-01. P.2(a)
Enforcement:
10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculation methods, or by the performance of a suitable testing program.
Contrary to the above, as of November 16, 2010, the licensee had not verified the adequacy of the containment spray additive tank design. Specifically, the licensee failed to account for vortexing when determining the maximum time available to secure the containment spray additive tank upon reaching the low level alarm. In addition, the effects of nitrogen entrainment into the pumps suction due to vortexing where not analyzed. Because this violation was of very low safety significance and it was entered into the licensees corrective action program as IR 1146838, this violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000456/2011002-02; 05000457/2011002-02, Failure to Account for Vortexing when Calculating the Maximum Available Time to Secure the Containment Spray Additive Tank).
- (2) Inadequate Instructions For Measuring Emergency Core Cooling System Voids
Introduction:
A finding of very low safety significance (Green) and associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, was identified by the inspectors for the licensees failure to establish instructions for measuring pipe voids detected during surveillances of the ECCS for gas accumulation. Specifically, instructions to measure the size of gas voids detected during venting at each safety injection and RHR system vent location were not provided so that the effect of the void on system operability could be evaluated.
Description:
On November 19, 2010, the inspectors identified that the licensee failed to establish adequate instructions in surveillance procedures used to monitor ECCS for gas accumulation.
In response to GL 2008-01, the licensee committed to revise the periodic venting procedures for the GL 2008-01 subject systems to include enhanced acceptance criteria and requirements to perform UT examinations on a graded approach as part of venting verifications of accessible high points.
In Section F.1 of procedures 1BwOSR 3.5.2.2-2, Unit One ECCS Venting and Valve Alignment Surveillance, and 2BwOSR 3.5.2.2-2, Unit Two ECCS Venting and Valve Alignment Surveillance, the licensee established instructions to vent the safety injection system, RHR pumps, and associated piping to satisfy TS Surveillance Requirement 3.5.2.3, Verify ECCS piping is full of water. The completion of this surveillance for each pipe segment was accomplished by one of five conditions as recorded on Attachment D, ECCS Venting and Valve Alignment Data Sheet, of these procedures. Condition 3 stated that the pipe segment was Actually Vented. However, the inspectors noted that during venting to satisfy Condition 3, a gas void could be detected and vented off without estimating the size of the pipe void. Specifically, these procedures did not provide instructions to time the duration of the gas released during venting, nor were instructions provided to measure the void volume with a UT examination prior to venting. The inspectors were concerned that the lack of written instructions to record the as-found condition could result in the licensees inability to properly assess the effect of a pipe void on ECCS functions (e.g., operability).
The operating surveillance procedures discussed above were accomplished in conjunction with procedures 1BwBVSR 3.5.2.3.1, Unit 1 Periodic Monitoring and Trending of Containment Spray and Emergency Core Cooling Systems for Gas Accumulation, and 2BwBVSR 3.5.2.3.1, Unit 2 Periodic Monitoring and Trending of Containment Spray and Emergency Core Cooling Systems for Gas Accumulation.
These procedures directed licensee staff to complete UT examinations on ECCS high points to monitor for gas accumulation. However, the inspectors noted that these procedures also did not provide instructions to measure the duration of venting to estimate the gas void size when adequate UT data was could not be obtained.
Specifically, Step E.10 of these procedures stated:
If UT exam cannot be performed due to extenuating circumstances (safe access, radiological concerns, etc.) at a location with an installed vent valve, then NOTIFY the Shift Manager to manually vent the location. An IR shall be generated to document the inability to perform the UT exam.
Therefore, this procedure step allowed venting ECCS pipe locations without recording any data to estimate the size of a gas void, if present. The licensee had applied Step E.10 provisions to vent in place of a UT examination since inception of these procedures. Specifically, in May of 2009 as documented in IR 924568, the licensee identified a dozen pipe locations in the Unit 1 and 2 ECCS with permanent insulation that precluded access for UT examinations. Consequently, each of these pipe segments required venting in accordance with Step E.10. The licensee staff stated that modifications were planned to remove this permanent insulation and replace it with removable insulation to enable the UT examination. A due date of February 2, 2011 had been established for this action.
A precaution at step D.10 of procedures 1BwOSR 3.5.2.2-2 and 2BwOSR 3.5.2.2-2 required recording the duration of gas release and vent valve position for venting gas identified at the RHR pump suction high point vent valves. This information was necessary to ensure the licensee could estimate the size of gas voids identified during venting of ECCS piping. However, similar guidance was not provided for measuring the duration or recording the valve position at other RHR and safety injection vent valve locations that could be opened to detect the presence of gas voids. The inspectors also noted that these procedures did not specify how to time the duration of the venting operation (e.g., record duration of gas flow using a stopwatch).
As a corrective action, the licensee initiated an IR 1142820 to document the additional valve locations where these instructions were to be applied. In addition, during the monthly performance of 2BwOSR 3.5.2.2-2, the licensees System Engineer briefed the operations staff to apply the precaution of Step D.10 to each of the ECCS vent locations and to use a stopwatch to measure gas vent durations. The licensee stated that they intended to continue to brief staff on their expectations for performing these surveillance procedures until procedure revisions were issued to provide additional guidance for recording data to size ECCS voids identified during venting operations.
Analysis:
The inspectors determined that the licensees failure to provide instructions for measuring pipe voids during ECCS venting was contrary to the requirements of 10 CFR Part 50, Appendix B, Criterion V, and was a performance deficiency. The performance deficiency was determined to be more than minor because if left uncorrected it would have the potential to lead to a more significant safety concern.
Specifically, since the licensees procedures do not contained instructions to properly document the void size when venting, the potential exists for an unacceptable void to go undetected affecting ECCS operability. Inoperable ECCS trains would place the plant at increased risk for core damage, which would affect the safety of an operating reactor.
The inspectors determined the finding could be evaluated using the SDP in accordance with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of findings, Table 4a for the mitigating system cornerstone. The finding screened as of very low safety significance (Green) because the finding was a qualification deficiency confirmed not to result in loss of operability or functionality. Specifically, the licensee performed a history review of their corrective action program documents since the implementation of their resolution of GL 2008-01 and found two occasions where a void was detected by venting activities. A qualitative assessment of the voids established reasonable assurance that they did not represent loss of operability. The inspectors did not have further concerns.
The inspectors did not find an applicable cross-cutting aspect which represented the underlying cause of this performance deficiency; therefore, no cross-cutting aspect was assigned.
Enforcement:
Chapter 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, required, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances.
Contrary to the above, as of November 19, 2010, the licensee did not establish ECCS surveillance procedures appropriate to the circumstances. Specifically, instructions were not provided to measure the size of gas voids detected by venting surveillances at each safety injection and RHR system vent location so that the effect of a void on system operability could be evaluated. Because this violation was of very low safety significance and it was entered into the licensees CAP as IR 1142820, this violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000456/2011002-03; 05000457/2011002-03, Inadequate Instructions for Measuring ECCS Voids).
- (3) Failure To Evaluate The Effects Of Dynamic Loads At The Containment Spray Discharge Piping
Introduction:
A finding of very low safety significance and associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified by the inspectors for the failure to evaluate the effects of dynamic loads at the containment spray discharge piping. Specifically, neither the structural design nor operation of the containment spray system addressed the dynamic loads that would result when normally voided discharge piping rapidly fill following system initiation.
Description:
On December 1, 2010, the inspectors identified that the licensee had not evaluated the potential effects of dynamic loads on the discharge piping of containment spray resulting from flow transients. The inspectors were concerned because portions of the containment spray discharge piping are normally voided by design and neither the structural design nor operation of the system addressed the dynamic loads that would result when the voided piping is rapidly filled following system initiation.
The containment spray system is designed to remove fission products, primarily iodine, from the containment atmosphere for the purpose of minimizing the offsite radiological consequences following the design-basis LOCA. At the same time, the spray water serves to nominally reduce containment temperature and pressure. In addition, the containment spray additive tank provide a sufficient quantity of 30 percent to 36 percent NaOH solution to the containment to form an 8.0-10.5 pH solution when combined with the spilled RCS water, the safety injection accumulator inventory, and the RWST inventory. This range of pH values bounds the evaluation of pH effects on equipment qualification and hydrogen generation described in the UFSAR.
The licensee incorporated ASME Section III into the design basis for the safety-related portion of containment spray. American Society of Mechanical EngineersSection III, 74-S75, NC-3112.3, Design Mechanical Loads, stated that Impact forces caused by either external or internal conditions shall be considered. Dynamic loads induced by flow transients are impact forces caused by an internal condition. However, the Piping System Specific Design Specification for containment spray, Document No. 01-10-52, Commonwealth Edison Company, Byron/Braidwood Stations, Units 1 and 2, Piping Design Specifications, Section CL2-3.5.3.6, Flow transient analysis, stated that No dynamic loads due to flow transient forces are considered in the analysis of the containment spray system. Since the structural design of containment spray did not consider dynamic loads, the inspectors questioned if the system was operated in a manner that would ensure that the resulting dynamic loads would be negligible when the system fills with water following system initiation. The licensee confirmed that the operation of the system has not been evaluated to determine whether or not the resulting dynamic loads were negligible. Specifically, the system is initiated via automatic action and the design of the automatic initiation did not consider dynamic loads induced by flow transients.
The resulting dynamic loads from a voided system are discussed in GL 2008-01. For instance, GL 2008-01 stated that additional work might be necessary to develop realistic criteria to determine the amount of gas that could impact operability including allowable limits for the pump discharge piping to alleviate water cannon effects on the piping. In addition, GL 2008-01 discusses operating experiences related to dynamic loads resulting from gas accumulation/intrusion issues.
The inspectors confirmed the piping at the containment penetration is always filled with water. Thus, no dynamic load will be induced on the penetration as the line fills.
Specifically, the containment spray containment isolation valves are cycled (i.e., opened and closed) once a quarter allowing the water level in the containment spray piping in containment to equalize with the water level in the RWST. The elevation of the minimum water level required by TS is greater than the elevation of the containment penetrations.
Therefore, the inspectors were not concerned with the integrity of the containment structure. However, an adverse dynamic load at the containment spray system discharge piping inside containment could render the system incapable of meeting its design basis functions.
As a result of the inspectors concerns, the licensee initiated an IR 1189277 and, at the time of the inspection, planned to review the design to ensure compliance with ASME Section III, 74-S75, NC-3112.3.
Analysis:
The inspectors determined that the failure to evaluate the effects of dynamic loads at the containment spray discharge piping was contrary to ASME Section III, 74-S75, NC-3112.3 and was a performance deficiency. The performance deficiency was determined to be more than minor because it was associated with the containment barrier cornerstone attribute of system, structures, and components and barrier performance and affected the cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, the inspectors had reasonable doubt on the operability of the containment spray system and the integrity of the reactor containment because the effects of flow transient induced dynamic loads in the containment spray discharge piping were not analyzed.
The inspectors determined the finding could be evaluated using the SDP in accordance with IMC 0609, Significance Determination Process, Appendix H, Containment Integrity Significance Determination Process, Table 6.1, Phase 1 Screening-Type B Findings at Full Power. The finding screened as Green because it did not affect either core damage frequency or large early release frequency. Specifically, containment spray impacts late containment failure and source terms, but not core damage frequency or large early release frequency.
The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because the licensee did not thoroughly evaluated external operating experience. Specifically, the licensee did not address potential water cannon effects at the containment spray discharge piping when evaluating the subject of gas accumulation/intrusion as requested by GL 2008-01. P.2(a)
Enforcement:
10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, procedures, and instructions. American Society of Mechanical EngineersSection III, 74-S75, NC-3112.3 was included in the design bases for the safety-related portion of the containment spray system.
Contrary to the above, as of December 1, 2010, the design control measures failed to translate applicable design basis into specifications. Specifically, neither the structural nor automatic initiation design of the containment spray system considered flow transient induced dynamic loads as required by ASME Section III, 74-S75, NC-3112.3. Because this violation was of very low safety significance and it was entered into the licensees corrective action program as IR 1189277, this violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000456/2011002-04; 05000457/2011002-04, Failure to Evaluate the Effects of Dynamic Loads at the Containment Spray Discharge Piping).
4OA6 Management Meetings
.1 Exit Meeting Summary
On April 6, 2011, the inspectors presented the inspection results to Mr. D. Enright, and other members of the licensee staff. The licensee acknowledged the issues presented.
The inspectors confirmed that none of the potential report input discussed was considered proprietary.
.2 Interim Exit Meetings
Interim exits were conducted for:
- The results of an Emergency Preparedness program inspection with Mr. L. Coyle on February 4, 2011.
- The results of a TI-177 inspection with Mr. D. Enright on March 18, 2011.
The inspectors confirmed that none of the potential report input discussed was considered proprietary. Proprietary material received during the inspection was returned to the licensee.
4OA7 Licensee-Identified Violations
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI.A.1 of the NRC Enforcement Policy for being dispositioned as an NCV.
A finding of very low safety significance (Green) and associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified by the licensee for the failure to ensure that the ECCS mode of operation of RHR would be capable of performing its mitigating function at Mode 4 following RHR realignment from its DHR mode of operation. Specifically, the operability requirements of RHR in Mode 4 defined by TS 3.5.3 were not translated into applicable procedures or specifications of the system in that neither the procedures nor design prevented the conditions that would lead to steam void formation during a LOCA that initiates at this Mode resulting in steam binding of the system pumps and/or an adverse waterhammer. The performance deficiency was determined to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of Equipment Performance and affected the cornerstone objective of ensuring the capability of systems that respond to initiating events to prevent undesirable consequences. An SDP Phase II evaluation concluded that the finding was of very low safety significance. The licensee entered this concern in its CAP as IR 1073616.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- D. Enright, Site Vice President
- M. Kanavos, Plant Manager
- P. Boyle, Maintenance
- P. Daly, Radiation Protection Manager
- A. Ferko, Engineering Director
- B. Finlay, Security Manager
- G. Galloway, Work Control Manager
- J. Gerrity, Regulatory Assurance
- M. Marchionda, Operations Manager
- S. McKinney, Emergency Preparedness Coordinator
- J. Mumford, Engineering
- R. Radulovich, Nuclear Oversight Manager
- J. Rappeport, Chemistry/Environmental Manager
- C. VanDenburgh, Regulatory Assurance Manager
- W. Waznis, Nuclear Oversight
Nuclear Regulatory Commission
- E. Duncan, Chief, Branch 3, Division of Reactor Projects
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
Opened
- 05000457/2011002-01 NCV Failure to Provide Complete and Accurate Information in an LER (Section 4OA3.1)
- 05000456/2011002-02; NCV Failure to Account for Vortexing When Calculating the
- 05000457/2011002-02 Maximum Available Time to Secure the Containment Spray Additive Tank (Section 4OA5.2.c(1))
- 05000456/2011002-03; NCV Inadequate Instructions for Measuring ECCS Voids
- 05000457/2011002-03 (Section 4OA5.2.c(2))
- 05000456/2011002-04; NCV Failure To Evaluate The Effects Of Dynamic Loads At The
- 05000457/2011002-04 Containment Spray Discharge Piping (Section 4OA5.2.c(3))
Closed
- 05000457/2011002-01 NCV Failure to Provide Complete and Accurate Information in an LER (Section 4OA3.1)
- 05000456/2011002-02; NCV Failure to Account for Vortexing When Calculating the
- 05000457/2011002-02 Maximum Available Time to Secure the Containment Spray Additive Tank (Section 4OA5.2.c(1))
Attachment
- 05000456/2011002-03; NCV Inadequate Instructions for Measuring ECCS Voids
- 05000457/2011002-03 (Section OA5.2.c(2))
- 05000456/2011002-04; NCV Failure To Evaluate The Effects Of Dynamic Loads At The
- 05000457/2011002-04 Containment Spray Discharge Piping (Section 4OA5.2.c(3))
- 05000456/2010004-04; URI Potentially Inadequate Licensee EP Critique
- 05000457/2010004-04 (Section 4OA5.1)
- 05000457/2010-004-00 LER Unplanned LCO Entry Due to Low Pressure on 2B Essential Service Water Pump (Section 4OA3.1)
Discussed
None Attachment